ML20150B297

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Forwards SALP Rept 50-352/87-99 for Feb 1987 - Apr 1988. Util Will Be Contacted to Schedule Meeting to Discuss Results
ML20150B297
Person / Time
Site: Limerick Constellation icon.png
Issue date: 07/07/1988
From: Russell W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To: Corbin McNeil
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
Shared Package
ML20150B299 List:
References
NUDOCS 8807110464
Download: ML20150B297 (3)


See also: IR 05000352/1987099

Text

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47 JUL 1988

Docket No. 50-352/NPF-39

Philadelphia Electric Company

ATTN: - Mr. C. A. >kNeill

-Executive Vice President-

Nuclear

2301 Market Streer

Philadelphia, Pennsylvania 19101

Gentlemen:

Subject: Sys+.ematic Assessment of Licensee Performance (SALP) Board Report

Number 50-352/87-99

- An NRC SALP bled has reviewed and evaluated the performance of activities at

the Limerick Gederating Station for the period of February 1,1987 through

April 30, 1988. The results of this assessment are documented in the enclosed

SALP Board Report. We will contact you soon to schedule a meeting to discuss

the SALP evaluation.

L

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At the SALP meetitg you should be prepared to discuss our assessments and your

plans to improve performance. The meet' g is intended to be a candid dialogue

wherein any comments you may have regarding our report are discussed.

Additionally, you may provide written comments within 20 days after the

meeting.

Your cooperation with us is appreciated.

Sincerely,

Originni Signed 37

ELIM T. P.US3M

William T. Russell

Regional Administrator

Enclosure: SALP Board Report No. 50-352/87-99

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0FFICIAL RECORD COPY SALP LIM 1 87-99 - 0001.0.0

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. Philadelphia Electric Company 2

07 JUL 1988

cc w/ enc 1:

John S. Kemper, Sr., Senior Vice President - Nuclear

E. C. Kistner, Chairman, Nuclear Review Board

Graham M. Leitch, Vice President, Limerick Generating Station

J. W. Gallagher, Vice President - Nuclear Services

Troy B. Conner, Jr. , Esquire

Eugene J. Bradley, Esquire, Assistant General Counsel

W. M. Alden, Director, Licensing Section -

Dave Honan

K. Abraham, PA0 (13)

Public Document Room (PDR)

local Public Document Room (LPDR)

Nuclear Safety Information Center (NSIC)

NRC Resident Inspector

Commonwealth of Pennsylvania

Chairman Zech

Commissioner Roberts

Commissioner Carr

Commissioner Rogers

bcc w/ encl:

Region I Docket Room (with concurrences)

Management Assistant, DRMA (w/o enc 1)

Section Chief, DRP

Robert J. Bores, DRSS

Region I SLO

W. Johnston, DRS

G. Sjoblom, DRSS

J. Taylor, DED0

W. Russell

J. Allan

J. Lieberman, OE

D. Holody

Board Members

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  • Gramm/rhl * Wenzinger *Kane A lan Russell

6/ /88 6/ /88 6/ /88 y/h/88 f/ /88

  • See previous concurrences

0FFICIAL RECORD COPY SALP LIM 1 87-99 - 0001.1.0

07/05/88

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Philadelphia Electric Company 2

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John S. Kemper, Sr., Senior Vice President - Nuclear g

E. C. Kistner, Chairman, Nuclear Review Board

Graham M. Leitch, Vice President, Limerick Generating Station

J. W. Gallagher, Vice President - Nuclear

Troy B. Conner, Jr., Esquire

Eugene J. Bradley, Esquire, Assistant General Counsel

W. M. Alden, Director, Licensing Section

Dave Honan

X. Abraham, PA0 (13)

Public Document Room (PDR)

Local Public Document Room (LPDR)

Nuclear Safety Information Center (NSIC)

NRC Resident Inspector

Commonwealth of Pennsylvania

Chairman Zech

Commissioner Roberts

Commissioner Carr

Commissioner Rogers

bcc w/enci:

Region I Docket Room (with concurrences)

Management Assistant, DRMA (w/o enc 1)

Section Chief, DRP

Robert J. Bores, DRSS

Region I SLO

W. Johnston, DRS

G. Sjoblom, DRSS

J. Taylor, DEDO

W. Russell

J. Allan

J. Lieberman, OE

D. Holody

Board Members

H. Eichenholz

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RI:D F !9 RI:DRA RI:RA

Gramm/rhl k nger K Allan Russell

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ENCLOSURE

SALP BOARD REPORT

U. S. NUCLEAR REGULATORY COMMISSION

REGION I

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

INSPECTION REPORT NO. 50-352/87-99

PHILADELPHIA ELECTRIC COMPANI

LIMERICK GENERATING STATION

UNIT 1

ASSESSMENT PERIOD: FEBRUARY 1, 1987 - APRIL 30, 1988

BOARD MEETING DATE: JUNE 8,1988

8807110470 880707

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TABLE OF CONTENTS

Page

I. INTRODUCTION ...... ................. 3

A. Purpose and Overview . . . . . . . . . . . . . . . . . 3

B. SALP Board Members . . . . . . . . . . . . . . . . . . 4

II. CRITERIA ..... . ................... 5

III. SUMMARY OF RESULTS . ................... 6

A. Overall Evaluation . ................. 6

B. Background Activities. . . . . . . . . . . . . . . . 7

1. Licensee. . . . . . . . . . . . . . . . . . . . . 7

2. Inspection. . .................. 9

C. Performance Summary. . ........ ....... 10

D. Unplanned Shutdowns, Scrams and Forced Outages . . . . 11

IV. PERFORMANCE ANALYSIS . . . . . . . . . . . . . . . . . . . 13

A. Plant Operations . . . . . . . . . . . . , , . . . . . 13

B. Radiological Controls ................ 16

C. Maintenance .... ................. 20

D. Surveillance . .. .................. 24

E. Engineering / Technical Support. ............ 27

F. Emergency Preparedness . . . . . . . . . . . . . . . . 31

G. Security and Safeguard: ...........,... 33

H. Safety Assessment / Quality Verification . . ...... 36

V. SUPPORTING DATA AND SUMMARIES . . . . . . . . . . . . . . . 39

A. Investigations and A11egaticns . . . . . . . .... 39

8. Escalated Enforcement Actions ............ 39

C. Management Conferences . . . . ............ 39

D. Licensee Event Reports . . . . ............ 39

1. Report Quality. .............. .. 39

2. Causal Analysis . ................ 40

Tables

Table 1 - Inspection Hours Summary ................. 43

T&ble 2 - Enforcement Summary . . .................. 44

Table 3 - Licensee Event Reports .................. 45

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I. INTRODUCTION

A. Purpose and Overview

The Systematic Assessment of Licensee Performance (SALP) is an ~

integrated NRC staff effort to collect observations and data on a

periodic basis and to evaluate licensee performance. The SALP pro-

cess is supplemental to normal regulatory processes used to ensure

compliance to NRC rules and regulations. SALP is intended to be

sufficiently diagnostic to provide a rational basis for allocating

NRC resources and to provide meaningful guidance to the licensee's

manacement to improve the quality and safety of plant operations.

An NRC SALP Board, composed of the staff members listed in Section B,

met on June 8, 1988 to review the collection of performance observa-

tions and data to assess the licensee's performance at the Limerick

Generating Station Unit 1. This assessment was conducted in accor-

dance with the guidance in NRC Manual Chapter 0516, "Systematic

Assessment of Licensee Performance." A summary of the guidance and

evaluation criteria is provided in Section 11 of this report.

This report is the SALP Board's assessment of the licensee's safety

performance at the Limerick Generating Station Unit 1 for the period

February 1, 1987 through April 30, 1988. The summary findings and

totals reflect a 15-month assessment period.

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B. SALP Board Members

Chairman

W. F. Kane, Director, Division of Reactor Projects (DRP),

Members

W. Johnson, Director, Division of Reactor Safety

G. Sjoblom, Acting Director, Division of Radiation Safety and

Safeguards

W. Butler, Director, Projects Directorate I-2, NRR

R. Capra, Acting Chief, Projects Branch No. 2, DRP-

R. Gallo, Chief, Operations Branch, DRS

S. Collins, Deputy Director, DRP (Part Time)

E. Kelly, Chief, Technical Support Section, DRP

J. Linvillo, Chiof, Projects Section 2A, DRP

R. Clark, Project Manager, NRR

Others

T. Kenny, Senior Resident Inspector, Limerick Unit 1

L. Scholl, Resident Inspector, Limerick Unit 1

R. Gramm, Senior Resident Inspector, Limerick Unit 2

T. Johnson, Senior Resident Inspector, Feach Dottom

J. Williams, Project Engineer, DRP

J. Gadzala, Reactor Engineer, DRP

W. Pasciak, Chief, Effluents Radiation Protection Section, DRSS

T. Dragoun, Senior Radiation Specialist

R. Summ2rs Emergency Responsive Coordinator, DRSS

R. Keimig, Chief, Security and Safeguards Section, DRS

H. Gregg, Senior Reactor Engineer, DRS

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II. CRITERIA

Licenseo performance is assessed in selected functional areas. Each

functional area represents areas significant to nuclear safety and

the environment, and are normal programmatic areas. The following

evaluation criteria were used as appropriate to assess each '

functional area.

l. Management involvement in assuring quality

2. Approach to resolution of technical issues from a safety standpoint

3. Responsiveness to NRC initiatives

4. Enforcement history

5. Reporting, analysis and corrective actions for operational events.

6. Staffing (including management)

7. Training effectiveness and qualification programs

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Based upon the SALP Board assessment each' *ianctional area evaluated

is classified into one of these performance categories. The definitions

of these performance categories are:

Cate_ gory 1. Reduced NRC attention may be appropriate. Licensee

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management attention and involvement are aggressive and oriented

toward nuclear safety; licensee resources are ample and effectively

used so C'at a high level of performance with respect to operational

safety is aeing achieved.

