ML14176A755

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Insp Rept 50-261/89-200 on 890522-26.No Violations Noted. Major Areas Inspected:To Determine Whether Motor Operated Valves Designed,Installed & Being Maintained in Manner That Would Ensure Capability to Perform
ML14176A755
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 07/12/1989
From: Imbro E, Jeffrey Jacobson, Lanning W
Office of Nuclear Reactor Regulation
To:
Shared Package
ML14176A754 List:
References
50-261-89-200, IEB-85-003, IEB-85-3, IEC-79-14, IEIN-79-03, IEIN-79-3, IEIN-79-36, IEIN-84-13, IEIN-86-002, IEIN-86-029, IEIN-86-2, IEIN-86-29, IEIN-88-084, IEIN-88-84, NUDOCS 8908250262
Download: ML14176A755 (11)


See also: IR 05000261/1989200

Text

U.S. NUCLEAR REGULATORY COMMISSION

OFFICE OF NUCLEAR REACTOR REGULATION

Division of Reactor Inspection and Safeguards

Report No.:

50-261/89-200

Docket No.:

50-261

Licensee:

Carolina Power and Light Company (CP&L)

Facility:

H. B. Robinson Steam Electric Plant Unit No. 2

Inspection Conducted: May 22-26, 1989

Inspection Team Members:

Team Leader:

J. B. Jacobson, RSIB, NRR

Regional Support

S. Tingen, Region II

A. Szczepaniec, Region II

Electrical Power:

S. V. Athavale, RSIB, NRR

Mechanical Systems: M. C. Singla, Consultant

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1. Introduction, Summary and Licensee Commitments

1.1

Introduction

As a result of the numerous findings involving motor-operated valves (MOVs) that

were identified during the performance of other NRC team inspections, a team

inspection specific to the area of MOVs was developed. The purpose of this

Motor Operated Valve Inspection (MOVI) was to determine whether the MOVs in the

H. B. Robinson plant are designed, installed, and being maintained In a manner

that would ensure their capability to perform their intended safety-related func

tions. During the inspection, programmatic reviews were conducted of engineering,

maintenance, training, and operations as applicable to the assessment of the MOVs.

1.2 Summary

As a result of this inspection, two potential enforcement findings and two open

items were identified. The first potential enforcement finding concerned the

inadequate documentation and/or evaluation of equipment failures. Three examples

of this finding were noted during the inspection, including the failure to docu

ment and evaluate a thermal overload to a MOV that had tripped during the last

three unit startups. The second potential enforcement finding concerned four

examples of inadequate, improperly engineered design modifications to the plant.

The examples noted included a case in which the licensee replaced valves with

those of a different type without performing the calculations necessary to ensure

adequate motor actuator sizing. As a result, several safety-related motor

actuators installed in the plant are now undersized and require replacement.

The two open items identified during the inspection pertained to the lack of a

basis for motor actuator torque switch settings and for thermal overload sizing.

In addition to these weaknesses, the team identified several strengths within the

h. B. Robinson MOV program. Specifically, the training of maintenance personnel,

the quality of applicable maintenance procedures, and the review of MOV generic

communication were identified as strengths by the inspection team.

1.3 Licensee Commitments

On June 6, 1989, a conference call was held between Carolina Power and Light

(CP&L,) NRR, and Region 1I staff concerning the two open items identified during

the inspection. During the call, CP&L committed to performing the following

actions:

(1) Within 90 days, a review will be performed of the adequacy of torque

switch settings for all safety-related MOVs installed at the H. B.

Robinson plant.

(2) Within 90 days, a review will be performed of the thermal overload

sizing relative to all safety-related MOVs where either the valve,

the rotor actuator, or the overload protective device has been modified

since original plant construction.

