ML14191B015

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Insp Rept 50-261/88-23 on 880811-0910.No Violations or Deviations Noted.Major Areas Inspected:Operational Safety Verification,Physical Protection,Surveillance & Maint Observation,Esf Sys Walkdown & Onsite Review Committee
ML14191B015
Person / Time
Site: Robinson 
Issue date: 10/12/1988
From: Garner L, Latta R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14191B014 List:
References
50-261-88-23, NUDOCS 8810250457
Download: ML14191B015 (12)


See also: IR 05000261/1988023

Text

-

'UNITED

STATES

NUCLEAR REGULATORY COMMISSION

REGION II

Qb

101 MARIETTA ST., N.W.

ATLANTA, GEORGIA 30323

.Report No.:

50-261/88-23

Licensee:

Carolina Power and Light Company

P. 0. Box 1551

Raleigh NC 27602

Docket No.:

50-261

License No.: DPR-23

Facility Name: H. B. Robinson

Inspection Conducted: August 11 -

September 10, 1988

TInspector:

120

______________

/

~

g

. W. Garner, Senior Wid

In spector

Date Signed

R. M. Latta, Residenflns

4tor

[ate Signed

Approved by:

P. E. Fredrickson, Chief

Date Signed

Reactor Projects Section 1A

Division of Reactor Projects

SUMMARY

Scope:

This routine,

announced inspection was conducted in the areas of

operational safety verification, physical protection,

surveillance

observation,

maintenance observation,

ESF system walkdown,

onsite

followup of events at operating power reactors,

and onsite review

committee.

Results:

No violations or deviations were identified.

8810250457 881013

PDR ADOCK 05000261

G

PNU

REPORT DETAILS

1. Licensee Employees Contacted

R. Barnett, Maintenance Supervisor, Electrical

R. Chambers, Engineering Supervisor, Performance

D. Crocker, Supervisor, Radiation Control

J. Curley, Director., Regulatory Compliance

  • C. Dietz, Manager, Robinson Nuclear Project Department

J. Eaddy, Supervisor, Environmental and Chemistry

W. Farmer, Senior Engineer, System Engineering

R. Femal, Shift Foreman, Operations

  • W. Flanagan, Manager, Design Engineering

W. Gainey, Support Supervisor, Operations

P. Harding, Project Specialist, Radiation Control

E. Harris, Director, Onsite Nuclear Safety

  • D. Ingram,,Project Engineer, Industrial Engineering

R. Johnson, Manager, Control and Administration

D. Knight, Shift Foreman, Operations

E. Lee, Shift Foreman, Operations

A. Lewis, Senior Engineer, NED

D. McCaskill, Shift Foreman, Operations

R. Miller, Maintenance Supervisor, Mechanical

J. Moon, Senior Engineer, System Engineer

R. Moore, Shift Foreman, Operations

R. Morgan, Plant General Manager

D. Myers, Shift Foreman, Operations

D. Nelson, Operating Supervisor, Operations

M.. Page, Engineering Supervisor, Plant Systems

  • D. Quick, Manager, Maintenance
  • D. Sayre, Senior Specialist, Regulatory Compliance

D. Seagle, Shift Foreman, Operations

J. Sheppard, Manager, Operations

R. Steele, Shift Foreman, Operations

H. Young, Director, Quality Assurance/Quality Control

Other licensee employees

contacted included technicians,

operators,

mechanics, security force member.s, and office personnel.

NRC Resident Inspectors

L. Garner

  • R. Latta
  • Attended exit interview-on September 13, 1988

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2

2.

Licensee Action on Previous Enforcement Matters (92702)

This area was not inspected.

3. Operational Safety Verification (71707)

The inspectors observed licensee activities to confirm that the facility

was being operated safely and in conformance with regulatory requirements,

and- that

licensee

management

was

effectively

discharging

its

responsibilities for continued safe operation.

These activities were

confirmed by direct observations, tours of the facility,, interviews and

discussions

with

licensee

management

and personnel,

independent

verifications of safety system

status and limiting conditions for

operation, and reviews of facility records.

Periodically, the inspectors reviewed shift logs, operations records, data

sheets, instrument traces, and records of equipment malfunctions to verify

operability of safety related equipment and compliance with TS.

