ML14181A615

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Insp Rept 50-261/94-23 on 940821-0924.Violations Noted.Major Areas Inspected:Operational Safety Verification,Surveillance Observation,Maint Observation,Operator Overtime & Followup
ML14181A615
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 10/05/1994
From: Christensen H, Ogle C, William Orders
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14181A612 List:
References
50-261-94-23, NUDOCS 9410190023
Download: ML14181A615 (17)


See also: IR 05000261/1994023

Text

C,

REU4

UNITED STATES

o

NUCLEAR REGULATORY COMMISSION

REGION II

0

101 MARIETTA STREET, N.W., SUITE 2900

U

ATLANTA, GEORGIA 30323-0199

Report No.:

50-261/94-23

Licensee:

Carolina Power and Light Company

P. 0. Box 1551

Raleigh, NC 27602

Docket No.:

50-261

License No.: DPR-23

Facility Name: H. B. Robinson Unit 2

Inspection Conducted: August 21 - September 24, 1994

Inspectors:

  1. 2

L4

/C 9

W/ T. Orders, Senfor

sident Inspector

Date Signed

R

lge, Re~ den Inspector

D

Signed

Approved by: ?0oCh

.0.2Christensen, Chief

Date Signed

Reactor Projects Section lA

Division of Reactor Projects

SUMMARY

Scope:

This routine, unannounced inspection was conducted in the areas of operational

safety verification, surveillance observation, maintenance observation,

operator overtime, and followup.

Results:

An apparent violation was identified involving the failure to properly

establish containment integrity (Paragraph 3.b); a second apparent violation

was identified involving pressurizer cooldown rates in excess of Technical

Specification Limits (Paragraph 3.d); a violation was identified involving the

failure to follow the physical security plan (Paragraph 3.e); an unresolved

item was identified involving the exhaust air quality through ASCO solenoid

valves (Paragraph 4.b); a second unresolved item was identified involving the

adequacy of control room exhaust damper testing (Paragraph 4.b); and a

weakness was identified with the routine use of overtime (Paragraph 3.c).

9410190023 941005

PDR ADOCK 05000261

G

PDR

REPORT DETAILS

1.

Persons Contacted

S. Billings, Technical Aide, Regulatory Compliance

  • W. Brand, Supervisor, Environmental Radiation Control
  • M. Brown, Manager, Design Engineering
  • A. Carley, Manager, Site Communications

M. Chmielecki, Manager, Computer Support

B. Clark, Manager, Maintenance

  • T. Cleary, Manager, Mechanical Maintenance

D. Crook, Senior Specialist, Regulatory Compliance

J. Eaddy, Manager, Environmental and Radiation Support

  • F. Eckert, Manager Integrated Scheduling
  • J. Epperly, Manager, Craft Resources
  • C. Gray, Manager, Materials and Contract Services
  • D. Gudger, Specialist Regulatory Affairs
  • S. Harrison, Manager, Environmental Radiation Control
  • M. Herrell, Acting Plant Manager
  • S. Hinnant, Vice President, Robinson Nuclear Project

K. Jury, Manager, Licensing/Regulatory Programs

  • J. Kozyra, Project Specialists, Licensing/Regulatory Programs
  • R. Krich, Manager, Regulatory Affairs

A. McCauley, Manager, Electrical Systems, Technical Support

  • D. Nelson, Manager, Outage Management

E. Shoemaker, Manager, Mechanical Systems, Technical Support

  • D. Taylor, Plant Controller

G. Walters, Manager, Support Training

  • R. Warden, Manager, Nuclear Assessment Section
  • W. Whelan, Industrial Hygiene and Safety Representative
  • L. Woods, Manager, Technical Support

Other licensee employees contacted included technicians, operators,

engineers, mechanics, security force members, and office personnel.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2. Plant Status

The unit operated throughout the report period at or near full power

with no major operational perturbances.

3. Operational Safety Verification (71707)

a.

General

The inspectors evaluated licensee activities to confirm that the

facility was being operated safely and in conformance with

regulatory requirements. These activities were confirmed by

direct observation, facility tours, interviews and discussions

with licensee personnel and management, verification of safety

system status, and review of facility records.

