ML14181A959

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Insp Rept 50-261/97-10 on 970831-1011.Violations Noted But Not Cited & Being Considered for Escalated Enforcement Action.Major Areas Inspected:Operations,Maintenance, Engineering & Plant Support
ML14181A959
Person / Time
Site: Robinson 
Issue date: 11/07/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14181A958 List:
References
50-261-97-10, NUDOCS 9711190135
Download: ML14181A959 (22)


See also: IR 05000261/1997010

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:

50-261

License Nos:

DPR-23

Report No:

50-261/97-10

Licensee:

Carolina Power & Light (CP&L)

Facility:

H. B. Robinson Unit 2

Location:

3581 West Entrance Road

Hartsville, SC 29550

Dates:

August 31 - October 11, 1997

Inspectors:

B. Desai, Senior Resident Inspector

J. Zeiler, Resident Inspector

Approved by:

M. Shymlock, Chief, Projects Branch 4

Division of Reactor.Projects

9711190135 971107

PDR

ADOCK 05000261

0

PDR

EXECUTIVE SUMMARY

H. B. Robinson Power Plant, Unit 2

NRC Inspection Report 50-261/97-10

This integrated inspection included aspects of licensee operations,

maintenance, engineering, and plant support. The report covers a six-week

period of resident inspection.

Operations

The conduct of operations was professional and safety-conscious

(Section 01.1).

Overall, control room operator logs were appropriately maintained;

however, one instance was noted where the status of a seismic monitor

was not appropriately logged. The safety significance of this was

minimal (Section 01.2).

Licensee actions following the receipt of Loose Part Monitoring System

(LPMS) alarms on Steam Generator A were responsive, thorough, and

indicative of strong management attention. Although the source of the

LPMS noise had not been positively identified by the end of the report

period, licensee troubleshooting plans were detailed and exhaustive.

Inconsistencies were identified in the licensee's implementation of

Regulatory Guide testing commitments and vendor recommended maintenance

related to the LPMS. An Unresolved Item (URI) was identified to

complete the review of these issues (Section 01.3).

A walkdown of the electrical distribution system did not result in any

significant problems being identified. A walkdown of the Control Room

Ventilation System revealed that the system was being operated in

accordance with system lineup procedures and the description in the

Updated Final Safety Analysis Report (UFSAR). The system was being

properly maintained for system readiness to perform its safety function

and Technical Specification (TS) surveillance requirements were met

(Section 02.1 and 02.2).

The onsite review functions of the Plant Nuclear Safety Committee (PNSC)

were conducted in accordance with TSs. PNSC meetings continued to be

well coordinated and meetings topics were thoroughly discussed and

evaluated. Likewise, the Nuclear Assessment Section (NAS) continued to

provide strong oversight of licensee activities. A negative observation

was identified associated with an error in classifying the significance

level of a Condition Report involving an issue that was reported to the

NRC under 10 CFR 50.72. This resulted in the NRC reportable event not

being reviewed by the PNSC and NAS. This error was considered to be an

isolated incident and had no safety consequence (Section 07.1).

An apparent violation was identified for the licensee's failure to

implement adequate configuration controls for positioning the Emergency

Diesel Generator (EDG) output breaker control switch. Associated with

this same incident, an apparent violation was identified for the failure

to identify and correct the mispositioned B EDG output breaker control

2

switch prior to identification by the NRC. This mispositioning issue

was originally identified as an URI in NRC Inspection Report 50-261/

97-09 (Section 08.1).

Maintenance

Observed maintenance and surveillance activities were performed

satisfactorily (Section M1.1).

The licensee's process for incorporating Probabilistic Safety Assessment

and Probabilistic Risk Assessment information in the planning of online

maintenance activities was considered a strength (Section M1.2).

Engineering

A spent fuel pool anti-siphon modification was properly implemented,

including the 10 CFR 50.59 evaluation, UFSAR updates, and post

modification testing. This modification further enhances plant safety,

in that, it eliminated the potential for a siphon induced draindown of

the spent fuel pool (Section E1.1).

Licensee management asked probing questions during maintenance rule

system review meetings that were recently initiated. The reviews

sensitized appropriate managers to the problems related to the discussed

systems. The overall impact of this initiative should result in better

focus and management of problems related to plant systems (Section

E2.1).

The licensee's actions upon discovery of a Unreviewed Safety Question

(USQ) associated with certain spent fuel shipping activities were

appropriate. The failure to meet 10 CFR 50.59 requirements for

performing a change involving a USQ without prior NRC approval was

identified as an Apparent Violation of 10 CFR 50.59. As described in

the cover letter to this report, this apparent violation will be

reviewed by NRC management and addressed in a separate correspondence

(Section E2.2).

The failure to provide adequate design controls related to alterations

and repairs to the Emergency Core Cooling System recirculation sump

screens was identified as a Non-Cited Violation of 10 CFR 50, Appendix

B. Criterion III, Design Control. This issue was originally identified

as a URI in NRC Inspection Report 50-261/96-12 (Section E8.1).

Plant Support

The licensee's corrective actions for problems related to personnel

entering the Radiation Control Area without appropriate monitoring was

considered aggressive (Section R1.2).

The licensee's efforts to provide the security force with an upgraded

firing range training facility was indicative of good management support

to further enhance security personnel performance (Section S1.2).

