ML14191B116

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Insp Rept 50-261/89-08 on 890311-0417.Violations Noted. Major Areas Inspected:Operational Safety Verification, Surveillance Observation,Maint Observation,Esf Sys Walkdown & Onsite Followup of Events at Operating Power Reactors
ML14191B116
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 05/18/1989
From: Dance H, Garner L, Jury K
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14191B115 List:
References
50-261-89-08, 50-261-89-8, GL-88-17, NUDOCS 8906050210
Download: ML14191B116 (17)


See also: IR 05000261/1989008

Text

PkREG,

1

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

.1

101 MARIETTA ST., N.W.

ATLANTA, GEORGIA 30323

Report No:

50-261/89-08

Licensee:

Carolina Power and Light Company

P. 0. Box 1551

Raleigh, NC 27602

Docket No.:

50-261

License No.: DPR-23

Facility Name: H.. B. Robinson

Inspection Conducted: March 11. - April 17,

1989

Inspectors:

A.,2

.

.4

'l

L. W. Garner, Seni

Resfent Inspector

D te

igned

K. R., Jury, Resident insoctor

Date S gn d

Approved by: /

Q

4:

H. C. Danc , Section Chief

Date ig ed

Reactor Projects Section 1A

Division of Reactor Projects

SUMMARY

Scope:

This routine, announced inspection was conducted in the areas of operational

safety verification, surveillance observation, maintenance observation,

ESF

system walkdown, onsite followup of events at operating power reactors, mid

loop operations, dry storage of spent nuclear fuel, onsite review committee,

drawing system verification, and followup on previous inspection items.

Results:

One violation was identified involving a failure to follow a procedure.

A

personnel error by a licensed operator resulted in a reactor trip, paragraph

6.a.

Using TI 2515/101 as a guide, the inspectors verified that the licensee's

actions prior to and during mid-loop operations, successfully addressed the

recommended expeditious actions of Generic Letter 88-17, paragraph 7.

A failure of an Electro-hydraulic power supply resulted in a reactor trip. The

failure appeared to be a result of aging balance of plant equipment, paragraph

6.b.

83906050210 B9051B

PDR

ADOCYK 05000261

0

PNU

2

The practice of lifting leads to unnecessarily defeat safeguard logic to

preclude inadvertent ESF logic actuations during shutdowns was discussed with

plant management, paragraph 4.

A drawing system verification was conducted in accordance with Resident Action

Item 88-01. No areas of significant concern were identified, paragraph 10.

During this inspection period, the first dry shielded canister containing spent

fuel was successfully loaded into the horizontal storage module, paragraph 8.

Housekeeping practices. in the cointainment vessel need

improvement as

demonstrated by the various miscellaneous pieces of debris and trash observed

during a management inspection, paragraph.2.

REPORT DETAILS

1. Licensee Employees Contacted

R. Barnett, Maintenance Supervisor,' Electrical

C. Bethea, Manager, Training

R. Chambers, Engineering Supervisor, Performance

D. Cracker, Supervisor, Radiation Control

  • D. Crook, Senior Specialist, Regulatory Compliance
  • J. Curley, Director, Regulatory Compliance.

R.1

  • C. Dietz, Manager,

uronson Nuclear Project Department

R. Femal, Shift Forema~n, Operations

W. Flanagan, Manager, Design Engineering

W. Gainey, Support Supervisor, Operations

D. Knight, Shift Foreman, Operations

D. McCaskill, Shift Foreman, Operations

R. Moore, Shift Foreman, Operations

  • R. Morgan, Plant General Manager

D. Myers, Shift Foreman, Operations

D. Nelson, Maintenance Supervisor, Mechanical

  • M. Page, Acting Manager, Technical Support

D. Quick, Manager, Maintenance

D. Seagle, Shift Foreman, Operations

  • J. Sheppard, Manager, Operations

R. Steele, Acting Supervisor, Operations

H. Young, Director, Quality Assurance/Quality Control

Other licensee employees contacted

included technicians, operators,

mechanics, security force members, and office personnel..

  • Attended exit interview on April 24, 1989.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2. -Operational Safety Verification (71707)

The inspectors observed licensee activities to confirm that the facility

was being operated safely and in conformance with regulatory requirements,

and that the licensee management

control

system

was effectively

discharging its responsibilities for continued safe operation.

These

activities were confirmed by direct observations, tours of the facility,

interviews

and discussions with licensee management

and personnel,

independent verifications of safety system status and LCOs, and reviews of

facility records.

