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Units 1 and 2 were at 100'r power. On 6/17/88, it was determined that the mounting of the pressure switches (PSs) 2 SW-PS-1995, 1996, 1998, and 1999 on the NSW header cooling water supply to the DGs (DGs 1-4) was not seismically qualified. These switches provide an automatic switch over of its diesel generator's service water normal supply to its alternate supply on low pressure.
At approximately 1700 hours0.0197 days <br />0.472 hours <br />0.00281 weeks <br />6.4685e-4 months <br /> on 6/29/88, a determination was made that Unit 2 was operating with a Nuclear Service Water (NSW) header pump lineup which could have resulted in inoperability (following a design seismic event) of emergency diesel generator (DGs) Nos. 3 and 4.
Inopert.bility of two diesel generators is outside the plant design basis (DGs 1-4 are common to both units).
This event had minimal direct impact on plant safety design.
The deficient PSs mounting was attributed to unknown cause(s) during original plant construction.
Unit 1 SSW was aligned (compensatory cetion) to the DGs until the PS mounting problem was corrected by plant modification.
The units' NSW headers to the DGs were returned to normel at 1700 on 7/2/88, b
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The units' common 4160 volt (V) alternating current (ac) emergency diesel generator (DG) Nos. 1-4 were operable and in standby readiness. On June 17, 1988, engineering design reviews and field inspections were in progress relative to planned replacement of the instrument isolation valve (IV) (EIIS/BI/ISV) of service water (SW) header pressure switch (PS), 2-SW-PS-1996, to No. 3 DG.
The subject pressure switch effects transfer of the DG normal SW supply from one unit to the alternate SW supply from the othar unit upon a sensed low pressure condition in the normal header. The normal SW supply for DG Nos.1 and 2 is from one of the Unit i nuclear SW (NSW) pumps (1A or 1B) (EIIS/BI/P) while the normal SW supply for DG Nos. 3 and 4 is from one of the Unit 2 NSW pumps (2A or 2B).
Event Description
on June 17, 1988, during a visual inspection of the instrument rack mounting of 2-SW-PS-1996, it was identified by the plant Technical Support Unit SW System Engineer, that a discrepancy existed between the actual field conditions and the respective design drawings. This concern was relative to the seismic qualification of the switch mounting.
Further investigation determined that this concern also existed with the corresponding SW header PSs (2-SW-PS-1995, 1998, snd 1999) of the remaining DGs.
In accordance with Operating Instruction (0I)-04, Limiting Condition for Operation (LCO) Evaluations and Follow Up, a preliminary engineering assessment was begun,.to be completed within the next 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, to assess whether the observed condition of the mounting met seismic l
requirements.
Later that same day, following reviews of original design drawings and field as-builts relative to the switch mounting, it was assessed that the pressure switch mountings met Short-Term Structural Integrity (STSI) requirements (would not fail in a seismic event).
In addition, the site Brunswick Engineering.6upport Unit (BESU) structural group was then requested to perform a follow-up evaluation to formally document seismic qualification of the mountings.
On June 28, 1988, the SW Systcm Engineer was notified by the BESU Structural group that the mounting for the PSs was not seismically qualified.
Plant management was informed of the BESU determination and a review and assessment or the SW System logic and operational status of the SW System pumps was performed with consideration of the single active failure criterion, in order to determine the effect of an assumed failure of the PSs during a design basis seismic event. The assessment concluded that with respect to an assumed failure of the subject PSs, the Final Safety Analysis Report (FSAR) requirement of at least three operable DGs for both units was met.
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. wm w..as wanc s w.nm At approximately 0830 hours0.00961 days <br />0.231 hours <br />0.00137 weeks <br />3.15815e-4 months <br /> on Tune 29, 1988, following reviews of the subject June 28 assessment, the Resid-e. NRC Inspector identified an additional component for consideration ;elacjve to single active failure criteria. This additional question was based upon an assumed failure of the PSs during a design basis seismic event (due to the inadequate PS seismic support) concurrent with the subject operating configuration of the Unit 2 NSW pumps.