Report Details

Summary of Plant Status

Robinson Unit 2 operated at full power for the entire report period with the

following exception. On September 6-7, power was reduced to approximately 65

percent to conduct testing of the turbine control valves.

I. Operations

01

Conduct of Operations

01.1 General Comments (71707)

The inspectors conducted frequent control room tours to verify proper

staffing, operator attentiveness and communications, and adherence to

approved procedures. The inspectors attended daily operation turnovers,

management reviews, and plan-of-the-day meetings to maintain awareness

of overall plant operations. Operator logs were reviewed to verify

operational safety and compliance with Technical Specifications (TSs).

Instrumentation, computer indications, and safety system lineups were

periodically reviewed from the Control Room to assess operability.

Frequent plant tours were conducted to observe equipment status and

housekeeping. Condition Reports (CRs) were routinely reviewed to assure

that potential safety concerns and equipment problems were reported and

resolved.

In general, the conduct of operations was professional and safety

conscious. Good plant equipment material conditions and housekeeping

continued to be observed throughout the report period.

01.2 Control Room Logging

a. Inspection Scope (71707)

The inspector reviewed control room logs, as well as other control room

documents to ascertain whether plant conditions, TS action statements,

equipment out-of-service. etc.. were appropriately documented.

b. Observations and Findings

The inspector noted that, overall, the detail and quality of control

room logs was good. However, the inspector did identify one instance

where a seismic monitor was still carried as being out-of-service when

it had actually been successfully returned to operable status, including

completion of required tests. Upon pointing this out to the operator,

the operator immediately rectified the documentation.

c. Conclusions

The inspector concluded that the overall control room logs were

appropriately maintained; however, one instance was noted where the

status of a seismic monitor was not appropriately logged. The safety

significance of this logging error was minimal.

2

01.3 -Potential Loose Part Evaluation for Steam Generator A

a. Inspection Scope (71707)

The inspector reviewed licensee activities associated with an evaluation

of a potential loose part in Steam Generator (SG) A.following alarms on

the Loose Parts Monitoring System (LPMS). The inspector reviewed the

LPMS vendor manual, operating and maintenance procedures, UFSAR Section

1.8, and Regulatory Guide (RG) 1.133, Loose Parts Detection Program for

the Primary System of Light Water Cooled Reactors.

b. Observations and Findings

On September 23, 1997, the licensee initiated an evaluation for a

potential loose part in SG A following the receipt of alarms on LPMS

channel 755. Channel 755 is associated with loose parts monitoring of

the secondary side of SG A. During normal operation, the LPMS is

configured to monitor the primary side channels for' each SG. LPMS

Channel 754 monitors noise on the primary side of SG A. Up until

September 23, channel 754 had been selected for automatic loose parts

monitoring of SG A, and although a slight increase in the number of

impact events below the alarm setpoint had been noticed, no alarms had

been received on channel 754.

Between September 23 and 25, 1997, the licensee worked with Westinghouse

Corporation in analyzing the LPMS output data from channels 755 and 754.

The results of this evaluation were documented in Westinghouse letter

dated September 25, 1997. Westinghouse determined that the source of

the impact events was not in the SG tube sheet region, and was most

likely, outside of the generator. The licensee's subsequent

troubleshooting and investigations narrowed the source of the noise to

be somewhere between the upper region of the generator to 50 feet

upstream of the feedwater inlet line from the generator. The inspector

noted that investigation efforts were well planned and exhaustive. At

the end of the report period, licensee investigations into the source of

the noise were still ongoing. The inspector determined that the

licensee had adequately evaluated the potential for a loose part in

SG A.

The inspector reviewed Operating Procedure (OP)-007, Loose Parts

Monitoring System, the Digital Metal Impact Monitoring System Vendor

Manual (CP&L Part No. 728-564-04), RG 1.133. and UFSAR Section 1.8

related to the licensee's conformance to RG 1.133. UFSAR Section 1.8

indicated that the LPMS at Robinson conformed to RG 1.133, revision 1,

dated May 1981, with the exception of sections C.1.g and C.1.h. Based

on a review of OP-007, the inspector determined that for the most part,

the licensee had implemented a loose part detection program in

accordance with RG 1.133. However, the inspector identified several

areas that did not appear to meet the RG 1.133 commitments related to

LPMS testing. Specifically, RG 1.133 Section C.3 required the

performance of a 31-day channel functional tests and 92-day background

noise and channel false signal checks. Based on review of OP-007, the

3

inspector was unable to verify whether these tests were being

accomplished. However, the LPMS vendor manual described certain tests

that the system hardware conducts automatically. At the end of the

report period, the inspector had been unable to positively confirm

whether all of the above RG 1.133 testing was included in the automatic

test features. The inspector determined that further review of the LPMS

system was necessary to conclude whether all RG 1.133 test commitments

were being conducted.

Also, the inspector noted that OP-007 only required an audible check of

the LPMS channels that were not selected for automatic monitoring.

These non-selected channels included the secondary side of the SGs,

including channel 755 for SG A. Had more than just audible checks been

performed, the licensee may have identified the change in channel 755

noise earlier.

The inspector also noted that the vendor manual recommended that the

LPMS backup battery be replaced every 6-months, however, the licensee

was replacing the battery at 18-month intervals. At the end of the

report period, the inspector was still reviewing with the licensee the

impact of the increased battery replacement schedule.