2

Periodically, the inspectors reviewed shift logs, operation's records,

data sheets, instrument traces, and records of equipment malfunctions to

verify operability of safety-related equipment and compliance with TS.

Specific items reviewed include control room logs, auxiliary operator

logs, operating orders, and equipment tag-out records.

Through periodic

observations of work in progress and discussions with operations'staff

members, the inspectors verified that the staff was knowledgeable of plant

conditions; responded properly to alarm conditions; adhered to procedures

and applicable administrative controls; and was

aware of equipment

out-of-service, on-going surveillance testing,-and maintenance activities

in progress.

The inspectors observed shift changes to verify that

continuity of system status was maintained and that proper control room

staffing existed. The inspectors also observed that access to the control

room was controlled and operations personnel were carrying out their

assigned duties in an attentive and professional manner. The control room

was observed to be free of unnecessary distractions.

The inspectors

performed channel checks,

reviewed component status and safety-related

parameters, including SPDS information, to .verify conformance with TS.

During this reporting interval, the inspectors verified compliance with

selected LCOs.

This verification was accomplished by direct observation

of monitoring instrumentation,

valve positions, switch positions, and

review of completed logs and records.

Plant tours were routinely conducted to verify the operability of stand-by

equipment; assess the general condition of plant equipment; and verify

that radiological controls, fire protection controls,

and equipment

tagging procedures were properly implemented.

These tours verified the

following: the absence of unusual fluid leaks; the lack of visual

degradation of pipe, conduit and seismic supports; the proper positions

and indications of valves and circuit breakers; the lack of conditions

which could invalidate EQ, the operability of safety-related instrumenta

tion; the calibration of safety-related and control instrumentation,

including area radiation monitors and friskers;

the operability of fire

suppression and fire fighting equipment; and the operability of emergency

lighting equipment.

The inspectors also verified that housekeeping was

adequate (except as noted below) and areas were free of unnecessary fire

hazards and combustible materials.

On April 10,

1989,

the inspectors accompanied plant management during

their closeout inspection of the CV.

This inspection was conducted in

preparation of Unit restart after work had been performed in the CV.

Several items of trash and miscellaneous debris were observed and removed.

These included: small pieces of insulating materials, partial rolls and

loose pieces of duct tape, small plastic bags,

and cable tie wraps. The

need to improve housekeeping practices in the CV was discussed with plant

management.

0II

3

In the course of the monthly activities, the inspectors included a review

of the licensee's physical security and radiological control programs.

The inspectors verified by general observation and perimeter walkdowns

that measures taken to assure the physical protection of the facility met

current requirements.

The inspectors verified station personnel adhered

to radiological controls.

No violations or deviations were identified within the areas inspected..

3. Monthly Surveillance Observation (61726)

The inspectors observed certain surveillance activities of safety-related

systems and components to ascertain that these activities were conducted

in accordance with license requirements.

For the surveillance test

procedures listed below, the inspectors determined that precautions and

LCOs were met, the tests were completed at the required frequency, and the

tests conformed to TS requirements and were accomplished by qualified

personnel in accordance with an approved test procedure.

Upon testing

completion,

the, inspectors verified that the recorded test data was

accurate, complete and met TS requirements,

and that test discrepancies

were properly rectified.

Specifically, the inspectors witnessed/reviewed

portions of the following test activities:

EST-048

(revision 6) Control Rod Drop Test

OST-406

(revision 6) TSC/EOF/PAP Diesel Generator

OST-617

(revision 8) Low Voltage Fire Detection and Actuation

System Zones 24, 25A, 25B, 25C, and 26

OST-910

(revision 11) Dedicated Shutdown Diesel Generator

No violations or deviations were identified within the areas inspected.

4. Monthly Maintenance Observation (62703)

The inspectors observed several maintenance activities on safety-related

systems and components to ascertain that these activities were conducted

in accordance with approved procedures and TS. The inspectors determined

that these activities did not violate LCOs, and that redundant components

were operable.

The inspectors also determined that activities were

accomplished by qualified personnel using approved procedures,

QC hold

points were established where required, required administrative approvals

and tagouts were obtained prior to work initiation, proper radiological

controls were adhered to, and the effected equipment was properly tested

before being returned to service. In particular, the inspectors observed/

reviewed the following maintenance activities:

WR/JO 89-AEDN1 - C S/G Tube Inspection

4

WR/JO 89-AEDS1 - HVH 4 Tube Inspection for Presence of

Biological Fouling

WR/JO 89-ADUB1 - Troubleshooting and Repair of E-H Power Supply

WR/JO 89-AEBK1

For several years,

the licensee has had an established practice of

defeating safeguard actuation logic when safeguards is not required to be

in-service per TS.

