ML14191B073

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Insp Rept 50-261/88-36 on 881219-21.Violations Noted.Major Areas Inspected:Followup on Recently Identified Operating Events Involving Nonenviron Qualified Splices on Containment Fans & RCS High Point Vent Sys Not on Master List
ML14191B073
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 01/19/1989
From: Colon T, Merriweather N, Paulk C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14191B072 List:
References
50-261-88-36, NUDOCS 8902030088
Download: ML14191B073 (8)


See also: IR 05000261/1988036

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION il

101 MARIETTA ST., N.W.

ATLANTA, GEORGIA 30323

Report No.:

50-261/88-36

Licensee: Carolina Power and Light Company

P. 0. Box 1551

Raleigh, NC 27602

Docket No.:

50-261

License No.: DPR-23

Facility Name: H. B. Robinson

Inspection Conducted: December 19 -

22, 1988

Inspectors:

e___,___

N. Merriweather

Date Signed

C.R1

Da e Signed

Approved b

. E. Conlon, Section Chief

Date Signed

Plant Systems Section

Engineering Branch

Division of Reactor Safety

SUMMARY

Scope:

This special, announced inspection was conducted to followup on

recently identified operating events involving Non-EQ splices on

Containment Fans,

RCS High Point Vent System not on the EQ Master

List and not EQ,

and improper setpoints on Motor Control Centers

(MCCs) 5 and 6 Feeder Breakers.

Results: In the areas inspected, three violations were identified involving:

(1) Unanalyzed Loss of Safety-Related MCCs 5 and 6, paragraph 3.a

(2) HVH 1-4 Penetration Splices Being Non-EQ, paragraph 3.b.

(3) Non-EQ Reactor Vessel Head Vent System, paragraph 3.c.

No specific strengths or weaknesses were identified in the licensee's

corrective actions for these operational events.

However,

the

licensee has made a concerted effort through the Design Basis

Reconstitution Program and the EQ Program Assessment Project to

identify, evaluate and correct problems at the plant.

Management

seems to be supporting this effort at all levels.

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REPORT DETAILS

1. Persons Contacted

Licensee Employees

  • D. Baur, Supervisor, QA (Acting Director-QA/QC)
  • S. Clark, Supervisor, Configuration Control
  • J. M. Curley, Director, Regulatory Compliance
  • C. R. Dietz, Manager, Robinson Nuclear Project Department
  • W. J. Flanagan, Manager, Modifications and Configuration Control
  • E..M. Harris, Director, On-Site Nuclear Safety
  • M. Heath, Project Engineer-EQ Coordinator
  • G. Shartzer, System Engineering Representative
  • D. A. Sayre, Senior Specialist-Regulatory Compliance

Other licensee employees contacted during this inspection included

engineers,

operators,

security force

members,

and administrative

personnel.

NRC Resident Inspector

L. Garner

  • Attended exit interview

2. Action on Previous Inspection Findings (92701)

a. (Closed)

Unresolved Item 50-261/88-30-01, Investigate Circumstances

Surrounding Improper Setpoints of MCC-5 and MCC-6 Feeder Breakers.

For discussion of findings see paragraph 3.a.

b. (Closed)

Unresolved Item 50-261/88-30-02,

Review Circumstances

Surrounding HVH 1-4 Penetration Splices Being Non-EQ. For discussion

of findings see paragraph 3.b.

3. Onsite Followup of Licensee Events at Operating Power Reactors (92700)

a. During reconstitution of the design basis for the electrical loading

of safety related MCCs,

the licensee discovered a potential overload

condition could exist under certain postulated accident conditions.

For example, should a LOCA occur while the plant is in hot shutdown

with off-site power available and there is a single failure of either

MCC-5 or MCC-6, the remaining MCC feeder breaker would have tripped

on overload. The licensee implemented compensatory measures prior to

confirming that the overload condition existed.

Once the overload

was confirmed, the proper reports were made to NRC.