2

The inspectors reviewed shift logs, Operation's records, data

sheets, instrument traces, and records of equipment malfunctions

to verify equipment operability and compliance with TS. The

inspectors verified the staff was knowledgeable of plant

conditions, responded properly to alarms, adhered to procedures

and applicable administrative controls, cognizant of in-progress

surveillance and maintenance activities, and aware of inoperable

equipment status through work observations and discussions with

Operations staff members. The inspectors performed channel

verifications and reviewed component status and safety-related

parameters to verify conformance with TS. Shift changes were

routinely observed, verifying that system status continuity was

maintained and that proper control room staffing existed. Access

to the control room was controlled and operations personnel

carried out their assigned duties in an effective manner. Control

room demeanor and communications were appropriate.

Plant tours were conducted to verify equipment operability, assess

the general condition of plant equipment, and to verify that

radiological controls, fire protection controls, physical

protection controls, and equipment tagging procedures were

properly implemented.

b.

Mispositioned Containment Isolation Valves

On August 29, 1994, with the unit at 100 percent power, an SRO

conducting a walkdown, observed that 9 normally closed main steam

line drain valves were open. Following this discovery, the

control room was notified, the valves were repositioned, and a

partial valve lineup for the main and reheat steam system was

conducted. No other valves were found to be in the incorrect

position. An ACR was generated to address this event.

The mispositioned valves were:

MS-19

SG "A" Steam Line Before Seat Drain Root

Isolation

MS-19A

SG "A" Steam Line Before Seat Drain Isolation

MS-21

SG "A" Steam Stop V1-3A After Seat Drain Root

Isolation

MS-28

SG "B" Steam Line Before Seat Drain Root

Isolation

MS-28A

SG "B" Steam Line Before Seat Drain Isolation

MS-30

SG "B" Steam Stop V1-3B After Seat Drain Root

Isolation

MS-37

SG "C" Steam Line Before Seat Drain Root

Isolation

MS-37A

SG "C" Steam Line Before Seat Drain Isolation

MS-39

SG "C" Steam Stop V1-3C After Seat Drain Root

Isolation

-3

These valves, along with six others, are used to drain the MSIVs

and the associated upstream steam piping. The drains are arranged

2-lines per steam header with 3 valves each in the before seat

drain lines and 2 valves each in the after seat drain lines.

According to the main steam system drawing, the Q-boundary ends

immediately after the root isolation valve in each of the drain

lines.

During plant startup, the valves are opened to drain the main

steam piping in the vicinity of the MSIVs. The valves are also

used to dissipate steam for RCS temperature.control while the unit

is in hot shutdown and during plant startup. All 15 valves are

closed during startup by a step in GP-005, Power Operation, which

designates the valves by number and name.

In response to this event, the inspectors reviewed the ACR

generated for this event as well as the licensee's documentation

relating to containment integrity. The inspectors also

interviewed the SCO and in-plant SRO responsible for aligning the

MSIV before and after seat drain valves during the plant startup

on August 6, 1994.

Finally, the inspectors reviewed the completed

GP-005 as well as the containment integrity valve lineup

procedure, OP-923, Containment Integrity.

On August 30, 1994, during this followup, the inspectors

determined that 3 of the mispositioned valves were designated as

containment isolation valves in the UFSAR and the licensee's

Generic Issue Document 90-181, Reactor Containment Isolation.

Specifically, the root isolation valves for the before seat

drains, MS-19, MS-28, and MS-37, were listed as containment

isolation valves in both references. The potential implications

of this discovery were discussed with licensee management later

that day. At approximately 8:05 a.m. on August 31, 1994, the

licensee determined that the 3 mispositioned containment isolation

valves represented a condition that was possibly outside the

design basis of the plant.

This determination was based on the

licensee's conclusion that although one closed manual valve

existed in the drain lines downstream of the containment isolation

valves, the valves were not seismically qualified. Hence, no

credit for the lines remaining intact downstream of the root

valves (containment isolation valves) could be taken.

Accordingly, at 8:56 a.m. that morning, the licensee made a one

hour non-emergency notification to the NRC pursuant to 10 CFR

50.72 (b)(1)(ii)(B).

On August 31, 1994, licensee personnel determined from a review of

the MSIV drawing that the valves identified as the MSIV after seat

drain root isolation valves, MS-21, MS-30, and MS-39 were in fact,

upstream of the MSIVs. The licensee determined that the plant

main steam drawing was in error since it showed the after seat

drain root isolation valves downstream of the MSIV seats. The

4

implication of this discovery was that a total of six containment

isolation valves had been open with the unit at 100% power.

