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MONTHYEARML20211N5061999-09-0909 September 1999 Forwards TSs Bases Pages B 3/4 10-2 & B 3/4 2-4 for LGS, Units 1 & 2,being Issued to Assure Distribution of Revised Bases Pages to All Holders of TSs Project stage: Other 1999-09-09
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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217D5211999-09-30030 September 1999 Informs That Remediating 3D Monicore Sys at Pbaps,Units 2 & 3 & 3D Monicore/Plant Monitoring Sys at Lgs,Unit 2 Has Been Completed Ahead of Schedule ML20216J3981999-09-29029 September 1999 Submits Comments for Lgs,Unit 1 & Pbaps,Units 2 & 3 Rvid,Rev 2,based on Review as Requested in GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity ML20212J6561999-09-29029 September 1999 Informs of Completion of mid-cycle PPR of Limerick Generating Station on 990913.Identified No Areas in Which Licensee Performance Warranted Addl Insp Beyond Core Insp Program.Historical Listing of Plant Issues Encl ML20212H6401999-09-24024 September 1999 Forwards Revised Epips,Including Rev 11 to ERP-101 & Rev 18 to ERP-800.Copy of Computer Generated Rept Index Identifying Latest Revs of LGS Erps,Encl ML20212E7941999-09-22022 September 1999 Requests Authorization for Listed Licensed Operators to Temporarily Suspend Participation in Licensed Operator Requalification Program at LGS ML20212E8081999-09-22022 September 1999 Provides Notification That Listed Operators Have Been Permanently Reassigned to Duties That Do Not Require Maintaining Licensed Operator Status,Per 10CFR50.74 ML20212F5481999-09-20020 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing, for Pbaps,Units 2 & 3 & Lgs,Units 1 & 2 ML20212F8991999-09-17017 September 1999 Provides Written Confirmation That Thermo-Lag 330-1 Fire Barrier Corrective Actions at Lgs,Units 1 & 2 Have Been Completed 05000353/LER-1999-010, Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl1999-09-16016 September 1999 Forwards LER 99-010-00,re Manual Actuation of Esf.Main CR Ventilation Sys Was Placed in Chlorine Isolation Mode Due to Rept of Faint Odor of Chlorine in Unit 2 Reactor Encl ML20216F7821999-09-16016 September 1999 Forwards Insp Repts 50-352/99-05 & 50-353/99-05 on 990713-0816.One Violation Noted & Being Treated as NCV, Consistent with App C of Enforcement Policy.Violation Re Inoperability of Automatic Depression Sys During Maint ML20212A8751999-09-13013 September 1999 Forwards Safety Evaluation of First & Second 10-year Interval Inservice Insp Plan Request for Relief ML20211N5061999-09-0909 September 1999 Forwards TSs Bases Pages B 3/4 10-2 & B 3/4 2-4 for LGS, Units 1 & 2,being Issued to Assure Distribution of Revised Bases Pages to All Holders of TSs ML20212A0091999-09-0909 September 1999 Provides Notification That Licenses SOP-11172 & SOP-11321, for SO Muntzenberger & Rh Wright,Respectively,Are No Longer Necessary as Result of Permanent Reassignment ML20211P8571999-09-0808 September 1999 Forwards Reactor Operator Retake Exams 50-352/99-303OL & 50-353/99-303OL Conducted on 990812 ML20211P3891999-09-0303 September 1999 Informs That During 990902 Telcon Between J Williams & B Tracy,Arrangements Were Made for NRC to Inspect Licensed Operator Requalification Program at Plant.Insp Planned for Wk of 991018 05000352/LER-1999-009, Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed1999-09-0101 September 1999 Forwards LER 99-009-00,providing 30-day Written follow-up Rept Re Performance of Maint That Affected Safeguard Sys for Which Compensatory Measures Had Not Been Employed ML20211H2571999-08-26026 August 1999 Informs of Individual Exam Result on Initial Retake Exam on 990812.One Individual Was Administered Exam & Passed ML20211E9191999-08-24024 August 1999 Forwards fitness-for-duty Program Performance Data for Jan-June 1999 for PBAPS & LGS IAW 10CFR26.71(d).Data Includes Listed Info ML20211E9731999-08-23023 August 1999 Forwards LGS Unit 2 Summary Rept for 970228 to 990525 Periodic ISI Rept Number 5, Per TS SRs 4.0.5 & 10CFR50.55a(g) ML20211D6761999-08-20020 August 1999 Forwards non-proprietary Revised Emergency Response Procedures (Erps),Including Rev 29 to ERP-110, Emergency Notification & Rev 17 to ERP-800, Maint Team & Proprietary App ERP-110-1.App Withheld Per 10CFR2.790(a)(6) ML20210T4271999-08-13013 August 1999 Informs That NRC Revised Info in Rvid & Releasing Rvid Version 2 as Result of Review of 980830 Responses to GL 92-01 Rev 1,GL 92-01 Rev 1 Suppl 1 & Suppl Rai.Tacs MA1197 & MA1198 Closed ML20210U2211999-08-10010 August 1999 Forwards Insp Repts 50-352/99-04 & 50-353/99-04 on 990525-0712.One Violation Occurred & Being Treated as NCV, Consistent with App C of Enforcement Policy.Violation Re Late Performance