IR 05000261/1986001

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Insp Rept 50-261/86-01 on 860111-0210.No Violation or Deviation Noted.One Unresolved Item & One Inspector Followup Item Noted.Major Areas Inspected:Ros,Site Security,Qa Practices & IE Bulletin & Notice Followup
ML14175B366
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 03/05/1986
From: Fredrickson P, Krug H
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14175B365 List:
References
50-261-86-01, 50-261-86-1, IEIN-85-094, IEIN-85-94, NUDOCS 8603110274
Download: ML14175B366 (15)


Text

U REGC A

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, Z mATLANTA, GEORGIA 30323 Report No.:

50-261/86-01 Licensee:

Carolina Power and Light Company P. 0. Box 1551 Raleigh, NC 27602 Docket No.:

50-261 License No.:

DPR-23 Facility Name:

H. B. Robinson Inspection Conducted:

January 11 - February 10, 1986 Inspector:

3__

H. E -. Krug, Senior Resi ent Inspector

/Date Signed Approved by: (

P. E. Fredrickson, Section Chief

/Date Signed Division of Reactor Projects SUMMARY Scope:

This routine, announced inspection involved 149 resident inspector-hours on site in the areas of Technical Specification (TS)

compliance, plant tour, operations performance, reportable occurrences, housekeeping, site security, surveillance activities, maintenance activities, quality assurance practices, radiation control activities, outstanding items review, IE Bulletin and IE Notice followup, organization and administration, independent inspection and Systematic Assessment of Licensee Performance (SALP).

Results:

Of the areas inspected, one unresolved item and one inspector followup item were identifie No violations or deviations were identifie Unresolved item 261/86-01-01:

"Challenges to Safety Systems," Paragraph 1 Inspector followup item 86-01-02:

"Loss of Offsite Power," Paragraph 1 PDR ADOCK 05000261 G

PDR

REPORT DETAILS Licensee Employees Contacted R. Barnett, Maintenance Supervisor, Electrical G. Beatty, Manager, Robinson Nuclear Project Department A. Beckman, Principal Specialist, Planning and Scheduling J. Benjamin, Supervisor, Operations R. Chambers, Engineering Supervisor, Performance C. Crawford, Manager, Maintenance D. Crocker, Principal Health Physics Specialist J. Curley, Director, Regulatory Compliance W. Ritchie, Supervisor (Acting), Radiation Control J. Eaddy, E&C Supervisor W. Flanagan, Manager, Design Engineering W. Gainey, Maintenance Supervisor, Mechnical G. Honma, Senior Specialist, Regulatory Compliance F. Lowery, Manager, Operations A. McCauley, Director (Acting), Onsite Nuclear Safety P. Harding, Project Specialist (Acting), Radiation Control M. Marquick, Senior Specialist, Planning and Scheduling R. Morgan, Plant General Manager M. Morrow, Specialist, Emergency Preparedness D. Nelson, Operating Supervisor B. Murphy, Senior Instrumentation and Control Engineer M. Page, Engineering Supervisor, Plant Systems R. Powell, Principal Specialist, Maintenance B. Rieck, Manager, Control and Administration R. Smith, Manager, Environmental and Radiation Control J. Sturdavant, Technician, Regulatory Compliance R. Wallace, Manager, Technical Support L. Williams, Supervisor, Security C. Wright, Senior Specialist, Quality Assurance/Quality Control H. Young, Director, Quality Assurance/Quality Control Other licensee employees contacted included technicians, operators, mechanics, security force members, and office personne.

Exit Interview (30702, 30703)

The inspection scope and findings were summarized on February 10, 1986, with the Plant General Manager and the Director of Regulatory Complianc No written material was provided to the licensee by the inspecto The licensee acknowledged the findings without exceptio The licensee did not identify as proprietary any of the materials provided to or reviewed by the S

inspector during this inspectio.

