ML14181A855

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Insp Rept 50-261/96-12 on 960928-1116.Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support
ML14181A855
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 12/16/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14181A853 List:
References
50-261-96-12, NUDOCS 9612230323
Download: ML14181A855 (60)


See also: IR 05000261/1996012

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket No:

50-261

License No:

DPR-23

Report No:

50-261/96-12

Licensee:

Carolina Power & Light (CP&L)

Facility:

H. B. Robinson Unit 2

Location:

2112 Old Camden Rd.

Hartsville, SC 29550

Dates:

September 28 - November 16, 1996

Inspectors:

J. Zeiler, Acting Senior Resident Inspector

P. Byron, Resident Inspector, Surry

J. Coley, Reactor Inspector, RII (Section M1.3)

E. Girard, Reactor Inspector, RII (Section E1.1)

M. Miller, Reactor Inspector, RII (Section M1.2)

W. Rankin, Reactor Inspector, RII (Sections R1

and R8)

G. Wiseman, Project Engineer, RII (Sections Fl,

F2, F3, F5, F7, and F8)

Accompanying Personnel: M. Holbrook, Consultant, Idaho National

Engineering Laboratory (INEL)

R. Hall, Intern, NRC Office of Nuclear

Reactor Regulation (NRR)

T. Scarbrough, NRR

Approved by:

M. Shymlock, Chief, Projects Branch 4

Division of Reactor Projects

Enclosure 2

9612230323 961216

PDR ADOCK 05000261

G

PDR

EXECUTIVE SUMMARY

H. B. Robinson Power Plant, Unit 2

NRC Inspection Report No. 50-261/96-12

This integrated inspection included aspects of licensee operations,

maintenance, engineering, and plant support. The report covers a six-week

period of inspection; in addition, it includes the results of an Inservice

Inspection conducted by a regional inspector, Generic Letter 89-10 program

implementation inspection by regional and headquarters inspectors,

radiological inspection by a regional inspector, and a fire protection

inspection by a regional projects engineer.

Operations

Containment integrity was not assured during core reload activities.

Operations procedures and controls were not adequate to ensure

containment integrity was established and maintained during refueling

operations. Contributing to this was inadequate oversight and

coordination of work activities affecting containment integrity status.

This issue was the subject of a Non-Cited Violation (Section 01.2).

Communication errors resulted in delays in the investigation of a water

hammer in the Safety Injection (SI) cold leg injection lines.

Engineering walkdowns and investigations adequately identified and

corrected damage resulting from the transient. The water hammer

resulted from the failure of operators to ensure that a loop seal was

configured in test apparatus hose connected. This was identified as a

violation for an inadequate surveillance procedure (Section 01.3).

Plant and operator response to an automatic reactor trip was

satisfactory. However, several minor operator training enhancements

were identified (Section 01.4).

An effective program was developed and implemented to protect plant

systems and equipment from cold weather (Section 01.5).

While a formal process for conducting containment coating repairs were

implemented, it was evident that coating upkeep in the past had not

received the appropriate level of attention. Overall progress toward

improving the condition of containment coatings has been slow, and not

consistent with good upgrades that have been implemented in the

Auxiliary and Turbine Buildings over the past year (Section 08.1).

Maintenance

Maintenance and surveillance activities observed were performed

satisfactorily (Section M1.1).

A thorough and detailed program to train and control contractor

personnel during Refueling Outage 17 was implemented. The Maintenance

Department continues to expedite and place emphasis on identifying and

resolving problems through the use of Condition Reports and self

assessment (Section M1.2).

2

Inservice Inspection (ISI) activities conducted during the current

refueling outage were found to have been performed and documented

satisfactorily. New personnel assigned to the ISI program prior to the

outage had conducted their assigned responsibilities effectively.

Problems continued in the area of updating isometric drawings after

welding or component modifications (Section M1.3).

Engineering

Satisfactory implementation of Generic Letter (GL) 89-10 "Safety-Related

Motor-Operated Valve Testing and Surveillance" had not been

accomplished. Several violations were identified involving: (1)

inadequate evaluation of test data, and, (2) inadequate design controls.

Additionally, the licensee's torque seating of butterfly valves was

considered a weakness, as this practice was contrary to the

recommendations of the vendor. Extensive efforts to dynamically test

all motor-operated valves practicable was considered a strength (Section

E1.1).

Engineering walkdowns identified ECCS containment sump deficiencies

which had been created by lack of adequate controls over previous sump

alterations and repairs. A 1988 engineering evaluation of a containment

reflood level error failed to adequately address the impact on the ECCS

sump filtration design (Section E8.5).

Plant Support

The radiological controls program was being effectively implemented and

good occupational exposure controls during outage conditions was

demonstrated.

Good radiological control performance was apparent in the

occupational exposure activities observed. An upgrade in radiation area

posting throughout the facility was evident. Continued emphasis on

procedural adherence to radiation control procedures remains a

challenge. A Non-Cited Violation was identified for failure of a

radiation worker to wear an appropriate monitoring device within the RCA

as required by procedure (Section R1.1).

A high level of personnel contamination events were noted during the

outage which represents a continuing challenge in the licensee's

radiological control program. However, no deficiencies were identified

with respect to adequacy of followup on individual personnel

contaminations or controls for contaminated areas. Although personnel

contaminated events remain relatively high and a challenge area in

radiological controls overall, actions with respect to improving

personnel contamination controls were determined to be appropriate

(Section R1.2).

Overall, the ALARA program was effectively controlling collective site

dose and the total site dose was on a favorable reducing trend (Section

R8.1).

3

Fire protection activities were acceptable. Good compliance with plant

fire prevention procedures was observed. The general housekeeping and

control of combustibles was satisfactory. The control of combustible

and flammable materials was effective (Section F1.1).

Good compliance with plant fire prevention procedures has resulted in a

low incident of fires within the plant protected area (Section F1.2).

When fire protection systems are found degraded or inoperable a high

priority is assigned to promptly return these systems to service. With

one exception, all fire protection features inspected were operational

and appeared to be well maintained. Minor configuration discrepancies

were noted with the pyrocrete fire barriers walls for the Charging Pump

Room (Section F2.1).

Implementation of the fire protection and prevention procedures was

satisfactory. A fire protection program weakness was identified in that

there was no overall plant administrative procedure that documented the

program positions, responsibilities, authorities, or the Fire Hazards

Analysis/Safe Shutdown Analysis and 10 CFR 50, Appendix R exemptions.

Engineering responsibilities for fire protection related activities were

not well defined. A recent 1996 Nuclear Assessment Section audit of the

fire protection program identified several similar weaknesses with fire

protection procedures (Section F3.1).

The performance of the fire brigade during a drill was marginally

satisfactory and did not appear to be up to the standards previously

demonstrated by the plant fire brigade. The fire brigade drill

performance was not as intense as it could have been and guidance to the

off-site fire department personnel was minimal (Section F5.1).

Audits and assessments of the facility's fire protection program were

thorough and appropriate corrective actions were being taken to resolve

the identified issues (Section F7.1).

Report Details

Summary of Plant Status

Unit 2 began the report period in day 21 of a scheduled 39 day refueling

outage (RFO-17).

Fuel reload was completed October 4. The unit was returned

to power operation on October 20 after completing a 42 day outage. That same

day, during power ascension, an automatic reactor trip occurred from 20

percent power due to a turbine trip on steam generator high level.

The unit

was placed back on-line October 21 and operated the remainder of the report

period at essentially full power.

I. Operations

01

Conduct of Operations

01.1 General Comments (71707)

The inspectors conducted frequent control room tours to verify proper

staffing, operator attentiveness and communications, and adherence to

approved procedures. The inspectors attended operations turnover, and

management review meetings to maintain awareness of overall plant

operations. Operator logs were reviewed to verify operational safety

and compliance with Technical Specifications (TSs).

Instrumentation,

computer indications, and safety system lineups were periodically

reviewed from the Control Room to assess operability. Plant tours were

conducted to observe equipment status and housekeeping. Condition

Reports (CRs) were reviewed to assure that potential safety concerns and

equipment problems were reported and resolved. Specific events and

noteworthy observations are detailed in the sections below.

01.2 Failure to Maintain Containment Integrity during Refueling Operations

a. Inspection Scope (71707)

The inspectors reviewed the events surrounding the licensee's

determination that containment integrity was not maintained during

refueling operations. This event was documented in CR 96-02595 and by

Licensee Event Report 50-261/96-06-00, dated November 4, 1996.

b. Observations and Findings

On October 3, 1996, reactor core fuel reload activities were in

progress. At 3:40 p.m., a maintenance contractor inside containment

performing welding to replace the bellows for Containment Penetration

Sleeve S-5, noted that air flow was coming into containment from the

opening in the bellows sleeve that was being welded. Readings obtained

with a hand held oxygen sensor indicated that the flow was air and not

argon gas as might have been expected. The individual expected to find

argon gas in the sample since an argon gas purge rig had been installed

on the auxiliary building side of the penetration to aid in the welding.

However, this rig had previously been isolated by the contractor to weld

the remaining small opening around the sleeve.

2

The control room was notified of the condition, and immediate actions

were taken to determine the source of the inleakage and if a potential

path from containment atmosphere to the outside existed. At the time,

fuel movement had already been placed on hold for an unrelated problem.

During the initial investigation, operations and engineering personnel

became aware that the gas purge rig had been connected to penetration

vent valve PP-58C which was an integral part of the penetration sleeve

boundary. It was noted that this gas rig also contained a vent valve

used by the welders to bleed off the argon gas upon completion of

purging. The position of the gas rig vent valve was checked and it was

discovered to have been open approximately 1/4 turn. The gas rig was

subsequently removed and a leak check of the penetration sleeve was

performed verifying that there was no leakage. Using valve lineup

procedures, operations conducted a verification of the status of all

other mechanical penetrations valves to ensure that no other potential

containment integrity problem existed. In addition, a detailed review

of outstanding clearances was performed to assure that no other

conditions affecting containment integrity existed.

The licensee determined that the most likely path of air flow was

through the gas rig vent valve that was found partially open. Since the

containment purge system was in operation during the welding activity,

the negative pressure created in containment would have drawn air into

containment from the open area in the sleeve that was still being

welded,-and then through this partially open vent valve. The inspectors

noted that during the period that containment integrity was not

maintained, the containment purge system was in operation and capable of

maintaining the containment at a negative pressure in relation to the

outside atmosphere, therefore, the actual safety consequences of this

event were minimal. The inspectors reviewed subsequent leak rate test

results for penetration sleeve S-5 to verify that leakage rates met TS

acceptance limits for plant startup.

The licensee's investigation of the event determined that there had been

inadequate oversight and coordination of the penetration sleeve work and

operations personnel had not adequately verified that containment

integrity was assured prior to refueling operations. Work activities

associated with the sleeve replacement were being performed in

accordance with modification ESR 94-00731. It was recognized that work

had the potential of affecting containment integrity and was supposed to

have been coordinated by working on one side or the other while

maintaining containment integrity of the side not being worked.

However, adequate oversight and coordination of work activities was not

maintained resulting in allowing contract welders to conduct activities

inside containment while the clearance boundary still allowed the

penetration sleeve vent valve on the auxiliary side to be open. The

inspectors reviewed General Procedure (GP)-10, Refueling, Revision 33.

Step 5.3.17.8 provided instructions for establishing refueling integrity

which included the completion of an attachment used to verify the status

of valves in certain penetrations. This attachment did not include all

containment penetration valves; the majority of the penetrations listed

were associated with containment air systems. GP-10 also required an

3

assessment of the status of containment penetrations via review of

outstanding clearances. While operations personnel performed this

action prior to initiating refueling activities on September 30, they

failed to identify that clearances for penetration sleeve 5 jeopardized

containment integrity.

The inspectors agreed with licensee's conclusions that the main cause of

the event was lack of adequate instructions and controls to assure that

refueling integrity was established and maintained prior to commencing

refueling operations. The licensee planned to revise GP-10 prior to the

next refueling outage to include provisions for more positive tracking

controls for all penetration valves during refueling operations.

Similar controls are already in place for conditions prior to refueling

operations such as for reduced inventory.

The failure to maintain containment integrity during refueling

operations was identified as a violation of TS 3.8.1.a. This licensee

identified and corrected violation is being treated as a Non-Cited

Violation (NCV), consistent with Section VII.B.1 of the NRC Enforcement

Policy. This issue was documented as NCV 50-261/96-12-01:

Failure to

Maintain Containment Integrity During Refueling.

c.

Conclusions

Procedures and controls for assuring containment integrity during

refueling operations were inadequate resulting in an open pathway

through a mechanical penetration. Contributing to this was inadequate

oversight and coordination of work activities affecting penetration

status. The licensee conducted a thorough investigation of the event

and initiated or planned suitable corrective actions. Therefore the

failure to maintain containment integrity during refueling operations

was identified as a NCV.

01.3 Water Hammer Event During RCS Check Valve Testing

a. Inspections Scope (71707, 61726)

On October 16, 1996, a water hammer occurred in the Safety Injection

(SI) cold leg injection lines while the licensee was conducting

backleakage testing of SI pressure isolation check valves connected to

the reactor coolant system (RCS).

As a result of the water hammer, a

seismic restraint support was damaged immediately downstream of where

the SI Accumulator A line discharged to the SI cold leg injection line.

The inspectors reviewed the licensee's assessment of the impact of the

water hammer on the piping and their investigation into the cause of the

incident. In addition, the inspectors performed an independent walkdown

of the piping affected by the water hammer.

b. Observations and Findings

On October 16, 1996, operations personnel were restoring the SI

Accumulator piping to its normal alignment after performing backleakage

4

testing of SI check valves that provide RCS pressure isolation. Testing

was conducted while the unit was still in cold shutdown in accordance

with Operations Surveillance Test (OST) procedure OST-160, Pressure

Isolation Check Valve Back Leakage Test, Revision 23. When the SI

Accumulator Discharge Valves (SI-865A, -865B, and -865C) were opened in

accordance with OST-160, water was admitted at 600 psig to partially

voided lines downstream in the SI cold leg injection lines. As a result

of the voided conditions, water hammers occurred in the lines.

Operations personnel in containment recognized from the noise that water

hammers had occurred and an engineering walkdown of the piping was

requested by operations management. Due to communication errors between

operations and engineering, piping in the charging system was examined

instead of the SI system. This error was recognized the following day

and engineering was directed to inspect the SI accumulator and cold leg

injection piping for potential damage.

Engineering inspections identified major damage to one seismic restraint

support, as well as other minor problems such as spalled concrete and a

loose restraint support nut. Damage to the seismic restraint supports

were repaired. Following these repairs, the inspectors conducted a

walkdown of the piping potentially affected by the transient. Repairs

to the restraint support were adequate and no other signs of piping,

insulation, or piping support damage was identified.

On October 18, the water hammer event and engineering findings were

discussed in a conference call between the licensee, NRC Region II, and

NRR management. At the request of NRC management, the licensee agreed

to conduct further inspections of a welded pipe attachment on the SI

piping that had not been visually examined for degradation in the

original scope of the walkdowns. This was accomplished that same day

and no damage was identified.

The inspectors reviewed OST-160 and CR 96-02754, which documented the

licensee's investigation of the transient. OST-160 involved

depressurizing piping upstream of check valves being tested and

pressurizing the downstream piping using a hydro pump. Leakage was then

measured by opening drain valves in the piping upstream of the check

valves. Sections 7.3, 7.5, and 7.7 of OST-160 provided instructions for

testing, among others, the first check valve connected to each SI cold

leg injection line from the Residual Heat Removal (RHR) system. In

order to test these check valves (SI-876A, -876B, -876C), drain valve

SI-876D, which was common to the upstream piping for each of the RHR

check valves, was opened to depressurize the piping. To prevent

draining the piping upstream of these check valves when SI-876D was

opened, a test apparatus was supposed to have been installed to the end

of SI-876D with a loop seal configured and the end of the test apparatus

hose routed to a floor drain. However, explicit instructions for

configuring this loop seal were not included in previous sections of the

procedure (step 7.1.13) which installed the test apparatus. A NOTE was

provided several steps prior to opening SI-876D in Section 7.3 to alert

the operators to route test apparatus hoses over the high point of the

line from which they drain to form a loop seal preventing excessive

5

draining. Similar notes were included in Sections 7.5 and 7.7 for

testing the RHR check valves for the remaining two SI cold leg injection

lines. The operators failed to follow these notes and it was not

recognized that the loop seal from SI-876D was not configured. Further,

the need for a loop seal was again not recognized after it was

identified that it took over four hours to allow SI-876D to depressurize

and drain when the valve was initially opened in Section 7.3 for testing

the RHR check valve to SI cold leg injection line 1. Opening SI-876D

without the loop seal allowed a drainage path for all three SI cold leg

injection lines due to backleakage through the RHR check valves. SI

876D was left open until completing Section 7.7 for SI cold leg loop 3.

