ML14181A978

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Insp Rept 50-261/97-14 on 971123-980103.No Violations Noted. Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support
ML14181A978
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 02/02/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14181A977 List:
References
50-261-97-14, NUDOCS 9802090232
Download: ML14181A978 (15)


See also: IR 05000261/1997014

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:

50-261

License Nos:

DPR-23

Report No:

50-261/97-14

Licensee:

Carolina Power & Light (CP&L)

Facility:

H. B. Robinson Unit 2

Location:

3581 West Entrance Road

Hartsville, SC 29550

Dates:

November 23 - January 3, 1998

Inspectors:

B. Desai, Senior Resident Inspector

J. Zeiler, Resident Inspector

Approved by:

M. Shymlock, Chief, Projects Branch 4

Division of Reactor Projects

9802090232 980202

PDR

ADOCK 05000261

G

PDR

EXECUTIVE SUMMARY

H. B. Robinson Power Plant, Unit 2

NRC Inspection Report 50-261/97-14

This integrated inspection included aspects of licensee operations,

maintenance, engineering, and plant support. The report covers a six-week

period of resident inspection.

Operations

The conduct of operations was professional and safety-conscious

(Section 01.1).

The inspector identified that the licensee had erroneously included the

wrong heatup and cooldown limit curves during the implementation of

improved TS. The licensee determined that these errors were caused by

inattention to detail. The potential safety implications were minimal

due to plant.procedures specifically prescribing the correct heatup and

cooldown limits (Section 01.2).

The inspector concluded that the licensee appropriately performed an

investigation of a problem related to secondary side oscillations

experienced earlier in the report period. Actions taken by the licensee

have contributed to the reduction of oscillations in recent weeks

(Section 01.3).

The licensee promptly and adequately implemented and planned corrective

actions to return the "A"

Emergency Diesel Generator to operable status

following inadvertent wetting of equipment due to inappropriate valve

lineup on the service water system (Section 02.1).

The onsite review functions of the Plant Nuclear Safety Committee (PNSC)

were conducted in accordance with Technical Specification (TS). The

PNSC meetings were well coordinated and meeting topics were thoroughly

discussed and evaluated. Nuclear Assurance Section (NAS) continued to

provide strong oversight of licensee activities (Section 07.1).

Maintenance

In general, routine maintenance activities were performed satisfactorily

(Section M1.1).

The inspector concluded that a weakness in the post maintenance testing

and planning existed, which necessitated a reentry in a TS action

statement. However, the licensee identified several problems with post

maintenance and surveillance testing that could place the unit in

TS 3.0.3. They stopped these test until the conditions could be

evaluated. An IFI was identified, pending licensee evaluation involving

Residual Heat Removal (RHR) Emergency Core Cooling System (ECCS)

flowpath operability with valve FCV-605 open (Section M1.2).

2

Engineering

The inspector concluded that overall, engineering support was effective

in maintaining safe operations of the plant (Section E1.1).

Plant Support

The inspectors concluded that radiation control and security practices

were proper (Section R1.1 and S1.1).

Report Details

Summary of Plant Status

The unit operated at rated power for the entire report period.

I. Operations

01

Conduct of Operations

01.1 General Comments (71707)

The inspectors conducted frequent control room tours to verify proper

staffing, operator attentiveness and communications, and adherence to

approved procedures. The inspectors attended daily operation turnovers,

management reviews, and plan-of-the-day meetings to maintain awareness

of overall plant operations. Operator logs were reviewed to verify

operational safety and compliance with Technical Specification (TS).

Instrumentation, computer indications, and safety system lineups were

periodically reviewed from the Control Room to assess operability.

Frequent plant tours were conducted to observe equipment status and

housekeeping. Condition Reports (CRs) were routinely reviewed to assure

that potential safety concerns and equipment problems were reported and

resolved.

In general, the conduct of operations was professional and safety

conscious; specific events and noteworthy observations are detailed in

the sections below.