-1-

2. Inspection Areas

2.1 Actuator Sizing

In order to assess the sizing of the motor actuators installed in the Robinson

plant, the team requested data for eight specific MOVs from a list of all

safety-related MOVs. The data requested included the valve type, size, stem

diameter, stem pitch, stem lead, and seat diameter, as well as the motor

actuator overall gear ratio, type, motor size, motor speed, and spring pack

type. In addition, data were requested pertaining to the applicable line

pressures, the maximum differential pressures, and the motor or motor control

center voltages. The line pressures, the differential pressures, and the

voltages given to the team were then evaluated by the appropriate mechanical

or electrical specialist team members. From these data, calculations were

generated for each MOV selected for valve-required thrust, torque, and for

maximum operator-available thrust or torque. From the calculations, it was

determined that all eight motor actuators could deliver enough torque or thrust

to stroke the selected valves under all design-basis conditions.

In addition to the eight selected valves, a review was performed of the licensee's

sizing calculations relative to the 11 MOVs subject to NRC Bulletin No. 85-03.

Of the 11 bulletin valves, the licensee had determined that 6 actuators might

not be sized sufficiently to complete valve stroking under all design-basis

conditions. As a result, the licensee had prepared a justification for continued

operation (JCO) for the six steam-driven auxiliary feedwater punip valves affected.

The JCO, Engineering Evaluation ENG-87191, was reviewed in detail by the team

during this inspection. The JCO was based upon licensee calculations that showed

that the subject valves would open but might not close under all design-basis

conditions. Specifically, it was calculated that valves V1-8A, B, and C on the

steam admission lines to the auxiliary feedwater pump turbines would not be

able to be remotely closed as a result of the motor actuator undersizing.

These valves would have to be closed following a steam-generator tube rupture

in order to prevent an unmonitored release to the environment through the steam

driven auxiliary feedwater pump steam exhaust line. Although the valves are not

capable of being remotely closed (from the control room), the team verified that

these valves could be manually closed because of their close proximity and acces

sibility to the control room. The V2-14A, B, and C steam-driven auxiliary

feedwater pump discharge isolation valves were also calculated to be undersized;

however, the postulated accident scenarios for these valves would not require

closing at maximum differential pressure.

During review of this JCO, the team determined that the licensee had used normal

bus voltages in lieu of actual postulated degraded voltages in their sizing

calculations. For instance, on the V2-14A, B, and C valves the licensee had

used 208 volts instead of the actual 180 volts calculated to exist at the motor

actuator during accident conditions. As a result, the licensee recalculated the

thrusts available at the motor actuators and determined that although less than

previously calculated, the actuators could still open but not close the valves

under design-basis conditions. In addition, the V2-16A, B, and C valves, not

subject to the original JCO, are now calculated to be marginally sized. The

licensee has committed to replacing the nine motor actuators for valves V1-8A,

B, and C; V2-14A, B, and C and V2-16A, B, and C during its next refueling outage

currently scheduled for March 1990.

-2-

2.2 Torque Switch Settings

During the inspection, it was determined that CP&L did not have calculations

to support the torque switch settings of safety-related MOVs except for the

11 valves subject to NRC Bulletin No. 85-03. Additionally, CP&L did not have

information relative to the original torque switch settings as determined by

either Limitorque or the valve vendor. Although the actual torque switch

settings on the valves are known, it is not known whether or not these settings

are correct. Except for the 11 MOVs subject to NRC Bulletin No. 85-03 and the

particular MOVs that may have been tested under design-basis differential pres

sure, no assurance exists that the torque switch settings on the remaining MOVs

correspond to those necessary to ensure operability. If the settings were too

low, power to the NOV would be interrupted before the MOV could complete its

intended function.

Using the data supplied by CP&L for the eight selected MOVs, calculations were

generated to determine the acceptability of the present torque switch settings.

Of the eight MOVs selected, one had its torque switch bypassed in the closed

direction. Of the remaining seven MOVs, calculations.showed that five had

adequate torque switch settings. The other two had settings that calculationally

appeared to be marginal. The licensee was able to demonstrate that one of these

MOVs had indeed been tested at full differential pressure. For the other valve,

the V6-12B auxiliary feedwater discharge cross-connect, the licensee could not

demonstrate that testing at full differential pressure had been performed.