From their review of this event, the inspectors determined that

apparently, a communications error between the in-plant SRO and

SCO resulted in the 9 valves listed above not being closed during

the August 6, 1994, startup.

As described by both SROs involved, the in-plant SRO was in the

field directing the efforts of A~s during the plant startup.

During the course of the startup, the SCO directed that the in

plant SRO close the before and after seat drains for the MSIVs.

The in-plant SRO assumed that this order was to isolate the drain

lines to control RCS temperature. The inspectors were advised

that when the drain lines are isolated to control RCS temperature,

only the downstream valves (MS-40, MS-41, MS-42, MS-43, MS-44, and

MS-45) are closed. The in-plant SRO told the inspectors that he

directed the A~s to close these six valves and witnessed them

being closed. In fact, the SCO intended that all 15 valves in the

MSIV before and after seat drain lines be closed to comply with

step 16 of GP-005. The in-plant SRO stated that he had a working

copy of GP-005 in his possession and had been using it during the

startup but admitted that he did not consult it for closing the

drain valves since he did not recognize this as a step in the GP.

At shift turnover, signatures were transferred from working copies

of the GP to the master control room copy. The in-plant SRO told

the inspectors that it was at this point that he recognized the

communications failure. However, based on his recollection that

the drain lines were isolated as a result of a control room order

and his personal observation of the AO actions, he signed the

master copy of GP-005 to reflect that all 15 valves were shut.

The in-plant SRO also advised the inspectors that fatigue

associated with lengthy work hours the day of the startup and

earlier that week may have contributed to his error. The

inspectors reviewed the in-plant.SRO's timecard for the week

before the startup and security logs for the day of the startup.

These records indicated that the in-plant SRO worked 59 hours6.828704e-4 days <br />0.0164 hours <br />9.755291e-5 weeks <br />2.24495e-5 months <br /> the

week before the startup, was off the day before the startup and

was on site for approximately 14 hours1.62037e-4 days <br />0.00389 hours <br />2.314815e-5 weeks <br />5.327e-6 months <br /> the day of the startup. The

inspectors were provided the administrative approvals granted per

PLP-15, Program for Nuclear Power Plant Staff Working Hours, which

authorized extended hours for this individual on August 3 and

August 6, 1994. As a result of these approvals and the day off on

August 5, 1994, the in-plant SRO appeared to be in compliance with

TS requirements for working hours the day of the startup.

The inspectors concluded that the failure to immediately verify

the position of the other drain valves when the communications

failure was recognized, represented a failure on the part of the

in-plant SRO.

5

During the course of their initial review of this event, the

licensee determined that selected necessary changes to plant

procedures and documents to support the Containment Isolation GID

which was completed in January 1994, had not been made. The GID

was developed and implemented-in January 1994 to formally

establish the plant's containment isolation design basis. It was

undertaken as a result repetitive problems associated with

inconsistencies in various plant documents on the exact

containment boundaries. The GID is a detailed document which

identifies and provides the supporting rationale for the

containment isolation boundaries for each containment penetration.

The cause for the disparity between some plant procedures and the

GID was not formally reviewed by the inspectors in this

inspection. The subject was reviewed by the Event Review Team

chartered by the licensee to investigate this event, and was the

topic of an enclosure to the team's (draft) report. The Event

Review Team noted that while the GID received the appropriate

design verification and safety reviews, no formal process existed

to ensure that changes to plant procedures would be implemented in

a timely fashion. Most importantly, OP-923 was not revised to

reflect the appropriate main steam drain valves as containment

isolation valves coincident with the issuance of the GID in

January 1994. The inspectors were informed that 3 of the 6

mispositioned containment isolation valves were identified on a

proposed change to OP-923 which had not been completed at the time

of the mispositioning.

To ensure that the existing plant containment isolation

configuration regarding manually closed containment isolation

valves met licensing basis requirements, the licensee completed a

safety review on containment isolation configuration on

September 3, 1994. This included a review of the valve lineup

conducted per OP-923. Valves listed in the GID as containment

isolation valves, but not included in OP-923 had been verified to

be in the correct position during a licensee walkdown on

September 2, 1994. No valves were reported to be found in the

incorrect position. The safety review concluded that the existing

configuration of the plant's manual containment isolation valves

meets the license requirement.