The licensee initiated a CR to review the above mentioned testing and

maintenance issues, as well as their verification of commitments

associated with RG 1.133. Pending completion of the licensee's review

of these items and subsequent review by the NRC, these issues were

identified as Unresolved Item (URI) 50-261/97-10-01: Complete Review of

LPMS Testing and Maintenance Activities.

c. Conclusions

The inspector concluded that licensee actions following the receipt of

LPMS alarms on SG A were responsive, thorough, and indicative of strong

management attention. Although the source of the LPMS noise had not

been positively identified by the end of the report period, licensee

troubleshooting plans were detailed and exhaustive. The inspector

identified weaknesses in the licensee's implementation of Regulatory

Guide LPMS testing commitments and vendor recommended LPMS maintenance.

An URI was identified to complete the review of these items.

02

Operational Status of Facilities and Equipment

02.1 Walkdown of Electrical Distribution System

a. Inspection Scope (71707)

The inspector performed a walkdown of portions of the electrical

distribution system.

4

b. Observations and Findings

The inspector verified the electrical distribution system was aligned in

accordance with OP-603, Electrical Distribution System Lineup. The as

built configuration was compared with the description of the electrical

system in Chapter 8 of the UFSAR. The inspector did not identify any

configuration or housekeeping issues. The inspector did note that the

labeling on the Motor Control Center panels for each breaker indicated

ON or OFF whereas OP-603 described breaker positions as Closed or Open.

This comment was passed on to the licensee.

c. Conclusions

The inspector did not identify any significant problems during the

walkdown of portions of the electrical distribution system..

02.2 Walkdown of Control Room Ventilation System

a. Inspection Scope (71707)

The inspector performed a walkdown of accessible, safety-related

portions of the Control Room Ventilation System (CRVS). The actual

plant configuration was compared with plant drawings, system lineup

procedures, as well as the UFSAR system description and drawings.

Additionally, completed surveillance test procedures and the status of

outstanding maintenance associated with the CRVS were reviewed.

b. Observations and Findings

The inspector verified that the actual plant configuration and operation

of the CRVS was consistent with the plant flow diagram G-190304,

Revision 5, operations lineup procedure OP-906, and the UFSAR Chapter

9.4 description and diagram. No discrepancies were identified from this

review.

The inspector verified that TS 4.15 surveillance requirements associated

with the CRVS were being performed as required via review of various

test procedures. These procedures included the following:

Operations Surveillance Test (OST)-750-1, Control Room Emergency

Ventilation System Train A (Monthly), Revision 6,

OST-750-2, Control Room Emergency Ventilation System Train B

(Monthly), Revision 6,

Engineering Surveillance Test (EST)-023, Control Room Emergency

Ventilation System (18 Month). Revision 13.

Additionally, the inspector reviewed the last completed performance of

the above procedures to verify that performance acceptance criteria were

met and the surveillances were performed at the proper frequency. No

discrepancies were identified from these reviews.

5

The inspector reviewed all open work items associated with the CRVS.

The inspector did not identify any outstanding work that could impact

the readiness of the system to properly perform its function.

c. Conclusions

The inspector concluded that the CRVS was being operated in accordance

with system lineup and system description in the UFSAR, was being tested

in accordance with TS surveillance requirements, and, was being properly

maintained for system readiness to perform its safety function.

07

Quality Assurance In Operations

07.1 Plant Nuclear Safety Committee and Nuclear Assessment Section Oversight

a. Inspection Scope (40500)

The inspector evaluated certain activities of the Plant Nuclear Safety

Committee (PNSC) and Nuclear Assessment Section (NAS) to determine

whether the onsite review functions were conducted in accordance with TS

and other regulatory requirements.

b. Observations and Findings

The inspector periodically attended PNSC meetings during the report

period. The presentations were thorough and the presenters readily

responded to all questions. The committee members asked probing

questions and were well prepared. The committee members displayed

understanding of the issues and potential risks. Further, the inspector

reviewed NAS audits and concluded that they were appropriately focused

to identify and enhance safety.

The inspector reviewed the implementation of PNSC and NAS activities

related to the requirements of TS 6.6.1.a. This TS required the PNSC to

review all NRC reportable events (i.e., 10 CFR 50.72 and 50.73) and

submit the event to the NAS Manager. The .inspector reviewed reportable

events initiated by the licensee in 1996 and 1997. With one exception,

the inspector determined that the PNSC and NAS reviews were completed as

required. The exception involved the licensee's NRC 10 CFR 50.72

notification on August 12, 1996., related to a "courtesy" offsite

notification that had been made to the South Carolina Department of

Health and Environmental Control concerning potential leakage from a

diesel fuel oil storage tank. This issue was documented by the licensee

in CR 96-1803. The CR was not reviewed by the PNSC and NAS due to the

CR evaluator classifying the CR as a Level 3, Non-Significant issue.

This CR should have been classified as Level 1, Significant. All CRs

classified as significant are automatically reviewed by the PNSC and

NAS. The licensee initiated a CR to address the error and on

October 13, 1997. the PNSC reviewed CR 96-1803 as part of a regularly

scheduled meeting. The inspector concluded that the licensee's program

for PNSC and NAS review of NRC reportable events was properly

6

implemented and the discrepancy with CR 96-1803 was an isolated.case of

an error in CR classification and had no safety consequence.

c. Conclusions

The inspector concluded that the onsite review functions of the PNSC

were conducted in accordance with TSs. The PNSC meetings attended by

the inspector were well coordinated and meetings topics were thoroughly

discussed and evaluated. NAS continued to provide strong oversight of

licensee activities. A negative observation was identified associated

with an error in classifying the significance level of a CR involving an

NRC reportable event. This resulted in the event not being reviewed by

the PNSC and NAS. This error was considered to be an isolated incident.