In addition to the team's sample inspection, it was noted that the licensee had

to increase the torque switch settings on the majority of its 11 bulletin valves.

As a result of these findings, the licensee was asked to expeditiously evaluate

the current torque switch settings on those MOVs on which full differential

pressure testing had not been performed. During a conference call on June 6,

1989, with NRR and Region II,

CP&L committed to performing this review within

90 days. This item is identified as Open Item 50-261/89-200-01.

2.3 Voltage Study

In order to ensure that the installed MOVs will function under design-basis

conditions, the team reviewed the voltage calculations used as inputs into the

MOV sizing calculations. As the available MOV motor torque decreases with the

square of the ac voltage, the ability of an MOV to operate under less than

nominal voltage requires specific analysis. During the inspection, the team

determined that CP&L does not currently have calculations that delineate the

motor terminal voltage at any specific MOV under design-basis conditions.

Although the team did review CP&L calculations RNP-E.0002 concerning a recently

performed voltage study, it was determined that this study did not address bus

voltages that were supplied from the plant's emergency diesel generators. In

addition, the study did not analyze what effects short-term transients such as

motor startups might have on the voltage being supplied to the MOVs. Until a

thorough electrical voltage study is completed, the actual voltage expected to

be delivered to a specific MOV under design basis-conditions cannot be deter

mined, however, due to the large margins identified during the teams review

of motor actuator sizing, no immediate safety concern was identified in this

area.

-3-

2.4 Thermal Overloads

During the inspection, a review was conducted of CP&L's program for sizing and

testing thermal overloads to MOV circuits at the H. B. Robinson plant. The

team determined that at Robinson, overload protection devices to safety-related

MOVs are installed and are not bypassed during the actuation of the emergency

core cooling systems. These thermal overload devices are also not periodically

tested. In addition, no direct indication exists in the controTl oom if a ther

mal overload trips and interrupts power to a safety-related MOV. As a result

of the above findings, arid in lieu of the two inadequate design modifications

pertaining to thermal overloads cited in Section 2.6 of this report, CP&L was

asked to expeditiously review the sizing of thermal overload devices in applica

tions in which either the actuator, valve, motor, or overload device itself may

have been changed since original plant design. During a conference call on

June 6, 1989, with NRR and Region II, CP&L conitted to completing such a

review within 90 days. This item is identified as Open Item 50-261/89-200-02.

2.5 Maintenance History Review and Evaluation

The licensee utilizes work request (WRs) to administratively control corrective

maintenance associated with MOVs. The inspectors reviewed WRs processed in 1988

and 1989 that required safety-related MOV maintenance. The purpose of this

review was to verify that adequate corrective action was being performed when

MOV problems were identified. The results of this review indicated that in

several instances valves repeatedly failed to operate because of insufficient

corrective action.

The first example concerned valve V2-16A, the auxiliary feedwater pump discharge

valve. On two occasions, May 14 and September 2, 1988, the valve could not be

shut electrically. For both failures the corrective action involved cleaning

the torque switch contacts and cycling the valve to verify operation. The cor

rective action did not address how the torque switch contacts got dirty or why

two failures for the same reason occurred in such a short interval.

During

the subsequent refueling outage, as a result of a 10 CFR Part 21 notification

received from Limitorque, CP&L performed inspections for crackeo nelamine torque

switches on several MOVs. Although exact records of the inspection were not

kept, a severely damaged torque switch was said to have been removed from either

valve V2-16A or B. It is therefore thought that this cracked torque switch was

the likely cause of failure for valve V2-16A and that had a thorough inspection

been performed when the valve originally failed to stroke, this deficiency might

have been discovered.