Specific

items reviewed include control room logs, maintenance work requests,

auxiliary logs, operating orders, standing orders, and equipment tagout

records.

Through periodic observations of work in progress

and

discussions with operations staff members,

the inspectors verified that

the staff was knowledgeable of plant conditions; responding properly to

-alarm

conditions; adhering to procedures and applicable administrative

controls; and aware of equipment out of service, surveillance testing, and

maintenance activities in progress.

The inspectors routinely observed

shift changes to verify that continuity of system status was maintained

and that proper control

room staffing existed.

The inspectors also

observed that access to the control room was controlled and operations

personnel were carrying out their assigned duties in an attentive and

professional

manner..

The control

room was

observed to be free of

unnecessary distractions.

The inspectors performed channel checks,

reviewed component status and safety related parameters, including SPDS

information, to verify conformance with the TS.

During this reporting interval, the inspectors verified compliance with

selected LCOs. This verification was accomplished by direct observation

of monitoring instrumentation,

valve positions, switch positions, and

review of completed logs and records. The inspectors verified the axial

flux difference was within the values required by the TS.

Plant tours were routinely conducted to verify the operability of standby

equipment; assess the general condition of plant equipment; and verify

that radiological controls, fire protection controls and equipment tag out

procedures were being properly implemented.

These tours verified .the

absence of unusual fluid leaks; the lack of visual degradation of pipe,

conduit and seismic supports; the proper positions and indications of

important valves and circuit breakers; the lack of conditions of which

3

could invalidate EQ; the operability of. safety related instrumentation;

the calibration of safety related and control instrumentation including

area radiation monitors, friskers and portal monitors; the operability of

fire suppression and fire fighting equipment; and the operability of

emergency lighting equipment.

The

inspectors also verified that

housekeeping was adequate and areas were free of unnecessary fire hazards

and combustible materials.

While the inspectors were in the control room at 6:09 a.m. on August 30,

1988,

they witnessed the response of the fire brigade to an unannounced

fire drill. The simulated fire was located in the component cooling water

pump

room in the auxiliary building.

The inspectors witnessed the

response of the fire brigade team leader (senior reactor operator on duty)

as well as the actions of other plant personnel who were utilizing Fire

Protection Procedure FP-001 (revision 11) titled "Fire Emergency", OMM-003

(revision 9) titled "Fire Protection Pre-Plans, Unit No. 2," and PEP-101

(revision 5) titled "Initial Emergency Actions." The inspectors observed

the donning of full turn-out gear and self-contained breathing apparatus

by

fire brigade members, as well

as the access control

of the

radiologically controlled area

by security personnel.

The inspectors

noted that the fire brigade personnel responded quickly to the alarm and

exhibited good fire fighting techniques throughout the drill. Additional

details regarding this unannounced fire drill are contained in Inspection

Report 50-261/88-25.

On August 26, 1988, the inspectors participated in an augmented emergency

preparedness drill.

The primary purpose of this exercise, which was

initiated at approximately 4:00 a.m., was to determine staff mobilization

capabilities for licensee personnel who would normally be required to

fulfill emergency preparedness core staffing positions during a site

emergency event.

The inspectors were notified at 4:12 a.m.

and were

onsite at approximately 4:45 a.m. The inspectors toured the TSC following

the security search and observed that the emergency preparedness supplies,

equipment and communications

systems were properly stationed

and

functional.

The inspectors also observed the reporting of specific

management and staff personnel in the TSC. Subsequent to the termination

of the drill, at approximately 6:30 a.m., the inspectors reviewed specific

personnel

response time records.

This review indicated that the

objectives of the drill were not totally satisfied in that all required

personnel did not respond within the stipulated time frame.

This

condition has been documented by the licensee on NCR 88/109 and will be

evaluated during future inspections. Additional details concerning this

augmented emergency preparedness drill are contained in Inspection Report

50-261/88-22.

No violations or deviations were identified.within the areas inspected.

4

4.

Physical Protection (71707)

In the course of the monthly activities, the inspectors included a review

of the licensee's physical security program. The inspectors verified by

general observation, perimeter walkdowns and interviews that measures

taken to assure the physical protection of the facility met current

requirements.

The performance of various shifts of the security, force was observed to

verify that daily activities were conducted in accordance with the

requirements of the

security plan.