At the time, the Unit 2 NSW header was being supplied from the 2A NSW pump and the 2B NSw' pump (redundant) was under equipment clearance.
Consequently, a situation could occur where a single active failure (in this case a failure of the 2A NSW pump) would result in a loss of the NSW header to DG Nos. 3 and 4 as the 2B NSW pump would be unable to supply the NSW supply header to the DGs.
It was therefore concluded that with the operating configuration of NSW pumps the Brunswick units were operating such that the subject DGs could have potentially been rendered inoperable as the result of the assumed failure of the PSs during a design basis seismic event.
Consequently, the design basis requirement of at least three operable DGs, as outlined in the FSAR, could not be assured.
Compensatory Action Compensatory actions were initiated to ensure that the DG (Nos. 1-4) were adequately supplied with cooling water as an interim action until the subject PS mounting could be seismically upgraded.
This was achievec by aligning the Unit 1 NSW header supply to provide cooling water to the DGs.
The Unit 1 NSW header isolation valve, 1-SW-255, a normally open motor-operated valve with no automatic logic features, was deenergized in the open position to preclude an inadvertent closure of the valve.
In order to assure alignment of the Unit 1 SSW header supply to the DGs, the respective Unit 1 NSW header supply valves (EIIS/BI/ISV) to the DGs, 1-SW-Y210 (DG No. 1), 1-SW-V211 (DG No. 2), 1-SV-V212 (DG No. 3), and 1-FW-V213 (DG No. 4) were deenergized and the valves were manually opened.
Following impicmentation of the subject compensatory actions, the operability of the DGs was reestablished.
Cause of Event
The discrepancy in the actual field conditions of the pressure switch mounting versus the respective design drawing is attributed to undetermined causes which occurred sometime during original plant construction, i
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On June 30, 1988, Plant Modification 87-226 was implemented for seismic j
upgrading of the subject PS mountings.
At 1700 hours0.0197 days <br />0.472 hours <br />0.00281 weeks <br />6.4685e-4 months <br />, on July 2, 1988, the modification was declared operable for the subject PSs on both units and the normal operating configuration of the.NSW header cooling watar supplies to the DGs was reestablished.
Event Assessment An assessment of this event under reasonable and credible alternative conditions has determined that a more serious event would not have occurred.
The identified PS mounting deficiency would create a failure only during a seismic event.
A seismic event, along with a LOCA, is not considered a reasonable nor credible event.
A review of pla,nt documentation shows this event is an isolated occurrence.
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--twame Brunswick Steam Electric Plant P. O. Box 10429 Southport, NC 28461-0429 July 28, 1988 FILE:
B09-13510C 10CFR50.73 SERIAL: BSEP/88-0736 U.S. Nuclear Regulatory Commission ATTN:
Document Control Desk Washington, DC 20:55 BRUNSWICK STEAM ELECTRIC PLANT UNIT 1 DOCKET NO. 50-325 LICENSE NO. DPR-71 LICENSEE EVENT REPORT 1-88-016 Gentlemen:
In accordance with Title 10 to the Code of Federal Regulations, the enclosed Licensee Event Report is submitted. This report fulfills the requirement for a wrftten report within thirty (30) days of a reportable occurrence and is in accordance with the format set forth in NUREG-1022, September 1983.