01.2 Technical Specification Reviews

a. Inspection Scope (71707)

The inspector reviewed licensee compliance with TS, including periodic

surveillance requirements, Limiting Conditions for Operations, and

Bases.

b. Observations and Findings

During a review of TS, the inspector noted discrepancies in the Reactor

Coolant System (RCS) Heatup and Cooldown limit curves (Figures 3.4.3-1

and 3.4.3-2 of TS 3.4, Reactor Coolant System). The heatup curve

(Figure 3.4.3-1) contained the same curve as the cooldown curve in

(Figure 3.4.3-2). The inspector notified the licensee of the

discrepancy. The licensee initiated a condition report to determine the

cause and corrective action. The licensee determined that the heatup

and cooldown curves associated with the original improved TS submittal

to the NRC were correct. However, during a later submittal of the same

curves to the NRC, the licensee mistakenly included the heatup curve for

the cooldown curve. The NRC subsequently issued the improved TS with

the curves submitted by the licensee. Then, during the licensee copying

of the NRC issued improved TS for distribution, an addition error was

2

made when the cooldown curve was copied for the heatup curve. Thus, the

controlled TS copies that were distributed were incorrect.

The licensee immediately initiated actions to correct the problem. This

included, change out of the page associated with the heatup curve to

incorporate the correct curve. The cooldown curve was technically

correct however, it was not the one submitted for approval by the NRC.

The licensee discussed theissue with Nuclear Reactor Regulation (NRR).

Current NRR plans to reissue the cooldown curve as an administrative

change. Additionally, the licensee issued a night order to make the

operating staff aware of the condition.

The inspector reviewed plant operating procedures that control

evolutions involving RCS heatup and cooldown. General Procedure

(GP)-002, Cold Shutdown to Hot Subcritical at No Load Tavg and GP-007,

Plant Cooldown from Hot Shutdown to Cold Shutdown, refer to the TS

heatup and cooldown limit curves in the precautions section. However,

the implementing section of the procedure specifically prescribed the

numeric valve limits. The inspector determined that while the

precautions were in error by virtue of reference to the wrong curves in

TS, the body of the procedure prescribed the correct heatup and cooldown

valves. Thus, adherence to procedures GP-002 and GP-007 would not have

led to exceeding cooldown or heatup limits. Additionally, since the

implementation of the improved TS. the plant has not had to perform any

evolution requiring RCS heatup or cooldown.

Conclusions

The inspector identified that the licensee had erroneously included the

wrong heatup and cooldown limit curves during the implementation of

improved TS. The licensee determined that these errors were most likely

caused by inattention to detail.

The potential safety implications were

minimal due to plant procedures specifically prescribing the correct

heatup and cooldown limits.

01.3 Secondary Plant Oscillations

a. Inspection Scope (71707)

The inspector monitored licensee response to secondary plant

oscillations that occurred during the report period.

b. Observations and Findings

The unit periodically experienced oscillations on the secondary side,

including unexpected changes in the heater drain tank level. These

oscillations also affected the feedwater system, resulting in the

receipt of low feedwater pressure alarms and swings in the feedwater

flow control valves, and oscillations in steam generator levels. Though

3

these oscillations were minor in nature, the licensee initiated an

investigation of the potential cause(s) of the oscillations.

During this investigation, the licensee determined that the oscillations

were most likely initiated due to a problem with Level Control Valve

(LCV) 1-530 A. This valve regulates flow through the heater drain tank

pumps to maintain the correct heater drain tank levels. The licensee

was postulating a problem internal to the valve, or with the control

system associated with the valve. As part of the investigiation, the

licensee opened (approximately five turns) the bypass valve to LCV

1530 A. This has reduced the occurrence of oscillations. The licensee

plans to troubleshoot the valve internals as well as control circuitry

during the upcoming refueling outage.

c. Conclusions

The inspector concluded that the licensee appropriately performed an

investigation into the problem related to secondary side oscillations

experienced earlier in the report period. Actions taken by the licensee

have contributed to the reduction of oscillations in recent weeks.

