IR 05000454/2022001

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Integrated Inspection Report 05000454/2022001 and 05000455/2022001
ML22122A259
Person / Time
Site: Byron  Constellation icon.png
Issue date: 05/03/2022
From: Hironori Peterson
Region 3 Branch 3
To: Rhoades D
Constellation Energy Generation, Constellation Nuclear
References
IR 2022001
Download: ML22122A259 (23)


Text

SUBJECT:

BYRON STATION - INTEGRATED INSPECTION REPORT 05000454/2022001 AND 05000455/2022001

Dear Mr. Rhoades:

On March 31, 2022, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Byron Station. On April 7, 2022, the NRC inspectors discussed the results of this inspection with Mr. J. Kowalski, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

Two findings of very low safety significance (Green) are documented in this report. Two of these findings involved violations of NRC requirements. We are treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violations or the significance or severity of the violations documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; the Director, Office of Enforcement; and the NRC Resident Inspector at Byron Station.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; and the NRC Resident Inspector at Byron Station.

May 3, 2022 This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Hironori Peterson, Chief Branch 3 Division of Reactor Projects Docket Nos. 05000454 and 05000455 License Nos. NPF-37 and NPF-66

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000454 and 05000455

License Numbers:

NPF-37 and NPF-66

Report Numbers:

05000454/2022001 and 05000455/2022001

Enterprise Identifier:

I-2022-001-0058

Licensee:

Constellation Energy Generation, LLC

Facility:

Byron Station

Location:

Byron, IL

Inspection Dates:

January 01, 2022 to March 31, 2022

Inspectors:

S. Bell, Health Physicist

D. Betancourt-Roldan, Senior Resident Inspector

N. Shah, Senior Project Engineer

C. Thompson, Illinois Emergency Management Agency

J. Vera, Acting Senior Resident Inspector

J. Weigandt, Resident Inspector

Approved By:

Hironori Peterson, Chief

Branch 3

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Byron Station, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Failure to Adhere to Plant Barrier Control Program Leads to a Failure to Enter Technical Specification Limiting Condition of Operation 3.8.1.F for Two Diesel Generators Inoperable Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000455/2022001-01 Open/Closed

[H.8] -

Procedure Adherence 71111.15 The inspectors identified a finding of very low safety significance with an associated non-cited violation (NCV) of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, when licensee personnel failed to adhere to the Plant Barrier Control Program. Specifically, the licensee failed to declare Unit 2 Emergency Diesel Generators (EDGs) inoperable and enter Technical Specification (TS) Limiting Condition of Operation (LCO) 3.8.1.F when maintenance personnel opened a credited hazard barrier.

Failure to Follow Surveillance Procedure Leads to Actuation of Carbon Dioxide Suppression System in Opposite Unit Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events Green NCV 05000454/2022001-02 Open/Closed

[H.2] - Field Presence 71111.22 A finding of very low safety significance (Green) and associated NCV of TS 5.4.1.c,

Procedures, was self-revealed on December 16, 2021, when the licensee failed to implement procedure MA-BY-EM-1-FP002-006, Fire Protection Zones 3.2B-2, 2Z2 Suppression Zones 2S-44 Detection Zones 2D-51 (Zone 3.2B-2),52, Revision 1. Specifically, while performing a surveillance on the Unit 2 lower cable spreading room (LCSR) CO2 fire suppression system the maintenance crew failed to follow procedure and actuated the Unit 1 LCSR CO2 suppression system.

Additional Tracking Items

Type Issue Number Title Report Section Status URI 05000454,05000455/20 21004-01 Applicability of Technical Specifications when opening EDG roll up doors 71111.15 Closed

PLANT STATUS

Unit 1 began the inspection period operating at full power. With the exception of minor reductions in power to support scheduled testing activities the unit remained at or near full power for the entire inspection period.

Unit 2 began the inspection period operating at full power. With the exception of minor reductions in power to support scheduled testing activities the unit remained at or near full power for most of the entire inspection period. At the end of the inspection period the unit was at 87 percent power and was in coast down for an upcoming refueling outage.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, Appendix D, Plant Status, conducted routine reviews using IP 71152, Problem Identification and Resolution, observed risk significant activities, and completed on-site portions of IPs. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Unit 1 'A' Residual Heat Removal (RH) for 'B' RH work window on January 12, 2022 (2)2B Component Cooling (CC) water prior to testing 2B, as documented in Work Order (WO) 5201522 on January 27, 2022
(3) Auxiliary Building Ventilation (VA) following Inaccessible Plenum Inspections on February 4, 2022
(4) Direct Current (DC) and instrument inverter alignment following 212 RTS on March 16, 2022

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1) South outdoor areas and Essential Service Water (SX) Cooling Tower on February 4, 2022
(2) Fire Zone (FZ) 11.5-0, North and South Boric Acid Tank Room on March 8, 2022
(3) North outdoor areas on March 15, 2022

71111.06 - Flood Protection Measures

Inspection Activities - Internal Flooding (IP Section 03.01) (2 Samples)