Overall; the inspectors concluded that six containment isolation

valves remained open between August 6, 1994 and August 23, 1994,

while the unit operated at full power.

Technical Specification 3.6.1 requires that containment integrity

be established whenever the reactor is not in a cold shutdown

condition. Additionally, GP-005, Power Operation, required the

nine drain valves to be closed during power operations.

From August 6, 1994, until August 29, 1994, containment integrity

was not properly established in that the MSIV Before and After

Seat Drain Valves, containment isolation valves, were open instead

6

of closed. During this period, the reactor was operating at

power. Additionally, the Containment Isolation GID was not

adequately implemented.

This is identified as an Apparent Violation, 94-23-01:

Failure To

Properly Establish Containment Integrity.

c.

Operator Overtime

The resident inspectors performed a review of H. B. Robinson's

program for controlling staff working hours, based on their

observations that licensed operators were working what appeared to

be a routine and in some cases excessive overtime.

Robinson Specifications Section 6.2.3.b requires that

administrative procedures be developed and implemented to limit

the working hours of plant Staff who perform safety related

functions.

The site's overtime plan is delineated in procedure PLP-015,

Program For Nuclear Power Plant Staff Working Hours. The stated

purpose of the procedure is to provide the instructions and

controls necessary to comply with Generic Letter No. 82-12,

"Nuclear Power Plant Staff Working Hours," and other regulatory

guidance regarding the limitation for nuclear power plant staff

overtime and work hours.

In general, Generic Letter No. 82-12 required that licensees of

operating plants include in their administrative procedures

provisions regarding required shift staffing, the objective of

which, was the prevention of situations where fatigue could reduce

the ability of operating personnel to keep the reactor in a safe

condition.

PLP-015, requires that enough plant operating personnel be

employed to maintain adequate shift coverage without routine heavy

use of overtime. The objective is to have operating personnel

work a normal shift, based on their work schedule while the plant

is operating. However, in the event that unforseen problems

require substantial amounts of overtime to be used, or during

extended periods of shutdown for refueling, major maintenance, or

major plant modifications, on a temporary basis, the following

guidelines are to be followed:

An individual should not be permitted to work more

than 16

hours straight, excluding shift turnover

time.

7

.

An individual should not be permitted to work more

than 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br /> in any 24-hour period, nor more than 24

hours in any 48-hour period, not more than 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> in

any seven day period, all excluding shift turnover

time.

.

A break of at least eight hours should be allowed

between work periods, including shift turnover time.

.

Except during extended shutdown periods, the use of

overtime should be considered on an individual basis

and not for the entire staff on a shift.

Briefly restated, overtime should be used in unforeseen activities

on a temporary basis, and should not be routine.

The procedure states that in the event that unusual work

conditions or emergencies require personnel to exceed scheduled

hours and/or work in excess of the established Technical

Specifications limits, the Plant Manager or his designee must

approve it.

The inspectors performed a detailed review of the amount of

overtime worked by licensed operators this calendar year. The

review indicated that the operating crews had routinely worked 18

20 percent overtime. Some licensed individuals had overtime rates

as high as 30 percent.

The inspectors reviewed documentation of plant management approval

to allow the operators to work this overtime, and detected no

cases in which management approval was not obtained, nor where the

requirements of Technical Specification 6.2.3.b had not been met.

The inspectors were concerned that the operators were working

routine overtime which is not in keeping with the intent of

Technical Specification 6.2.3.b. These observations were

discussed with licensee management who agreed that the documented

overtime was routine, but informed the inspectors that recent

actions had been taken to minimize the use of operator overtime.

The goal in mind was for 10 percent or less.

The inspectors concluded that this routine use of overtime is

marginally acceptable and is considered a weakness. The

inspectors will monitor the licensee's efforts to reduce routine

use of overtime.

d.

Excessive Pressurizer Cooldown Rate

Unresolved Item, URI 94-22-01, documents the inspectors'

inspection activities associated with pressurizer cooldown rates

which were apparently in excess of TS limits. These cooldown

rates occurred while collapsing the pressurizer bubble on

February 26, 1994, during a plant shutdown. At 10:30 a.m. on

August 19, 1994, after a preliminary verification of the

inspectors' observations, the licensee entered an operability

determination on the pressurizer. The operability determination

was completed on August 22, 1994 and concluded that the

February 26, 1994 transient

"...

did not damage the structural

integrity of the pressurizer or surge line and that continued

operation is acceptable."