Very truly yours, f
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L. Harness, General Manager Brunswick Steam Electric Plant MJP/ah Enclosure cc:
Dr. J. N. Grace Mr. E. D. Sylvester BSEP NRC Resident Office s
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| 05000324/LER-1988-001, :on 880102,manual Reactor Protection Sys Trip (Scram) Initiated Due to Decreasing Condenser Vacuum. Definite Root Cause Not Identified.Contractor Svcs Retained |
- on 880102,manual Reactor Protection Sys Trip (Scram) Initiated Due to Decreasing Condenser Vacuum. Definite Root Cause Not Identified.Contractor Svcs Retained
| | | 05000324/LER-1988-001-01, :on 880102,manual Reactor Protection Sys Trip Scram Initiated Due to Decreasing Condenser Vacuum.Caused by Leaks on Main Turbine.Surveillance Activity Initiated on Failure of Valves to Open |
- on 880102,manual Reactor Protection Sys Trip Scram Initiated Due to Decreasing Condenser Vacuum.Caused by Leaks on Main Turbine.Surveillance Activity Initiated on Failure of Valves to Open
| | | 05000325/LER-1988-001-01, :on 880104,unexpected Primary Containment Group 6 Isolation,Reactor Bldg Ventilation Isolation & Auto Start of Standby Gas Treatment Sys Occurred.Caused by Inadequate Review of Plant Mod & Procedure Rev |
- on 880104,unexpected Primary Containment Group 6 Isolation,Reactor Bldg Ventilation Isolation & Auto Start of Standby Gas Treatment Sys Occurred.Caused by Inadequate Review of Plant Mod & Procedure Rev
| | | 05000325/LER-1988-002-03, :on 880209,auto-isolation of RWCU Sys Inlet Outboard Isolation Valve 2-G31-F004 Occurred.Caused by Actuation of One or More of RWCU Steam Leak Detection Temp Modules.Group 3 Isolation Signal Reset |
- on 880209,auto-isolation of RWCU Sys Inlet Outboard Isolation Valve 2-G31-F004 Occurred.Caused by Actuation of One or More of RWCU Steam Leak Detection Temp Modules.Group 3 Isolation Signal Reset
| | | 05000325/LER-1988-003, :on 880108,Tech Spec Surveillance 4.8.1.1.1.a to Demonstrate Operability of Offsite Ac Power Sources Missed.Caused by Shift Foreman Not Adequately Tracking & Verifying Completion of Surveillance |
- on 880108,Tech Spec Surveillance 4.8.1.1.1.a to Demonstrate Operability of Offsite Ac Power Sources Missed.Caused by Shift Foreman Not Adequately Tracking & Verifying Completion of Surveillance
| | | 05000324/LER-1988-004-02, :on 880224,standby Gas Treatment Sys Trains 2A & 2B Autostarted & Reactor Bldg Ventilation Autoisolated. Caused by Blown Power Supply Fuse in Div I Trouble/Start Relay Logic Circuitry.Fuse Replaced |
- on 880224,standby Gas Treatment Sys Trains 2A & 2B Autostarted & Reactor Bldg Ventilation Autoisolated. Caused by Blown Power Supply Fuse in Div I Trouble/Start Relay Logic Circuitry.Fuse Replaced
| | | 05000325/LER-1988-004, :on 880115,while Placing RWCU Sys Filter Demineralizer a Into Svc,Primary Containment Isolation Sys (PCIS) Group 3 Isolation Occurred.Caused by Exceeding PCIS Leakage Actuation Setpoint.Gaskets Replaced |
- on 880115,while Placing RWCU Sys Filter Demineralizer a Into Svc,Primary Containment Isolation Sys (PCIS) Group 3 Isolation Occurred.Caused by Exceeding PCIS Leakage Actuation Setpoint.Gaskets Replaced
| | | 05000324/LER-1988-005-02, :on 880204,safety Relief Valves Setpoints Exceeded During Testing at Wyle Labs.Caused by Corrosion Induced Bonding of Pilot Valve Disc to Seat Surface.Valves Refurbished.Maint Personnel Counseled |
- on 880204,safety Relief Valves Setpoints Exceeded During Testing at Wyle Labs.Caused by Corrosion Induced Bonding of Pilot Valve Disc to Seat Surface.Valves Refurbished.Maint Personnel Counseled