Upon opening the SI Accumulator discharge valves at the completion of

testing, water hammers resulted due to the rapid pressurization of the

partially drained SI cold leg piping.

The inspectors concluded that OST-160 did not provide clear instructions

for ensuring that a proper test configuration was established for

testing the check valves. Operations personnel involved with the test

coordination and performance demonstrated a lack of test understanding

and attention to procedural detail in not resolving anomalous draining

problems encountered and recognizing procedural notes that would have

identified the improper loop seal configuration. This issue was

considered a violation of TS 6.5.1.1.1 for inadequate surveillance test

procedure. This item was identified as Violation 50-261/96-12-02:

Inadequate Safety Injection Check Valve Testing.

c. Conclusions

Communication errors resulted in delays in the investigation of water

hammers in the SI cold leg injection lines. Engineering walkdowns and

investigations were considered satisfactory for identifying and

correcting damage resulting from the transient. The water hammer

resulted from the failure of operators to ensure that a loop seal was

installed for certain test apparatus used. This was identified as a

violation for failure to follow surveillance procedures.

01.4 Automatic Reactor Trip due to Feedwater Control Malfunction

a. Inspection Scope (71707, 93702 and 40500)

On October 20, 1996, while restarting from RFO-17, an automatic reactor trip occurred from 20% power. The reactor tripped following a turbine

trip on high steam generator level which resulted when the B Feedwater

Regulating Valve (FRV) started to go full open unexpectedly. The

inspectors responded to the site following the trip and observed

operator actions to stabilize the plant. The inspectors evaluated plant

and operator response to the trip, reviewed the licensee's reactor trip

report and corrective actions to address the cause of the trip.

6

b. Observations and Findings

Upon arrival in the Control Room, the inspectors reviewed control board

indications and determined that the plant had been adequately stabilized

at zero percent power and hot shutdown conditions. The inspectors

reviewed plant trip data and determined that all plant safety systems

responded as designed. The loss of both main feedwater pumps resulted

in the start of both motor driven Auxiliary Feedwater pumps as expected.

The inspectors verified that a 4-hour notification was completed as

required by 10 CFR 50.72. The inspectors reviewed initial operator

response to the trip and determined that applicable emergency procedures

were entered and followed appropriately.

The inspectors reviewed the trip data and the licensee's preliminary

trip report. The following sequence of events were reconstructed from

interviews with the operators, trip data, and preliminary trip report.

At 12:36 p.m. on October 20, the unit was placed online following

reactor startup from RFO-17. During the time the reactor was placed

online until approximately 12% power, the FRVs were controlled in manual

using the bypass valves. As the demand for feedwater was increased,

control was transferred from the bypass valves to the FRVs and their

auto-manual control station placed in automatic. Reactor power was

increased to approximately 20%. At this low power, the FRVs were in the

minimum open position which created inherent instabilities. During this

transient time period, oscillations in the B Steam Generator (SG)

level/feedwater flow occurred. The feedwater control stations for all

three SGs were in automatic for approximately 30 minutes when the

control board operator observed a rapid increase in demand for the B

FRV. The B FRV auto-manual control station was placed in manual and the

close pushbutton depressed to drive the FRV to the close position to

prevent overfeed of the B SG. Even though the closed pushbutton was

depressed the operator observed the demand to increase. After matching

indicated feed flow with steam flow, the operator stopped closing the

valve. As a result of the swell from the amount of relatively cold

incoming feedwater, level in the B steam generator reached the high

level turbine trip setpoint of 75%.

The inspectors determined that operator actions prior to the trip were

adequate. Good control board monitoring was evident by the immediate

observation of the rapid FRV demand change. However, several potential

training enhancements were considered appropriate. For example, the

oscillations in feedwater flow and level observed were not considered

excessive due to experience that the feedwater control system was

instable at low power. However, it was not clear to the inspectors that

this phenomenon was clearly understood by operations personnel with

regard to the magnitude of the oscillations expected. Additionally, the

control board operator stopped closing the B FRV momentarily after

matching feedwater flow to steam flow. This indicated a lack of

understanding regarding the magnitude of the potential swell that was to

be expected after overfeeding the generator. The inspectors did not

consider these items indicative of a major training or knowledge

deficiency.

7

A team was formed to investigate the cause of the unexpected opening of

the B FRV. As a result of this investigation, failure of the B FRV

auto-manual control station was determined to be the most likely cause.

The control station was replaced and the unit was placed back online

October 21. No further problems were experienced with the feedwater

controls during the subsequent power ascension. Details of the

licensee's investigation of the auto-manual control station are

discussed further in Section M1.2 of this report.

c. Conclusions

The inspectors determined that the plant and operator response to the

reactor trip were satisfactory. However, several minor operator

training enhancements were identified. While conclusive evidence could

not be ascertained as to the root cause of the unexpected opening of the

B FRV, failure of the B auto-manual control station was considered the

most likely cause.

01.5 Cold Weather Preparations Review

a. Inspection Scope (71707, 71714)

The inspectors reviewed the licensee's procedures and controls to

determine whether the licensee had effectively implemented a program to

protect plant equipment against extreme cold weather. This included a

review of Administrative Procedure (AP)-008, Cold Weather Preparations,

Revision 1, and Operating Procedure (OP)-925, Cold Weather Operation,

Revision 9. The inspectors performed walkdowns to verify that cold

weather preparations had been implemented and that freeze protection

equipment was operating properly. In addition, the inspectors reviewed

CRs from the previous year involving freeze protection problems to

ensure that appropriate corrective actions had been completed.

b. Observations and Findings

The inspectors determined that AP-008 adequately established the overall

plant organizational responsibilities and guidance for implementing cold

weather activities. The procedure included requirements for checking

the proper operation of freeze protection equipment such as Freeze

Protection Circuits, Steam Unit Heaters and space heaters, well in

advance of the onset of freezing weather. Between November 1 and April

1, weekly checks of Freeze Protection Circuits are conducted by

maintenance personnel to ensure continued operability. The inspectors

reviewed completed Work Requests to verify that these checks were being

completed.

The majority of the responsibility for monitoring and protecting plant

equipment from cold weather lies with operations in the implementation

of OP-925. This procedure provided instructions for preparing the plant

for cold weather and for implementing periodic precautionary measures as

the outside temperature decreases. Periodic cold weather measures are

implemented when outside temperatures below 420F are imminent. OP-925

8

is considered to be "in

effect" at that time. Further precautionary

measures are implemented as the outside temperature decreases below

350F, 220F, and 180F. Major precautionary measures conducted when OP 925 is in effect include: running idle equipment susceptible to

freezing, verifying outside doors and air louvers are closed, and

verifying proper operation of Freeze Protection Circuits. The

inspectors determined that OP-925 provided comprehensive actions for

protecting plant equipment from cold weather conditions.

Based on plant walkdowns, review of operator log entries, and completed

copies of OP-925, the inspectors verified that preparations for cold

weather in accordance with AP-008 and OP-925 had been completed and

periodic precautionary measures were being implemented as outside

temperatures decreased below 42 and 35F.

The inspectors identified one action described in OP-925 and AP-008 that

was not performed adequately. This action involved the erection of

temporary enclosures to protect risk significant areas located outside.

Areas where enclosures were to be installed included: turbine first

stage pressure transmitters, main steam pressure transmitter enclosure,

condenser hotwell level controls, turbine Electro-Hydraulic skid area,

primary air compressor area, and the screen wash and fire pumps at the

service water intake structure. All of the enclosures had been erected

except the last items for the service water intake structure. Based on

discussions with operations personnel and management, there had been a

conscious decision not to erect this enclosure due to the opinion that

it was no longer needed. Apparently, there had been freezing problems

in the past associated with the fire pumps. As a result of those

problems, AP-008 and OP-925 were revised to add the service water areas

to the enclosure erection list. Following this, the freeze protection

equipment at the service water intake was upgraded which resolved the

earlier deficiencies resulting in freezing problems. Based on

confirmation with engineering personnel that problems with the freeze

protection equipment had been corrected, the inspectors agreed with

operation's determination that the enclosure was not necessary.

However, deviating from the procedure should have been documented and/or

a procedure revision implemented. The licensee indicated that AP-008

and OP-925 would be revised to remove the action for erecting this

enclosure.

On November 11, with the outside temperature near freezing, the

inspectors conducted a walkdown of various Freeze Protection Panels to

verify that Freeze Protection Circuits were energized. The inspectors

identified that the power status lights for four circuits in the turbine

building were extinguished. The inspectors alerted operations personnel

about the problems. Work Requests were initiated to investigate and

repair the circuits.

The inspectors reviewed CRs 96-00269 and 96-00270 which were initiated

during the past winter for several plant items that froze. CR 96-00269

involved the freezing of pressure instrumentation lines for the steam

driven auxiliary feedwater pump due to lack of insulation on a small

9

section of the instrument tubing. The inspectors walked down this and

other pump instrumentation to verify that exposed tubing was properly

insulated. Freezing of the unloader valves associated with the primary

air compressor was one of the more significant items identified in CR

96-00270. Corrective actions included revising AP-008 for erecting an

enclosure around the compressors in order to block wind drafts in the

area. As previously discussed, the inspectors verified that the

procedure revision had been implemented and that the enclosure was

installed.

c. Conclusions

The inspectors concluded that the licensee had effectively established

and implemented a program to protect plant systems and equipment from

cold weather. A decision not to erect a cold weather protection

enclosure at the service water intake was justified, but was not

documented properly.

08

Miscellaneous Operational Issues (92901)

08.1 (Closed) Escalated Enforcement Item (EEI) 50-261/94-23-01, Failure to

Properly Establish Containment Integrity: This incident involved two

separate issues that were cited in separate violations as follows:

Violation A - TS Containment Integrity Violation:

A violation of TS containment integrity requirements occurred as a

result of operators failing to position six main steam line drain

containment isolation valves in their required closed position. Due to

operator confusion, procedures were signed off indicating that the

valves were closed when in fact they had been throttled for RCS

temperature control.

Contributing to the event was the lack of adequate

documentation and configuration control of main steam line drain valves

when being manipulated for reactor coolant system temperature control

during hot shutdown conditions.

The licensee responded to the violation by letter dated December 27,

1994. Corrective actions included disciplinary action for the operator

who erroneously signed off procedures indicating that the valves were

closed. In addition, expectations for documenting equipment

manipulations conducted in the field were reinforced with operations

personnel via Real Time Training, RTT-94-004, completed November 29,

1994. To ensure that plant configuration is properly maintained when

using the valves for temperature control, the licensee developed new

instructions for controlling the process. OP-405, Main and Reheat Steam

System, was revised to add these instructions. The inspectors reviewed

Revision 29 of OP-405 and determined that the new instructions were

detailed and adequately controlled RCS temperature and the configuration

of the main steam drain valves. In addition, the inspectors reviewed

OP-923, Containment Integrity, Revision 18, to ensure that the valves

were added to the containment integrity checklists. The inspectors

determined that adequate corrective actions had been implemented.

10

Violation B - Inadequate Corrective Action:

This issue involved the licensee's failure to promptly revise plant

documents after a non-validated Generic Issue Document (GID) review on

the Containment Isolation System identified that certain valves needed

to be reclassified as containment isolation valves. Included among

these valves were the main steam isolation drain valves. Plant

procedures and documents were not updated to reflect the valve status

change due to the lack of a formal process for reviewing and accepting

non-validated GIDs and Design Basis Documents (DBDs).

Licensee corrective actions included revising OP-923 to identify the

main steam isolation drain line valves as containment isolation valves.

As previously discussed, the inspectors verified that the valves were

added to the procedure. As part of the corrective actions to address

the problem with the non-validated GID review, the licensee stated that

they would implement a procedure to perform formal reviews of the non

validated DBDs and GIDs for possible impact upon other plant

documentation. The inspectors noted that only one non-validated DBD

(Main Steam System) was reviewed under a pilot evaluation. This

evaluation was completed December 5, 1995, and documented in CR 94

01294. Based on no significant findings being identified from this

pilot evaluation, the licensee decided not to perform similar

evaluations of the remaining non-validated DBDs (Feedwater, Condensate,

and Radiation Monitoring Systems) and 11 non-validated GIDs. The

inspectors determined that further NRC review was needed to determine

whether there was adequate justification for not completing these

reviews. This aspect of Violation B will remain open pending completion

of this review. This was identified as Inspector Followup Item (IFI)

50-261/96-12-03: Review Licensee Justification for not Completing Non

Validated DBD and GID Evaluations.

08.2 (Closed) Licensee Event Reports (LER) 50-261/94-20-00, Condition Outside

Design Basis Due to Mispositioned Valves:

and,

(Closed) LER 50-261/94-20-01, Technical Specification Violation Due to

Mispositioned Valves:

The above LERs documented a violation of TS containment integrity

requirements as a result of operator errors in failing to position six

main steam line drain containment isolation valves in their required

closed position. This issue was the subject of NRC Violation A for EEI

50-261/94-23-01 which was discussed in Section 08.1 above. The

licensee's corrective actions addressed in the LERs were reviewed as

part of the inspector's review of the violation. Therefore, based on

these previous reviews, these LERs were closed.

08.3 (Closed) VIO 50-261/95-12-01, Operations Failure To Follow Procedure

During OST-254: This violation contained two examples of failure to

follow procedures. On April 11. 1995, the licensee performed

Operations Surveillance Test (OST)-254, Residual Heat Removal (RHR)

System and RHR Loop Sampling System Leak Test. During the performance

of the OST, the operators detected an unidentified reactor coolant leak

of 24.8 gallons per minute (gpm). The operators terminated the test and

closed valve HCV-142 which reduced leakage to 15.6 gpm. The leakage was

terminated by closing manual isolation valve CVC-205B. The licensee

declared an Unusual Event due to reactor coolant leakage exceeding 10

gpm approximately 45 minutes after detecting the excessive leakage and

it was terminated 33 minutes later after confirmatory tests. This event

is described in more detail in Section 3.b of Inspection Report 50

261/95-12. The licensee issued CR 95-00942 to follow the issue.

On April 12, an Event Review Team (ERT) was formed to evaluate: the root

cause of the event; the surveillance procedure and determine its

adequacy; and the declaration of the Unusual Event and actions taken by

the crew. The ERT was unable to determine the exact leak path and as a

result were unable to determine a root cause. The licensee's

investigation identified that an operator was able to shut valve RHR

757D an additional 1/4 turn. OST-254 requires verification that the RHR

system is aligned in accordance with Operating Procedure (OP)-201,

Residual Heat Removal System, Revision 28, Section 6.2.2.1, which

requires that valve RHR-757D be locked shut. This was the first example

of the violation.

OST-254 is an infrequently performed evolution and a pre-job brief was

required to be given by a Management Designated Monitor (MDM) in

accordance with Plant Programs (PLP) Procedure-037,Conduct of

Infrequently Performed Tests or Evolutions. The ERT determined that the

MDM performed a pre-job brief for all individuals involved in the

evolution except the onshift operations crew. Nor did he specify in

writing the duties, authority, and responsibilities of the extra

personnel or discuss a similar licensee event which had occurred within

the previous 14 months. This was contrary to the requirements of PLP

037 and was the second example of the violation.

The ERT's investigation revealed that the test should not be performed

at power. OST-254 was required to be performed annually. They

determined that the test was originally performed during refueling

outages which were on a 12 month cycle. The licensee extended the

refueling interval to 18 months but failed to change the frequency of

the RHR leak test to coincide with refueling outages. The licensee

requested relief from the annual test. The NRC granted the requested

relief in Amendment 163 to the TS, Section 4.4.3 which permits Post

Accident RHR system leakage testing on a refueling basis rather than

annually.

The inspectors reviewed CR 95-00942 which contained the ERT report. The

ERT drew the following conclusions:

OST-254 was technically accurate but did not provide specific

guidance to address a potential reactor coolant leak.

12

The performance of the PLP-037 was deficient.

The operation of HCV-142 had been erratic and previous corrective

actions to repair the valve had not been effective.

Performance of OST-254 was not recommended.

The operating crew demonstrated conservative decision making and

performed as expected.

No human performance errors were apparent.

The inspectors concluded that the ERT report was thorough and went into

great depth in attempting to determine the cause of the event.

Performing OST-254 during refueling outages appears to have been an

adequate corrective action and this item is closed.