Activities inspected included

protected and vital areas, access controls,

searching of personnel,

packages and vehicles, badge issuance and retrieval, patrols, escorting of

visitors, and compensatory measures.

In addition,

the

inspectors

routinely observed protected and vital area lighting and barrier

integrity.

On September 6, 1988, while the inspectors were in the operations and

maintenance building located inside the protected area, they observed an

individual displaying a visitors badge who was not accompanied by his

escort. The individual was questioned by the inspectors and was unable to

immediately determine the location of his escort.

While the inspectors

were questioning the visitor, the assigned escort approached the area from

another section of the building.

The inspectors noted the names and

badge numbers of the individuals involved and notified security of the

event. Subsequently,

the inspectors were informed that the escorting

individual has been temporarily removed from escort responsibilities and

that the licensee has initiated an investigation of the incident.

The

inspectors also reviewed the corrective actions specified in Field Report

88/083 and examined security incident reports maintained by the licensee.

This review indicated that this occurrence appeared to be an isolated

incident which will be evaluated during future routine inspections

conducted in the area of physical security.

This is an IFI:

Review of

Escort Responsibilities Within the Protected Area (261/88-23-01).

No violations or deviations were identified within the areas inspected.

5. Monthly Surveillance Observation (61726)

The inspectors observed certain surveillance related activities of safety

related systems and components to ascertain that these activities were

conducted in accordance with license requirements.

For the surveillance

test procedures listed below, the inspectors determined that precautions

and LCOs were met; the tests were completed at the required frequency; the

tests conformed to TS requirements; the required administrative approvals

and tagouts were obtained prior to initiating the tests; the testing was

accomplished by qualified personnel *in accordance with an approved test

procedure; and the required test instrumentation was properly 'calibrated.

Upon completion of the testing, the inspectors observed that the recorded

test data was accurate, complete,

and met TS requirements,

and test

discrepancies were properly rectified.

The inspectors independently

verified that

the

systems were properly

returned

to

service.

Specifically, the inspectors witnessed/reviewed portions of the following

test activities:

a. OST-405 (revision 4) TSC/EOF/PAP Diesel Generator (Semiannual)

The inspectors witnessed all aspects of this surveillance test which

is designed to verify the mechanical and electrical performance of

the security diesel generator and to assess the operational readiness

of the related.components to fulfill their required support function

during emergency conditions. Specifically, the inspectors witnessed

the preoperational checks on the

PAP diesel including engine oil

.level, coolant quantity, visual inspection of the engine and the

recording of fuel

oil storage tank level.

The inspectors also

observed the completion-of required breaker lineups, the verification

of control power, and the recording of local control panel readings.

During

the pretest breaker lineups the inspectors did

note a

component labeling discrepancy in that the breaker identified in the

procedure as "Generator Disc (TSC/PAP

BLDG)"

was physically labeled

"Emergency Generator,

400 A CB".

The inspectors observed that the

operations personnel involved in the test functionally verified the

breaker by reference to appropriate logic diagrams and initiated

action to correct the labeling discrepancy.

b. EST-008 (revision 2) Service Water Booster Pump Bearing Temperature

Test

EST-008 reflects the licensees implementation of subsection IWP of

Section XI, ASME Code pertaining to the operational measurement of

the service water booster pump bearing temperature. This test was

completed only on the "A" service water booster pump,

subsequent to

its replacement due to increasing vibrational amplitude.

The

inspectors determined that the stabilized bearing temperatures were

within the acceptable range and that the contact pyrometer utilized

was properly calibrated.

c. MST-020 (revision 4) Reactor Protection Logic Train "A" at Power

The inspectors witnessed the performance of this surveillance test

which ensures that the reactor protection. logic train "A" functions

properly. In particular the inspectors witnessed the racking in of

the "A" bypass breaker and the tripping of the "A" reactor trip

breaker during the initial phase of the test.

The inspectors also

witnessed selected portions of the logic combination testing of the

reactor

trip breaker

and

determined

that each

combination.

de-energized the undervoltage coil for the trip breaker as required.

6

The inspectors determined that all stated acceptance criteria were

satisfied and that the system was properly returned to service

subsequent to testing.

d. MST-022 (revision 1) Safeguard Relay Rack Train "A"

The inspectors also witnessed the performance of MST-022 which

verifies the operability of the safeguard logic for train "A",

including

operability

of

the associated test and status lights

required for proper indication.

