IR 05000293/1987036

From kanterella
Revision as of 11:50, 25 October 2020 by StriderTol (talk | contribs) (StriderTol Bot insert)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
Ack Receipt of 871026 Ltr Informing NRC of Steps Taken to Correction Violations Noted in Insp Rept 50-293/87-36.As Result of Review & Evaluation of Paragraph 2 of Response, Severity Level IV Changed to Level V
ML20151G587
Person / Time
Site: Pilgrim
Issue date: 11/13/1987
From: Johnston W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To: Bird R
BOSTON EDISON CO.
Shared Package
ML20151G582 List:
References
NUDOCS 8804200059
Download: ML20151G587 (1)


Text

. : '

Docket No. 50-293 License No. DDR-35 Boston Edison Company ATTN: Ralph G. Bird Senior Vice President - Nuclear 800 Boylston Street Boston, Massachusetts 02199 Gentlemen:

Subject: Inspection No. 50-293/87-36 This refers to your letter dated October 26, 1987, in response to our letter dated September 24, 1987.

Thank you for informing us of the corrective and preventive actions documented in your letter. These actions will be examined during a future inspection of your licensed program.

Also, as a result of our review and evaluation of paragraph 2 of your response to the Notice of Violation, as noted above, we have changed the Severity Level from IV to V.

Your cooperation with us is appreciated.

Sincerely, William V. Johnston, Acting Director Division of Reactor Safety cc:

Public Document Room (PDR)

Nuclear Safety Information Cenier (NSIC)

Commonwealth of Massachusetts (2 copies)

bec:

Region I Docket Room (w/ concurrences)

RI:DRS ,

k@

W1:0RS

/

RI:DRS RI:DRS RI:DRS P/lt s l Bissett djh Blumberg gBlough Gallo Durr Jogos700 11/lY87 11/k/87 11 A 3/87 11/ /27 11/ /87 0FFICIAL RECORD COPY RL PILGRIM 87-36 - 0001.0.0 11/10/8e 8804200059 880411 ,

PD3 ADOCK 05.000293  !

g DCD l

_ _ _ - _ . _ _ _ _

-

- -

-

. .

  1. i sosn m aus m Executive Offices 800 Boylston Street Boston, Massachusetts 02199 i Ralph G. Bird Senior Vice President - Nuclear

-

October 26, 1987 BECo Ltr. #87 167 U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555 License No. DPR-35 Docket No. 50-293 Subject: NRC Inspection Report No. 50-293/87-36

Dear Sir:

Attached is Boston Edison Company's response to the Notice of Violation contained in the subject inspection report.

Please contact me directly if you have any questions on this response.

Attachment cc: Regional Administrator U.S. Nuclear Regulatory Commission Region I 631 Park Avenue King of Prussia, PA 19406

~

Sr. Resident Inspector -

,

r11/0%1 Vfl /ll?

2 wnet a f

< . . -

., l l

.

l ATTACHMENT I Boston Edison Company Docket No. 50-293 Pilgrim Nuclear Power Station License No. DPR-35 l

Notice of Violation: j

!

10CFR50, Appendix B, Criterion XI, states in part, "Test results shall be... evaluated to assure that test requirenants have been satisfied."

10CFR50, Appendix B, Criterion XVI, states in part, "measures shall be established to assure that...nonconformances are promptly identified and corrected."

Contrary to the above, as of August 27, 1987, post maintenance test results that failed to meet acceptance criteria had not been adequately evaluated. As a result of the inadequate evaluations, these unsatisfactory test results were not identified and subsequently corrected. Two instances were noted where completed test results of 480 volts (MR No.86-273) and 520 volts (MR No.

86-14-25) had exceeded the acceptance criteria of 460 volts specified in Procedure No. 3.H.4-10, Attachment C Revision 6. Both test results had been accepted as satisfactorily completed following a supervisory and a Quality Control review on April 10, 1986 and August 15, 1987, respectively. This is a Severity Level IV violation (Supplement I) applicable to DPR-35.