Plant Tour (71707, 62703, 71710)

The inspector conducted plant tours periodically during the inspection interval to verify that monitoring equipment was recording as required, equipment was properly tagged, operations personnel were aware of plant conditions and maintenance activities, and plant housekeeping efforts were adequate. The inspector determined that appropriate radiation controls were properly established, excess equipment or material was stored properly, and combustible material was disposed of expeditiousl During tours, the inspector looked for the existence of unusual fluid leaks, piping vibrations, pipe hanger and seismic restraint abnormal settings, various valve and breaker positions, equipment clearance tags and component status, adequacy of fire fighting equipment, and instrument calibration date Some tours were conducted on backshift Plant housekeeping was observed to be goo The inspector performed system status checks on the following systems:

a. Vital Station Batteries b. Emergency Diesel Generators c. Emergency Electrical Switchgear d. Safety Injection System e. Residual Heat Removal System No violations or deviations were identified within the areas inspecte.

Technical Specification Compliance (71707, 62703, 61726)

During this reporting interval, the inspector verified compliance with selected limiting conditions for operation and reviewed results of certain surveillance and maintenance activitie These verifications were accomplished by direct observation of monitoring instrumentation, valve positions, switch positions, and review of completed logs and record The licensee provided an update on the phased implementation of the Radiological Environmental Technical Specification (RETS)

for the Robinson station. Included was a description of ongoing coordination with NRR on the RETS as well as the status of minor corrections being implemented by the license No violations or deviations were identified within the areas inspecte.

Plant Operations Review (71707, 62703, 61726, 61707, 61711)

Periodically during the inspection interval, the inspector reviewed shift logs and operations records, including data sheets, instrument traces, and records of equipment malfunctions. This review included control room logs, maintenance work requests, auxiliary logs, operating orders, standing orders, night orders, jumper logs, and equipment tagout record The

  • inspector routinely observed operator alertness and demeanor during plant tours and observed them to be excellen The inspector conducted random off-hours inspections during the reporting interval to assure that operations and security remained at an acceptable leve The inspector periodically verified the reactor shutdown margi The inspector also periodically observed the reactor axial flux difference and compared the observed valves with those required by the T A reactor trip followed by a trip of the startup transformer occurred on January 28, 198 The licensee then began a refueling outage which had been scheduled for February 1, 198 While the inspector was in the control room at 6:29 on January 17, 1986, a containment smoke alarm annunciated inside the control roo A small fire, less than one square foot, was located in "C" reactor coolant pump bay on the cold leg near the pump outle The licensee executed fire procedure FP-001, "Fire Emergency."

At the time of the fire, the operators were performing a normal plant heatup using general procedure GP-002,

"Cold Solid to Hot Subcritical at No Load T-AVG."

The Shift Foreman stated that the fire was probably due to local condensation of oil vapor during the last shutdown, which then ignited during heatup when the primary system temperature reached approximately 480 degrees The fire was easily extinguished by the local application of halo The Shift Foreman announced the fire all clear at 065 No violations or deviations were identified within the areas inspecte.

Physical Protection (71707)

The inspector verified by observation, perimeter walkdowns and interviews that measures taken to assure the physical protection of the facility met current requirement Areas inspected included the organization of the security force, the physical condition of gates, doors and isolation zones; the performance of access control and searchs; communications procedures; and the enforcement of escorting rul During the inspection period, the inspector continued to monitor the progress and activities of the HBR Security System Upgrade Project. The new card readers are now in use throughout the plant and no problems were observe No violations or deviations were identified within the areas inspecte. Monthly Surveillance Observation (61726)

The inspector observed portions of a number of surveillance activities of safety-related systems and components to ascertain that these activities were conducted in accordance with license requirement On January 24, 1986, the inspector observed all aspects of operations surveillance test OST-010 (Revision 5),

"Power Range Calorimetric During Power Operation."

  • The inspector determined that the surveillance test procedure conformed to TS requirements, that all precautions and LCO were met and that the surveillance test was completed at the required frequenc The inspector also verified that the required administrative approvals were obtained prior to initiating the test, that the testing was accomplished by qualified personnel in accordance with the current version of an approved test procedure and that the required test instrumentation was properly calibrated. Upon completion of the testing, the inspector observed that the recorded test data was accurate, complete and met TS requirement There were no test discrepancie No violations or deviations were identified within the areas inspecte.