The inspectors evaluated internal flooding mitigation protections in the:

(1) Turbine Building basement on February 18, 2022
(2) Unit 1 Auxiliary Feedwater (AF) areas on February 23. 2022

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated the performance of a complex casualty graded scenario by a crew of licensed plant operators in the facility's simulator on March 2, 2022.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (2 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:

(1) Unit 1 EDGs on February 1, 2022 (2)a(3) Assessment on February 18, 2022 Quality Control (IP Section 03.02) (1 Partial)

The inspectors evaluated the effectiveness of maintenance and quality control activities to ensure the following SSC remains capable of performing its intended function:

(1)

(Partial)

Unit 1B Containment Spray System work window on January 20, 2022

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1) Evaluation of the emergent work associated with Unit 1 secondary repairs, as documented in Issue Reports (IRs) 4470112, 4470127, and 4470158 (Work Order (WO) 5219491) on January 6, 2022
(2) Evaluation of the planned work associated with 2B RH Work Window, as documented in WOs 5035414, 5036233, and 5042626 on February 15, 2022
(3) Evaluation of the planned and emergent work associated with the 2A CC Pump, as documented in WO5166103-1 on March 2, 2022
(4) Evaluation of the planned work associated with new fuel receipt, as documented in WO 5166103-1 on March 10, 2022

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (5 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:

(1) Evaluation of the operability of the Unit 2 AF Pumps following identification of incomplete post-maintenance testing, as documented in IR 4474490
(2) Evaluation of the operability of the 0C Control Room Chiller following identification of a degraded air intake ionization chamber, as documented in IR 4470508
(3) Evaluation of the operability of the 1SI8880, Unit 1 Accumulator N2 Supply Outside Containment Isolation Valve following identification of questions on its position indication, as documented in IR 4480465
(4) Evaluation of the operability of the 1C steam generator power operated relief valve following identification receipt of unexpected alarms, as documented in IRs 4471047 and 4474434
(5) Evaluation of the operability of the 2B AF pump following identification failure of fire seal, as documented in IR 4482988

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (1 Sample)

The inspectors evaluated the following temporary or permanent modifications:

(1) Engineering Change 634411: Revise documents to permanently isolate the essential service water (SX) pump oil coolers on February 14, 2022

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the following post-maintenance testing activities to verify system operability and/or functionality:

(1) Functional and operational testing of the 1CS01PB following maintenance outage window, as document in WO 05200036-02 on January 20, 2022
(2) Functional and operational testing of the 2B RH Pump following several work activities, as documented in WOs 5035414, 5036233, 5037850, and 5042626 on February 16, 2022
(3) Functional and operational testing of the 0SX163C 0A SX Cooling Tower Riser Isolation Motor Operated Valve following post-maintenance inspections and diagnostic test, as documented in WOs 5135939-3 and 5009251-4 on March 10, 2021
(4) Functional and operational testing of the Unit 1B SX Pump following a work window, as documented in WOs 5140534 and 5140535 on March 23, 2022

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Partial)

(1)

(Partial)

The inspectors evaluated fuel receipt, outage scope, and outage risk for upcoming Refueling Outage B2R23.

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance testing activities to verify system operability and/or functionality:

Surveillance Tests (other) (IP Section 03.01) (4 Samples)

(1)1BOSR 5.5.8.SI.5-2A; 1B Safety Injection (SI) Test, as documented in WO 5205758 (2)1BOSR 5.5.8.CV.5-2A; 1B Charging Pump Test, as documented in WO 5217092 (3)0BOSR 7.9.6-2 and 5.5.8.SX.5-2C; (0B SX Makeup Pump monthly and comprehensive tests), as documented in WOs 5230238 and 5217094

(4) Inadvertent actuation of the carbon dioxide (CO2) system on Unit 1 during work, as documented in IR 4467164

Inservice Testing (IP Section 03.01) (1 Sample)

(1)1BOSR 5.5.8.SX.5-2C; 1B SX Comprehensive Test, as documented in WO

RADIATION SAFETY

71124.06 - Radioactive Gaseous and Liquid Effluent Treatment

Walkdowns and Observations (IP Section 03.01) (3 Samples)

The inspectors evaluated the following radioactive effluent systems during walkdowns:

(1) Liquid effluent discharge system, including the effluent release tanks, radwaste release tank monitor (0RE-PR001), and the station blowdown monitor (0RE-PR010)
(2) Liquid effluent secondary system components in the Turbine Building, including the turbine building fire and oil sump monitor (0RE-PR005) and the condensate polisher sump monitor (0RE-PR-041)
(3) Auxiliary Building ventilation system, including effluent monitors Unit 1 auxiliary building vent effluent monitor (1RE-PR028) and the Unit 2 auxiliary building vent effluent monitor (2RE-PR028)

Sampling and Analysis (IP Section 03.02) (5 Samples)

Inspectors evaluated the following effluent samples, sampling processes and compensatory samples:

(1) The inspectors observed the effluent sampling of the 0WX26T liquid effluent tank on January 11, 2022
(2) The inspectors evaluated the operability of the radwaste release tank monitor (0RE-PR001) and the requirements for compensatory samples
(3) The inspectors evaluated the sampling and analysis of the gaseous effluent contained within the waste gas decay tank system
(4) The inspectors evaluated the sampling and analysis of the gaseous effluents released from the Unit 1 and Unit 2 auxiliary building vents
(5) The inspectors evaluated the sampling and analysis of the liquid effluents released via station liquid effluent tanks

Dose Calculations (IP Section 03.03) (2 Samples)

The inspectors evaluated the following dose calculations:

(1) Gaseous effluent releases for December 2021
(2) Liquid effluent releases for December

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:

IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01)===

(1) Unit 1 (January 1, 2021 through December 31, 2021)
(2) Unit 2 (January 1, 2021 through December 31, 2021)

IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 02.02) (2 Samples)

(1) Unit 1 (January 1, 2021 through December 31, 2021)
(2) Unit 2 (January 1, 2021 through December 31, 2021)

IE04: Unplanned Scrams with Complications (USwC) Sample (IP Section 02.03) (2 Samples)

(1) Unit 1 (January 1, 2021 through December 31, 2021)
(2) Unit 2 (January 1, 2021 through December 31, 2021)

71152A - Annual Follow-Up Problem Identification and Resolution Annual Follow-Up of Selected Issues (Section 03.03)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) Silting issues in the SX flow lines on February 11,

INSPECTION RESULTS

Failure to Adhere to Plant Barrier Control Program Leads to a Failure to Enter Technical Specification Limiting Condition of Operation 3.8.1.F for Two Diesel Generators Inoperable Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000455/2022001-01 Open/Closed

[H.8] -

Procedure Adherence 71111.15 The inspectors identified a finding of very low safety significance with an associated non-cited violation (NCV) of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, when licensee personnel failed to adhere to the Plant Barrier Control Program.

Specifically, the licensee failed to declare Unit 2 Emergency Diesel Generators (EDGs)inoperable and enter Technical Specification (TS) Limiting Condition of Operation (LCO)3.8.1.F when maintenance personnel opened a credited hazard barrier.

Description:

On December 10, 2021, while performing a review of Unit 2 A EDG work activities (check valve and starting air compressor motor replacement WO# 5196347), the inspectors noted that the 0DSSD167, 2A EDG roll-up door had been opened without following guidance to enter Limiting Condition of Operation Action Requirement (LCOAR) for both trains of EDGs.

The door was opened to facilitate movement of a lifting device and the air compressor motors during motor replacement. Records indicated the door was opened for 8 minutes on the evening of December 9th and 11 minutes on the 10th. According to BAP 1100-3A3, Pre-Evaluated Plant Barrier Matrix, the High Energy Line Break (HELB) barrier compensatory actions stated, in part, the following:

H14 Door Open 1. Enter LCOAR 1/2BOL 8.1 for both trains of DG.

Inspectors questioned licensee staff about not entering the 2-hour LCO per the BAP 1100-3A3 and local signage. Licensee personnel stated to the resident inspectors that they did not want to impose additional time pressure on the workers, and that they had an evaluation to support not entering the LCO. The licensee conducted the activities using the prepared Plant Barrier Impairment (PBI) Permit, CC-AA-201-F-01 (PBI # 21-267) and associated evaluation CC-AA-201-F-02, Plant Barrier Impairment Permit Evaluation. The evaluation stated, in part:

An open roll-up door may affect the operability of BOTH trains of EDG because of HELB considerations on the wall separating the two trains of DG. BAP 1100-3A3 directs entry into LCOAR 1/2BOL 8.1 for both trains of DG. In lieu of the LCOAR entry, the activity must be planned and conducted to limit the risk to the EDGs. Measures to limit risk include the following:

1. The door is not degraded and is capable of being closed during this activity.

2. The plant should not have steam leaks that are considered imminent HELB threats.

3. The activity should be planned to ensure the large component and the transport

device will fit through the door.

4. Personnel shall be ready for transfer of the equipment immediately following opening

of the door.

5. In addition, both the door and the equipment shall be in continuous attendance to

permit the door to be closed expeditiously if adverse plant conditions develop.

6. The door will be closed and secured (as required) immediately following the

equipment move.

These actions will ensure that the risk to the EDGs will be minimal such that LCOAR entry is not required during this activity.

Further inspection prompted questions related to the compensatory actions and EDG operability. The PBI Permit showed Yes per BAP 1100-3A3 was marked for compensatory action required and listed 4 items in the Compensatory Action section. The governing procedure, CC-AA-201, Plant Barrier Control Program, includes a step (6.1.2.1.A)to list the pre-evaluated compensatory measures (see H14 above). The H14 verbiage would have directed entry into TS LCO 3.8.1.F. However, the H14 verbiage was not listed on the PBI Permit. Instead, the Compensatory Action section listed items from the evaluation outlined above.