Category 2 NRC attention should b; maintained at-normal levels.

Licensee ranagement attention and involvement are evident and

conce.ner with nuclear safety; licensee resources are adequate and

reason'aly effective such that satisfactory performance with respect

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to operational safety is being achieved.

Category 3. Both NRC and licensee attention should be ine-eased.

Licensee management attention or involvement is acceptable and

considers nuclear safety, but weaknesses are evident; licensee

resources appear strained or not effectively used so that minimally

satisfactory performance with respect to operational safety is being

achieved.

Trend: The SALP Board may dacide to include an appraisal of the

performanca trend of a functional area. Normally, this ti end

will only be used when both a definite trend of performance is

discernible to the Board, and the Board believes that

contir.vation of the trend will result in a change of performance

level.

Improv jin : Licen.see performance was determined to be improving

near the close of the assessment period.

Declini_ng: 1.icensee performance was determined to be declining i

near the close of the assessment period.  !

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III. SUMMARY OF REST ' s

A. Oveiall Evalui ,

During the asse- .t period site performance has remained strong

despite additio... pressure associated with a major corporate reorgani-

zation. Site ranagement has been very effective in providing the

leade.- ship necessary te achieve this per'ormance, to maintain good

morale and to fo ,ter a strong safety perspective throughout the site

organization. The completion cf the reversal in oerformance in the

security area of two SALP periods ago, resulting in excellent

performance in the security area during the current assessment

period, is the result of strong site management with support from

corporate management.

While co: 2 rate support was evident for the security crea, in other

areas se:n as engineering and technical support, and emergency

preparedness inef fective c.orporate oversight and support has resulted

in a decline in performance. In the area of energency preparednes>

lack of corporate accountability and oversight extends back into the

previous assessment period. While the reorganization has resulted in

enhancements in oversight functions associated with the offsite Nuclear

Review Board and the unification of the previously fragmented quality

organization, further corporate management attention appears to be

necessary to assure accountability from corporate A.pport groups.

Strong performance has continued in plant operations, radiological

controls, maintenance and surveillance. In opera tions a strong team

of operators, operations roanagement, technical support and site

managers have produced a safe operating record. In spite of an

unanticipated outage extension, ALARA performance was effective and

total radiation exposures compared favorably with other newly licensed

BWRs this period. Corporate support for the radiological environ-

mental monitoring wus de.nonstrated in that activities in this area

were effectively carried out by contractors. Improvements are

evident in the site management of maintenance work backlogs and

control of contractors. Deficiencies in maintenance procedures are

being correcteJ and the conduct of maintenance and surveillar.ce is

typified by strict adherence to procedures. Safety review committees

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are used effectively.

Site management and supervision have been effective in maintaining a

positive attitude of teamwork at all levels of the orgcnization.

This is considered to be the principal factor in the continuation of

the overall strong performance exhibiter' in prior SAlP periods.

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B. Background Activities

1. Licensee

Unit 1 completed a 198-day continuous power run at the end of

the previous assessment, followed by a controlled shutdown to

repair three valves that were contributing to drywell leakage.

The unit began the assessment period at full power and remained

at _ power for the next three and a half months in an end-of-cycle

coastdown mode of operation towards the first refueling outage

which began on May 15, 1987.

The first Unit I refueling outage lasted 108 days. Major

activities consisted of: full core offload for refueling and

core alterations; a containment integrated leak rate test;

license condition modifications including tie-in of the standby

gas treatment system to the refueling floor; major cnrrective

maintenance to 20 control rod drives, rebuilding of feedwater

valves, the replacement of all 14 main steam safety relief

valves, and extensive preventive maintenance including tear-down

and overhaul of Reacter Core Isolation Cooling, (RCIC), all four

diesel generators and the main generator and turbine.

Startup from the outage began on August 26 and, following minor

repairs to High Pressure Coolant Injection (HPCI) steam supply

valves, the main generator was synchronized to the grid on

August 31. Power ascension occurred over the period September 1

through 7 to 83% power. An automatic scram occurred on

September 7 due to a turbine trip on high water level in a

moisture separator because of an isolated instrument air supply

to the moisture separator level centrols. Recovery from the

scram began the following day and full power was achieved by

September 17. Full power operation cont:nued for approximately

five days until an automatic scram occurred on September 19, due

to a turbine trip caused by rupture of a weld on an electre-

hydraulic control (EHC) system line to a main turbine control

., valve.

Recovery from the September 19 scram began the following day,

but the unit remained at 85% power for the foi:ow~;g two months

until November 21 while investigations proceeded to a solution

for the turbine EHC system vibrations. On November 21, 1987,

Unit I was returned to full power.

Full power operation continued for 126 consecutive days until a

fuel cladding leak was discovered on March 25, 1988 as evidenced

by increased steam jet air ejector radiation levels. The

licensee suspected the leak to be a form of crud-induced

localized corrosion. No detectable increase in offgas releases

was experienced, although coolant radioiodine activities

increased by a factor of about ten. Reactor power was

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maini:ained below 85% as a precautionary measure for the next

two weeks until a planned shutdown was begun on April 8

following 195 consecutive days at power since September 19,

1987.

The planned outage lasted 10 days and was for condenser tube

cleaning and circulating water system improvements. Feedwater

valve repairs, Intermediate Range Monitor (!RM) replacements and

several modifications were also accomplished. Unit 1 was

returned to power on April 22. At the end of the assessment

period Unit I was operating at reduced power because of the feel

leak.

Organizational changes at the station level and at corporate

occurred throughout the assessment, including reassignment of

the station manager to Peach Bottom and announcement of a new

station manager on January 1, 1988. The prospective station

manager remained in a special license familiarization training

program through the end of this assessment period, and is

expected to assume the duties of Limerick Unit 1 Station Manager

in August 1988.

The licensee announced a major corporate reorganization of the

company's Nuclear Operations and Support Services which became

ef fective or November 1,1987. Changes included creation of: a

Vice President for the Limerick Station, assumed by the former

Unit 1 Plant Manager; torporate Vice Presidents for r,ewly formed

Divisions of Nuclear Services and Nuclear Engineering; and a

Senior Vice President, Nuclear. The reorganization also involved

recenstituting the Nuclear Review Board (NRB) to include member-

ship of three senior executives outside of PEco. The sita

oroanizations operated in c transition for the latter part of

.-is assessment. The Vice President of Limerick remained in an

ace J station manager position tnrough the end of the assessment

period.

On February 2, 1988, the President and Chief Operating O'(icer

announced his retirement effective Maren 1, 1988. On February

16, 1988, a new Executive Director Nuclear from outside the

PECo organization was announced who subsequently

became a PECo employee and assumed the title of Executive Vice

President Nuclear on March 13, 1988. The company's Cnairman and

Chief Executive Officer announced his retirement effective April

13, the date of the licensee's annual board meeting. The Bot.,f of

Directors elected a new Chairman and Chief Executive Officer,

a former PECo Vice President who had recently been ?lected

President and Chief Operating Officer at another utility.

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2. Inspection

Two NRC resident inspectors were assigned to the site during the

assessment period. A new resident inspector was assigned in

December 1987 and a new senior resident in March 1988. The

total NRC inspection time expended during the 15 month assess-

ment period was 4,032 hours3.703704e-4 days <br />0.00889 hours <br />5.291005e-5 weeks <br />1.2176e-5 months <br /> or 3,226 hours0.00262 days <br />0.0628 hours <br />3.736772e-4 weeks <br />8.5993e-5 months <br /> on an annualized

basis. Distribution of these hours by functional area is

depicted in Table 1. A summary of enforcement activities is

provided in Table 2.

During this assessment perioJ, the second year of commercial

operat.ons was reviewed as well as the Unit 1 initial refueling

outage. NRC inspec' ion teams evaluated restart from the

refueling outage in August 1987, the environmental qualification

programs in February 1988 and an emergency preparedness exercise

on April 6, 1988.

This report includes evaluation of Safety Assessment / Quality

Verification as a new functional area. The topics assessed in

this new area include Licensing activities as well as what

was formerly covered under the Assurance of Quality. Also,

Training and Qualifications is no longer a separate functional

area and is included.

Refueling activities were evaluated as part of the Er.gineering/

Technical Support . functional area for the first time during this

assessment period. Fire protection is assessed, ao in previous

assessments, in the functional area of Operations, since there

was no special programmatic inspection in this area. House-

keeping is irciaded in the area of maintenance. Security

concinued to receive increased inspection effort, as in previous

assessments, because of past identified weaknesses.

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C. Performance Summa _ry

Functional Category Category

Area last Period Ttis Period

(2/1/86 - 1/31/87) (2/175, - 4/55788)

'A. Plart

Operations 1 1

B. Radiological

Controls 1 1

C. Maintenance 1 1

D. Surveillance 1 1

E. Engineering / Technical 1 2

Support

F. Emergency

Preparedness 1 2

G. Security and

Safeguards 2 1

H. Safety Assessment /

Quality Verification 1

I. Training & Quali-

fication Effectiveness

1

J. Licensing Activities 2 ***

K. Assurance of Quality 1

  • Not evaluated as a separate functional area last period
    • Criterien for all functional areas, and no longer a separate area
      • Now evaluated under Safety Assessmer.t

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D. Unplanned Shutdowns, Scrams and Forced Outages

Date & Root Functional

Power Level Description Cause Area

6/12/88 Defueled Reactor scram signal Inedequate Operations

during refuel outage procedure

with core offloaded due compounded

to radiography in by blocking

the vicinity of the deficiency

main steam line

radiation monitors.