of off-gas Grab Sample Surveillance 05000353/LER-1999-005, Forwards LER 99-005-00,re Actuation of Primary Containment & Reactor Vessel Isolation Control Sys,Esf.Fuse Failed Due to Mechanical Failure of Cold Solder Joint1999-08-10010 August 1999 Forwards LER 99-005-00,re Actuation of Primary Containment & Reactor Vessel Isolation Control Sys,Esf.Fuse Failed Due to Mechanical Failure of Cold Solder Joint ML20211B7881999-08-10010 August 1999 Transmits Summary of Two Meetings with Risk-Informed TS Task Force in Rockville,Md on 990514 & 0714 ML20210M7571999-08-0404 August 1999 Forwards Response to Requesting Addl Info Re Status of Decommissioning Funding for Lgs,Pbaps & Sngs. Attachment Provides Restatement of Questions Followed by Response ML20210P4191999-08-0404 August 1999 Forwards Initial Exam Repts 50-352/99-302 & 50-353/99-302 on 990702-04 (Administration) & 990715-22 (Grading).Six of Limited SRO Applicants Passed All Portion of Exam NUREG-1092, Informs J Armstrong of Individual Exam Results for Applicants on Initial Exam Conducted on 990702 & 990712-14 at Facility.All Six Individuals Who Were Administered Exam, Passed Exam.Without Encls1999-08-0303 August 1999 Informs J Armstrong of Individual Exam Results for Applicants on Initial Exam Conducted on 990702 & 990712-14 at Facility.All Six Individuals Who Were Administered Exam, Passed Exam.Without Encls ML20210L2011999-07-28028 July 1999 Forwards Final Personal Qualification Statement (NRC Form 398) for Reactor Operator License Candidate LB Mchugh ML20211F2641999-07-27027 July 1999 Forwards Three Copies of Rev 12 to LGS Physical Security Plan, Rev 4 to LGS Training & Qualification Plan & Rev 2 to LGS Safeguards Contingency Plan. Without Encls 05000352/LER-1999-008, Forwards LER 99-008-00 Re 990623 Failure of Plant HPCI Sys to Start Due to Failure of HPCI Turbine,Hydraulic Actuator1999-07-23023 July 1999 Forwards LER 99-008-00 Re 990623 Failure of Plant HPCI Sys to Start Due to Failure of HPCI Turbine,Hydraulic Actuator 05000353/LER-1999-004, Forwards LER 99-004-00 Re 990701 Discovery of Pressure Setpoint Drift of Thirteen Mss SRV Due to Corrosion Induced Bonding within SRVs1999-07-23023 July 1999 Forwards LER 99-004-00 Re 990701 Discovery of Pressure Setpoint Drift of Thirteen Mss SRV Due to Corrosion Induced Bonding within SRVs ML20210E6211999-07-22022 July 1999 Submits Rev to non-limiting Licensing Basis LOCA Peak Clad Temps (Pcts) for Limerick Generating Station (Lgs),Units 1 & 2 & Pbaps,Units 2 & 3 ML20216D3081999-07-19019 July 1999 Requests Renewal of OLs for Listed Individuals,Iaw 10CFR55.57.NRC Forms 398 & 396,encl for Applicants.Without Encl ML20216D8041999-07-19019 July 1999 Submits Summary of Final PECO Nuclear Actions Taken to Resolve Scram Solenoid Pilot Valve Issues Identified in Info Notice 96-007 05000352/LER-1999-006, Forwards LER 99-006-00 Re 990614 Discovery That Grab Sample of Plant Offgas Sys Was Not Obtained within Time Limit Required by TS 3.3.7.12,Action 110 Due to Personnel Error1999-07-12012 July 1999 Forwards LER 99-006-00 Re 990614 Discovery That Grab Sample of Plant Offgas Sys Was Not Obtained within Time Limit Required by TS 3.3.7.12,Action 110 Due to Personnel Error ML20209F6341999-07-0909 July 1999 Submits Supplemental Response to GL 94-03, Intergranular Stress Corrosion Cracking of Core Shrouds in Bwrs, for Unit 2.Rev 0 to 1H61R & GE-NE-B13-02010-33NP Repts & Revised Pages to Summary Rept Previously Submitted,Encl ML20209G9121999-07-0909 July 1999 Informs That Ja Hutton Has Been Appointed Director,Licensing for PECO Nuclear,Effective 990715.Previous Correspondence Addressed to Gd Edwards Should Now Be Sent to Ja Hutton ML20209C9041999-07-0808 July 1999 Forwards Monthly Operating Repts for June 1999 for Limerick Generating Station,Units 1 & 2 & Revised Monthly Repts for May 1999 ML20210B4441999-07-0808 July 1999 Forwards Preliminary NRC Form 398 & NRC Form 396 for Reactor Operator for License Candidate LB Mchugh.Candidate Failed Category B Portion of Operating Exam Given at LGS During Week of 990315.Tentative re-exam Has Been Scheduled 990812 05000353/LER-1999-003, Forwards LER 99-003-00,re Bypass of RW Cleanup Leak Detection Sys Isolation Function on Three Separate Occasions.Bypass of Safety Function Was Caused by Inadequate Review & Approval of Change to Procedure1999-07-0707 July 1999 Forwards LER 99-003-00,re Bypass of RW Cleanup Leak Detection Sys Isolation Function on Three Separate Occasions.Bypass of Safety Function Was Caused by Inadequate Review & Approval of Change to Procedure ML20209D8821999-07-0707 July 1999 Submits Estimate of Number of Licensing Actions Expected to Be Submitted in Years 2000 & 2001,as Requested by Administrative Ltr 99-02.Renewal Applications