ML14181B010

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Insp Rept 50-261/98-05 on 980329-0509.Violations Noted.Major Areas Inspected:Aspects of Licensee Operations,Maint, Engineering & Plant Support
ML14181B010
Person / Time
Site: Robinson 
Issue date: 06/08/1998
From: Ernstes M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14181B008 List:
References
50-261-98-05, 50-261-98-5, NUDOCS 9806160186
Download: ML14181B010 (25)


See also: IR 05000261/1998005

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket No:

50-261

License No:

DPR-23

Report No:

50-261/98-05

Licensee:

Carolina Power & Light (CP&L)

Facility:

H. B. Robinson Unit 2

Location:

3581 West Entrance Road

Hartsville, SC 29550

Dates:

March 29 - May 9, 1998

Inspectors:

B. Desai, Senior Resident Inspector

A. Hutto, Resident Inspector

F. Wright, Region II Inspector

G. MacDonald, Region II Project Engineer

Approved by:

M. Ernstes, Acting Chief, Projects

Branch 4

Division of Reactor Projects

0

Enclosure 2

9806160186 980608

PDR

ADOCK 05000261

G

PDR

EXECUTIVE SUMMARY

H. B. Robinson Power Plant, Unit 2

NRC Integrated Inspection Report 50-261/98-05

This integrated inspection included aspects of licensee operations,

maintenance, engineering, and plant support. The report covers a six-week

period of resident inspection; in addition, it includes the results of

inspections by Region II based inspectors.

Operations

The conduct of operations was professional, risk informed, and safety

conscious (Section 01.1).

A non-cited violation involving inadequate testing of refueling

equipment was identified. There were no direct safety consequences of

the fuel assembly drop incident. Had an irradiated assembly been

subject to a similar drop, any release of radioactivity would have been

contained, due to containment closure requirements during fuel movement.

Licensee follow up to this, event was appropriate (Section 01.2).

The inspector observed portions of startup related activities and

concluded that management decision to suspend startup to verify

potential affects of the seismic event were conservative. The inspector

did not note any affect to the plant as a result of the seismic event.

Operator performance during startup was considered good (Section 01.3).

Reactor operator response to the failed closed turbine control valve was

incorrect. Licensee plans to review this event to enhance future

training activities. Overall plant response was appropriate. Reactor

startup activities following the trip were uneventful (Section 02.1).

A violation for failure to perform a required surveillance test on the

containment personnel air lock test was identified (Section 04.1).

Nuclear Assessment Section and Plant Nuclear $afety Committee continued

to provide strong oversight, including during refueling outage 18

(Section 07.1).

Maintenance

Maintenance and surveillance activities were performed satisfactorily.

The inspector noted good controls of housekeeping and good supervisor

oversight of work activities (Section M1.1).

The repairs on the service water (SW) header were appropriately

completed. Management oversight of this problem was considered good

(Section M2.1).

The "A"

motor driven auxiliary feedwater (MDAFW) pump was deadheaded

during a test configuration. This did not cause damage to the pump.

Licensee actions to determine the root cause, including formation of an

event review team (ERT), were appropriate.

2

Two orifices on the MDAFW recirculation lines that had been worked on

during the outage were installed backwards due to inattention to detail

on the part of the mechanic. This issue was identified as a non-cited

violation. The incorrectly installed orifices did not contribute to the

pump deadheading (Section M4.1).

Engineering

Modification packages reviewed were acceptable. Modification 97-382

implemented corrective action to restore the damper control scheme for

the Containment Recirculation Cooling System units (Section E1.1).

The environmental qualification (EQ) components inside containment which

were inspected were being maintained with qualified seals in accordance

with EQ program requirements. The EQ data packages reviewed were being

updated in accordance with procedure EGR-NGGC-156, Environmental

Qualification Of Electrical Equipment Important To Safety. No backlog

of unincorporated engineering service requests (ESRs) was noted (Section

E2.1).

The licensee was conservative in evaluating a Westinghouse BF relay

failure during RFO-18 testing. The relay testing discrepancies were

being dispositioned in accordance with corrective action program

requirements (Section E2.2).

In response to the licensee's letter of April 4, 1998, several examples

of cauculational deficiencies identified in Notice of Violation dated

March 4, 1998, have been withdrawn and will be tracked as an Unresolved

Item (Section E8.1).

Plant Support

Housekeeping and cleanliness within the radiation control area were

acceptable (Section R1.1).

Overall, the inspectors observed good radiological controls and

radiation worker compliance throughout the inspection (Section R1.1).

A Non-Cited Violation was identified for radiation worker's failure to

comply with radiation protection procedures (Section R1.1).

The effectiveness of the licensee's dose reduction efforts in non-outage

periods during 1997 were very good and had resulted in the site'-s lowest

annual collective dose. The 1997 collective dose was 13 person-rem

(Section R1.2).

Overall, as-low-as-reasonably-achievable (ALARA) planning efforts were

appropriate and were effectively implemented for most outage work

activities. Unanticipated problems and poor planning resulted in excess

dose of 13 person-rem for three of the thirty-one planned projects

(Section R1.2).

3

Overall licensee contamination control measures were effective in

containing radioactive byproduct contamination and minimizing radiation

exposures to the contamination (Section R1.3).

Personnel contaminations were down from previous outages. The licensee

was evaluating the events to identify their causes and was taking

corrective actions to reduce the number of personnel contaminations.

The 14 Personnel Contamination Events (PCEs) documented in 1997 were the

site's lowest (Section R1.3).

Licensee use of self assessments in the radiation protection program

area was good (Section R7.1).

Report Details

Summary of Plant Status

Robinson Unit 2 was in Refueling Outage (RFO) 18 at the beginning of the

report period. Plant startup activities were initiated on April 10, 1998 and

the unit entered Mode 1 on April 10. Full power was reached on April 18. On

April 25, the unit experienced an automatic reactor trip from 100 percent

power due to low Steam Generator (SG) level.