02

Operational Status of Facilities and Equipment

0.2.1 Water Intrusion into Emergency Diesel Generator "A"

Electrical

Components

a. Inspection Scope (71707)

The inspector reviewed the circumstances involving the "A"

EDG being

declared inoperable following the intrusion of leaking water from the

service water system into the generator control panel,.current

transformer cabinet, and air compressor control circuitry. The water

drained from the ventilation ducts located in the EDG room ceiling

following an operator's failure to conduct a proper valve lineup. The

inspector discussed the incident with operations, maintenance, and

engineering personnel, and reviewed procedures related to the

configuration control of cooling water systems isolated for cold weather

protection.

b. Observations and Findings

On December 28, 1997, the Inside Auxiliary Operator (IAO) was assigned

to support chemistry personnel in aligning service water cooling flow to

the "C"

Auxiliary Boiler Sample Cooler. Service water to the sample

cooler, as well as other non-essential service water cooling loads, such.

as the Evaporative Air Coolers (EACs), had previously been isolated and

the piping drained/vented to prevent freezing in accordance with

Operating Procedure (OP)-925, Cold Weather Operation. During the

alignment of cooling water to the sample cooler, the IAO opened valves

admitting service water to the EACs. The IAO failed to realize that the

4

EAC vent/drain valves located in the EDG Ventilation Fan rooms, directly

above the EDG rooms, were still open per OP-925. This allowed service

water to flow out of the open vent valves, onto the floor of the fan

rooms, and into the EDG ventilation duct which opened into the ceiling

of the EDG rooms. Water entering the EDG room got on several EDG

electrical components including the generator control panel, current

transformer cabinet, and air -compressor. The control room was alerted

to the problem after receiving several alarms, including,-a fire

protection panel FDAP B-1 trouble, vital battery charger trouble, and

air compressor trouble/trip. Upon investigation, the operators

discovered the source of the water and isolated the valves. The "A"

EDG

was declared out-of-service at 8:59 a.m., requiring entry into a seven

day action statement per TS 3.8.1.B. Recovery actions were developed to

inspect, repair, and return the EDG to an operable status.

The inspector reviewed the extent of the impact from the water intrusion

and the licensee's recovery activities. The licensee inspected all

areas that were wetted. Moisture was found on the generator buss bars

and current transformers. These areas were dried with portable heaters

and the current transformers meggered to verify proper performance. The

air compressor was allowed to.dry and visually verified to operate

properly following re-energization. The EDG ventilation ductwork was

also dried and inspected for any damage. Inspection of the "B"

EDG room

revealed that no water had reached this area. Following all inspections

and repairs, the EDG was operated to verify operability, and was

returned to service at 2:45 a.m. on December 29, 1998. The inspector

determined that the licensee had adequately inspected and taken actions

to restore the equipment to a reliable condition.

The inspector reviewed CR 97-2508 which documented the licensee's

investigation of the incident. The CR identified several deficiencies

in the actions taken by the IAO during the alignment of service water to

the sample cooler. While the IAO had been authorized at the pre-shift

briefing that morning to align sample cooling water to the boiler, he

had not consulted with his supervisor when he determined that there was

no actual procedure specifically designed to accomplish this task. The

IAO also had not reviewed OP-925 to understand how service water had

been isolated to the EACs for cold weather protection. As a result. he

did not realize that there were open vents/drains in the EAC lineup that

needed to be closed prior to aligning service water to the sample

cooler. The licensee determined that this incident could have been

prevented had proper procedure usage and self-checking been performed.

The licensee's corrective actions for this incident included the

following: 1) guidance was sent to each shift to review existing

procedure usage guidelines, reinforcing the expectations that approved

procedures be utilized where appropriate, 2) a modification was

initiated to provide an alternate source of cooling water to the

auxiliary heating system, and, 3) formal operator training was to be

developed and implemented to address weaknesses in the operator

5

understanding of system configurations associated with the cold weather

protection lineup, EAC cooling water lineup, and alternate cooling to

the auxiliary heating system. The licensee also planned to revise OP 925 to provide greater controls, e.g., caution/clearance tagging, of

systems temporarily aligned for cold weather protection in order to

heighten operator awareness of the configurations.

As a result of this and several other recent operator errors, operations

management identified a negative trend in operator human performance

errors. The licensee plans to conduct stand-down meetings with each

operations shift. At these stand-down meetings, the Shift

Superintendent of Operations plans to discuss the declining trend in

human performance, the specific human performance errors identified

recently, and emphasize.the need to ensure clear communication and

understanding of task assignment details, proper self-checking

techniques, and the use of three way communications, etc.

c. Conclusions

The inspector concluded that the licensee had promptly implemented

adequate recovery actions to return EDG "A"

to an operable status

following the intrusion of service water into EDG electrical components.