08

Miscellaneous Operations Issues (92901)

08.1 (Closed) URI 50-261/97-09-01, Review Licensee Evaluation of EDG Output

Breaker Control Switch Mispositioning: This URI involved the

inspector's identification of the B Emergency Diesel Generator (EDG)

output breaker control switch in the partial PULL-OUT (i.e., pull-to

lock) position rather than the NEUTRAL (i.e., normal) position on

August 20, 1997. The licensee later determined that, with the switch in

this position, the B EDG output breaker would have immediately reopened

following closure, in the event of an EDG start and undervoltage

condition on the E-2 Emergency Bus. As a result, the B EDG was

incapable of automatically energizing the E-2 Emergency Bus, and was

therefore, inoperable.

During this report period, the inspector reviewed the results of the

licensee's Event Review Team that was assembled to investigate the

circumstances related to the cause of the switch mispositioning. The

results of this investigation were documented in CR 97-01754 and

Licensee Event Report (LER) 50-261/97-10-00, dated September 12, 1997.

The licensee was unable to identify the exact time and circumstance

related to the output breaker control switch mispositioning. Several

scenarios that could have resulted in the mispositioning were examined

in detail.

These scenarios included the following: (1)

the switch was

over-rotated past the TRIP position when the output breaker was manually

tripped during the July 28, 1997, routine EDG surveillance test, (2)

the

switch was inadvertently manipulated, i.e.. bumped, and (3)

the switch

was intentionally mispositioned. The results of licensee's

investigations determined that, most likely. the switch was

inadvertently bumped sometime after 4:12 p.m. on August 16, 1997.

However, no specific activity could be identified that might have

resulted in the actual mispositioning.

As a result of the licensee's interviews with personnel that had

recently been in the EDG room, a Shift Superintendent of Operations

(SSO) recalled observing that the switch was in its proper position on

August 16 during a routine walkdown in the Auxiliary Building. Security

logs for that day confirmed that the individual had last exited the

Auxiliary Building at 4:12 p.m. The licensee believed that the switch

.7

was mispositioned sometime after 4:12 p.m. on August 16, 1997. Based on

this, the licensee concluded that the B EDG was potentially inoperable

from 4:12 p.m. on August 16, 1997 until the output breaker control

switch was returned to its normal position at 3:44 p.m. on August 20,

1997.

While the exact root cause of this switch mispositioning could not be

determined, the Event Review Team identified several weaknesses in the

physical and administrative barriers that could have either prevented

the switch mispositioning or alerted personnel earlier to the

mispositioning. These weaknesses included the following: 1) the proper

switch position was not being verified periodically during routine

operator rounds nor after switch manipulations following the quarterly

EDG surveillance test; 2) protective covers were not installed to

prevent the inadvertent bumping of the switch, even though a similar

mispositioning involving the EDG voltage control knobs had occurred in

1993; and, 3) the EDG control circuitry was not designed with alarms or

indications that would have alerted personnel that the switch had been

mispositioned.

The licensee's planned corrective actions included the

installation of protective covers on both EDG generator control panels

to prevent the switches from being bumped in the future. In addition,

caution tags were placed on both switches until operating lineup and

testing procedures were revised to include verifications of the proper

switch position, both periodically and after manipulation during the

quarterly EDG test.

The licensee completed a safety review that considered the B EDG

inoperable from 4:12 p.m. on August 16, 1997 until 3:44 p.m. on

August 20, 1997. During this period, several A train safety'-related

equipment/components were removed from service for maintenance. As

defined by TS 1.3, when a system, subsystem, train, component or device

is determined to be inoperable solely because its emergency power source

is inoperable, or solely because it normal power source is inoperable,

it may be considered operable provided its.emergency power source is

operable and all of its redundant systems, subsystems, trains,

components and devices are operable. Based on this definition of

operability, while the A train equipment was out of service for

maintenance, concurrent with the inoperability of the B train emergency

power, the A train equipment was considered inoperable. Therefore, this

condition resulted in both trains of equipment being inoperable due to

the equipment's opposite train emergency power source being inoperable.

The A train equipment removed from service and its associated risk

significance included the following:

A Train Engineered Safety Features Actuation System (ESFAS):

Between 7:51 p.m. and 9:17 p.m. on August 17, 1997, A train ESFAS

testing was conducted. When each individual A train ESFAS logic

function was momentarily placed in test, this resulted in both ESF

trains being inoperable since the emergency power source for. B

train was inoperable. However, both trains of ESFAS would have

still operated properly since it is powered from the A and B train

125 Volt DC vital batteries which remained operable during the

8

timeframe. Therefore, the risk significance of this condition was

minimal since there was no actual loss of ESFAS capability.

A Train Vital Battery:

For approximately six minutes, while

swapping from the A-1 Vital Emergency Battery Charger to the A

charger on August 18, 1997, both vital battery chargers were

considered inoperable. The risk significance of this condition

was minimal since both trains of vital batteries were still

operable during this short time period.