08.4 (Closed) VIO 50-261/95-14-03, OST-156 Valve Lineup Improperly

Established:

On May 8, 1995, the inspectors questioned the valve lineup

for OST-156, Safety Injection and Containment Spray Systems Suction

Lines Leak Test, after observing that valve SI-887, the RHR Pump

Discharge to Safety Injection (SI) and CV Spray Suction valve was

closed. The inspectors concluded that with SI-887 shut, test pressure

could not be applied between it and the SI-863A and B valves. OST-156

was revised and the surveillance was reperformed.

On May 15 while conducting a post test review, the inspectors detected

another deficiency in OST-156. The valve lineup requires that valve SI

862A, Refueling Water Storage Tank to RHR, be closed. In that

configuration, the piping between valves SI-862A and SI-862B would not

be tested. However, End Path Procedure (EPP)-9, Transfer to Cold Leg

Recirculation, permits the operators to close either SI-862A or SI-862B

while establishing the long term recirculation line-up. The inspectors

were concerned that OST-156 as conducted, did not test all portions of

the piping within the test boundaries. CR 95-01104 was issued to follow

this issue.

The licensee's investigation determined that OST-156 verified the valve

positions of the boundary valves but failed to verify the valve

positions within the test boundaries. OST-156 was a new procedure and

the procedure writer assumed that the system was in a normal lineup.

The surveillance was performed with the unit in cold shutdown during

RFO-16 and as such valve line ups were not normal.

The deficiency associated with the section of piping between valves SI

862A and SI-862B resulted from the failure of the procedure writer to

account for a single active failure of Emergency Core Cooling System

(ECCS) components. Existing cold shutdown OSTs for leakage testing of

ECCS piping and components did not account for a single active failure.

A deficiency in the procedure development process combined with a lack

of knowledge on the part of the procedure writer and the reviewers

13

resulted in the failure to test the section of piping between valves SI

862A and SI-862B.

The licensee revised OST-156 and successfully reperformed the

surveillance. Operations personnel reviewed ten OST procedures related

to ECCS leakage testing. Enhancements were made to one OST and three

were revised to assure correct system alignment inside test boundaries

and assure that single active failures are accounted for in the

determination of test boundaries. This event was incorporated into the

operator's training.

The inspectors reviewed CR 95-01104 and considered it to be adequate.

They reviewed training records and verified that training was given.

OST-155, Revision 14; OST-156, Revision 4; OST-355, Revision 10; and

OST-355, Revision 16 were reviewed and the inspectors verified that the

proposed changes included in the corrective actions of CR 95-01104 were

added to the last three OSTs. This item is closed.

08.5 (Closed) VIO 50-261/95-19-01, Operations Configuration Control Events

Concerning RHR Pump Flow Path, Valve SI-883R, Steam Driven Auxiliary

Feedwater, and The Containment ventilation Unit:

This violation was

comprised of six separate examples. Each example will be addressed

separately.

1.

Clearance Procedure Error

On May 26, 1995, the licensee experienced difficulty filling the safety

injection accumulators. Investigation determined that valve SI-883R was

shut with a clearance tag (No.20) attached which was from Local

Clearance and Test Request (LCTR 95-F0013) that had been cleared 24 days

earlier. CR 95-01352 was written to address the issue. The licensee

determined that an auxiliary operator and an independent verifier

initialed LCTR 95-F0013 that clearance tag number 20 had been removed

and the valve opened. A Senior Reactor Operator (SRO) also signed the

clearance to indicate that he had verified that all tags removed from

this clearance.

Licensee procedure Operations Management Manual (OMM)-005, Clearance and

Test Request, requires that pulled tags be delivered to the Work Control

Center (WCC) for verification. Operators are required to notify the WCC

to update the clearance before destroying any potentially contaminated

tags. The operators did not manipulate the valve as the valve had

additional tags attached to it which required the valve to be closed nor

did they remove the tag. In addition, the operators destroyed the tags

without notifying the WCC from the Containment Vessel (CV). They

departed the CV and reported to the WCC to update the master copy of the

clearance from memory. They initialed the master clearance that they

had removed the tag and opened the valve.

The licensee determined that the operators failure to follow OMM-005 was

the root cause of the event and inadequate guidance in the procedure was

14

a contributing factor. The operators were counselled and OMM-005 was

revised.

The inspectors reviewed OMM-005, Revision 33 and verified that Section

5.2.19 addresses the proper method to account for contaminated tags.

They also reviewed the completed CR 95-01352 package and considered that

the licensee addressed all the issues.

2.

Containment Fan Operated With Flow Paths Isolated

On May 26, 1995, during a tour of containment the inspectors noted an

abnormal noise emanating from containment recirculation fan, HVH-2.

They observed that both the inlet damper and inlet butterfly valve were

closed with the unit operating. The control room was notified and the

unit was shut down. CR 95-01354 was written to address the issue.

The inspectors determined that LCTR 95-FO476 was in effect at the time

of the observation. The clearance isolated the instrument air supply to

the damper activator which caused the damper to be failed. Neither the

butterfly valve or its air supply were affected by the clearance which

specified that a Clearance Information Tag (CIT) be affixed to the HVH-2

RTGB control switch. There was no CIT attached to the RTGB switch nor

did the clearance reflect that one had been affixed.

The SRO who prepared the clearance was unaware that the butterfly valve

was supplied by a separate air supply and assumed it would fail open

with the loss of air. Assuming that a flow path existed, the SRO did

not believe a CIT was required to be placed on the RTGB switch. However

one was prepared but not placed on the switch.

The licensee's review of Operations Surveillance Test (OST)-902,

Containment Fan Coolers Component Test (Monthly), and the Heating and

Air Conditioning drawing identified the butterfly valve as V12-2A.

Neither the Containment Air Handling Operating Procedure, OP-921, nor

OP-905, Instrument and Station Air System, identified V12-2A as the HVH

2 butterfly valve. The licensee concluded that it was not apparent

using controlled documents that V12-2A had an independent instrument air

header. They concluded both reviewers failed to identify the need to

place a CIT on the control switch.

The SRO was counselled and a CIT was added to the clearance. Additional

corrective actions included revising OMM-005 to add a CIT sign off and

OP-905 was revised to identify the instrument air supplies.

The inspectors reviewed OP-905, Revision 47 and noted that page 30 of

Attachment 9.1 lists separate instrument air supplies for the HVH-2

damper and V12-2A. OP-921, Revision 23, Section 8.4.2.1 identified V12

2A as the butterfly valve. OST-902, Revision 22, Section 6.5 addresses

V12-2A as the butterfly valve. The inspectors review of OMM-005,

Revision 33 did not identify any CIT signoffs. Their review of CR 95

01354 verified that the issues had been adequately addressed.

15

3.

RHR Pump Operated with No Flow

On June 3, 1995, the licensee was preparing to restart the unit

following a refueling outage. The control room operators were

performing steps to depressurize and cooldown the "A" RHR train in

accordance with GP-002, Cold Shutdown To Hot Subcritical At No Load

Tavg. This is accomplished by recirculating the isolated train through

its associated heat exchanger until it has cooled to 150 0F.

Approximately 15 minutes into the evolution the operators had not

observed the expected temperature decrease. The control room operators

increased cooling water to the heat exchanger and then checked on the

position of valve RHR-743 which is in the recirculation flow path.

Finally the control room operators had an AO check the local flow

indicator, as RHR recirculation flow is not read in the control room.

The local indicator indicated no flow and the operators secured the "A"

RHR pump.

The "A" RHR pump had run for approximately 66 minutes with

essentially no flow. The pump was declared inoperable.

The licensee

issued CR 95-01474 to address the issue.

The licensee disassembled the "A" RHR pump and found no damage to the

pump. The licensee's investigation revealed that valve RHR-743 had been

operated with a reach rod. The AO stated that he attempted to open the

valve but it did not move and assumed that it was open.

The licensee's corrective action was to change the makeup of the crew to

strengthen leadership. Operations Management Manual (OMM)-001,

Operations-Conduct of Operations, was revised to provide additional

instructions on how to verify the position of manual valves that have

reach rods. Procedure GP-002 was revised to provide a step to verify

that valve RHR-743 is open prior to isolating the RHR system and verify

recirculation flow immediately after isolating the system. Engineering

Service Request (ESR) 95-00640 was issued to remove the reach rod on

RHR-743 and was accomplished by Work Request 95-AHWE1.

The inspectors reviewed OMM-01-8, Revision 01, Section 5.4.2.2.12 and

verified that additional instructions had been provided to verify the

position of manual valves with reach rods. Their review of GP-002,

Revision 67, Section 5.4.2.1 verified that a verification step had been

provided to ensure valve RHR-743 was open prior to isolating the RHR

system and verify recirculation flow immediately after system isolation.

The inspectors review of CR 95-01474 verified that the license had

adequately addressed the issues.

4.

RHR Pump Operated With No Flow

On June 9, 1995, the control room operators were aligning the "A"

RHR

pump to place it in service in accordance with Operating Procedure (OP)

201, RHR System, following its reassembly. The "B" RHR pump was

operating in a configuration which bypassed its heat exchanger. In this

configuration the common discharge valve (HCV-758) for the heat

exchangers for both RHR heat exchangers was closed. The "A" pump was

started and the "B" pump secured. The operators observed decaying RHR

16

flow and restored the pumps to their original condition. The operators

determined that the "A"

RHR pump had been started without a flow path.

The cross connect valve (RHR-757C) was opened to provide a flow path and

the pump was successfully started. The pump was operated for

approximately two minutes with minimal flow as HCV-758 leaked by. This

was the second time in six days that the operators ran the "A" RHR pump

with inadequate flow. The inspectors concluded that OP-201 was

inadequate in that it did not align the system to provide a flow path.

The licensee's corrective actions were to revise OP-201 and again

restructure the crew.

The inspectors reviewed OP-201, Revision 28, Section 6.1.2.3 and

verified that a flow path was provided by requiring that valve RHR-757C

be open prior to starting RHR pumps. The inspectors also reviewed

nonsignificant CR 95-01510 and determined that it adequately addressed

the issue.

5.

Auxiliary Feed Water (AFW) Pump Auto Start During Steam Generator

(SG) Draindown

On June 14, 1995, both AFW pumps started and the SG blowdown isolation

valves on all three SGs shut due to a low-low level in the "B" SG. The

operators responded by defeating the AFW pump auto-start logic, stopped

the pumps, and opened the blow down isolation valves. Draining the SGs

was accomplished in accordance with Operating Procedure (OP)-406, Steam

Generator Blowdown/Wet Layup System. Section 4.1 requires four key

switches be taken to the "defeat" position prior to draining the SGs.

This action blocks the SG low and low-low level signals from the AFW

autostart circuit during draindown. The licensee issued CR 95-01566 to

track this event.

The key switches were found in the "normal" position. Investigation

revealed that the AO had initialed OP-406 as having verified that the

key switches were in the "defeat" position. The AO stated that he had

called the control room SRO to verify that the switches were in the

"defeat" position. He initialed the procedural step after receiving

confirmation from the SRO. The SRO did not visually verify that the key

switches were in the proper position but was based on the illuminated

Train A and Train B AFW Auto Initiation Defeated warning lights.

However, these lights can be illuminated without the four key switches

being in the defeated position.

The licensee disciplined the operator and all crews were counselled. In

addition, during Licensed Operator Requalification (LOR) the licensee

reinforced the OMM-001 requirements concerning individual accountability

for signoffs.

The inspectors reviewed OP-406, Revision 34, Section 4.1 and verified

the requirement to place the four key switches in "defeat" prior to

draining to draining the SGs. A review of CR 95-01566 indicated that

the licensee's actions were adequate.

17

6.

Inadequate Clearance For Work On Valve V1-8A

On April 17, 1995, the licensee attempted to perform lubrication

preventive maintenance on valve V1-8A, one of three steam valves to the

steam driven AFW pump turbine. The turbine commenced to roll when valve

V1-8A was opened. Investigation revealed that valve MS-20 which is

immediately upstream of valve V1-8A was in the open position.

The clearance (LCTR 95-00748) for the V1-8A preventative maintenance did

not address valve MS-20. OMM-005, Section 5.1.31 requires that all

valves necessary to protect personnel and equipment are properly closed

or open as necessary. The inspectors considered LCTR 95-00748 to be

inadequate in that it did not address valve MS-20 which would have

protected the turbine.

The licensee's corrective action was to add MS-20 to the LCTR and the

corrected LCTR was added as a standard to the history file in the LCTR

database for valves V1-8A, B, and C.

The inspectors reviewed OMM-005, Revision 33, Section 5.1.31 and

verified that it contained requirements to position valves and switches

to protect personnel and equipment. They also reviewed two non

significant CRs (95-00961 and 95-00962) which were written to address

this issue. Neither CR addressed the adequacy of LCTR 95-00748 or its

review. The inspectors considered that the main steam line valve (MS

20) upstream of V1-8A should have been included in the LCTR as required

by OMM-005. They consider that this deficiency should have been

identified during the LCTR review. When questioned by the inspectors

the licensee's response was that the maintenance had always been

performed during an outage and this was the first time it had been

performed on line. When asked why a steam valve was not isolated to

protect the down stream equipment, the licensee responded that they

didn't believe that the available steam was sufficient to rotate the AFW

turbine. The inspectors considered that the evaluation of CRs95-961

and 95-962 were inadequate in that they did not address the human

performance issues.

The inspectors discussed their concern with the licensee who

acknowledged that the CR review was inadequate. Discussions with the

licensee revealed that they had revisited this issue and incorporated it

into a roll up multiple personnel issues. In addition, the licensee

previously scheduled a corrective action self-assessment for

December 1996. The adequacy of CR reviews will be part of the

assessment.

The licensee issued CR 95-01816 to address all six issues encompassed in

the violation as a common problem and represented a serious management

concern. The inspectors reviewed this CR and noted that it incorporated

all the above discussion. In addition, it addressed the human

performance issue involved with item 6. above. The inspectors consider

that the issues were adequately addressed and were raised to a

sufficient level of management. The corrective actions were to be

18

adequate and were verified to have been completed by the inspectors.

This item is closed.

08.6 (Closed) Unresolved Item (URI) 50-261/95-19-02, Safety Injection Pump

Breaker Racked-In with LTOP in Service:

This issue involved a licensing

basis question regarding TS 3.3.1.3 which requires the SI pump power

supply breakers to be racked out when the RCS is below 3500F and the RCS

is not vented to containment atmosphere. On May 30, 1995, the licensee

identified that the A SI pump motor breaker was racked in for

approximately five minutes to fill the SI Accumulators without an RCS

vent path established via an open Pressurizer Power-Operated Relief

Valve.

The inspectors reviewed the basis of TSs 3.3.1.3, 3.1.2, Amendment 42 to

the TSs and associated NRC Safety Evaluation Report (SER) which

evaluated the licensee's addition of the Low Temperature Overpressure

Protection (LTOP) System, and CR 95-01355 which documented the

licensee's evaluation of this incident. The inspectors determined from

review of the chronology of the event that during the short period that

the SI pump motor was racked in and the PORVs were closed, LTOP was

armed and capable of performing its overpressure protection function.

Design basis analyses support the capability of LTOP to perform its

intended function of relieving RCS overpressurization from the

inadvertent actuation of an SI pump. Further, the NRC SER recognized

the possibility that an SI pump may be racked in under LTOP conditions

for periodic or post-maintenance operational testing. The inspectors

concluded that the licensee had not operated outside of TSs as a result

of racking in the SI pump since LTOP had been operable. Based on this

review, this URI was closed.

08.7 (Closed) URI 50-261/95-19-03, Loose Paint in Containment: This issue

involved concerns over the amount of loose paint identified by NRC

inspectors during containment walkdowns in the previous refueling outage

(RFO-16). The main areas where loose or peeling paint was identified

was on the high traffic area of the floor of the first level of

containment. Other less affected areas included the containment fan

cooling units, operating deck, and polar crane.

The inspectors reviewed CR 95-01506 which was initiated by the licensee

to address the loose paint concerns. Prior to startup the licensee

performed inspections of containment and corrected areas needing

immediate repairs. The licensee determined that the normally expected

walkdown of containment by engineering personnel to identify and correct

coating problems was not performed. To ensure walkdowns were completed

during subsequent RFOs, a preventive maintenance work request was

developed to require the inspections during every RFO.

During RFO-17, the inspectors determined that WR/JO AHWU was performed

to inspect the condition of containment coatings. The inspectors also

accompanied engineering personnel on coating inspections of containment.