The root cause of the incident was attributed to weak procedural usage,

understanding of the cold weather protection, and service water

alignment to out-of-service equipment. The licensee promptly and

adequately implemented and planned corrective actions to return the A

EDG to operable status following inadvertent wetting of equipment due to

inappropriate valve lineup on the service water system.

07

Quality Assurance In Operations

07.1 Plant Nuclear Safety Committee and Nuclear Assessment Section Oversight

a. Inspection Scope (40500)

The inspector evaluated certain activities of the Plant Nuclear Safety

Committee (PNSC) and Nuclear Assessment Section (NAS) to determine

whether the onsite review functions were conducted in accordance with TS

and other regulatory requirements.

b. Observations and Findings

The inspector periodically attended PNSC meetings during the report

period. The presentations were thorough and the presenters readily

responded to all questions. The committee members asked probing

questions and were well prepared. The committee members displayed a

good understanding of the issues and their potential risks. Further,

the inspector reviewed NAS audits and concluded that they were

appropriately focused to identify and enhance safety.

6

c. Conclusions

The inspector concluded that the onsite review functions of the PNSC

were conducted in accordance with TS. The PNSC meetings attended by the

inspector were well coordinated a.nd meetings topics were thoroughly

discussed and evaluated. NAS continued to provide strong oversight of

licensee activities.

08

Miscellaneous Operations Issues (71707)

08.1

(Closed) Licensee Event Report (LER) 50-261/97-10. Emergency Diesel

Generator(EDG) Inoperability Due to Mispositioned Output Breaker Control

Switch:

This LER was issued by the licensee on September 15, 1997.

following the identification of a mispositioned B EDG output breaker

control switch. In this condition, the breaker was not available to

supply power to the associated emergency bus. While the exact time of

mispositioning was not determined, the B EDG was thus determined to be

inoperable at least for a period of approximately four days. The NRC

issued a Severity Level III violation on December 12, 1997 (EA 97-490)

as a result of this issue. Items EEI 50-261/97-10-02 and 50-261/97-10

03 associated with this issue remain open, pending NRC review of

licensee corrective actions as a result of the violation. Based on

this, the LER is closed.

08.2 (Closed) LER 50-261/97-11, Reactor Trip Due to Condensate Pump "B"

Shaft

Failure:

This LER was submitted by the licensee on December 16, 1997

following a reactor trip from 100 percent power on November 16. 1997.

The circumstances related to the reactor trip were discussed in NRC

inspection report 50-261/97-11, dated November 7, 1997. The inspector

reviewed completed and planned corrective actions related to the reactor

trip. Based on satisfactory assessment of licensee actions, this LER is

closed.

II. Maintenance

M1

Conduct of Maintenance

M1.1 General Comments

a. Inspection Scope (61726 and 62707)

The inspector reviewed/observed all or portions of the following

maintenance related-work requests/job orders (WRs/JOs) and/or

surveillances and reviewed the associated documentation:

OST 910 Dedicated Diesel Generator Monthly

Engineering Surveillance Test (EST)-146, End-of-Life Moderator

Temperature Coefficient Measurement,

7

Maintenance Surveillance Test (MST)-014, Steam Generator Pressure

Protection Channel Testing.

WR/JO 97-ACPD1, Replacement of Hagan Modules in Steam Generator

Pressure Protection Circuitry,

WR/JO AAOU-002, Limitorque Grease Inspection of Containment Fan

Cooler Service Water Valve V6-33E.

b. Observations and Findings

The inspector observed that these activities were performed by personnel

who were experienced and knowledgeable of their assigned tasks.

Procedures were present at the work location and being followed.

Procedures provided sufficient detail and guidance for the intended

activities. Activities were properly authorized and coordinated with

operations prior to starting. Test and maintenance equipment in use was

properly calibrated, procedure prerequisites were met, and system

restoration was completed. Since the performance of surveillance EST

146 was considered to be an infrequent activity, a detailed pre-job

briefing, which included management oversight and coordination, was

provided. Good three-way communication was observed between maintenance

personnel during the performance of MST-014. Maintenance personnel

performing safeguards system Hagan module replacement activities

associated with WR/JO 97-ACPD1 were very experienced and knowledgeable

of the system and were deliberate in their actions. Operations

management provided guidance on the proper implementation of Improved

Technical Specifications during Hagan module replacements via a detailed

Night Order.

c. Conclusions

The inspector concluded that routine and preventative maintenance

activities observed, as well as surveillances, were performed

satisfactorily.