Specifically, logics for phase A and B containment

isolation, containment spray, and SI initiation are defeated by lifting

leads from their respective actuation relay coils.

The lifting of leads

and system restoration is controlled by procedure SPP-011,

Removal and

Restoration of SI Actuation.

This procedure contains verification sign

off steps that the lifted leads are reconnected.

However, the verifica

tion is not specified to be an independent process (i.e., the second

person does not necessarily verify the restored connections are tight).

Furthermore,

neither post-maintenance nor functional testing of the

restored system is performed. The manner in which safeguards is defeated

does not result in abnormal indications in the control room; restoration

of the system is strictly governed by administrative controls.

The

failure of these administrative controls is unlikely; however,

the

potential consequences of having safeguards unavailable if needed, are

large (i.e., severe accident).

In the past, utilization of SPP-011 has

sometimes been for reasons other than personnel safety and equipment

protection (i.e., eliminating the chance of an inadvertent ESF actuation,

thereby reducing the number of reportable events).

Defeating safeguard

logic for these other reasons constitutes an unnecessary defeating of

safeguards.

The currently authorized method of and reasons for defeating

safeguards is a poor practice.

The inspectors discussed with plant

management recommended controls for lifted wire leads contained in IEN

84-37, Use of Lifted Leads and Jumpers during Maintenance or Surveillance

Testing.

The inspectors requested that management review under what

conditions SPP-011 should be utilized, and whether development of an

alternate methodology is practical, preferably a method which would

provide indication. that safeguards is defeated.

Management agreed to

review their current utilization of SPP-011.

No violations or deviations were identified within the areas inspected.

5.

ESF System Walkdown (71710)

The inspectors performed a field walkdown of portions of the RHR system

located in the RHR pit and inside the CV.

Additionally, the SI

accumulator discharge piping from the accumulators to the RCS cold legs

was

inspected.

The

inspectors verified that the sub-systems are

configured as shown on drawings 5379-1082 sheet 4 (revision 20) and sheet

5 (revision 25)

and 5379-1484 sheet 1 (revision 16).

Items .examined

included pumps, valves, instrumentation, piping, and pipe supports. The

inspectors verified that all major valves were in their correct position,

5

manual valves were locked as required, instrumentation was valved into

service, and that power was available to MOVs,

as indicated by the RTGB

indicators and MCC breaker positions. Minor seal weepage (approximately 1

drop or less per minute) was observed on both the A and B RHR pumps.

The

licensee was already aware of and evaluating this condition. Additionally,

two conduit clamps on the hard conduit associated with SI-862A, the RHR

suction valve from the RWST,

were observed to be missing and loose.

This

condition was reported to the licensee for correction.

No conditions

which could render these sub-systems incapable of performing their safety

function were observed.

No violations or deviations were identified within the areas inspected.

6. Onsite Followup of Events at Operating Power Reactors (93702)

a. Personnel Error Causes Reactor Scram

On March 22, 1989, at 2:22 a.m., the reactor experienced a low-low

steam generator level trip from 100% power.

All ESF systems

performed

as expected.

The trip occurred when

an operator

inadvertently closed MS-V1-3A, the A main steamline isolation valve,

while performing OST-202,

Steam Driven Auxiliary Feedwater System

Component Test.

Step 7.2.30.3 of OST-202 requires closing MS-V1-8C,

the SDAFW C steam supply isolation valve. During performance of this

step, the nearby MS-V1-3A switch was operated instead of the MS-V1-8C

switch.

Failure to follow procedure OST-202 is a violation:

Failure

to Follow OST-202 Results in a Reactor Scram, (89-08-01).

The licensee performed a post trip review and returned the Unit to

service at 5:27 p.m., on March 22.

The inspectors reviewed the post

trip review and do not have any unresolved concerns.

b. E-H Power Supply Failure Initiates a Reactor Trip

On March 30,

1989, at 3:20 a.m.,

the reactor experienced a turbine

tri.p/reactor trip from 100% power.

The plant responded as expected

to the transient and all

ESF systems functioned as required.