9/7/87 83% Automatic scram upon Drawing did Engineering

closure of the turbine not include

stop valves caused by individual

high level in a moisture tag nos. for

separator. Instrument instrument air

air valve was not root valves

properly positioned.

9/19/87 90% Automatic scram due to EHC weid Engineering

a main turbine trip failure induced

caused by the failure by new load due

of a pipe weld in the to EHC modift-

turbine electrohydraulic cations

control system. A leak

at the failed weld was

discovered and & plant

shutdown from full

power was in progress at

the time o) the scram.

4/9/88 <1% Automatic scram due to Personnel Operations

a high flux trip while error

power was in the inter-

mediate range during a

planned shutdown. A

half scram had been ,

manually inserted due

to IRM inoperability

and when power increased

due to moderator tempera-

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ture decrease a trip signal

l was generated by the 'C'

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intermediate range monitor

(IRM) while set on range 2.

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Date &- Root Functional

Power Level Description Cause Area

4/9/88 0% Auton.atic Scram While

in cold shutdown Component N/A

an upscale spike failtire

occurred on the 'F'

channel IRM (Range 1)

due to the failure of

the detector. This

spike in conjunction

with a manually inserted

half scram (due to

inoperable IRMs) caused

a full scram. All rods

were fully inserted at

the time of the scram

thus no rod motion occurred.

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IV. PERFORMANCE ANALYSIS

A. flant Operations (1191 hours0.0138 days <br />0.331 hours <br />0.00197 weeks <br />4.531755e-4 months <br />; 29%)

Analysis

This area was rated Category.1 in the previous two assessments, with

a decreasing number of reportable events attributable to operator

error, low scram rates and good safety attitudes exhibited by the

operating staff. Exceptions were found in the management of fire

protection activities. Improvements were noted in the reduction of

unnecessary alarms and improved control room access controls.

During this assessment period the shift superintendent is a recog-

nized part of the station's management structure and the responsi-

bility vested in this role is evident by their visible leadership, a

l key in the achievement of a successful operating team not exclusively

l limited to operations personnel. Two new shift superintendents were

selected during this pericd as a result of a rigorous selection process

whereby promotions are peer-evaluated and are not solely the result

of seniority.

The licensee has placed a high priority on the perception and

attitudes of licensed operators. Operator feedback is of paramount

importance as evidenced by the shift superintendents' regular

briefing to Nuclear Review Board (NRB), the plant ir.cident review

committees, and the shift update notebook. Training has been pro-

vided to prepare operators to better deal with shift work such that

attentiveness is maximized and good morale is maintained.

Management's efforts have instilled a philosophy of safe operation.

One scram occurred because an operator did not react to IRM signals

during an full rod insertion shutdown for the 10-day condenser

outage. rograms devised to prevent scrams include color-coded

instrument panels in the auxiliary equipment room; A-day /B-day

surveillance test schedules; and a rigorous process for operational

condition change POI review.

l Access controls continued to be effective in limitine nonessential

l- personnel and noise in the main control room. However, due to the

design of Limerick's control room (common to both units), this is

still a concern because of Unit 2 construction and testing activities

which the licensee has recognized and continues to underscore in

shift meetings and turnovers.

L Communication techniques have been refined using administrative

guidelines, so that a marked reduction in reportable events attri-

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buted to breakdowns in communications is evident. Communications

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among the plant staff have been enhanced by publication of reports of

routine meetings and by tracking issues to completion through a

clearly accountable individual. Turnover between shift superinten-

dents is thorough. The shift superintendent is aided by detailed

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logkeeping and the use of a' marker to track operating problems. As a

result,-the status and disposition of all problems that develop

during the shift are addressed during shift turnover.

Extra licensed expertise was staffed for Unit 1 operation throughout

this period. This additional staffing has helped to maintain a gcod

safety record by effectively controlling overtime and is in antic'-

pation of Un;t 2 demands. Full-time day work positions were created

for shift superintendents as career paths outside of the control

room. The licensee has also provided for six month assignments (off

shift work) on a rotating basis. The licensee has recruited poten-

tial operators with two year associate degrees or previous reactor

experience. All nuclear plant operators (the most seninr nonlicensed

position) hold reactor operator licenses. An auxiliary snif t is

strategically used to augment peak day work tasks. A full time

position (the 13th SRO) on day shift is dedicated as a supervisor for

blocking and permit coordination. This individual has provided for

the successful removal and return to service of important plant

equipment, as well as elimination of a backlog of maintenance work,

better independent verifications, improved engineered safety feature

system blocks and ultimately, fewer reportable events.

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The shift technical advisor (STA) has been a key in operational

problem analysis, as reflected in post-scram evaluations and Upset

Reports. The first generation of Unit 1 STAS, who gained experience

during power ascension testing and Cycle 1 operation, have been

blended into other site organizations such as outage planning and

maintenance. This spread of operating expertise has been beneficial.

NRC review of the requalification program in March 1987 found

weaknetses with respect to simulator training scenarios, the

licensee's examination piecess and difficulties in the use of emer-

! gency operating procedures Training deficien:les and program

l weaknesses vere corrected by the licensee. Simulator training has

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proven valuable during several plant fe2dwater transients in which

operators quickly acted to prevent a scram.

In the last quarter of this assessment period, the position of the

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onsite fire protection engineer was filled with a qualified indivi-

! dual. The fire protection group was realigned and more clearly

defined as a station organization. A contract was initiated with a

specialist to resolve high priority sprinkler modifications and

improvements to the motor driven fire pump. Although both site and

corporate management were slow to recognize needed changes the newly

organized fire group new appears to have proper staffing, sepervision

and engineering support and represents a distinct improvement over

previous assessments.

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15

Better results were experienced with the use of a computerized system

- for blocking sequences prepared prior to use. The system reduced

errors, particularly for complex evolutions and outage work. Safe

accurate blocking sequences were provided during the refueling

outage, due in part to the assignment of an extra licensed supervisor

for blocking and permit coordination, as well as the practice of

independently verifying application and removal of blocks on safety

equipment. Few instances occurred during this assessment period

where blocking was not properly administered; however, the licensee

became immediately aware of these breakdowns due to good communica-

tions. The licensee has a'so devoted experienced licensed staff to

prepare Unit 2 blocks. Management commitment of.these resour ces

demonstrates recognition of the importance of removal and return to

service of safety equipment.

Summary

A strono operating team concept with effective leadership from shift

superintendents, integration of technical support organitations,

refined communications and explicit support from management have 4

produced a safe operating record. Advanced planning for Unit 2

startup is evident, while the impact on Unit I has been minimized.

Reductions in reportable events, low scram frequency, and continued

good personnel attitudes with ongoing re-organizational pressures

are products of the site management commitment to safe operation.

Previous fire protection concerns identified by the NRC have been

diagnosed and addressed by appropriata staffing and corporate

support, but more importantly by a recognition of a need to revise

the fire pr ogram. The need to apply resources to critical areas,

such as permits and blocking, has been quickly racognized. Formali-

zation during this assessment period of previously existing good

practices has sustained performance as standards are continually

raised.

Conclusion

Category 1

Trend

Board Recommandations

None

_ _ .

- _ _ _ _ _ _ _ ._ _ _ _ _ _ _ ._. . _ _ _ _ - - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

. .

16

B. Radiological Controls (429 hours0.00497 days <br />0.119 hours <br />7.093254e-4 weeks <br />1.632345e-4 months <br />; 11%)

Analysis

The previous assessment covered the first post-licensing period of

refueling and operation and was rated as Category 1. Weaknesses

were noted in the areas of ALARA, potential heat stress of workers

and review of design modifications, which were attributed to lack of

policy making at the corporate level. Minor weaknesses were noted in

monitoring non-radiological chemistry parameters. Also, post

accident sampling system reliability problems were identified.

1. In Plant Radiation Protection

During this assessment periou site management at all levels

continues to effectively plan and direct activities related to

radiation safety. The station manager personally emphasized the

importance of the Station ALARA Review Committee (SARC) with his

staff after poor attendance at SARC meetings was noted. The

Health Physics supervisors are directly involved in setting daily

priorities for rou+t;e HP surveillance and other technician

activities. During the refueling outage, senior HP technicians

were assigned to coordinate HP support in designated areas of

the plant. Other technicians were loaned to various work groups

such as maintenance to augment GET training of workers, act as

an interface for work scheduling, and ensuring incorporation of

ALARA into the early stages of job planning. Good management

oversight and control of the on-site contractor that collects,

transfers for laundering, and restocks protective clothing was

noteo.

In August 1987, the licensee committed to various improvements

,

in corporate involvement in radiological controls. Implementa-

l tion was not complete by the end of the current assessment

period. Resolution of technical and safety issues related i o

radio'.ogical controls is also sometimes delayed. An excellent

l Heat Stress program was not implemented until one year after

i problems became known. The Hot Particle program has been

unnecessarily delayed by a management decision to adopt the

'

program being developed at the licensee's Peach Bottom facility,

l which is progressing slowly. In the interim, indicators of the

l onset of a hot particle problem such as reactor coolant analysis

I

and personnel contamination reports are being monitored. The

l licensee's approach to technical issues from a safety standpoint

'

is very good although corporate technical support is lacking and

some implementation delays occurred.

-. _ -. - . . _ _

.. .

.

17

The on site program for the calibration and maintenance of

radiation survey meters is excellent and is conducted by compe-

tent contractor personnel. A "hot tool" crib is under construc-

tion that will censolidate into one location all contaminated

tools regardless of the ownership. However, the Radiological

Awareness Reporting remains weak, as emphasis is placed on

prompt correction of problems without the need for documentation

which denies management the data to detect adverse trends. This

is compensated somewhat by the very good communication that

exists between most departments and supervisory levels on site.