The inspectors reviewed Byrons Final Safety Analysis Report and saw that it states that the EDGs are credited equipment for mitigating a postulated design basis event, including steam system piping failure (Ref. Tables 15.0-7 and 15.1-2) and HELB events. Inspectors determined that the EDG roll-up doors are credited as HELB barriers and are located near large high energy (main steam and main feedwater) piping. As such, personnel compensatory actions would not be reliable if a HELB event occurred.

Similarly, the inspectors identified that RIS 2001-09, Control of Hazard Barriers provides an AFW example in the main body and Example 3 that clarify TS applicability with respect to HELB barriers. The RIS states: For example, an auxiliary feedwater (AFW) pump that is credited with mitigating a HELB event would be rendered inoperable if a barrier that is credited with protecting the AFW pump from the effects of the postulated HELB event is removed to allow maintenance to be performed in the AFW pump room. It also states: It may be possible to take compensatory measures to maintain pump operability and avoid entering the TS action statement for shutting down the reactor (e.g., installing a temporary barrier that provides equivalent protection). As the RIS example demonstrates, without appropriate compensatory actions to mitigate the risk of a HELB event, the conditions for entry to the LCO for EDGs would apply.

The licensees position was that as the roll-up doors are being used for their intended purpose of ingress/egress for maintenance purposes the momentary opening of the door would not require entering the LCO. In addition, they are referencing industry position documented on APC 15-31, NEI Regulatory Issues Task Force Position Paper Managing Risk and Operability While Opening Doors on Seismically Qualified Cabinets, as providing basis for their position. The inspectors pointed out to the licensee that the roll-up door does not meet the definition for normal ingress/egress in the plant barrier impairment program. In particular, Step 2.12 of CC-AA-201 states the following:

2.12. Door Designed for Personnel Ingress/Egress: A hinged door separating two areas, both of which are accessible during all operating modes. This definition excludes roll-up doors, HVAC duct access hatches, condenser hatches.

As the roll-up doors are not designated as normal ingress/egress the procedure requires for the removal of the barrier be evaluated.

The inspectors reached out with the information above to the NRR Technical Specifications Branch to establish whether the momentary opening of the door would not require entering the LCO. Based on the discussion it was determined that the roll-up door protects both EDGs, and both would be affected when the roll-up door is open. Therefore, during the time the roll-up door is open, the licensee should enter LCO 3.8.1 Condition F for both EDGs inoperable.

Corrective Actions: The licensee has entered the inspectors concern into their corrective action program under AR# 4470117, NRC ID: Question related to EDG roll-up door usage, 01/05/2022.

Corrective Action References: AR 4470117

Performance Assessment:

Performance Deficiency: The licensees failure to properly follow their Plant Barrier Control Program when opening a credited HELB barrier was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Configuration Control attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the licensee opened a credited HELB barrier without properly following the Plant Barrier Control Program, resulting in an unplanned inoperability of the Unit 2 EDGs.

Significance: The inspectors assessed the significance of the finding using Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The team determined that this finding was of very low safety significance (Green) because it was not a deficiency affecting the design or qualification of a mitigating SSC, did not represent a loss of the Probabilistic Risk Assessment (PRA) function of a single train TS system for greater than its TS allowed outage time, did not represent a loss of the PRA function of one train of a multi-train TS system for greater than its TS allowed outage time, did not represent a loss of the PRA function of two separate TS systems for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, did not represent a loss of a PRA system and/or function for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, and did not represent a loss of the PRA function of one or more non-TS trains of equipment designated as risk significant in accordance with the licensees maintenance rule program for greater than 3 days.

Cross-Cutting Aspect: H.8 - Procedure Adherence: Individuals follow processes, procedures, and work instructions. Specifically, the licensee failed to follow their PBI steps that would have directed entry into the TS LCO. BAP 1100-3A3 directs entry into LCOAR 1/2BOL 8.1 for both trains of DG. Instead, licensee personnel incorrectly used compensatory steps in lieu of entering the appropriate TS LCO.

Enforcement:

Violation: 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, requires, in part, that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings. The licensee established CC-AA-201 revision 13, Plant Barrier Control Program as the implementing procedure for barrier impairment, an activity affecting quality.

Procedure CC-AA-201, Steps 6.4.2 and 6.4.3 state REVIEW the PBI PRMIT and ensure the compensatory actions and Operability Impact is acceptable. and DETERMINE if any Technical Specification, Technical Requirement Manual or other administrative tracking requirement action statement is required to impair the barrier.

Contrary to the above, on December 9th and on the 10th, the licensee failed to follow Steps 6.4.2 and 6.4.3 of CC-AA-201. Specifically, Operations Management did not adequately ensure the compensatory actions for HELB would maintain Unit 2 EDGs Operable.

Additionally, Operations Management failed to determine Technical Specification Limiting Condition of Operation (LCO) 3.8.1.F as applicable.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

The disposition of this finding and associated violation closes URI: 05000454,05000455/2021004-01.