The inspectors confirmed that the

required annunciators

on the

RTGB

responded properly, that the

stipulated relay logic switch combinations were satisfactorily tested

and that the status light voltage checks were

acceptable.

No

deficiencies were identified during the conduct of this surveillance

test.

No violations or deviations were identified within the areas inspected.

6. Monthly Maintenance Observation (62703)

The inspectors

observed several maintenance related activities of

safety-related systems and components to ascertain that these activities

were conducted in accordance with approved procedures, TS, and appropriate

industry codes and standards.

The inspectors determined that these

activities were not violating LCOs and that redundant components were

operable.

The

inspectors

also determined

that

activities were

accomplished by qualified personnel using approved procedures,

QC hold

points were established where required, required administrative approvals

and tagouts were obtained prior to work initiation, proper radiological

controls were adhered to,

appropriate ignition and fire prevention

controls were

implemented,

replacement parts and materials used were

properly certified, and the effected equipment was properly tested before

being returned to service.

In particular, the inspectors observed/

reviewed the following maintenance activities:

a. WR/JO 88-AHMK1 Replace "A" SWBP motor and align pump to motor

b. WR/JO 88-AIMW1 Adjust packing on V2-16A, AFW header discharge to S/G,

"A".

c. WR/JO 88-BOM361 Perform "F" delta "I" calibration.

d. WR/JO 88-AIIW1 Disassemble and reassemble "B" SWBP,

set impeller

clearances, and align pump to motor.

No violations or deviations were identified within the areas inspected.

7

7. ESF System Walkdown (71710)

The inspectors verified the operability of an ESF system by performing a

walkdown of the major components and flow paths of the AFW system.

The

inspectors confirmed that the system lineup procedures matched plant

drawings and the as-built condition.

The inspectors examined piping and

component configurations in the turbine building, auxiliary feedwater pump

room, condensate storage tank area, component cooling water pump room, and

in the control room.

Observed conditions were determined to be in

agreement with the flow diagram, G-190197, titled "Feedwater, Condensate,

and Air Evacuation System",

sheet 1 (revision 38)

and sheet 4 (revision

15).

The inspectors examined the general condition of valves in the

system and verified that they were installed correctly, that they did not

exhibit excessive packing leakage, and that other adverse conditions were

not evident.

The inspectors also verified that valves were. locked as

required,

system pumps were lubricated, valves required for automatic

operation were energized,

and both local and remote indications agi'eed.

with actual valve stem positions.

On August

13; 1988,

the inspectors found snubber #30,

located on the

steamline to the SDAFW pump turbine adjacent to valve V1-8B, loose. When

the inspectors checked the snubber for freedom of movement, the snubber

rotated onto its side, uncovering the oil surge line port. The inspectors

returned the snubber to its as-found position and notified the shift

foreman. The inspectors demonstrated for an auxiliary operator how little

movement was required to allow the snubber to freely rotate to an

uncovered port position. The licensee determined that the jam nut had

come loose. No specific cause for the loose nut could be determined. The

licensee functionally tested the snubber satisfactorily and returned it to

service.

Snubbers of similar size (1.5

kip) were randomly inspected

by the licensee to ensure that they were properly installed and tight. No

similar condition was found during this inspection.

The inspectors also identified a pipe support in the auxiliary feedwater

pump room which was improperly made up, as well as a wall mounted pressure

gage which was loose in its bracket. Additionally, the component label

plates on the MDAFW flow control valves did not agree with the valve

numbers specified on the flow diagram on the AFW system valve checklist.

These items were identified to the licensee and corrective action work

requests were initiated.

On August 29, 1988, the inspectors witnessed the operability testing of

the SDAFW pump, conducted in accordance with OST-202 (revision 13), titled

"Steam

Driven Auxiliary Feedwater System Component Test". It is noted

that the frequency .of this surveillance test had been increased in

accordance with the provisions of the subject procedure as -a result of

high vibrational amplitude (alert range)

detected in the horizontal

direction on August

17,

1988.