| | | 05000325/LER-1988-005, :on 880124,limiting Condition for Primary Containment Oxygen Concentration Exceeding Tech Spec 3.0.3 Entered.Caused by Incorrectly Configured Control Switch. Control Switch 1-C11-CS-Z8-S1 Replaced |
- on 880124,limiting Condition for Primary Containment Oxygen Concentration Exceeding Tech Spec 3.0.3 Entered.Caused by Incorrectly Configured Control Switch. Control Switch 1-C11-CS-Z8-S1 Replaced
| | | 05000325/LER-1988-006-01, :on 880219,several Bolt Head Failures of silicon-bronze Carriage Bolts in 125-volt & 250-volt Dc Switchboards Identified.Caused by Igscc.Bolts Replaced W/ Bolts Made from Mild Carbon Steel |
- on 880219,several Bolt Head Failures of silicon-bronze Carriage Bolts in 125-volt & 250-volt Dc Switchboards Identified.Caused by Igscc.Bolts Replaced W/ Bolts Made from Mild Carbon Steel
| | | 05000325/LER-1988-006, :on 880219,numerous Bolt Head Failures of 5/16- Inch X 1/2-inch Silicon Bronze Carriage Bolts Noted in Bus/ Bar Connections of Electrical Switchboards.Caused by Igscc. Bolts Replaced.Reportable Per Part 21 |
- on 880219,numerous Bolt Head Failures of 5/16- Inch X 1/2-inch Silicon Bronze Carriage Bolts Noted in Bus/ Bar Connections of Electrical Switchboards.Caused by Igscc. Bolts Replaced.Reportable Per Part 21
| | | 05000324/LER-1988-006-02, :on 880308,control Rod 10-39 Unknowingly Withdrawn W/Reactor Protection Sys Shorting Links Installed. Caused by Personnel Error.Individuals Involved Counseled & Process of Software Mod to Be Reviewed |
- on 880308,control Rod 10-39 Unknowingly Withdrawn W/Reactor Protection Sys Shorting Links Installed. Caused by Personnel Error.Individuals Involved Counseled & Process of Software Mod to Be Reviewed
| | | 05000325/LER-1988-007, :on 880218,primary Containment Group 1 Isolation Signal Received Following Reset of Main Turbine Trip Signal.Caused by Inadvertent Main Turbine Stop Valve Opening.Appropriate Procedural Changes Planned |
- on 880218,primary Containment Group 1 Isolation Signal Received Following Reset of Main Turbine Trip Signal.Caused by Inadvertent Main Turbine Stop Valve Opening.Appropriate Procedural Changes Planned
| | | 05000324/LER-1988-007-01, :on 880319,visual & Liquid Penetrant Insps of Unit CRD Insert/Withdraw Lines Revealed Existence of Pinhole & Linear Indications in Lines.Caused by Chloride Contamination.Affected Lines Replaced |
- on 880319,visual & Liquid Penetrant Insps of Unit CRD Insert/Withdraw Lines Revealed Existence of Pinhole & Linear Indications in Lines.Caused by Chloride Contamination.Affected Lines Replaced
| | | 05000325/LER-1988-008, :on 880302,discovered That Generic Failure Mechanism Existed for Supply Fans of Diesel Generator Bldg Ventilation Sys.Caused by Excessive Start/Stop of Fans.Fan Rotors Replaced & Returned to Svc |
- on 880302,discovered That Generic Failure Mechanism Existed for Supply Fans of Diesel Generator Bldg Ventilation Sys.Caused by Excessive Start/Stop of Fans.Fan Rotors Replaced & Returned to Svc
| | | 05000325/LER-1988-008-01, :on 880302,determined That Generic Failure Mechanism Existed for Supply Fans of Common Diesel Generator Bldg Ventilation Sys.Caused by Cracks Due to Frequent Stop & Start.A & B Rotors Replaced |
- on 880302,determined That Generic Failure Mechanism Existed for Supply Fans of Common Diesel Generator Bldg Ventilation Sys.Caused by Cracks Due to Frequent Stop & Start.A & B Rotors Replaced