The unit was started up on April

26 and returned to full power on April 27. The unit operated at 100 percent

for the remaining portion of the report period.

I. Operations

01

Conduct of Operations

01.1 General Comments (71707)

The inspector conducted frequent control room tours to verify proper

staffing, operator attentiveness and communications, and adherence to

approved procedures. The.inspectors.attended daily operation turnovers,

management reviews, and plan-of-the-day meetings to maintain awareness

of overall plant operations. Operator logs were reviewed to verify

operational safety and compliance with TSs. Instrumentation, computer

indications, and safety.system lineups were periodically reviewed from

the Control Room to assess operability. Frequent plant tours were

conducted to observe equipment status and housekeeping. Condition

Reports (CRs) were routinely reviewed to assure that potential safety

concerns and equipment problems were reported and resolved. Good plant

equipment material conditions and housekeeping continued to be observed

throughout the report period.

In general, the conduct of operations was risk informed, professional,

and safety conscious.

01.2 Refueling Activities

a. Inspection Scope (71707)

The inspector monitored refueling activities during RFO-18, including

those related to the failure of the reactor building side upender

lifting cable.

b. Observations and Findings

Core reload activities were started on March 27, 1998, in accordance

with procedure FHP-006, Fuel Assembly And Insert Handling During Core

Loading, revision 8. Twenty-one assemblies were transferred to the

reactor vessel from the spent fuel pool without incident. On March 28,

at approximately 4:27 a.m., while upending new fuel assembly, AA16, with

the reactor side upender, the lifting cable associated with the upender

failed, while the upender was in the vertical position. The upender and

the transfer basket (with the fuel assembly) pivoted back (gravity fall

2

with water resistance) to the horizontal position on to the fuel

transfer cart. The licensee immediately stopped fuel movement

activities. No change in radiological conditions was noted as monitored

by the area monitors as well as in samples drawn from the cavity water.

The li-censee formed an ERT and initiated condition report CR 98-00736.

The investigation revealed that the shaft that coupled the hoist (motor)

drive to the programmable limit switch (resolver) had sheared. The

hoist/resolver shaft was a two-piece shaft pinned together. The failure

caused the resolver to also fail, resulting in the upender "FRAME-UP"

and "UP OVERTRAVEL" limits to not come in. This resulted in the hoist

continuing to run, pulling the upender cable past its intended position.

The tension on the cable increased as the hoist continued to run beyond

the "UP OVERTRAVEL" limit, causing the #2 sheave/pulley, mounted on the

refueling cavity wall, to be partially pulled off its support plate.

This rotation of the sheave caused the cable to contact the keeper,

which increased the stress on the cable, resulting in the snapping of

the cable. The upender and the transfer cart (with the new fuel

assembly) pivoted back to the horizontal position with 51 inches of the

cable attached. The hoist continued to reel the cable onto the drum.

The ERT was not conclusively able to determine what stopped the motor.

However, the ERT did conclude that a diverse means of stopping the hoist

motor did not function as intended. This means was through a proximity

switch which actuates when a ball mounted on the upender cable comes in

proximity to the switch. This diverse means of stopping the hoist did

not function as the ball was positioned such that it fell short in

actuating the sensing proximity switch. A modification had been

performed in December, 1993 which had replaced the ball and the

associate proximity switch. Post modification testing from this

modification did not adequately demonstrate that the proximity switch

would limit the upper travel of the hoist. Additionally, Engineering

Surveillance Test, EST-030, Fuel Handling Equipment Interlock and

Operation Test, was performed prior to operation of the upender. This

EST includes testing of protective features provided by the resolver and

the proximity switch. However, the correct position of the ball

relative to the proximity sensor was not verified, nor was a functional

test performed for the ball limit stop for the upender. 10 CFR 50:

Appendix B, Design Control requires that measures shall provide for

verifying or checking the adequacy of design. Further, 10 CFR 50, Appendix B, Inspection, Procedures, and Drawings requires that

procedures include appropriate quantitative Or qualitative acceptance

criteria for determining that important activities have been

satisfactorily accomplished. Contrary to these requirements, the post

modification procedure as well as the surveillance procedure associated

with Fuel Handling Equipment did not verify the correct position of the

ball relative to the proximity sensor. This resulted in the proximity

switch not appropriately stopping hoist movement following the failure

of the limit switch. This self identified , corrected, and non

repetitive violation is treated as an NCV, consistent with Section

VII.B.1 of the NRC enforcement policy. This issue is documented as NCV

50-261/98-05-01: Upender Failure during RFO 18.

3

Licensee corrective actions included replacement of the sheared shaft

with a newer design, replacement of the #2 sheave/pulley and cable,

inspection of the spent fuel side hoist/resolver shaft, and

repositioning and functional testing of the proximity sensor to correct

distance from the magnetic ball. The licensee also inspected portions of

the refuel movement apparatus on the spent fuel pool side. The

ball/limit on the spent fuel side did not need any adjustment. The

licensee also has plans to further enhance EST-30 prior to the next

planned use of fuel handling equipment.

Following completion of repair and testing, refueling activities were

commenced and completed without any incidents. A new fuel assembly was

procured as a replacement. Assembly AA16, was transferred back to the

spent fuel pool and current plans are to send it back to the

manufacturer (Siemens).

c. Conclusions

A NCV involving inadequate testing of refueling equipment was

identified. The direct safety consequences of the fuel assembly drop

were none. Had an irradiated assembly been subject to a similar drop,

any release of radioactivity would have been contained, due to

containment closure requirements during fuel movement. Licensee follow

up to this event was appropriate.

01.3 Plant Startup From Refueling

a. Inspection Scope (71707)

The inspector monitored startup activities for RFO-18.

b. Observations and Findings

On April 13, plant startup activities were in.progress in accordance

with procedure GP-003, Normal Plant Startup form Hot Shutdown to

Critical.