This conclusion was based on an initial

assessment of the transient data by Westinghouse and a

satisfactory RCS hydrostatic test which was conducted during the

startup after the cooldown. It was also documented in the

operability package, that a more detailed analysis of the

transient by Westinghouse would be forthcoming. An ACR was

generated to address the event.

In response to this issue, the inspectors reviewed portions of the

operability package as well as the results of the initial

Westinghouse assessment of the February 26 cooldown data. The

inspectors also examined the results of a licensee review of

previous pressurizer cooldowns conducted to determine if similar

transients had occurred. The ACR was still being evaluated by the

licensee at the end of the inspection period, thus a final version

was not reviewed.

The licensee's preliminary analysis of the pressurizer transient

contained in the August 22, 1994, operability package, established

the following pressurizer cooldown/heatup rates:

Steam temperature cooldown:

212F/hr

Water temperature cooldown:

207F in 46 minutes (270F/hr)

Surge line heatup:

101F/hr.

The inspectors independently reviewed the February 26 data and

determined the following regarding the pressurizer cooldown/

heatup:

Steam temperature cooldown:

Exceeded 200F/hr from

5:53 p.m. to 6:10 p.m.

Maximum rate observed in one

hour 212F/hr

Water temperature cooldown:

Exceeded 200F/hr from

5:35 p.m. to 6:07 p.m.

Maximum rate observed in one

hour 240F/hr

Surge Line Temperature:

Exceeded 200F/hr from

6:02 p.m. to 6:07 p.m.

Maximum rate observed in one

hour 215F/hr

Shorter intervals were more

erratic. For example: 164F @

5:56 p.m. to 360F @ 6:01 p.m.

or 196F in 5 minutes or

470F/hr heatup rate.

The inspectors used moving 1-hour intervals to obtain the cooldown

rates identified above. No effort was made to identify

pressurizer cooldown rates over shorter intervals. The inspectors

noted from a licensee memo documenting their review of prior

pressurizer cooldown transients, that similar cooldown rates

excursions in excess of the 200F/hr TS 3.1.2.3 limit had occurred.

The licensee documented 3 such occurrences between August 1989 and

November 1993. In these instances, the timeframe of the apparent

excessive pressurizer cooldown rates was reported by the licensee

as ranging from 4 to 18 minutes. Multiple instances of excessive

cooldown rates were reported in two of the subject cooldowns.

(The licensee indicated that the results of this initial review

were preliminary and that the data from these cooldowns was

provided to Westinghouse for further analysis.)

The licensee also

determined that sufficient data was not available in seven of the

pressurizer cooldowns to reconstruct a cooldown rate. For the

remaining cooldowns, the licensee review noted that the available

data or method of cooldown made excessive pressurizer cooldown

rates unlikely. The inspectors did not independently review

temperature data for pressurizer cooldowns prior to the

February 26, 1994, cooldown.

Technical Specification 3.1.2.3 limits the maximum pressurizer

cooldown rate to 200 degrees Fahrenheit per hour. Additionally,

Precaution and Limitation 3 of General Procedure, GP-007, Plant

Cooldown From Hot Shutdown To Cold Shutdown, specifies that the

maximum pressurizer cooldown rate shall not exceed 200 degrees

Fahrenheit per hour.

On February 26, 1994, the pressurizer cooldown rate exceeded 200

degrees Fahrenheit per hour when operators were collapsing the

pressurizer bubble. Pressurizer water space, steam space, and

surge line cooldown rates all exceeded the Technical Specification

limit with maximum cooldown rate observed approaching 240 degrees

Fahrenheit per hour.

The excessive pressurizer cooldown of February 26, 1994, is

identified as an Apparent Violation, 94-23-02: Pressurizer

Cooldown In Excess of Technical Specification Limits. URI 94

22-01 is closed

e.

Failure To Follow Security Procedures

On September 15, 1994, during a routine tour, the inspectors

observed that one of two individuals encountered had no visible

security badge. When questioned, the individual produced an

10

"escort required" badge from his pocket. The other individual

also had an "escort required" badge. These individuals informed

the inspectors that their escort was in an adjacent restroom.