Steam Driven Auxiliary Feedwater (SDAFW) Pump:

On August 20,

1997, at 3:44 a.m., the SDAFW pump discharge flow control valve

was cycled to support scheduled surveillance testing. During this

short period (i.e., two minutes), the SDAFW pump was inoperable,

concurrent with the inoperability of the B Motor Driven AFW

(MDAFW) pump due to its emergency power supply being unavailable.

The licensee determined that the inoperability of the SDAFW and

one MDAFW resulted in the highest increase in instantaneous core

damage frequency (i.e., from 2E-4 to 1E-3). However, the A train

MDAFW pump remained operable during this period. The risk

significance of this condition was still considered minimal since

one MDAFW pump can supply sufficient feedwater for decay heat

removal during design basis accident conditions.

A Train ECCS Pump Room Cooler:

On August 20, 1997, at 5:30 a.m.,

the A train Safety Injection (SI) and Containment.Spray (CS) pumps

were declared inoperable by the licensee due to scheduled

maintenance on HVH-6A, the A train SI pump room air cooler. This

maintenance involved replacement of two service water supply

valves to HVH-6A. Since the B train emergency power supply source

was inoperable due to the output breaker control switch

mispositioning, the B train ECCS room cooler, HVH-6B, was also

technically inoperable. This resulted in both trains of SI and CS

being inoperable. On August 20, 1997, at 6:39 p.m., work was

completed on HVH-6A and it was returned to service. The actual

risk significance of this condition while both room coolers were

inoperable was considered to be minimal.

The licensee had

previously calculated that all safety-related equipment, including

the SI and CS pumps in the ECCS pump room, could still perform

their design function without HVH-6A and HVH-6B in operation. In

addition, work on HVH-6A could have been expedited to return it to

service sooner if this had been necessary.

The inspector determined that between 5:30 a.m. and 3:44 p.m. on

August 20, 1997, the plant had been in the action requirement of TS 3.0

as a result of having both the A and B train SI and CS pumps inoperable.

TS 3.0 required that the plant be placed in Hot Shutdown within eight

hours. This required the licensee to have placed the plant in Hot

Shutdown by 1:30 p.m. on August 20, 1997. Since the B EDG was not

returned to service until 3:44 p.m., the allowable TS 3.0 time to Hot

Shutdown was exceeded.

9

10 CFR 50, Appendix B, Criterion II, "Quality Assurance Program,"

requires., in part, that the quality assurance program shall provide

control over activities affecting the quality of systems and components,

to an extent consistent with their importance to safety.

The licensee's quality assurance program did not provide controls over

activities affecting the quality of systems and components, to an extent

consistent with their importance to safety. Specifically, the licensee

failed to assure adequate configuration control of the position of the B

EDG output breaker control switch. This resulted in the inoperability

of the EDG from potentially August 16 until August 20, 1997, due to the

inadvertent mispositioning of the switch. Controls for ensuring that

the switch could not be inadvertently "bumped" were not implemented,

e.g., switch protection covers, etc. Existing procedures did not

require verifications that the switch was in its correct position

following switch manipulations for quarterly EDG testing, nor

periodically during routine operator walkdowns. Additionally, the EDG

control system was not designed with positive controls, e.g., alarms, to

indicate that the switch was not in its correct position.

This issue is identified as an apparent violation of 10 CFR 50, Appendix

B, Criterion II. This issue is identified as Escalated Enforcement Item

(EEI) 50-261/97-10-02: Apparent Violation of 10 CFR 50, Appendix B,

Criterion II,

for Mispositioned EDG Switch.

In addition, 10 CFR 50, Appendix B, Criterion XVI, "Corrective Action,"

requires, in part, that measures shall be established to assure that

conditions adverse to quality, such as failures, malfunctions,

deficiencies, deviations, defective material and equipment, and

nonconformances are promptly identified and corrected.

As of August 20, 1997, the licensee did not establish measures to assure

that conditions adverse to quality were promptly identified and

corrected. Specifically, the licensee failed to identify and correct

that the B EDG output breaker control switch was mispositioned from

potentially August 16, 1997, when the switch was last observed by an SSO

to be in its correct position, until August 20, 1997, when the switch

was found mispositioned by the inspector. The licensee's failure to

identify and correct the mispositioned switch prior to identification by

the NRC, is considered to be an Apparent Violation of 10 CFR 50,

Appendix B, Criterion XVI, Corrective Actions. This issue is identified

Criterion XVI, for Mispositioned EDG Switch.

10

II.

Maintenance

M1

Conduct of Maintenance

M1.1 General Comments

a. Inspection Scope (61726 and 62707) (92902)

The inspector reviewed/observed all or portions of the following

maintenance related work requests/job orders (WRs/J~s) and surveillances

and reviewed the associated documentation:

WR/JO AHGX-002

Perform Capacity Test of Station Battery A-i

WR/JO AARL-002

Motor Driven Auxiliary Feedwater System (MDAFW)

Pump Oil Cooler Maintenance

WR/JO 97-AEJUl

HVH-6B Repairs

OST 201-A

MDAFW Component Test - Train A

OST 251-1 and 2 Residual Heat Removal Pump A Component Test

OST 401-2

EDG B Slow Speed Start

OST 402-2

EDG B Diesel Fuel Oil System Flow Test

b. Observations and Findings

The inspector observed that these activities were performed by personnel

who were experienced and knowledgeable of their assigned tasks.

Procedures were present at the work location and being followed.