ALARA performance continues to be effective with challenging

goals selected by site management. Total exposure for the

period including the outage was about 174 person-rem. This

exceeded the original goal of 150 person-rem due to an unantici-

pated extension of the outage to deal with additional control

rod drive rebuilds and other undervessel work. However, the

total exposure compares very favorably with other newly licensed

BWR stations.

Training and qualification programs are very well developed and

make a positive contribution to the technical performance of the

station staff. The training and testing of contractor health

physics technicians hired for outage support is effective in

ensuring the required knowledge level of radiation safety pro-

cedures. An excellent program for the repair aro calibration

of sophisticated radiation monitoring equipment by Instrumen-

tation and Control (I&C) technicians was noted. This is

attributed, in part, to a rigorous training program for I&C

technicians which spans several years and only accepts personnel

possessing two year degrees.

2. Effluent Control and Environmental Monitoring

The licensee has effective oversight of effluent controls at the

site. Positions and clear lines of authority were established

in the chemistry and health physics support ;roup who sample and

analyze effluents, and implement the Offsite Oose Calculation

Manual (0DCM) respectively. Audits were found to be thorough

and comprehensive in scope. S+affing was generally complete

with little reliance on contractor personnel. There was

inadequate review of effluent data as indicated by errors in the

licensee's Semi-annual Effluent Release Report which were noted

as a result of a change in the computer group's technical staff

members who support the effort. Two LERs related to ef fluent

sampling were noted as attributable to personnel error, sug-

gesting a minor weakness in technician training.

\

--

_

.. . - _ . . _ _ _ _

. .

e

-

18

An effective Radiological Environmental Monitoring Program

(REMP) is being implemented by the licensee. Good corporate

management was demonstrated for this program in which all

activities are contracted. QA audits are thorough and of

sufficient technical depth to adequately assess capabilities and

performance of the REMP. Training for both licensee and

contractor personnel is effective.

3. Radiological Confirmatory Mecsurements

The licensee maintains good capability for determination of

radioactivity in gaseous and liquid effluents as demonstrated by

the comparison of measurements with the NRC Mobile Lab Clear

lines of authority and adcquate stcffing were noted as positive

attributes in management controls. QA audits are conducted at

regular intervals, are technically competent and meet stated

objectives. Procedures are generally adequate to meet program

needs but show indications that timely reviews fer accuracy and

content may not be done in a thorough manner. Example problems

include charcoal cartridge efficiencier tnat were not correlated

to flow and the absence of a requirement for use of a reducing

agent for iodine separation. Two LERs relevant to the chemistry

area occurred within ten days of each other and were attributed

to personnel errors.

4. Non-Radiological Chemistry

Lines of authority are clear and plant senior management support

appears strong as evidenced by recent acquisitions of laboratory

equipment. In spite of adequate staffing and state-of-the-art

measurement equipment, weaknesses in laboratory measurements

were identified in the licensee's capability to monitor chemical

parameters in various plant systems with respect to Technical

Specification, fuel warranty and other regulatory requirements.

These findings indicate inattention to detail in the laboratory

chemistry measurement program some of which were also identified

during the last SALP period.

Summary

During this assessment period, licensee management demonstrated the

ability to conduct routine radiological operations and conducs a

refueling outage while maintaining a high level of radiation safety

performance. In addition, program enhancements and policy improve-

ments were developed and implemented on site in spite of minimal

technical support and guidance from the corporate staff. The

licensee has been slow to respond to problems in areas such as worker

heat stress, hot particles, non-radiological chemistry laboratory

measurements and in providing corporate support to the site.

l

1

, _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _

. .

.

19

Conclusion

Category 1

Board Recommendations

Licensee

Increased attention should be focused on (1) development of a

program for hot particles; (2) weaknesses identified in the

non-radiological water chemistry measurement program; and (3)

improved corporate support for the site.

!

9

.

. ,

20

C. Maintenance (503 hours0.00582 days <br />0.14 hours <br />8.316799e-4 weeks <br />1.913915e-4 months <br />; 12*J)

Analysis -

This area was rated Category 1 in the previous assessment, with good

supervision of craft and engineering support noted, system status

control and post-maintenance testing as strengths, and excellent

equipment and plant reliability.

During this assessment period well organized and ef fectively managed

maintenance programs that are founded upon a teamwork concept were

evident. Quality workmanship resulted from excellent craft skill

levels, a large amount of specific equipment expertise, and increased

participation of foremen at the site. Several levels of site manage-

ment are routinely involved in oversight of work, including regular

plant tours and cognizance of plant c.onditions. Management goals

related to overtime, ALARA, reportable actuations and work backlogs

have clear accountability. Progress towards those goals has been

measured in the monthly site Vice President meetings. ,

Foremen and supervisors have been carefully selected, and growth

potential is evident in maintenance organizations by promotions

throughout the period. A culture of accountability exists, in part,

because of healthy organizational relations with other work groups.

The reorganization at the end of the period strengthened maintenance

groups on site, by better int 39 rating the previously sound technical

support functions, and has improved morale due to assignment of the

former Ma :ager of the Maintenance Division as Station Manager. A

self-assessment was conducted towards the end of the period and

action plans to improve various programs were underway.

,

Predictive programs were better developed as new technology (thermo-

l

graphy) and existing techniques (vibration analysis) were factored

l into a performance group formalized auring the last half of the

period. The group utilizes a preventive maintenance (PM) coordinator

'

and dedicated staff to assemble computerized data from testing,

failure data cnd other sources to perform trend analysis. Limited

use of the program has nonetheless identified potential problems for

,

l

investigation or increased maintenance. Priority has been placed

upon completing overdue PM's and maintaining a balance of preventive

l and corrective work as a means of assuring safe reliable operation.

, Also, deferred PM work has written justification and is still entered

! in historical records based on technical evaluation. Although the

Probabilistic Risk Assessment (PRA) has been kept updated and used in

,

limited fashion for licensing and design decisions, its potential for

l removal of equipment from service for PM work has not been fully

explored. ,

l

l

l

l

l

4 &

.

21

Important equipment has had planned overhauls during this period and

experienced good reliability as a result, A valve

repacking program, including live loading for all air and motor-

operated valves and manual valves with a failure history, was

implemented during the refueling outage and has been successful as

indicated by low unidentified leakage and few radiological hazards.

Problems 4:ith RWCU pump seal failures noted in previous periods were

significantly reduced as only one seal failed this period. No

unplanned shutdowns were attributable to maintenance activities.

However, control structure chiller availability was low and increased

vendor expertise and technical coordination were required. Main

condenser tube leaks and air inleakage, and circulating water system

problems also challenged the plant staff this period, and a planned

two-week shutdown was conducted in April 1988 to repair these and

otner problems.

One measure of management's influence in this area is the high level

of plant housekeeping maintained, as well as clear commitments to

industrial safety. Controls on scaffolding particularly following

the refueling outage were lax, but improvements were instituted to

more carefully consider erection near safety equipment and to promptly

. remove scaffolding when work was completed. Fluid leaks are not

widespread and are promptly repaired, control room and local alarm

panels have few chronically annunciated conditions, and access to

equipment is generally easy- A formally controlled lubrication

prugram is strictly maintained using grease pro.'dures and locally

posted instructions on proper lubricant and fill points. However,

control structure cniller availability was low and increased vendor

'

expertise and technical coordination were required. Main condenser

tube leaks and air inleakage, and circulating water system problems

also challenged the plant staff this period, and a planned two-week

shutdown was conducted in April 1988 to repair these and other

problems.

Conduct of maintenanct <, typified by strict adherence to procedures

and a teamwork approach such as on the refueling floor during the

outage. Professional courteous work relationships found throughout

other work groups extend to maintenance personnel as well. Dedicated

planners and licensed or Shift Technical Advisor (STA) experience

within the staff ensure that work is accomplished smoothly. Self-

critiques are regularly conducted using videotapes and involve

appropriate craft and management. The licensee has recognized the

continuing challenge of making the HP-maintenance worker interface

successful. Detailed workmanship and attention is evident in the

more challenging jobs performed.

i

l

l

I

l

L

_ _ - - - - - - _ - - _ _ - - - - - _ _ _ _

, ,

.

.

22

f

Procedures have been technically sound, but need better human

factors and conciseness. Improvements were being undertaken for

clarity, usability and incorporation of computer-drawn sketches,

diagrams and pictures. Site management has recognized this

problem. They are solving it by craft / foreman feedback in critiques

and validation of procedures using mockups. One reportable event-

was attributed to a procedual inadequacy in this erea.

An effective automated' system (CHAMPS) enables better management and

knowledge of job status at any time. A complex but well understood

administrative procedure governs work. Accurate controlling docu-

ments (maintenance request forms) allow for easily understood post

maintenance testing and comprehensive maintenance history. A very

low backlog of work is maintained. Backlog statistics are refined to

a number of meaningful measures such as: high priority non-outage

workable corrective jobs older than 60 aays and total number of jobs

completed but not yet entered to history older than three to six

months. In the latter category, an NRC violation resulted in a more

challenging goal and better equipment history available at the end of

the period. Trend analysis of this history identified a high failure

rate for feedwater minimum flow recirculation valves which were

repaired during the April 1988 outage.

Staf fing was improved by consolidation of maintenance groups as part

of the corporate the reorganization. The licensee s'apports a program

to train high school graduates to be technicians, including formal

education towards a two year college associate degree and an 18 month

plant systems course. Training is closely coordinated with craft /

Supervisor .'eedback and supported by a site maintenance training

representative. Special courses have been devised and plant specific

mockups are effectively employed.

