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| {{Adams | | {{Adams |
| | number = ML20138R802 | | | number = ML20197J548 |
| | issue date = 11/13/1985 | | | issue date = 05/06/1986 |
| | title = Safety Insp Rept 50-454/85-42 on 850812-1018.Violation Noted:Improper Operation of Eccs,Failure to Follow Tech Spec Requirements & Reactor Core Licensed Thermal Power Rating Exceeded | | | title = Forwards Insp Repts 50-454/85-42,50-454/85-43 & 50-454/85-56 on 850812-1031 & Notice of Violation & Proposed Imposition of Civil Penalty |
| | author name = Warnick R | | | author name = Keppler J |
| | author affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) | | | author affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
| | addressee name = | | | addressee name = Oconnor J |
| | addressee affiliation = | | | addressee affiliation = COMMONWEALTH EDISON CO. |
| | docket = 05000454 | | | docket = 05000454 |
| | license number = | | | license number = |
| | contact person = | | | contact person = |
| | document report number = 50-454-85-42, NUDOCS 8511190053 | | | document report number = EA-86-048, EA-86-48, NUDOCS 8605200070 |
| | package number = ML20138R795 | | | package number = ML20197J553 |
| | document type = INSPECTION REPORT, NRC-GENERATED, INSPECTION REPORT, UTILITY, TEXT-INSPECTION & AUDIT & I&E CIRCULARS | | | document type = CORRESPONDENCE-LETTERS, NRC TO UTILITY, OUTGOING CORRESPONDENCE |
| | page count = 12 | | | page count = 4 |
| }} | | }} |
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| U.S. NUCLEAR REGULATORY COMISSION
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| ==REGION III==
| | MAY 6 1986 Docket No. 50-454 License No. NPF-37 EA 86-48 Commonwealth Edison Company ATTN: Mr. James J. O'Connor President Post Office Box 767 |
| Report No. 50-454/85042(DRP)
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| Docket No. 50-454 License No. NPF-37 Licensee: Commonwealth Edison Company Post Office Box 767 Chicago, IL 60690 Facility Name: Byron Station, Unit 1 Inspection At: Byron Station, Byron, IL Inspection Conducted: August 12 through October 18, 1985 Enforcement Conference: Scheduled for November 22, 1985 Inspectors: W. L. Forney P. G. Brochman Approved By:
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| RFklarnlh R. F. Warnick, Chief ////S/J'5'
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| Reactor Projects Branch 1 Da'te '
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| Inspection Summary Inspection on August 12 through October 18, 1985 (Report No. 50-454/85042(DRP))
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| Areas Inspected: Special unannounced safety inspection by a regional inspector and a resident inspector to review licensee performance in complying with the Facility License and Technical Specification requirements. 'An Enforcement Conference is scheduled for November 22, 1985. The inspection consisted of 69 inspector-hours onsite and at the Region III office by two NRC inspector Results: _This report identified three apparent violations of NRC requirements:
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| (1) operation of the ECCS system designed to mitigate serious safety ;
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| events such that it could not have performed its intended safety function and
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| failure to follow the applicable Technical Specification Action Requirements -
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| Paragraph 3; (2) failure of management controls necessary to assure compliance with the Technical Specifications, 3 examples - Paragraphs 4, 5, and 6; and (3) exceeding the reactor core licensed thermal power rating - Paragraph These violations are considered to be of safety significance with the potential to effect the public's health and safet PDR
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| DETAILS 1. Persons Contacted Commonwealth Edison Company R. Querio, Station Manager-R. Pleniewicz, Production Superintendent T. Tulon, Operating Engineer D. Brindle, Operating Engineer F. Hornbeak, Technical Staff Supervisor C. Kilbride, Technical Staff E. Wurtz, Technical Staff 2. General This inspection was conducted as a result of Region III management's continuing concern regarding Unit 1 unplanned reactor trips, missed Technical Specification surveillances, failure to meet Technical Specification Limiting Conditions for Operation Action Statement requirements, and the large number of Licensee Event Reports (LER)
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| issued to dat The inspection which began on August 12, 1985 and concluded on October 18, 1985, included reviews of the LERs and the circumstances surrounding: (1) operation of the unit in Mode 1 with both subsystems of the Emergency Core Cooling System (ECCS) inoperable; (2) operation of the unit in Mode 3 with Channel 8 of the Engineered Safety Features Actuation System (ESFAS) inoperable for a period of time in excess of that allowed by the Technical Specification Action Requirement; (3) operation of the Radioactive Gaseous Effluent system with concentrations of Hydrogen (H2 )
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| and Oxygen (0 2 ) in excess of that allowed by Technical Specifications; (4) failure to take grab samples when Radioactive Gaseous Effluent Monitors for H2 and 02 were inoperable; and (5) operation of the unit at re ntor core thermal power levels in excess of that allowed by the Facility Operating Licens The inspector's evaluation of these 5 events consisted of a review of the circumstances surrounding each LER and interviews with licensee personne For each LER the inspector developed a chronology; reviewed the functioning of safety systems required by plant conditions; reviewed licensee actions to verify consistency with the Facility Operating License, Technical Specifications, and implementing procedures; reviewed the licensee evaluation of the event; and reviewed previously identified problems of a similar nature. Details of the events are provided in Paragraphs 3 through 7 belo . Operating With Both ECCS Subsystems Inoperable (Closed) LER (454/85081-LL): This LER described events on March 6 through July 24, 1985, while in Mode 1 (power operations greater than 5% power),
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| involving inoperability of both ECCS subsystems and the failure to follow
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| Technical Specification Action Requirements. This event was discovered by licensee personnel following identification of a similar problem at the Callaway Nuclear Power Station by the NR The low pressure injection portion of the ECCS consists of two Residual Heat Removal (RHR) pumps, two RHR Heat Exchangers, and suction and discharge flowpaths (see Attachment 1). Technical Specification 3. states, in part: "Two independent . . . ECCS subsystems shall be OPERABLE. . . ," when in Modes 1, 2, or 3. The Safety Analysis, contained in the Byron FSAR, for a Large Break - Loss of Coolant Accident (LB-LOCA)
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| assumes that each RHR pump is capable of injecting cold borated water into all four Reactor Coolant System (RC) cold legs during the " Injection Phase" of ECCS operatio Both subsystems of the ECCS were rendered inoperable during the performance of Byron Technical Staff Surveillances 1BVS 5.2.f.3-1,
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| "ASME Surveillance Requirements for Residual Heat Removal Pump 1RH01PA"
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| [A Subsystem] and 1BVS 5.2.f.3-2, "ASME Surveillance Requirements for Residual Heat Removal Pump 1RH01PB" [B Subsystem] when valves 1RH8716A and ISI8809A (see Attachment 1) were shut during the performance of the RHR pump 1A surveillance and also when valves 1RH8716B and ISI8809B were shut during the performance of the RHR pump 18 surveillanc Byron FSAR, Figure 6.3-2 (see Attachment 1) and its notes define the position of valves 1RH8716A, 1RH8716B, ISI8809A and ISI8809B as open during the injection phase of the ECCS operation. With valves 1RH8716A or ISI8809A shut and RHR pump 1A isolated, the B subsystem would have only been capable of injecting water into a maximum of two RC cold legs (1 and 2). Conversely, with valves 1RH8716B or 15I8809B shut and RHR pump 1B isolated, the A subsystem would have only been capable of injecting water into a maximum of two RC cold legs (3 and 4). Consequently, with this valve configuration both ECCS subsystems should have been considered inoperabl Both ECCS subsystems were inoperable on nine separate instances during surveillance testing while in Mode 1. The dates of these events and the approximate length of time the valves were shut (both subsystems inoperable) is as follows:
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| Date Time Shut March 6, 1985 13.0 hours March 7, 1985 13.0 hours April 20, 1985 30.7 hours April 23,1985 6.3 hours May 30, 1985 30.2 hours May 31, 1985 5.5 hours July 24, 1985 3.5 hours July 24, 1985 1.9 hours July 24, 1985 6.9 hours
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| With both ECCS subsystems inoperable, Technical Specification 3. required that within one hour action should have been initiated to place the unit in Hot Standby (Mode 3) within the next six hours and the unit should have been placed in Hot Shutdown (Mode 4) within the following six hours. Licensee personnel failed: (1) to initiate action within one hour on the following dates: March 6, 7, April 20, 23, May 30, 31, and July 24; (2) to place the unit in Mode 3 within the next six hours on the following dates: March, 6, 7, April 20, and May 30; (3) to place the unit in Mode 4 within the following six hours on the following dates:
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| April 20 and May 3 With one RHR pump isolated and the other RHR pump capable of only injecting water into a maximum of two RC Cold Legs, both ECCS subsystems were rendered inoperable and thus a system designed to mitigate serious safety events [LB-LOCA] would not have been able to perform its intended safety function. With both ECCS subsystems inoperable, the licensee failed to initiate the required actions. These failures are an apparent violation of Technical Specifications 3.5.2 and 3.0.3 (454/85042-01(DRP)).
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| If necessary, the licensed operators in the control room could have opened the valves, upon receipt of a Safety Injection signal, with the valves taking less than 10 seconds to ope A previous violation of regulatory requirements in which both subsystems of ECCS were inoperable is described in Inspection Report No. 454/85002(DRP).