for PBAPS, Units 2 & 3,will Be Submitted in Second Half of 2001 ML20209D2671999-07-0202 July 1999 Responds to NRC 990322 & 0420 RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20196J6301999-07-0101 July 1999 Requests Addl Info Re Status of Decommissioning Funding for Limerick Generating Station,Units 1 & 2,Peach Bottom Atomic Power Station,Units 1,2 & 3 & Salem Nuclear Generating Station,Units 1 & 2 05000352/LER-1999-004, Forwards LER 99-004-00,re Inoperability of Automatic Depressurization Sys Portion of Eccs.Condition Resulted from Incomplete Impact Review of Isolating Portion of ADS Nitrogen Backup Supply on Operability of ECCS Sys1999-07-0101 July 1999 Forwards LER 99-004-00,re Inoperability of Automatic Depressurization Sys Portion of Eccs.Condition Resulted from Incomplete Impact Review of Isolating Portion of ADS Nitrogen Backup Supply on Operability of ECCS Sys ML20209B7001999-06-30030 June 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20212J5401999-06-28028 June 1999 Discusses Completion of Licensing Action for NRC Bulletin 96-003, Potential Plugging of ECC Suction Strainers by Debris in Bwrs. Bulletin Closed for Unit 2 by NRC ML20207H8271999-06-24024 June 1999 Informs NRC That Util Has Completed Core Shroud Insps for LGS Unit 2.Proprietary Rept GE-NE-B13-02010-33P & non-proprietary Rev 0 to 1H61R,encl.Proprietary Rept Withheld,Per 10CFR2.790(a)(4) ML20196G7041999-06-24024 June 1999 Forwards Insp Repts 50-352/99-03 & 50-353/99-03 on 990413- 0524.No Violations Noted.Nrc Concluded That Licensee Staff Continued to Operate Both Units Safely ML20196A5641999-06-15015 June 1999 Provides Info Re Util Use of Four Previously Irradiated LGS, Unit 1,GE11 Assemblies in Unit 2 Cycle 6.Encl 990518 GE Ltr Provides Objective of Lead Use Assemblies Program & Outlines Kinds of Measurements That Will Be Made on Assemblies ML20195J6831999-06-11011 June 1999 Provides Proprietary Objectives for Lgs,Units 1 & 2,1999 Emergency Preparedness Exercise Scheduled to Be Conducted on 990914.Licensee Identifies Which Individuals Should Receive Copies of Info.Proprietary Info Withheld 1999-09-09
[Table view] Category:OUTGOING CORRESPONDENCE
MONTHYEARML20212J6561999-09-29029 September 1999 Informs of Completion of mid-cycle PPR of Limerick Generating Station on 990913.Identified No Areas in Which Licensee Performance Warranted Addl Insp Beyond Core Insp Program.Historical Listing of Plant Issues Encl ML20216F7821999-09-16016 September 1999 Forwards Insp Repts 50-352/99-05 & 50-353/99-05 on 990713-0816.One Violation Noted & Being Treated as NCV, Consistent with App C of Enforcement Policy.Violation Re Inoperability of Automatic Depression Sys During Maint ML20212A8751999-09-13013 September 1999 Forwards Safety Evaluation of First & Second 10-year Interval Inservice Insp Plan Request for Relief ML20211N5061999-09-0909 September 1999 Forwards TSs Bases Pages B 3/4 10-2 & B 3/4 2-4 for LGS, Units 1 & 2,being Issued to Assure Distribution of Revised Bases Pages to All Holders of TSs ML20211P8571999-09-0808 September 1999 Forwards Reactor Operator Retake Exams 50-352/99-303OL & 50-353/99-303OL Conducted on 990812 ML20211P3891999-09-0303 September 1999 Informs That During 990902 Telcon Between J Williams & B Tracy,Arrangements Were Made for NRC to Inspect Licensed Operator Requalification Program at Plant.Insp Planned for Wk of 991018 ML20211H2571999-08-26026 August 1999 Informs of Individual Exam Result on Initial Retake Exam on 990812.One Individual Was Administered Exam & Passed ML20210T4271999-08-13013 August 1999 Informs That NRC Revised Info in Rvid & Releasing Rvid Version 2 as Result of Review of 980830 Responses to GL 92-01 Rev 1,GL 92-01 Rev 1 Suppl 1 & Suppl Rai.Tacs MA1197 & MA1198 Closed ML20211B7881999-08-10010 August 1999 Transmits Summary of Two Meetings with Risk-Informed TS Task Force in Rockville,Md on 990514 & 0714 ML20210U2211999-08-10010 August 1999 Forwards Insp Repts 50-352/99-04 & 50-353/99-04 on 990525-0712.One Violation Occurred & Being Treated as NCV, Consistent with App C of Enforcement Policy.Violation Re Late Performance of off-gas Grab Sample Surveillance ML20210P4191999-08-0404 August 1999 Forwards Initial Exam Repts 50-352/99-302 & 50-353/99-302 on 990702-04 (Administration) & 990715-22 (Grading).Six of Limited SRO Applicants Passed All Portion of Exam NUREG-1092, Informs J Armstrong of Individual Exam Results for Applicants on Initial Exam Conducted on 990702 & 990712-14 at Facility.All Six Individuals Who Were Administered Exam, Passed Exam.Without Encls1999-08-0303 August 1999 Informs J Armstrong of Individual Exam Results for Applicants on Initial Exam Conducted on 990702 & 990712-14 at Facility.All Six Individuals Who Were Administered