The second example concerned valve CC-730, the reactor coolant pump bearing,

component cooling water return, isolation valve. On January 10, 1989, the valve

could not be fully opened electrically. Corrective action involved lubricating

the stem and cycling the valve several times to achieve proper operation. On

April 6, 1989, valve CC-730 again failed, but this time the valve could not be

shut electrically. Corrective action involved cleaning the torque switch

contacts and cycling the valve to verify proper operation. Review of periodic

maintenance records revealed that on November 28 and 29, 1988, the CC-730 valve

stem had been lubricated and the torque switch contacts cleaned. The corrective

action for the valve CC-730 failures did not address why the stem had to be

relubricated and the torque switch contacts reclearied at such short intervals.

The failures associated with valve CC-730 are similar to the failures described

-4-

in the 10 CFR Part 21 Limitorque notification previously discussed. CC-730 has

been identified by the licensee as possibly containing a melamine torque switch;

however, an inspection of this torque switch has not yet been performed.

As a

result, it appears that the true problems associated with this valve have neither

been identified nor corrected.

The third example of inadequate corrective action was associated with valve

V2-6A, a main feedwater isolation valve. On October 28, 1988, WR 88-ALCC1 was

written which stated that during the last three unit startups the valve would

not stroke.

Upon investigation it was determined that the thermal overload

device for this valve had tripped.

No evaluation of this problem was performed and

corrective action consisted of merely resetting the thermal overload device and

restroking the valve. During the inspection, discussions with operations

revealed that the thermal overload trips had occurred when transferring from

the startup to the normal mode of steam generator feeding. Under these

conditions, a higher than normal differential pressure existed across the valve,

resulting in more current being required by the motor actuator. In addition,

it was determined that the motor for the V2-6A actuator had previously been

replaced with a motor that drew more current. During the modifications, no

review of thermal overload sizing was performed.

As a result of the team's

review of this one work request, three separate deficiencies were identified.

First, the thermal overload trips were not documented until the third occur

rence.

The team informed CP&L that all thermal overload trips must be

documented and evaluated and that the CP&L practice of only documenting

repetitive thermal overload trips was unacceptable. Second, when the thermal

overload trip was finally documented, no engineering evaluation was performed.

Third, the motor for the V2-6A actuator was replaced without performing an

evaluation on thermal overload sizing. All three of these practices led to

the repetitive failure of valve V2-6A.

These examples of MOV failures illustrate that licensee corrective action was

inadequate to preclude additional similar failures and that valve failures were

sometimes :not documented to initiate corrective action. Failure to take

adequate corrective action in response to YOV failures and to properly document

MOV failures so that corrective action could be initiated is identified as

Potential Enforcement Item 50-261/89-200-03.

2.6 Modifications

In order to ensure that properly designed original equipment is not being

adversely altered a review was conducted of several modifications to the plant

that involved MOVs. From this review, it was apparent that, although equipment

may have originally been properly designed, CP&L made changes that may have

compromised equipment performance and operability.

The following examples

involve modifications performed to the plant in which the modification's effect

on overall system performance was either overlooked or improperly evaluated.

Yodificaticn 551 - This modification performed during 1980-81 replaced valves

V2-16A, B, and C and valves V2-14A, B, and C, which are on the discharge side

of the motor-driven auxiliary feedwater pumps and the steam-driven auxiliary

feedwater pumps, respectively.

The original valves were replaced with 4-inch

gate valves with flange ratings of 900 psi from the Anchor/Darling Valve Co.

During review of this modification package, it was noted that no sizing or

-5-

thrust calculations had been performed for these valves and that the modifica

tion indicated that the old valve actuators were to be used. No justification

for assuming the old actuators were still adequate was found.

During the testing and calculations required by NRC Bulletin No. 85-03, CP&L

determined that the V2-14A, B and C valve actuators were undersized. Addi

tionally, the V2-16A, B, and C valve actuators were calculated as being only

marginally large enough.

As a result of these findings, CP&L is to replace

all six valve actuators during the next refueling outage.

Had proper sizing

calculations been performed during the modification, this problem probably

would have not occurred.