Supervision and control of contractor maintenance is a recognized

i

problem, as evident in the undervessel damage incurred during the CRD

l rebuilds and by QA audits of selected outage jobs. The licensee has

already taken steps towards improving contractor workmanthip by

appointing a dedicated licensee foreman for outage undervessel work,

a supervisory engineer for reactor work during refueling, and better

screening and training of contractors.

Summary

In summary, several levels of management are effectively involved in

maintenance; equipment reliability has been excellent; maintanance

groups are well staffed, trained, and supported; teamwork and

accountability are evident; and self-assessments and root cause

analysis programs are maintaining a high quality program. Outage

demands and technical problems were successfully met and solved.

Repetitive failures rarely occur but nonetheless are quickly

recognized and presented to management for solution. Maintenance

personnel follow procedures, include pre-job ALARA-conscious

decisions, and respond capably to contingencies. Work planning is

e

c -

. _ - - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ ..

L , .

.

. 23

extensive and better predictive capability is being developed.

Improvements are underway to make maintenance procedures more usable,

better control contract work, and manage work _ backlogs.

Conclusion

Category'l

Board Recommendations

None

%-

_ _ _ _ _ _ _

. .

.

24

D. Surveillance (549 hours0.00635 days <br />0.153 hours <br />9.077381e-4 weeks <br />2.088945e-4 months <br />; 14%)

Analysis

Surveillance was rated Category 1 during the previous assessment.

Testing successfully confirmed operability and identified equipment

problems, und benefited from involved supervision and good engineer-

ing support. Relatively few instances of missed tests occurred.

During this assessment period the success of the programs depended

upcn strong accountability to a surveillance test coordinator. Test

philosophy extends beyond compliance, including routine tests not

required by technical specifications but important for safety system

availability. However, the number of reportable events attributed to

personnel errors continued at approximately the same rate and there

were no reactor scrams caused by testing. Problems from previous

assessments were significantly reduced such as instrument valving

errors, missed fire watches, reactor water cleanup system isolations

and difficulties with toxic gas analyzers.

Survelliance Testing continues to be effective in identifying equip-

ment problems, especially with the emergence of performance monitor-

ing to trend equipment reliability and allow early prediction of

failures. A performance monitoring group was established with

dedicated staff in the technical engineering group. Trending is also

reported routinely to the PORC. Another useful trending initiative

is the plant electronic notebook system (PENS) which involves

computerized data entry from the dally surveillance log.

Staffing was sufficient to support surveillance testing as reflected

by strict adherence to test schedules and the ability to find

problems. Although half of the I&C technician staff are contractors,

these personnel have been at Limerick since preoperational testing

and exhibit good understanding and respect for station administrative

controls.

The licensee's sensitivity to scram potential is demonstrated by an

A-day /B-day logic channel test schedule: coded into the computerized

scheduling system and incorporated in administrative procedures;

stamped in red on procedures; and posted in the main control and

auxiliary equipment rooms. This disciplined approach to testing is

used to prevent coincident logic actuations and demonstrates good

control over testing.

The conduct of testing is founded on effective communications and

professional working relationships between test personnel and

licensed operators. Technical staff are assigned as test directors

and a licensed operator is routinely dedicated to complex testing

such as safeguards bus logic. This was evident during extensive

modit aation testing during the refueling outage. Inservice Testing

(IST) is similarly well-coordinated. Some managem7nt deficiencies

.

F

-- _

. .

.

25

were noted with the Containment Integrated Leak Rate Test (CILRT)

involving overuse of tags, an extensively revised procedure, building

access control, and communications with operators.

Areas where room for improvement exists are QC witnessing of

routine testing, and the control of temporary procedure changes.

Also, the daily surveillance log performed by operators to fulfill

channel checks failed (over two shifts) because of an unspecified

normal range to detect reversed thermocouple leads on a temperature

monitor that had been improperly restored following a surveillance.

A key aspect of programs is the computer based scheduling system

maintained by a dedicated test coordinator. Overdue tests are

quickly identified, as in one case where planning for weekend wo 9

loads identified an incorrect test date. The master test scheduie is

routinely checked by station supervision and plant management, and

has enabled recognition of problems. This planning enables good

management of an extensive test program.

Test procedures have proved to be usable, and were recently revised

with consistent human factor improvements. Independent verification

following testing is sound and successful, and provides a true

independent validation with a high degree of confidence in system

configuration. An exception was reported in LER 88-01 involving

undetected reversal of thermocouple leads. Test procedures implicitly

allow for sound communications between test personnel and contrcl

room operating staff, incleding a pretest briefing on expected alarms

and the impact on system oferability. A consistent technician

approach is to suspend tert activity when a procedural error or

equipment discrepancy is found until the problem can ce resolved.

The licensee has created an atmosphere wherein personnel routinely

exhibit attention to detail and involve their supervision when

activities are 'n question. Color coded instrument cabinets in the

auxiliary equipment room have reduced the potential for human error

associated with divisionalized testing. The licensee mirimized the

use of lif ted leads during testing and has virtually eliminated

inaccessible test points. Station management has communicated to

work groups that activities should be conducted with the idea of

eliminating system challenges.

Improved communications between test personnel and operators,

development and use of procedures that comply with human factors

guidelines, involvement of first line-supervision, and rout.Me use of

root CaJse analysis programs indicate a desire to find and correct

problems. Corrective action programs are persistent, as indicated by

frequent revisions to LERs to describe additional information

uncovered by investigations.

- -

. .

.

- 26

i-

Certification trdining during this assessment period has been effe:-

tive in plant staff and management understanding of the operation of

plant systems. Training during the period on human performance

evaluation techniques has been applied to a limited extent to the

surveillance test program to effect simple but effective solutions.

Less formal training has also been influential as evidenced by

creation of a shift superintendent update notebook to describe

ongoing technical issues,

e

Much of the quality oversight of surveillance is accomplished in PORC

meetings. A plant incident tracking system has been effective in

focusing c. the more safety significant issues that occur from

day-to-day. The licensee's QA and QC involvement in surveillance

testing has been minimal, ar.d has not provided assurance of the

effectiveness in activities in areas such as indapendent verifica-

tions.

Summary

Management's oversight of testing has been stro ig. Clear account-

ability for testing performance is ensured by t ie scheduling program.

Workers and technicians exhibit attention to de: ail and have the

benefit of dedicated technical support, includiig new developments in

trending. . The licensee has demonstrated an agg essive approach to

testing beyond mere compliance with requirements,.

Conclusion

Category 1

Board Recommendations

None

!

!

t

L_

_ . - _ _ __ __

-. ..

1P

. 27

E. Engineering / Technical Support (958 hours0.0111 days <br />0.266 hours <br />0.00158 weeks <br />3.64519e-4 months <br />, 24%)

-Analysis

This area was rated as Category 1 during the last assessment with

strengths.in the integration of technical expertise among all site

work groups, valuable contributions from test and field engineers,

and responsive professional. interaction with corporate engineering.

Considerable inspection effort was devoted to this area this period,

including team inspection of the environmental qualification program

and assessments of the interface between site technical organizations

and corporate engineering. Major licensee reorganizations occurred .

'

near the end of the period, involving both corporite and site

technical functions. A new Vice President devoted solely to nuclear

engineering was appointed in January 1988. Personnel appeared to be

generally receptive and optimistic regarding the changes.

There were two unplanned scrams from power which occurred within a

, month of startup from the first refueling outage and both were caused

by failures of balance-of plant equipment. The first was due to

erratic moisture separator water level control attributed to inst-

rument air. valves that had not been adequately verified as open. The

other scram occurred due to a ruptured control fluid line to the main

turbine control valves caused by resonant vibrations resulting from a

modification. The licensee displayed a sensitivity to scram poten-

tial by restricting the unit to 85% power for two months until a

solution to the vibrations could be achieved.

Site engineering support for the inservice testing (IST) of pumps and

valves was found to be well coordinated, staffed with technically

competent personnel and had a high degree of site management involve-

ment. The IST organization was a knowledgeable cohes.ive group that

closely interfaced with their maintenance department counterparts.

Site engineering interfaced with corporate engineering and requested

their assistance when needed. However, corporate engineering

guidance appeared to be 1 scking and did not appear to thoroughly

evaluate some issues. Examples included programmatic deficiencies

with document control, ill-defined organizational and personnel

'

responsibilities, and discrepancies between the licensee's criteria

and ASME Code Section XI. In response to past engineering support

deficiencies, corporate engineering is presently taking the lead in

efforts to improve IST based on NRC findings at Peach Bottom.

A special fire protection inspection in response to the licensee's

identified issue that an Appendix R postulated fire in the service

. water pipe tunnel area could disable all fcur emergency diesel

l generators (EDGs), resulted in escalated enforcement. Although an

l.

associated problem involving a deficiency in the EDG time delay

l

setting was identified by the licensee as early as June 1984, the

l

. . _ -

.. .

28

lack of separation of fire protection circuitry was not identified by

.the licensee until October 1987. This was an indication that

management attention may have been lacking. Pricr evaluations and

reporting involving interaction between safety and non-safety related

systems may also have been inadequate. Considerable NRC effort was

required to bring the problems to the surface. Once the Appendix R

problem was identified, the circuitry was promptly corrected.

Another identified weakness in corporate engineering support to the

site was found during audit of the environmental qualification (EQ)

program. Procedures adequately documented EQ packages, and were

generally well organized, however, some packages were not updated on

time resulting in three violations in the qualification of Rockbestos

cable. EQ maintenance and plant modification activities at the site

were found to be well supported. Established EQ related training

exists for individuals performing installation, modification, repair,

maintenance and procurement. Personnel have also participated in EQ

associated courses sponsored by industry and institutions. Personnel

were aware of regulatory requirements and of the licensee's commit-

ments to implement a fundamentally sound EQ program.