Exam, Passed Exam.Without Encls ML20196J6301999-07-0101 July 1999 Requests Addl Info Re Status of Decommissioning Funding for Limerick Generating Station,Units 1 & 2,Peach Bottom Atomic Power Station,Units 1,2 & 3 & Salem Nuclear Generating Station,Units 1 & 2 ML20212J5401999-06-28028 June 1999 Discusses Completion of Licensing Action for NRC Bulletin 96-003, Potential Plugging of ECC Suction Strainers by Debris in Bwrs. Bulletin Closed for Unit 2 by NRC ML20196G7041999-06-24024 June 1999 Forwards Insp Repts 50-352/99-03 & 50-353/99-03 on 990413- 0524.No Violations Noted.Nrc Concluded That Licensee Staff Continued to Operate Both Units Safely ML20206Q5871999-05-14014 May 1999 Advises That Info Contained in ,Which Submitted Revised Procedures for Plant EP Response Procedures Will Be Withheld from Public Disclosure,Per 10CFR2.790(a)(6) ML20206R3031999-05-11011 May 1999 Informs That on 990407,NRC Administered GFE Section of Written Operator Licensing Exam to Employees of Facility. Forwards Copies of Both Forms of Exam,Including Answer Keys & Grading Results of Facility ML20206N1111999-05-0707 May 1999 Forwards Insp Repts 50-352/99-02 & 50-353/99-02 on 990302-0412.Three Violations of NRC Requirements Occurred & Being Treated as non-cited Violations,Consistent with App C of Enforcement Policy ML20206H2651999-05-0606 May 1999 Informs That on 990112 Licensee Submitted to NRC Core Shroud Insp Plan for Plant,Unit 2,in Response to GL 94-03, Intergranular Stress Corrosion Cracking of Core Shrouds in Boiling Water Reactors ML20206G5131999-05-0303 May 1999 Approves Change of Completion Date for Implementation of Thermo-Lag Fire Barrier Corrective Actions at Plant from End of April 1999 Limerick Unit 2 RFO to 990930 ML20206H8301999-04-30030 April 1999 Forwards Exam Repts 50-352/99-301 & 50-353/99-301 on 990312-19 (Administration) & 22-26 (Grading).Four of Five RO Applicants & Three of Four SRO Applicants Passed All Portions of Exams ML20206E6951999-04-30030 April 1999 Advises That Plant,Unit 2 Cycle 6 Safety Limit Mcpr, ,contained in PECO Energy Co 990311 Application & 990204 Affidavit Will Be Withheld from Public Disclosure,Per 10CFR2.790 ML20206F4221999-04-27027 April 1999 Informs of Individual Exam Results for Applicants on Initial Exam Conducted on 990312 & 990315-19 at Facility.Completed ES-501-2,power Plant Licensing Exam Results Summary & Summary of Overall Exam Results Encl.Without Encl ML20205N2291999-04-0909 April 1999 Discusses Limerick Generating Station Plant Performance Review Conducted for Period April 1998 Through 990115 & Informs of NRC Planned Insp Effort Resulting from Review. Historial Listing of Plant Issues,Encl IR 05000352/19980091999-03-30030 March 1999 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Repts 50-352/98-09 & 50-353/98-09 Issued on 990106.Actions Will Be Examined During Future Insp of Licensed Program ML20205C2711999-03-26026 March 1999 Forwards Insp Repts 50-352/99-01 & 50-353/99-01 on 990112-0301.One Violation Noted & Being Treated as Non-Cited Violation.Staff Conduct of Activities During Insp Generally Characterized by Safe & Conservative Decision Making ML20205G7651999-03-22022 March 1999 Forwards RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs, for Plant, Units 1 & 2.Response Requested within 90 Days of Receipt of Ltr ML20204G9721999-03-11011 March 1999 Informs of Completion of Review of Changes Proposed by PECO Energy Co to Lgs,Units 1 & 2,EALs.Proposed EALs Incorporate Guidance in NUMARC/NESP-007,Rev 2.Forwards Safety Evaluation Supporting Proposed Changes ML20204H8171999-03-10010 March 1999 Discusses Request That NEDC-32645P, Limerick Generating Station,Units 1 & 2,SRV Setpoint Tolerance Relaxation Licensing Rept, Rev 2,dtd Dec 1998,be Withheld from Public Disclosure.Determined Info Proprietary & Will Be Withheld ML20207J0611999-03-0808 March 1999 Provides Authorization to Administer Initial Written Exams to Listed Applicants on 990312.NRC Region I Operator Licensing Staff Will Administer Operating Tests on 990315-19 at Limerick Generating Station ML20203G6721999-02-17017 February 1999 Second Partial Response to FOIA Request for Documents. Records in App D Encl & Being Made Available in Pdr.App E Records Being Withheld in Part (Ref FOIA Exemption 5) & App F Records Completely Withheld (Ref FOIA Exemptions 6 & 7) ML20203B9001999-02-0808 February 1999 First Partial Response to FOIA Request for Documents. Forwards Documents Listed in App a Already Available in PDR, Documents in App B Released in Entirety & Documents in App C Being Withheld in Part (Ref Exemption 6) ML20202J0261999-02-0303 February 1999 Informs of Completion of Licensing Action for NRC Bulletin 96-03, Potential Plugging of Emergency Core Cooling