Modification 939 - This modification was performed as a result of an inspection

conducted by CP&L Corporate Nuclear Safety that revealed a number of cases of

improperly coordinated protective devices. Modification 939 was initiated in

August 1988 to upgrade circuit breakers and overload devices in motor control

centers 5, 6, 9, and 10 and to ensure that protective devices could clear

system faults in a safe and efficient manner.

The overload devices and

circuit breakers for approximately 10 safety-related MOVs were replaced.

After the installation of Modification 939, spurious trips of motors started

to occur, including trips of MOVs.

The spurious trips were attributed to

inadequately sized thermal overloads and circuit breakers installed by the

modification. Corrective action involved the replacement or adjustment of

the newly installed circuit breakers, the reinstallation of the original

thermal overload devices, or the installation of re-sized thermal overload

devices. The apparent cause for the miscalculations was that the actual

locked-rotor currents for the motors were unavailable and estimated values

were used as inputs for thermal overload sizing calculations during prepara

tion of the modification.

The locked rotor currents were underestimated by

CP&L.

Modification 638 - This modification performed during June 1982 involved the

replacement of the V1-3A, B, and C main steam isolation bypass valves.

The

replacement valves were 2-inch, 900 psi rated gate valves with Limitorque

SMB-000-02 motor actuators. No thrust calculations or actuator sizing calcu

lations were found in the modification package.

Valve Specification L2-M-011,

Revision 1, included in the modification package delineated a motor actuator

voltage of 120/2000 volts. Later this was changed in Design Change Notice

638-1 to 208/416 volts.

The actual voltage that will be supplied to these

MOVs was calculated by CP&L during the inspection to be as low as 180 volts.

Motors rated at 208 volts may not be able to deliver the torque required under

postulated degraded voltage conditions.

Work Requests 87-AFBRI and 87-AFWSI - These work requests authorized the

replacement of the motor on valve actuator V2-6A.

The motor on this valve was

replaced because it had a magnesium rotor that had been identified as being

susceptible to degradation.

Although the new motor was said to have the same

torque output ratings, it required more current to achieve its rated value.

No

thermal overload sizing calculation was performed in the work request.

Sub

  • sequently, the thermal overload device to this valve tripped upon valve actuation

at least three times as reported by Work Request 88-ALCC1.

Had a thermal

overload device calculation been performed before the replacement, the problem

with the overload device prematurely tripping would probably not have occurred.

-6-

CP&L's failure to properly consider the effects of the modifications on overall

system functionality is identified as Potential Enforcement Item 50-261/89-200-04.

2.7 Training

The training and qualification program at H. B. Robinson specifically includes

a subprogram for MOVs. The qualification requirements are only applicable to

the shop personnel. Under the guidance of the foreman and supervisors, an

initial qualification is obtained and documented on a qualification card. After

initial qualification, each qualified individual must be requalified at regular

intervals. Currently, the MOV requalification period is 2 years.

MOV qualification is specialized for either a power plant mechanic or a power

plant electrician. In both cases, a basic MOV course must be successfully com

pleted at the Harris Energy and Environmental Center.

The mechanics take Valve

Operator Repair Course ME 400G and then obtain further on-the-job training at

H. B. Robinson. The electricians take Motorized Valve Operator Course EL S37G,

followed by an advanced course, Motorized Valve Operator Course EL 537R, at

H. B. Robinson. On-the-job training is also provided.for both mechanics and

electricians. Shop foremen then approve completion of the MOV qualification

cards.

Requalification for all shop personnel is at the discretion and approval of the

responsible foreman.

This decision is based on the training, job performance,

and experience of the personnel being requalified. For power plant mechanics,

this approval includes satisfactory performance by the individual of the

following: explanation of the fundamentals of MOVs, troubleshooting of an MOV,

and repair of an MOV. Power plant electricians must demonstrate satisfactory

performance by explaining the functions and operations of MOVs and components,

verifying valve travel positions and indications, operating a valve operator in

the manual mode, and cycling the valve operator in the electrical mode. Each

foreman tracks the requalification requirements for his assigned personnel.