Monthly Maintenance Observation (62703)

The inspector observed the performance of maintenance surveillance test MST-902 (Revision 6),

"Battery Test" to ascertain that this test was conducted in accordance with approved procedures, TS and appropriate industry codes and standards. The inspector determined that the performance of this test did not violate any LCOs and that redundant components were operabl The inspector also determined (1) that the procedure used was adequate to control the activity, (2) that required administrative approvals were obtained prior to work initiation, and (3) that appropriate ignition and fire prevention controls were implemente The inspector verified that this activity was accomplished by qualified personnel using an approved procedur No grounds were indicated on the "A" charging circuit; however, the inspector observed a 70 volt ground on the "B" charging circuit ground indicator. The inspector questioned the maintenance technician performing MST 902, who said that the ground was observed following the reactor trip on January 28, 198 The inspector informed the licensee's Regulatory Compliance organization to insure that this information was fully availabl Additionally, the inspector reviewed several outstanding job orders to determine that the licensee was giving priority to safety-related maintenance and that a backlog which might affect its performance was not developing on a given syste No violations or deviations were identified within the areas inspecte.

Operational Safety Verification (71707)

The inspector observed licensee activities to ascertain that the facility was being operated safely and in conformance with regulatory requirements, and that the licensee management control system was effectively discharging its responsibilities for continued safe operation by direct observation of activities, tours of the facility, interviews and discussions with licensee management and personnel, independent verification of safety system status, LCO, and reviewing facility record No violations or deviations were identified within the areas inspecte II5 1 ESF System Walkdown and Monthly Surveillance Observation (71710, 61726, 56700)

The inspector verified the operability of the "A" and "B" vital battery system. The inspector confirmed that the licensee's system lineup procedures matched plant drawings and the as-built configuration. The inspector looked for equipment conditions and items that might degrade performance (hangers and supports were operable, housekeeping, etc.) and inspected for debris, loose material, jumpers, evidence of rodents, etc. The inspector verified that switches were in proper position and power was availabl The inspector observed that the battery trouble alarm indication in the control room was illuminated, which was caused by the ground indicated on the "B" battery charging pane Beginning at about 11:30 on February 1, 1986, the inspector observed licensee activities associated with the execution of operations surveillance test procedure OST-162 (Revision 3) titled "Emergency Diesel Generator Auto Start on Loss of Power and Safety Injection - Emergency Diesel Trips Defeat (Refueling)."

A regional inspector was also presen Prior to the test, the test director conducted a detailed briefing of what was to be accomplished, by whom, and answered questions raised by the test personne If needed, offsite power was quickly available via the auxiliary transforme At 1:38 on February 2, 1986, OST-162 was properly executed and demonstrated the features described in subsequent paragraph Following initiation by a loss of power to the vital buses in conjunction with a manual actuation, both diesels automatically started and load shedding and restoration to operation of the required equipment occurre The diesels assumed the required load within 50 seconds after the initial starting signa As designed, while in the "trips defeat" position, the test demonstrated that the diesel protective trip devices would not trip the diesel The operability of the manual block/unblock safety switches on the reactor control board was satisfactorily demonstrated, as was the operability of the emergency power supply to the pressurizer heater The test was performed by qualified personnel using an approved procedure and was excellent in every respect observe No violations or deviations were identified within the areas inspecte L

1 Onsite Followup of Events and Subsequent Written Reports of Nonroutine Events at Power Reactor Facilities (92700, 90714, 93702, 40700)