2

The licensee determined that, prior to the compensatory measures, the

plant was operated with an unanalyzed condition. That is, the loss

of all 480V safety related MCC power:

MCCs-5,6,9 and 10,

and,

Instrument Buses 1,4,6 and 9. Most of the safety related loads are

motor operated valves that would fail as is on the loss of power. In

the above scenario, when the single failure occurs, redundant loads

are started on the other MCC resulting in the overcurrent condition.

This would result in the feeder breaker tripping shortly after the

transfer of loads, almost instantly.

Since the loss of both MCCs

occur very quickly, the motor operated valves would be de-energized

in their normal operating position. The result of this would be no

flow path available for Containment Spray, RHR, or Safety Injection

(except for the Accumulators). The pumps for these systems would be

running at shut off head without any area fan coolers operating.

Other equipment that would be lost includes:

the Iodine Removal

Units (HVE-3

and 4); steam supplies to the Steam Driven Feedwater

Pump (V1-8A and 8B); the Charcoal Filter Booster Fans (HVE-5A

and

5B); both Service Water Booster Pumps; AFW discharge valves; and the

Pressurizer Relief Isolation Valves.

On August 11,

1974, the licensee experienced an event which resulted

in the loss of MCC-5 and MCC-6,

possibly at the same time, as the

result of an overcurrent trip on the feeder breaker to MCC-6.

The

event was reported to the NRC via a letter dated January 3, 1975.

The letter detailed the accounts of the event. It took the operators

approximately two minutes to identify that MCC-6 was de-energized.

After an additional thirteen minutes, the operators discovered that

MCC-5 was de-energized. After re-energizing MCC-5, MCC-6 was found

de-energized approximately one minute later.

The licensee stated

that there was approximately a two minute period where both MCCs

possibly could have been de-energized at the same time, but it was

not confirmed. That time period was the first two minutes of the

accident.

The letter does not discuss whether the ECCS systems

functioned properly during the event. It does state that there was

no damage to systems or components,

no radiation exposures,

nor

radioactive releases.

As a result of the 1974 event, the licensee increased the overcurrent

trip setpoint from 600 amps to 720 amps.

Sometime later, the set

point was increased to 800 amps. In both cases, there was no docu

mentation to indicate that the setpoint was adequate and acceptable

since it was not controlled by any program at those times.

As can be seen from the list of equipment that was previously

discussed, in the event that a LOCA occurs with offsite power avail

able, concurrent with the single failure of MCC-5 or 6, and the loss

of the other MCC on overcurrent, a majority of the ECCS subsystems

would not be available. This event was not analyzed and could result

in safety systems designed to prevent or mitigate a serious accident not

being able to perform their intended functions under certain

conditions.

3

The compensatory measures discussed in NRC Report No. 50-261/88-30

were initiated in a timely manner by the licensee and have been

evaluated as acceptable for short term operation.

The licensee has

subsequently initiated plant modifications to transfer loads from

MCC-5 and 6 to other BOP MCCs. The loads that are to be removed are

the Reactor Support Cooling Fans (HVE-6A,B), the Concrete Shield Wall

Cooling Fans

(HVH-9A,B),

the turbine auxiliaries, and the duct

heaters for HVE-15A. These activities are scheduled to be completed

during the present outage.

If the duct heaters are not completed

prior to restart, they will be done at a later date since they are

not required during plant operation,

only during refueling

activities.

Based on the above, URI 50-261/88-30-01 will be closed and Violation

50-261/88-36-01, Unanalyzed Loss of Safety Related MCCs, is opened.

b.

On October 27, 1988, the licensee determined that the penetration to

pigtail splice configuration for the 480 volt power leads to the

Reactor Containment Fan Coolers

(HVH

1-4) were neither environ

mentally qualified nor qualifiable.

The licensee subsequently

declared the HVH 1-4 units inoperable and commenced reactor shutdown.

Hot shutdown was obtained at 2:03 a.m.,

on October 28,

1988.

The

unqualified cable splice configurations (Rayclad heat shrink tubing)

were replaced with qualified Raychem heat shrink and the plant

returned to power operation on October 29,

1988.

This issue was

initially investigated by the NRC Resident Inspector and documented

as Unresolved Item 88-30-02.