Subsequent investigation by the licensee revealed that both the A and

B E-H +15 Vdc power supplies had blown fuses. Troubleshooting of the

A +15

Vdc power supply

revealed that several transistors were

leaking.

As a result, the licensee replaced five transistors in the

power supply.

Testing of other components in both the A and B E-H

power supplies did not reveal further cause for the failures.

The

licensee determined.that the most probable failure scenario involved

the following sequence:

-

Failure of the transistors in the A +15

Vdc power supply

resulted .in

an excessive output voltage.

6

A sensing circuit detected the overvoltage condition and blew

the A +15 Vdc power supply fuse as designed.

This circuit also

appeared to prepare the B power supply to pick up the load.

-

This preparation or feedback, plus the loading of the B power

supply, coupled with an output voltage set close to its maximum

limit, resulted in the B +15 Vdc power supply output fuse being

blown by its output voltage sensing circuit.

The licensee was unable to verify this failure sequence as the vendor

no longer employed anyone technically familiar with this obsolete

type of power supply.

The original drawings of the power supplies

had been transmitted to the licensee in late 1988; however, they

could not be located.

After repairs were completed, testing was

performed to demonstrate that the +15

Vdc power supplies would

function properly.

Included in this testing was turning the power

supplies on and off one at a time, with the turbine on-line and below

the turbine trip/reactor trip setpoint.

The inspectors witnessed

portions of this troubleshooting and testing.

In addition, the

inspectors attended a special PNSC which evaluated the actions taken

prior to Unit restart.

The inspectors determined that the licensee

performed as thorough a root cause determination as possible with the

information available.

During

the

November

1988 refueling outage,

the licensee had

originally planned to replace the E-H power supplies with a state of

the art model.

However, due to miscommunication with the vendor, all

the required replacement components were not ordered.

The licensee

then attempted to rebuild the power supplies; however, they were

limited to only a partial overhaul due to lack of available parts.

The most likely failure cause was end of life or aging. Much of the

BOP control systems are original hardware which is outdated.

This

situation has

been discussed with plant management.

A study,

initiated earlier this year, is in progress to evaluate what E-H

system improvements need to be made. Results of the study should be

available by the end of 1989.

c. Loose Part in C S/G

On April 2, 1989, at 7:09 p.m., 7:57 p.m., and 8:12 p.m., both the

secondary and primary side LPMS channels associated with the C S/G

alarmed.

The last alarm sealed-in and could not be. reset. Tours of

the secondary side, both inside and outside of the CV, as well as the

primary side of the C S/G, revealed no external cause for the LPMS

alarm.

Evaluation of the audio signals indicated that there was a

loose part in the C S/G hot leg channel head.

As a result, at 3:52

a.m.

the reactor was placed in hot shutdown.

Based upon a

recommendation from

Westinghouse,

the C RCP was left in service

until preparations were completed to enter the.C S/G.

Retrieval of

7

the loose part required the Unit to be placed in mid-loop operation.

Inspection of mid-loop operations per. TI 2515/101 is discussed in

paragraph 7.

On April 7, during removal of the manway diaphragm, a loose part fell

out of the S/G.

Having prepared for such a potential event, the part

was rapidly retrieved with tongs and placed in a lead pig.

Visual

inspection by a remote monitor identified the piece as a control rod

guide tube support pin nut (split pin nut).

The piece was found to

be approximately 1 inch in length, 0.75 inches in diameter, and 0.25

lbs.

in weight.

The piece was shipped to Westinghouse,

which

subsequently confirmed the piece as being a split pin nut with the

threaded section of the split pin stud contained within. Examination

by a scanning electron microscope of the pin shank fracture face

revealed that the failure of the pin shank-below the threaded area

resulted from stress corrosion cracking.

No previous failures of split pins have occurred at HBR; however,

similar failures have occurred at other plants. The only difference

between this occurrence and other industry occurrences is the long

-service time before failure.

Typically, split pin failures have

occurred within the first four or five years of commercial operation.

HBR has been in operation for eighteen years.

Westinghouse has

performed a safety evaluation, SECL-89-630, which justifies operation

of the Unit until the next refuelina' outage. The inspectors reviewed

this evaluation and attended the special PNSC meeting on April 10,

which reviewed Westinghouse's input and authorized restart of the

Unit. In summary, restart was authorized based upon the following:

(1) Operation with a broken split pin is not a concern since the

remaining section is trapped between the guide tube flange and

upper core plate, thereby still providing lateral support for

the guide tube as designed.