Failure to Follow Surveillance Procedure Leads to Actuation of Carbon Dioxide Suppression System in Opposite Unit Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events Green NCV 05000454/2022001-02 Open/Closed

[H.2] - Field Presence 71111.22 A finding of very low safety significance (Green) and associated NCV of TS 5.4.1.c, Procedures, was self-revealed on December 16, 2021, when the licensee failed to implement procedure MA-BY-EM-1-FP002-006, Fire Protection Zones 3.2B-2, 2Z2 Suppression Zones 2S-44 Detection Zones 2D-51 (Zone 3.2B-2),52, Revision 1.

Specifically, while performing a surveillance on the Unit 2 lower cable spreading room (LCSR)

CO2 fire suppression system the maintenance crew failed to follow procedure and actuated the Unit 1 LCSR CO2 suppression system.

Description:

The Unit 1 and Unit 2 LCSRs at Byron are protected by a CO2 suppression system. This system is required to be periodically tested in accordance with the Fire Protection Program.

This is accomplished by utilizing surveillance procedure MA-BY-EM-1-FP002-006, Fire Protection Zones 3.2B-2, 2Z2 Suppression Zones 2S-44 Detection Zones 2D-51 (Zone 3.2B-2),52, Revision 1. On December 16, 2021, the Electrical Maintenance Department was tasked with the performance of the prior mentioned surveillance on the Unit 2 LCSR. This work is performed with the Unit 2 LCSR CO2 suppression system out of service to prevent the system from discharging CO2 into the Unit 2 LCSR areas.

Part of the surveillance is to perform an Abort Switch Test for the Unit 2 LCSR suppression zone 2S-44. This part of the surveillance actuates the CO2 suppression portion of the system with the associated zone isolated from CO2. The steps to be performed per the procedure were the following:

11.1 Remove cover to local pushbutton 2HS-CO048 (439 P-22); and

11.2 Push local pushbutton 2HS-CO048 (439 P-22) and Begin timing evacuation.

The crew assigned to perform the Abort Switch Test searched for the pushbutton (2HS-CO048) that is designed to actuate CO2 suppression in the 2S-44 zone for approximately twenty minutes. After failing to find the pushbutton, the technicians requested support from the lead Senior Technician via radio to help locate the component. Following a walkdown Unit 1 and Unit 2 LCSR zones the lead technician notified the crew performing that he found a CO048 pushbutton on the Unit 1 side of the LCSR and verbally led that crew to the location. The step in the surveillance to actuate the 2HS-CO048 (Step 11.2) requires signatures from both the performer and the verifier identifying that the correct component prior to actuation. Contrary to that action the crew did not verify the Unit designation and proceeded to press the pushbutton on the panel. After a few seconds, the crew heard dampers closing and smelled wintergreen. Recognizing that CO2 suppression was actuated, they immediately evacuated the Unit 1 LCSR. The Control Room made the announcement over the plant paging system that CO2 was being discharged on the Unit 1 side of the Auxiliary Building and instructed all personnel to evacuate the area. Following the discharge of the CO2 system, the site instituted fire rounds on all affected areas until the CO2 system was restored.

Following the event, the licensee performed an investigation and uncovered that the start of the surveillance was delayed due to conflicting station priorities, which placed perceived time pressure on the shop Supervisors. A thorough Pre-Job Brief of the individuals was also not performed even though some of the individuals were not familiar with the task or had not performed it in three or more years.

Corrective Actions: Planned corrective actions for this event include changes to the procedure that would isolate CO2 to the station prior to performing surveillances. This would also include the use of fire watches while the system is isolated.

Corrective Action References: AR 04467164

Performance Assessment:

Performance Deficiency: The licensees failure to properly follow surveillance MA-BY-EM-1-FP002-006 when performing testing in the Unit 2 LCSR was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Human Performance attribute of the Initiating Events cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, maintenance technicians failure to follow the procedure led to them incorrectly pressing local push button 1HS-CO048, vice 2HS-CO048. This led to the initiation of the Unit 1 LCSR CO2 suppression system and the evacuation of the affected area.

Significance: The inspectors assessed the significance of the finding using Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspectors screened the finding against the Initiating Event screening questions in Exhibit 1 and determined that it did not impact the frequency of a fire or internal flooding initiating event. Therefore, the finding screened to very low safety significance (Green).

Cross-Cutting Aspect: H.2 - Field Presence: Leaders are commonly seen in the work areas of the plant observing, coaching, and reinforcing standards and expectations. Deviations from standards and expectations are corrected promptly. Senior managers ensure supervisory and management oversight of work activities, including contractors and supplemental personnel. Specifically, licensee supervision failed to ensure that technicians applied adequate peer checks or other human performance tools (e.g., Pre-Job briefs) during the surveillance.

Enforcement:

Violation: Technical Specification 5.4.1.c, "Procedures" requires, in part, that written procedures shall be established, implemented, and maintained covering the following activities: Fire Protection Program implementation.