At approximately 5:56 a.m., tremors were felt in the plant.

A 3.9 (Richter Scale) seismic event was recorded at a location

approximately 25 miles from the plant. The site seismic recorder did

not register any seismic activity as it was below the trigger value.

The licensee entered Abnormal Operating Procedure 21, Seismic

Disturbances, as a result of the tremor. Startup activities were

suspended and a general inspection of the plant was conducted to

ascertain any consequences. After confirming no effect on the plant,

startup activities were recommenced. The plant reached Mode 2 at 2:10 pm

and Mode 1 at 6:31 pm on April 13. The unit reached 100 percent power on

April 18.

c. Conclusion

The inspector concluded that the management decision to suspend startup

to verify potential effects of the seismic event were conservative. The

4

inspector did not note any affect to the plant as a result of the

seismic event. Operator performance during startup was considered good.

02

Operational Status of Facilities and Equipment

02.1 Reactor Trip and Subsequent Unit Startup

a. Inspection Scope (71707)

Robinson Unit 2 experienced an automatic reactor trip from 100% power on

April 25, 1998 at approximately 1:34 p.m. The resident inspector

responded to the site.

b. Observations and Findings

The first out annunciator was low-low (16%) "A"

Steam Generator (SG)

level. A review of Emergency Response Facility Information System

(ERFIS) data archived after the trip indicated that the initiating event

was the closing of the turbine governor valves. This led to a shrink in

all the SGs caused by reduced steam flow and resultant higher steam

pressure. The shrink was enough to reduce the SG levels to below the

low-low SG level reactor trip set point.

Control room operators initially noticed SG level deviation alarms,

concurrent with control rods inserting rapidly. Reactor Coolant System

(RCS) Tref. as well as first stage impulse pressure were also noted to

be dropping rapidly. The operators' initial diagnosis was that a first

stage pressure channel had failed low. Thus, they reacted by placing

control rods -in

manual.

All four governor valves were then noted shut

and the control room shift supervisor (CRSS) directed manually tripping

the reactor. Just prior to manually tripping the reactor, the reactor

automatically tripped on low-low SG level.

An Event Review Team (ERT) was formed to investigate the reactor trip.

Following extensive troubleshooting, the licensee was not able to

positively identify the root cause. However, during troubleshooting of

the Electro Hydraulic Control (EHC) system, it was revealed that a 35

psi change in impulse pressure output (PT-1359), when the governor

valves are open 90%, will cause the governor valves to close. The

licensee did not identify a cause for the 35 psi change in impulse

pressure nor were they able to confirm that any change in impulse

pressure or PT-1359 had actually occurred. The above scenario was

thought of as the most likely scenario for the unexpected closing of the

governor valves. A Westinghouse representative assisted the licensee in

the troubleshooting process.

Post trip plant response was as expected. A Power Operated Relief Valve

(PORV) opened momentarily to relieve RCS pressure. Reactor operator

response to the initiating event was incorrect. The RO reacted thinking

the turbine first stage pressure channel had failed low. He did not

incorporate the sharp decline in the generated megawatts in his

5

decision. This led him to place the rods in

manual, thus stopping

inward rod motion.

This incorrect response did not have any overall

impact on the plant as the reactor tripped shortly thereafter. However,

the licensee plans to include this scenario during future operator

training activities.

As corrective action, the licensee replaced impulse pressure transmitter

PT-1359. Further, the licensee started and operated the plant in the

"impulse pressure out" Mode. The EHC system was instrumented to capture

any additional anomalies. No anomalies in EHC operation were noted

during start-up and for the remainder of this inspection period.

c.

Conclusion

Reactor operator response to the failed closed turbine overnor valves

was incorrect. Licensee plans to review this event to enhance future

training activities.. Overall plant response was appropriate. Reactor

startup activities following the trip were uneventful.

04

Operator Knowledge and Performance

04.1 Missed Technical Specification Surveillance (61726. 71707)

a. Inspection Scope

The inspector reviewed circumstances related to a missed TS

surveillance. The missed surveillance, OST-014, Local Leak Rate Testing

(LLRT) of Personnel Air Lock Door Seals, placed the unit in TS 3.0.3.

This condition was identified by the control room shift supervisor

(CRSS).

b. Observations and Findings

OST-14 was successfully performed on April 10, 1998, as a prerequisite

for entering Mode 4. OST-14 ensures containment air lock operability

per TS 3.6.2. Further. TS 5.5.16, Containment Leakage Testing Program,

requires implementation of a containment leak rate testing program in

accordance with 10 CFR 50. Appendix J. 10 CFR 50, Appendix J. Section

D.2.ii and iii requires that air locks opened during periods when

containment integrity is required by TS shall be tested within three

days after being opened; and for air lock doors opened more frequently

than once every three days, the air lock shall be tested at least once

every three days during the period of frequent openings.

The unit entered Mode 4 at approximately 8:16 p.m. on April 10. at which

time the operability requirement, for the containment air lock became

effective. Further with the air lock door utilized for personnel

entry/exit, the three day testing requirements were effective in

accordance with 10 CFR 50 Appendix J. The next performance was due to

be performed by 4:45 a.m. on April 13. This was written and tracked on

the white board above the CRSS desk in

the control room.

6

On April 13 at approximately 9:32 -a.m., upon noticing the note on the

white board, a CRSS questioned it. At this time it was recognized that

OST-14 had not been performed as required between April 10 and April 13.

Upon identification, the plant entered TS 3.0.3 and immediately

requested performance of OST-14, which was successfully completed at

11:15 a.m. on April 13.

The licensee initiated CR 98-00890 which concluded that the primary

cause for the missed surveillance was inadequate administrative controls

to ensure event based surveillance requirements. The term "event based"

implies surveillances that are not scheduled through the Surveillance

Tracking System.