(2) Examination of the C S/G internals, including tubesheet, tube

ends, tube to tubesheet welds, divider plates, and tube sheet to

divider plate welds,

did not reveal conditions that required

immediate repair (initial phase of the inspection was observed

by the inspectors).

(3) Failure of other split pins would not cause damage to the

reactor or its internals which would result in a safety concern.

Transport of a loose part into a S/G would result in a forced

shutdown to remove it.

With regard to item (1) above, prolonged operation could result in

wear of the pin body, thereby allowing a limited amount of lateral

displacement of the bottom of the guide tube.

This could result in

additional RCCA frictional forces with the side of the guide tube,

8

resulting in an increase in scram time for the affected RCCA. Based

upon analysis for similar plants, the maximum scram time is not

anticipated to exceed the HBR TS value. However, as no analysis was

performed

specifically for

HBR,

Westinghouse

recommended the

following actions be taken:

(1) verify rod drop times prior to power

operation; (2) review previous rod drop data to assure no increasing

trend of rod drop times; and (3) evaluate.rod stepping tests for

abnormalities.

On April 11,

the licensee performed cold rod drop

tests and subsequently determined that there was not an increasing

trend for any rod.

The inspectors independently reviewed the rod

drop test times since November 1984,

and determined that there was

not a discernible pattern which would indicate degradation of any

RCCA scram time.

Cold rod drop times ranged between 1.14 and 1.30

seconds.

Comparison of previous hot and cold test data indicates

there is no significant difference between the times measured at cold

conditions and those measured at hot conditions.

The licensee anticipates an action plan will be developed by July

1989,

to address this issue during the upcoming refueling outages.

This issue is an IFI:

Review Long Term Resolution of Split Pin

Cracking Issue, (89-08-02).

d. RHR System Leakage Design Basis Not Met

On April 10,

1989, the licensee determined that potential leakage

into the RHR pit could not be successfully isolated under certain

accident conditions as required by the system design basis. Actions

taken by the licensee to address this item,

as well

as the

inspectors'

verification of these actions, will be discussed in

Inspection Report 89-09.

One violation was identified in the areas inspected.

7. Loss of Decay Heat Removal, GL 88-17 (TI 2515/101)

On October 17, 1988, the NRC issued GL 88-17, Loss of Decay Heat Removal.

On January 3, 1989, the licensee submitted to the NRC what actions they

had taken in implementing the eight GL recommended expeditious actions.

The inspectors reviewed the licensee's response and verified that the

actions committed to had been implemented prior to entering mid-loop

operations on April 6, 1989.

The

inspectors verified, via review of the lesson plan,

Mid-loop

Operations and Loss of Decay of Heat Removal,

and training records from

TI-906 and TI-301, that licensed operators were provided training on

previous applicable industry events that occurred during mid-loop

operations. This included the April 10, 1987 Diablo Canyon event, as well

as events at San Onofre 2 and Waterford 3. For each case, the sequence of

events,

safety concerns,

and contributing factors were addressed with

9

emphasis placed on applicability to HBR.

Special topics included

pressurization, vortexing, RHR flow changes, and instrumentation problems.

Through discussions with licensed operators, the inspectors verified they

were knowledgeable of the concerns associated with mid-loop operations.

The procedural changes to address the GL 88-17 action items were developed

subsequent to this training.

The inspectors verified, via interviews with

operations personnel,

that shift training was conducted on the revised

procedures prior to the shifts standing watch during mid-loop operations.

The inspectors consider item 1 of GL 88-17 as being satisfactorily

addressed.

The inspectors reviewed OMM-030,

Control of CV Penetrations During Mid

Loop Operations, revision 0, and GP-008,

Draining the Reactor Coolant

System,

revision 18.

The inspectors verified that these procedures

contain sufficient detailed instructions to establish and maintain CV

integrity as described in GL 88-17.

This meets GL 88-17 item 2. GP-008

also provides the requirements to record four core exit thermocouple

temperatures (one of the designated two trains) every 15 minutes and log

water level values every 15 minutes.

The water level values are taken

remotely from control room instrument LT-403 and locally at the B loop

standpipe (associated with LT-403) and at a standpipe installed on loop C.

The inspectors evaluated the routing of the C loop standpipe to ensure

that no conditions existed to render the indicated level inaccurate.

The

inspectors also visually verified that the B loop and C loop standpipes

provided consistent level data and that this data,

as well as temperature

data was recorded every 15 minutes. In addition, GP-008 provides that one

SI pump and one charging pump must be available with injection pathways,

prior to reducing water level to -36 inches below the RV flange.