Suction Strainers by Debris in Boiling-Water Reactors ML20203A6111999-01-22022 January 1999 Confirms 990115 Conversation Between Mj Williams & P Orphanos Re Arrangements Made for Administration of Licensing Exam at Limerrick Generating Station & Peach Bottom Atomic Power Station During Week of 990705 ML20199F9251999-01-11011 January 1999 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Repts 50-352/98-05 & 50-353/98-05 ML20199C6501999-01-0606 January 1999 Forwards Insp Repts 50-352/98-09 & 50-353/98-09 on 981018- 1130 & Notice of Violation.Violation of Concern Because Technicians Exercised Poor Judgement & Deviated from Procedure in Attempt to Resolve Problem Without Mgt ML20198H4951998-12-18018 December 1998 Forwards Results of Audit of Licensee Year 2000 Program for Limerick Generating Station,Units 1 & 2 ML20198A3721998-12-10010 December 1998 Forwards Safety Evaluation Re Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20198B1751998-12-0808 December 1998 Advises of Planned Insp Effort Resulting from Limerick mid-year Insp Resource Planning Meeting Held on 981110. Historical Listing of Plant Issues & Details of Insp Plan for Next Six Months Encl IR 05000352/19980081998-11-23023 November 1998 Discusses licensee-identified Issue Involving Potential for Bypass of Suppression Pool as Documented in Insp Repts 50-352/98-08 & 50-353/98-08.NOV Will Not Be Issued & Civil Penalty Will Not Be Proposed ML20196C3311998-11-23023 November 1998 Forwards Insp Repts 50-352/98-08 & 50-353/98-08 on 980901-1017.No Violation Identified.Security Program Insp Identified That Security Program Effectively Protects Public Health & Safety ML20195D1491998-11-13013 November 1998 Forwards RAI Re on-going Review of IPEEE Submittal Dtd 951014.Understands That Licensee Will Inform NRC in Writing, by 981130,on How Question Re Effects of New Probable Max Precipitation at Plant,Units 2 & 3 Will Be Addressed IR 05000352/19980061998-10-15015 October 1998 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Repts 50-352/98-06 & 50-353/98-06 on 980826.Finds C/As for Violation Involving Failure to Select Performance Measures to Be Acceptable ML20154F8191998-10-0101 October 1998 Forwards Notice of Withdrawal of 960503 & Suppl Application for Amend to Fols.Amend Would Have Modified Facility TSs Pertaining to Rev to Frequency of Testing Stand Gas Treatment Sys & Reactor Encl Recirculation Sys ML20154A3461998-09-25025 September 1998 Forwards Insp Repts 50-352/98-07 & 50-353/98-07 on 980707-0831.No Violations Noted.Weaknesses Noted with Reactor Engineering Support to Rod Pattern Adjustment ML20153G4291998-09-24024 September 1998 Forwards Request for Addl Info Re Licensee Revised Emergency Action Level Guidelines for Limerick Generating Station, Units 1 & 2 & Peach Bottom Atomic Power Station,Units 2 & 3. Response Requested within 30 Days of Receipt of Ltr ML20153D0151998-09-21021 September 1998 Informs of Completion of Licensing Action for GL 92-08, Thermo-Lag 330-1 Fire Barriers, for Plant, Units 1 & 2 ML20151X2421998-09-11011 September 1998 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Repts 50-352/98-04 & 50-353/98-04 on 980805 ML20151W9601998-09-10010 September 1998 Informs That as Part of NRC PRA Implementation Plan, Commission Has Assigned Two Senior Reactor Analysts (Sras) to Each Regional Ofc.T Shedlosky & J Trapp Were Selected as SRAs for Region I ML20237D5421998-08-26026 August 1998 Ack Receipt of & Fee for $55,000 in Payment for Civil Penalty Proposed by NRC in .C/As Will Be Examined During Future Insps 1999-09-09
[Table view] |
Text
. .
Mr. Jim:s A. Hutton September 9, 1999 Director-Licen:ing, MC 62A-1 PECO Energy Company 1 Nuclear Group Headquarters Correspondence Control Desk P.O. Box No.195 -
Wayne, PA 19087-0195
SUBJECT:
UPDATED TECHNICAL SPECIFICATIONS (TS) BASES PAGES - LIMERICK GENERATING STATION (LGS), UNITS 1 AND 2 (TAC NOS. MA5924 AND MA5925)
Dear Mr. Hutton:
By letter dated June 9,1999, the PECO Energy Company submitted a change to TS Bases Section 3/4.10.8," Inservice Leak and Hydrostatic Testing," and TS Bases Section 3/4.2.3," Minimum Critical Power Ratio." Bases Section 3/4.10.8 was revised to clarify that the f requirements for the Reactor Enclosure Secondary Containment apply to an extended area I encompassing both the Reactor Enclosure and the Refueling Area during inservice Leak and Hydrostatic Testing. Bases Section 3/4.2.3 was revised to remove the operating limit dependence on the recirculation system motor generator set stop limiter settings. We have no objection to the wording. The enclosed revised TS Bases pages B 3/410-2 and B 3/4 s-4 for LGS, Units 1 and 2, are being issued to assure distribution of the revised bases pages to all holders of the TS.