On January 15, 1986, during the performance of maintenance surveillance test MST-013 titled "Steam Generator Water Level Protection Channel Testing (Monthly)," the "A" feed water regulating valve opened overfeeding the "A" steam generato The resulting high water level caused a turbine trip which initiated a reactor trip at 10:26 All safety equipment operated as designe On January 15, 1986, the Plant General Manager charged the Acting Director of Onsite Nuclear Safety with the task of evaluating the cause of the reactor trip. At 4:30 on January 16, 1986, the licensee convened a special PNSC to evaluate the cause of the trip. ONS reported its evaluation which was based on a review which included analysis of the sequence of events recorder, instrument traces, results of tests and surveillances conducted after the trip, and interviews with plant personne The test and surveillance activities uncovered no significant plant equipment problem However, the licensee found a loose test terminal on level comparitor LC-476, which continues to be a subject of study by the license Discussions with plant personnel disclosed that the trip occurred at a point in MST-013 where approximately five previous trips occurred, and where a recent procedure modification was implemented to prevent such trip The PNSC concluded that, at the time of the trip, the technicians executing the surveillance were ahead of their procedure and that the evidence strongly indicated that this was the root cause of the trip; however, evaluation of the loose test terminal as a cause or contributor would continu Two procedure difficulties were identified. The first involved verifying that the reactor operator had placed the appropriate feed water regulating valve in manual control before proceeding furthe With respect to the second, the PNSC concluded that the procedure, which includes hundreds of steps, needed to be reorganized to put those functions which could generate a reactor trip at the beginning of the procedure, rather than at the en The inspector will continue to monitor the licensee's evaluatio On January 21, 1986, with the reactor at 71 percent power, while licensee personnel were performing surveillance on level transmitter LT-460, voltage spikes occurred on instrument busses 2 and 7, which both caused the "B" steam generator regulating valve to open and overfeed the "B" steam generator, and also caused a main turbine runbac The resulting high-high water level in the "B" steam generator caused a turbine trip which initiated a reactor trip at 8:49 a.m. All safety systems functioned as designe The licensee established that the instrument bus voltage spikes on busses 2 and 7 were caused by a short resulting from the attempted reinsertion by surveillance personnel of a misaligned multi-pronged jack, back into its socket in the level transmitter module cabine Reinsertion of the jack required the technician to perform a contorting arm extension during which it was difficult to maintain the required jack-socket alignment necessary to

  • prevent an electrical faul The licensee is evaluating ways to prevent such misalignments in the futur The inspector will continue to monitor the licensee's actions concerning this proble On January 22, 1986, while the reactor was at 33 percent power, technicians were in the process of resetting the nuclear instrumentation trip set points to 55 percent because of the recent axial power history (accumulation of

"penalty minutes" per TS).

The specific instruments, power range neutron monitors, N-41, N-42, N-43, and N-44 are arranged in a 2 out of 4 logic sequence to provide a reactor tri The technicians completed work on N-4 They then calibrated N-42 but did not restore it to servic When they next tripped N-43 for recalibration, the 2 out of 4 trip logic was satisfied and a reactor trip occurred at 11:27 All safety systems functioned properly. The licensee concluded that the reactor trip was the result of personnel erro The inspector's report of the reactor trip which occurred on January 28, 1986, is included in paragraph 12 of this repor At 11:17 on January 30, 1986, a reactor safety injection signal occurred while the licensee was cooling down the plant in accordance with general procedure GP-007 (Revision 4), titled "Plant Cooldown from Hot Shutdown to Cold Shutdown."

As primary pressure was above the safety injection pump discharge pressure, no water was injected into the vesse The safety injection signal was actuated by the generation of a high steam line differential pressure signal, which the licensee attributed to personnel error caused by an excessively rapid cooldow The licensee also stated that it is examining procedure GP-007 to determine if an improvement will reduce the probability of a personnel erro The recently issued NRC SALP report noted the historically higher than average trip rate at Robinson and the licensee's in-place and proposed corrective actions addressing this issu At the time of the trip on January 15, 1986, the Robinson plant completed the longest power run in its history, 93 days and set a licensee record for energy generatio Furthermore, on January 15, 1986, the reactor was about two weeks away from the schedule refueling outage. In addition, the trip history during the recent operating cycle suggested some trend towards a reduced trip rate; which when considered along with the record run close to the end of the cycle, indicated quantitative improvemen However, as a result of the reactor trips which occurred on January 15 and 21-22, 1986, the Plant General Manager, on January 24, 1986, convened a special management meeting to formulate and promulgate a corrective action pla The Managers of Maintenance, Regulatory Compliance, Operations, Environmental and Radiation Control and Technical Support were presen Specific action items with associated completion dates were assigned to the attendees by the Plant General Manage The first three action items, completed on January 24, 1986, imposed measures designed to reduce personnel errors through the use of additional independent verification, improved component labeling and counseling of technicians responsible for maintenance and surveillanc In addition, two senior managers were tasked by the Plant General Manager to act as an ad hoc committee (AHC)

to take a comprehensive look at the last three trips and initiate any appropriate non-conformance reports (NCR).