| | | 05000324/LER-1988-008-02, :on 880331,full Reactor Protection Sys Trip Occurred When Mode Switch of APRM Rotated Beyond Switch Mechanical Stop Position.Caused by Improperly Configured Switch.Switch Replaced |
- on 880331,full Reactor Protection Sys Trip Occurred When Mode Switch of APRM Rotated Beyond Switch Mechanical Stop Position.Caused by Improperly Configured Switch.Switch Replaced
| | | 05000325/LER-1988-009, :on 880309,primary Containment Group 6 Isolation of Reactor Bldg Ventilation Sys & Auto Start of Standby Gas Treatment Sys Trains a & B Occurred.Caused by Accidental Opening of Circuit Breaker |
- on 880309,primary Containment Group 6 Isolation of Reactor Bldg Ventilation Sys & Auto Start of Standby Gas Treatment Sys Trains a & B Occurred.Caused by Accidental Opening of Circuit Breaker
| | | 05000324/LER-1988-009-01, :on 880331,full Reactor Protection Sys Trip Occurred Due to Upscale Trip of Intermediate Range Monitor. Caused by Spurious Electronic Noise.Electronic Noise Suppressors Installed in Circuitry |
- on 880331,full Reactor Protection Sys Trip Occurred Due to Upscale Trip of Intermediate Range Monitor. Caused by Spurious Electronic Noise.Electronic Noise Suppressors Installed in Circuitry
| | | 05000325/LER-1988-010-03, :on 880502,during Routine Maint,Common Control Bldg Emergency Air Filtration Sys & Common Control Bldg Heating Automatically Isolated.Cause Undetermined.Event Considered Isolated Occurrence.No Action Taken |
- on 880502,during Routine Maint,Common Control Bldg Emergency Air Filtration Sys & Common Control Bldg Heating Automatically Isolated.Cause Undetermined.Event Considered Isolated Occurrence.No Action Taken
| | | 05000324/LER-1988-010, :on 880420,RWCU Inlet Inboard Primary Containment Isolation Valve Automatically Closed.Caused by Momentary RWCU Sys Flow Perturbation.Plant Procedures Revised to Alert Operator to Problem |
- on 880420,RWCU Inlet Inboard Primary Containment Isolation Valve Automatically Closed.Caused by Momentary RWCU Sys Flow Perturbation.Plant Procedures Revised to Alert Operator to Problem
| | | 05000324/LER-1988-011-01, :on 880725,RHR/primary Containment Isolation Inboard Isolation Valve E11-F009 Failed to Open.Caused by Failure of Electrical Contacts in Switch Number 1 to Close. Wiring Reconfigured to Utilize Spare Switch 2 |
- on 880725,RHR/primary Containment Isolation Inboard Isolation Valve E11-F009 Failed to Open.Caused by Failure of Electrical Contacts in Switch Number 1 to Close. Wiring Reconfigured to Utilize Spare Switch 2
| | | 05000324/LER-1988-011-03, :on 880725,reactor RHR Shutdown Cooling Sys Primary Containment Isolation Sys Inboard Isolation Valve Would Not Open.Caused by Electrical Malfunction.Wiring of Instrument Reconfigured to Utilize Switch 2 |
- on 880725,reactor RHR Shutdown Cooling Sys Primary Containment Isolation Sys Inboard Isolation Valve Would Not Open.Caused by Electrical Malfunction.Wiring of Instrument Reconfigured to Utilize Switch 2
| | | 05000325/LER-1988-011, :on 880420,HPCI Pump Suction from Suppression Pool E41-F041 Would Not Open During Instrument Channel Calibr & Functional Test.Probably Caused by Breakdown of motor-winding Insulation |
- on 880420,HPCI Pump Suction from Suppression Pool E41-F041 Would Not Open During Instrument Channel Calibr & Functional Test.Probably Caused by Breakdown of motor-winding Insulation
| | | 05000325/LER-1988-012-01, :on 880528,HPCI Turbine Steam Supply Isolation Valve Would Not Open,Resulting in HPCI Being Declared Inoperable.Caused by Failure of Valve Motor Windings.Hole Drilled in Valve Disc |