Response:

1. Summary:

Boston Edison concurs with the facts stated in the Notice of Violation.

The fundamental violation was personnel failing to identify discrepancies between acceptance criteria and recorded test results as required by Procedure 3.H.4-10. Corrective action has been taken to resolve that problem as described in Section 4 of this letter.

Based on a review of the facts of the violation Boston Edison requests the i Severity Level be changed from IV to V. 10CFR Part 2 Appendix C states that Severity Level V violations, "have minor safety or environmental !

significance". He consider this. violation to meet that criterion since an !

evaluation has concluded that the motors would not be adversely affected '

by the observed elevated voltages.

A discussion of the pertinent technical details is provided below to support our position.

Page 1 of 3 l I e

,

- - -

- -

_ _ _ _ _ - . _ _.

' . ..

'

ATTACHHENT I (Centd 2. Discussion:  ;

!

'

Elevated AC voltages have negligible effect on motor RPM and therefore l will not significantly affect valve stroke time. Elevated voltages (i.e. j approximately 520 volts) increase motor heating but do not exceed the  ;

motor's temperature rise capability /reting due to the short operating time.

During a previous outage, prior to the subject work being pr'ormed, an i informal assessment of the discrepancy between nameplate voltage (460V) )

and actual bus voltage had been performed on a generic basis. This , '

informal assessment was performed by a senior Boston Edison electrical engineer and recently was confirmed by the Nuclear Engineering Department ,

'

by memo dated October 21, 1987.

The subject Procedure, No. 3.M.4-10 "Valve Maintenance" was not being used to demonstrate valve operability, therefore valve operability was not comoromised by this error. A separate operating procedure was used to confirm valve operability.

This violation therefore meets the criterion for severity Level V.

3. Cause:

Personnel failed to identify a discrepancy between the stated "Acceptance Criteria" and the recorded test results. This violation was caused by personnel 1) failing to follow procedures and 2) relying upon a previous informai evaluation which concluded that voltages up to 520 volts were acceptable.

In retrospect, the procedure should have either been revised to delete voltage as an acceptance criteria or the discrepancy evaluated each time Procedure 3.M.4-10 was used.

4. Corrective Actions Taken to Avoid Future Violations and Results Achieved:

The Quality Control and Maintenance personnel involved in the violation were counseled on the importance of procedural adherence.

The Operations QC Group Leader conducted a training session of QC personnel on August 28, 1987 and reinforced their responsibility to question and document discrepancies between identified "Acceptance Criteria" and recorded test data. The QC Group Leader also issued a change to the "Quality Control Inspection" procedure to include the attachment of the acceptance criteria to the quality control inspection report to facilitate independent review. Additionally, previous uses of Procedure 3.M.4-10 from January 1987 to the present have been reviewed.

Olscrepancies have been documented and resolved.

The Cnief Maintenance Engineer took prompt action to revise procedure 3.M.4-10 (Rev. 8 issued August 21, 1987) to address the immediate concern of the voltage data and its intended use. This change deleted voltage as an acceptance criteria but retained .ua requirement to record voltage at the MCC.

Page 2 of 3

.

. .' ; * **

ATTACHMENT I (Cont.)

.

On August 28, 1987, the Senior Vice Presidaat, Nuclear empha- %ed to site personnel at an "All Hands" meeting the importance of prc:erural adherence. He also noted that if a procedure cannot be followed as written then work should be stopped and the pr.cedure corrected. On September 9,1987, a brief summary of the "All Hands ineeting was posted on the bulletin boards throughout the site. This recent emphasi;, as well as continuing training and implementation of the formal Plant Management Monitoring Program are expected to lessen the likelihood of future violations.

5. Date of Full Compliance:

Full compliance was achieved on August 21, 1987 when procedure 3.M.4-10 was revised. Additionally, the QC effort to review previous uses of Procedure 3.M.4-10, from January 1987 to the present, was concluded on October 21, 1987,

l

.

l l

l

!

l I

Page 3 of 3

'

,_ _