As corrective action, the licensee plans to revise OMM-007 to track

similar surveillances in the Equipment Inoperable Record (EIR) logs.

This would allow a positive tracking control, rather than a note on the

board. The inspector will review operator performance in this area to

determine similarity and effectiveness of corrective actions. NCV 97

12-01: Failure to Log TS Surveillance Completion in accordance with OST

20 was reviewed. This NCV was attributed to inattention to detail and

log keeping accuracy on the part of the operator when the control rod.

insertion limit monitor (RILM) was inoperable. NCV 97-12-02: Failure to

Verify Dose Equivalent 1-131 in accordance with GP-005, involved a

missed TS surveillance, also due to lack of operator attention to detail

and inadequate supervisory oversight during periods of high control room

activities. The inspector determined that the recent failure to perform

OST-14 was partially attributable to inattention to detail on the part

of the operating crew. This failure to perform the required

surveillance in accordance with 10 CFR 50, Appendix J is identified as

violation 50-261/98-05-02: Failure to Perform Personnel Air Lock Test.

c. Conclusion

A violation for failure to perform a required surveillance test on the

containment personnel air lock was identified..

07

Quality Assurance In Operations

07.1 Plant Nuclear Safety Committee and Nuclear Assessment Section Oversight

a. Inspection Scope (40500)

The inspector evaluated certain activities of the Plant Nuclear Safety

Committee (PNSC) and Nuclear Assessment Section (NAS) to determine

whether the onsite review functions were conducted in accordance with TS

and other regulatory requirements.

7

b. Observations and Findings

The inspector periodically attended PNSC meetings during the report

period. The presentations were thorough and the presenters readily

responded to all questions. The committee members asked probing

questions and were well prepared. The committee members displayed

understanding of the issues and potential risks. Further, the inspector

reviewed NAS audits and concluded that they were appropriately focused

to identify and enhance safety.

c. Conclusions

The inspector concluded that the onsite review functions of the PNSC

were conducted in accordance with TSs. The PNSC meetings attended by

the inspector were well coordinated and meetings topics were thoroughly

discussed and evaluated. NAS continued to provide strong oversight of

licensee activities.

II.

Maintenance

M1

Conduct of Maintenance

M1.1 General Comments' (62707,61726)

The inspector reviewed/observed all or portions of the following

maintenance and/or surveillances and reviewed the associated

documentation:

OST 401-2, Emergency Diesel Generator Slow Start

OST 402-2, Emergency Diesel Fuel Oil Flow Test

OST 302-1, Service Water System Component Test

Service Water Leak Repair Activities

Maintenance and surveillance activities observed were performed

satisfactorily. The inspector noted good controls of housekeeping and

good supervisor oversight of work activities.

M2

Maintenance and Material Condition of Facilities and Equipment

M2.1 Service Water System Leak Repairs (62707)

a. Inspection Scope

The inspector reviewed and observed licensee actions related to a leak

in the service water (SW) system. The SW system is a safety related

system. The discharge flow to the plant from the four SW pumps is

through two headers, the North and South header. These two headers

constitute the two redundant trains. This leak was in the North header

and was approximated to be 10 gpm.

8

b. Observations and Findings

A leak in the SW system was suspected when a water puddle near the

vicinity of the radwaste system was noted on March 27, 1998. A portion

of the SW header is located underground in the vicinity of the radwaste

Building. The licensee confirmed that the leak was in the SW system by

chlorinating the SW headers and sampling the leaked water. Following

extensive excavation, the licensee located the leak.

The leak was repaired by a welding a "cap assembly" over the section of

the small hole. The welding repair activities were conducted through

ESR 98-00202. The ESR documented the 10 CFR 50.59 evaluation associated

with the repair. The repair was successfully completed in accordance

with ANSI B31.1-1980. The root cause of the leak was determined to be

general corrosion, not particularly attributed to any single mechanism.

c. Conclusions

The repairs on the SW header were appropriately completed. Management

oversight of this problem was considered good.

M4

Maintenance Staff Knowledge and Performance

M4.1 Motor Driven Auxiliary Feedwater Pump 'A'

Trip During Testing (61726.

62707)

a. Inspection Scope

The inspector reviewed circumstances related to the tripping of the "A"

Motor Driven Auxiliary Feedwater Pump (MDAFW) during performance of

Operations Surveillance Test (OST)-163, Safety Injection Test and

Emergency Diesel Generator Autostart on Loss of Power and Safety

Injection.

b. Observations and Findings

During performance of OST-163. both the MDAFW pumps auto started as

designed. The valve configuration during the test precluded flow to the

SG. For the purpose of the test, the manual valves on the discharge

lines were maintained CLOSED.

Approximately 11 minutes into the OST, the "A"

MDAFW pump tripped on low

discharge pressure. Subsequently, the "A"

MDAFW pump was restarted.

Four minutes following the restart, the "A"

MDAFW pump tripped again on

low discharge pressure. OST-163 was continued by adding a component

cooling water pump to provide the compensating electrical load to

complete the OST.

Following completion of the OST, the licensee formed an Event Review

Team (ERT) to determine cause of the "A"

MDAFW pump trip. The ERT noted

that the "A"

MDAFW pump casing temperature was approximately 189 degrees

F one hour after the trip, indicative of liquid flashing to steam within

9

the pump.

During an-initial system walkdown, the system engineer

determined by visual inspection that the recirculation line flow

restriction orifices (RO-1400A and RO-1400B) on the "A"

and "B"

MDAFW

pumps were installed backwards. Although the orifice plates were

reversed, the system engineer did not expect that this was the cause of

the trip, since the flow through the orifice was not changed

significantly by the reverse installation. The insignificant change in

flow was based on the flow orifice design.