(The individuals were approximately four feet from the door of the

restroom. The door to the restroom was closed when the inspectors

made their observations.) The inspectors accompanied the

individuals into the restroom and confirmed that the responsible

escort was indeed present. Based on the inspectors' observations,

it was estimated that the two individuals were not under the

control of the escort for approximately one minute.

Licensee Physical Security Plan, paragraph 4.5, Escorts, states

"Personnel authorized entry to the protected area as Escorted

Personnel shall be escorted." Additionally, paragraph 3.2.1.6,

Picture Badge System states, "while in the protected area, badges

will be displayed in a conspicuous manner on the upper front

torso, preferably in the vicinity of the collar at shoulder

height."

On September 15, the licensee failed to comply with the above

requirements, in that, the NRC Inspectors observed that:

1)

An assigned escort left two visitors unattended in the

turbine building while he used an adjacent restroom.

2)

One of the two visitors failed to display his security badge

on his upper front torso while in the protected area. The

badge was in the visitor's possession in his pocket.

These two examples constitute a violation, VIO 94-23-03:

Failure

To Follow Physical Security Plan.

Three violations were identified.

Except as noted above, the

area/program was adequately implemented.

4.

Maintenance Observation (62703)

a.

General

The inspectors observed safety-related maintenance activities on

systems and components to ascertain that these activities were

conducted in accordance with TSs, approved procedures, and

appropriate industry codes and standards. The inspectors

determined that these activities did not violate LCOs and that

required redundant components were operable. The inspectors

verified that required administrative, material, testing,

radiological, and fire prevention controls were adhered to. In

particular, the inspectors observed/reviewed the following

maintenance activities detailed below:

WR/JO 94-BTTOO1

Calibrate MDAFW Pump B Discharge

Pressure Gauge

WR/JO 94-BYE191

Calibrate RWST LI 969 and LT 969

WR/JO 94-ANIQI

Replace Control Room Exhaust Damper

Air Solenoid Valve

b.

Control Room Exhaust Damper Maintenance

On September 8, 1994, the inspectors witnessed maintenance on

control room exhaust damper CRD1A accomplished in accordance with

WR/JO ANIQI.

The maintenance effort consisted of replacing the

ASCO solenoid valve in the instrument air line to remedy a 30

second delay observed in the damper operation. The actuator, air

filter/regulator, and solenoid valve for the damper were removed

to facilitate the maintenance.

Overall, the repair efforts were satisfactory. Positive

attributes noted included involvement by the I&C supervisor during

the task and a questioning attitude on the part of the technicians

regarding difficulties in reconnecting the instrument air lines.

This questioning attitude resulted in the discovery and repair of

improperly configured connections in the instrument air tubing.

As part of this inspection, the inspectors reviewed Engineering

Evaluation, EE 94-133, Equivalency Evaluation For Control Room

Damper Solenoid Valves SV-6521 and SV-6522. This EE was performed

to allow the use of a replacement ASCO solenoid valves in the

damper control circuit which had different elastomer materials.

The replacement solenoid valves had ethylene propylene elastomers

while the installed solenoid valves had Viton elastomer materials.

The EE stated that the replacement valve was identical in all

other respects.

The ASCO literature enclosed in the EE noted that "Ethylene

propylene... has the distinct disadvantage that it cannot be used

with petroleum-based fluids or fluids so contaminated (such as

lubricated air)."

The EE addressed this caveat by stating that

instrument air is provided from non-lubricated air compressors and

that prefilters are provided in the system to remove oil and

water. Additionally, the EE noted that as described in the FSAR

the instrument air design basis is to supply oil free air, free of

foreign materials. Based on these arguments the EE concluded "it

has been demonstrated that the air supply to the subject valves

does not contain lubricated air, therefore, the use of ethylene

propylene elastomers for the subject valves will not present any

adverse concerns."

To confirm the validity of the premise for this conclusion, the

inspectors reviewed analyses of instrument air samples which

revealed methane, total gaseous hydrocarbons and oil mist/

12

particulate in small but measurable quantities. Following

inspector questioning, the licensee provided additional

information which demonstrated that the replacement valves

remained acceptable despite the air quality test results.