The main concern left outstanding

involved the root cause determination or reason why these particular

splice configurations were not included in the licensee's original

scope of corrective action to resolve item 50-261/87-10-02, Crouse-Hinds

Electrical Penetrations.

The inspector concentrated on trying to

determine the root cause for why these splices were not corrected and

to evaluate the safety significance of the splices being non-EQ.

Inspection Report 87-10 is the report which initially identified the

deficiency that the Heat Shrink Sleeve at the penetration to pigtail

splice on Crouse-Hinds electrical penetrations

(EPAs)

were not

environmentally qualified. The example cited in the report involved

generic qualification file 9.0 for Crouse-Hinds EPAs, Model 751.

The licensee attempted to correct all unqualified EPA splice

configurations by implementing Special Procedure SP-775,

Penetra

tion/Pigtail Splice Repair (May 1987). SP-775 typically replaced the

penetration-to-pigtail splices with individual

Raychem over

uninsulated butt splice connectors and the pigtail-to-field cables

splices with insulated butt splice connectors covered with an overall

Raychem sleeve.

This splice combination was later found to be

unqualified allowing moisture intrusion from the open ended cable

jacket at the penetration-to-pigtail splice, through the pigtail up

to the insulated butt splices, and consequently, the possibility for

4

a line-to-line leakage path was created. Modification M-928, Repair

of EQ Splices Installed under SP-775 was issued to address this

latter potential moisture intrusion problem.

In June 1988,

the licensee began a review of internal and NRC

generated EQ violations to assure that all necessary corrective

actions had been completed. On October 27, 1988, a review of records

for completed

EQ special procedures and modification packages,

revealed that EQ documentation did not exist to show that the HVH

splices had ever been modified to a qualified configuration or were

qualified by the penetration manufacturer, Crouse-Hinds.

After making this determination, the licensee made a containment

entry, at or near full power, to inspect the suspect splices.

The

results of the inspection confirmed that the splice configurations

were the original installations with Rayclad heat shrink tubing.

Engineering review and subsequent review by the PNSC determined that

the splices were not EQ qualified or qualifiable.

Recently, the licensee learned that qualification testing had been

performed on the Crouse-Hinds Penetration Splice configuration for

another utility. The licensee developed draft Engineering Evaluation

ENG 88-186 (December 16,

1988) to provide justification that the HVH

1-4 penetration splices were environmentally qualified, prior to the

repair. The NRC inspectors had serious concerns regarding the use of

this test report alone as establishing the basis for qualification of

the H. B. Robinson penetration splices. Concerns which the licensee

could not adequately address involved aging of test specimens versus

naturally aged splices at Robinson, similarity between test specimens

versus Robinson's as-found configurations (sleeves separating from

substrate), utilizing post testing aging to satisfy pre-test aging,

and applied test voltages and currents on specimens did not envelope

plant conditions.

All the above concerns, in particular, the

deteriorated condition observed for the as-found splice configura

tions at Robinson posed serious questions regarding the applicability

of this test report.

The licensee agreed that it might not be

possible to show qualification using the subject report. Therefore,

since the licensee did not have documentation in a file to establish

qualification for the subject penetration splice configurations these

items were considered unqualified and not qualifiable.

The HVH units provide containment pressure reduction and residual

heat removal from containment following a design basis accident. The

unqualified penetration splices on the

HVH units made them

technically inoperable, creating an unanalyzed condition that would

seriously degrade the plants capability for mitigating the

consequences of an accident.

The accident analysis described in the

FSAR considered two of four fan coolers being operable with one

containment spray pump.

5

Plant Technical Specification 3.3.2.1.c requires all four fan cooler

units to be operable whenever the reactor is made critical.

Tech

Spec 3.3.2.2.1 allows one fan cooler unit to become inoperable

for up to 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, provided both containment spray pumps are demon

strated operable.

The failure of the licensee to establish environmental qualification

for the penetration splices for the HVH 1-4 Containment Fan Coolers

is an apparent violation of 10 CFR 50.49(f) and (k).