These

procedure requirements are sufficient to address items 3, 4, and 6 of GL 88-17.

GP-008 also contains a caution note to: "Avoid any evolution that could

result in perturbation of the RCS while in a reduced inventory condition.

This includes anything that could impact RCS level, the operating train of

RHR,

or any required support equipment."

The inspectors consider this

caution note coupled with the recovery steps provided in AOP-020, Loss of

Residual Heat Removal (Shutdown Cooling), Revision 6, to be adequate to

address item 5 of GL 88-17.

The licensee's response concerning use of aluminum nozzle covers on the

S/G to preclude materials from falling into the RCS is considered adequate

to address item 7 of the GL 88-17.

However, the inspector requested the

licensee to establish measures to ensure this item is addressed if nozzle

dams are used in the future at HBR.

The inspectors determined that

item 8, concerning loop stop valves, is not applicable to HBR, as HBR does

not have loop stop valves.

Based upon the above described inspections, the inspectors considered that

the licensee has taken satisfactory interim measures to address the eight

expeditious actions of GL 88-17 (which preclude or successfully mitigate

10

the loss of decay heat removal during reduced inventory conditions.)

The

inspectors plan to review implementation of the six programmed enhancement

recommendations of GL 88-17 as they are completed.

No violations or deviations were identified in the ares inspected.

8. Loading of First DSC Into HSM (TI 2690/004)

On March.16, 1989, the inspectors witnessed the alignment and loading of

the first DSC containing spent fuel assemblies into the HSM.. . The

inspectors verified that the docking of the trailer and movement of the

DSC into the HSM.was performed in accordance-with procedure ISFS-004,

Alignment and Loading of the Dry Shielded Canister into the Horizontal

Storage Module, revision 4. The inspectors verified that HP practices and

procedures were adhered to during this operation.

Additionally, the inspectors reviewed ISFS-006, Startup Monitoring of the

Horizontal Storage Module, revision 0. ISFS-006 acceptance criteria for

dose rates are less than 200 mrem/hr (neutron + gamma) at center of air

inlets or outlets and front access cover,

and less than 50 mrem/hr

(neutron + gamma)

at other locations.

Data taken indicated that these

acceptance criteria were met.

Maximum total neutron and gamma doses

measured were 40.5 mrem/hr at the front air outlet (200

mrem/hr

allowable),

20.5 mrem/hr on the roof (50 mrem/hr allowable),

and 15.5

mrem/hr at the air inlet (200 mrem/hr allowable).

The maximum neutron

dose measured was 2.5 mrem/hr in front of the HSM. In addition, the air

temperature rise through the HSM was shown to be 28 degrees F, well below

the 100 degrees F allowable.

On April 12,

1989,

a second DSC was loaded into the HSM.

Measured

radiation dose rates for the second DSC were similar to those described

above for the first DSC.

The inspectors plan to periodically monitor

future activities involving the DSCs and their respective loadings into

the HSMs.

No violations or deviations were identified in the areas inspected.

9. Onsite Review Committee (40700)

The inspectors evaluated certain activities of the PNSC to determine

whether the onsite review functions were conducted in accordance with TS

and other regulatory requirements. In particular, the inspectors attended

the March 30,

1989 PNSC concerning the E-H power failure, the April 10,

1989 PNSC concerning the loose part in C S/G and RHR pit leakage, and the

April

13,

1989

PNSC concerning the RHR pit leakage issue.

<It was

ascertained that provisions of the TS dealing with membership, review

process,

frequency,

and qualifications were satisfied.

The inspectors

followed

up

on selected previously identified PNSC activities to

independently confirm that corrective actions were progressing

satisfactorily.

11

No violations or deviations were identified within the areas inspected.

10.

Drawing System Verification

The inspectors performed an inspection per RAI 88-01 of the licensee's

drawing control system.

The inspection consisted of:

(1) a drawing

quality review (legibility); (2) current revision verification; (3)

verification that drawings reflect as-built configuration; (4) review of

the drawing backlog requiring changes; and (5) review of controls to

maintain marked up drawings prior to permanent revisions.

Items (1) and

(5) involved review of the controlled copies assigned to the control room.

Item (2) involved controlled copies assigned to the control room and the

EOF.

The drawing control system associated with drawings important to

facility operation was found to be adequate, with minor exceptions.