The purpose of the inspections by engineering were to determine areas

needing immediate repairs to remove loose or peeling paint and areas

19

that needed to be scheduled for repair in the next RFO. Based on the

large number of items identified needing repairs, it was evident that

coating upkeep in the past had not received the appropriate level of

attention by the licensee. During containment closeout walkdowns, the

inspectors verified that repairs had been completed for areas

representing immediate concerns. While the inspectors noted that

several small floor areas of the first level of the containment and some

equipment were repainted during the outage as part of preventive coating

upgrades, progress toward improving the overall degraded conditions of

containment coatings was progressing slowly. This was inconsistent with

the good upgrades in coating repairs that the licensee had implemented

in the Auxiliary and Turbine Buildings over the past year. This issue

was considered a licensee weakness. Engineering personnel indicated

that more aggressive coating upgrades were planned for the next RFO.

Based on the licensee's implementation of a more formal process for

inspecting the condition of containment coatings and efforts to address

long term coating improvements, this item was closed.

II. Maintenance

M1

Conduct of Maintenance

M1.1 General Comments

a. Inspection Scope (61726 and 62707)

The inspectors observed all or portions of the following maintenance

related WRs/JOs and surveillances and reviewed the associated

documentation:

WR/JO 95-ALTE1, Reactor Coolant Pump A Seal Inspection, Repair,

and Reinstallation

WR/JO 96-ADIF1, Replace Mechanical Seal on Emergency Diesel

Generator (EDG) A Standby Circulating Pump

WR/JO 96-ABKG1, Replace Oil Seals on Control Shaft of EDG A

Governor

OST-163, Safety Injection Test and Emergency Diesel Generator Auto

Start on Loss of Power and Safety Injection, Revision 27

b. Observations and Findings

The inspectors observed that these activities were performed by

personnel who were experienced and knowledgeable of their assigned

tasks. Work and surveillance procedures were present at the work

location and being adhered to. Procedures provided sufficient detail

and guidance for the intended activities. Activities were properly

authorized and coordinated with operations prior to start. Test

equipment in use was calibrated, procedure prerequisites were met,

20

system restoration was completed, and surveillance acceptance criteria

were met.

c. Conclusions

The inspectors concluded that maintenance and surveillance activities

were performed satisfactorily.

M1.2 Maintenance Related Outage Activities

a. Inspection Scope (62700)

The inspectors reviewed documentation for maintenance activities

performed for the refueling outage to determine if the activities met

regulatory requirements and were performed in accordance with approved

procedures and appropriate maintenance standards. The inspectors

reviewed outage maintenance related CRs and the maintenance outage

contractor training program. The inspectors observed a post maintenance

lessons learned critique. In addition, the circumstances associated

with the October 20 reactor trip were reviewed to determine if the root

cause was identified.

b. Observations and Findings

Contractor Craft Maintenance Program - The inspectors reviewed the

maintenance program for using contractor personnel from Becon

Construction Company for work during RFO-17. The program included the

requirements for the craft certification process; the training

department and staffing plan; the Desk Top Guide; training categories;

and lessons plans. The "Desk Top Guide For Training Becon Personnel

Hired To Perform Outage And Maintenance Work At The Robinson Nuclear

Plant" described the requirements for training and the responsibilities

for all Becon personnel for RFO-17 work. Detailed training requirements

and lessons plans were specified for each category of workers. The

categories included: 1) Civil Trades, 2) Mechanical Trades including

welders, 3) Electrical Trades, and 4) Maintenance Workers. The

inspectors reviewed the training lessons and training matrix to verify

all 195 contractor personnel had received the appropriate and required

training. The program was considered very thorough and detailed.

Maintenance Condition Reports - The inspectors reviewed the "Maintenance

Condition Report Status Report" dated October 24, 1996, to evaluate the

status of outstanding CRs. In the group of CRs categorized as

"Significant," there were five open evaluations and one open corrective

action. These numbers were down from an average of 30 open evaluations

and 212 open corrective actions. In the group of "Non-Significant" CRs,

the open evaluations were up from an average of 17 to 39; and the open

corrective actions were down from an average of 83 to 31. In the group

of "Improvement" CRs, the open evaluations were down from an average of

29 to 3; and the open corrective actions were down from an average of

172 to 10. The Maintenance Department performance has significantly

improved for processing CRs. The inspector reviewed 27 CRs to determine

21

what types of problems were being reported to maintenance and if any

trends were identified. Five different CRs identified that work was

performed on live electrical circuits. The cause was personnel error in

most of the cases. However, the licensee agreed that more attention

should be placed in this area concerning work on live electrical

circuits.

CR 96-02505 involved a plant clearance for the electrical circuit for

motor operated valve MOV RHR-744B during plant modification ESR 95

00764. The clearance was taken out by the contractor to do the work,

however, plant Instrumentation and Control (I&C) personnel did not sign

on. When the work was completed, the contractor closed the clearance as

required by the modification work procedure to allow I&C to test the

valve. The clearance was removed to allow power to be restored to the

MOV for testing. At that time, testing could not be performed and the

clearance was not re-initiated. Several hours later, Operations

personnel operated the valve although testing and the modification were

not completed. No damage was done to the valve and no procedures were

violated concerning the clearance or work. However, a weakness was

identified in the "clearance" area concerning electrical power. The

licensee agreed to address this weakness and implement appropriate

corrective action.

Reactor Trip - The inspectors reviewed CR 96-02804, concerning the

investigation into the reactor trip following plant startup after RFO

17. After the trip, I&C personnel performed multiple checks to

determine what caused the auto-manual control station to fail. No

equipment failure was identified; the auto-manual control station

functioned properly. However, I&C replaced the control station with

another unit. (The reactor was placed on back on line with no other

problems). The control station was taken back to the I&C shop for

evaluation and testing. No problems had been noted. The inspectors

examined the control station and reviewed its testing. No problems were

identified. The licensee indicated that a previous problem had been

identified with the auto-manual control station for the B FRV during

RFO-17. As a result this problem, defective capacitors had been

replaced. The inspectors concluded that the root cause of the reactor

trip could not be verified since the auto-manual control station had not

failed since the trip. In addition, engineering stated that at low

power operation (below 20% power) the feedwater control system has been

known to suffer some instability in the automatic mode of operation.

The control system works well above 20% power and is stable.

Post Outage Review - The inspectors observed a post outage lessons

learned critique by the maintenance department management. The critique

was held as a self assessment to identify problems during the outage.

The inspectors reviewed 169 comments where the maintenance department

identified areas for improvement. Many of the problems identified were

to be shared with the other sites. The inspectors concluded the

maintenance department was implementing another tool for self assessment

and improvement in their work methods.

22

c. Conclusions

The inspectors concluded that the Maintenance Department had implemented

a thorough and detailed program to train and control contract personnel

during RFO-17. The Maintenance Department continues to expedite and

place emphasis on identifying and resolving problems through the use of

CRs and self assessment. The root cause of the reactor trip during re

start after RFO-17 could not be identified as equipment failure with the

feedwater control system "Auto-Manual Control Station".

M1.3

Inservice Inspection Activities Performed in Refueling Outage 17

a. Inspection Scope (73753)

In October, 1996, the licensee completed the 1st refueling outage (RFO

17) in the 2nd 40-month inspection period of the 3rd 10-year inservice

inspection (ISI) interval. There will be one more refueling outage in

the 2nd 40-month inspection period. The applicable code for ISI in the

3rd 10-year examination interval is the American Society of Mechanical

Engineers (ASME) Code,Section XI, 1986 edition with no addenda.

The following licensee documents and ISI activities were reviewed: the

third ten-year interval inspection program including relief requests and

augmented examinations, RFO-17 examination plan, ISI program procedures

and other plant interfacing procedures, completed examination

documentation, personnel and equipment certifications, Code repairs, and

the effectiveness of licensee controls for ISI.

b. Observations and Findings

The third ten-year interval program was reviewed to determine whether

the first inspection period sample of examinations met minimum Code

requirements and which relief requests had been approved by NRC and

implemented by the licensee. The review revealed that all 1st period

examinations had been performed as required and the total number of

examinations performed exceeded Code minimum requirements. Approved

relief requests were also properly implemented.

The RFO-17 examination plan was reviewed in order to select a diverse

sample of 10 completed line item examinations for a detailed review.

The review of the completed examination records revealed that the

examinations had been conducted and documented as required by the

approved ISI procedures, and personnel and equipment certifications were

in accordance with Code requirements. Instructions and documentation

for two Code repairs and the results of the eddy current examinations

for the "A" steam generator were reviewed and also found to be

satisfactory.

ISI program procedures, as well as procedures for post maintenance

testing, work control processes, engineering services, and documents

such as CRs and licensee assessments were reviewed to determine the

effectiveness of licensee controls for ISI. The inspectors identified

23

eight recent CRs which involved ISI. Six of these reports had been

written to document tardiness of ISI personnel in assigning post

maintenance test requirements (PMTRs) or unclear PMTRs. All of these

CRs were open and licensee corrective actions had not been documented.

The inspectors determined that sufficient procedural requirements were

in place for the ISI program; therefore, additional training and closer

supervision of the process should be sufficient corrective action.

The two other CRs (96-01899 & 96-02437) dealt with the potential problem

that ASME ISI isometric piping drawings may not reflect new welds added

to, or old welds deleted from, the ISI program via the work

request/modification process. Similar drawing error problems were

identified in previous NRC inspections of the licensee's ISI program

(see NRC Violation 50-261/90-24-01). The need for more accurate as

built and formalized drawings was discussed during this previous

inspection.

A licensee self-assessment performed in October 1994, on the ISI 10-year

plan for the third inspection interval, found numerous examples where

specific welds or components were identified in the plan but not on

isometric drawings. In addition, a NAS audit of the ISI program (Report

File No. R-ES-95-02) identified that during RFO-16, Modification MOD

1164 removed several supports within the ISI program scope; however, the

modification package did not identify the ISI program isometrics as

requiring revisions. Both of these assessments recommended that the ISI

isometric drawings be made controlled documents.

In mid-1995 the licensee completed corrective actions for NRC Violation

90-24-01. These actions included verification of the accuracy of

isometric drawings and formalizing the control of these drawings.

However, as discussed above CR 96-02437 reported that a potential

problem still existed because of the numerous questions that had been

raised by ISI and nondestructive examination personnel on the process

for adding and deleting welds that are required to be examined in

accordance with the Code.

Enhancements being considered by the licensee to address this continuing

problem were to ensure that procedural requirements for drawing controls

were adequate and clear, and that applicable personnel were

knowledgeable of the requirements for revising drawings. In order to

verify adequate implementation and completion of the licensee's

corrective actions, this issue was identified as an IFI 50-261/96-12-04:

Review Licensee Actions to Address Potential ISI Isometric Drawing

Problems.

c. Conclusions

ISI activities examined by the inspectors were found to be satisfactory.

The licensee had recently replaced personnel responsible for ISI.

The

inspectors found that the new personnel had assumed their duties in an

effective manner. Problems continued in the area of updating isometric

drawings after welding or component modifications.

24

M8

Miscellaneous Maintenance Issues (92902)

M8.1 (Closed) LER 50-261/94-02-01, Plant Condition Outside Design Basis Due

to MSIV Inoperability: This supplemental LER provided information

clarifying details contained in the originally submitted LER and

information provided in a Notice of Violation response from the

licensee. The corrective actions in the LER were the same as those

included in the response to NRC violation 50-261/94-16-05: Inadequate

Corrective Actions Concerning MSIV Accumulator Volume, which was

reviewed and documented in NRC Inspection Report 50-261/96-08. This LER

was closed based on the previous review of the violation and associated

corrective actions.

M8.2 (Closed) EEI 50-261/94-16-03, Inadequate Corrective Action to Potential

TS Deficiencies: This violation involved the failure to take adequate

corrective action in a timely fashion for potential TS deficiencies

identified by an internal assessment of compliance with the surveillance

requirements of TS Table 4.1-1 conducted by Enercon Services, Inc.

between 1991 and 1992.

The licensee responded to this violation by letter dated September 29,

1994. The cause of the violation was determined to be the lack of

management oversight and involvement in the Corrective Action Program.

The corrective action process was not effectively used to ensure methods

and timely schedules for addressing the deficiencies. Also, because the

Enercon assessment had been directed by the Plant Nuclear Safety

Committee (PNSC) in 1990, accountability for resolution of the results

were not clearly established.

Licensee corrective actions for the violation included enhancing the

corrective action process to provide greater management oversight and

tracking of CR schedules and the quality of evaluations. In addition,

PNSC Action Items were to be formally assigned to the responsible

organization unit and tracked to completion. The inspectors reviewed

Plant Program (PLP) procedure PLP-026, Revision 18, which implemented

the licensee's enhancements. Major changes noted included: 1)

clarification of responsibilities and criteria for completing CR

reportability reviews, trending, and evaluations, 2) another level of

CRs was created for lesser significant "improvement" conditions in order

to foster the identification of problems, and, 3) management was

assigned responsibility for trending CRs. Based on review of the

current version of PLP-026 (Revision 24), the inspectors determined that

these, as well as other enhancements made since the earlier revision,

were still in effect. The inspectors reviewed PLP-001, Plant Nuclear

Safety Committee, Revision 16, and determined that provisions for

assigning and tracking PNSC Action Items were established. The

inspectors reviewed the electronic CR database and determined that PNSC

Action Items were correctly being entered into the licensee's CR

database. The inspectors concluded that the licensee's corrective

actions for this violation had been adequately implemented.

25

M8.3 (Closed) LER 50-261/94-01-00, -01, Failure to Test Instrumentation

Channels Per Technical Specifications: These LERs dealt with

inadequacies in surveillance test procedures that resulted in portions

of the 4 Kilo-Volt Undervoltage trip circuitry and Overpressure

Protection System not being properly tested in accordance with TSs. The

tests for the applicable TS Surveillance Requirements were revised to

include the untested portion of the equipment in question and were later

performed with satisfactory results. These procedural discrepancies

were previously identified in 1992 during an independent assessment of

the TS surveillance program but were not promptly resolved. The root

cause for the failure to promptly resolve the issues was the result of

program weaknesses in the licensee's corrective action process.

The inspectors previously reviewed the technical aspects associated with

the LERs in NRC Inspection Report 50-261/94-16. The LER supplement (94

01-01) was submitted primarily to provide corrective actions to address

weaknesses in the licensee's corrective action program. The corrective

actions described in the LER were the same as those in the licensee's

response to violation EEI 50-261/94-16-03: Inadequate Corrective Action

to Potential TS Deficiencies, discussed separately in this report.

These LERs are closed based on the review of the violation and

associated corrective actions.

M8.4 (Closed) VIO 50-261/95-12-03, Maintenance Planner Fails To Properly

Develop Breaker PMTR:

On April 6, 1995, the licensee removed circuit

breaker HVH-2 (52-20C) from service to perform preventative maintenance

(PMs).

Material deficiencies were observed during the PMs and a

replacement circuit breaker was installed. The inspectors observed the

PMTR for the replacement circuit breaker and questioned its adequacy.

The PMTR consisted of the operators closing the breaker from the RTGB.

The inspectors did not consider that the PMTR met the requirements of

Maintenance Management Manual Procedure (MMM)-003, Appendix A, Post

Maintenance Testing. This procedure requires that post maintenance

testing demonstrate that the circuit breaker responds to all demand

signals. It also requires that breakers on the E-1 and E-2 busses which

respond to an autostart signal from a safeguards actuation have a time

test as part of its PMTR. The licensee opened the replacement circuit

breaker from the RTGB and performed a time test in response to the

inspectors' concerns. CR 95-00927 was written to address the issue.

Investigation revealed that Work Request (WR) 95-AEPZ1 was issued to

change the contacts on circuit breaker 52/20C. The planner was

requested to revise the WR to perform PM-402, Inspection nd Testing of

Circuit Breakers for 480 Volt Bus E-1, on the spare circuit breaker as a

contingency. The planner was asked to revise WR 95-AEPZ1 to include

instructions to install the spare circuit breaker if the repairs to the

installed circuit breaker were unsuccessful.

Post maintenance testing

was determined from WR history and a review of PM-402 and CM-305,

Westinghouse "DB" Type Circuit Breaker Maintenance. Past practice had

not been to verify post maintenance testing in MMM-003, Appendix "A".

The licensee determined that MMM-003, Appendix "A" had been revised on

June 16, 1994. The planning organization was unaware of the change as

26

they were not included in the review process for this procedure.

Administration Procedure (AP)-022, Document Change Procedure, Attachment

9.2 Review assignment criteria Section 29 for Work Control did not list

MMM-003 as required to be reviewed by Work Control.