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| In that report the violation concerned the isolation of both Safety Injection pump flowpaths. The licensee's permanent corrective action in response to violation (454/85002-02(DRP)) was submitted to the NRC in a letter from D. L. Farrar to J. G. Keppler on July 10, 1985, and stated:
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| " Station personnel licer.:ed at the Senior Reactor Operator level conducted a review of all operating prcradures involving ECCS systems, even as a support system, to determine those prut.edures that could impact Technical Specification LCO's. As a result of this review, affected operating procedures were revised." The licensee's corrective action for this violation does not appear to have been effective in that it failed to identify that both ECCS systems would be inoperable during the performance of BVS 5.2.f.3-1 and 5.2.f.3- A previously identified violation (2 examples) of regulatory requirements was described in Inspection Report No. 454/85016(DRP). Violation N /85016-01(DRP) related to the failure to follow Technical Specification Action Requirements within the specified time limits. This violation concerned the failure to shut and de-energize the Pressurizer Power Operated Relief Valve (PORV) block valves when the PORVs were inoperable and the failure to place the Control Room Ventilation system in the makeup mode with an inoperable radiation monito The inspector identified a concern to the licensee that LERs 454/85017 and 454/85040 documented the failure to follow Technical Specification Action requirements and LER 454/85011 documented the failure to maintain
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| c two operable ECCS' subsystems and questioned whether these LERs should have been listed on LER 454/85081 as " previous similar events" as required by 10 CFR 50.73(b)(2)(ii)(J)(5). Additionally, the inspector questioned the LER's lack of an assessment of the safety consequences and implications of the event as required by 10 CFR 50.73(b)(2)(ii)(J)(3). These concerns will be followed as an Unresolved Item (454/85042-02(DRP)).
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| The inspector identified to the licensee that the' valve identification numbers and valve positions described in the notes attached to Byron FSAR, Figure 6.3-2, Sheet 3 were not correct for the valves labeled as numbers "22," "23," "24," "25," and "26." The licensee has committed to issuing an amendment to the FSAR to correct this problem and accomplish-ment of this action will be followed as an Open Item (454/85042-03(DRP)).
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| 4 .~ Failure to Follow Technical Specifications With ESFAS Channel B Inoperable (Closed) LER (454/85069-LL): This LER described an event on July 14-15, 1985, while in Mode 3, involving the failure to place the unit in the applicable mode when required by Technical Specification 3.3.2, Table 3.3-3, Action Statement 2 At 1904 on July 14, 1985, an instrument mechanic shorted out the power supply for Channel B of ESFAS causing a Reactor Trip. The channel was declared inoperable and licensee personnel erroneously began following the requirements of Table 3.3-3, Action Statement 14. Action Statement 14 required that the unit be placed in Cold Shutdown (Mode 5) within the next 30 hours. Licensee personnel failed to realize that Table 3.3-3, Action Statement 21 was applicable and was more restrictive than Action Statement 1 Table 3.3-3, Action Statement 21 states: "With the number of OPERABLE channels one less than the Minimum Channels OPERABLE. requirement, be in at least HOT STANDBY [ Mode 3] within 6 hours and in at least HOT SHUTDOWN
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| [ Mode 4] within the following 6 hours; however, one channel may be bypassed for up to 2 hours for surveillance testing per Specification 4.3.2.1 provided the other channel is OPERABLE." Action Statement 21 was invoked by Technical Specification 3.3.2, Table 3.3-3, Function Units 4.b, "Steamline Isolation, Automatic Actuation Logic and Actuation Relays" and 6.b, " Auxiliary Feedwater, Isolation Automatic Actuation Logic and Actuation Relays". Each of these functional units required a minimum of two OPERABLE channels when in Mode 1, 2, and 3, or else follow Action Statement 2 At 1910 on July 14, 1985, Channel B was placed in the test position
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| [ bypassed condition]. At 0104 on July 15, 1985, the unit should have been placed in Mode 4 due to the inoperability of the Steamline Isolation and Auxiliary Feedwater functions. At 0320 on July 15 licensee personnel discovered that Action Statement 21 was applicable and by 0512 had begun a cooldown to place the unit in Mode 4.
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| At 2307 on July 14, following replacement of the damaged power supply a surveillance to verify Channel B operability was performed. The Main Steam Isolation and Auxiliary Feedwater functions passed; however, several other functions failed to pass the surveillance. At 0200 on July 15 licensee personnel voided the surveillance. A voided surveillance is not an acceptable record to furnish evidence for activities affecting qualit Licensee personnel failed to recognize that the voided surveillance could not be used as evidence of the operability of the Main Steam Isolation or Auxiliary Feedwater Function At 0552 on July 15, ESFAS Channel B was placed in Normal (after having been in Test for 10.7 hours) and the cooldown was terminated. At 0612 on July 15 licensee personnel questioned the operability of the Auxiliary Feedwater Function and resumed the cooldow Mode 4 was entered at 1439 on July 15,19.6 hours after Channel B was declared inoperable; Mode 5 was entered at 2048 on July 15. The failure to place the unit in Mode 4 within six hours and placing ESFAS Channel B in Test for greater than two hours is an apparent violation of Technical Specification 3.3.2 and an example of the failure of management controls necessary to assure compliance with the Technical Specifications (454/85042-04a(DRP)).
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| ESFAS Channel A remained operable throughout the course of this event and manual initiation of these ESF components could have been performed by the licensed operators in the control room, if necessar This event is indicative of failure of corrective actions provided in response to previous!y identified violations of regulatory requirements as described in Inspection Report (454/85016(DRP)), to ensure that Technical Specification Action Requirements are correctly identified and followe (See Report Section 3)
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| The inspector identified a concern to the licensee that LERs 454/85017 and 454/85040 documented the failure to follow Technical Specification Action requirements and questioned whether these LERs should have been listed on LER 454/85069 as " previous similar events" as required by 10 CFR 50.73(b)(2)(ii)(J)(5). This concern will be followed as an Unresolved Item (454/85042-05(DRP)). An additional concern relating to use of voided documents to provide an acceptable record to furnish evidence of activities affecting quality will be followed as an Open Item (454/85042-06(DRP)).
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| 5. Explosive Gas Concentrations in the Radioactive Gaseous Effluent System (Closed) LER (454/85067-LL): This LER described events on July 6-14, 1985, while in Mode 1, involving failure to follow Technical Specifications Action Requirements for Radioactive Gaseous Effluents relating to the Hydrogen (H 2) and Oxygen (02 ) concentrations present in the Waste Gas syste )
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| On July 6, 1985, an Equipment Attendant recorded a 2H concentration of 5.5% and at 1140 a chemist recorded an 20 concentration of 3.9% on i Special Chemistry Data Sheet, BCP-400-T.60, Revision 0. Technical '
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| Specification 3.11.2.5, " Radioactive Effluents Explosive Gas Mixture,"
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| states: "The concentration of oxygen in the WASTE GAS HOLDUP SYSTEM shall be limited to less than or equal to 2% by volume whenever the hydrogen concentration exceeds 4% by volume." Applicability of this specification is "at all times." Technical Specification 3.11.2.5.a states: "With the concentration of oxygen in the WASTE GAS HOLDUP SYSTEM greater than 2%
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| by volume but less than or equal to 4% by volume, reduce the oxygen concentration to the above limits within 48 hours." The OD Waste Gas Decay tank was taken out of service on July 6, 1985, and records indicate that the tank remained out of service, with concentration of 0 2/H2 greater than that allowed by Technical Specification 3.11.2.5.a, until July 11, 1985. There is no record to indicate that the licensee initiated any action to reduce the 02 concentration at any time prior to July 11, 1985, in accordance with Byron Abnormal Operating Procedure OBOA PRI-8, "02/H2 Explosive Mixture Units 0, 1, 2."
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| Technical Specification 3.11.2.5.b states: "With the concentration of oxygen in the WASTE GAS HOLDUP SYSTEM greater than 4% by volume, immediately suspend all additions of waste gases to the system and reduce the concentration of oxygen to less than or equal to 4% by volume then take ACTION a above." At 2120 on July 11, 1985, the 0 2/H2 concentrations of the OD tank were recorded as 10.8%/4.1% respectively and remained greater than that allowed by Technical Specification 3.11.2.5.b until 1348 on July 14, 198 Review of the licensee records indicate that OB0A-PRI-8 was entered, for tank OD, on July 11, 1985, to reduce the explosive mixture of 02/H2 .
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| Licensee personnel attempted to reduce the 02 concentration below the limit of Technical Specification 3.11.2.5.b by releasing the tank; however, the release was terminated when it was determined that Radiation Monitor 0PR02J, which controls the Waste Gas discharge valve position, was inoperable due to insufficient amount of vacuum above the low limit alarm setpoint. Subsequently, a temporary alteration was installed on July 12, 1985, which would allow the release to be accomplished. At 2100 on July 12, the release from the OD tank was recommenced; however, it was observed that the pressure in tank OA was also showing a decrease and the release was terminated once again. The reason the relear was terminated was that Byron procedures do not allow for more than one Waste Gas Decay tank to be released at the same time. A nuclear work request was initiated to repair the 0A tank manual release valve, and after repairs were completed tha OD tank release was recommenced and a nitrogen purge was initiated. The talease and the purge were terminated at 1348 on July 14, 1985, when the 0 2/H2 concentrations were determined to be less than the limits of Technical Specification 3.11.2. Failure of the licensee's management systems to identify the high
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| ! concentrations of 02 /H 2 on July 6, 1985, resulted in no action being taken by the licensee to reduce these concentrations below Technical i
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| Specifications limits from July 6 until July 11, 1985. After identifi-cation by the licensee on July 11, that the 0 /H 2 2concentration in the OD tank exceeded the limits of Technical Specification 3.11.2.5.b, subsequent management decisions and management systems failed to reduce the 02/H 2 concentrations below Technical Specifications limits until July 14, 198 The inspector's review determined that the items listed below were contributing factors to this event: Incomplete / inaccurate Rad-Chem records, Incomplete Limiting Condition for Operation Action Requirement (LC0AR) data sheet Inadequate tracking of LC0AR conditions by management / supervisio Inadequate review and assessment by management / supervision of appropriate corrective actions to be accomplishe Failure of management / supervision to ensure that corrective actions identified were accomplished in a timely manne An apparent attitude of management / supervision to disregard Technical Specification Action Requirements that do not provide specific primary plant operational penaltie The failure to reduce the explosive concentrations of 0 2/H2 present in the Waste Gas system is an apparent violation of Technical Specification 3.11.2.5 and an example of the failure of management controls necessary to assure compliance with the Technical Specifications (454/85042-04b(DRP)).