Section 4.0 of the Byron Fire Protection Report states that the CO2 system will be subjected to periodic tests.

The licensee established MA-BY-EM-1-FP002-006, Fire Protection Zones 3.2B-2, 2Z2 Suppression Zones 2S-44 Detection Zones 2D-51 (Zone 3.2B-2),52, Revision 1, as the implementing procedure for testing the CO2 system in the LCSR. Section 11 of the procedure, Abort Switch Testing, contained the following steps:

11.1 Remove cover to local pushbutton 2HS-CO048 (439 P-22); and

11.2 Push local pushbutton 2HS-CO048 (439 P-22) and Begin timing evacuation.

Contrary to the above, on December 16, 2021, the licensee failed to follow Steps 11.1 and 11.2 while performing the surveillance MA-BY-EM-1-FP002-006 on Unit 2. Specifically, Maintenance personnel failed to verify the Unit designation prior to proceeded to press the pushbutton. This led to 1HS-CO048 being pressed vice 2HS-CO048 and caused the actuation of the CO2 system in the Unit 1 LCSR.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On April 7, 2022, the inspectors presented the integrated inspection results to Mr. J. Kowalski, Site Vice President, and other members of the licensee staff.

On January 14, 2022, the inspectors presented the radiation protection baseline inspection results to Mr. J. Kowalski, Site Vice President, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Drawings

6E-2-4002F

Single Line Diagram 120V AC ESF Instrument Inverter

Bus 212 and 214 125V DC ESF Distribution Center 212

G

BOP CC-E2B

Component Cooling System Train B Electrical Line Up

(Unit 2)

BOP CC-M2B

Train B Component Cooling System Valve Lineup (Train

B Safety Loop and Seal Water HX)

BOP FP-M1

Fire Protection System Valve Lineup

BOP RH-E1A

Residual Heat Removal System Train A Electrical Lineup

(Unit 1)

BOP RH-M1A

Train "A" Residual Heat Removal System Valve Lineup

BOP VA-E1

Auxiliary Building Ventilation Electrical Lineup (Unit 1)

BOP VA-E2

Auxiliary Building Ventilation Electrical Lineup (Unit 2)

BOP VA-E3

Auxiliary Building Ventilation Electrical Lineup (Unit 0)

