ML20151G587

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Ack Receipt of Informing NRC of Steps Taken to Correction Violations Noted in Insp Rept 50-293/87-36.As Result of Review & Evaluation of Paragraph 2 of Response, Severity Level IV Changed to Level V
ML20151G587
Person / Time
Site: Pilgrim
Issue date: 11/13/1987
From: Johnston W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To: Bird R
BOSTON EDISON CO.
Shared Package
ML20151G582 List:
References
NUDOCS 8804200059
Download: ML20151G587 (1)


See also: IR 05000293/1987036

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Docket No. 50-293

License No. DDR-35

Boston Edison Company

ATTN:

Ralph G. Bird

Senior Vice President - Nuclear

800 Boylston Street

Boston, Massachusetts 02199

Gentlemen:

Subject:

Inspection No. 50-293/87-36

This refers to your letter dated October 26, 1987, in response to our letter

dated September 24, 1987.

Thank you for informing us of the corrective and preventive actions documented

in your letter.

These actions will be examined during a future inspection of

your licensed program.

Also, as a result of our review and evaluation of paragraph 2 of your response

to the Notice of Violation, as noted above, we have changed the Severity Level

from IV to V.

Your cooperation with us is appreciated.

Sincerely,

William V. Johnston, Acting Director

Division of Reactor Safety

cc:

Public Document Room (PDR)

Nuclear Safety Information Cenier (NSIC)

Commonwealth of Massachusetts (2 copies)

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Region I Docket Room (w/ concurrences)

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Executive Offices

800 Boylston Street

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Ralph G. Bird

Senior Vice President - Nuclear

October

26, 1987

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BECo Ltr. #87 167

U.S. Nuclear Regulatory Commission

Attn: Document Control Desk

Washington, DC 20555

License No. DPR-35

Docket No. 50-293

Subject: NRC Inspection Report No. 50-293/87-36

Dear Sir:

Attached is Boston Edison Company's response to the Notice of Violation

contained in the subject inspection report.

Please contact me directly if you have any questions on this response.

Attachment

cc: Regional Administrator

U.S. Nuclear Regulatory Commission

Region I

631 Park Avenue

King of Prussia, PA 19406

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Sr. Resident Inspector

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ATTACHMENT I

Boston Edison Company

Docket No. 50-293

Pilgrim Nuclear Power Station

License No. DPR-35

Notice of Violation:

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10CFR50, Appendix B, Criterion XI, states in part, "Test results shall

be... evaluated to assure that test requirenants have been satisfied."

10CFR50, Appendix B, Criterion XVI, states in part, "measures shall be

established to assure that...nonconformances are promptly identified and

corrected."

Contrary to the above, as of August 27, 1987, post maintenance test results

that failed to meet acceptance criteria had not been adequately evaluated. As

a result of the inadequate evaluations, these unsatisfactory test results were

not identified and subsequently corrected.

Two instances were noted where

completed test results of 480 volts (MR No.86-273) and 520 volts (MR No.

86-14-25) had exceeded the acceptance criteria of 460 volts specified in

Procedure No. 3.H.4-10, Attachment C Revision 6.

Both test results had been

accepted as satisfactorily completed following a supervisory and a Quality

Control review on April 10, 1986 and August 15, 1987, respectively.

This is a

Severity Level IV violation (Supplement I) applicable to DPR-35.

Response:

1.

Summary:

Boston Edison concurs with the facts stated in the Notice of Violation.

The fundamental violation was personnel failing to identify discrepancies

between acceptance criteria and recorded test results as required by

Procedure 3.H.4-10.

Corrective action has been taken to resolve that

problem as described in Section 4 of this letter.

Based on a review of the facts of the violation Boston Edison requests the

Severity Level be changed from IV to V.

10CFR Part 2 Appendix C states

that Severity Level V violations, "have minor safety or environmental

significance". He consider this. violation to meet that criterion since an

evaluation has concluded that the motors would not be adversely affected

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by the observed elevated voltages.

A discussion of the pertinent technical details is provided below to

support our position.

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ATTACHHENT I (Centd

2.

Discussion:

Elevated AC voltages have negligible effect on motor RPM and therefore

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will not significantly affect valve stroke time.

Elevated voltages (i.e.

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approximately 520 volts) increase motor heating but do not exceed the

motor's temperature rise capability /reting due to the short operating time.

During a previous outage, prior to the subject work being pr'ormed, an

informal assessment of the discrepancy between nameplate voltage (460V)

and actual bus voltage had been performed on a generic basis.

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informal assessment was performed by a senior Boston Edison electrical

engineer and recently was confirmed by the Nuclear Engineering Department

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by memo dated October 21, 1987.

The subject Procedure, No. 3.M.4-10 "Valve Maintenance" was not being used

to demonstrate valve operability, therefore valve operability was not

comoromised by this error. A separate operating procedure was used to

confirm valve operability.

This violation therefore meets the criterion for severity Level V.

3.

Cause:

Personnel failed to identify a discrepancy between the stated "Acceptance

Criteria" and the recorded test results. This violation was caused by

personnel 1) failing to follow procedures and 2) relying upon a previous

informai evaluation which concluded that voltages up to 520 volts were

acceptable.

In retrospect, the procedure should have either been revised to delete

voltage as an acceptance criteria or the discrepancy evaluated each time

Procedure 3.M.4-10 was used.

4.

Corrective Actions Taken to Avoid Future Violations and Results Achieved:

The Quality Control and Maintenance personnel involved in the violation

were counseled on the importance of procedural adherence.

The Operations QC Group Leader conducted a training session of QC

personnel on August 28, 1987 and reinforced their responsibility to

question and document discrepancies between identified "Acceptance

Criteria" and recorded test data.

The QC Group Leader also issued a

change to the "Quality Control Inspection" procedure to include the

attachment of the acceptance criteria to the quality control inspection

report to facilitate independent review. Additionally, previous uses of

Procedure 3.M.4-10 from January 1987 to the present have been reviewed.

Olscrepancies have been documented and resolved.

The Cnief Maintenance Engineer took prompt action to revise procedure

3.M.4-10 (Rev. 8 issued August 21, 1987) to address the immediate concern

of the voltage data and its intended use.

This change deleted voltage as

an acceptance criteria but retained .ua requirement to record voltage at

the MCC.

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ATTACHMENT I (Cont.)

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On August 28, 1987, the Senior Vice Presidaat, Nuclear empha- %ed to site

personnel at an "All Hands" meeting the importance of prc:erural

adherence. He also noted that if a procedure cannot be followed as

written then work should be stopped and the pr.cedure corrected. On

September 9,1987, a brief summary of the "All Hands ineeting was posted

on the bulletin boards throughout the site.

This recent emphasi;, as well

as continuing training and implementation of the formal Plant Management

Monitoring Program are expected to lessen the likelihood of future

violations.

5.

Date of Full Compliance:

Full compliance was achieved on August 21, 1987 when procedure 3.M.4-10

was revised. Additionally, the QC effort to review previous uses of

Procedure 3.M.4-10, from January 1987 to the present, was concluded on

October 21, 1987,

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