Procedures provided sufficient detail and guidance for the intended

activities. Activities were properly authorized and coordinated with

operations prior to starting. Test and maintenance equipment in use was

calibrated, procedure prerequisites were met, and system restoration was

completed. The inspector verified that the surveillance tests were

performed within their required frequencies, associated documentation

was found satisfactory, and test results met acceptance criteria

contained in the procedure.

c. Conclusions

The inspector concluded that maintenance and surveillance activities

were performed satisfactorily.

M1.2

Maintenance Planning

a. Inspection Scope (62707)

The inspector reviewed the licensee's process forutilizing

Probabilistic Safety Assessment (PSA) and Probabilistic Risk Assessment

(PRA) information in the scheduling of maintenance activities.

b. Observations and Findings

The inspector reviewed the licensee's process for incorporating PSA/PRA

information into the scheduling of planned, as well as unplanned

activities, including on-line maintenance activities. Plant procedure

(PLP)-056, Work Control Process, implements licensee expectations to

assess the impact on overall plant safety when plant equipment or

combinations of equipment are removed from service for on-line

maintenance. This procedure identifies the risk impact of various

combinations of equipment safety functions that are planned to be

unavailable and provides a risk matrix that recommends what activities

can or cannot be performed from a risk stand point.

Additionally, the inspector reviewed a new initiative by the licensee

that identifies the increase in risk from the base core damage frequency

for planned maintenance in the upcoming two weeks. This information is

presented in a user friendly way and is prominently displayed at various

locations.

c. Conclusions

The inspector concluded that the licensee's process for incorporating

PSA/PRA information in the planning of online maintenance activities was

considered a strength.

III. Engineering

El

Conduct of Engineering

E1.1

Spent Fuel Anti-Siphon Modification

a. Inspection Scope (37551)

The inspector reviewed modification package Engineering Service Request

(ESR) 9700018, Spent Fuel Pool Cooling System (SFPCS) Anti-Siphon

Modification, as well as the field installation of the modification.

b. Observations and Findings

ESR 9700018 was initiated by the licensee to address a concern related

to the existence of a drain line at Robinson that extends to near the

bottom of the SFP, without any passive engineered anti-siphon device.

Two locked closed manual isolation valves provided protection against an

inadvertent draindown. However, in the absence of an engineered

anti-siphon protection, the NRC had expressed concern to the licensee,

including the potential of considering Backfit (NRC to CP&L letter dated

October, 10, 1996). While Robinson was in compliance with its licensing

basis, the lack of an engineered anti-siphon protection did not conform

to current standards.

12

The anti-siphon modification included the installation of a spectacle

flange on the four-inch line between the two closed isolation valves.

The licensee opted for this solution since the majority of the drain

line was embedded in concrete, thus disallowing the installation for a

siphon-breaking vent hole on the drain line. In addition to the flange,

the licensee plans to continue to maintain the two isolation valves in

the closed position.

c. Conclusions

The inspector concluded that the modification was appropriately

accomplished, including the 10 CFR 50.59 evaluation, UFSAR updates, and

post modification testing. The installation of this modification

further enhanced plant safety by eliminating the potential for a siphon

induced spent fuel pool draindown..

E2

Engineering Support of Facilities and Equipment

E2.1 Maintenance Rule Plant System Reviews

a. Inspection Scope (37551)

The inspector attended several system review meetings that were held.

This was a new licensee initiative, partly in preparation for the

upcoming maintenance rule.team inspection.

b. Observations and Findings

The system review meetings discuss outstanding WR/JOs, ESRs, pending

modifications, maintenance rule status, functional failures,

unavailability, and any other items of interest related to the system.

The system engineer is primarily the source of the information and the

meeting is typically attended by the Plant Manager, Engineering Manager,

Operations Manager, and Maintenance Manager. The current licensee focus

is on maintenance rule a(1) systems. The licensee plans to continue

this effort and not limit the review to just a(1) systems.

c. Conclusions

The inspector noted that licensee management asked appropriate questions

during the reviews. Further, the reviews sensitized appropriate

managers to the problems related to the discussed systems. The

inspector concluded that the overall impact of this initiative will

result in better focus and management of problems related to plant

systems.

13

E2.2 Unreviewed Safety Question Associated with Spent Fuel Shipping Cask

a. Inspection Scope (37551)

The inspector reviewed licensee investigation and actions related to an

Unreviewed Safety Question (USQ) that was identified by the licensee as

a result of NRC Bulletin 96-02, Movement of Heavy Loads Over Spent Fuel.

b. Observations and Findings

On December 24, 1996, the NRC requested additional information from the

licensee regarding NRC Bulletin 96-02, Movement of Heavy Loads Over

Spent Fuel, Over Fuel in the Reactor Core, or Over Safety-Related

Equipment. During CP&L's review of this request, the licensee

determined that certain spent fuel shipping cask handling activities had

been conducted outside design and licensing bases of the plant.

Specifically, at Robinson, the IF-300 spent fuel shipping cask was

configured for fuel loading by removing the cask valve box covers as

governed by procedure SFS-001, IF-300 Shipping Cask Operation. The cask

was then lifted with a non-single failure proof crane from the cask

decontamination facility to the cask rail car, where the cask valve box

covers were installed. Lifting the cask with the non-single failure

proof crane with the valve box covers removed is not covered by the

shipping configuration drop analysis. The drop analysis was applicable

for a cask drop accident from 30 feet and in a fully secured, ready for

shipment configuration.