Legibility of drawings was found to be acceptable.

All major flow path

components on P&IDs were readable.

Cross references.from one line to

another were readable. A small number of vent valves, drain valves and

instrument numbers were legible, although difficult to read.

Examples

include: instrument TE-3092C on G-190199 sheet 1, valve SW-88 on G-190199

sheet 6, instruments TX-1683B and PX-1619 on G-190199 sheet 9, valves

SW-548 and SW-549 on G-190199 sheet 4, and valve CAR-10 on G-190197 sheet

2. On sheet 11 of G-190199, a valve adjacent to valve SW-616 on piping

line 2-CW-280 was not readable.

One example was identified in which the

revision number was not legible (drawing 5379-3232).

Each P&ID maintained

in the control room for major systems are in plastic folders.

This

practice greatly reduces the amount of drawing wear and tear which would

normally otherwise occur. Safeguards System and Reactor Protection System

drawings contain many relay contacts and instrument.numbers which are

difficult to read.

However, by comparing similar components in the other

division, process of elimination, and/or deductive reasoning,

(e.g.

sequence and patterns of labeling nomenclature),

it is possible to deduct

the proper numbers.

This area could be improved.

Eighty-eight drawing revisions were audited for latest revision number by

comparing the field revision with that contained in the master index or

with the current document control drawing.

Discrepancies were not

identified in the control room drawings set; however, the drawings in the

EOF were observed to have three discrepancies.

An outdated revision of

drawing G-1990199 had not been removed.

Sheets 3 and 4 of drawing

5379-1082 were misfiled with HBR2-8255 sheet 5.

Revision 13 of drawing

5379-3238 was filed in the proper place; however, the latest revision,

number 14, was filed in front of the set of drawings. The TSC drawing set

was not audited, as the same individual responsible for the EOF drawings

is also responsible for the TSC drawings. The licensee conducts an audit

program which verifies proper revisions and current condition of each

controlled drawing set.

During review of this program, the inspectors

discovered that the audit scope and frequency were not procedurally well

defined.

Thus,

when drawing personnel were changed in 1987, the audit

12

scope changed due to a misunderstanding of what had been done previously.

The inspectors also determined that the master index (hard copy) had four

erroneous entries (i.e., revision numbers were not updated when the

drawings were issued).

This condition apparently occurred earlier in the

year when reassignment of duties resulted in a different individual being

responsible for maintaining the master index current. In each instance,

the computer-based system, utilized by operations, contained the correct

information.

Selected portions of the SI,

RHR,

and Feedwater Systems drawings were

as-built verified by field walkdowns.

No major discrepancies were

identified.

The P&IDs as structured by the licensee do not contain

instrument vent, drain, and other instrument valving downstream of the

instrument root isolation valves.

The inspectors observed that check

valves were not consistently tagged.

Also, several valve tags were

missing.

Examples include FCV-1424 and-small test vent and drain valves.

With one exception, all configurations were correct as shown.

Flow

element FE-1425C and associated root valves AFW-96 and AFW-97 are shown on

sheet 4 of G-190197 as being located in the AFW pump room.

A November

1988 outage modification moved the flow element to the auxiliary building

hallway.

The inspectors were unable to determine before issuance of this

report if a change had been initiated to correct G-190197.

Revisions to drawings are controlled in accordance with MOD-004,

Plant

Drawing Preparation, Revision, and Approval.

Attachment 6.3 of MOD-004

requires updating of priority A drawings within 28 working days of

submitted changes to drafting.

Priority B drawings are required in 35

working daysand priority C drawings are to be issued within 60 days.

Flow, logic, safeguard, reactor protection, and control wiring diagrams

are assigned a priority A. Valve and instrument lists, as well as piping

and electrical penetration drawings are categorized as priority B.

The

drawings in the control room,

TSC and EOF are generally priority A

drawings.

A review of the outstanding drawing revision index did not

reveal a backlog of priority A and B drawings, (i.e., outstanding A and B

priority drawing revisions were either in process, or the change had just

been received).

Review of revision issue dates for this year indicated

that the' 28 and 35 day requirements were being met.

During the last

refueling outage, priority A and B drawings were completed prior to

declaring modifications operable. Thus, there are no "red-lined" drawings

currently in use.

MOD-004 does provide for issuing a drawing revision

notification to all controlled drawing copy holders if a drawing revision

is not anticipated to be available when needed.