The ERT subsequently developed an action plan to determine the nature of

the event, a problem definition, and an investigation process to gather

any other data from the event. During this investigation, the ERT

determined that the during the OST, the "B"

MDAFW pump started first as

designed, since the E-1 bus had to be energized by EDG-A before the A

train sequencer could sequence loads on. The E-2 bus remained on off

site power for this part of the test. The "B"

MDAFW pump developed full

pressure in a few seconds. Since the cross connects were open and the

isolations valves to the steam generators were closed, this pressure

transmitted to the discharge side of the "A"

AFW pump check valve. This

caused the check valve to not open or to partially come off the seat.,

thus reducing flow from the "A"

MDAFW pump. This was further

substantiated by ERFIS data. This data indicated the presence of flow

in the pump discharge headers downstream of the recirculation lines.

This was consistent with flow from the "B"

AFW pump, to the cross

connect header, to the "A"

AFW pump-recirculation line. This

"deadheaded" the "A"

AFW pump resulting in insufficient flow from the

pump.

The ERT concluded that the AFW pump had insufficient flow resulting in

increased temperatures until the liquid in the "A"

MDAFW pump casing

flashed. This resulted in heating of the casing and reduction in

pressure until the pump tripped. The cause of the loss of flow was

concluded to be the effect of deadheading the "A"

MDAFW pump by "B"

AFW

pump pressure, preventing opening of the discharge check valve. The ERT

also concluded that the system was not susceptible to a similar problem

during normal operation and when the MDAFW pumps are required to be

operable because of a different valve configuration. The "A"

MDAFW pump

was externally inspected for any possible damage and none was found.

Further, the vendor was contacted with the data gathered. Per the

vendor recommendations, the pump was successfully started and no changes

in vibration and temperatures were noted. The pump was subsequently

declared operable.

With regard to the restricting orifices installed backwards, the

licensee determined that during RFO-18, the two orifices were

disassembled to perform an inspection. Following the inspection, the

orifices were re-installed backwards. The inspection and installation

activities were conducted under a work request(WR). The WR did not

specify any particular orifice orientation, however, the orifices were

clearly stamped identifying the inlet orientation. This job was

performed by a shared resources maintenance mechanic from the Brunswick

plant. The work was considered within the skill of the craft.

10

Notwithstanding, procedure MMM-001, Maintenance Administration Program,

section 3.1.1 required the craftsmen to restore an area to its design

condition following completion of maintenance activities! Further,

section 2.4.1 of MMM-001 required the mechanic to "THINK" and "APPLY" a

healthy skepticism to review each step of the job before doing to

prevent errors. Contrary to the requirements of MMM-001, absent clear

written instructions, the mechanic did not appropriately conduct the

skill of the craft maintenance activities involving orifice

installation. This resulted in the backward installation of two

orifices on the auxiliary feedwater system. The backward installed

orifices did not negatively impact system performance and thus the

overall significance of the condition was minor. The inspector

determined that failure to follow MMM-001 was a violation. This

licensee identified, corrected, and non-.repetitive violation is treated

as an NCV, consistent with Section VII.B.1 of the NRC enforcement

policy. This issue is documented as NCV 50-261/98-05-03: Backward

Orifice Installation on MDAFW system.

c. Conclusions

The "A"

MDAFW pump was deadheaded during a test configuration. This did

not cause damage to the pump. Licensee actions to determine root cause,

including formation of an ERT, were appropriate. Two orifices on the

MDAFW pump recirculation lines that had been worked on during the outage

were installed backwards due to inattention to detail on part of the

mechanic. This did not contribute to the pump deadheading.

III. Engineering

El

Conduct of Engineering

E1.1 Review of Modifications

a. Inspection Scope (37551)

The inspectors reviewed portions of modifications97-469 and 97-382.

b. Observations and Findings

During Refueling Outage 17 (RFO-17) the Containment Air Recirculation

Cooling system (HVH) unit damper control scheme was changed to have the

normal damper closed and the emergency damper open with no safeguards

signal damper repositioning required post accident. This configuration

reduced the performance of the containment coolers. NRC violation 50

261/97-12-04 was issued regarding the post maintenance testing of this

modification. The licensee's January 21, 1998, violation response

indicated that the pre-RFO-17 configuration would be restored for the

HVH unit dampers. Modification 97-382 was implemented to complete the

restoration. This modification changed the HVH unit damper

configuration to normal damper open and emergency damper open with the

normal damper closing on safeguards signal. The inspector noted that

the modification did not address the impact of the new HVH unit damper

configuration scheme on the HVH unit fan motor current.

Modification 97-469 was an EQ related modification which replaced the

cable to solenoid valve SVA33 for the normal damper of HVH unit HVH-1

with an environmentally qualified cable. The inspectors reviewed the

modification package and verified the package adequately addressed

technical and environmental qualification requirements for the

replacement cable.

The inspectors performed a walkdown and verified

that hardware and equipment were installed in accordance with

modification requirements.

c. Conclusions

Modification packages reviewed were acceptable. Modification 97-382

implemented corrective action.to restore the damper control scheme for

the Containment Recirculation Cooling system units.

E2

Engineering Support of Facilities and Equipment

E2.1 Review of Environmental Qualification Program

a. Inspection Scope (37551)

The inspector performed a walkdown of selected inside containment

Environmental Qualification (EQ) Program components and reviewed several

of the associated EQ Data Packages (EQDPs).

b. Observations and Findings

Selected EQ components were inspected to verify their EQ sealing

requirements were met. Twenty eight transmitters with Patel conduit

seals and twenty one solenoid valves with Patel conduit seals were

inspected. The inspectors determined that the equipment sealing for the

components inspected met-the requirements of TMM-019, List of

Environmentally Qualified Electric Equipment, revision 29, CM-310.

Installation of Patel Conduit Seals, revision 10, and EQDP 21.0, Patel

Conduit Seals. Additionally, eight limit Switches with Namco EC210

conduit seals were inspected. The inspectors determined that the

equipment sealing for the components inspected met the requirements of

TMM-019, List of Environmentally Qualified Electric Equipment, TMM-036.