Procedures

BOP VA-M1

Auxiliary Building HVAC System Mechanical Line-Up

5065965

Clean/Inspect Instrument Inverter

03/16/2022

71111.04

Work Orders

201522

(NEIL)- 2CC01PA Comprehensive IST Rqmts for CC

Pump

01/27/2022

PFP AB 401-0 FZ

11.5-0 N

Pre-Fire Plan Auxiliary Building 401-0 Elevation General

Area North Fz 11.5-0 North

PFP AB 401-0 FZ

11.5-0 S

Pre-Fire Plan Auxiliary Building 401-0 Elevation General

Area South FZ 11.5-0 South

PFP SXCT FZ

18.14A-1,2

Pre-Fire Plan Essential Service Water Cooling Tower

Electrical Substation 0B/SX Cooling Tower

Fire Plans

PFP SXCT FZ

18.14B-1,2

Pre-Fire Plan Essential Service Water Cooling Tower

Electrical Substation 0A/SX Cooling Tower

0BOSR 10.B.5-1

Quarterly Fire Protection Valve Lineup Surveillance

71111.05

Procedures

BOP FP-M1

Fire Protection System Valve Lineup

Corrective Action

Documents

4482988

2B AF Pump Room Fire Sealant Failure

03/07/2022

M-518

Auxiliary Building Process Pipe Sleeve Sealing Schedule

AA

M-556-14

Diesel Oil Exhaust

K

71111.06

Drawings

NP14-11

Self-Supporting High-Density Gel Typical Mechanical

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Seals

NP14-14

TS-MS-0091 Boot Seal

S-697

Auxiliary Building Floor Framing Plan EL 401'-0 Area 3

CV

Miscellaneous

BB-PRA-012

Internal Flood Evaluation Summary Notebook, BYR/BRW

Unit 1 & 2

71111.11Q

Miscellaneous

2-2-1 OBE

Byron Station Licensed Operator Requalification

Simulator Scenario Guide

04401914

1A DG Jacket Water Cooler SX leak

2/12/2021

04402538

1B DG Jacket Water Overflow Pipe Has Oil Coming Out

of It

2/15/2021

04409626

Potential Cause for 1B Diesel Generator Degradation

03/17/2021

04409647

Potential Cause for 1A Diesel Generator Degradation

03/17/2021

04419373

1A DG Jacket Water Lower Cooler 1DG01KA Leaking SX

04/27/2021

04419745

1A DG Manually Secured due to Exhaust Leak

04/28/2021

04429554

Tube Plugging for 1B DG Lower JW Cooler

06/15/2021

04432379

1A DG Secured due to Low Indicated SX Flow

06/30/2021

Corrective Action

Documents

04465820

1A EDG Non-Emergency Trip Circuit Test and Tighten

2/10/2021

Corrective Action

Documents

Resulting from

Inspection

4472772

NRC ID: No Fire Extinguisher During Hot Work Fire

Watch

01/19/222

Maintenance Rule a(3) Assessment

09/30/2021

Miscellaneous

Maintenance Rule a(3) Assessment

1/2020 -

6/2021

ER-AA-320

Maintenance Rule Implementation Per NEI 18-10

Procedures

ER-AA-320-1007

Maintenance Rule 18-10 - Periodic a(3) Assessment

1538757-1

EWP-MM Overhaul Operator / Stem

01/20/2022

1538757-8

EM Perform Valve as Left Diagnostic Testing 1CS001B

01/20/2022

1807588

MM - 1CS049B Replace Valve

01/19/2022

5110561-1

EWP MM - Perform Relief Valve Testing - Autogen

01/20/2022

71111.12

Work Orders

5110562-1

EWP MM - Perform Relief Valve Testing - Autogen

01/20/2022

71111.13

Corrective Action

Documents

4470112

11C Heater High/High 2 Caused 1C LP Htr String to

Isolate

01/05/2022

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

4470126

1CB025, Low Pressure HTRS Bypass Valve, Not Closing

01/05/2022

4470127

2C Low Pressure Heater Relief Valve Not Reseating

01/05/2022

4470158

2B FW Heater Level Indication About 12 Above

Expected

01/05/2022

4479890

Lessons Learned Rollup for 11C FW Heater Response

2/22/2022

4481336

2A CC Pump Impeller Degradation Identified.

2/28/2022

OP-AA-201-004

Fire Prevention for Hot Work

Procedures

OP-BY-108-117-

1000

Byron Protected Equipment Program

20415

2CC01PA Has Outboard Seal Leak/Chemical Buildup

03/05/2022

5035414-01

Change/Sample Motor Bearing Lubricant

2/14/2022

5036233

Perform Inspection of Motor (2RH01PB-M)

2/15/2022

5037850

PM Inspection, In-Service Diag Test, PIT

2/15/2022

5166103-01

RXS New Fuel Receipt and Inspection for U-2 Outage

03/10/2022

219491

1C Flash Tank Level Controller Not Working

01/13/2022

WR 1508224

1CB025, Low Pressure HTRS Bypass Valve, Not Closing

01/07/2022

Work Orders

WR 1508229

2B FW Heater Level Indication About 12 Above

Expected

01/10/2022

04470508

"A" VC Outside Air Intake Detector Trouble

01/07/2022

04471047

Unexpected Alarm 1C SG PORV Trouble

01/10/2022

04474434

1C SG PORV UPS Trouble

01/28/2022

04482988

2B AF Pump Room Fire Sealant Failure

03/07/2022

447440

Incomplete PMT for MCB Hand Switch Replacement

01/28/2022

4474490

Incomplete PMT for MCB Hand Switch Replacement

01/28/2022

Corrective Action

Documents

4480465

Possible Limit Switch Issue on 1SI8880

2/24/2022

4477314

Lessons Learned for DG Roll Up Door PBI's

2/10/2022

4479992

URI: Applicability of TS when Opening EDG Roll Up

Doors

2/22/2022

4480538

Historical Issue with 0DSSD167

2/24/2022

4482059

Minor Cracking on the Cell Covers for Batt. 211

03/02/2022

Corrective Action

Documents

Resulting from

Inspection

4483464

Request Inspect/Replace L2X Relay - 2B AF Pump

03/08/2022

71111.15

Drawings

6E-2-4030AF01

Schematic Diagram Auxiliary Feedwater Pump 2A

2AF01PA

AA

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

6E-2-4030AF02

Schematic Diagram Auxiliary Feedwater Pump 2B (Diesel

Driven) 2AF01PB

Z

Miscellaneous

1BOSR 6.3.5-

11.BY01

Acceptance Criteria Data Sheet

1BOSR 0.5-2.SI.3-4

1SI8880, 1SI8964, 1SI8871 and 1SI8888 Position

Indication Test

Procedures

1BOSR 6.3.5-11

1SI8880, 1SI8964, 1SI8871 and 1SI8888 Stroke Test

Calculations

LTC1003573270010-

R(1)

SX Pump Lube Oil Cooler Elimination Analysis

08/11/2021

71111.18

Engineering

Changes

634411

Revise Documents to Permanently Isolate SX Pump Oil

Coolers

Corrective Action

Documents

4483969

PMTs for SXCT Riser Valve MOV Inspections

03/10/2022

4474522

Container Used in RCA with No Radioactive Material

Sticker

01/28/2022

4485004

Leak By Greater Than 20GPM On 0SX163C

03/15/2022

4485067

NRC ID Observation Working at Heights

03/15/2022

Corrective Action

Documents

Resulting from

Inspection

4486869

NRC ID: 1B SX PP Oil Low In Sight Glass After Work

Window

03/23/2022

5009251

PM Inspection, In-service Diag. Test, PIT

03/10/2022

27570-3

OPS PMT - 1FI-SX042, 1SX200B, 1SX200D

03/22/2022

5035414-2

OPS PMT - Verify Proper RH Pump Motor Oil Level

2/16/2022

5036233

Perform Inspection of Motor (2RH01PB-M)