I Sincerely, Bartholomew C. u ley Sr rofect%linager, Section 2 Project Directorate l Division of Licensing Project Management j Office of Nuclear Reactor Regulation Docket Nos. 50-352 and 50-353
Enclosure:
As stated cc w/ encl: See next page o\
DISTRIBUTION:
- Docketfilesg; 1IC B. Buckle'y PUBLIC OGC 9
PDl-2 r/f ACRS M. O'Brien DOCUMENT NAME: G:\PDI-2\ Limerick \LIA5924.MEM *See previous concurrence ;
- To receive a copy of this document, indicate in the box: "C" = Copy without I attachment / enclosure "E" = Copy with attachment / enclosure "N" = No copy !
0FFICE PM:PDI-2 @[] l E LA:PDI-2 e, 1 SRxB* l SPLB* l SCfjf-2 l !
NAME BBuckley ' M0'Brien (UlOj/O JWermlel JHannon JClifford I DATE 09/'7/99 09/ff/99 08/06/99 08/31/99 d{/1/99 9909130008 990909 cial Record Copy PDR ADOCK 05000352 P PDR
- v. .
Mr. James A. Hutton September 9, 1999 Dir:ctor-Licensing, MC 62A-1
' PECO Energy Company Nuclear Group Headquarters 1 Correspondence Control Desk i P.O. Box No.195 '
Wayne, PA 19087-0195 i
SUBJECT:
. UPDATED TECHNICAL SPECIFICATIONS (TS) BASES PAGES - LIMERICK GENERATING STATION (LGS), UNITS 1 AND 2 (TAC NOS. MA5924 AND MA5925) {
l
Dear Mr. Hutton:
By letter dated June 9,1999, the PECO Energy Company submitted a change to TS
{
Bases Section 3/4.10.8, " Inservice Leak and Hydrostatic Testing," and TS Bases Section 3/4.2.3, " Minimum Critical Power Ratio." Bases Section 3/4.10.8 was revised to clarify that the 1 requirements for the Reactor Enclosure Secondary Containment apply to an extended area encompassing both the Reactor Enclosure and the Refueling Area during inservice Leak and Hydrostatic Testing. Bases Section 3/4.2.3 was revised to remove the operating limit dependence on the recirculation system motor generator set stop limiter settings. We have no
' objection to the wording. The enclosed revised TS Bases pages B 3/410-2 and B 3/4 2-4 for LGS, Units 1 and 2, are being issued to assure distribution of the revised bases pages to all holders of the TS.
Sincerely, Bartholomew C. uble"y Sr rofect%linager, Section 2 Project Directorate i Division of Licensing Project Management Office of Nuclear Reactor Regulation .
Docket Nos. 50-352 and 50-353
Enclosure:
As stated cc w/ encl:- See next page plSTRIBUTION:
Docket Files B. Buckley PUBLIC OGC PDI-2 r/f ACRS M. O'Brien DOCUMENT NAME: G:\PDl-2\ Limerick \LIA5924.MEM *See previous concurrence To receive a copy of this document, indicate in the box: "C" = Copy without attachment / enclosure "E" = Copy with attachment / enclosure "N" = No copy
{
OFFICE PM:PDl-2 % lE LA:PDI-2 .lL SRXB* l SPLB* l SCfjf-2 l I NAME BBuckley H0'Brien JWermiel JHafinon JClifford DATE 09/'T/99 09/F/99 08/06/99 08/31/99 L9/1/99 Official Record Copy i l
ps>* *'% 9 i
[L 4 UNITED STATES
{ jt NUCLEAR REGULATORY COMMISSION WASHINGTON, D.C. 20555-0001 September.9, 1999 Mr. James A. Hutton Director-Licensing, MC 62A-1 PECO Energy Company Nuclear Group Headquarters
= Correspondence Control Desk P.O. Box No.195 Wayne, PA 19087-0195-
SUBJECT:
UPDATED TECHNICAL SPECIFICATIONS (TS) BASES PAGES - LIMERICK GENERATING STATION (LGS), UNITS 1 AND 2 (TAC NOS. MA5924 AND MA5925)
Dear Mr. Hutton:
By letter dated June 9,1999, the PECO Energy Company submitted a change to TS Bases Section 3/4.10.8," Inservice Leak and Hydrostatic Testing," and TS Bases Section 3/4.2.3, " Minimum Critical Power Ratio." Bases Sectior. 3/4.10.8 was revised to clarify that the requirements for the Reactor Enclosure Secondary Containment apply to an extended area encompassing both the Reactor Enclosure and the Refueling Area during inservice Leak and Hydrostatic Testing. Bases Section 3/4.2.3 was revised to remove the operating limit dependence on the recirculation system motor generator set stop limiter settings. We have no objection to the wording. The enclosed revised TS Bases pages B 3/410-2 and B 3/4 2-4 for LGS, Units 1 and 2, are being issued to assure distribution of the revised bases pages to all holders of trw TS.