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| 6. Failure to Take Grab Samples With Inoperable Radioactive Gaseous Effluent Monitors (Closed) LER 454/85082 described events on July 28 through August 4, 1985, while in Modes 1 - 4, relating to the failure to obtain and analyze grab samples from the Waste Gas system when two channels of Radioactive Effluent Monitoring Instrumentation were inoperabl At 2200 on July 16, 1985, Technical Specification 3.3.3.10, Table 3.3-13, Instrument 3.a, 0AT-GW8000, " Hydrogen Analyzer" was taken out of servic At 0720 on July 20,1985, Table 3.3-13, Instrument 3.b, 0AT-GW8003,
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| " Oxygen Analyzer" was taken out of servic Technical Specification 3.3.3.10, Table 3.3-13, Instrument 3.a required a minimum of one channel to be operable at all times, or else follow Action Statement 38. Instrument 3.b required a minimum of two channels to be operable at all times, or else follow Action Statement 38. Action Statement 38 states, in part: "With the number of channels OPERABLE one less than required by the Minimum Channels OPERABLE requirement, operation of this system may continue provided grab samples are taken and analyzed at least once per 24 hours . . . ."
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| With system operation continuing licensee personnel began taking and analyzing grab samples every 24 hours. This requirement was listed on a f
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| status board in the Rad-Chem office. On July 27 this requirement was inadvertently erased from the status board by licensee personnel. As a consequence, the licensee failed to take and analyze grab samples on the following dates: While in Mode 3: July 28, 1985 While in Mode 4: July 29 - 31,1985 While in Mode 2: August 1, 1985 While in Mode 1: August 2 - 4, 198 The failure to obtain and analyze grab samples at least once every 24 hours is an apparent violation of Technical Specification 3.3.3.10 and an example of the failure of management controls necessary to assure compliance with the Technical Specifications (454/85042-04c(DRP)).
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| The failure to obtain samples required by Technical Specifications was previously described in Inspection Report 454/85021(ORP). The licensee's permanent corrective action in response to violation 454/85021-01b(DRP)
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| was submitted to the NRC in a letter from D. L. Farrar to J. G. Keppler on July 19, 1985, and stated, in part: "A file organizer has been placed in the Station counting room for initiated surveillance procedure Technicians are periodically instructed by the responsible foreman to review the file for initiated surveillances. Initiated surveillances are also tracked on the counting room shift turnover sheet . . . ." This violation is indicative of the licensee addressing the specific violation only, but not addressing the root cause of the problem. Consequently, the action taken to avoid further violations was not effectiv These three examples (Paragraphs 4, 5, and 6) of apparent violations of Technical Specifications are indicative of the failure of Management /
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| management systems and failure of corrective actions provided in response to previously identified violations of regulatory requirements, as described in Irspection Reports No. 454/85016(DRP) and No. 454/85021(DRP)
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| to ensure that Byron's operations are conducted in accordance with regulatory requirement . Exceeding the Reactor Core Thermal Power Limit (Closed) LER (454/85080-LL): This LER described events on Auguit 6-7, 1985, while in Mode 1, involving exceeding the reactor core licensed thermal power ratin Licensee personnel monitor reactor core thermal p'ower with 4 channels of Nuclear Instruments (NI). These channels of Power Range" NI are calibrated by the performance of a secondary heat balan:: Byron Technical Specification Surveillance 180S 3.1.1-2, " Calorimetric Calculation Surveillance", accomplished this heat balance. This procedure compares the heat transferred into the steam generators with the heat transferred out of the steam generators by calculating the enthalpy of the water going in and out times its flow rate. Based on this heat balance the core thermal power is determined and the " Power Range" NI are adjusted so that 100% indicated power is equal to 3411 megawatts thermal (HWT).
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| Byron Station Facility Operating License NPF-37, License Condition 2.C(1)
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| states, in part: "The licensee is authorized to operate the facility at reactor core power levels not in excess of 3411 megawatts thermal (100%
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| power) . . . . "
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| A licensed operator perfonning the procedure identified that a portion
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| ! of the feedwater flow rate was not being accounted for. In Byron's
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| Westinghouse Model "D-4" Steam Generators the feedwater flow is split
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| into two paths. One of these paths, the tempering line feedwater flow rate was not accounted for in the surveillance procedure; consequently, a nonconservative error was introduced into the surveillance and the
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| " Power Range" NI were adjusted so that indicated power was lower than the actual reactor core power. Subsequently, licensee personnel reviewed the plant computer records and determined that this error had caused the
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| licensed thermal power limit to be exceede The NRC's policy regarding exceeding licensed power levels is that the l average power level over any eight hour shift should not exceed the full steady-state licensed power level. While it is permissible to briefly l exceed the full steady-state licensed power level by as much as 2% for as
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| | : SUBJECT: NOTICE OF VIOLATION AND PROPOSED IMPOSITION OF' CIVIL PENALTY (NRC INSPECTION REPORTS NO. 50-454/85042(DRP); 50-454/85043(DRP) |
| long as 15 minutes, in no case is it permissible for 102% power to be exceeded. Power excursions to less than 102% for periods longer than 15
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| ; minutes are permissible (i.e.,101% for 30 minutes,100.5% for one hour,
| | This refers to inspections conducted during the periods August 12 through October 18, 1985 and October 2-31, 1985 of activities authorized by NRC Operating License NPF-37 for the Byron Nuclear Power Station, Unit 1. As a result of these inspections, certain of your activities appeared to be in violation of NRC requirements. The violations were identified in the above referenced reports sent to you by letters dated November 14, 1985 and November 22, 1985, |
| ! etc.) provided that the power level, averaged over an eight hour shift, does not exceed 100%.
| | - respectively. They were also the subject of an Enforcement Conference held in the Region III office on November 27, 1985, between Mr. Bide L. Thomas and other members of your staff, and myself and other members of the NRC staf Item I discussed in the enclosed Notice of Violation and Proposed Imposition of Civil Penalties occurred on March 6, 7, April 20, 23, an'd May 30, 31, 1985 and on 3 different occasions on July 24, 198 It involved the use of procedures containing instructions for incorrect valve alignments to conduct technical specification (TS) surveillances on the residual heat removal system (RHR). |
| Reactor core power (MWT) was greater than 100% power, averaged over an eight hour shift, on the following three instances:
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| l on July 26, 1985 - 100.06%/3413 MWT on July 27, 1985 - 100.18%/3417 MWT i on July 27, 1985 - 100.30%/3421 MWT.
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| ! Additionally, the average reactor core power equaled or exceeded 100.5%
| | This rendered both trains of RHR, a subsystem of the emergency core cooling system (ECCS), inoperable in that neither train was capable of injecting into all four reactor coolant system (RCS) cold legs while the plant was in Mode The Byron Unit 1 Final Safety Analysis Report (FSAR), Chapter 6, for a Large Break Loss of Coolant Accident (LOCA) states that the ECCS fulfills its safety function by injecting into all 4 RCS cold leg These events are significant because with both RHR trains only able to inject into 2 cold legs, the plants' |
| for greater than one hour on two instances: on July 26, 1985 - 100.50%/3428 MWT on July 27, 1985 - 100.68%/3434 MW The failure to maintain reactor core power less than or equal to 3411 MWT I is an apparent violation of Facilit Condition 2.C(1) (454/85042-06(DRP)y Operating
| | ability to adequately respond to a large break LOCA was significantly degrade On June 5,1985, the NRC issued a Severity Level IV Notice of Violation because two safety injection pumps were isolated while the plant was in Mode 3 (Inspection Report No. 454/85002(DRP). Your corrective actions for that violation, as stated in your letter dated July 10, 1985, included reviewing and revising all operating procedures involving ECCS systems that could affect technical specification LCOs. Apparently, these corrective actions were inadequate because RHR procedures still contained incorrect valve alignment instruction CERTIFIED MAIL 0605200070 860506 RETURN RECEIPT REQUESTED PDR ADOCK 050004 4 O |
| ). Additionally, the License licensee NPF-37, failed License to submit a written report of this event within the 30 day time limit requirement of Facility Operating License NPF-37, License Condition Both this apparent violation and the apparent violation described in Paragraph 3 are examples of licensee personnel failing to correctly
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| preparc surveillance procedures and licensee management failing to l adequately review surveillance procedures to ensure that all applicable safety analysis conditions had been satisfied.