The NRC team evaluation of Unit I restart from the refueling outage

identified a weakness with the liberal use of temporary circuit

alterations (TCAs) to implement short-term modifications. Although a

past-identified issue. significant numbers of outstanding TCAs

existed throughout the period, many dating back to original fLei load

over three years ago. Application of TCAs had doubled over each of

the past three years, with appr3ximately 25% not restored or

permanently modified. While co porate engineering provided timely

engineered design packages to support major refueling outage license

condition modifications, the increasing number of TCAs indicated an

inability to support routine plant operation. In the latter half of

the assessment period the licensee initiated corrective action to

reduce the number of TCAs and assign high priorities to design

engineering for those TCAs (two thirds of total) awaiting permanent

modifications.

Reportable issues identified during the period pointed to engineering

or technical dif ficulties requiring more aggressive corrective

action, such as the inordinately large number of secondary contain-

I ment isolations. While various root causes could be assigned to

l these, the overriding issue involves blocking and tagging errors due

I to lack of identification of instrument air lines. This problem was

also the apparent cause of a scram in September 1987. Site technical

engineers completed an exhaustive walkdown of accessible air lines by

the end of the period. This concern was also raised by the Nuclear

Review Board but longer term solutions are still forthcoming. Past

chronic reportable events invoh ing chlorine and toxic gas detectors

received considerable technical attention. The toxic gas detector

problems were effectively addressed by logic changes and responsive

engineering; however, the chlorine detector problems persist and an

. ._ _.

,

-. ,

.

. 29

engineering solucion has been delayed. In certain other events (e.g.

LER 87-42 regarding RPS relays) the licensee demonstrated a-

philosophy to go beyond mere compliance with requirements.in pursuit

of the root cause.

Planning and technical support were excellent for the refueling

outage. Staffing in health physics, QA and QC were increased,

assuring better outage coverage, including detailed audits for

license conditions. Management concern for reactor safety was

evident by establishment of a refueling floor outage organization

with well defined lines of communication and by certain outage

conservatisms including the NRB's concern to assure backup decay heat

removal using fuel pool cooling systems during planned modifications

to emergency service water systems. Although management's decision

to secure ventilation systems on the refueling floor in August during

hot humid weather necessary to tie-in standby gas treatment caused

worker heat stress problems and rome ALARA ccncerns (see section

III.8), that philosophy was abandoned and contingencies were employed

after worker feedback was received. The licensee successfully

employed a modification coordinator (similar to test coordinators for

complex surveillances described in Section III.C) for critically

complicated changes, such as the SCTS tie-in, which involved many

work groups.

A high degree of technicci and management support of the ISI Program

was evidenced by the use of the General Electric Company "Smart UT"

which is an advanced system for recording and processing ultrasonic

examination data, and by the comprehensive QA coverage of ISI activi-

ties. The ISI Program is adequately staffed with well trained

personnel. QA staff responsible for ISI are knowledgeable and

competent to monito.- these activities.

The licensee has maintained an up-to-date PRA, primarily in antici-

pation of Unit I licensing questions. However, extensive use of the

study where it would seemingly contribute to Unit 1 operating

decisions such as preventive maintenance and modifications has not

been mat'e. Certain Unit 2 milestones such as tie-in of service water

systems 'ticularly for diesel preoperational testing) have been

well pla..cd and were presented to the NRC in advance of dual unit

operation. Also, engineering solutions to past problems such as PASS

reliability and interunit contamination of shared systems have been

effectively resolved and applied to Unit 2 as well.

Summary

In summary, although engineering and technical support for the first

refueling outage modifications was generally good, corporate support

in resolving some chronic operational problems associated with

(

chlorine detectors and in addressing specialized areas such as EDG

'

fire protection instrumentation and environmental qualification left

considerable room for improvement. Thus while long term preplanned

i

support for outage activities was effective, corporate support for

l routine operating activities was not always so.

t

I

,

me - w

_ _ - - _ _ _ _ _ _ _ _ _

.. .

.,.

30

'

Near the end of this evaluation period an increase in iodine

activity in the coolant was identified as due to' leaking fuel. Heat

flux restrictions to minimize further fuel degradation have caused a

power derating of the plant. Although the cause of the leakage has

not been fully detennined, a synergistic effect of zirconium cladding

fabrication variations and copper and iron impurities in the

feedwater may be responsible however, it is unusual for this to

result in cladding failure early in the life.of the plant. The

response, including corrective action, taken in response to this

event will be significant in the longer term operation of the

plant.

Conclusion

Category 2

Board Recommendations

Licensee: Meet with NRC to review the status of the identification

of the root cause of the fuel leak and the corrective actions being

taken.

_NRC : Increase attention to assure that licensee response to the

fuel leak is comprehensive

i

l

l

t

-

- - , . . , , - . _ - , - , - - -

_ .

. ...

31

F. Emercengy Preparedness (121 hours0.0014 days <br />0.0336 hours <br />2.000661e-4 weeks <br />4.60405e-5 months <br />; 3%)

Analysis

During the previous assessment period, licensee performance in this

area was rated Category 1. This was based upon good exercise

performance and the licensee's own initiatives in routine emergency

preparedness activities.

During the current assessment period, one routine safety inspection

was conducted, one full participation emergency exercise was

observed, and changes to emergency plans and implementing procedures

were reviewed.

During the routine inspection performed in January 1988, several

significant areas of concern were identified. Deficiencies were

found in programmatic areas such as the ability to resolve exercise

critique items, implementing procedure revisions, performance of

related tests, and training of off site response personnel. NRC

review of licensee audit results revealed that some of these areas

were previously identified as deficient and in need of correction.

The open item tracking system used by the licensee Emergency

Preparedness Section identifies significant program deficiencies

outstanding for approximately two to three years that have not

received appropriate management attention and evaluation. Although

many of the individual deficiencies were not of major significance a

violation was issued for the licensee's failure to take corrective

' action on outstanding Emergency Preparedness Program deficiencies

identified by their own audit program.

The audits of the Emergency Plan, Emergency Plan Procedures, and

Corporate Procedures noted in the preceeding paragraph have been

conducted by the corporate organization with contractor support every

12 months. These audits were performed in adequate detail to provide

assurance that potential weaknesses were identified and discussed

with emergency preparedness management. However, two separate 1986

independent audits were perforned which identified recurrent program

deficiencies. The results of both audits were sent to the Director,

Emergency Preparedness. No action was taken by the corporate Emergency

Preparedness staff or other management to correct these identified

deficiencies. This led ; an NRC finding that formal distribution of

the 1986 audit results to appropriate plant or corporate management

was not made. In the licensee's 1987 QA audit report several new

findings were identified in addition to recurring program deficiencies,

i

which indicates an inadequate response to self identified problems.

Deficiencies associated with program management and the independent

I review process remained unresolved, an Action Item Management Team

!

was established to address these concerns.

1

!

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.

. 32

During the unannounced, full participation exercise held on April 5,

1988, the licensee's execution and participation demonstrated

acceptable planning and thorough accident management.' The NRC team

obse rved several minor performance weaknesses in the areas of infor-

mation flow, use of Emergency Plan Procedures (EPP), and training of

personnel to effectively carry out EPP's. The licensee also demon-

strated adequate corrective action for previously identified NRC

exercise items through appropriate program changes and retraining.

The level of staffing and resources maintaining the Emergency

Preparedness program is strained and the effectiveness of the Site

Emergency Preparedness Coordinator (SEPC) in completing task assign-

ments has suf fered as a result. Scenario development and review via

!

contract support has been acceptable. The Director, Emergency

Preparedness was also overburdened in that oversight responsibility

for program administration, on site planning support, off site

planning support, and drill / exercise conduct must be implemented at

both the Limerick and Peach Bottom sites. Near the end of the SALP

period the licensee implemented management changes and also dedicated

additional corporate support to the Emergency Preparedness progran;

however the effectivness of these improvemeats have not yet been

assessed by the NRC.

Emergency Response Facilities (ERF) are dedicated and have been

adequately maintained throughout the period.

Summary

In summary there appears to be adequate ability to respond to

emergencies, however, it appears that the strong interface exhibited in

previous assessments between the corporate emergency preparedness

staff and the SEPC/ site support staff has been weakened. Responsi-

bility for assignment and completion of site duties is assumed by the

SEPC without adequate resources or direction frcm the corporate

staff.

Conclusion

,

Category 2

l

Board Recommendations

Licensee

1. Focus additional attention on resolving outstanding audit

findings and institute more timely corrective action for them.

2. Ensure effective completion of required Emergency Preparedness

Program tasks, including planned corr '<ve action resulting

from identified deficiencies.

- , .,

-

_ _ - -

. .

. 33-

G. Security and Safeguards (281 hours0.00325 days <br />0.0781 hours <br />4.646164e-4 weeks <br />1.069205e-4 months <br />, 7*;)

Analysis

During the provious assessment period, this area was rated category

2. The licensee and the security force contractor aggressively

pursued a planned course of action to identify and correct the root

causes of their identified poor performance and implemented many

changes in an effort to improve the overall security program.

Those changes included a significant increase, on the part of the

licensee, in program oversight and direction, management involvement

and support, and training program enhancements.

A high degree of licensee management attention to and involvement in

the program continued to be evident during this assessment period and

was n.atched to a substantial degree by the licensee's security

contractcr. This combined effort to estaolish and maintain an

effective and high quality security program resulted ia excellent

performance throughout the period (one minor violation), in addition

to further program enhancements.