- on 880528,HPCI Turbine Steam Supply Isolation Valve Would Not Open,Resulting in HPCI Being Declared Inoperable.Caused by Failure of Valve Motor Windings.Hole Drilled in Valve Disc
| | | 05000325/LER-1988-012, :on 880528,HPCI Sys Declared Inoperable Due to Turbine Steam Supply Isolation Valve E41-F001 Not Opening. Caused by Failure of Valve Motor Windings Resulting from Mechanical Binding of Valve Disc.Repairs Made |
- on 880528,HPCI Sys Declared Inoperable Due to Turbine Steam Supply Isolation Valve E41-F001 Not Opening. Caused by Failure of Valve Motor Windings Resulting from Mechanical Binding of Valve Disc.Repairs Made
| | | 05000324/LER-1988-012, :on 880725,HPCI Declared Inoperable Due to Inability to Determine Environ Qualification of Electrical Termination/Splices of Auxiliary Oil Pump.Caused by Inadequate Workmanship When Splices Made |
- on 880725,HPCI Declared Inoperable Due to Inability to Determine Environ Qualification of Electrical Termination/Splices of Auxiliary Oil Pump.Caused by Inadequate Workmanship When Splices Made
| | | 05000325/LER-1988-013, :on 880424,failure of Svc Water Sys Nuclear Header Supply Isolation Valve to Open Due to Oxidation of Valve Geared Limit Switch Electrical Contacts. Oxidation of Electrical Contacts Removed |
- on 880424,failure of Svc Water Sys Nuclear Header Supply Isolation Valve to Open Due to Oxidation of Valve Geared Limit Switch Electrical Contacts. Oxidation of Electrical Contacts Removed
| | | 05000324/LER-1988-013-03, :on 880802,reactor Protection Sys Bus a Automatically Deenergized.Caused by Tripping of Electrical Protection Assemblies 5 & 6 & Reactor Protection Sys Logic a Scram Signal.Power to Bus Aligned to Normal |
- on 880802,reactor Protection Sys Bus a Automatically Deenergized.Caused by Tripping of Electrical Protection Assemblies 5 & 6 & Reactor Protection Sys Logic a Scram Signal.Power to Bus Aligned to Normal
| | | 05000325/LER-1988-014-01, :on 880606,RCIC Sys Steam Leak Detection Instrumentation Setpoints Determined to Be Set Nonconservatively High.Cause Not Determined.Unit 2 Piping Misconfiguration Corrected |
- on 880606,RCIC Sys Steam Leak Detection Instrumentation Setpoints Determined to Be Set Nonconservatively High.Cause Not Determined.Unit 2 Piping Misconfiguration Corrected
| | | 05000324/LER-1988-015, :on 880426,limiting Conditions of Tech Specs 3.5.3.2,3.6.1.1,3.6.1.2 & 3.6.1.3 Not Met While Performing Startup Testing to Meet Tech Specs.Caused by Not Recognizing Mode Change.Standing Instruction Issued |
- on 880426,limiting Conditions of Tech Specs 3.5.3.2,3.6.1.1,3.6.1.2 & 3.6.1.3 Not Met While Performing Startup Testing to Meet Tech Specs.Caused by Not Recognizing Mode Change.Standing Instruction Issued
| | | 05000325/LER-1988-015-01, :on 880612,control Bldg Emergency Air Filtration & HVAC Sys Automatically Isolated Due to Actuation of Chlorine Detector in Tank Car Storage Area. Cause Undetermined |
- on 880612,control Bldg Emergency Air Filtration & HVAC Sys Automatically Isolated Due to Actuation of Chlorine Detector in Tank Car Storage Area. Cause Undetermined
| | | 05000325/LER-1988-016-01, :on 880617,determined That Mounting of Pressure Switches on Nuclear Svc Water Header Cooling Water Supply to Diesel Generators Not Seismically Qualified.Cause Undetermined.Mod Implemented |
- on 880617,determined That Mounting of Pressure Switches on Nuclear Svc Water Header Cooling Water Supply to Diesel Generators Not Seismically Qualified.Cause Undetermined.Mod Implemented