The licensee concluded that a cask drop with the valve box covers

removed could lead to an off-site release that exceeds the "no-release"

result of a cask drop accident that is in the current licensing basis.

Specifically, an estimation of the off-site dose resulting from a cask

drop without the valve covers installed concluded that the whole body

dose would be 0.0072 rem and for the thyroid would be 0.1233 rem. This

represented a small fraction of the 10 CFR 100 limits and the acceptable

limits in the Standard Review Plan.

Consequently. CP&L stopped any further cask movement, restricted use of

procedure SFS-001, reported the condition to the NRC (10 CFR 50.72

report and LER 50-261/97-05), and, submitted the condition to the NRC on

August 28, 1997 for review after concluding the issue involved an USQ.

10 CFR 50.59 allows licensees to make changes in the facility and

governing procedures as described in the safety analysis report without

NRC approval, unless it involves an unreviewed safety question. In

addition, it requires that licensee maintain records of changes in the

facility and that these records must indicate a written safety

evaluation which provides the bases for the determination that the

change does not involve an unreviewed safety question.

Section 15.7.5, Spent Fuel Cask Drop Accidents, of the Robinson UFSAR,

states that a potential cask drop could occur while the cask is being

lifted with the non-redundant yoke between the decontamination facility

14

and the shipping railcar. The UFSAR did not discuss movement of the

cask with the valve box covers removed. Thus, movement of the cask

without the valve box covers constituted a change to the facility. The

change had not been adequately evaluated in any safety evaluation

pursuant to 10 CFR 50.59, including that associated with procedure SFS

001 prior to the NRC Bulletin 96-02 request for additional information.

Movement of the cask without the valve covers installed had occurred a

number of times at Robinson. This condition is considered an Apparent

Violation of 10 CFR 50.59 for performing a change involving an

unreviewed safety question without prior NRC approval. This issue is

identified as EEI 50-261/97-10-04: Failure to Meet 10 CFR 50.59

Requirements for USQ Related to Spent Fuel Cask Movement.

c. Conclusions

The inspector concluded that the licensee's actions upon discovery of a

USQ associated with certain spent fuel shipping activities were

appropriate. The failure to meet 10 CFR 50.59 requirements for

performing a change involving a USQ without prior NRC approval was

identified as an Apparent Violation of 10 CFR 50.59. As described in

the cover letter to this report, this apparent violation will be

reviewed by NRC management and addressed in a separate correspondence.

NRC inspection followup of your corrective actions will be tracked

during our review of LER 50-261/97-05.

E7

Quality Assurance in

Engineering Activities

E7.1 Special UFSAR Review (37551)

A recent discovery of a licensee operating their facility in a manner

contrary to the UFSAR description highlighted the need for a special

focused review that compares plant practices, procedures and/or

parameters to the UFSAR descriptions. While performing the inspections

discussed in this report, the inspector reviewed the applicable portions

of the UFSAR related to the areas inspected. The inspector verified

that for the select portions of the UFSAR reviewed, the UFSAR wording

was consistent with the observed plant practices, procedures and/or

parameters.

E8

Miscellaneous Engineering Issues (92903 and 37551)

E8.1 (Closed) URI 50-261/96-12-08, Resolution of ECCS Sump Design Issues:

This URI involved two separate parts. The first part involved the

licensee's identification of openings in the containment Emergency Core

Cooling System (ECCS) sump screens that were in excess of the 7/32 inch

screen mesh size. The inspector previously verified that appropriate

repairs had been made to the sump screens during the October 1996

refueling outage. The licensee determined the cause of the degraded

sump screen condition was the lack of adequate configuration controls.

The sump screens had been altered in the past to accommodate piping

changes through the sump. Additionally, various repairs had been made

to the sump screens over the years due to damage, tears. etc. During

these alterations and repairs, personnel failed to recognize and enforce

the design requirements and configuration control standards for.the

sump. The licensee's analysis of the impact of the degraded sump

condition determined that the openings could have allowed debris larger

than the screen design to enter the sump and ECCS recirculation

flowpath, resulting in potential clogging of some of the containment

spray system nozzles. However, the licensee concluded that there was

little likelihood that the number of nozzles clogged would impact the

available performance margin of the spray system. The inspector

previously reviewed the licensee's corrective actions for this issue

during review of LER 50-261/96-005-00 in NRC Inspection Report 50

261/97-08.

The inspector determined that the failure to provide adequate design

controls related to alterations and repairs to the ECCS sump screens was

a violation of 10 CFR 50, Appendix B, Criterion III, Design Control.

This non-repetitive, licensee-identified and corrected violation is

being treated as a Non-Cited Violation (NCV), consistent with Section

VII.B.1 of the NRC Enforcement Policy. This issue is documented as NCV

50-261/97-10-05:

Inadequate Design Controls Resulting in Degraded ECCS

Sump Screens.

The second part of this URI involved review of the licensee's evaluation

related to the impact of higher containment recirculation flood level on

the design of the ECCS sump filtration function. The UFSAR indicated

that floating and submerged debris was excluded from entering the sump

by the baffle located at the sump entrance. As a result of discovering

that the containment flood level would be higher than previously

calculated, the water level exceeded the height of this baffle wall.

The inspector reviewed ESR 9600646, dated October 13, 1996, which

examined the impact of the recirculation water level exceeding the

height of the sump baffle wall.