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| | $ Commonwealth Edison Company 2 MAY 6 1986 Item II of the enclosed Notice involves several examples of your failure to understand technical specifications, system operability, and associated action statements. Specifically, Violation II. A involves your determination after completing a July 15, 1985 surveillance test that Train B of the solid state protection system was operable, even though the main steam line isolation and auxiliary feedwater functions had not been verified during the test. Violation II.B involves your application of the wrong action statement after engineered safety features actuation system (ESFAS) Train B was declared inoperabl It also addresses the fact that ESFAS Train B was left in the test position in excess of the two hours allowed by plant technical specification Violations II.C and II.D involve the fact that action statement requirements were not met after plant personnel discovered potentially explosive gas mixtures in the waste gas holdup tank on July 6 and 11, 1985. Violation II.E involves your failure to take TS required grab samples of the waste gas holdup tank while hydrogen and oxygen analysers were out of service. Violation II.F involves your failure to perform adequate post-maintenance inspections on the control room ventilation system which resulted in components not being able to maintain the required negative pressur We are concerned that it appears that the above violations occurred as a result of inadequate management and supervision with regard to technical specification requirements. We are further concerned that some of these events should not have occurred if corrective actions to previous licensee event reports or NRC-i.dentified violations had been effectiv ' |
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| | To emphasize the need for you to ensure that: (1) the accident response capability for safety related systems is not adversely affected when performing surveillance procedure requirements; (2) system operability is evaluated by management personnel more effectively; (3) action statements are properly implemented when applicable; and (4) corrective actions taken in response to violations of NRC requirements are effective, I have been authorized, after consultation with the Director, Office of Inspection and Enforcement, to issue the enclosed Notice of Violation and Proposed Imposition of Civil Penalties in the amount of One Hundred Thousand Dollars (5100,000) for the Violations described in the enclosed Notice. In accordance with the " General Statement of Policy and Procedure for NRC Enforcement Actions," 10 CFR Part 2, Appendix C (1985) (Enforcement Policy), Item I described in the enclosed Notice has been categorized as a Severity Level III violation and Item II as a Severity Level III problem. The base value of a civil penalty for each Severity Level III violation or problem is Fifty Thousand Dollars (S50,000). The escalation and mitigation factors in the enforcement policy were considered. While I recognize that you identified the violations and took prompt and extensive corrective actions, mitigation of the civil penalties would not be appropriate because of your prior poor performance related to Item I and the multiple examples of violations in Item I You are required to respond to this letter and should follow the instructions specified in the enclosed Notice when preparing your response. In your response, you should document the specific actions taken and any additional action you plan to prevent recurrence. After reviewing your response to this Notice, including your corrective actions, the NRC will determine whether further NRC enforcement action is necessary to ensure compliance with regulatory requirement s L |
| | . Commonwealth Edison Company 3 MAY 6 1986 In accordance with 2.790 of the NRC's " Rules of Practice," Part 2, Title 10, Code of Federal Regulations, a copy of this letter and its enclosure will be placed in the NRC Public Document Roo The responses directed by this letter and the enclosed Notice are not subject to the clearance procedures of the Office of Management and Budget as required by the Paperwork Reduction Act of 1980, PL 96-511 |
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| 1 L | | Sincerely, Cr::,'-:1 % 0by |
| | .N : ] 0, ,'. ':r James G. Keppler Regional Administrator Enclosures: Notice of Violation and t Proposed Imposition of Civil Penalties Inspection Reports No. 50-454/85042(DRP); |
| | No. 50-454/85043(DRP); and |
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| | No. 50-454/85056(DRP) |
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| | cc w/ enclosures: |
| | D. L. Farrar, Director of Nuclear Licensing V. I. Schlosser, Project Manager Gunner Sorensen, Site Project Superintendent R. E. Querto, Plant Manager DCS/RSB (RIDS) |
| | Licensing Fee Management Branch Resident Inspector, RIII Byron Resident Inspector, RIII Braidwood Phyllis Dunton, Attorney General's Office, Environmental Control Division D. W. Cassel, Jr. , Es Diane Chavez, DAARE/ SAFE Steve Lewis, ELD L. 01shan, NRR LPM H. S. Taylor, Quality Assurance Division g6 |
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| | RI RIII R I RIII Nore bis Std ton D vis K er G, 6l f Gl613b |
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| .. Enforcement Conference Scheduled For November 22, 1985 An enforcement conference is scheduled for November 22,1985, to be held at the Region III office. . The inspectors met with licensee representatives on October 28, 1985 and summarized the purpose and scope of the inspection and the apparent findings. The inspectors discussed the likely informa-tional content of the inspection report with regard to documents or pr?: esses reviewed by the inspectors during the inspection. The licensee did not identify any such documents / processes as proprietar . Unresolved Items Unresolved items are matters about which more information is required in order to ascertain whether they are acceptable items, violations, or
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| deviations. Unresolved items disclosed during the inspection are discussed in Paragraphs 3 and . 'Open Items Open items are matters which have been discussed with the licensee, which will be reviewed further by the inspectors, and which involve some action on the part of the NRC or licensee or both. Open items disclosed during the inspection are discussed in Paragraphs 3 and O
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| | Commonwealth Edison Ccmpany |
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| | , MY 6 1986 Distribution PDR SECY CA JMTaylor, IE RVollmer, IE JAxelrad, IE TPoindexter, IE JGKeppler, RIII JLieberman, ELD HDenton, NRR Enforcement Coordinators RI, RII, RIII, RIV, RV |
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| | BHayes, 01 SConnelly, OIA JCrooks, AE0D IE:ES IE:EA DCS NRC Resident Inspector Project Manager, NRR State of Illinois |
| 3 gg i AMENDMEIET 44 Hot I.egs DECDEER 1983 Free SI pumps
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Similar Documents at Byron |
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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217P6171999-10-21021 October 1999 Forwards non-proprietary & Proprietary Versions of HI-982083, Licensing Rept for Byron & Braidwood Nuclear Stations. Proprietary Rept Withheld,Per 10CFR2.790(b)(4) ML20217M2871999-10-21021 October 1999 Refers to Rev 5 Submitted in May 1999 for Portions of Byron Nuclear Power Station Generating Stations Emergency Plan Site Annex.Informs That NRC Approval Not Required Based on Determination That Plan Effectiveness Not Decreased ML20217H4661999-10-18018 October 1999 Forwards Changes to EPIPs IAW 10CFR50.54(q) & 10CFR50,App E, Section V.Details of Changes Encl ML20217F7891999-10-0808 October 1999 Forwards Insp Repts 50-454/99-12 & 50-455/99-12 on 990803- 0916.One Violation Occurred Being Treated as NCV ML20217B6351999-10-0505 October 1999 Forwards for Info,Final Accident Sequence Precursor Analysis of Operational Event at Byron Station,Unit 1,reported in LER 454/98-018 & NRC Responses to Util Specific Comments Provided in ML20212L1791999-10-0505 October 1999 Informs That as Result of Staff Review of Util Responses to GL 92-01,rev 1,suppl 1 & Suppl 1 Rai,Staff Revised Info in Rvid & Is Releasing Rvid Version 2 ML20217B2991999-10-0101 October 1999 Forwards Insp Repts 50-454/99-16 & 50-455/99-16 on 990907-10.No Violations Noted.Water Chemisty Program Was Well Implemented,Resulted in Effective Control of Plant Water Chemistry ML20216J8241999-09-30030 September 1999 Notifies of Removal of NRC Headquarters & Region III Offices from Controlled Copy Distribution of Certain CE Documents. Specific Documents,Associated Controlled Copy Numbers & NRC Location Affected Are Shown on Attachment to Ltr ML20212J6751999-09-30030 September 1999 Forwards Replacement Pages Eight Through Eleven of Insp Repts 50-454/99-15 & 50-455/99-15.Several Inaccuracies with Docket Numbers & Tracking Numbers Occurred in Repts ML20217A5821999-09-29029 September 1999 Advises