The inspectors concluded that the EE failed to adequately address

the impact of known instrument air contaminants documented in

existing test results on the replacement solenoid valve. While

the safety significance of this failure was minimal, this is

considered a weakness.

The manufacturer's literature provided to address the inspector's

concerns on instrument air contaminants contained a precaution

regarding the ASCO valves used in nuclear power plant

applications. The precaution stated that the quality of the air

flowing through the ASCO valve during both the exhaust and

pressurization cycles must meet the ASCO recommendations.

As configured in the control room damper installation, the damper

actuator is continually pressurized by instrument air supplied

through the ASCO solenoid valve. To close the damper, the

instrument air between the solenoid and the actuator is vented

through the solenoid and the actuator spring closes the damper.

Hence, the air in contact with the actuator is vented back through

the -ASCO solenoid. During the performance of the maintenance, the

inspectors noted an oily residue in the bottom of the instrument

air connection to the actuator (This material was subsequently

removed by the I&C technicians with swabs.) A review of the

actuator technical manual indicated that a DuBois MPG-2 grease or

equal is used in the actuator. On September 15, 1994, the

inspectors questioned the licensee on their compliance with the

ASCO recommendation on exhaust air quality given the observed oily

residue in the actuators air connection. Pending the licensee's

evaluation of this question, this will be tracked as an unresolved

item, URI 94-23-04:

Exhaust Air Quality Through ASCO Solenoid

Valve.

The inspectors also questioned the adequacy of the licensee's

testing of the exhaust dampers following the repair effort. The

inspectors' questions initially centered on the need to test the

capability of the CRD1A damper to seal following actuator removal

and installation. The inspectors were provided sufficient

information to demonstrate that a degradation in the sealing

capability of the damper following the observed maintenance was

unlikely. However, the inspectors questioned the licensee's

previous testing program for the exhaust dampers. The inspectors

were advised by the licensee that no testing was performed to

demonstrate the capability of a single exhaust damper to provide

sufficient isolation to allow control room pressurization. In as

much as the system was designed to remain operable following a

single active failure, the inspectors questioned the lack of a

test to demonstrate that the CR could be pressurized given the

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failure of one exhaust damper to close. Pending further

inspection, this item will be tracked as an Unresolved Item,

URI, 94-23-05: Adequacy Of Control Room Exhaust Damper Testing.

No violations or deviations were identified. Except as noted above, the

area/program was adequately implemented.

c.

Surveillance Observation (61726)

The inspectors observed certain safety-related surveillance

activities on systems and components to ascertain that these

activities were conducted in accordance with license requirements.

For the surveillance test procedures listed below, the inspectors

determined that precautions and LCOs were adhered to, the required

administrative .approvals and tagouts were obtained prior to test

initiation, testing was accomplished by qualified personnel in

accordance with an approved test procedure, and test

instrumentation was properly calibrated. Upon test completion,

the inspectors verified the recorded test data was complete,

accurate, and met TS requirements, test discrepancies were

properly documented and rectified, and that the systems were

properly returned to service. Specifically, the inspectors

witnessed/reviewed portions of the following test activities:

OST-401

Emergency Diesels (Slow Speed Start)

(EDG A Only)

No violations or deviations were identified.

5.

Review of LERs (30703)

a.

(Closed) LER 92-010-00 and LER 92-010-01, Technical Specification

violation due to inadequate surveillance testing.

LER 92-010-00 and LER 92-010-01 which dealt with surveillance

testing of auxiliary feedwater flow were reviewed to determine if

the information provided met NRC requirements. The determination

included: adequacy of description, verification of compliance with

Technical Specifications and regulatory requirements, corrective

action taken, existence of potential-generic problems, reporting

requirements satisfied, and the relative safety significance of

the event. These LERs are closed.

b.

(Open) LER 94-13-00, EDG Fire Of June 6, 1994

This voluntary LER 94-13-00, which is being generated by the

licensee, involves an incident which occurred on June 6, 1994. A

small fire occurred on the "A" Emergency Diesel Generator (EDG)

during a test run. The fire was first observed by the System

Engineer who reported it to the Control Room at 11:39 a.m. The

site Fire Brigade was activated but during diesel load reduction,

the fire went out. The fire was reported out at 11:44 a.m.