Environmentally Qualified Electric Equipment Required Maintenance, and

EQDP 25.0, Namco Limit Switches.

12

The following EQDPs were reviewed.

EQDP 3.0 - Rockbestos Cabling

EQDP 21.0 - Patel Conduit Seals

EQDP 11.2 - Kerite Cabling

EQDP 28.0 - Brand Rex Cabling

EQDP 25.0 - Namco Limit Switches

EQDP 40.0 - Ram-Q Cable Connector Assemblies

The inspectors reviewed the Nuclear Records Control System (NRCS)

database to determine all ESRs which were posted against the above

listed EQDPs. All ESRs posted against the listed EQDPs had been

incorporated into the EQDPs except for current RFO-18 open outage ESRs.

No backlog of unincorporated ESRs was noted.

c. Conclusions

The EQ components inside containment which were inspected were being

maintained with qualified seals in accordance with EQ program

requirements. The EQDPs reviewed were being updated in accordance with

procedure EGR-NGGC-156, Environmental Qualification Of Electrical

Equipment Important To Safety. No backlog of unincorporated ESRs was

noted.

E2.2 Westinghouse BF Relays

a., Inspection Scope (37551)

The inspectors reviewed the licensee's activities related to resolution

of Westinghouse BF relay performance discrepancies.

b. Observations and Findings

In January 1997, BF relay 412C1 failed during surveillance testing. The

relay actuated correctly when denergized but experienced a delay during

re-energization. The relay was a normally energized relay used in a

Reactor Protection System (RPS) Overpower/Overtemperature (OP/OT)

Delta T application. Significant Condition Report (CR) 9700092 was

initiated for resolution and root cause evaluation. The relay was sent

to the Harris Energy and Environmental Center (HEEC) for failure

analysis. The analysis concluded that the energization delay was due to

the relay armature pin contacting the internal surface of the relay

casing.

A 1979 vendor technical bulletin documented a problem with BFD (DC)

relays experiencing armature pin binding. No problem was identified

with BF (AC) relays. The vendor evaluation indicated that this was an

isolated case but instituted a relay improvement to epoxy the armature

pin to prevent movement.

Relay 412C1 was one of 46 relays replaced in 1988 due to relay contact

deterioration. The replacement relays did not have epoxy on the

13

armature pin to restrict pin movement. The corrective actions developed

in CR 9700092 consisted of pro-active measures to replace the relays.

During RFO-18 twenty percent of the BF relays in RPS and Safeguards

System were scheduled to be replaced with nuclear qualified relays.

Additionally the licensee will analyze and evaluate the BF relays

removed in RFO-18 and determine if additional BF relay replacements are

necessary.

During BF relay testing during RFO-18, relay TC-432B1-XB failed to go to

the energized position, The relay would denergize and drop out but was

erratic in its pull in times when energized. Upon disassembly, the

armature pin was found binding on the side of the relay internal

surface. This relay was also an OP/OT Delta T relay which had been

replaced in 1988. A significant CR (98-751) was initiated for

resolution. The common factors between the failures in January 1997,

and March 1998, were that both relays were BF relays from the same 1988

procurement and both relays were used in RPS OP/DT Delta T input relay

applications which received more frequent cycling due to more frequent

testing than the other RPS and Safeguards BF relays.

The inspectors reviewed procurement records and verified that the failed

relays were from the same procurement purchase and installed on the same

work orders in 1988. The inspectors reviewed the procurement issue

history and determined that the licensee had relays during 1988 without

epoxy on the armature pin. The licensee developed an action plan for

relay replacement to address relays from the same procurement batch and

those with higher cycling rate and those which were energized to

complete the safety function. Forty one BF relays were scheduled to be

replaced in the RPS and 15 relays in Safeguards System during RFO-18 to

implement the corrective actions of CR 9700092. Based on the second

failure of a BF relay, an additional group of relays was replaced to

address the relays from the 1988 procurement activity. The new

replacement relays were purchased nuclear grade. Samples of the new

relays were inspected and none were noted without the epoxy on the

armature pin.

c. Conclusions

The licensee was conservative in evaluating a BF relay failure during

RFO-18 testing and accelerating relay replacements. The relay testing

discrepancies were being dispositioned in accordance with corrective

action program requirements.

E7.1 Special UFSAR Review (37551)

A recent discovery of a licensee operating their facility in a manner

contrary to the UFSAR description highlighted the need for a special

focused review that compares plant practices, procedures and/or

parameters to the UFSAR descriptions. While performing the inspections

discussed in this report, the inspector reviewed the applicable portions

of the UFSAR related to the areas inspected. The inspector verified

that for the select portions.of the UFSAR reviewed, the UFSAR wording

14

was consistent with the observed plant practices, procedures and/or

parameters.

E8

Miscellaneous Engineering Issues

E8.1

(Open) Unresolved Item 50-261/98-05-05: Questions on Design Calculations

NRC Inspection Report 50-261/98-03, dated February 6, 1998, included an

apparent violation for a number of calculational deficiencies identified

in the NRC Design Inspection. A Notice of Violation was issued on

March 4, 1998, for these calculational deficiencies. The licensee

response of April 3, 1998, to the Notice of Violation, stated that

examples 4,6,12,13, and 14.of violation B and example 1 of violation D

were not violations of NRC requirements. These violation examples are

withdrawn and will be tracked as Unresolved item 50-261/98-05-05,

Questions on Design Calculations, pending further NRC review of the

information provided in the April 3, 1998 violation response.