Also, maintenance surveillance tests associated with steam generator level protection and control were required to be revised, to reduce personnel error, prior to their next us The licensee has also created a "special" trip reduction review subcommittee (SRS)

to perform an analytical evaluation of recent trips and to recommend corrective actio The SRS which reports to the AHC described in the previous paragraph is composed of three Principal Engineer One of the three, the Acting Director of Onsite Nuclear Safety at Robinson, also heads the subcommitte The members include one representative from Corporate Nuclear Safety and one from Brunswic The latter individual devised and participated in the trip reduction program at Brunswic All three SRS members are trained in the use of Management Oriented Risk Tree (MORT)

techniques, which they are using to perform their analysi Finally, at the request of the licensee, an INPO team is currently scheduled to be onsite during the first week in March to perform an evaluation of the proble In summary, the trip on January 15, 1986, appears to involve both an inadequate procedure and personnel error; although the question of the loose test terminal is ope The trip on January 21, 1986 involved the manually misaligned reinsertion of an electrical plu The licensee stated that the trip on January 22, 1986, was the result of a failure to follow a procedur Although, based on what is now known, the trip on January 28, 1986, does not appear to involve an inadequate procedure or a personnel error, the root cause of the trip has not been identified. Finally, the SI signal generated on January 30, 1986, was deemed by the licensee to be a personnel erro Consequently, pending the outcome of additional evaluation by both the inspector and the licensee, the inspector has identified the recent challenges to safety systems as an unresolved ite Unresolved Item 50-261/86-01-01; "Challenges to Safety Systems."

12. Onsite Followup of Events at Operating Power Reactors (93702)

At 9:17 on January 28, 1986, a reactor trip occurred on Unit 2 from 80 percent power due to high pressurizer pressure. The root cause of this trip is still not completely identifie *

A fault occurred on emergency bus E-2 which caused a loss of voltage on instrument bus 4 -

initiating a main turbine runback. The control rods were in manua When the runback occurred, the control operator switched the rods into automatic, but rod insertion did not occur because nuclear power indicator N-44 failed low as a result of lost voltage on instrument bus The resulting load reduction caused a primary pressure increase leading to a reactor trip on high pressurizer pressur This was confirmed both by the sequence of events recorder and the first out annunciator pane The reactor trip was norma At the time of the reactor trip, the "B" diesel generator was out of service in order to perform a scheduled modification to the output breaker trip mechanism to convert it to solid state actuatio The important aspects of the event as reconstructed from the sequence of events recorder and the operations log is as follows:

09:17:15 Fault on emergency bus E-2, instrument bus 4 voltage lost, main turbine run back 09:17:35 Pressurizer high pressure, normal reactor trip 09:18:35 Loss of offsite power, "A" diesel generator picked up load as designed, the "B" motor driven aux. feed pump automatically started and fed the steam generators, "B" diesel out of service for breaker modification Pressurizer level dropped to 12 percent and recovered to 20 percent Reactor coolant pumps automatically tripped, natural circulation established by procedure Safety injection signal received (no injection occurred since primary pressure greater than 1500 psig)

09:35 Unusual event declared 09:46

"B" diesel generator restored 535 degrees F -

2000 psig -

unit stable 10:52 Pressurizer heaters available 12:29

"C" steam generator PORV, which was manually opened to balance loop temperatures for natural circulation, failed open 12:32 Safety injection signal caused by high steam line delta P (no injection since primary pressure greater than 1500 psig).