2/15/2022

5037850-4

OPS PMT - PIT & Stroke Test

2/16/2022

5084416-3

OPS PMT - Stroke and PIT

2/15/2022

5135939

LR-SXCT C Cell Inspection per TRM

03/10/2022

5140534-2

OP PMT: Verify Proper SX Pump/Motor Oil Level

03/22/2022

5140535-2

OP-Perform PMT

03/22/2022

71111.19

Work Orders

200036

(NEIL)-1CS01PB Comprehensive IST Rqmts for

Containment Spray

01/20/2022

Corrective Action

Documents

4467164

CO2 Storage Tank Trouble Alarm

2/16/2021

71111.22

Procedures

MA-BY-EM-FP002-

006

Fire Protection Zones 3.2B-2, 2Z2 Suppression Zones

2S-44 Detection Zones 2D-51 (Zone 3.2B-2), 52

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

04973623-01

LCSR Fire Protection Zones Low Pressure CO2 System

Actuation

205758-01

OPS 1BOSR 5.5.8.SI.5-2A 1B SI IST Group A Pump Test

2/11/2022

217089-1

LR-OPS: 1BOSR 5.5.8.SX.5-2C 1B SX Comprehensive

03/22/2022

217092

(NEIL)- 1CV01PB Group A Ist Requirements For CV

Pump

2/15/2022

217094-01

OPS 0BOSR 5.5.8.SX.5-2C 0B SX Comprehensive

03/18/2022

Work Orders

230238-01

LR-0BOSR 7.9.6-2, SX Makeup Pump 0B Monthly

Operability

03/18/2022

AR 04333196

CWBD ODCM Compositor No Flow

04/06/2020

AR 04343530

Re-establish Continuous Flow for CWBD ODCM

Sampling

05/15/2020

Corrective Action

Documents

AR 04412979

Effluent Report

03/31/2021

Engineering

Evaluations

Offsite Dose Calculation Manual Revision Documentation

15-17

2019 Annual Radioactive Effluent Release Report

04/23/2020

20 Annual Radioactive Effluent Release Report

04/21/2021

20 Annual Land Use Census

09/01/2020

G-20210630-296-B

Unit 1 Containment Effluent Release

06/30/2021

G-20210818-351-B

Waste Gas Decay Tank B Batch Effluent Release

08/20/2021

Miscellaneous

L-20220111-153-B

Liquid Effluent Batch 0WX26T Tank Release

01/11/2022

BCP-400-

ECNMT/ROUTINE

Gaseous Effluent Release Form - Routine Containment

Release

BCP-400-EWASTE

GAS

Gaseous Effluent Release Form Type: Waste Gas Decay

Tank

BCP-400-EWX01

Liquid Radwaste Release Form for Release Tank

OX-O1T

CY-BY-130-300-300-

Compositing Continuous Liquid Effluent Samples

CY-BY-170-200-F-

400-46

Waste Gas Decay Tank Sample Form

Procedures

CY-BY-170-301

Offsite Dose Calculation Manual

15, 17

71124.06

Radiation

Surveys

Unit 1 Auxiliary Building Vent Effluent Monitor

1RE-PR028 Effluent Sample Data (Tritium, Noble Gas,

01/10/2022

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Particulate and Iodine)

Unit 2 Auxiliary Building Vent Effluent Monitor 2RE-

PR028 Sample Data (Tritium, Noble Gas, Particulate, and

Iodine)

01/10/2022

Miscellaneous

Operating Logs from January - December 2021

71151

Procedures

LS-AA-2001

Collecting and Reporting of NRC ROP Performance

Indicator Data

4470437

Security Vehicle Left Running in Protected Area

01/06/2022

4474460

NRC ID: Summary of 4Q21 Integrated Inspection Exit

Meeting

01/28/2022

4474556

NRC ID: Pipe 1ES87AB May Be Rubbing Against a

Snubber

01/28/2022

4475505

ES Line Pipe Support Broken (First One)- Line Vibration

2/02/2022

4475509

ES Line Pipe Support Broken (Second One)- Line

Vibration

2/02/2022

4481241

NRC 4Q21: Minor Violation - Inadequate Operator Logs

2/28/2022

4486245

NRC ID - Floor Drain Covered

03/21/2022

4486246

NRC ID: 0A SX Pump Gear Box Breather Dirty

03/21/2022

4486246

0A SX Pump Gear Box Breather Dirty

03/21/2022

71152A

Corrective Action

Documents

Resulting from

Inspection

4486623

NRC ID: Potential Trend in Timely Completion of HURB

Actions

03/22/2022