The revision to MMM-003 which added the circuit breaker timing test

requirement did not include any acceptance criteria. The licensee

determined that the requirement to perform the timing test was included

in a note in the Circuit Breaker Maintenance Section and was not listed

in the test requirements. In addition, it was not added to PM-402 or

PM-163 which was for bus E-2.

Engineering Service Request (ESR) 95-00357 was initiated to provide

guidance on acceptable closing time for HVH-2 to meet the requirements

of MMM-003. Engineering determined that in this application that

circuit breaker closing within 0.5 seconds would not impact the

capability of the motors fed from buses E-1 or E-2 to start when

required.

The licensee's corrective actions included successfully performing the

timing test and the planner was issued and required to use OMM-003,

Appendix "A". Procedure AP-022 was revised to require Work Control

review of changes to MMM-003 which was also revised to clearly state

when circuit breaker testing was required and list acceptance criteria.

PM-402 and PM-163 were revised to include circuit breaker timing testing

as part of in-process testing.

The inspectors reviewed WR 95-AEPZ1 and noted that the request for

testing was vague,"perform the appropriate testing." Procedure CM-305,

Revision 6 was reviewed and the inspectors did not locate any references

to circuit breaker timing tests. The inspectors verified that Procedure

AP-022, Revision 25, Section 9.2.29.4 contains the requirement that Work

control review all changes to MMM-003. They also verified that

Procedures PM-163, Revision 2, Section 7.24 and Attachment 10.8.5,

Section 7.24.7 and PM-402, Revision 13, Section 7.24 and Attachment

10.8., Section 7.24.7 specify that a closing time test is required for

circuit breakers 52/24B (HVH-4) and 52/20C respectively, the acceptance

criteria is also listed. The inspectors verified that MMM-003, Appendix

"A", Revision 18, Attachment 7.4.1, Section 1.1.5 contains requirements

to perform a timing test for safety related DB-50 circuit breakers and

specifies acceptance criteria. The inspectors noted that the acceptance

criteria specified in MMM-003 is more conservative than that listed in

ESR 95-00357 (200 vs 500 msecs). The inspectors questioned the licensee

about the difference in circuit breaker closing times. The 500 msecs

closing time was obtained from CP&L calculation RNP-E-8.002, Attachment

0, Overall Load Block Tolerance. ESR 95-00360 was issued to evaluate

the closing time requirements of all circuit breakers on the E-1 and E-2

busses. The Revision 2 response to the ESR provided vendor design data

for DB circuit breaker closing times. Westinghouse Letter RCS/ESE(95)1

145 stated that the DB circuit breakers were designed to close

electrically within 200 msecs. Engineering recommended that MMM-003,

Appendix A be revised to reflect the design closing times. The

27

inspectors verified the licensee's corrective actions and this item is

closed.

M8.5 (Closed) VIO 50-261/95-14-01, Inadequate Control Of Contractor Services:

Three examples of inadequate licensee control of contractor services

were identified between May 3 and May 8,1995. Each example will be

addressed separately.

1.

Collision of Polar Crane and Manipulator Crane

On May 3, 1995, the containment polar crane collided with the refueling

manipulator crane. A contracted refueling technician had moved the

manipulator crane in the path of the polar crane. Subsequently, a

contracted crane operator moved the polar crane without verifying the

position of the manipulator crane. The polar crane collided with a

cross piece on the manipulator crane's monorail. The top of the

manipulator crane was bent approximately two to three feet and resulted

in the failure of three welds.

Investigation of the event revealed that the refueling technician had

not received CP&L crane training nor had the polar crane operator been

trained on Maintenance Instruction (MI)-510, Polar Crane General

Instructions. A copy of MI-510 was not in the crane's cab as required

nor had the operator been given a proficiency examination. In addition,

the licensee did not have a formal coordination process to use when

multiple cranes were in use.

The licensee determined that the event

was caused by a series of personnel errors and an over reliance on an

inadequate Polar Crane protective System.

The licensee formed an Event Review Team (ERT) to determine the cause of

this event. CR 95-01069 was issued to track this event. Engineering

Service Request (ESR) 95-00427 was issued to evaluate the structural

damage to the manipulator crane. Engineering determined that the

structural deformation was within acceptable limits. The damaged welds

were repaired by Work Request (WR) 95-AFNS1. The inspectors reviewed

the ESR and WR and verified that the recommended work had ben completed.

2.

Polar Crane Auxiliary Hook Strikes Steam Generator Cubicle

On May 4, 1995, the polar crane auxiliary hook struck the concrete

cubicle surrounding the "C" steam generator. The crane operator had

been operating the crane from the refueling floor. He had lowered the

auxiliary hook for a planned lift but lift priorities changed. He moved

the polar crane to position it for the next lift but failed to adjust

the height of the auxiliary hook. The crane operator commenced to

reposition the polar crane on his own initiative without direction from

the signalman. The polar crane's auxiliary hook hit the north side of

the concrete cubicle around the "C" steam generator. The crane operator

was the same that was involved in the previous event. He was reassigned

to other duties.

28

The licensee expanded the scope of the ERT's charter to include this

event which was also addressed in CR 95-01069. ESR 95-00436 was issued

to provide an engineering inspection of the "C" steam generator cubicle.

The inspection revealed that there was no structural damage and only

scuff marks were observed on the concrete.

The inspectors reviewed CR 95-01069 which included the ERT's findings

and recommendations. The ERT concluded that the polar crane operator

had worked 28 hours3.240741e-4 days <br />0.00778 hours <br />4.62963e-5 weeks <br />1.0654e-5 months <br /> in the previous 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Technical specification

work limitations were imposed on the craft. The design limitations for

the polar crane interlock system were evaluated and recommendations were

made. The preferred solution was to enhance training. The ERT

concluded that the contractors training was inadequate. They also

concluded that CP&L Procedure MMM-009, Operation, Testing and Inspection

of Cranes and Material Handling Equipment, was inadequate in that it was

weak in specifying training and testing requirements for non CP&L

personnel.

The inspectors concluded that the ERT report was thorough

and in-depth. MMM-009, Revision 18 was reviewed and the inspectors

verified that the recommended procedural changes had been incorporated.

The changes included training and testing requirements.

3.

Inadequate Control of Contract Refueling Personnel.

On May 8, 1995, during the performance the initial steps of the insert

shuffle in the Spent Fuel Pit (SFP) in accordance with Fuel Movement

Procedure (FMP)-019, Fuel and Insert Shuffle, 19 steps were initialed as

complete when no thimble plugs had been removed. The refueling crew,

after discovering the problem, verified that no thimble plugs had been

moved. The crew consisted of a qualified contractor refueling, two CP&L

refueling technicians, and a SFP reactor operator (RO).

They

determined that the tool being used was 90 degrees out of align. The

tool was realigned and additional lighting was acquired. The crew

initiated repeating steps commencing with the first step of the shuffle.

The crew failed to notify Management of their problems. CR 95-01132 was

initiated to follow this issue.

The licensee's investigation revealed that the event was caused by

inattention to detail and crew members making assumptions as to actions

by the other crew members. The contractor supervisor failed to verify

the alignment of the thimble plug tool as required by FHP-001, fuel

Handling Tools Operation and which clearly delineates the correct

orientation. The area of the SFP in which they were working was not

well lit and the water was quite turbulent. The SFP RO was able to

verify SFP grid locations but unable to view the assemblies because of

water conditions. The refueling technicians on the refueling bridge had

difficulty viewing the assemblies. The crew discovered their error when

work moved to a better lighted area of the SFP. Crew members assumed

that someone else had notified the control room and/or management. The

event was not discovered until the next day during a review of the logs.

The licensee's corrective actions were to relieve the contractor

supervisor, stand down meetings with the refueling contractor and

29

operations, and provide additional crew members as well as contractor

oversight. In addition, under water TV cameras and improved SFP

lighting were provided. The inspectors reviewed CR 95-01132 and

consider it to address all the issues.

In addition, the licensee initiated Significant CR 95012632 to address

issues relating to procedure adherence and personnel errors committed by

their labor contractor (Becon) which were identified during refueling

outage (RFO)-16 and documented in CRs. The licensee determined that the

personnel provided by the contractor frequently lacked experience in the

nuclear industry and were not adequately trained. The licensee surveyed

the contractor craft and the results of the survey supported their

findings. The licensee concluded that its contract was inadequate and

renegotiated a new contract to address the identified issues. The

inspectors consider that the licensee addressed this issue in sufficient

depth and this item is closed.

III. Engineering

El

Conduct of Engineering

E1.1 Generic Letter (GL) 89-10 Program Implementation

a. Inspection Scope (TI 2515/109)

The licensee's completion of implementation of GL 89-10 "Safety-Related

Motor-Operational Valve Testing and Surveillance" was assessed by the

NRC inspectors.

The licensee had committed to implement GL 89-10 in

letters dated December 27, 1989 and June 6, 1991, and had subsequently

notified the NRC that implementation was complete in a letter dated July

28, 1994. In a letter dated December 28, 1995, the licensee submitted

information to support closure of the NRC review of GL 89-10

implementation for Robinson.

The inspectors conducted the assessment through a review of the

licensee's GL 89-10 implementing documentation and through interviews

with licensee personnel.

The inspectors first reviewed the documents

that prescribed the program and methods used to implement GL 89-10 and

the documents that summarized information from related licensee testing

and evaluations. These documents included the licensee's December 28,

1995 letter (referred to above); Technical Management Manual Procedure

TMM-032, "Motor Operated Valve Program," Rev. 8, dated June 10, 1996;

Standard Procedure EGR-NGGC-0203, "Motor-Operated Valve Performance

Predication, Actuator Settings, and Diagnostic Test Data

Reconciliation," Rev. 0, dated May 31, 1996; and an informal tabulation

of information from the testing performed on all motor operated valves

(MOVs) in the GL 89-10 program. Following review of the preceding

documents, the inspectors performed the following reviews of

computations, tests, and evaluations which the licensee used to

determine and verify the settings and capabilities of their MOVs:

30

The inspectors selected and reviewed calculations and test data

for a sample of rising stem (gate and globe) and butterfly valves.

The sample included valves whose settings were based on all

methods which the licensee used to demonstrate design-basis

capability in accordance with GL 89-10. The valves were as

follows:

AFW-V2-14A Steam Drive Auxiliary Feed Water Pump Discharge Valve

to Steam Generator "A"

FP-248

Electrical Penetration Sprinkler System Upstream

Isolation Valve

MS-V1-8B

Steam Admission Valve to Steam Drive Auxiliary Feed

Water Turbine

RHR-744A

Residual Heat Removal Loop to Reactor Coolant System

Cold Leg

SI-870A

Boron Injection Tank Outlet Isolation Valve

SI-880D

Containment Spray Pump B Discharge Isolation Valve

V6-16B

Service Water to Turbine Building Isolation Valve

The scope of valves originally in the licensee's GL 89-10 program

had been reviewed previously by the NRC and would be considered

acceptable based on current NRC positions. The inspectors

reviewed the subsequent changes which the licensee had made to the

scope of valves included in the program to assure that any

deletions were adequately justified. The inspectors identified

the changes by comparing the valves in the original program (TMM

032, Rev. 0) with those in the current program (TMM-032, Rev. 8).

The inspectors then verified satisfactory bases for all valves

deleted from the scope of the program. The verifications were

accomplished through a review of justifications for excluding the

valves described in the licensee's "Mechanical Analysis and

Calculations" (e.g., RNP-M/MECH-1401 for valve CC-716) and through

a review of functional information described in the licensee's

design basis document (DBD/R87038) and Updated Final Safety

Analysis Report (UFSAR).

The inspectors reviewed the licensee's documented evaluation of

potential pressure locking in response to GL 95-07. For three

groups of valves potentially susceptible to pressure locking, the

inspectors assessed the actions which the licensee had or was

taking to ensure that pressure locking would not prevent the

valves from performing their design-basis functions. These valves

were:

RC-535 and 536

PORV Block Valves

(3-inch Westinghouse flexible-wedge gate valves)

31

RHR-744A and B

RHR Cold Leg Injection Valves

(10-inch Velan flexible-wedge gate valves)

SI-870A and B

Boron Injection Tank Outlet Isolation Valves

(3-inch Anchor/Darling double-disk gate valves)

b. Observations and Findings

1.

Program Scope Changes

The MOV program currently contained 58 valves. Thirty-two valves had

been removed from the scope of the program previously reviewed by the

NRC. The inspectors found the bases for the removal of these 32 valves

was satisfactory. They had been removed either because they did not

have a safety function or because they were excluded by Supplement 7 to

GL 89-10.

2.

MOV Sizing and Switch Settings

Robinson's thrust calculations typically utilized standard industry

equations to determine setting requirements for rising stem gate and

globe valves. Mean seat diameter was used to calculate valve seat area.

Valve factors were obtained from in-plant test results or from other

industry sources, as specified by the licensee's methodology. A stem

friction coefficient of 0.20 was typically used for determination of

actuator output thrust capability. The licensee applied a 20% bias

margin that was intended to cover load sensitive behavior. Thrust

requirements were adjusted to account for diagnostic equipment

uncertainty (except as noted in 6 below) and torque switch

repeatability.

3.

Valve Factor (VF) and Grouping

The licensee had not divided their MOVs into groups of similar valves

and used the test data from the dynamically tested MOVs within a group

to establish settings for the non-dynamically tested MOVs. They had

attempted to dynamically test as many MOVs as possible but had not been

able to perform satisfactory dynamic tests on all of the MOVs in their

GL 89-10 program. The settings of gate valves that were not

satisfactorily dynamically tested were generally calculated assuming a

generic VF of 0.50. When justification for their use of this VF

assumption was requested by the inspectors, licensee personnel stated

that it was based on "industry experience."

However, the licensee

indicated they could not provide a documented analysis of applicable

industry test data to support this assumption. The inspectors noted

that utility and industry test programs have found VFs in excess of 0.50

for some valves under certain fluid conditions.

The following are examples of valves for which the licensee did not have

satisfactory dynamic test measurements for VF determination and the

licensee assumed a 0.50 VF without any written justification:

32

Velan 3" Flex-Wedge Gate Valve: CC-735 and FCV-626

Crane 16" Solid-Wedge Gate Valve:

CC-749A and CC-749B

Crane Aloyco 3" Double Disc Gate Valve: CVC-381

Copes Vulcan 14" Double Disc Gate Valve:

RHR-750 and RHR-751

Anchor Darling 14" Double Disc Gate Valve: SI-860A, SI-860B,

S1861A, SI-861B, SI-862A, and SI-862B

Anchor Darling 16" Double Disc Gate Valve: SI-864A and SI-864B

Anchor Darling 3" Double Disc Gate Valve: SI-869

Anchor Darling 6" Double Disc Gate Valve: SI-880A and SI-880C.

The licensee's failure to justify the VF assumptions used in MOV setting

calculations was considered to represent inadequate design control and

is identified-as Example 1.a of Violation 50-261/96-12-05:

Unjustified

Design Assumptions and Incorrect Stem Rejection Load.

Valve factor is used to relate the valve stem force required to overcome

disc/seat friction to the differential pressure pushing the disc against

the valve seat. During review of licensee procedure EGR-NGGC-0203, the

inspectors noted that Section 6.6 (Diagnostic Test Data Reconciliation),

provided the option to use either of two different equations for

calculating open VF from the licensee's stem thrust measurements.

Measured stem thrust includes both the thrust force required to overcome

the disc/seat friction load and the force required to overcome other

loads, such as stem rejection and packing loads. The licensee's

equations for calculating VF provided for separate determination and

removal of the loads not associated with disc/seat friction, one

correctly and the other incorrectly. The first equation which EGR-NGGC

0203 specified for determining VF subtracted out the packing load

obtained in static testing and added the stem rejection load calculated

based on line pressure and stem area. This equation resulted in correct

open VF determinations. It was the only equation contained in the older

dynamic test evaluations that were evaluated by the inspectors. In the

second equation stem rejection and packing loads were accounted for by

simply subtracting out the running load measured during the opening

dynamic test (when the valve is unseated and partially open) from the

initial opening thrust required to overcome dynamic effects. This

equation was incorrect, because it did not properly account for the stem

rejection being greater at the beginning of an open stroke (when the

line pressure forcing the stem out is higher) than when the running load

was measured. Help due to stem rejection is less during the running

portion of the open stroke in a dynamic test (where the second equation

measures running loads) because the pressure pushing against the stem is

lower than when the valve initially starts to open. Therefore, the

equation did not properly account for the helping force provided by stem

rejection at the point of the open stroke where the VF was measured.