of NRC Plans for Future Insp Activities at Facility for Licensee to Have Opportunity to Prepare for Insps & to Provide NRC with Feedback on Any Planned Insps Which May Conflict with Plant Activities ML20216F8051999-09-17017 September 1999 Forwards Insp Rept 50-454/99-14 & 50-455/99-14 on 990823-27. Security Program Was Effectively Implemented in Areas Inspected.No Violations Were Identified ML20211P1841999-09-0808 September 1999 Forwards Insp Repts 50-454/99-15 & 50-455/99-15 on 990824- 26.No Violations Noted.Objective of Insp to Determine Whether Byron Nuclear Generating Station Emergency Plan Adequate & If Emergency Plan Properly Implemented ML20211Q6821999-09-0606 September 1999 Informs That NRC Tentatively Scheduled Initial Licensing Exam for Byron Operator Licesne Applicants During Wks of 000619 & 26.Validation of Exam Will Occur at Station During Wk of 000529 ML20211N5151999-09-0303 September 1999 Ack Receipt of Re Safety Culture & Overtime Practices at Byron Nuclear Power Station.Copy of Recent Ltr from NRC to Commonwealth Edison Re Overtime Practices & Safety Culture Being Provided ML20211K1081999-09-0202 September 1999 Responds to Request for Addl Info to GL 92-01,Rev 1,Suppl 1, Reactor Vessel Structural Integrity, for Braidwood,Units 1 & 2 & Byron,Unit 2 ML20211M1371999-09-0202 September 1999 Discusses 990527 Meeting with Ceco & Byron Station Mgt Re Overtime Practices & Conduciveness of Work Environ to Raising Safety Concerns at Byron Station.Insp Rept Assigned for NRC Tracking Purposes.No Insp Rept Encl ML20211G1221999-08-27027 August 1999 Forwards fitness-for-duty Program Performance Data for Each of Comm Ed Nuclear Power Stations & Corporate Support Employees within Scope of Rule for six-month Period Ending 990630,IAW 10CFR26.71(d) ML20211G4021999-08-25025 August 1999 Forwards Insp Repts 50-454/99-10 & 50-455/99-10 on 990622-0802.No Violations Noted ML20211B8691999-08-20020 August 1999 Forwards Insp Repts 50-254/99-10,50-265/99-10,50-454/99-09, 50-455/99-09,50-456/99-10 & 50-457/99-10 on 990628-0721. Action Plans Developed to Address Configuration Control Weaknesses Not Totally Effective as Listed 05000454/LER-1998-008, Informs That Licensee Determined That Suppl Rept to LER 98-008 Is Not Warranted.No Addl Info Was Generated Following Completion of Root Cause Investigation of Following Completion of Corrective Actions Stated in Original LER1999-08-12012 August 1999 Informs That Licensee Determined That Suppl Rept to LER 98-008 Is Not Warranted.No Addl Info Was Generated Following Completion of Root Cause Investigation of Following Completion of Corrective Actions Stated in Original LER ML20210N5651999-08-0606 August 1999 Forwards Rev 8 to Nuclear Generating Stations Emergency Plan, for Plants.With Summary of Changes ML20210M9131999-08-0202 August 1999 Forwards Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for Fys 2000 & 2001 for Comed ML20210K0771999-07-30030 July 1999 Submits 30-day Rept Re Discovery of ECCS Evaluation Model Error for Byron & Braidwood Stations,As Required by 10CFR50.46 ML20210J8951999-07-29029 July 1999 Submits Other Actions,As Described,To Be Taken for Valves to Resolve Potential Pressure Locking Concerns,In Light of Extended Period for Valve Bonnet Natural Depressurization,In Response to GL 95-07, Pressure Locking & Thermal.. ML20210E2151999-07-23023 July 1999 Forwards Byron Unit 1 B1R09 ISI Summary Rept Spring 1999 Outage,980309-990424, in Compliance with Requirements of Article IWA-6000, Records & Repts of Section XI of ASME & P&PV,1989 Edition ML20209H2991999-07-16016 July 1999 Withdraws 980529 LAR to Credit Automatic PORV Operation for Mitigation of Inadvertent Safety Injection at Power Accident.Response to NRC 990513 RAI Re LAR Encl ML20210A3151999-07-16016 July 1999 Forwards Insp Repts 50-454/99-08 & 50-455/99-08 on 990511-0621.Three Violations Being Treated as Noncited Violations ML20210B7071999-07-16016 July 1999 Responds to Requesting Review & Approval of Three Proposed Changes to Ceco QA TR,CE-1A Per 10CFR50.54(a)(3) & 10CFR50.4(b)(7) ML20207H7501999-07-12012 July 1999 Forwards Revised Pressure Temp Limits Rept, for Byron Station,Units 1 & 2.Revised Pressurized Thermal Shock Evaluations,Surveillance Capsule Rept & Credibility Repts, Also Encl ML20209G1391999-07-0909 July 1999 Forwards Results of SG Tube Insps Performed During Byron Station,Unit 1,Cycle 9 Refueling Outage within 12 Months Following Completion of Insps ML20196J9131999-07-0101 July 1999 Submits Status of Nuclear Property Insurance Currently Maintained for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR50.54(w)(3) ML20196J9061999-07-0101 July 1999 Provides Evidence That Util Maintains Guarantee of Payment of Deferred Premiums in Amount of $10 Million for Each of Thirteen Reactors,Per 10CFR140.21 ML20209B8241999-06-30030 June 1999 Forwards Five 3.5 Inch Computer Diskettes Containing Revised Annual Dose Repts for 1994 Through 1998 for Individuals Receiving Neutron Dose Not Previously Included in Reported Total Effective Dose Equivalent Values.Without Diskettes ML20196K0161999-06-30030 June 1999 Discusses 990622 Meeting at Byron Nuclear Power Station in Byron,Il.Purpose of Visit Was to Meet with PRA Staff to Discuss Ceco Initiatives in Risk Area & to Establish Dialog Between SRAs & PRA Staff ML20196G2161999-06-25025 June 1999 Forwards for NRC Region III Emergency Preparedness Inspector,Two Copies of Comed Emergency Preparedness Exercise Manual for 1999 Byron Station Annual Exercise. Exercise Is Scheduled for 990825.Without Encls ML20212H8241999-06-24024 June 1999 Informs That Effective 990531 NRC Project Mgt Responsibility for Byron & Braidwood Stations Was Transferred to Gf Dick ML20209D4861999-06-17017 June 1999 Informs That R Heinen,License OP-30953-1 & a Snow,License SOP-30212-3,no Longer Require License at Byron Station 05000454/LER-1999-002, Forwards LER 99-002-00,IAW 10CFR50.73(a)(2)(i)(b).There Are Two Actions Remaining to Address Cause of Event.Both Actions Are Listed1999-06-0808 June 1999 Forwards LER 99-002-00,IAW 10CFR50.73(a)(2)(i)(b).There Are Two Actions Remaining to Address Cause of Event.Both Actions Are Listed ML20207G0601999-06-0707 June 1999 Provides Updated Info Re Number of Failures Associated with Initial Operator License Exam Administered from 980914-0918. NRC Will Review Progress Wrt Corrective Actions During Future Insps ML20207G0421999-06-0404 June 1999 Forwards Insp Repts 50-454/99-04 & 50-455/99-04 on 990330-0510.Violations Identified & Being Treated as non-cited Violations ML20195D6351999-06-0404 June 1999 Notifies NRC of Actions That Has Been Taken in Accordance with 10CFR26, Fitness for Duty Programs ML20207E5451999-05-28028 May 1999 Forwards Insp Repts 50-454/99-07 & 50-455/99-07 on 990517-20.No Violations Noted.Fire Protection Program Was Effective ML20211M1611999-05-28028 May 1999 Discusses 990527 Meeting with Comed Re Safety Culture & Overtime Control at Byron Nuclear Plant from Videoconference Location at NRC Headquarters.Requests That Aggressive Actions Be Taken to Ensure That Comed Meets Expectations ML20207D5261999-05-26026 May 1999 Forwards Response to NRC 990318 RAI Concerning Alleged Chilling Effect at Byron Station.Attachment Contains Responses to NRC 12 Questions ML20207B6361999-05-25025 May 1999 Forwards SE Accepting Revised SG Tube Rupture (SGTR) Analysis for Bryon & Braidwood Stations.Revised Analysis Was Submitted to Support SG Replacement at Unit 1 of Each Station ML20211M1781999-05-25025 May 1999 Summarizes Concerns with Chilling Effect & Overtime Abuses at Commonwealth Edison,Byron Station.Request That Ltr Be Made Part of Permanent Record of 990527 Meeting ML20195C7911999-05-25025 May 1999 Forwards Revised COLR for Byron Unit 2,IAW 10CFR50.59.Rev Accounts for Planned Increase of Reactor Coolant Full Power Average Operating Temp from 581 F to 583 F 05000454/LER-1999-001, Forwards LER 99-001-00,IAW 10CFR50.73(a)(2)(i)(B).Required Actions to Address Causes of Event Listed1999-05-21021 May 1999 Forwards LER 99-001-00,IAW 10CFR50.73(a)(2)(i)(B).Required Actions to Address Causes of Event Listed ML20206U3471999-05-20020 May 1999 Forwards Insp Rept 50-454/99-05 on 990401-22.No Violations Noted.Insp Reviewed Activities Associated with ISI Efforts Including Selective Exam of SG Maint & Exam Records, Calculations,Observation of Exam Performance & Interviews ML20207A2151999-05-19019 May 1999 Forwards Insp Repts 50-454/99-06 & 50-455/99-06 on 990419-23.No Violations Noted.Insp Consisted of Review of Liquid & Gaseous Effluent Program,Radiological Environmental Monitoring Program,Auditing Program & Outage Activities 1999-09-08
[Table view] Category:NRC TO UTILITY