The additional enhancements included: (1) establishiig a Security

Incident Review Committee composed of operations and security

management personne?, to evaluate all security events for plant

safety and security consequences; (2) providing proprietary shift

supervisors specialized training in alarn station operations, audits,

surveillance testing techniques, and emergency preparedness; and (3)

developing an action plan and tracking system to provide for a smooth

integration of Unit 2 systems and equipment into the Unit I program

and assigning responsibility for the transition to an individual with

no concurrent Unit 1 program duties. The implementation of further

enhancements provide continued evidence or managements' further

I interest in maintaining an effective program rather than a compliance

oriented program.

The licensee continued to use a self-appraisal program to monitor the

on going performtnce of the security force ?nd to identify potential

problems easily and correct them effectively. The responsibility for

implementing this program was reassigned from the security contractor

to the licentee's proprietary supervisors during this period. The

self-appraisal program combined with other security program audits

and surveillances, and the NRC required annual program review, is

believed by NRC, to be a significant factor in improving the security

l program and is indicative of the licensee's desire tc achieve high

quality in its program implementation. This was also apparent by the

licensee's actions in response to generic Regulatory Effectiveness

Review findings. In that regard, the licensee, on its own initia-

tive, actively pursued the generic findings at the Limerick

Generating Station to determine if any similar deficiencies existed

and, as appropriate, promrtly corrected potential problems.

.._- - . ,

p,,e ,

)'

34

The licensee's _ security contract also cmtinued to make enhancements

'to~its portion of the program. These included: (1) improving tti

established security force training program by refining lesson plans

and obtaining additional training aids; (2) providing additional

emergency preparedness task training (3) renovating the equipnent and

arms room and revising arms issue procedures; (4) developing a pool

of traiaed and qualified supervisory personnel to provide an effec-

tive line of succession; and (5) developing and implementing on-nost

security task certifications. In addition, the contractor exerted a

commendable effort to improve employment benefits and human factors

for the guard force in order to strengthen morale.

Security management involvement in industry and NRC initiatives

involving nuclear power plant security progressed throughout the

period in response to identified problens, demonstrating management

support of the program. In addition, the licensee has taken very

aggressive measures to reinforce i;s Fitness for Duty Policy and to

achieve a drug free work place for personnel at the Limerick

Generating Station. On several o:casions during the period, the

licensee conoucted drug sweeps of the Station using specially trained

dogs, pursued in-depth investigations of allaged drug related

activities, provided special drug awareness training sessions for

supervisory personnel. and enforced appropriate disciplinary actions

for offenders. The licensee's initiatives in this regard are

exemplary and demonstrate a very responsible position to ensure

public health and safety.

The training program is implemented by well qualified and

experienced instructors with no concurrent duties. Facilities and

equipment are adequate and lesson plans are well developed and kept

current through vcrious feedback mechanisms, including the self-

assessmer.t and on post task certification programs. The initiatives

implemented during the previcus rssessnert period, particularly the

revisions to nrocedures and post instructions to make them clear and

! concise, were apparently effective as indicated by the relatively

small number of guard force personnel errors.

Staffing of the proprietary and contractor organization is effactive

as evidenced by the effective oversight and excellent performance

l during the period. Staffing of the guaru fnrce also appears to be

sufficient as indicated by the 'imited cse overtime. This is also

considered by the NR to be a significant factoi in improving the

program and indicath. of the licensee's desire to achieve high

quality in program iraplementation. '

l- The licensee's event reporting procedures were found to be clear and

consistent with the NRC's new reportirg requirements. Seven event

reports were submitted to the NRC during the period. Four of the

reports resulted from the licensee's follow-up of drug related

activities: one involved an inattentive guard; another reeulted from

a computer failure, and the se enth resulted from the detection of a

%

. .

v

l 35

weapon at a protected area access cont.;l point. Each report was

cleer and corcise, and indicated appropriate response to the reported

event.

During the assessment parfod, the licensee submitted two revisions

to the security plan under the provisions of 10 CFR 50.54(p). The

licensee's corporate security staff is responsible for ensu.ing that

plans are current and for coordinating changes, when required. The

?icensee's e,taff is very effective in carrying out this responsibi-

lity. They oftan communicate and review changes with the NRC to

ensure a clear understanding. When the plan changes are submitted to

NRC, they are of good quality, which is indicative of a thorough

review and a comprehensive understanding of NRC security performance

objectives.

Summary

In summary, the licensee and iti, security contractor continued to

strive for an effective and high quality program throughout the

period. Significant improvements wr.re made to the program ared these

resulted in excellent performance and imp'ementation of a security

program that is oriented toward meeting the NRC's nuclear plant

security objectives rather than merely regulatory compliance. The

efforts expended during this period (and the preceding period) are

commendable and demonstrate the licensee's ability to turn a carginal

program into a high quality program through management irvclvement,

attention and oversight.

Conclusion

Category 1

Board Recommendations

Iicensee: Continue initiatives to further enhance program.

!

'

l- # _ . . __ __

. _ _ _ _ _ _ _ _ _ _ - - _ _ _ _ .

~

. .

.

.

36

H. Safety Assessment / Quality Verification

Analysis

Assurance of quality has been considered as a separate functional

area in past SALPs, in addition to being one of the evaluation

criteria in functional areas, aad was rated as Category 1. This area

has been expanded to encompass activities previously evaluated in

Licensing, incluaing safety evaluations. This discussion is a

synopsis of quality and rafety evaluation philosophies reflected in

other functional areas. In assessing this area, the SALP Board has

considered attributes which are key contributors in assuring safety

and verifying quality. Implementation of managemer.t goals, planning

of routine activities, worker enthusiasm, management involvement, and .

training are e>amples. .

.

The previous SALP noted that the licensee had demonstrated consider-

able technical capability and evidence of management involvement in

licensing activities. The weakness noted was the quality of the no

significant hazards determinations (NSHDs) associated with license

amendment applications. The SALP Board recommended monthly meetings

between the licensee and NRC staff, which have been held.

During this SALP period, management took an active role in resolution

of any problems and ensured that schedules were met without sacri-

f:cing quality. There was a noted improvement in the thoroughness

and scope of the NSHDs. There are only four multi plant generic

issues remaining to be closed on Limerick 1 and these are nearing

resolut ons.

Licensee management has upgraded training programs for the licensing

staff and arranged for the personnel to spend more time onsite.

Licensing activities are conducted by a well staffed and well trained

group. Management overview is evident as warranted.

The Plant Operations Reviqw Committu (PORC) continues to be forceful

in maintaining safe operation. Use of a sub-PORC process keeps the

focus of the full committee on significant safety issues. Use of a

specially devised PORC process whenever operational conditions change

has insured that no problems remain unaddressed prior to startup;

however, more visible involvement by the ISEG and QA in that process ,

is warranted. Rou',ine meetings are reflected by excellent written '

minutes that. provide a good reference for station performance. The

value of PORC safety dec:sions is a result of the professional

meting atmosphere developed by past station managers and continu :d

under the strong leadership of the Superintendent of Operations.

The licensee conveys quality messages to workers in relatively simple

ways. Signs are evident throughout the plant underscoring the

importance to safety of routine tasks, including quality and

i

_

_

. _ _ _ _ - - _ _ _ _ _ _ _ _ .

n , ,;

.

-

37

- ,

excellence banners. Station inanager memoranda to site personnel

commend them for a job well done such as the outage, or serva as

reminders for careful work practices such as fire doors.

Management and corporate involvement with worker exposure programs

was still of some concern to NRC in that a Station ALARA Review

Committee had never formally met until NRC concerns were raised.

However, dissemination of the ALARA message to work groups was

evident.

The licensee has instituted unique corrective action programs which

are sufficiently self-critical to prevent recurrence and get at the

root cause of problems. An example was the video tape of skits

performed by operators designed to show that well-executed routine

activities can significantly reduce risk and enhance safe oparation.

Safety evaluations (modifications, TCA>, nen procedures, and general

plant issues) have been insightful and complete.

Prior to the reorganization the licensee's quality verification

groups (QA/0C) were fragmented among work organizations which diluted

their effectivenass at times. Some problems in communicating quality

concerns to operating staff were noted. However, because of excel-

lent work performance and the ability of work groups to find and

correct their own problems, QA/QC has not been an essential.ingred-

tent in assuring operating et ellence. Quality group involvement in

certain areas scch as surveillance testing has been minimal, and has

not allowed for an even assurance of activities such as independent

verifications. Quality auditors and inspectors are generally well

qualified and very consciantious as reflected in audits which were

detailed and critical of activities such as emergency preparedness,

fire protection, and maintenance.

As discussed in Section IV.0, technician qualifications and involve-

ment of first-line supervision have resulted in high quality test

programs. Supervision's attention to detail has.been instrumental in

effectively getting to root cause and preventing problems from

i recurr'.g.

L The Nuclear Review Board (NRB) was reconstituted at the beginning of

l

this period, including the addition of three senior consultants. The

Board nas prcgressed to a more thoughtful diagnosis of problems, as

evidenced by focus on issues during the refueling outage concerni g

.

decay heat removal and the increased numbar of personnel contamina -

l tions. All of the licensee's shif t superintendents have had an

E opportunity to address the NRB in a full meeting on topics ranging

I from Peach Bot +om feedback to the selection pincess for promotions.

The NRB has also expressed increased awareness f.e the effect of Unit

l 2 preoperational test preparations,

t

t

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. _ _ _ . _ _ _ _ _ _ _ ._

.

e

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.

. 38

Corrective action programs are portrayed by the quality of LERs, with

the exception of design problems manifest in secondary containment

.isolations and chlorine detectors. Past events due to instrument

valving errors, missed fire watches, and safety system actuations

have b?en eliminated. The detail presented in LERs has been excel-

lent, reflecting tne s'.rong technical expertise of the staff.