14

There were no injuriesor equipment damage, nor was offsite

assistance required. Because the fire occurred on safety related

equipment, the site Emergency Plan required that an ALERT

condition be declared. Since no further emergency actions were

required after the fire was extinguished, the ALERT was terminated

shortly after being declared. The small fire was caused by lube

oil leaking from the engine where the exhaust manifolds attach to

the engine casing. The licensee subsequently determined that the

torque which had been applied to the bolts which secure the

manifolds to the engine had relaxed due to apparent thermal cycle

induced compression/crushing of the exhaust manifold gasket

material. A subsequent inspection of the disassembled exhaust

system also identified that the exhaust heat shield in the area of

the fire had been installed upside down. In this configuration,

the exhaust heat shield formed a small reservoir into which the

leaking oil had accumulated. This small accumulation of oil had

apparently resulted in the fire on June 6. The exhaust manifolds

were reinstalled and torqued to the proper value. A surveillance

program to monitor the EDGs for oil leakage was implemented as an

interim corrective action until long term corrective actions could

be identified and implemented.

After repairs were completed on June 9, 1994, the "A" EDG was

satisfactorily run with no leakage observed at the cylinder to

exhaust manifold interface, and the diesel was returned to

service.

The resident inspectors have routinely monitored the EDG's during

surveillance tests performed since June 9, 1994. It has been

noted that both EDG's continue to have oil leaks in the previously

identified exhaust manifold areas.

The licensee, as part of their Integrated Emergency Diesel Action

Plan, is communicating with other owners of Fairbanks Morse EDG's

to determine the extent of the problem, and to identify and

correct the root cause. The resident inspectors will continue to

monitor the diesels and the licensee's efforts to correct the

problem.

6.

Licensee Action on Previous Findings (92701, 90702)

(Closed) VIO 90-11-01, Inadequate Procedures To Implement TS

Surveillance.

This violation pertained to the lack of procedures to facilitate the

testing of power range high flux and two-out-of-three loop low flow

reactor trip logic channels.

A review of corrective actions indicated that the licensee has

implemented procedure changes to facilitate the required testing, and

performed an independent study to determine if there were other examples

15

of TS requirements which had not been implemented due to procedural

deficiencies. The independent study has been completed. This item is

closed.

(Closed) VIO 92-34-01, Failure To Follow Procedure While Performing

Spent Fuel Pool Cooling Surveillance.

This violation involved the performance of a single point temperature

calibration instead of a three point which was required. Corrective

actions included personnel counseling, and the installation of new

temperature indicating equipment which is easier to maintain. This item

is closed.

7.

Exit Interview (71701)

The inspection scope and findings were summarized on September 23, 1994,

with those persons indicated in paragraph 1. The inspectors described

the areas inspected and discussed in detail the inspection findings

listed below and in the summary. There were no dissenting comments

received from the licensee. The licensee did not identify as

proprietary any of the materials provided to or reviewed by the

inspectors during this inspection.

Item Number

Description/Reference Paragraph

Apparent Violation 94-23-01:

Failure To Properly Establish

Containment Integrity

(Paragraph 3.b).

Apparent Violation 94-23-02:

Pressurizer Cooldown In Excess of

Technical Specification Limits

(Paragraph 3.d).

Violation 94-23-03:

Failure To Follow Physical Security

Plan (Paragraph 3.e).

Unresolved Item 94-23-04:

Exhaust Air Quality Through ASCO

Solenoid Valve (Paragraph 4.b).

Unresolved Item 94-23-05:

Adequacy Of Control Room Exhaust

Damper Testing (Paragraph 4.b).

8.

List of Acronyms and Initialisms

ACR

Adverse Condition Report

AO

Auxiliary Operator

CFR

Code of Federal Regulations

CR

Control Room

EDG

Emergency Diesel Generator

EE

Engineering Evaluation

GID

Generic Issue Document

LCO

Limiting Condition for Operation

16

LER

Licensee Event Report

MDAFW

Motor Driven Auxiliary Feedwater Pump

MS

Main Steam

MSIV

Main Steam Isolation Valve

NRC

Nuclear Regulatory Commission

RCS

Reactor Coolant System

RWST

Refueling Water Storage Tank

SCO

Senior Controls Operator

SG

Steam Generator

SRO

Senior Reactor Operator

TS

Technical Specification

UFSAR

Updated Final Safety Analysis Report

URI

Unresolved Item

VIO

Violation

WR/JO

Work Request/Job Order