MONTHYEARML20217A1551990-11-14014 November 1990 Forwards Safety Insp Rept 50-455/90-22 on 901002-1107. Violations Noted ML20217A4431990-11-14014 November 1990 Forwards Safety Insp Rept 50-455/90-21 on 900910-11,24-26 & 1107.No Violations Noted ML20058G3241990-11-0505 November 1990 Forwards Page 9 of Insp Repts 50-454/90-16 & 50-455/90-15. Page Erroneously Deleted from Original Rept ML20058E7141990-10-30030 October 1990 Forwards Exam Forms & Answer Keys,Grading Results & Individual Answer Sheets for Each Applicant ML20059M2101990-09-25025 September 1990 Forwards Info Re Generic Fundamentals Exam Section of Operator Licensing Written Exams to Be Administered on 901010,including Map of Area Where Exams Will Be Taken, Preliminary Instructions for Exam & Equation Sheet ML20059L3051990-09-14014 September 1990 Forwards SER Re Util 900706 Request for Relief Concerning Inservice Testing Program.Relief Granted from Testing Requirements Which Would Impose Undue Hardship If Immediate Compliance Was Imposed ML20059L4531990-09-14014 September 1990 Forwards Suppl to SER Re Results of Inservice Testing Program Changes Based on Review of 881221 & 890203 Submittals.Changes Acceptable ML20059E1141990-08-30030 August 1990 Forwards Safety Insp Repts 50-454/90-16 & 50-455/90-15 on 900814-17.No Violations Noted ML20059B4271990-08-17017 August 1990 Forwards Safety Insp Repts 50-454/90-17 & 50-455/90-16 on 900701-0811.No Violations Noted ML20059A2401990-08-14014 August 1990 Advises That Operator & Senior Operator Licensing Exams Scheduled for Wk of 901203.Preliminary License Applications Should Be Submitted at Least 30 Days Before First Exam Dates in Order to Review Training & Experience of Candidates ML20058M6141990-08-0707 August 1990 Forwards Sample Registration Ltr for 901010 Generic Fundamentals Section of Written Operator Licensing Exam. Registration Ltr Listing Names of Candidates Taking Exam Should Be Submitted to Region 30 Days Prior to Exam Date ML20058L9911990-08-0606 August 1990 Forwards SERs of Responses & Associated Science Application Intl Corp 900614 Technical Evaluation Rept SAIC-89/1640 Re Station Blackout.Revised Response Addressing Areas of Nonconformance Should Be Submitted within 60 Days ML20056A4981990-08-0101 August 1990 Forwards Master Bwr/Pwr Generic Fundamentals Exam Section W/Answer Key.W/O Encls ML20055J1521990-07-20020 July 1990 Forwards Final SALP Repts 50-454/90-01 & 50-455/90-01 for Nov 1989 - Mar 1990 ML20055G6661990-07-18018 July 1990 Confirms 900802 Enforcement Conference in Region III Ofc to Discuss Ofc of Investigations & Regional Findings Re Lack of Control of Operability Determinations Involving Emergency Diesel Generators at Plant.Listed Items to Be Discussed ML20055G3301990-07-17017 July 1990 Forwards Safety Insp Repts 50-454/90-14 & 50-455/90-13 on 900513-0630.No Violations Noted ML20055E2171990-07-0202 July 1990 Forwards Requalification Exam Rept 50-454/OL-90-01 for Units 1 & 2 Administered During Wks of 900528 & 0604.Requests Response to Issue of Training & Evaluating Operators on Uncontrolled Depressurization of Steam Generators ML20055D0251990-06-28028 June 1990 Forwards Safety Insp Repts 50-454/90-15 & 50-455/90-14 on 900611-14.No Violations Noted ML20055E8791990-06-27027 June 1990 Forwards Notice of Withdrawal of 880302 Application for Amend to Change Tech Spec 4.6.1.6.1.d,to Reduce Containment Tendon Design Stresses to Incorporate Addl Design Margin Not Reflected in Values Currently in Tech Specs,Per ML20059M8791990-06-13013 June 1990 Forwards NRC Performance Indicators for First Quarter 1990. W/O Encl ML20055C6341990-05-23023 May 1990 Advises That Revised Schedule to Perform Blackness Testing within 2 Yrs of Placing Racks in Svc & Every 5 Yrs Thereafter,Acceptable ML20055C5731990-05-16016 May 1990 Ack Receipt of 900430 Response to Allegation RIII-90-A-0011 Re Employee Fitness for Duty.Confirms That Results of fitness-for-duty Test Negative & Allegation Unsubstantiated ML20055C3921990-02-26026 February 1990 Approves Util 900214 Request for Use of B&W Steam Generator Plugs W/Alloy 690 as Alternative to Alloy 600.Alternate Matl Is nickel-base Alloy (ASME Designation SB-166) ML20248D4981989-09-26026 September 1989 Accepts Scope & Objectives for Annual Emergency Preparedness Exercise Scheduled for 891206 & 07,submitted by ML20247H6411989-09-12012 September 1989 Advises That 890816 Revisions to ATWS Mitigation Sys Acceptable W/Requirements of 10CFR50.62(c)(1) ML20246M5921989-08-29029 August 1989 Forwards Safety Insp Repts 50-454/89-16 & 50-455/89-18 on 890701-0819 & Notice of Violation ML20246H8321989-08-28028 August 1989 Advises That plant-specific Reactor Coolant Pump Trip Setpoint Development,Per TMI Action Plan Item II.K.3.5 Acceptable,Based on NRC Approval of Westinghouse Owners Group Methodology Per Generic Ltr 85-12 ML20246L5111989-08-15015 August 1989 Advises That No Violations of NRC Requirements Identified in Review & Allegation RIII-88-A-0112 Considered Closed IR 05000455/19890061989-08-0909 August 1989 Advises That Violations 50-455/89-06-02 & 50-455/89-06-03 Reclassified as Severity Level V Based on 890522 & 0711 Addl Info & Minimal Safety Significance of Specific Example ML20248D5471989-08-0707 August 1989 Forwards SER Accepting Util 881130 Rept Entitled, Seismic Qualification of Byron Deep Wells & Addl Info Submitted on 890411,0427 & 0523.Related 890524 Amend Request Still Under Review ML20248D6921989-08-0404 August 1989 Advises That Rev 6b to Generating Stations Emergency Plan Transmitted by Util 890710 Form Acceptable & Does Not Decrease Effectiveness of Plan ML20245E7601989-08-0303 August 1989 Notifies That Written & Oral Operator & Senior Operator Licensing Exams Scheduled for Wk of 891127.Encl Reference Matl Requested within 60 Days Prior to Exam Date ML20247H6891989-07-25025 July 1989 Requests Proposed Design Change to Containment Hydrogen Monitoring Sys,W/Schedule for Implementing Change or Justification for Existing Configuration ML20246L6731989-07-11011 July 1989 Forwards Safety Insp Repts 50-454/89-14 & 50-455/89-16 on 890518-0630.No Violations Noted.Open Item Noted Re Testing of Safety Injection Circuitry in Remote Shutdown Panel ML20246K9541989-07-10010 July 1989 Forwards Safety Insp Repts 50-454/89-15 & 50-455/89-17 on 890612-20.No Violations Noted ML20246L3251989-07-0707 July 1989 Ack Receipt of 890613 Submittal of Rev 3c to Emergency Plan, Including Partial Rev to Emergency Action Levels in Table Bya 5-1.Plan Considered Acceptable When Revised Page Bya 5-1.16 Received by Region III ML20246D7091989-07-0606 July 1989 Ack Receipt of Re Allegation Discussed in NRC Concerning Vital Area Door Not Being Checked at Required Frequency.Investigation Supports Conclusion That Allegation RIII-89-A-0055 Unsubstantiated ML20246B5991989-07-0505 July 1989 Ack Receipt of & Payment for Civil Penalty in Amount of $50,000 Proposed in NRC ML20246E1871989-06-28028 June 1989 Advises That Changes to Security Plan Transmitted by Consistent W/Provisions of 10CFR50.54(p) & Acceptable ML20246C2421989-06-28028 June 1989 Expresses Appreciation for Hosting Operational Safety Review Team (Osart) at Plant.Comments Would Be Welcomed by Commission on Osart Insp ML20246P9211989-06-27027 June 1989 Requests That Util Fully Analyze Allegation RIII-88-A-0112 & Take Appropriate Actions to Resolve Issue ML20245F2691989-06-16016 June 1989 Forwards SER Accepting Licensee 850612 Response to Generic Ltr 83-28,Item 4.5.3 Re Trip Reliability & on-line Functional Testing of Trip Sys ML20245B1731989-06-15015 June 1989 Ack Receipt of Rev 55 to QA Topical Rept CE-1-A.Program Satisfies Requirements of 10CFR50,App B & Acceptable ML20244D8131989-06-13013 June 1989 Forwards SER Accepting Util ATWS Mitigating Sys Actuation Circuitry Designs & Compliance W/Atws Rule (10CFR50.62). Conclusion Based on Certain Human Factors Engineering Reviews ML20244C2941989-06-0909 June 1989 Advises Tht Util 890329 Request for Approval to Use Fuses for Electrical Isolation of non-Class 1E Dc Power Sys Acceptable Provided That Circuit Breaker in Parallel to Two Fuses Locked Open ML20244C4941989-06-0606 June 1989 Forwards Safety Insp Repts 50-454/89-10 & 50-455/89-12 on 890401-0517.No Violations Noted.Physical Inoperability of Diesel Generator 1A Discussed in Rept ML20244A5471989-06-0202 June 1989 Responds to Requesting Reconsideration of Violation 3 Noted in Insp Repts 50-454/89-09 & 50-455/89-06. Violation Considered Valid.Issue Re Design Requirements Not Meeting Seismic Qualifications Needs Further Attention ML20244C5091989-06-0101 June 1989 Advises That Bunker Ramo Penetration Assemblies Environmentally Qualified to Perform Intended Functions for Plants,Per 890224 Rept & .Concerns Expressed in Re Byron Unit 2 Satisfied ML20248C1931989-05-31031 May 1989 Advises That 890511 Revised Condition 6 EALs Consistent w/10CFR50.54(q) & Acceptable ML20248C2031989-05-26026 May 1989 Forwards Safety Insp Repts 50-454/89-13 & 50-455/89-15 on 890424-28.No Violations Noted 1990-09-25
[Table view] Category:OUTGOING CORRESPONDENCE