Sincerely, e s C Bartholomew C. Buckley, Sr. Project Manager, Section 2 Project Directorate l Division of Licensing Project Management Office of Nuclear Reactor Regulation
- Docket Nos. 50-352 and 50-353
Enclosure:
As stated cc w/ encl: See next page
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Limerick Generating Station, Units 1 & 2 .,
cc:
J. W.- Durham, Sr., Esquire Chief-Division of Nuclear Safety Sr. V.P. & General Counsel PA Dept. of Environmental Resources PECO Energy Cornpany P.O. Box 8469 2301 Market Street Harrisburg, PA 17105-8469 Philadelphia, PA 19101 Manager-Limerick Licensing,62A-1 Director-Site Engineering PECO Energy Company Limerick Generating Station 965 Chesterbrook Boulevard P.O. Box 2300 Wayne, PA 19087-5691 Sanatoga, PA 19464 Mr. James D. von Suskil, Vice President !
Limerick Generating Station Manager-Experience Assessment Post Office Box 2300 Limerick Generating Station Sanatoga, PA 19464 P.O. Box 2300 Sanatoga, PA 19464 Plant Manager Limerick Generating Station Library P.O. Box 2300 U.S. Nuclear Regulatory Commission Sanatoga, PA 19464 Region i 475 Allendale Road Regional Administrator, Region i King of Prussia, PA 19406 U.S. Nuclear Regulatory Commission 475 Allendale Road -
Senior Manager-Operations King of Prussia, PA 19406 Limerick Generating Station P.O. Box 2300 Senior Resident inspector Sanatoga, PA 19464 U.S. Nuclear Regulatory Commission Limerick Generating Station Dr. Judith Johnsrud P.O. Box 596 National Energy Committee Pottstown, PA 19464 ' Sierra Club 433 Orlando Avenue Chairman State College, PA 16803 J Board of Supervisors of L.imerick Township 646 West Ridge Pike Linfield, PA 19468 l
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?!4.10 SPECIAL TEST EXCEP C NS BASES 3/4.10.8 INSERVICE LEAK AND WYDR0 STATIC TESTING
- This special test exception permits certain reactor coolant pressure tests to be performed in OPERATIONAL CONDITION 4 when the metallurgical characteristics of th~e reactor pressure vessel (RPV) or plant temperature control capabilities during these tests require the pressure testing at temperatures greater than 200*F and less than or equal to 212*F (normally corresponding to OPERATIONAL CONDITION 3). The additionally imposed OPERATIONAL CONDITION 3 requirements for SECONDARY CONTAINMENT INTEGRITY provide conservatism in response to an operational event.
Invoking the requirement for Refueling Area Secondary Containment Integrity along with the requirement for Reactor Enclosure Secondary Containment Integrity applies the requirements for Reactor Enclosure Secondary Containment Integrity to an extended area encompassing Zones 1 and 3. Operations with the Potential for Draining the Vessel, Core alterations, and fuel handling are prohibited in this secondary containment configuration. Drawdown and inleakage testing performed for the combined zone system alignment, shall be considered adequate to demonstrate integrity of the combined zones.
Inservice hydrostatic testing and inservice leak pressure tests required by Section XI of the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code are performed prior to the reactor going critical after a refueling outage. The minimum temperatures (at the required pressures) allowed for these tests are determined from the RPV pressure.and temperature (P/T) limits required by LCO 3.4.6, Reactor Coolant System Pressure / Temperature Limits. These limits are conservatively based on the fracture toughness of the reactor vessel, taking into accounta anticipated vessel neutron fluence. With increased reactcIr fluence ovir tMie, the minimum allowable vessel temperature increases at a given pressure. Periodic updates to the RCS P/T limit curves are performed as necessary, based upon the results of analysis of irradiated surveillance specimens removed from the vessel.
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MAY 0 61999 LIMERICK - UNIT 1 B 3/4 10-2 Amendment No. 188 ECR 99-00864 Revised by NRC letter dated
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3/4.10 SPECIAL TEST EXCEPTIONS BASES 3/4.10.8 INSERVICE LEAK AND HYDROSTATIC TESTING This special test exception permits certain reactor coolant pressure tests to be performed in OPERATIONAL CONDITION 4 when the metallurgical characteristics of the reactor pressure vessel (RPV) or plant temperature control capabilities during these tests require the pressure testing at temperatures greater than 200*F and less than or equal to 212*F (normally corresponding to OPERATIONAL CONDITION 3). The additionally imposed OPERATIONAL CONDITION 3 requirements for SECONDARY CONTAINMENT INTEGRITY provide conservatism in response to an operational event.