| | | 05000324/LER-1988-016-02, :on 880908,Div 2 Svc Water Vital Header Leak Resulted in Manual Isolation of Associated Header.Caused by Excessive Corrosion of 3/4-inch Blank Flange on Bypass Line. Flange Replaced & Vital Header Returned to Svc |
- on 880908,Div 2 Svc Water Vital Header Leak Resulted in Manual Isolation of Associated Header.Caused by Excessive Corrosion of 3/4-inch Blank Flange on Bypass Line. Flange Replaced & Vital Header Returned to Svc
| | | 05000325/LER-1988-017, :on 880630,HPCI Sys Declared Inoperable Due to Inoperability of Steam Line Flow Instrument.Also on 880701, Hcpi Turbine Steam Supply Isolation Would Not Open.Caused by Failure of Valve Motor Windings |
- on 880630,HPCI Sys Declared Inoperable Due to Inoperability of Steam Line Flow Instrument.Also on 880701, Hcpi Turbine Steam Supply Isolation Would Not Open.Caused by Failure of Valve Motor Windings
| | | 05000324/LER-1988-017-03, :on 881005,HPCI Vacuum Breaker Isolation Valve (2-E41-F079) Automatically Closed as Result of False Initiation Signal.Caused by Short Across High Drywell Pressure Relay.Equipment Tested Daily |
- on 881005,HPCI Vacuum Breaker Isolation Valve (2-E41-F079) Automatically Closed as Result of False Initiation Signal.Caused by Short Across High Drywell Pressure Relay.Equipment Tested Daily
| | | 05000325/LER-1988-018, :on 880713,testing Revealed That HPCI Pump Suction Primary Containment Inboard Isolation Valve Would Not Open.Caused by Loss of Electrical Continuity in Opening Logic.Valve Geared Limit Panel Replaced |
- on 880713,testing Revealed That HPCI Pump Suction Primary Containment Inboard Isolation Valve Would Not Open.Caused by Loss of Electrical Continuity in Opening Logic.Valve Geared Limit Panel Replaced
| | | 05000325/LER-1988-020-01, :on 880915,RCIC Sys E51 Received Logic Channel B Supply Line Isolation,Closing Outboard Steam Supply Isolation Valve.Caused by Damage to Speed Sensor & Connector.Warning Signs Posted |
- on 880915,RCIC Sys E51 Received Logic Channel B Supply Line Isolation,Closing Outboard Steam Supply Isolation Valve.Caused by Damage to Speed Sensor & Connector.Warning Signs Posted
| | | 05000325/LER-1988-021-02, :on 880926,Group 6 Isolation Occurred Due to Actuation of Logic Circuitry of Auxiliary Trip Unit of Reactor Bldg Ventilation Exhaust Monitor.Technicians Checked Battery of Instrumentation & Control Group |
- on 880926,Group 6 Isolation Occurred Due to Actuation of Logic Circuitry of Auxiliary Trip Unit of Reactor Bldg Ventilation Exhaust Monitor.Technicians Checked Battery of Instrumentation & Control Group
| | | 05000325/LER-1988-022-02, :on 881014,control Rooms Received Primary Containment Isolation Sys Group 6 Isolation,Causing Auto Start of Standby Gas Treatment Sys.Caused by Initiation of hi-hi Radiation Alarm Signals.Signals Reset |
- on 881014,control Rooms Received Primary Containment Isolation Sys Group 6 Isolation,Causing Auto Start of Standby Gas Treatment Sys.Caused by Initiation of hi-hi Radiation Alarm Signals.Signals Reset
| | | 05000325/LER-1988-023-03, On 881021,Unit Automatically Scrammed Due to Main Turbine Trip/Turbine Stop Valve Closure.Caused by High Electrical Resistance Across Contacts 3 7 4 in Feedwater Control Transfer Relay.Relay Replaced | On 881021,Unit Automatically Scrammed Due to Main Turbine Trip/Turbine Stop Valve Closure.Caused by High Electrical Resistance Across Contacts 3 7 4 in Feedwater Control Transfer Relay.Relay Replaced | | | 05000325/LER-1988-023-01, :on 871231 HPCI Sys (E41) Inoperable.Caused by Failure of HPCI Turbine Steam Inlet Isolation Valve E41-F001 Motor.Valve Motor Replaced |