MONTHYEARML20217M2871999-10-21021 October 1999 Refers to Rev 5 Submitted in May 1999 for Portions of Byron Nuclear Power Station Generating Stations Emergency Plan Site Annex.Informs That NRC Approval Not Required Based on Determination That Plan Effectiveness Not Decreased ML20217F7891999-10-0808 October 1999 Forwards Insp Repts 50-454/99-12 & 50-455/99-12 on 990803- 0916.One Violation Occurred Being Treated as NCV ML20217B6351999-10-0505 October 1999 Forwards for Info,Final Accident Sequence Precursor Analysis of Operational Event at Byron Station,Unit 1,reported in LER 454/98-018 & NRC Responses to Util Specific Comments Provided in ML20212L1791999-10-0505 October 1999 Informs That as Result of Staff Review of Util Responses to GL 92-01,rev 1,suppl 1 & Suppl 1 Rai,Staff Revised Info in Rvid & Is Releasing Rvid Version 2 ML20217B2991999-10-0101 October 1999 Forwards Insp Repts 50-454/99-16 & 50-455/99-16 on 990907-10.No Violations Noted.Water Chemisty Program Was Well Implemented,Resulted in Effective Control of Plant Water Chemistry ML20212J6751999-09-30030 September 1999 Forwards Replacement Pages Eight Through Eleven of Insp Repts 50-454/99-15 & 50-455/99-15.Several Inaccuracies with Docket Numbers & Tracking Numbers Occurred in Repts ML20217A5821999-09-29029 September 1999 Advises of NRC Plans for Future Insp Activities at Facility for Licensee to Have Opportunity to Prepare for Insps & to Provide NRC with Feedback on Any Planned Insps Which May Conflict with Plant Activities ML20216F8051999-09-17017 September 1999 Forwards Insp Rept 50-454/99-14 & 50-455/99-14 on 990823-27. Security Program Was Effectively Implemented in Areas Inspected.No Violations Were Identified ML20211P1841999-09-0808 September 1999 Forwards Insp Repts 50-454/99-15 & 50-455/99-15 on 990824- 26.No Violations Noted.Objective of Insp to Determine Whether Byron Nuclear Generating Station Emergency Plan Adequate & If Emergency Plan Properly Implemented ML20211Q6821999-09-0606 September 1999 Informs That NRC Tentatively Scheduled Initial Licensing Exam for Byron Operator Licesne Applicants During Wks of 000619 & 26.Validation of Exam Will Occur at Station During Wk of 000529 ML20211N5151999-09-0303 September 1999 Ack Receipt of Re Safety Culture & Overtime Practices at Byron Nuclear Power Station.Copy of Recent Ltr from NRC to Commonwealth Edison Re Overtime Practices & Safety Culture Being Provided ML20211K1081999-09-0202 September 1999 Responds to Request for Addl Info to GL 92-01,Rev 1,Suppl 1, Reactor Vessel Structural Integrity, for Braidwood,Units 1 & 2 & Byron,Unit 2 ML20211M1371999-09-0202 September 1999 Discusses 990527 Meeting with Ceco & Byron Station Mgt Re Overtime Practices & Conduciveness of Work Environ to Raising Safety Concerns at Byron Station.Insp Rept Assigned for NRC Tracking Purposes.No Insp Rept Encl ML20211G4021999-08-25025 August 1999 Forwards Insp Repts 50-454/99-10 & 50-455/99-10 on 990622-0802.No Violations Noted ML20211B8691999-08-20020 August 1999 Forwards Insp Repts 50-254/99-10,50-265/99-10,50-454/99-09, 50-455/99-09,50-456/99-10 & 50-457/99-10 on 990628-0721. Action Plans Developed to Address Configuration Control Weaknesses Not Totally Effective as Listed ML20210A3151999-07-16016 July 1999 Forwards Insp Repts 50-454/99-08 & 50-455/99-08 on 990511-0621.Three Violations Being Treated as Noncited Violations ML20210B7071999-07-16016 July 1999 Responds to Requesting Review & Approval of Three Proposed Changes to Ceco QA TR,CE-1A Per 10CFR50.54(a)(3) & 10CFR50.4(b)(7) ML20196K0161999-06-30030 June 1999 Discusses 990622 Meeting at Byron Nuclear Power Station in Byron,Il.Purpose of Visit Was to Meet with PRA Staff to Discuss Ceco Initiatives in Risk Area & to Establish Dialog Between SRAs & PRA Staff ML20212H8241999-06-24024 June 1999 Informs That Effective 990531 NRC Project Mgt Responsibility for Byron & Braidwood Stations Was Transferred to Gf Dick ML20207G0601999-06-0707 June 1999 Provides Updated Info Re Number of Failures Associated with Initial Operator License Exam Administered from 980914-0918. NRC Will Review Progress Wrt Corrective Actions During Future Insps ML20207G0421999-06-0404 June 1999 Forwards Insp Repts 50-454/99-04 & 50-455/99-04 on 990330-0510.Violations Identified & Being Treated as non-cited Violations ML20207E5451999-05-28028 May 1999 Forwards Insp Repts 50-454/99-07 & 50-455/99-07 on 990517-20.No Violations Noted.Fire Protection Program Was Effective ML20207B6361999-05-25025 May 1999 Forwards SE Accepting Revised SG Tube Rupture (SGTR) Analysis for Bryon & Braidwood Stations.Revised Analysis Was Submitted to Support SG Replacement at Unit 1 of Each Station ML20206U3471999-05-20020 May 1999 Forwards Insp Rept 50-454/99-05 on 990401-22.No Violations Noted.Insp Reviewed Activities Associated with ISI Efforts Including Selective Exam of SG Maint & Exam Records, Calculations,Observation of Exam Performance & Interviews ML20207A2151999-05-19019 May 1999 Forwards Insp Repts 50-454/99-06 & 50-455/99-06 on 990419-23.No Violations Noted.Insp Consisted of Review of Liquid & Gaseous Effluent Program,Radiological Environmental Monitoring Program,Auditing Program & Outage Activities ML20207B8751999-05-18018 May 1999 Responds to Ltr Dtd 990225,expressing Concerns That Low Staffing Levels & Excessive Staff Overtime May Present Serious Safety Hazards at Some Commercial Nuclear Power Plants in Us ML20206N4791999-05-13013 May 1999 Forwards RAI Re 980529 Amend Request for Byron & Braidwood to Credit Automatic PORV Operation for Mitigation of Inadvertent SI at Power Accident.Response Requested 60 Days After Receipt Date ML20206J1981999-05-0505 May 1999 Forwards Exam Answer Key for Forms a & B,Grading Results for Facility & Copies of Individual Answer Sheets for Each Individual Taking Gfes of Written Operator Licensing Exam Administered by NRC on 990407.Without Encls ML20206E7021999-05-0303 May 1999 Advises That Info Contained in Document Entitled, Licensing Rept for Sf Rack Installation at Byron & Braidwood Stations, HI-982083,will Be Withheld from Public Disclosure Per 10CFR2.790 ML20206D0361999-04-28028 April 1999 Confirms Plans to Have Meeting on 990527 in Lisle,Illinois to Discuss Results of Ceco Evaluation on Potential Chilling Effect Concern within Working Environ & Use of Overtime within Operations Dept Organization at Byron Station ML20205Q2621999-04-14014 April 1999 Forwards Insp Repts 50-454/99-03 & 50-455/99-03 on 990217-0329.Five Violations Identified & Treated as Ncvs. Expresses Continued Concern with Configuration Control & Human Performance Errors at Byron Station ML20206U3261999-03-29029 March 1999 Forwards RAI Re 981208 Response & Suppls to NRC Re Use of Overtime in Byron Station Operations Dept.Response Requested within 30 Days of Date of Ltr ML20196K8821999-03-26026 March 1999 Advises of Completion of Plant Performance Review on 990201 to Develop Integrated Understanding of Safety Performance. Overall Performance Acceptable.Plant Issues Matrix & Insp Plan Encl ML20205B4901999-03-26026 March 1999 Forwards SER Authorizing Util 981022 Relief Requests 12R-24, Rev 0,which Requests Deferral of Rv shell-to-flange Vessel Weld Exam to End of Second 10-year Insp Interval,Pursuant to 10CFR50.55a(a)(3)(ii) & 12R-34,rev 0 ML20204G3641999-03-19019 March 1999 Forwards Safety Evaluation & Technical Ltr Rept Re Second 10-yr Interval ISI Request for Relief 12R-11,rev 2.Licensee Proposed Alternative to code-required Pressure Test Authorized for Current Interval ML20204E2631999-03-18018 March 1999 Discusses Review of Ceco Evaluation of Chilling Effect on Byron Station Personnel.Identified Number of Questions Re Ceco Findings & C/As.Requests Further Evaluation of Chilling Effect at Byron Be Conducted & Response to Encl Questions ML20204D1971999-03-16016 March 1999 Discusses Review of Revision 4Q to Portions of Licensee Emergency Plan Site Annex ML20204B6721999-03-12012 March 1999 Forwards Copy of Preliminary Accident Sequence Precursor Analysis of Operational Condition Discovered at Plant on 980912 ML20207K1861999-03-11011 March 1999 Discusses Review of Rev 4P to Portions of Byron Power Station EP Site Annex.Based on Determinations That Changes Do Not Decrease Effectiveness of EP & Plan Continues to Meet Standards of 10CFR50.47(b),NRC Approval Not Required ML20207J5201999-03-10010 March 1999 Forwards Insp Repts 50-454/99-02 & 50-455/99-02 on 990105-0216.No Violations Noted.Expresses Concern Re Trend of Configuration Control & Human Performance Errors at Byron Station ML20203G7981999-02-11011 February 1999 Forwards Insp Repts 50-454/99-01 & 50-455/99-01 on 990119-22.No Violations Noted.Insp Involved Exam of Maint & Engineering Related Activities for Electrical Circuit Breakers ML20203F2541999-02-10010 February 1999 Informs That Beginning 990216,DE Hills Will Be Chief of Operations Branch Which Includes Operator Licensing Function ML20203C9861999-02-0808 February 1999 Ack Receipt of ,Which Transmitted Changes Identified as Rev 52 to Security Plan.No NRC Approval Required ML20202H9401999-02-0303 February 1999 Informs That Update of Set Number 58 of UFSAR Has Been Completed.Confirmation Sheet Providing Update Encl ML20199H8561999-01-19019 January 1999 Discusses Insp Repts 50-454/98-25 & 50-455/98-25 on 981124-990104 & Forwards Nov.Violation Identified Involving Unacceptable Preconditioning of Stroke Time Testing of AFW Pump Discharge Valves ML20199E8861999-01-15015 January 1999 Discusses Two Unresolved Security Items Identified in Sections S3.b1 & S3.b2 of Insp Repts 50-454/98-03 & 50-455/98-03,dtd 980211.One Item Re Adequacy of Alarm Sys Testing When Two Alarm Zones Were Returned to Svc ML20198N8261998-12-30030 December 1998 Forwards Insp Repts 50-454/98-24 & 50-455/98-24 on 981130- 1204.No Violations Noted.Purpose of Insp Was to Determine If Licensed Operator Requalification Training Activities Conducted IAW with NRC Requirements ML20198J0211998-12-18018 December 1998 Forwards Insp Repts 50-454/98-20 & 50-455/98-20 on 981006- 1123.No Violations Noted ML20198F4451998-12-17017 December 1998 Forwards Insp Repts 50-454/98-23 & 50-455/98-23 on 981116-14.No Violations Noted.Purpose of Insp Was to Verify Accuracy of Licensee Response to Region III Questions Re Grid Stability ML20206N4431998-12-10010 December 1998 Forwards Security Insp Repts 50-454/98-22 & 50-455/98-22 on 981116-20.No Violations noted.Challenge-testing of Some Detection Equipment Showed Some Vulnerabilities That Util Indicated Would Be Corrected 1999-09-08