33

This resulted in a nonconservative prediction of open VF. The

inspectors noted during review of dynamic test evaluation packages for

MS-V1-8B, AFW-V2-14A, FP-248, and SI-880D, that the opening VF had been

calculated incorrectly, as the running load was used without any

correction for the reduced pressure at the point where running load was

measured. The inspectors noted that the effect of this error would

typically be small and that the existing practice could be corrected by

adding an additional term to account for the difference in stem

rejection between the start of the open stroke and the running portion

of the open stroke. The licensee's incorrect calculation of opening VFs

was considered to represent inadequate design control and is identified

as Example 2 of Violation 50-261/96-12-05: Unjustified Design

Assumptions and Incorrect Stem Rejection Load.

During the review of the close dynamic test for AFW-V2-14A (Steam Drive

Auxiliary Feed Water Pump Discharge Valve to Steam Generator "A"), the

inspectors noted that licensee personnel selected an apparently

nonconservative point on the close force trace to represent the force

needed to achieve flow isolation (VOTES mark C10).

This is the force

point that would be used to calculate an apparent VF. Valve AFW-V2-14A

is a 4" Anchor Darling double disc gate valve which uses an internal

wedging action to seal off flow. The inspectors noted that the selected

point might be nonconservative because the force trace continued to

increase significantly prior to reaching hard seat contact (VOTES mark

C11). The inspectors also noted that the licensee had not used any

other diagnostic sensor (e.g., accelerometer) to confirm their choice

for flow isolation. Robinson personnel indicated that this valve did

not have a leakage criteria requirement and that total flow isolation

was not necessary. The inspectors considered the licensee's argument to

be adequate for the purpose of an operability assessment.

4.

Load Sensitive Behavior

In determining settings for rising-stem MOVs that were dynamically

tested, the licensee used the measured load sensitive behavior values.

The licensee's MOV switch setting methodology specified a margin of 20%

to account for the effects of load sensitive behavior for MOVs that were

not dynamically tested. When the justification for this margin was

requested by the inspectors, licensee personnel stated that it was based

on testing performed at the Brunswick plant. However, no justification

was provided to show that the Brunswick data was applicable to Robinson.

Given the sensitivity of load sensitive behavior to differences in 1)

load profiles during a valve stroke under dynamic conditions, 2)

potential differences in thread surface conditions, 3) types of stem

lubricants used, and 4) methods and frequency of lubricant application,

the inspectors did not consider the use of results from a different

facility to be adequate when load sensitive behavior data was available

from the testing performed on Robinson's MOVs. Licensee personnel

offered no explanation for not analyzing the load sensitive behavior

performance at Robinson. Supplement 6 to GL 89-10 indicated that, for

valves that could not be satisfactorily dynamically tested, the use of

34

plant-specific data (i.

e., Robinson data) was considered more reliable

than use of data from other plants.

Licensee personnel performed an initial review of the available load

sensitive behavior data obtained from their dynamic test program and

determined an average load sensitive behavior value of approximately

12%. However, using an average value was not acceptable due to the high

probability that a 12% margin would be nonconservative for many MOVs in

Robinson's generic letter program. The inspectors performed an

independent evaluation of Robinson's load sensitive behavior data and

determined that a mean plus 2 standard deviations of the available data

was equal to approximately 27%. This indicated that Robinson's 20%

margin might be nonconservative. The licensee's failure to justify the

load sensitive behavior assumed in their setting calculations was

considered to represent inadequate design control and is identified as

Example 1.b of Violation 50-261/96-12-05: Unjustified Design

Assumptions and Incorrect Stem Rejection Load.

5.

Stem Friction Coefficient

The licensee's thrust calculations typically assumed the use of a 0.20

stem friction coefficient (SFC) in the open direction and 0.15 for the

close direction. The licensee had statically measured the SFCs of their

valves at torque switch trip and, when a measured value exceeded the

assumed value, the measured value was used. The licensee had not

monitored SFC performance during dynamic tests and had no analysis to

justify the adequacy of the values which they had assumed in their

calculations of design-basis capabilities.

The inspectors noted that

this was inadequate, as industry testing has shown that stem friction

coefficients measured under design-basis conditions are typically higher

than values measured at torque switch trip during a static test. This

is of particular concern for the open direction because the licensee did

not include any margin for load sensitive behavior in the open

direction. The licensee's failure to justify the SFC assumed in their

setting calculations was considered to represent inadequate design

control and is identified as Example 1.c of Violation 50-261/96-12-05:

Unjustified Design Assumptions and Incorrect Stem Rejection Load.

6.

Design-Basis Capability

The inspectors found that the dynamic force traces for valves MS-V1-8B,

SI-870A, and FP-248, were similar in response characteristics to those

obtained for these valves under static (no flow) test conditions. This

indicated that the tests might not have achieved the intended

differential pressures and flows. This was not recognized in the

licensee calculations which evaluated the results of the tests. The

inspectors reviewed the test conditions described in the licensee's

completed test procedures for these valves and found further indications

that the intended differential pressures and flows had not been

achieved. Their findings for each valve were as follows:

35

MS-V1-8B: This is the steam admission valve to the steam driven

auxiliary feedwater pump turbine. The licensee's test lineup for

this valve provided both upstream and downstream pressure

instrumentation. However, the downstream pressure was obtained by

recording the data manually from a pressure instrument and could

not be correlated precisely with valve position. There was no

instrument available to measure steam flow. The auxiliary

feedwater pump was aligned for recirculation back to the

condensate storage tank and was not pumping water into the steam

generators (as would happen under accident scenarios). This

recirculation lineup would be expected to provide only about 10%

of the volumetric flow rate that would be achieved when

discharging to the steam generators. Therefore, the steam flow

through the turbine and through MS-V1-8B would be small, as

compared to design-basis conditions. The actual differential

pressure at the time of valve closure may have been much less than

recorded, due to the turbine's condenser vacuum quickly drawing

the downstream piping pressure so that the pressure instrument

indicated zero psi when test personnel recorded the test

differential pressure data.

SI-870A This is the boron injection tank outlet isolation valve.

The inspectors' review of the system piping diagram and the

completed dynamic test procedure found that a downstream valve was

positioned to throttle flow to approximately 300 gpm during the

test. This throttle valve was located between SI-870A and the

downstream pressure gauge. Therefore, the recorded downstream

pressure did not reflect the true pressure at SI-870A at the point

of flow isolation. (The licensee's evaluation for this valve was

documented in Calculation RNP-M/MECH-1473, Rev. 0)

FP-248 This is the electrical penetration sprinkler system

upstream isolation valve. The dynamic test lineup for this valve

involved discharging into a temporary fire hose connected to a

flush station. Flow was controlled by downstream manual valve FP

294. Step 7.2.14 of Special Procedure SP-1042, "Fire Protection

System MOV Full Differential Pressure Stroke Test," cracked open

FP-294 to initiate flow in the system. No measurement of system

flow conditions were recorded during the test. Given the effect

on flow rate that a downstream throttle valve which is cracked

open would have, the inspectors believed this to be the cause of

the dynamic force trace appearing similar to a static force trace.

Flow through this valve would be much higher when the system is

performing its safety function to supply the containment

electrical penetration sprinkler system. Therefore, this was not

considered to be a near design-basis test and the intended test

conditions were apparently not achieved.

Based on the above, the inspectors found that the licensee's evaluations

of the results of the subject MOV tests were inadequate, as they failed

to recognize that the dynamic test results were not consistent with the

perceived test conditions. Further, the original test procedures did

36

not assure that the intended design-basis test conditions were achieved

during the tests. This was considered indicative of inadequate test

control and is identified as Example 1 of Violation 50-261/96-12-06:

Inadequate Evaluation of Test Results.

During the review of Robinson's diagnostic test evaluations, the

inspectors noted that the licensee had not made adjustments to open

thrust measurements to account for the measurement uncertainty

identified by the licensee's VOTES diagnostic equipment vendor, Liberty

Technologies, in Customer Service Bulletin 31 (issued November 19,

1993). At Robinson, open thrust requirements were compared to the

actuator's capability under degraded voltage conditions without

considering this diagnostic equipment uncertainty associated with open

VOTES measurements. This uncertainty applies when tension measurements

are significantly outside the test sensor's calibration range. The

licensee's failure to consider this uncertainty in evaluating their test

results was considered a further example of the inadequate test control

referred to in the previous paragraph and identified as Example 2 of

Violation 50-261/96-12-06:

Inadequate Evaluation of Test Results.

During the review of the dynamic test package for MS-V1-8B, the

inspectors noted that the open force trace for the dynamic test

performed on November 13, 1993, exhibited a large sustained increase of

approximately 10,000 lbf, starting approximately 3 seconds into the open

stroke, and continuing throughout the remaining open stroke. Section 7

of Calculation No. RNP-M/MECH-1406, "Evaluation of Differential Pressure

Test Data of MS-V1-8B, Steam Admission Valve to SDAFW Turbine," did note

the anomaly but did not resolve the issue. Licensee personnel stated

that no condition report was initiated to resolve this anomaly or to

correct any potential problems related to the VOTES sensor location.

The licensee's failure to evaluate the significance of this anomaly was

considered indicative of inadequate test control.

This was identified

as Example 3 of Violation 50-261/96-12-06:

Inadequate Evaluation of

Test Results.

7.

Pressure Locking

For the three groups of valves reviewed by the inspectors, the licensee

used calculations to demonstrate that the valves could overcome pressure

locking and perform their design functions. A double-disk area formula

was used in predicting the thrust required to overcome pressure locking

and GL 89-10 program calculations were used to predict the thrust

available from the motor actuators. The inspectors found that the

licensee had not validated its calculation method for predicting the

  • thrust required to overcome pressure locking as part of its long-term

actions in response to GL 95-07. Further, the licensee relied on

pressure measurement in the injection line between the check valves and

RHR-744A/B to demonstrate that check valve leakage was currently low,

resulting in an MOV bonnet pressure much lower than reactor coolant

system pressure. However, the licensee did not justify that the valve

bonnet pressure for RHR-744A/B would remain low over time.

37

Although referencing its general thrust prediction equation, the

licensee had not documented the specific calculations for predicting the

thrust required to overcome pressure locking for its valves. The

inspectors performed independent calculations and did not identify any

immediate concerns regarding operability of SI-870A/B, RC-535/536 and

RHR-744A/B. However, the licensee had not adequately justified its

analytical method to predict the capability of MOVs to overcome pressure

locking as a long-term response consistent with the recommendations of

GL 95-07. In response to this issue, in its letter dated February 13,

1996, the licensee committed to modify SI-870A/B to prevent pressure

locking during refueling outage RO-18 in 1998. At the time of the

inspection, the licensee was relying on the actuator capability of RC

535/536 and RHR-744 A/B to overcome pressure locking and did not have

any plans to modify these valves. However, the licensee stated that

they would address concerns regarding the long term capabilities of

RC-535/536 and RHR-744 A/B as part of a response to an NRC request,

dated July 3, 1996, for additional information. The licensee plans to

submit this response by November 22, 1996. The NRC staff is continuing

its evaluation of these MOVs and others within the scope of GL 95-07 as

part of its review of the licensee's response to potential pressure

locking and thermal binding.

The adequacy of the licensee's long term actions to preclude pressure

locking of the above valves was identified as IFI 50-261/96-12-07:

Actions to Preclude Pressure Locking.

8.

Butterfly Valves

The licensee had only three butterfly valves in its GL 89-10 program.

These were identical 16-inch Allis-Chalmers butterfly valves. The

safety function of each was to close and closure was controlled by

torque switch settings with the valves torquing closed into stopnuts.

The valves normally operated at a differential pressure exceeding that

experienced in a design-basis accident, demonstrating the adequacy of

the licensee's torque settings. However, the inspectors observed that

torque closure of these valves into the actuator stopnuts was contrary

to the recommendations of the actuator vendor and they considered this a

weakness. The inspectors reviewed the licensee's maintenance history (6

years) for one of the valves and the results of a recent inspection of

such valves for evidence of damage from torque seating. There was no

evidence that the torque seating had resulted in damage. The inspectors

did not consider the licensee to have sufficiently justified its long

term reliance on torque closure of butterfly valves into their stopnuts.

The NRC will review this issue further during a future inspection of

Robinson's implementation of GL 89-10.

c. Conclusions

The licensee had not satisfactorily implemented GL 89-10. Important

assumptions used in setting and capability calculations had not been

justified and calculations used in determining valve opening setting

requirements contained errors. These were indicative of inadequate

38

design control and were cited as Violation 50-261/96-12-05, Unjustified

Design Assumptions and Incorrect Stem Rejection Load. Further, the

licensee's test data had not been adequately evaluated, as valve opening

thrust measurement error had not been adequately assessed, the licensee

failed to recognize that test conditions were not as intended, and

anomalous data was not resolved. These were indicative of inadequate

test control and were identified as Violation 50-261/96-12-06,

Inadequate Evaluation of Test Results.

E7

Quality Assurance in Engineering Activities

E7.1 Special UFSAR Review

A recent discovery of a licensee operating their facility in a manner

contrary to the Updated Final Safety Analysis Report (UFSAR) description

highlighted the need for a special focused review that compares plant

practices, procedures and/or parameters to the UFSAR descriptions.

While performing the inspection discussed in this report, the inspectors

reviewed selected portions of the UFSAR that related to the areas

inspected. The inspectors verified that for the select portions of the

UFSAR reviewed, the UFSAR wording was consistent with the observed plant

practices, procedures and/or parameters.

E8

Miscellaneous Engineering Issues (37551 and 92903)

E8.1

(Closed) LER 50-261/93-20-00, Technical Specification Violation Due to

Exceeding F-Delta-H Hot Channel Factor:

On December 3, 1993, the

licensee determined that while operating at 30% reactor power prior to

November 17, 1993, the Technical Specification hot channel factor F

Delta-H limit was exceeded. The reason for exceeding the thermal limit

was determined to be the result of six misloaded fuel assemblies placed

in the core during the previous reload. The corrective actions included

in the LER were similar as those included in the licensee's response to

Violation 50-261/93-34-02: QA Failure. The inspectors reviewed the

licensee's corrective actions associated with this violation previously

in NRC Inspection Report 50-261/95-21. This LER was closed based on

previous review of the violation and associated corrective actions.

E8.2

(Closed) IFI 50-261/94-06-05, Adequacy of Periodic Verification Methods:

Recently the NRC has issued GL 96-05 on periodic verification of design

basis capability of safety-related motor-operated valves. Further NRC

assessment of the licensee's periodic verification will be addressed in

regard to this generic letter.

E8.3 (Closed) IFI 50-261/94-06-07, Mispositioning: This issue dealt with a

GL 89-10 recommendation to ensure that valves could return to their

safety positions, if inadvertently mispositioned. Supplement 7 to GL 89-10 removed this recommendation.

E8.4 (Closed) VIO 50-261/94-27-07, Failure to Adequately Control

Calorimetric: This violation of 10 CFR 50, Appendix B, Criterion II,

Quality Assurance Program, involved inadequate controls associated with

39

the licensee's power range calorimetric program. Deficiencies

identified included use of uncalibrated instrumentation, failure to

control the plant condition prerequisites under which the program

results were valid, failure to specify a timing for acquiring manually

input data, lack of verification of automatically input data, and

inconsistent controls on the instruments used in the program. These

problems did not result in exceeding any licensed thermal power level.

The licensee responded to this violation by letter dated January 30,

1995. The licensee determined that lack of proper management oversight

for control of the calorimetric program was the cause of this violation.

Corrective actions included verifying that all inputs to the program

were using calibrated instrumentation. Some instrumentation had to be

replaced with new calibrated equipment. The licensee revised

maintenance procedures to require a review of the impact of

instrumentation used in the program that are found out of calibration.

This change was documented in Revision 13 of Maintenance Management

Manual (MMM) procedure MMM-002, Maintenance Procedure Preparation. In

addition, the inspectors noted that MMM-006, Calibration Program,

Revision 17, also contained formal provisions ensuring that the impact

of out-of-tolerance instruments are evaluated by a Technical Reviewer

with assistance from the system engineer. Corrective actions to address

control of plant conditions during performance of the calorimetric were

accomplished by a revision of OST-010, Power Range Calorimetric During

Power Operation Daily. The inspectors reviewed Revision 22 of OST-010

and determined that adequate controls were implemented to ensure that

stable plant conditions are required during performance of the

calorimetric. The inspectors concluded that the licensee's corrective

actions had been adequately implemented.