Invoking the requirement for Refueling Area Secondary Containment Integrity along with the requirement for Reactor Enclosure Secondary Containment Integrity applies the requirements'for Reactor Enclosure Secondary Containment Integrity to an extended area encompassing Zones 2 and 3. Operations with the Potential for Draining the Vessel, Core alterations, and fuel handling are prohibited in this secondary containment configuration. Drawdown and inleakage testing performed for !
the combined zone system alignment shall be considered adequate to demonstrate i integrity of the combined zones. 1 Inservice hydrostatic testing and inservice leak pressure tests required by Section XI of the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code are perfor:r.cd prior to the reactor going critical after a refuel 1r.; outage. The minimum temperatures (at the required pressures) allowed for these tests are determined from the RPV pressure and temperature (P/T) limits required by LC0 3.4.6, Reactor Coolant System Pressure / Temperature Limits. These limits are conserwahvely based on the fracture toughness of the reactor vessel, takinq into account anticipated vessel neutron fluence. With increased reactor f' uence over time, the minimum allowable vessel temperature increases at a given pressure. Periodic updates to the RCS P/T limit curves are performed as necessary, based upon the results of analysis of irradiated surveillance specimens removed from the vessel.
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MAY 0 61999 LIMERICK - UNIT 2 B 3/4 10-2 Amendment No. 95 ECR 99-00864 Revised by NRC letter dated
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POWER DISTRIBUTION llMITS BASES
.3/4.2,3 MINIMUM CRITICAL POWER RATIO The required operating limit MCPRs at steady-state operating conditions
> as specified in Specification 3.2.3 are derived from the established fuel cladding transients.integrity Safety Limit MCPR, and an analysis of abnormal operational For any abnormal operating transient analysis evaluation with the initial condition of the reactor being at the steady-state operating limit, it is required that the resulting MCPR does not decrease below the Safety Limit
'in Specification 2.2.MCPR at any time during the transient assuming-instrument trip To assure that the fuel cladding integrity Safety Limit is not exceeded during any anticipated abnormal operational transient, the most limiting tran-sients have been analyzed to determine which result in.the largest reduction in CRITICAL POWER RATIO CPR . The t {
flow, increase in pressur(e an)d power,ype of transients positive reactivity evaluated insertion, and were loss of coolant temperature decrease.
The evaluation of a given transient begins with the system initial para-meters shown in FSAR Table 15.0-2 that are input to a GE-core dynamic behavior transient computer program. The codes used to evaluate transients are discussed j in Reference 2.
The MCPR operating limits derived from the transient analysis are dependest on the operating core flow and power state (MCPR(F , and MCPR(P), respectively 10 ensure adherence to fuel design limits during the w)orst transient that occurs e).f with moderate frequency (Ref. 6). Flow dependent MCPR limits determined by steady state thermal hydraulic methods with key p(MCPR(F))
hysics response are 4
analyze slow flow runout transients. inputs benchmarked using- the three d dimensional transient code (Ref. 8). Power dependent MCPR limits (MCP Due to the sensitivity of the transient response to initial core flow levels at power levels below those at which the turbine stop valve closure and turbine control valve fast closure scrans are between 25% RTP and 30% RTP. bypassed, high and low flow MCPR(P), op The MCPR operating limits specified in the COLR are the result of).ho-ro.-
Design Basis Accident (DBA) and transient analysis.
is determined by the larger of the MCPR(F), and MCPR(P) limits.The operating limit MCP JUN 0 31999 LIMERICK - UNIT 1 B 3/4 2-4 Amendment No. 7 M, M, W, #
ECRLG99-0113d i Revised by NRC letter dated
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POWER DISTRIBUTION LIMITS BA3ES 3/4.2.3 MINIMUM CRITICAL POWER RATIO The required operating limit MCPRs at steady-state operating conditions as specified in Specification 3.2.3 are derived from the established fuel cladding integrity Safety Limit MCPR, and an analysis of abnormal operational transients. For any abnormal operating transient analysis evaluation with the initial condition of the reactor being at the steady-state operating limit, it is required that the resulting MCPR does not decrease below the Safety Limit MCPR at any time during the transient assuming instrument trip setting given in Specification 2.2.
To assure that the fuel cladding integrity Satety Limit is not exceeded during any anticipated abnormal operational transient, the most limiting tran-sients have been analyzed to determine which result in the largest reduction in CRITICAL POWER RATIO (CPR). The type of transients evaluated were loss of flow, increase in pressure and power, positive reactivity insertion, and coolant temperature decrease.
The evaluation of a given transient begins with the system initial para-meters shown in FSAR Table 15.0-2 that are input to a GE-core dynamic behavior transient computer program. The codes used to evaluate transients are discussed in Reference 2.
The MCPR operating limits derived from the transient analysis are dependent on the operating core flow and power state (MCPR(F), and MCPR(P), respective 4pttet ensure adherence to fuel design limits during the worst transient that occurs with moderate frequency (Ref. 6). Flow dependent MCPR limits (MCPR(F)) are determined by steady state thermal hydraulic methods with key physics response inputs benchmarked using the three dimensional BWR simulator code (Ref. 7) to analyze slow flow runout transients.
Power dependent MCPR limits (MCPR(P)) are determined mainly by the one dimensional transient code (Ref. 8). Due to the sensitivity of the transient response to initial core flow levels at power levels below those at which the turbine stop valve closure and turbine control valve fast closure scrams are bypassed, high and low flow MCPR(P), operating limits are provided for operating between 25% RTP and 30% RTP.
The MCPR operating limits specified in the COLR are the result of the Design Basis Accident (DBA) and transient analysis. The operating limit MCPR is determined by the larger of the MCPR(F), and MCPR(P) limits.
JUN 0 31999 LIMERICK - UNIT 2 B 3/4 2-4 Amendment No. +, 40-ECR LG 99-01138 Revised by NRC letter dated
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