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Inspection Report - Byron - 1985042 |
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MAY 6 1986 Docket No. 50-454 License No. NPF-37 EA 86-48 Commonwealth Edison Company ATTN: Mr. James J. O'Connor President Post Office Box 767
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Chicago, IL 60690 l
Gentlemen:
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- SUBJECT: NOTICE OF VIOLATION AND PROPOSED IMPOSITION OF' CIVIL PENALTY (NRC INSPECTION REPORTS NO. 50-454/85042(DRP); 50-454/85043(DRP)
and 50-454/85056(DRP))
This refers to inspections conducted during the periods August 12 through October 18, 1985 and October 2-31, 1985 of activities authorized by NRC Operating License NPF-37 for the Byron Nuclear Power Station, Unit 1. As a result of these inspections, certain of your activities appeared to be in violation of NRC requirements. The violations were identified in the above referenced reports sent to you by letters dated November 14, 1985 and November 22, 1985,
- respectively. They were also the subject of an Enforcement Conference held in the Region III office on November 27, 1985, between Mr. Bide L. Thomas and other members of your staff, and myself and other members of the NRC staf Item I discussed in the enclosed Notice of Violation and Proposed Imposition of Civil Penalties occurred on March 6, 7, April 20, 23, an'd May 30, 31, 1985 and on 3 different occasions on July 24, 198 It involved the use of procedures containing instructions for incorrect valve alignments to conduct technical specification (TS) surveillances on the residual heat removal system (RHR).
This rendered both trains of RHR, a subsystem of the emergency core cooling system (ECCS), inoperable in that neither train was capable of injecting into all four reactor coolant system (RCS) cold legs while the plant was in Mode The Byron Unit 1 Final Safety Analysis Report (FSAR), Chapter 6, for a Large Break Loss of Coolant Accident (LOCA) states that the ECCS fulfills its safety function by injecting into all 4 RCS cold leg These events are significant because with both RHR trains only able to inject into 2 cold legs, the plants'
ability to adequately respond to a large break LOCA was significantly degrade On June 5,1985, the NRC issued a Severity Level IV Notice of Violation because two safety injection pumps were isolated while the plant was in Mode 3 (Inspection Report No. 454/85002(DRP). Your corrective actions for that violation, as stated in your letter dated July 10, 1985, included reviewing and revising all operating procedures involving ECCS systems that could affect technical specification LCOs. Apparently, these corrective actions were inadequate because RHR procedures still contained incorrect valve alignment instruction CERTIFIED MAIL 0605200070 860506 RETURN RECEIPT REQUESTED PDR ADOCK 050004 4 O
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$ Commonwealth Edison Company 2 MAY 6 1986 Item II of the enclosed Notice involves several examples of your failure to understand technical specifications, system operability, and associated action statements. Specifically, Violation II. A involves your determination after completing a July 15, 1985 surveillance test that Train B of the solid state protection system was operable, even though the main steam line isolation and auxiliary feedwater functions had not been verified during the test. Violation II.B involves your application of the wrong action statement after engineered safety features actuation system (ESFAS) Train B was declared inoperabl It also addresses the fact that ESFAS Train B was left in the test position in excess of the two hours allowed by plant technical specification Violations II.C and II.D involve the fact that action statement requirements were not met after plant personnel discovered potentially explosive gas mixtures in the waste gas holdup tank on July 6 and 11, 1985. Violation II.E involves your failure to take TS required grab samples of the waste gas holdup tank while hydrogen and oxygen analysers were out of service. Violation II.F involves your failure to perform adequate post-maintenance inspections on the control room ventilation system which resulted in components not being able to maintain the required negative pressur We are concerned that it appears that the above violations occurred as a result of inadequate management and supervision with regard to technical specification requirements. We are further concerned that some of these events should not have occurred if corrective actions to previous licensee event reports or NRC-i.dentified violations had been effectiv '
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To emphasize the need for you to ensure that: (1) the accident response capability for safety related systems is not adversely affected when performing surveillance procedure requirements; (2) system operability is evaluated by management personnel more effectively; (3) action statements are properly implemented when applicable; and (4) corrective actions taken in response to violations of NRC requirements are effective, I have been authorized, after consultation with the Director, Office of Inspection and Enforcement, to issue the enclosed Notice of Violation and Proposed Imposition of Civil Penalties in the amount of One Hundred Thousand Dollars (5100,000) for the Violations described in the enclosed Notice. In accordance with the " General Statement of Policy and Procedure for NRC Enforcement Actions," 10 CFR Part 2, Appendix C (1985) (Enforcement Policy), Item I described in the enclosed Notice has been categorized as a Severity Level III violation and Item II as a Severity Level III problem. The base value of a civil penalty for each Severity Level III violation or problem is Fifty Thousand Dollars (S50,000). The escalation and mitigation factors in the enforcement policy were considered. While I recognize that you identified the violations and took prompt and extensive corrective actions, mitigation of the civil penalties would not be appropriate because of your prior poor performance related to Item I and the multiple examples of violations in Item I You are required to respond to this letter and should follow the instructions specified in the enclosed Notice when preparing your response. In your response, you should document the specific actions taken and any additional action you plan to prevent recurrence. After reviewing your response to this Notice, including your corrective actions, the NRC will determine whether further NRC enforcement action is necessary to ensure compliance with regulatory requirement s L
. Commonwealth Edison Company 3 MAY 6 1986 In accordance with 2.790 of the NRC's " Rules of Practice," Part 2, Title 10, Code of Federal Regulations, a copy of this letter and its enclosure will be placed in the NRC Public Document Roo The responses directed by this letter and the enclosed Notice are not subject to the clearance procedures of the Office of Management and Budget as required by the Paperwork Reduction Act of 1980, PL 96-511
Sincerely, Cr::,'-:1 % 0by
.N : ] 0, ,'. ':r James G. Keppler Regional Administrator Enclosures: Notice of Violation and t Proposed Imposition of Civil Penalties Inspection Reports No. 50-454/85042(DRP);
No. 50-454/85043(DRP); and
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No. 50-454/85056(DRP)
. .,
cc w/ enclosures:
D. L. Farrar, Director of Nuclear Licensing V. I. Schlosser, Project Manager Gunner Sorensen, Site Project Superintendent R. E. Querto, Plant Manager DCS/RSB (RIDS)
Licensing Fee Management Branch Resident Inspector, RIII Byron Resident Inspector, RIII Braidwood Phyllis Dunton, Attorney General's Office, Environmental Control Division D. W. Cassel, Jr. , Es Diane Chavez, DAARE/ SAFE Steve Lewis, ELD L. 01shan, NRR LPM H. S. Taylor, Quality Assurance Division g6
RI RIII R I RIII Nore bis Std ton D vis K er G, 6l f Gl613b
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Commonwealth Edison Ccmpany
, MY 6 1986 Distribution PDR SECY CA JMTaylor, IE RVollmer, IE JAxelrad, IE TPoindexter, IE JGKeppler, RIII JLieberman, ELD HDenton, NRR Enforcement Coordinators RI, RII, RIII, RIV, RV
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BHayes, 01 SConnelly, OIA JCrooks, AE0D IE:ES IE:EA DCS NRC Resident Inspector Project Manager, NRR State of Illinois
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