There is no in-house training program for MOV diagnostic testing.

The licensee,

however, has sent personnel, including a foreman and two electricians, to a

MAC Testing Course provided by Limitorque.

No further training of this type is

currently planned. In summary, the training and qualification program at

H. B. Robinson was identified as a strength in that it provides adequate initial

training and required demonstration of satisfactory performance to maintain

qualifications for those personnel assigned to work on MOVs.

2.8 Maintenance Procedures

Three preventive maintenance procedures were reviewed. These were PM-112,

"Limitorque Inspection No. 1," Revision 6, dated July 15, 1987; PM-113,

"Limitorque Inspection No. 2," Revision 3, dated June 7, 1988; and PM-423,

"Limitorque Inspection No. 3," Revision 5, dated July 2, 1987.

The main purposes of the procedures are to provide guidelines for lubrication

of the main gearbox (PM-112), lubrication of the geared limit switch (PM-113),

and maintenance of the valve switches and controls (PM-423). The procedures

.

automatically schedule the maintenance at specified intervals.

-7-

The three procedures had been properly approved, were very detailed and easy to

follow, and provided space for reporting findings and collecting maintenance

data. Specifically, the control of the grease and lubricants, the inspection

of grease and switches, and the verification of torque switch settings, were

well defined in the procedures. In general, all three procedures appeared to

be adequate for the provision of the proper preventive maintenance for MOVs.

Additionally, the maintenance data sheets for each of the three procedures were

reviewed for eight different MOVs. The sheets and the maintenance data were

found to be properly complete and acceptable in each case.

Although most Limitorque preventive maintenance recommendations were followed

strictly, the licensee did not do so in one case. Limitorque recommends an

initial interval of 18 months for inspection and cleaning of MOV switches,

recognizing that the interval could be changed, based on plant experience and

judgment. The licensee established this maintenance interval as 36 months.

When questioned concerning the extended interval, the licensee cited the

allowance by Limitorque and the maintenance history record of the MOVs.

No specific documentation discussing or justifying the change was available.

In light of some of the current operational problems discussed elsewhere in

this report, and with new programs regarding problem trending and root cause

analysis being implemented, proper documentation of any changes to

recommended maintenance intervals would be appropriate and expected.

No

action is required of, or anticipated by, the licensee at this time; however,

it is expected that based on the developing maintenance histories, changes

to the preventive maintenance intervals will be made as appropriate. In

general, the quality of the maintenance procedures was seen as a strength

within the licensee's MOV program.

2.9 Evaluation of Generic Communication

During the inspection, a review was conducted of CP&L's evaluations of MOV

related generic communication.

Evaluations of the following NRC information

notices, NRC bulletins, and 10 CFR Part 21 reports were reviewed by the inspec

tion team.

IE Notice No. 79-03, dated February 9, 1979, "Limitorque Valve Geared Limit

Switch Lubricant" - The licensee's response was reviewed and found acceptable.

By procedure, the licensee does not use Beacon 325 lubricant in the geared

limit switch.

IE Circular No. 79-04, dated June 7, 1979, "Loose Locking Nut on Limitorque

Valve Operators" - In accordance with the licensee's trouble ticket ENG-090,

all Limitorque-type SMB valve operators were inspected and the locknuts were

properly staked. No mention of SMC-type valves was made in the licensee's

internal response, but licensee personnel have stated that none of these

type valves were installed in the plant at that time.

The response was

satisfactory.

TE Notice No. 84-36, Supplement 1, dated September 11, 1984, "Loosening of

Locking Nut of Limitorque Operator" - The supplement corrected information

  • provided in IE Notice No. 84-36.

The supplement identified that the bearing

locknut on the actuator worm shaft was backed out as a result of the loosening

of a set screw, which subsequently led to inoperability of a safety-related

valve.