E8.5 Degraded ECCS Sump Screen Design Issues

On September 11, after having shutdown for RFO-17, engineering walkdowns

of the containment ECCS sump identified openings that were in excess of

the sump screen mesh size of 7/32 inch. An assessment of the impact of

the openings was initiated. On September 30, after identifying actual

debris in the sump piping that was greater than the screen mesh size,

the licensee concluded that the ECCS sump screens were not consistent

with their design. The openings could have allowed debris greater than

the sump screen design to enter the sump and related ECCS recirculation

flowpath. Debris larger than 3/8 inch could have resulted in potential

clogging of the Containment Spray (CS) System nozzles. An LER

describing the impact of the degraded sump condition was issued on

October 30. During RFO-17, the licensee performed repairs to the sump

screens to ensure that there were no openings greater than screen design

requirements. The inspectors inspected the sump repairs and determined

that the licensee had adequately completed these repairs and returned

the screens to an acceptable condition. The licensee planned to replace

the screens in their entirety during the next refueling outage.

The licensee determined from a "qualitative" assessment of the affects

of the degraded screen condition that the likelihood of adverse impact

40

on the operation of ECCS equipment was small.

Part of the information

used to support this position was a statement in the original FSAR that

"one-fifth of CS nozzles in one train of the CS system, complete outage

of the other train, and disability of all four containment fan coolers

could be tolerated at the time of recirculation without losing the

ability to transfer residual heat from the containment atmosphere."

This statement was no longer in the current UFSAR. The inspectors

requested that the licensee provide additional information to support

this and other qualitative conclusions. The inspectors concluded that

further review of this information was necessary in order to evaluate

the full impact of the degraded ECCS sump condition on the operation of

the ECCS equipment. This was identified as URI 50-261/96-12-08:

Resolution of ECCS Sump Design Issues.

The licensee determined that the cause of the degraded screen condition

was the lack of adequate control over previous alterations to the sump.

Alterations were previously made to accommodate pipe restraints and

piping that was routed through the screens, as well as the result of

general screen repairs that had been made as a result of identified

discrepancies. While procedures existed to inspect the condition of the

sump, sensitivity to the size of openings had not been previously

recognized.

During review of this issue, the licensee became aware of another design

problem with the ECCS sumps that had previously been identified and

evaluated in 1988. This previous design problem involved identification

that the original calculated containment vessel flood level of 3.2 feet

above the containment floor elevation was in error. New calculations

determined the actual level to be 6.2 feet above the floor elevation.

The licensee's previous evaluation of the impact from this difference

was mainly related to the Environmental Qualification of equipment not

previously known to be in the flood zone. The evaluation was performed

under Engineering Evaluation No.88-132. However, this previous

evaluation failed to consider the impact of the higher flood level on

the operation of the ECCS sump screens during sump long term

recirculation conditions. In particular, UFSAR Section 6.3.2.2.2,

Recirculation Phase, states as one of the screen filtration functions,

that the sump baffle wall excludes floating debris from entering the RHR

suction. However, as a result of the higher flood level, the top of

this baffle wall would be below the water level allowing debris which

reached the baffle to float into the sump.

The licensee conducted an evaluation of the impact of the higher flood

level on the design of the ECCS sump filtration function. The results

of this evaluation concluded that the ECCS sump would continue to

perform its design function with the flood level above the height of the

baffle wall.

This was based on the determination that no additional

floating debris would be deposited on the screens as long as the upper

portion of the screen was above the flood water level.

At the end of

the report period, the inspectors were continuing to review the impact

of the higher flood level on the ECCS sump screen design. This issue

41

was identified as part of URI 50-261/96-12-08: Resolution of ECCS Sump

Design Issues.

IV. Plant Support

R1

Radiological Protection and Chemistry Controls

R1.1 Radiological Controls

a. Inspection Scope (83750)

The inspectors evaluated the adequacy of licensee radiological controls

with emphasis on external occupational exposure controls during outage

operations. Areas inspected included locked high and very high

radiation area controls, radiation area postings, radiation work permit

controls, and labeling of rad material.

The inspectors made frequent

tours of the radiologically controlled area (RCA), observed compliance

of licensee personnel with radiation protection procedures for high dose

outage work evolutions, and conducted interviews with licensee personnel

with respect to knowledge of radiological controls and working

conditions.

b. Observations and Findings

The inspectors verified observed controls for external and internal

exposures met applicable regulatory requirements and were designed to

maintain exposures ALARA. The inspectors reviewed several Radiation

Work Permits (RWPs) utilized to control ongoing outage work within the

RCA, including high dose activities within containment, and noted that

the controls observed were appropriate for the described tasks and

radiological conditions.

During plant walkdowns within the RCA, the inspectors conducted

interviews at random with radiation workers inside containment. The

interviews were conducted with workers of various disciplines in order

to determine the level of understanding of RWP requirements from a

representative cross-section of plant workers. The workers interviewed

were verified to have signed onto an RWP, were wearing electronic

dosimetry appropriate to their work activities within the RCA in

accordance with plant procedures, and were performing specific work

activities on several different RWPs. The workers interviewed signified

that they had in fact read and understood the conditions and

requirements of the RWP being logged in on in accordance with

procedures. The questions asked included the RWP number of the RWP

signed in on, electronic dosimetry dose limits, and general radiological

working conditions for the areas worked in. For the workers

interviewed, a good knowledge of RWP requirements and a good knowledge

of radiological working conditions, generally, was demonstrated.

The inspectors reviewed total whole body exposures for all plant

radiation workers and determined that all whole body exposures assigned

since the beginning of the SALP cycle (6/18/95) through the end of this

42

inspection were within 10 CFR Part 20 limits. A review of licensee

personnel exposure records indicated the following maximum individual

exposures at the plant during this period: Total Effective Dose

Equivalent (TEDE): 1390 mrem; Committed Effective Dose Equivalent

(CEDE): 32 mrem; and Shallow Dose Equivalent (SDE) whole body: 3633

mrem. A 54 mrem CEDE internal dose occurred on 5/13/95 which was prior

to the current SALP cycle. The inspectors determined the licensee had

adequately monitored and tracked individual occupational radiation

exposures in accordance with 10 CFR Part 20 requirements and that all

doses reported were at a small percentage of applicable regulatory

limits.

The inspectors reviewed and discussed with licensee representatives the

program for controlling access to high radiation areas (HRAs), locked

high radiation areas (LHRAs), and very high radiation areas (VHRAs).

These areas were inspected during tours for proper posting and access

controls.

No HRAs, LHRAs, or VHRAs were identified where required

postings were needed but not posted. Areas controlled as LHRAs were

inspected and found locked in accordance with licensee procedures. The

licensee had completed a posting upgrade with respect to radiation areas

to achieve full conformance with the regulatory intent of 10 CFR

20.1902. The inspectors noted significantly upgraded and improved

posting practices throughout the plant.

Key controls for entry into locked and very high radiation areas were

evaluated against the requirements of the licensee's administrative

control procedure and determined to be controlled in accordance with the

procedure. During a tour of the Spent Fuel Pool the inspectors observed

no items hanging from the side of the pool and good radiological

controls in place in this area overall. A large sample of survey

instruments and respirators available for issuance were inspected

and all determined to have current calibration dates. Radiation workers

during peak traffic periods were observed exiting the RCA fully in

accordance with procedures for frisking out of the RCA to include

properly clearing small articles with the small articles monitor.

Pre-job RWP work planning and ALARA briefings for observed ongoing

outage work evolutions inside containment, including the tasks of

reactor head stud tensioning and decon of a transfer canal hot spot,

were found to be conducted in an indepth, effective manner. During

tours of the plant, the inspectors observed Health Physics (HP)

technicians performing radiation and contamination surveys in accordance

with procedures. Also, during inspection of the tool issuance rooms,

good controls for slightly contaminated tools inside the RCA, and for

clean tools outside the RCA, were noted.

On October 8, 1996, the inspectors observed a worker exiting the RCA

whose electronic dosimeter (ED) was in the pause mode. Upon further

review it was determined that the ED had not been turned on at the time

the worker had entered the RCA. A check of the Radiation Information

Monitoring System (RIMS) disclosed that the worker was not logged in on

an RWP, nor was the worker wearing a TLD. A reconstruction of the

worker's activities while in the RCA for a relatively short period

43

indicated the likelihood of the worker having received significant dose

was minimal and the overall safety significance of the incident was low

from this standpoint. However, contrary to the external whole body

monitoring requirements of licensee procedure NGGM-PM-0002, Radiation

Control and Protection Manual, Revision 26, Paragraph 6.13.1, dated

August 30, 1996, all individuals who enter the primary Radiation Control

Area shall be monitored for external whole body radiation exposure using

an appropriate individual monitoring device. Although most workers

entering the plant RCA are not likely to receive an occupational dose

exceeding ten percent of annual regulatory limits, the licensee has

chosen to require monitoring on a more conservative basis by procedure.

This non-compliance with licensee procedures was not isolated in that on

September 29, 1996, another radiation worker entered the RCA and was

inside a high radiation area briefly without electronic dosimetry as

required by RWP. Significant condition reports were issued for both

incidents which required root cause analysis and commitment to

corrective actions although the corrective actions were not complete at

the conclusion of the inspection.

The incident on October 8, 1996, as documented in Condition Report 96

02636, is a violation of paragraph 6.13.1, External Whole Body

Monitoring, of licensee procedure NGGM-PM-0002, Radiation Control and

Protection Manual. This licensee identified and corrected violation is

being treated as a Non-Cited Violation (NCV), consistent with Section

VII.B.1 of the NRC Enforcement Policy. This issue was documented as NCV

50-261/96-12-09: Failure to Comply with Radiation Monitoring Procedure.

c. Conclusions

The radiological controls program was being effectively implemented and

good occupational exposure controls during outage conditions was

demonstrated. Good radiological control performance was apparent in the

occupational exposure activities observed by the inspectors. An upgrade

in radiation area posting throughout the facility was evident.

Continued emphasis on procedural adherence to radiation control

procedures remains a challenge. One NCV was identified for failure of a

radiation worker to wear an appropriate monitoring device within the RCA

as required by procedure.

R1.2 Contamination Controls

a. Inspection Scope (83750)

The inspectors evaluated the licensee's increasing numbers of personnel

contamination events (PCEs) and the adequacy of corrective actions and

related followup. Also evaluated was the adequacy of contamination

surveys required to evaluate the extent of the radiation hazard to

workers and the adequacy of contaminated area controls.

44

b. Observations and Findings

During the ongoing outage through October 10, 1996, the site had

incurred 146 PCEs which substantially exceeded the initial outage goal,

of 100. The licensee has also exceeded the annual PCE goal of 130 with

172 incurred through the same period. Although the number of PCEs

incurred is not a significant radiological safety concern considered

alone, high numbers of PCEs do reflect on the quality and effectiveness

of an organization's contamination control program as well as the

adherence of radiation workers to fundamental contamination control

practices. Furthermore, those PCEs which stem from hot or discrete

particles are the most likely to cause a significant skin exposure which

may challenge regulatory limits. The licensee applies a rigorous PCE

definition (100 ccpm) but the numbers of PCEs being experienced are high

for a single unit PWR. During the current outage, the licensee

experienced high numbers early in the outage (i.e., between September

11-14) with another spike toward the end (October 7-9). Of particular

concern to the inspectors was that over half of the PCEs were

attributable to discrete particle activity and several PCEs (>10

percent) were found in "clean" areas. In order to independently

determine the effectiveness of the licensee's contamination control

program, the inspectors, with RC Technician support, selected

approximately 70 swipe locations in likely locations within the RCA for

smearable contamination. Although all smears were within licensee

limits, and most were negligible, two approached the licensee's dpm

limit. The inspectors also selectively reviewed the higher assigned

dose PCE reports and noted no assessment or procedural errors. Where a

skin dose assessment was required by licensee procedure based on the

level of skin activity in corrected counts per minute, the inspectors

were able to verify the assessment had been performed as per procedure

with conservative dose assessment methodology utilized.

The licensee, in response to the high number of PCEs being experienced,

initiated a significant condition report evaluation which will require a

root cause and corrective action plan for the negative PCE trend. The

licensee will evaluate the effectiveness of the laundry vendor in

decontaminating protective clothing, the limited vacuuming time (partly

on outage critical path) used during the outage which may have

contributed to higher contamination conditions at the start of the

outage, effect of heat stress concerns, close contact in undress areas,

reduced use of double sets of protective clothing this outage, worker

practices, and effectiveness of worker training programs.

c. Conclusions

The licensee continues to experience a high level of personnel

contamination events which represent a continuing challenge in the

licensee's radiological control program although no deficiencies were

identified with respect to adequacy of followup on individual personnel

contaminations or controls for contaminated areas. Although PCEs remain

relatively high and a challenge area in radiological controls overall,

licensee actions with respect to improving personnel contamination

45

controls were determined to be appropriate with no regulatory concerns

noted.

R8 Miscellaneous Radiation Protection and Chemistry Issues

R8.1 ALARA Program Effectiveness

a. Inspection Scope (83750)

Part 20 to the Code of Federal Regulations requires that licensees use,

to the extent practicable, procedures and engineering controls based

upon sound radiation protection principles to achieve occupational doses

and doses to members of the public that are as low as reasonably

achievable. The ALARA area was evaluated to determine whether the

licensee was establishing and tracking performance against ALARA goals,

whether continuing ALARA initiatives are ongoing to reduce dose, and to

evaluate the overall effectiveness of the ALARA program.

b. Observations and Findings

Through October 8, 1996, the licensee projected a total site dose goal

of 187 person rem but actually achieved a reduced 129 person rem

(approximately 30 percent less than goal). The licensee is now on track

to achieve less than their annual dose goal of 211 rem based on good

dose performance during the refueling outage (which represents 75

percent of annual planned dose) and due to very low dose accrual during

power operations the first nine months of 1996. The inspectors observed

pre-job ALARA briefings and evaluated ALARA pre-work packages for select

high dose outage activities. During the pre-job ALARA briefings, the

inspectors noted thorough and detailed pre-job planning for specific

high dose activities and observed good task analysis as well as a

questioning attitude as to potential dose saving opportunities for the

planned activities. The inspectors reviewed with the licensee current

and planned ALARA initiatives. During 1996, the licensee has undertaken

several dose reduction initiatives including an expanded use of video

monitoring technology, expanded application of long term shielding,

additional advanced radiation worker training, additional ALARA training

for engineering personnel, evaluation of preventative maintenance

frequencies for possible reduction, and evaluation of chemical

decontamination for the RHR system. The licensee has established an

aggressive exposure goal for 1996 which, if achieved, will represent a

very low exposure at the site for a refueling outage year and approach

the favorable dose performance of 1991 (193 rem).

The licensee did not

undertake a full system chemical decon during the outage but did realize

good curie removal results from a primary system hydrogen peroxide wash.

The licensee indicated an intent to evaluate the feasibility of

conducting a full system chemical decon as an ALARA initiative during

future outages. Overall, the inspectors determined that collective dose

is being effectively controlled and reduced.

46

c. Conclusions

Overall, based on an evaluation of ALARA initiatives and ALARA work

plans for high dose work evolutions, the inspectors concluded that the

licensee's ALARA program was effectively controlling collective site

dose and that the total site dose was on a favorable reducing trend.

S8

Miscellaneous Security Issues (92904)

S8.1 (Closed) VIO 50-261/95-12-05, Failure To Control Safeguards Information:

On April 5, 1995, the inspectors observed unsecured Safeguards

information (SGI) stored on a bookshelf in the shift supervisor's

office, which was adjacent to the active control room. The shift

supervisor's office was often unoccupied which resulted in Safeguards

information not being under the control of an authorized individual.

The inspector notified the site Security manager who had the SGI moved

to the control room. CR 95-00900 was written to address the issue.

Control room modifications were in progress at the time of the event and

the licensee had moved the SGI to the shift supervisor's office for

better control. The licensee's corrective action included placing

control of SGI under the Security organization and relocating the

control room SGI to the Secondary Access Station (SAS). The SGI program

was reviewed by the licensee and improvements were initiated where

required. The inspectors reviewed CR 95-00900 and found it to be

adequate. No other control of SGI in the control room issues have been

identified and this item is closed. However, other control of SGI

issues have been subsequently identified and are documented in

Inspection Reports 50-261/96-02 and 50-261/96-03. Escalated Enforcement

Item (EEI) 50-261/96-03-02 was issued for control of SGI violations.