M1.2 Planning of Post Maintenance Testing

a. Inspection Scope (62707)

The inspector reviewed circumstances surrounding a corrective

maintenance activity on air operated valves HCV-758 and FCV-605. on the

Residual Heat Removal(RHR) System.

b. Observations and Finding

The licensee conducted planned maintenance on RHR valves FCV-605 and

HCV-758. These valves are required by TS 3.5.2.B to be maintained

closed with the motive air isolated.

The maintenance conducted on these valves involved motive air regulator

filter replacement. Following filter replacement. the air regulator

8

setpoint check was not initially performed as part of post maintenance

testing (PMT). due to poor communication between shifts as well as poor

planning. This required reentry in TS 3.5.2.B to accomplish that PMT

requirement.

Further, it was not initially recognized that another PMT requirement

involving valve stroking would potentially place the unit in TS 3.0.3.

Therefore, the PMT involving valve stroking was not performed pending

resolution of issue involving TS 3.0.3 entry. A CR was initiated by the

licensee to evaluate the circumstances leading to this situation as well

as resolve the TS 3.0.3 applicability. Since the above valves are not

allowed to be opened in Modes 1, 2. and 3, the PMT involving valve

stroking was postponed until the next available opportunity (upcoming

refueling outage).

During the CR evaluation, the licensee also recognized that Operations

Surveillance Test (OST) Procedures OST-251-1, RHR Pump "A" and

Components Test, and OST-251-2, RHR Pump "B"

and Components Test

requires the opening of valve FCV-605 to accomplish RHR pump discharge

check valve testing under circumstances where a sufficient differential

pressure across tested check valves cannot be obtained under normal

circumstances. However, the OSTs did not recognize that opening valve

FCV-605 potentially places the unit in T.S 3.0.3. The licensee plans to

evaluate the OSTs prior to their next required performance. Pending

licensee completion of the review associated with this issue, it will be

classified as Inspector Followup Item (IFI) 97-14-01. Opening of RHR

Valves FCV-605 or HCV-758 During Testing.

The inspector discussed the issue with the licensee and verified that

appropriate controls were in place to preclude inadvertent opening of

valves HCV-758 and FCV-605, pending resolution of the issue.

c. Conclusion

The inspector concluded that a weakness in the post maintenance testing

and planning existed, which necessitated a reentry in a TS action

statement. However, the licensee identified several problems with post

maintenance and surveillance testing that could place the Unit in

TS 3.0.3. They stopped these test until the conditions could be

evaluated. An IFI was identified, pending licensee evaluation involving

.RHR ECCS flowpath operability with valve FCV-605 open.

9

M8

Miscellaneous Maintenance Issues (92902)

M8.1 (CLOSED) Unresolved Item (URI) 50-261/96-06-03, Review Licensee

Assessment of Need to Supplement Licensee Event Report (LER) 50-261/95

001-00: LER 50-261/95-001-00 involved the licensee's identification that

ASME Section XI Inservice Testing of Safety Injection (SI) valves,

potentially rendered the SI system inoperable as a result of the test

configuration. The LER indicated that an evaluation had been initiated

to determine conclusively whether the SI system had been inoperable in

the testing configuration. The licensee completed their evaluation in

April 1995, at which time it was confirmed that the system had been

inoperable. During a previous inspection, the inspector reviewed the

LER, subsequent licensee evaluation and corrective actions. Non-Cited

Violation 50-261/97-06-02 was issued for inadequate test procedures

which allowed the adverse test configuration.

During review of the LER, licensee evaluation results, and corrective

actions in the previous inspection, the inspector noted that the

licensee had failed to provide a supplement to the LER describing the

results of the April 1995 evaluation and corrective actions. The

inspector believed that the LER had not provided complete information

regarding the cause of the condition or corrective action. As a result

of the inspector's comments, the licensee initiated CR 97-01045 to

evaluate whether a supplement was warranted.