The problem occurred because the design incorporated a left-handed

-8-

thread which is unusual in these types of valves.

The licensee evaluation stated

that the licensee valves did not have this particular design and, therefore, the

notice was not applicable. It appears that the response was properly evaluated

at the time and that the response is satisfactory.

IE Notice No. 84-13 dated February 28, 1984, "Potential Deficiency in Motor

Operated Valve Control Circuits and Annunciation" - The licensee's evaluation

determined that the thermal overload devices installed in Robinson MOV circuits

are not bypassed during actuation of the safety systems.

The problem of not

knowing whether an overload device has tripped is applicable to the Robinson

plant, however, because the control room valve position lights are not extin

guished nor are thermal overload alarm circuits installed at the Robinson

plant.

The licensee is aware of this potential problem and plans on taking no

specific action at the current tie.

NRC Information Notice No. 88-84, dated October 20, 1988, "Defective Motor Shaft

Keys in Limitorque Motor Actuators" - This information notice, which concerned

nonconforming shaft key materials, had been received by CP&L but had not yet

been evaluated because of a backlog of work. During the inspection, Action

Item No.89-027 was assigned by CP&L for completion of this evaluation.

IE Information Notice No. 86-02, dated January 6, 1989, "Failure of Valve

Operator Motor During Environmental Qualification Testing" - The licensee's

evaluation of this information notice, which concerned failure of magnesium

rotor motors in harsh environments, was found to be very thorough.

During this

evaluation, CP&L determined that not only is the problem with magnesium rotor

motors apparent in a harsh environment, but also that these types of motors can

also exhibit failures in relatively mild environments.

As a result, CP&L is

replacing all magnesium rotor motors at the Brunswick plant.

Limitorque 10 CFR Part 21 Modification, dated November 3, 1988 - CP&L's evaluation

of this Part 21 notification concerning melamine torque switch failures was

reviewed during the inspection.

The licensee has identified 36 safety-related

and 24 nonsafety-related Limitorque actuators that will require torque switch

inspections to verify whether melamine torque switches are installed.

The licen

see has scheduled to complete the inspection and replacement of all affected

torque switches by March 16, 1990.

IE Notice No. 86-29, dated April 28, 1986, "Effects of Changing Valve Motor Operator

Switch Settings" - This information notice was provided to alert recipients to

the consequences of changing switch settings without adequate prior evaluation.

The inspectors' review of the licensee's internal response to IE Notice No. 86-29

indicated that the contents of the IE notice were incorporated into the licensee

MOV program. Review of the licensee's program indicated that switch settings were

controlled and maintained, and changes to switch settings were adequately evaluated.

0II

3.0 Exit Meeting

Upon completion of the inspection an exit meeting was held on May 26, 1989. The

following individuals attended:

S. G. Tingen

NRC -

Region 11

A. J. Szczepaniec

NRC -

Region 11

M. C. Singla

NRC -

Consultant

T. G. Scarbrough

NRC -

NRR

J. B. Jacobson

NRC - NRR

Russell F. Powell

CP&L - Engineering Supervisor

Keith R. Jury

NRC -

Resident Inspector

Ronnie Lo

NRC -

NRR -

Project Manager

L. W. Garner

NRC -

Sr. Resident Inspector

R. D. Crook

Sr. Specialist - Regulatory Compliance

E. M. Harris, Jr.

Director - Onsite Nuclear Safety

John F. Benjamin

Engineering Supervisor -

Plant Systems

(Technical Support)

C. R. Dietz

Manager -

RNPD

Gary D. Shartzer

Senior Engineering -

Technical Support

RNP

Richard V. Cady

Senior Engineering -

Configuration Control

RNP

C. A. Bethea

Manager -

Training

D. R. Quick

Acting General Manager -

RNPD

S. V. Athavale

Electrical Engineer -

NRR

J. M. Curley

Director Regulatory Compliance

Gene Imbro

NRC -

NRR - Section Chief

RSIB

-10-