- on 871231 HPCI Sys (E41) Inoperable.Caused by Failure of HPCI Turbine Steam Inlet Isolation Valve E41-F001 Motor.Valve Motor Replaced
| | | 05000325/LER-1988-024, :on 881110,reactor Scrammed Due to Momentary Turbine Control Valve Fast Closure Circuitry Trip.Caused by Electrical Noise Generated in Electrohydraulic Control Sys During Performance of Test.Diodes Installed |
- on 881110,reactor Scrammed Due to Momentary Turbine Control Valve Fast Closure Circuitry Trip.Caused by Electrical Noise Generated in Electrohydraulic Control Sys During Performance of Test.Diodes Installed
| | | 05000325/LER-1988-025, :on 881115,failure to Meet Tech Specs 3.61.2b & 3.6.1.2c Revealed Through Local Leak Rate Testing.Caused by Manpower Constraints.Valves Listed in Table 1 Are on Separate Containment Penetrations |
- on 881115,failure to Meet Tech Specs 3.61.2b & 3.6.1.2c Revealed Through Local Leak Rate Testing.Caused by Manpower Constraints.Valves Listed in Table 1 Are on Separate Containment Penetrations
| | | 05000325/LER-1988-028, :on 881123,pipe Crack Indications Revealed Existence of 238 Indications in 19 of 65 Welds.Caused by IGSCC of Associated Welds.Addl Testing,Repair &/Or Mods Will Be Conducted Per Generic Ltr in Future Outages |
- on 881123,pipe Crack Indications Revealed Existence of 238 Indications in 19 of 65 Welds.Caused by IGSCC of Associated Welds.Addl Testing,Repair &/Or Mods Will Be Conducted Per Generic Ltr in Future Outages
| | | 05000325/LER-1988-030, :on 881130,testing of Safety Relief Valves Revealed That 9 of 11 Valves Tested Lifted at Pressures Outside Tech Spec Tolerance of +/- 1%.Caused by Corrosion Induced Bonding of Pilot Valved Disc |
- on 881130,testing of Safety Relief Valves Revealed That 9 of 11 Valves Tested Lifted at Pressures Outside Tech Spec Tolerance of +/- 1%.Caused by Corrosion Induced Bonding of Pilot Valved Disc
| | | 05000325/LER-1988-031, :on 881214,reactor Protection Trip Occurred Due to False Scram Discharge Vol High Level.Caused by Design Problem W/Scram Discharge Vol High Level Trip Switches. Switches Will Be Replaced |
- on 881214,reactor Protection Trip Occurred Due to False Scram Discharge Vol High Level.Caused by Design Problem W/Scram Discharge Vol High Level Trip Switches. Switches Will Be Replaced
| | | 05000325/LER-1988-032, :on 881214,standby Gas Treatment a & B Train Maint Inlet Valves Only 5-10% Open.Caused by Design Deficiency.Plant Mods Completed & Training Session Provided. Part 21 Related |
- on 881214,standby Gas Treatment a & B Train Maint Inlet Valves Only 5-10% Open.Caused by Design Deficiency.Plant Mods Completed & Training Session Provided. Part 21 Related
| | | 05000325/LER-1988-033, :on 881214,determined That Valve Body Erosion Generic Concern on Both Units.Erosion Resulted from Flow Induced Cavitation Due to Throttling Isolation Valves Below Design Limit.Instructions Re RHR Loops Revised |
- on 881214,determined That Valve Body Erosion Generic Concern on Both Units.Erosion Resulted from Flow Induced Cavitation Due to Throttling Isolation Valves Below Design Limit.Instructions Re RHR Loops Revised
| | | 05000325/LER-1988-034, :on 881216,clearance Hug on Drywell Instrument Air Sys Which Could Have Prevented Secondary Containment Isolation Dampers from Operating as Required.Caused by Design Deficiency.Standing Instruction Issued |
- on 881216,clearance Hug on Drywell Instrument Air Sys Which Could Have Prevented Secondary Containment Isolation Dampers from Operating as Required.Caused by Design Deficiency.Standing Instruction Issued
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