During the conduct of the test on

8

August 21,

1988,

the SDAW

pump went into the alert range in both the

horizontal the SDAFW pump went into the alert range in both the horizontal

and vertical direction. The inspectors determined that the licensee had

performed additional diagnostic testing on the vibrational frequencies for

pump operation in the recirculation mode and with the system lined up to

feed the steam generators.

Augmented testing of the SDAFW pump has been

scheduled when plant conditions allowed.

The inspectors will continue

to follow this activity during future inspections.

No violations or deviations were identified within the areas inspected.

8. Onsite Followup of Events at Operating Power Reactors (93702)

a.

Fire Barrier Penetration Degradation

On August 26,

1988, with the Unit operating at 100% reactor power,

the licensee determined that a fire barrier penetration (No. EP49-70)

with 3 trays was inoperable. Upon examination it was determined that

the area under the cable tray covers for this penetration, located in

the cable spreading room, was not completely filled with fire barrier

sealant. Subsequently, on September 1, 1988, the licensee determined

that a similar condition existed in two adjacent block-out fire

barrier penetrations. These penetrations were declared inoperable

and repair activities were initiated in accordance with WR/JO

88-AJBK1. Concurrent with this activity, the licensee examined all

remaining cable trays and bus ducts for adequacy of fire barrier

sealant. This activity resulted in repair to and/or repair and

evaluation

of

38

total

penetrations.

All

penetration

repairs were completed within seven days of the discovery of inoperable

status in accordance with TS Section 3.14.7.2.c.

b. Containment Fan Cooler Degradation Conditions

As stated in CP&L correspondence. to the NRC, Serial: RNPD/88-3170,

dated July 22, 1988, the licensee has committed to repair or replace

portions of the service water piping inside containment,

where

internal pipe pressure is less than the containment pressure during a

design basis accident (42 psig), during the upcoming refueling outage

scheduled to start on November 14, 1988. The scope of the SW piping

replacement inside containment as stipulated in Plant Modification

M-858 was based on test results obtained in the 1981 performance of

SP-291. However, the 4-20 psig current operating pressures-of the SW

system in the return piping from the HVH coolers, measured in the

charging pump room, did not correlate with the 1981 test data of

41-59 psig.

In order to provide additional information for service water piping

replacement inside containment, the licensee conducted

SP-811

on'

August 22, 1988. Test results from this procedure indicated that two

9

of the containment fan coolers (HVH-3

and 4) exhibited negative

discharge pressures at the locally mounted gage on the service water

return line manifold. HVH-4, which demonstrated a discharge pressure

of -7.8 ps.ia, was the limiting worst case.

Subsequent to the conduct of SP-811, the licensee performed an evaluation

.to determine the synergetic effects of the indicated changes in the SW

system within the eight year period between 1981 and 1988.

This .

evaluation, which included input from Westinghouse, considered: (1) cooler

fouling; (2) air entrainment in the cooling units; (3) the siphoning

effects resulting from the rerouting of the SW return piping (M-686) in

1984; and (4) the replacement of the original copper U-tube design cooling

coils in 1983 (M-769) with AL6X three pass straight tube cooling coil

units.

In order to validate the observed SW system pressures and flows the

licensee initiated development of an additional test (SP-812) to verify

that the subject HVH coolers were not airbound. On August 24, 1988, the

inspectors attended a special PNSC (see paragraph 9 of this report) in

which operability issues concerning the containment fan coolers, as well

as containment integrity relative to MIC were discussed. Several action

items were initiated as a result of plant management concern regarding SW

issues. These included the preparation of a JCO supporting containment

fan cooler operability, the evaluation of potential two phase flow in the

containment coolers, a.nd the questionable accuracy of test pressure data

obtained from SP-811. During this period of time, the HVH supplier

(Westinghouse) was directed by the licensee to evaluate the differential

pressure across coolers HVH-3 and 4,

the impact on heat transfer

coefficient, fouling factor effects, and required flow rates.

On August 29, 1988, Westinghouse advised the licensee that under the

existing operating conditions, assuming the test pressures obtained in

SP-811, approximately one half of the heat removal capability of HVH-4 and

about one sixth that of HVH-3 would be lost under worst case conditions.

Based on the preliminary results of the above mentioned Westinghouse

analysis, which indicated potential two-phase flow on the outlet side of

HVH-4 due to negative pressure and the resultant decrease in the heat

removal capability, the subject containment fan cooler-was declared

inoperable at 2:30 p.m. on the same day.