Although increasing trends for LERs have been noted, such as during

the refueling outage, the licensee properly interpreted those trends.

Some late LERs and the practice of extending them by supplements to

provide all required information suggest a management weakness in the

utility's Licensing organization. Corrective actions in response to

recurrent licensee identified deficiencies in the Emergency Preparec-

ness Program were unnecessarily delayed because of a lack of corporate

management oversight and of a lack of line management accountability

for program audit findings.

The licensee's initiatives in the area of fitness for duty have been

progressive, employing competent onsite security investigators, using drug

dogs as an effective deterrent, instituting policies for drug screening of.

contract organizations, and maintaining consistent communications with the

NRC regarding fitness for duty issues. The licensee has sent a clear

message to all site employees regarding expected levels of fitness for

duty.

Summary

Quality programs at Limerick have, in an integrated fashion, fostered

a healthy working atmosphere. Programs have sufficient overlap and

depth such that there is high assurance that undetected errors are

rare. Site management prevents significant problems by early

detection and unique resolution such that recurrences are infrequent.

The preponderant cultural attitude is one of se 'tivity to people,

and has allowed for the plant to survive difficult reorganizational

phases and other high expectations in light of questions regarding

Peach Bottom. The leadership of superintendents and front-line

. supervisors, and the management which is an out-fall from the PORC,

have been instrumental in assuring quality.

Conclusion

Category 1

Board Recommendetions

Nane

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. 39

V. SUPPOPTING DATA AND SUMMARIES

A. Investigations and Allegations

No NRC Office of Investigations reviews were conducted during the

assessment period.

Three allegations of drug use by ontract personnel during this

t' period resulted in the discharge of several workers when drug tests

confirmed the information or when they refused 'o submit t a test.

A forth drug allegation could not be pursuei due to inadequate

information from an anonymous source.

B. Escal.ated Enforcement Actions

Level III violation (no civil penalty) for Appendix R diesel fire

flow switch design.

C. Management Conferences

On July 7, 1987, t eh licensee met with NRC management on site to

discuss the previous SALP report findings.

On October 8, 1987, licensee engineering reoresentatives met with NRC

Region I personnel in King of Prussia to discuss the technical

aspects relating to flow switches in the fire suppression system

which could have affected diesel generator operability.

On October 22, 1987, an enforcement conferer.ce was held at the NRC

Region i office in King of Prussia to discuss a violation of 10 CFR

50, Appendix R requirements involving the diesel generator flow

switch cable routing.

D. Licensee Event Reports (LER).

1. Report Quality

Utilizing the basic evaluation methodology presented in NUREG-

1022, Supplement 2, overall quality of licensee event reports

(LERs) is very geod. A strong point for Limerick LERs continues

to be the in-depth discussion of failure and root cause.

'

There

has been improvement in the identification of previous occur-

rences. There has also been improvement in the safety assess-

ment discussions, but this is an area which would benefit from

added attention. The licensee routinely supplements LERs with

additional findings and has a go,d practice of using diagrams

where appropriate. While reviewing 82 LERs this assessment

period, clarification was only needed on several occasions by

the staff. However, in several instances LERs were late.

.

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.. -. _ . .

_ _ . .

..,. ,.

.

. 40

2. Causal Analysis

Number Percent

A. Personnel Error 32 39~

B. Design /Manuf./Constr./ Install. 21 26

.

C. External Cause 0 -

D. Procedure Inadequacy 8 10

E. Component Failure 12 15

X. Other (incl. unknown) 9 10

TOTAL 82 100

Events

A tabulation of LERs by functional area is attached as

Table 3.

-

LER Nos. 86-57, 87-01 to 87-70, and 88-01 to 88-11

were received and reviewed by the NRC during the

assessment period.

-

The 82 LERs which were reported during the assessment

period were also subject to an ongoing review as part

of NRC inspections for trends and root cause

l

identification. The following sets of common mode

l

events were identified:

l

l a. Thirty-two LERs were attributed to personnel error.

L (Approximately 26 on an ann- lized basis.) These LERs

! accounted for approximately ,J% of the events reported as

.

was the case during the previous assessment period.

.4e>

As shown in the following table the refueling outage period

accounted f:r a significant percentage (56%) of the total

number of personnal error LERs. For the periods outside of

the outage, there appears to be a gradually improving trend

in the number of personnel error LERs as well as the

percentage of the total.

c

M- a _ _ , _ _ _ _ . _ , . . , , , _ _ , _ . , . _ --. , , .. . _ _ _

, _ . _ _ _ _ . _ . .

_ _ _ - - _ _ _ _ _ _ _ - _ - - _ _

.. < ,

.

. 41

Personnel Error  % of

Time Frame (Quarterly) LERs Total

Feb 1-Apr 30, 1987 4 31

May 1-Jul 31,1987 14 56

Aug 1-Oct 31, 1987 9 39

Nov 1, 1987-Jan 31, 1988 3 25

Feb 1-Apr 30, 1988 2 22

May 15-Aug 26, 1987 18 60

(Refueling Outage)

A different breakdown of the personnel errors indicates

that approximately 62% were partially or wholly a result of

inattention to detail, whereas a lack of knowledge

necessary to complete a specific task or poor judgement

were primary factors in 25% and 13%, respectively, of the

remaining LERs.

Increased management attention to personnel errcrs as a

result of the significant increase during the outage

appears to have been effective.

b. Twenty-one LERs were attributed to design, manufacturing,

construction or installation problems. Of these, five were

again a result of the sensitivity of the control room

chlorine detectors to moisture and the fact that onr. of two

instruments will initiate a control room isolation.

Further modifications were planned to revise the system

logic so that spurious signals on one instrument will not

cause an isolation, although this has been a chronic

problem.

o

'

The remaining LERs were the result of various problems

however, there did not appear to be any common cause or

programmatic deficiencies evident.

c. LER 87-47 was attributed to an external cause in that a

control room isolation occurred in respcise to apparentir

l higher than normal chlorine levels in the atmosphere

however the source of the chlorine could not be identified.

d. Eight LERs were a result of procedural deficiencies. On an

annualizec basis this represents an approximate 20%

reduction from the previous assessment period and mairitains

a downward trend noted in the previous SALP. A detailed

, review of the eigh. LERs did not reveal any cause for

! cnncern that a systematic problem may be present in the

station's procedure writing and revision programs.

l

1

, _ .

. _

.,

7

o . .

A

- 42

e. Component failures accounted for 12 LERs during the period.

This represents a negligible increase in the rate of

component failures over the number experienced during the

previous period. A detailed review did not indicate any

maintenance program, procedure, or performance problems

which may have contributed to the failures,

i

1

i

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[- --

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, . .

.

i . 43

TABLE 1

Inspection Hours Summary

February 1, 1987 - April 30, 1988

Limerick Generating Station Unit 1

Hours  % of Time

A. Plant Operations 1191 29

B. Radiological Controls 429 11

C. Maintenance 503 12

D. Surveillance 549 14

E. Engineering / Technical Support 958 24

F. Emergency Preparedness 121 3

G. Security and Safeguards 281 7

H. Safety Assessment / Quality Verification *

__

TOTAL 4032 100

  • Hours expended in the area of safety assessment / quality verification are

included in other functional areas.

Inspection hours are the result of NRC Inspection Report Numbers 87-05 through

31, anc Numbers 88-01 through 0 3.

i

Total hours represent a 15-month assessment period, and are equivalent to 3226

hours on an annualized basis. Approximately two-thirds of th( total time (2650

hours) was expended by resident inspection documented in 11 reports. The other

one-third of the total time (1382 hours0.016 days <br />0.384 hours <br />0.00229 weeks <br />5.25851e-4 months <br />) was expended by specialist or team

inspections (EQ, EP, Restart and E0P teams) as documented in 22 reports during

the assessment period,

i

l

l

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i

l

L

l

i

i

, ; ,_ . -, - _. . . .. . . _ . . - _ . . - - . .

e <* .

,

, 44

TABLE 2

Enfor ement Summary

Limerick Unit 1

'

2/1/87 - 4/30/88 .

Violations and

S_everity Level

Functional Area III IV V Subtotal

A. Plant Operations 0 2 1 3

B. Radiological Controls 0 0 0 0

C. Maintenance 0 0 1 1 ,.

D. Surveillance 0 0 0 0

E, Engineering / Technical 1 4 0 5

Support

F. Emergency P.eparedness 0 2 0 2

G. Security / Safeguards 0 1 0 1

H. Safety Assessment /

Quelity Verification r

TOTAL 1 9 2 12

l

1

I

L

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-

,

<$ ~

, 45

TABLE 3

Licensee Event Reports

Limerick Unit 1

2/1/87 - 4/30/88

Number by Cause

Functional Area A B C D E X Subtotal

i

A. Plant Operations 20 2 0 1 4 3 20

B. Radiological Controls 0 0 0 0 0 0 0

C. Maintenance 3 1 0 0 2 1 7

D. Surveillance 16 1 0 6 4 0 27

E. Engineering / Technical 3 17 0 1 2 5 28

Support

F. Emergency Preparedness 0 0 0 0 0 0 0

G. Security /Saf(guards *

H. Safety Assessment / 0 0 0 0 0 0 0

Quality Verification

TOTALS 32 21 0 8 12 9 82

  • Security Event Reports are discussed separately in Section III.G.

Causal Codes: A. Personnel Error

B. Design, Manufacturing or Installation

C. Unknown or External Cause

D. Procedure Inadequacy

E. Component Failure

X. Othe-

As discussed in Section V.0, LER tabulations include LER Nos. 86-57, 87-01

to 70, and 68-01 to 11.

i