F1

Control of Fire Protection Activities

F1.1 Observation of Plant Areas

a. Inspections Scope (64704)

A general plant walkdown inspection was performed by the inspectors to

verify: acceptable housekeeping; compliance with the plant's fire

prevention procedures such as "Hot Work" permits and transient

combustibles; operability of the fire detection and suppression systems;

emergency lighting; and, installation and operability of fire barriers,

fire stop and penetration seals (fire doors, dampers, electrical

penetration seals, etc.).

b. Observations and Findings

Within the areas observed, the inspectors determined that the general

housekeeping was satisfactory, considering that the unit had just

restarted from a refueling outage and maintenance and repair activities

had been ongoing. During maintenance activities the inspectors observed

that fire protection equipment was readily accessible. The majority of

47

the wood used during plant activities was treated to make it fire

retardant. Fire retardant plastic sheeting and film materials were also

being used. Lubricants and oils were properly stored in approved safety

containers.

No discrepancies were noted with the fire pumps, outside fire hose

houses, fire main valves or headers. Carbon dioxide (CO

2) storage

cylinders were at the proper fill pressures and fire extinguishers had

been inspected and had a current inspection date. Controls were being

maintained for transient combustibles and areas containing potential

lubrication oil and diesel fuel leaks, such as the diesel generator

rooms, were being controlled.

c. Conclusions

Good compliance with plant fire prevention procedures was observed. The

general housekeeping and control of combustibles was satisfactory. The

control of combustible and flammable materials was effective.

F1.2 Fire Reports

a. Inspection Scope (64704)

The inspectors reviewed the plant fire incident reports for 1996 in

order to assess maintenance related or material condition problems with

plant systems and equipment that initiated fire events. The inspectors

verified that plant fire protection requirements were met in accordance

with Fire Protection Procedure FP-002, Fire Report, Revision 5, when

fire related events occurred.

b. Observations and Findings

The fire incident reports indicated that there were eight incidents of

fires in 1996, of which three required fire brigade response. There had

been only one minor fire event involving cutting or welding activities

associated with the refueling outage, and the remainder were minor fires

involving electrical failures. Only two of the eight fires had occurred

within the plant protected area.

c.

Conclusions

Good compliance with plant fire prevention procedures has resulted in a

low incident of fire within the plant protected area.

F2

Status of Fire Protection Facilities and Equipment

F2.1 General Comments

a. Inspection Scope (64704)

The inspectors reviewed fire protection Equipment Inoperable Records

(EIRs) from January 1996 to the present to assess maintenance-related or

48

material condition problems with fire protection systems and equipment.

The inspectors verified that plant fire protection requirements were met

in accordance with OMM-007, Equipment Inoperable Record, Revision 36,

when the equipment was declared out of service. Fire protection water

supply systems, the dedicated safe-shutdown system, and plant fire

barriers were inspected to determine the material conditions of the

plant's fire protection systems, equipment and features.

b. Observations and Findings

The EIRs indicated that the number of fire protection impairments for

repairs recorded for the ten month period was relatively small and

adequately monitored to limit their duration. The inspectors determined

that most of the plant repair impairments involved problems with fire

doors, however, in all cases, the repair impairments had been restored

to service within 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />. A small backlog of open work orders

remained for scheduled completion.

The inspectors toured the following plant fire zones/areas and inspected

the fire protection features to determine if the systems were operable

and properly maintained:

Unit 2 electric and diesel driven fire pumps (Fire Zone 29),

Pyrocrete fire barrier walls for Charging Pump Room (Fire Zone 4),

Appendix R eight-hour emergency light units for the dedicated

safe-shutdown system (Fire Zone 25),

Sprinklers for Auxiliary Building Hallway (Fire Zone 7), and,

1-Hour Fire Wrap for Component Cooling Water Pumps (Fire Zone 5).

The inspectors noted that all of the fire protection systems inspected

were operational and appeared to be well maintained, however, minor

configuration discrepancies were noted with the pyrocrete fire barriers

walls. The barrier contained several exposed bolts and a cable junction

box connected to the barrier but not coated with fire resistant

material. The licensee was unable to locate Generic Letter 86-10

engineering evaluation documentation in the Fire Hazards Analysis (FHA)

nor the Safe Shutdown Analysis (SSA) that justify these deviations from

tested fire barrier configuration. The inspectors determined that no

operability concern existed based on review of available fire test

results of the pyrocrete fire barrier material. The licensee indicated

that this item would be reevaluated under corrective actions to CR 96

00733. This CR identified similar licensee identified issues where the

FHA/SSA did not accurately reflect the current plant configuration.

This issue was considered a fire barrier configuration weakness.

49

c. Conclusions

When fire protection systems are found degraded or inoperable, a high

priority is assigned to promptly return these systems to service. The

number of fire protection impairments for repairs recorded for the last

ten month period was relatively small and adequately monitored to limit

their duration. With one exception noted above, all of the fire

protection features inspected were operational and appeared to be well

maintained. Most of the plant repair impairments involved problems with

fire doors, however, in all cases the repair impairments had been

restored to service in a timely manner.

F3

Fire Protection Procedures and Documentation

F3.1 General Comments

a. Inspection Scope (64704)

The following Plant Operating Manual and Fire Protection Procedures were

reviewed for compliance with NRC requirements and guidelines:

OMM-002, Fire Protection Manual, Revision 25,

OMM-009, Locked Valve List, Revision 57,

FP-001, Fire Emergency, Revision 29,

FP-002, Fire Report, Revision 5,

FP-009, Surveillance of Fire Protection Activities, Revision 6,

FP-012, Fire Protection Systems Minimum Equipment and Compensatory

Actions, Revision 4.

Plant tours were performed to determine procedure compliance.

b. Observations and Findings

The above procedures established the guidance used to implement the fire

protection program at Robinson and included the requirements for the

control of combustibles, ignition sources and fire brigade organization

and training. The specific procedures were satisfactory and met NRC

requirements and guidelines.

The operability, surveillance and test requirements for the fire

protection systems and features had been removed from the TSs and

incorporated into the site fire protection administrative procedures.

In general, these requirements met the requirements for the fire

protection features which were formerly in the TSs. However, there was

no overall plant administrative procedure that documented the Fire

Protection Program positions, responsibilities, authorities, or the Safe

Shutdown Analysis and 10 CFR 50, Appendix R exemptions. Engineering

50

responsibilities for fire protection related activities were not well

defined in the fire protection procedures. A recent 1996 Nuclear

Assessment Section (NAS) audit of the fire protection program identified

several similar weaknesses with fire protection procedures.

c. Conclusions

Implementation of the fire protection and prevention procedures was

satisfactory. However, there was no overall plant administrative

procedure that documented the Fire Protection Program positions,

responsibilities, authorities, or the Safe Shutdown Analysis and 10 CFR

50, Appendix R exemptions. Engineering responsibilities for fire

protection related activities were not well defined. A recent 1996

Nuclear Assessment Section (NAS) audit of the fire protection program

identified several similar weaknesses with fire protection procedures.

This was identified as a program weakness.

F5

Fire Protection Staff Training and Qualification

F5.1 Fire Brigade Drill

a. Inspection Scope (64704)

The inspectors witnessed a fire brigade drill for compliance with the

facility's fire protection program and the NRC guidelines and

requirements.

b. Observations and Findings

On October 22, 1996, the inspectors witnessed a fire brigade drill with

the off-site fire department located in Hartsville, South Carolina. The

drill involved a simulated fuel oil fire on the Unit 1 fossil plant

boiler. The Unit 2 fire brigade team leader and five fire brigade

members responded in full fire fighting turnout gear. Personnel from

Unit 1 operations, security and off-site emergency medical services also

responded to the drill.

The actions by the fire brigade and support

personnel were satisfactory except that it appeared that there was some

confusion between the fire brigade team leader and the off-site

department related to a fire fighting strategy.

The plant fire team

leader committed to a defensive strategy, electing to let the fire on

the boiler burn while protecting the surrounding plant structures.

The

off-site Fire Department was expecting an offensive strategy, which led

to some confusion and time delay in setting up fire attack hose lines

and the off-site aerial fire truck. A drill critique was conducted with

the fire brigade members following the drill. The drill controllers

addressed several weaknesses and "lessons learned" which had been

identified during the drill.

These included additional training planned

for fire brigade team leaders, use of additional fire drill props to

improve fire drill realism, and improved access of the fire equipment

cart through security vehicle barriers.

These corrective actions were

scheduled to be completed by January 1997.

51

c. Conclusions

The performance by the fire brigade during the drill was marginally

satisfactory and did not appear to be up to the standards previously

demonstrated by the plant fire brigade. The fire brigade drill

performance was not as intense as it could have been and guidance to the

off-site fire department personnel was minimal.

F7

Quality Assurance in Fire Protection Activities

F7.1 General Comments

a. Inspection Scope (64704)

The following reports and responses for audits performed by the licensee

Quality Assurance (QA) organization, NAS, and licensee insurer (Nuclear

Mutual Limited (NML)) were reviewed:

NAS Assessment R-FP-95-01, Fire Protection, April 11, 1995,

NAS Assessment R-FP-96-01, Fire Protection, March 15, 1996,

NML Audit 9501, Property Loss Prevention Report, March 15, 1995,

NML Audit 9502, Property Loss Prevention Report, November 14,

1995.

b. Observations and Findings

The audits were thorough and identified a number of issues, enhancements

and observations for resolution to improve the facility's fire

protection program. The inspectors reviewed the audit issues and

recommended enhancements from each QA report and determined that timely,

appropriate corrective action had been taken on all of the identified

issues.

The 1996 NAS audit identified four issues and three weaknesses. Two of

the identified weaknesses, R-FP-96-01-W1 and -W2 were related to plant

Fire Protection Program procedural problems. These open items were: (1)

the plant does not have a stand alone Fire Protection Plan that

encompasses the overall Fire Protection Program positions,

responsibilities, authorities, equipment, and Safe Shutdown Analysis,

(2)

the engineering responsibilities are not well defined in any

document, and, (3)

the administrative and technical content of Fire

Protection Procedures does not meet management standards (CRs 96-00733

and 96-00735). As previously discussed in Section F3.1, the inspectors

identified similar examples of these types of FHA/SSA discrepancies.

Licensee corrective actions for the NAS weaknesses were scheduled for

implementation by February 28, 1997. The effectiveness of the

licensee's corrective actions associated with these Fire Protection

Program issues will be reviewed during future NRC inspections.

52

c. Conclusions

The audits and assessments of the facility's fire protection program

were thorough and appropriate corrective actions were being taken to

resolve identified issues. During this inspection period, similar

examples of FHA/SSA discrepancies were identified. The effectiveness of

the licensee's corrective actions associated with these Fire Protection

Program issues will be reviewed during future NRC inspections.

F8

Miscellaneous Fire Protection Issues

F8.1 Fire Protection Related NRC Information Notices (64704)

The inspectors reviewed the licensee's evaluation for the following NRC

Information Notices (IN):

IN 92-18, Potential Loss of Shutdown Capacity During a Control

Room Fire,

IN 94-28, Potential Problems with Fire Barrier Penetration Seals,

and,

IN 95-36, Emergency Lighting.

The licensee's evaluations for these INs were appropriate and the

required corrective actions had been completed.

V. Management Meetings

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee

management at the conclusion of the inspection on November 20, 1996. Interim

exits were conducted on October 11, 25, November 1 and 8, 1996. The licensee

acknowledged the findings presented.

The inspectors asked the licensee whether any materials examined during the

inspection should be considered proprietary. No proprietary information was

identified.

53

PARTIAL LIST OF PERSONS CONTACTED

Licensee

H. Chernoff, Supervisor, Licensing/Regulatory Programs

J. Clements, Manager, Site Support Services

D. Crook, Senior Specialist, Licensing/Regulatory Compliance

C. Hinnant, Vice President, Robinson Nuclear Plant

J. Keenan, Director, Site Operations

B. Meyer, Manager, Operations

G. Miller, Manager, Robinson Engineering Support Services

R. Moore, Manager, Outages/Scheduling

J. Moyer, Manager, Maintenance

D. Stoddard, Supervisor, Operating Experience Assessment

R. Warden, Manager, Nuclear Assessment Section

T. Wilkerson, Manager, Environmental Control

D. Young, General Manager, Robinson Plant

NRC

J. Zeiler, Acting Senior Resident Inspector

P. Byron, Resident Inspector, Surry

54

INSPECTION PROCEDURES USED

IP 37551:

Onsite Engineering

IP 40500:

Evaluation of Licensee Self-Assessment Capability

IP 61726:

Surveillance Observations

IP 62700:

Maintenance Implementation

IP 62707:

Maintenance Observation

IP 64704:

Fire Protection Program

IP 71707:

Plant Operations

IP 71714:

Cold Weather Preparations

IP 71750:

Plant Support Activities

IP 73753:

Inservice Inspections

IP 83750:

Occupational Radiation Exposure

IP 92901:

Followup - Operations

IP 92902:

Followup - Maintenance

IP 92903:

Followup - Engineering

IP 92904:

Followup - Plant Support

IP 93702:

Prompt Onsite Response to Events at Operating Power Reactor

T12515/109: Inspection Requirements for Generic Letter 89-10, Safety-Related

Motor-Operated Valve Testing and Surveillance

ITEMS OPENED, CLOSED, AND DISCUSSED

.

Opened

lype

Item Number

Status

Description and Reference

NCV

50-261/96-12-01

Open

Failure to Maintain Containment Integrity

During Refueling (Section 01.2)

VIO

50-261/96-12-02

Open

Inadequate Safety Injection Check Valve

Testing (Section 01.3)

IFI

50-261/96-12-03

Open

Review Licensee Justification for not

Completing Non-Validated DBD and GID

Evaluations (Section 08.1)

IFI

50-261/96-12-04

Open

Review Licensee Actions to Address

Potential ISI Isometric Drawing Problems

(Section M1.3)

VIO

50-261/96-12-05

Open

Unjustified Design Assumptions and

Incorrect Stem Rejection Load (Sections

E1.1.b.3, 4, and 5)

VIO

50-261/96-12-06

Open

Inadequate Evaluation of Test Results

(Section E1.1.b.6)

IFI

50-261/96-12-07

Open

Actions to Preclude Pressure Locking

(Section E1.1.b.7)

55

URI

50-261/96-12-08

Open

Resolution of ECCS Sump Design Issues

(Section E8.5)

NCV

50-261/96-12-09

Open

Failure to Comply with Radiation

Monitoring Procedures (Section R1.1)

Closed

Iype

Item Number

Status

Description and Reference

EEI

50-261/94-23-01

Closed

Failure to Properly Establish Containment

Integrity (Section 08.1)

LER

50-261/94-20-00

Closed

Condition Outside Design Basis Due to

Mispositioned Valves (Section 08.2)

LER

50-261/94-20-01

Closed

Technical Specification Violation Due to

Mispositioned Valves (Section 08.2)

VIO

50-261/95-12-01

Closed

Operations Failure To Follow Procedure

During OST-254 (Section 08.3)

VIO

50-261/95-14-03

Closed

OST-156 Valve Lineup Improperly

Established (Section 08.4)

VIO

50-261/95-19-01

Closed

Operations Configuration Control Events

Concerning RHR Pump Flow Path, Valve SI

883R, Steam Driven Auxiliary Feedwater,

and The Containment ventilation Unit

(Section 08.5)

URI

50-261/95-19-02

Closed

Safety Injection Pump Breaker Racked-In

with LTOP in Service (Section 08.6)

URI

50-261/95-19-03

Closed

Loose Paint in Containment (Section 08.7)

LER

50-261/94-02-01

Closed

Plant Condition Outside Design Basis Due

to MSIV Inoperability (Section M8.1)

EET 50-261/94-16-03

Closed

Inadequate Corrective Action to Potential

TS Deficiencies (Section M8.2)

[ER

50-261/94-01-00

Closed

Failure to Test Instrumentation Channels

Per Technical Specifications (Section

M8 .3)

LER

50-261/94-01-01

Closed

Failure to Test Instrumentation Channels

Per Technical Specifications (Section

M8.3)

VIO

50-261/95-12-03

Closed

Maintenance Planner Fails To Properly

Develop Breaker PMTR (Section M8.4)

56

VIO

50-261/95-14-01

Closed

Inadequate Control Of Contractor Services

(Section M8.5)

LER

50-261/93-20-00

Closed

Technical Specification Violation Due to

Exceeding F-Delta-H Hot Channel Factor

(Section E8.1)

IFI

50-261/94-06-05

Closed

Adequacy of Periodic Verification Methods

(Section E8.2)

IFI

50-261/94-06-07

Closed

Mispositioning (Section E8.3)

VIO

50-261/94-27-07

Closed

Failure to Adequately Control Calorimetric

(Section E8.4)

VEO

50-261/95-12-05

Closed

Failure To Control Safeguards Information

(Section S8.1)