IV. Plant Support

R1

Radiological Protection and Chemistry Controls

R1.1 Conduct of Radiological Protection Controls (83750)

a. Inspection Scope

Radiological controls associated with RFO-18 were reviewed to verify

that the licensee was effectively implementing the radiation protection

program and meeting 10 CFR Part 20, Standards for Protection Against

Radiation. requirements. In particular, the inspectors reviewed and

evaluated the adequacy of general housekeeping, radiological controls,

area radiological postings, radiation worker compliance with radiation

protection procedures, and controls of radioactive materials.

b. Observations and Findings

Overall, the inspector noted appropriate levels of housekeeping and

cleanliness within the observed work areas and radioactive material

storage areas. Housekeeping practices within the Containment Building

(CB) were considered acceptable. However, the inspector did find loose

debris and standing water on portions of the first floor of the CB.

The inspector made independent radiation surveys of areas, equipment,

and containers within the Radiation Control Area (RCA). The licensee's

radiation survey results compared well with the inspector's surveys.

Licensee radiological area postings met posting requirements for the

areas surveyed by the inspector and were consistent. Vacuum cleaners,

portable air filtration systems, and containers of radioactive materials

within the RCA were properly labeled. Observed radiological controls

met licensee and NRC requirements and were good overall.

During the tours within the RCA, the inspector found all portable

radiation survey meters and air sampling equipment in use possessed

valid calibration stickers. Radiation and contamination monitoring

equipment had recent response checks.

The inspector observed radiation workers performing various tasks in the

Unit 2 CB, Fuel Building, ReactorAuxiliary Building and yard areas

wi.thin the primary RCA. The inspector discussed radiological work

controls with Health Physics (HP) staff. Radiological controls for the

various tasks were appropriate for the radiological conditions.

Observed radiation worker and HP interactions were good.

On March 14, 1998, an employee working in the CB failed to immediately

exit a radiation area when his Electronic Personal Dosimeter (EPD)

alarmed. The EPD was designed to give an audible alarm for the user

when either a dose rate was too high or a predetermined dose limit was

reached. The worker's dosimeter was set to alarm at a dose rate of 200

mrem/hr and a dose of 100 mrem. The alarm showed the worker had

exceeded an authorized radiation dose for the job he was working. After

the EPD alarmed, the worker remained in the radiation area approximately

10 additional minutes to complete his assigned task with his dosimetry

in continuous alarm. The worker exceeded the authorized dose for the

job by approximately ten mrem. While the employee's actions did not

result in exceeding any regulatory limits, the employee failed to follow

guidance provided in the licensee's radiation protection training and

procedures. Specifically, the incident was a violation of paragraph 12

of Attachment 3 to licensee procedure DOS-NGGC-0016, Electronic Personal

Dosimeter System Operation, Rev 2. As stated in the licensee's

procedures, upon activation of the dose alarm workers should exit the

area immediately and report to radiation control.

The licensee documented the event as a significant condition in CR 98

00572. The licensee investigated and took immediate corrective actions.

Corrective actions to prevent recurrence were also made. The inspectors

found the licensee's corrective measures were.very good. This non

repetitive, licensee-identified, and corrected violation is being

treated as a Non-Cited Violation (NCV), consistent with Section VII.B.1

of the NRC Enforcement Policy. NCV 50-261/98-05-04, Radiation Worker's

Failure to Comply with Radiation Protection Procedures

c. Conclusions

Housekeeping and cleanliness within the RCA were acceptable.

Overall, the inspector observed good radiological controls and radiation

worker compliance with those controls throughout the inspection.

A Non-Cited Violation was identified for radiation worker's failure to

comply with radiation protection procedures.

16

R1.2 As Low As Reasonability Achievable (ALARA)(83750)

a. Inspection Scope

.The licensee's goals, plans, and implementation of the site ALARA

program was reviewed.

b. Observations and Findings

The 1997 collective dose goal was established at 22 person-rem. That

goal included a contingency exposure budget of 3.619 person-rem.

However, the licensee did not need the contingency as the plant was

operational for approximately 360 days in 1997. The licensee ended 1997

with an annual collective dose of approximately 13 person-rem. That was

the lowest annual exposure ever at the H. B. Robinson site. The 1997

annual collective dose was also the lowest for any Carolina Power and

Light (CP&L) nuclear facility. The licensee attributed the record to

detailed planning, ALARA culture, excellent operational performance, and

good plant chemistry.

Annual and RFO collective dose goals for 1998 were set at 165 and 155

person-rem respectively. When the inspection began, most of the outage

work had been completed and the licensee was approximately 10 person-rem

above the dose the licensee had projected for that day in the outage.

The inspectors reviewed the status of jobs resulting in significant

collective radiation exposures. Most tasks were being completed with

collective doses well within budget. However, three tasks had

significantly contributed to the increased collective dose. The

licensee had not planned to repair a main flange gasket on the "C"

reactor coolant pump that resulted in approximately eight person-rem.

Actual person-hours for sludge lancing and Steam Generator (SG) eddy

current activities were approximately three and two times projected

hours for those projects respectively. As a result, sludge lancing

exceeded the projected dose of eight person-rem by eight person-rem and

the eddy current projected dose of 6.6 person.-rem was exceeded by

approximately 2.4 person-rem. A new vendor was used for the sludge

lancing activities with unanticipated work and poor planning

contributing to the dose over run. Steam generators were empty longer

than expected and higher dose rates adversely affected the eddy current

project. Through the end of inspection, the licensee had closed the gap

between the actual and projected outage dose.' Outage collective doses

were approximately two person-rem above the projected dose.

The licensee continued to improve the process for accurately assigning

doses to very specific tasks. The licensee began the process of

assigning dose to specific work request and job orders in 1996 and was

continuing to improve its use. The process had not been fully

implemented and the implementation progress had been slow. The process

when fully carried out could be a valuable tool for the ALARA and plant

management staffs. With full implementation the licensee would have

0

more accurate time and dose information for planning activities.

17

Management support of the ALARA program was evidenced in the increased

staffing levels of the outage ALARA group, increased use of remote

monitoring equipment, visibility of ALARA goals, application of shutdown

chemistry controls, and activities of the Robinson ALARA Committee.

c. Conclusions

The effectiveness of the licensee's dose reduction efforts in non-outage

periods during 1997 were very good and had resulted in the site's lowest

annual collective dose. The 1997 collective dose was 13 person-rem.