The licensee's evaluation results

showed that no additional floating debris would be deposited on the

screens as long as the baffle wall is higher than the top of the

screens, thus, ensuring that floating material would not be deposited on

the screens as the water level rises. This item is closed.

IV.

Plant Support

R1

Radiological Protection and Chemistry Controls

R1.1 General Comments (71750)

The inspector periodically toured the Radiological Control Area (RCA)

during the inspection period. Radiological control practices were

observed and discussed with radiological control personnel including RCA

entry and exit, survey postings, locked high radiation areas, and

radiological area material conditions. The inspector concluded that

radiation control practices were proper.

16

R1.2 New Turnstile at the Radiation Control Access Entrance

a. Inspection Scope (71750)

The licensee added a new turnstile at the RCA entrance to prevent

entries into the RCA without Electronic Dosimeter (ED).

b. Observations and Findings

The inspector documented in the recent past, several instances where

entries were made into the RCA by individuals without appropriate

electronic dose monitoring. As corrective action to preclude

recurrence, the licensee installed a turnstile at the main entrance to

the RCA. All individuals entering the RCA are now required to insert

the ED into the portal monitor. The portal monitor only allows entrance

into the RCA following confirmation that the ED has been appropriately

activated. Current licensee plans are to add approximately five of

these turnstiles at all RCA entrance points.

In addition to the turnstile, the inspector noted increased efforts on

the part of Radiation Technicians to assure that personnel entering the

RCA had reviewed applicable survey maps and Radiation Work Permits, as

well as were appropriately wearing an ED.

c. Conclusions

The inspector concluded that the licensee corrective actions resulting

from the problem related to personnel entering the RCA without

appropriate monitoring was aggressive.

S1

Conduct of Security and Safeguards Activities

S1.1 General Comments (71750)

During the period, the inspector toured the protected area and noted

that the perimeter fence was intact and not compromised by erosion nor

disrepair. Isolation zones were maintained on both sides of the barrier

and were free of objects which could shield or conceal an individual.

The inspector periodically observed personnel, packages, and vehicles

entering the protected area and verified that necessary searches,

visitor escorting, and special purpose detectors were used as applicable

prior to entry. Lighting of the perimeter and of the protected area was

acceptable and met illumination requirements.

S1.2 New Security Firing Range

a. Inspection Scope (71750)

The inspector toured the renovated/upgraded firing range that was

recently completed to train security staff at Robinson.

17

b. Observations and Findings

The inspector noted that the firing range had undergone major

renovations and repairs. The range now includes 20 foot berms, Hogans

Alley (live fire building with moving and pop-up electronic targets),

elevated shooting platform, storage building, and a classroom building.

c. Conclusions

The inspector concluded that the licensee's efforts to provide the

security force with an upgraded firing range training facility was

indicative of good management support to further enhance security

personnel performance.

V. Management Meetings

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee

management at the conclusion of the inspection on October 24, 1997. No

proprietary information was identified.

18

PARTIAL LIST OF PERSONS CONTACTED

Licensee

J. Boska, Manager, Operations

H. Chernoff, Supervisor, Licensing/Regulatory Programs

T. Cleary, Manager, Maintenance

J. Clements, Manager, Site Support Services

J. Henderson, Manager, Environmental and Radiation Controls

J. Keenan, Vice President, Robinson Nuclear Plant

R. Duncan, Manager, Robinson Engineering Support Services

R. Moore, Manager, Outage Management

J. Moyer, Manager, Robinson Plant

R. Warden, Manager, Nuclear Assessment Section

T. Wilkerson, Manager, Regulatory Affairs

D. Young, Director, Site Operations

NRC

B. Desai, Senior Resident Inspector

J. Zeiler, Resident Inspector

19

INSPECTION PROCEDURES USED

IP 37551:

Onsite Engineering

IP 40500:

Effectiveness of Licensee Controls in Identifying, Resolving, and

Preventing Problems

IP 61726:

Surveillance Observations

IP 62707:

Maintenance Observation

IP 71707:

Plant Operations

IP 71750:

Plant Support Activities

IP 92901:

Followup - Operations

IP 92903:

Followup - Engineering

IP 92902:

Followup - Maintenance

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

Type Item Number

Status

Description and Reference

URI

50-261/97-10-01

Open

Complete Review of LPMS Testing and

Maintenance Activities (Section 01.3)

EEI

50-261/97-10-02

Open

Apparent Violation of 10 CFR 50, Appendix

B, Criterion II,

for Mispositioned EDG

Switch (Section 08.1)

EEI

50-261/97-10-03

Open

Apparent Violation of 10 CFR 50, Appendix

B, Criterion XVI

for Mispositioned EDG

Switch (Section 08.1)

EEl

50-261/97-10-04

Open

Apparent Violation of 10 CFR 50.59

Requirements for USQ Related to Spent Fuel

Cask Movement (Section E2.2)

NCV

50-261/97-10-05

Open

Inadequate Design Controls Resulting in

Degraded ECCS Sump Screens (Section E8.1)

Closed*

Type Item Number

Status

Description and Reference

URI

50-261/97-09-01

Closed

Review Licensee Evaluation of EDG Output

Breaker Control Switch Mispositioning

(Section 08.1)

URI

50-261/96-12-08

Closed

Resolution of ECCS Sump Design Issue

(Section E8.1)

NCV

50-261/97-10-05

Closed

Inadequate Design Controls Resulting in

Degraded ECCS Sump Screens (Section E8.1)