On January 8. 1998. the licensee submitted LER 50-261/95-001-01, which

provided the results of the aforementioned April 1995 evaluation and

subsequent corrective actions. The inspector reviewed the LER and

determined that the licensee had provided adequate details regarding the

resolution of this issue. Based on review of LER 50-261/95-001-01, this

URI is closed.

M8.2 (Closed) LER 50-261/95-001-01, Safety Injection Pump Testing Requires TS 3.0 Entry: As discussed in Section M8.1 of this report, the licensee

supplied this LER supplement to provide additional information regarding

the results of an evaluation to determine conclusively whether the SI

system had been inoperable in certain ASME Section XI Inservice test

configurations, as well as the corrective actions to address the

incident. Based on review of the licensee's evaluation results and.

corrective action, this LER is closed.

III. Engineering

El

Conduct of Engineering

E1.1 General Comments (37551)

The inspector periodically assessed engineering support of activities

affecting plant operations and maintenance. The inspector concluded

10

that overall, engineering support was effective in maintaining safe

operations of the plant.

IV.

Plant Support

R1

Radiological Protection and Chemistry Controls

R1.1 General Comments (71750)

The inspector periodically toured the Radiological Control Area (RCA)

during the inspection period. Radiological control practices were

observed and discussed with radiological control personnel including RCA

entry and exit, survey postings, locked high radiation areas, and

radiological area material conditions. The inspector concluded that

radiation control practices were proper.

Si

Conduct of Security and Safeguards Activities

S1.1 General Comments (71750)

During the period, the inspector toured the protected area and noted

that the perimeter fence was intact and not compromised by erosion nor

disrepair. Isolation zones were maintained on both sides of the barrier

and were free of objects which could shield or conceal an individual.

The inspector periodically observed personnel, packages, and vehicles

entering the protected area and verified that necessary searches,

visitor escorting, and special purpose detectors were used as applicable

prior to entry. Lighting of the perimeter and of the protected area was

acceptable and met illumination requirements.

V. Management Meetings

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee

management at the conclusion of the inspection on January 16, 1998. No

proprietary information was identified.

  • ieneePARTIAL

LIST OF PERSONS CONTACTED

Li censee

J. Boska. Manager. Operations

H. Chernoff, Supervisor. Licensing/Regulatory Programs

T. Cleary. Manager, Maintenance

J. Clements. Manager, Site Support Services

J. Keenan, Vice President, Robinson Nuclear Plant

R. Duncan, Manager, Robinson Engineering Support Services

R. Moore, Manager. Outage Management

J. Moyer, Manager, Robinson Plant

R. Warden, Manager, Nuclear Assessment Section

T. Wilkerson, Manager, Regulatory Affairs

D. Young, Director. Site Operations

NRC

B. Desai, Senior Resident Inspector

J. Zeiler, Resident Inspector

12

INSPECTION PROCEDURES USED

IP 37551:

Onsite Engineering

IP 40500:

Effectiveness of Licensee Controls in Identifying. Resolving, and

Preventing Problems

IP 61726:

Surveillance Observations

IP 62707:

Maintenance Observation

IP 71707:

Plant Operations

IP 71750:

Plant Support Activities

IP 92902:

Followup - Maintenance

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

Type Item Number

Status

Description and Reference

IFI

50-261/97-14-01

Open

Opening of RHR Valves FCV-605 and HCV-758

During Testing (Section M1.2)

Closed

Oype

Item Number

Status

Description and Reference

LER

50-261/97-10

Closed

Emergency Diesel Generator(EDG)

Inoperability Due to Mispositioned Output

Breaker Control Switch (Section 08.1)

LER

50-261/97-11

Closed

Reactor Trip Due to Condensate Pump "B"

Shaft Failure (Section 08.2)

URI

50-261/96-06-03

Closed

Review Licensee Assessment of Need to

Supplement Licensee Event Report (LER) 50

261/95-001-00 (Section M8.1)

LER

50-261/95-001-01 Closed

Safety Injection Pump Testing Requires TS 3.0 Entry (Section M8.2)

Discussed

Type Item Number

Status

Description and Reference

NONE

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