Overall, ALARA planning efforts were appropriate and were effectively

implemented for most outage work activities. Unanticipated problems and

poor planning resulted in excess dose of 13 person-rem for three of the

thirty-one planned projects.

R1.3 Personnel Contamination Controls (83750)

a. Inspection Scope

Work activities in the licensee contaminated areas were observed by the

inspectors to verify the licensee was implementing appropriate personnel

contamination controls. Personnel contamination reports were reviewed

to determine the frequency of Personnel Contamination Events (PCEs) and

the adequacy of the licensee's response to the events.

b. Observations and Findings

Good contamination control measures were observed during the inspection.

Inspectors found the contamination controls appropriate for the .

contamination levels and the work being performed. Radiation workers

were properly wearing anti-contamination clothing as specified on

Radiation Work Permits (RWPs). Good use of containments and engineering

controls to reduce transport of radioactive contamination were also

observed.

The licensee documented PCEs for all contaminations having radioactivity

greater than 100 corrected counts per minute. The number of.PCEs

documented by the licensee in 1994, 1995, 1996. and 1997 were 54, 129,

207, and 14 respectively. The frequency of PCEs increased during outage

periods. The PCE goal for 1997 was 50.

Plant operability was very good

in 1997 and there were only a few outage days. The fourteen PCEs for

were the lowest in the site's history.

The annual and RFO goals for

1998 were 90 and 70 respectively. As of April 2, 1998. the numbers of

PCEs documented were 60 and 53.

The inspectors found the Environmental and Radiation Control.(E&RC)

Manager was reviewing all PCEs and had sorted and characterized the PCEs

looking for trends and causes.

Inspectors also reviewed the PCE reports

and found approximately half involved discrete radioactive particles.

The inspectors determined the licensee had taken measures to control the

dispersion of the particles.

No other PCE cause categories were

18

distinguishing. The radioactivity of the particles were all low and

only a few had resulted in skin doses.

c. Conclusions

Overall licensee contamination control measures were effective in

containing radioactive byproduct contamination and minimizing radiation

exposures to the contamination.

Personnel contaminations were down from previous outages. The licensee

evaluated the events to identify their causes and was took corrective

actions to reduce the number of personnel contaminations.

The number

of PCE's documented in 1997 were the site's lowest.

R7

Quality Assurance in RPC Activities

R7.1 Radiological Protection Program Self Assessments (83750)

a. Inspection Scope

Self Assessments of the radiation protection program.were reviewed to

verify the licensee-was identifying and correcting radiation protection

program problems.

b. Observations and Findings

The inspectors reviewed several self assessments of various radiation

protection programs completed in 1997. The inspectors found the .

licensee's self assessments of radiation protection programs were

critical and findings were being identified. All findings were

documented in a corrective action program and the staff was doing a good

job of tracking and trending problems identified in the process.

c. Conclusions

Licensee use of self assessments in the radiation protection program

area was good.

S1 -

Conduct of Security and Safeguards Activities

S1.1 General Comments (71750)

During the period, the inspector toured the protected area and noted

that the perimeter fence was intact and not compromised by erosion or

disrepair. Isolation zones were maintained on both sides of the barrier

and were free of objects which could shield or conceal an individual.

The inspector periodically observed personnel, packages, and vehicles

entering the protected area and verified that necessary searches,

visitor escorting, and special purpose detectors were used as applicable

prior to entry. Lighting of the perimeter and of the protected area was

acceptable and met illumination requirements:

19

V. Management Meetings

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee

management at the conclusion of the inspection on May 19, 1998. No

proprietary information was identified.

20

PARTIAL LIST OF PERSONS CONTACTED

Licensee

J. Boska, Manager, Operations

H. Chernoff, Supervisor, Licensing/Regulatory Programs

T. Cleary, Manager, Maintenance

J. Clements, Manager, Site Support Services

J. Keenan, Vice President, Robinson Nuclear Plant

R. Duncan, Manager, Robinson EngineeringSupport Services

R. Moore, Manager, Outage Management

J. Moyer, Manager, Robinson Plant

D. Stoddard, Manager, Operating Experience Assessment

R. Warden, Manager, Nuclear Assessment Section

T. Wilkerson, Manager, Regulatory Affairs

D. Young, Director, Site Operations

NRC

B. Desai, Senior Resident Inspector

M. Ernstes, Acting Branch Chief, Region II

21

INSPECTION PROCEDURES USED

IP 37551:

Onsite Engineering

IP 40500:

Effectiveness of Licensee Controls in Identifying, Resolving, and

Preventing Problems

IP 61726:

Surveillance Observations

IP 62707:

Maintenance Observation

IP 71707:

Plant Operations

IP 71750:

Plant Support Activities

IP 83750:

Occupational Radiation Exposure used

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

Type Item Number

Status

Description and Reference

NCV

98-05-01

Open

Upender Failure during RFO 18 (Section

01.2).

VIO

98-05-02

Open

Failure to Perform Personnel Air Lock

(Section 04.1).

NCV

98-05-03

Open

Backward Orifice Installation on MDAFW

system (Section M4.1).

NCV

98-05-04

Open

Radiation Worker's Failure to Comply with

Radiation Protection Procedures

(Section R1.1)

URI

98-05-05

Open

Questions on Design Calculations (Section

E8.1)

Closed

Ixpe Item Number

Status

Descri tion and Reference

NCV

98-05-01

Closed

Upender Failure during RFO 18 (Section

01.2).

NCV

98-05-03

Closed

Backward Orifice Installation on MDAFW

system (Section M4.1).

NCV

98-05-04

Closed

Radiation Worker's Failure to Comply with

Radiation Protection Procedures

(Section R1.1)