This lead to an

apparent violation of the above Technical Specifications because the

licensee operated the plant at various power levels and at hot

shutdown with all four fan coolers being inoperable due to a lack of

EQ documentation for the splices.

The root cause of the violation

appears to be the result of the licensee's failure to replace the

penetration to pigtail splices as part of the previous corrective

action for item 261/87-10-02.

This also is considered an apparent

violation of 10 CFR 50, Appendix B, Criterion XVI for failure to take

adequate corrective action for a known condition adverse to quality.

These concerns will be identified as Violation 50-261/88-36-02.

The

unresolved item (88-30-02) is now considered closed.

C. On September 14,

1988, while the plant was in cold shutdown for

maintenance, the licensee discovered that the Reactor Vessel Head

Vent System Solenoid operated valves were not properly installed to

meet EQ requirements and were not included on the Robinson Master

List of EQ equipment.

The licensee discovered this problem while

investigating some potentially generic EQ issues involving Target

Rock Solenoid valves that had been initially identified at the Harris

plant in August of 1988.

The extent of the deficiencies involved:

(1) failure to install

qualified penetration to pigtail splice configurations as discussed

in item b above; (2) failure to install conduit entrance seals at the

solenoid valve housing; and (3) failure to include the valves on the

Robinson EQ Master List.

The licensee took necessary corrective action by reworking the

solenoid valves to meet EQ requirements, installing cable entrance

seals, and reworking penetration splices. The inspector examined the

as-built configuration of the solenoid valves and confirmed that

cable entrance seals were installed.

Review of completed work

records confirmed that the solenoid valves were repaired and penetra

tion splices were replaced with a qualified configuration.

The Licensee Event Report (LER 88-020-00) indicated that the original

installation was intended to be fully EQ qualified.

The cable and

valves were purchased as EQ qualified.

However, at the time of

installation, the problems with containment penetration splices and

conduit entrance seals were not understood by the licensee to be

6

required to qualify the Target.Rock SOVs. Additionally, the licensee

indicated that the failure to include the NUREG 0737 Reactor Vessel

Heat Vent System in the EQ Program was an oversight since the Head

Vent System was installed prior to the compliance date for 10 CFR 50.49.

10 CFR 50.44(c)(3)(iii) requires the installation of high point vents

for the reactor coolant system, and the reactor vessel head to vent

non-condensable gases from the RCS which may inhibit core cooling

during natural circulation.

The licensee indicated that although

these valves may have been inoperable during a design basis event,

other methods would be available to remove voids from the reactor

vessel head area.

However, the failure to install the head vent

valves in a qualified configuration and the failure to include the

solenoid valves in the EQ Program is an apparent violation of both

10 CFR 50.44(c)(3)(iii) and 10 CFR 50.49(d), (f), (j) and (k).

This item will be identified as violation 50-261/88-36-03.

4. Exit Interview

The inspection scope and results were summarized on December 22, 1988,

with those persons indicated in paragraph 1. The inspectors described the

areas inspected and discussed in detail the inspection results listed

below. Although reviewed during this inspection, proprietary information

is not contained in this report.

Furthermore, dissenting comments were

not received from the licensee.

Violation 50-261/88-36-01, Unanalyzed Loss of Safety-Related MCCs 5 and 6,

paragraph 3.a.

Violation 50-261/88-36-02,

HVH 1-4 Penetration Splices Being Non-EQ,

paragraph 3.b.

Violation 50-261/88-36-03,

Non-EQ Reactor Vessel

Head Vent System,

paragraph 3.c.

5. Acronyms and Initialisms

AFW - Auxiliary Feedwater

BOP - Balance of Plant

CFR - Code of Federal Regulations

ECCS - Emergency Core Cooling System

EPA - Electrical Penetration Assembly

EQ - Environmental Qualification

FSAR -

Final Safety Analysis Report

HVH -

Reactor Containment Fan Cooler

LER - Licensee Event Report

MCC - Motor Control Center

PNSC - Plant Nuclear Safety Committee

7

QA - Quality Assurance

QC - Quality Control

RHR - Residual Heat Removal

SP - Special Procedures

URI - Unresolved Item