Pressure drops to its minimum of 1840 psig due to cool down 12:40

"C" SG PORV closed after the air supply valve was locally closed

12:42 Pressure 1920 psig Pressurizer level 22 percent Subcooling 120 degrees F Condensate Storage Tank Level was 45 percent Refueling Water Storage Tank Level was 75 percent Unit stable 12:55 El bus connected to offsite power

"A" diesel on standby 16:03 E2 bus connected to offsite power 16:07

"B" diesel on standby 16:20

"B" reactor coolant pumps restarted 16:34 Unusual event terminated Upon reaching the control room, the inspector immediately and independently determined that the reactor core was being properly cooled, and what the cooling configuration being used at the time was, by a walkdown of the control boards and instrumentation panel The Shift Foreman and other operations personnel provided a status summary of available plant equipment and associated problem The Acting Site Emergency Coordinator was present in the control room and gave the inspector the status of the unusual even The inspector, using the Emergency Notification System (ENS)

phone, then reported the status of the plant to senior NRC personnel both in Region II and Bethesd During the remaining time period until the licensee terminated the unusual event at 4:34 p.m.,

the inspector monitored the subcooling meters, the reactor coolant pump seal flows, hot and cold leg temperatures, pressurizer pressure and level, steam generator levels, operator actions, and control room personnel deliberation At no time did the inspector observe any indication that the core was being, or had been, inadequately coole At all times, the reactor instrumentation indications correlated in ways characteristic of proper natural circulatio The dose equivalent iodine-131 concentration prior to the trip was 0.00212 micro-curies per gram of reactor coolant -

a concentration typical of equilibrium conditions at Robinson, and a small fraction of the TS limi Approximately ninety minutes after the trip, the licensee used a survey meter to establish that the reactor coolant activity was "high-normal,"

indicating no fuel damage. Additionally, primary coolant leakage was within TS limits and there was negligible primary-to-secondary system leakage across the steam generator tubes, which had been replaced approximately a year and a half earlie In addition to the normal shift complement, the licensee quickly provided, in the control room after the reactor trip, a number of highly qualified and experienced personnel including the Operations Supervisor, the Director of Regulatory Compliance, additional shift foremen and other licensed operators, and the Manager of Maintenance -

who was the Acting Site Emergency Coordinato As observed by the inspector, all licensee actions and activities were performed in a calm, deliberate, conservative, and highly professional manne Licensee personnel in the control room, in every capacity, maintained the awareness, control and communications necessary for effective recovery operation Licensee personnel kept the inspector well informed throughout the event. The licensed operator acting as the communications interface on the ENS phone, between NRC personnel and personnel in the control room, performed in an exemplary fashio This item is identified as inspector followup item IFI-50-261/86-01-02,

"Loss of Offsite Power."

13. Organization and Administration (36700)

The inspector reviewed aspects of the on-site licensee organization to ascertain that the licensee's onsite organization is in conformance with the requirements of the TS by verifying that (1) the established organization is functioning as described in the TS and is effective, (2) personnel qualification levels are in conformance with applicable codes and standards, and (3) the lines of authority and responsibility are in conformance with TS and applicable codes and standards..

Comprehensive discussions of current safety-related activities were conducted with plant management and technical personnel during this reporting period including, and in particular, Operations, Environmental and Radiation Controls, Quality Assurance, Regulatory Compliance and Onsite Nuclear Safety organizations. Topics discussed included licensee activities associated with plant operations activities, especially the evaluation of the causes of recent reactor trips as well as the licensee's actions and plans associated with corrective actions; plant modifications, including the security system upgrade and the work in progress on the "C" reactor coolant pump; the fire protection system; and communications interface No violations or deviations were identified within the areas inspecte. Plant Nuclear Safety Committee (PNSC) (40700)

The inspector reviewed certain activities of the PNSC to ascertain whether the onsite review functions were conducted in accordance with TS and other regulatory requirement The inspector (1) attended the regularly scheduled PNSC meeting held on January 17, 1986 and observed the conduct of the meeting, (2) ascertained that provisions of the TS dealing with membership, review process, frequency, qualifications, etc.,

were satisfied, and (3)

followed up on previously identified PNSC activities to independently confirm that corrective actions were progressing satisfactoril The inspection emphasized a number of item Recent procedure changes processed by Onsite Nuclear Safety personnel were reviewed as were immediate notifications to the NRC and TS changes being considered by the license At 1:30 on January 17, 1986, the inspector attended another regularly scheduled PNSC meetin The routine agenda format was followe In particular, the licensee fully discussed the fire which occurred inside containment in the "C" reactor coolant pump bay on the cold leg, at 6:29 a.m. on January 17, 198 The PNSC concluded that the fire was not reportable because the burning area was less than one square foot, was easily extinguished, caused no damage and could not reoccur while the plant was ho The PNSC also reviewed fuel management procedure FMP-014,

"Rod Bank Insertion Limits."