In summary, the drawing control 'system is well maintaining drawings most

likely required to be referenced during normal and emergency operating

situations with only minor exceptions as noted above. The exceptions were

discussed with the licensee for correction as they deem necessary.

No violations .or deviations were identified within the areas inspected.

13

11.

Licensee Action on Previously Identified Inspection Items (92701)

(CLOSED) LER 87-30, Non-redundant Power Supply To Vital Equipment Due to

Original System Design.

On December 20,

1988,

the licensee declared

Modification M-966 operable.

M-966 corrected the single failure design

problem by installing two redundant pressure switches,

PC-600A and

PC-601A, such that each switch is associated with only one division of

SI-862 and SI-863 valves.

Switch PC-600A is wired into the control

circuit for SI-862B -and 863B; switch PC-600B is wired into the control

circuit for SI-862A and 863A.

Hence, the failure of one switch would

affect only the valves of its respective division.

The inspectors

verified that the redesigned circuit meets the single failure criteria,

the switches had been calibrated, and the acceptance test performed was

adequate to demonstrate proper functioning of the valve interlocks.

(OPEN) IFI 88-28-05, Licensee to Develop Methodology to Detect Biological

Growth in HVH 1-4.

During the November 1988 refueling Outage, the

licensee modified the SW System to control the biological growth in the SW

System by chlorination.

The purpose was to reduce the potential for

biological fouling of components served by the SW System (i.e., the CV fan

coolers).

On April 9, 1989, the inspectors witnessed inspection of the

HVH-4 upper tube bundle.

An insignificant amount of what may have been

biological material was observed at the tube edges. This material did not

effect the SW flow through the cooler; however, six tubes were partially

blocked by foreign material,

possibly weld slag.

The small number of

affected tubes have no impact on the operability of the cooler.

Based

upon the inspection, the chlorination program appears to be successfully

controlling biological growth.

During early April,

a monitoring system was installed to help detect

fouling in HVH-4.

This item remains open pending review of the

effectiveness of this system and the effectiveness of the chlorination

system during different seasons.

No violations or deviations were identified within the areas inspected.

12.

Exit Interview (30703)

The inspection scope and findings were summarized on April 24,

1989, with

those persons indicated in paragraph 1.

The inspectors described the

areas inspected and discussed in detail the inspection findings listed

below and those addressed in the report summary. Dissenting comments were

not received from the licensee.

Proprietary information is not contained

in this report.

14

Item Number

Description/Reference Paragraph

89-08-01

VIO

-

Failure to Follow OST-202,

Resulting in a Reactor Scram,

paragraph 6.a.

89-08-02

IFI -

Review Long Term Resolution of

Split Pin Cracking Issue,

paragraph

6.c.

13.

Acronyms and Initialisms

AOP

Abnormal Operating Procedure

AFW

Auxiliary Feedwater

BOP

Balance of Plant

CV

Containment Vessel

DSC

Dry Shielded Canister

  • E-H

Electro-hydraulic

EOF

Emergency Operation Facility

ESF

Engineered Safety Feature

EST

Engineering Surveillance Test

F

Fahrenheit

FCV

Flow Control Valve

FE

Flow Element

GL

Generic Letter

GP

General Procedure

HBR

H. B. Robinson

HP

Health Physics

HSM

Horizontal Storage Module

HVH

Heating Ventilation Handling

IFI

Inspector Followup Item

ISFS

Independent Spent Fuel Storage

LCO

Limiting Condition for Operation

LER

Licensee Event Report

LPMS

Loose Parts Monitoring System

LT

Level Transmitter

MCC

Motor Control Center

MOV

Motor Operated Valve

mrem/hr

millirem/hour

MS

Main Steam

NSSS

Nuclear Steam Supply System

OMM

Operations Management Manual

OST

Operations Surveillance Test

P&ID

Piping and Instrumentation Diagram

PAP

Personnel Access Portal

PNSC

Plant Nuclear Safety Committee

RAI

Resident Action Item

RCP

Reactor Coolant Pump

RCS

Reactor Coolant System

RHR

Residual Heat Removal

15

RTGB

Reactor Turbine Generator Board

RV

Reactor Vessel

SDAFW

Steam Driven Auxiliary Feedwater

S/G

Steam Generator

SI

Safety Injection

SPDS

Safety Parameter Display System

SPP

Special Process Procedure

SW

Service Water

TI

Temporary Instruction

TS

Technical Specification

TSC

Technical Support Center

Vdc

Volts Direct Comment

WR/JO

Work Request/Job Order