With

HVH-4 containment

fan

cooler declared inoperable

and

Westinghouse continuing their analysis of HVH-4,

the licensee

conducted SP-812 on cooler HVH-4. The purpose of this procedure was

to determine if the discharge pressure at the cooler outlet could be

raised by throttling down on the SW discharge valve associated with

HVH-4. This was predicated on the Westinghouse determination that a

positive pressure reading, if achieved during SP-812, would provide a

basis for declaring HVH-4 operable. Review of the test data obtained

10

during

the

conduct of SP-812, indicated a positive pressure

(approximately 10 psi) at the top of the HVH-4 cooler, and it

was

declared operable at 5:00 a.m.

on August 30,

1988. However, the

discharge pressure from the "B" SW booster pump was determined to be

below the pump curve and the pump was taken out of service to adjust

the clearances per WR/JO 88-AIIW1.

On August 30, 1988, subsequent to returning the "B" SW booster pump to

service, HVH-4 was again declared inoperable in order to further test the

SW system pressure characteristics associated with this containment fan

cooler. Because of the cumulative effects of system test restrictions

(entering and exiting LCOs)

at power, limited testing configuration

conditions, inconclusive test data, and questionable parameters for

operation, the licensee decided to take the Unit to cold shutdown.

Subsequent problems and repairs of the HVH coolers will be addressed

in a subsequent inspection report.

No violations or deviations were identified within the areas inspected.

9. Onsite Review Committee (40700)

The inspectors evaluated certain activities of the -PNSC to determine

whether the onsite review functions were conducted in accordance with TS

and other regulatory requirements. In particular, the inspectors attended

the special PNSC

meeting which was convened on August 24,

1988,

to

evaluate the service water system/HVH containment fan cooler issue.

The

inspection ascertained that provisions of the TS dealing with membership,

review process, frequency, and qualifications were satisfied.

Previous

meeting minutes were

reviewed

to

confirm that decisions

and

recommendations were accurately reflected in the minutes. The inspectors

also followed up on selected previously identified PNSC activities to

independently

confirm that

corrective

actions

were

progressing

satisfactorily.

No violations or deviations were identified within the areas inspected.

10.

Exit Interview (30703)

The inspection scope and findings were summarized on September 13,

1988,

with those persons indicated in paragraph 1. The inspectors described the

areas inspected and discussed in detail the inspection results. Dissenting

comments were not received from the licensee. Proprietary information is

not contained in this report.

No written material was given to the

licensee by the resident inspectors during this report period.

Item Number

Status

Description/Reference Paragraph

88-23-01

Open

IFI -

Review of Escort

Responsibilities Within the Protected

Area (paragraph 4).

11.

List of Abbreviations

AFW

Auxiliary Feedwater

ASME

American Society of Mechanical Engineers

BLDG

Building

CB

Circuit Breaker

CP&L

Carolina Power & Light

EOF

Emergency Operation Facilities

EQ

Environmental Qualifications

ESF

Engineered Safety Feature

EST

Engineering Surveillance Test

DISC

Disconnect

FP

Fire Protection

HVH

Heating Ventilation Handling

IFI

Inspector Followup Item

IWP

Inservice Inspection Pump Testing

JCO

Justification for Continued Operation

LCO

Limiting Condition for Operation

MDAFW

Motor Driven Auxiliary Feed Water

MIC

Microbiologically Induced Corrosion

MST

Maintenance Surveillance Test

NCR

Nonconformance Report

NED

Nuclear Engineering Department

NRC

Nuclear Regulatory Commission

OMM

Operations Management Manual

0ST

Operations Surveillance Test

PAP

Personnel Access Portal

PEP

Plant Emergency Procedure

PNSC

Plant Nuclear Safety Committee

QC

Quality Control

RNPD

Robinson Nuclear Project Department

RTGB

Reactor Turbine Generator Board

SDAFW

Steam Driven Auxiliary Feed Water (Pump)

S/G

Steam Generator

SPDS

Safety Parameter Display System

SW

Service Water

SWBP

Service Water Booster Pump

TS

Technical Specification

TSC

Technical Support Center

WR/JO

Work Request/Job Order