No violations or deviations were identified within the areas inspecte. Plant Procedures (42700, 61700)

The inspector reviewed portions of the established procedure program to ascertain whether overall plant procedures were in accordance with regulatory requirements, temporary procedures and procedure changes were made in accordance with TS requirements, and the technical adequacy of the reviewed procedures was consistent with desired actions and modes of operation. Procedures examined included general plant operating procedures, startup, operation and shutdown of safety-related system procedures, abnormal condition procedures, procedures for emergency and other significant events, maintenance procedures and administrative procedure No violations or deviations were identified within the areas inspecte.

Preparation for Refueling (60705, 37700)

A refueling outage commenced on February 1, 1986. The inspector continued to review licensee preparations for refueling including the adequacy of procedures and administrative controls for the refueling activities/outag The inspector reviewed the licensee Cycle 11 -

10 CFR 50.59 Evaluation as prepared for review by the PNS Cycle 11 is similar to Cycle 1 The licensee evaluation was comprehensive and included a comparison of the Cycle 10 and Cycle 11 neutron kinetics parameters and limiting heat transfer limit Based on the parameters presented in the evaluation, the licensee reached the conclusion that the Cycle 11 evaluation was bounded by the Cycle 10 evaluation and therefore did not represent an unreviewed safety questio The inspector did not identify any information which would tend to invalidate the licensee's conclusion No violations or deviations were identified within the areas inspecte.

Review of Information Notice IEN 85-94 (92717)

As a result of its normal review process, the licensee determined that IE Information Notice N, entitled "Potential For Loss of Minimum Flow Paths Leading to ECCS Pump Damage During a LOCA" contained information pertinent to Robinson. Consequently, the licensee performed a review of the Robinson Safety Injection Syste On January 7, 1986, a design deficiency was discovered in the SI pump minimum flow recirculation pat The three recirculation lines for the three SI pumps connect to a common return line which leads to the refueling water storage tank (RWST).

There are two isolation valves, SI-856A and B in series in the return line which are normally open, air-operated valves. The design deficiency is that these two valves fail closed on loss of air pressure or loss of electrical powe Also, the valve position indication in the control room for these valves is powered from the same breaker as the valve control circuit, so that a single failure of the breaker associated with either valve would also cause the loss of the valve position indication in the control room for the failed valv The SI recirculation system was designed to both provide a flow test loop for each SI pump and to prevent the pump damage which would result from SI pump operation at a zero flow rat In addition, the licensee stated that the valves were initially designed to fail closed to help ensure that radioactive water from the containment sump would not be pumped outside containment to the RWST during the recirculation phas Since protection against a small break LOCA became a design requirement, a new problem was defined by the possibility, during the injection phase, of SI pump operation at primary pressures below the SI initiation setpoint but above the SI pump shutoff head pressure, i.e., SI pump operation at zero injection flow. While unlikely, closure of either SI-856 A or B under these conditions could lead to failure of all three SI pump The licensee's interim corrective action was completed on January 7, 1986, and consisted of mechanically blocking open both recirculation shut off valves so that loss of electrical power or air pressure will not cause them to clos The minor changes needed to modify the procedure were also completed. The SI recirculation shut off valves are accessible in the SI pump room outside containmen The licensee stated that the permanent modification, to be implemented in the future, will consist of a modification to convert the valves to either manual or fail-as-positioned valves, along with the removal of the mechanical block. The inspector will continue to monitor this activit On January 15, 1986, the licensee stated that their review of the plant safety analysis verified that the SI pumps provided sufficient flow to the primary system for all break sizes with the SI pump recirculation line valves open; so that there was no need to stop SI pump recirculation flow before the end of the post-LOCA injection phas No violations or deviations were identified within the areas inspected.