IR 05000261/1980023

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IE Insp Rept 50-261/80-23 on 800903-05.No Noncompliance Noted.Major Areas Inspected:Inservice Insp Program, Procedures,Records & IE Bulletin 79-13
ML19339A585
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 09/22/1980
From: Blake J, Herdt A
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14175B196 List:
References
50-261-80-23, IEB-79-13, NUDOCS 8011040357
Download: ML19339A585 (4)


Text

>n ne4 9'o UNITED STATES

NUCLEAR REGULATORY COMMISSION o

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$

[E REGION 11 o,

101 MARIETTA ST N.W.. SUITE 3100 g

e ATLANTA, GEORGIA 30303 c..... o Report No. 50-261/80-23 Licensee: Carolina Power and Light Company 411 Fayetteville Street Raleigh, NC 27602 Facility Name:

H. B. Robinson Docket No. 50-261 License No. DPR-23 Inspection at H. B. Robinson site near Hartsville, S.C.

Inspector:

2 Su J.

Da'te Signed Approved by:

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et A. R. Herdt, Section Chief, RCES Branch Nate' Signed SUMMARY Inspection on September 3 through 5,1980 Areas Inspected

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This routine announced inspection involved 24 inspector-hours on site in the areas of Inservice Inspection Program, Procedures and Records, IE Bulletin 79-13 Followup Inspection, CRD Canopy Repair Work, Previously identified Inspection Findings.

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Lesults Of the four areas inspected, no items of noncompliance or deviations were identified.

8011040

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W DETAILS 1.

Persons Contacted Licensee Employees

  • R. B. Starkey, Sr., Site Manager
  • J. M. Curly, Engineering Supervisor
  • H. S. Zimmerman, Technical and Administrative Manager M. F. Page, Engineer B. W. Garrison, QA Superviso'r D. H. Bauer, QA Specialist C. Hardee, Engineer T. Hudson, Associate Engineer Other licensee employees contacted included several technicians, security force meubers and office personnel.

NRC Resident Inspector

  • S. Weise
  • Attended exit interview

2.

Exit Interview The inspection scope and findings were summarized on September 5, 1980 with those persons indicated in Paragraph I above.

The inspector expressed concern over the repetitive nature of the CRDM carfoy leak problem.

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3.

Licensee Action on Previous Inspection Findings

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(Closed) Unresolved Item (50-261/79-23-01) " Documentation of Inspection

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Coverage".

The final report for the 1979 outage inservice isnpection

provided an explanation of the notation " PAR" which appeared on the inspec-

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tion data report. In addition, during the 1980 outage inspections the data was being supplemented with descriptions or sketches.

4.

Unresolved Items Unresolved items were not identified during this inspection.

5.

Inservice Inspection (ISI)

a.

Program

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The inspector reviewed the licensee's program for the control and l

conduct of.the inservice inspection of Class 1, 2, and 3 systems. The licensee's inservice inspection responsibilities and reporting require-

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Y-2-ments, as described in the current administrative procedures are not up to date with the requirements of ASME Section XI, 74 and 75 which is the plant commitment. During discussion of this matter with the licensee's engineering personnel, the inspector was shown a draft diange to sections 4 and 12 of the Administrative Procedures manual which describes the areas of responsibility and the reporting require-ments afor the Class 1, 2, and 3 inservice inspection. The inspector informed the licensee that the change to the procedure would be the subject of an inspector follow-up item, 50-261/80-23-01, Administrative Procedure - Inservice Inspection - Functional and Reporting Requirements.

b.

Data Review - 1979 Outage

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The report for the results of the inservice inspection'during the 1979 refueling outage were reported by the licensees letter Serial: RSEP/

80-410 (undated), received by Region II on April 9,1980.

This report was reviewed in detail in the Region II office and at this time the inspector has no questions concerning the content of the report.

c.

Inservice Inspection - 1980 Outage At the time of the inspection the inservice inspection work activities had been essentially compl:ted and the data was being reviewed for preparation of the final report.

The licensee stated that the ISI contractor, Westinghouse Nuclear Service' Division, was in the process of reviewing previous inspection records and fabrication radiographs in an effort to resolve an indication recorded during the ultrasonic inspection of a weld in the regenerative heat exchanger.

The inspector made a general review of the inspection generated during this outage. The detail review of the data records will be conducted after the licensee accepts the results presented by his contractor and forwards the report to the NRC.

These were no items of noncompliance or deviations in this area of the inspection.

16.

IE Bulletin 79-13 Followup Inspection The licensee had completed the re-inspection of the steam generator feedwater line welds and base material areas required by the IEB 79-13. This re-inspec-tion was required because of the repairs required during the last outag i

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-3-The inspector reviewed the radiographs fc-the following welds:

16-FW-9-25-FW12 16-FW-9-25-W2 16-FW-10-37-FW21 16-FW-10-37-W2 16-FW-10-37-W1 16-FW-10-FW20 16-FW-11-51-FW33 16-FW-11-51-W2 16-FW-11-51-W1

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16-FW-11-FW32 16-FW-11-FW27 The inspector also reviewed the radiographs for the feedwater base material adjacent to the auxiliary feedwater connection.

These were no items of noncompliance or deviations in this area of the inspection.

7.

CRDM Seal Canopy Repairs During inspection of the canopy seal welds, the inspector found indications of leakage through three of the canopies. The indications noted were as follows:

Mechanism D-4 Four Pinholes Mechanism K06 Two Linears Mechanism L-5 Three Pinholes At the time of this inspection the repair welding operations had been i

completed by Westinghouse Nuclear Service Division using procedure No.

RAN-51233-1 Rev.

3.

The inspector reviewed the LER file for similar problems and noted that weld repairs were made to crdm canopies during the 1976, 78, 79 and 80 outages.

(There was no outage in 1977). The mechanisms repaired were as follows:

1976 C-9; D-4; L-13 1978 D-4; G-7 1979 K-6; L-5; M-6; N-7 1980 D-4, K-6, L-5 This showed that all three mechanism positions repaired during this outage were repeats. This was discussed with the licensee as an area of concern.

The licensee indicated that the repetitive nature of the problem was under review with consideration being given to additional work being done during the 1981 outage which is scheduled to be a major outage as it is the final i

outage interval.

There were no items of noncompliance or deviations noted in this area of the inspection.

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