IR 05000261/1979022

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IE Insp Rept 50-261/79-22 on 790925-28.Noncompliance Noted: Inadequate Radwaste Operating Procedures
ML14175B103
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 10/18/1979
From: Gibson A, Jenkins G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14175B099 List:
References
50-261-79-22, NUDOCS 7912030083
Download: ML14175B103 (7)


Text

0 RUNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA ST., N.W., SUITE 3100 ATLANTA, GEORGIA 30303 Report No. 50-261/79-22 Licensee:

Carolina Power and Light 411 Fayetteville Street Raleigh, North Carolina 27602 Docket No. 50-261 License No. DPR-23 Inspection at H. B. RAi on site near Hartsville, South Carolina Inspector:

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G. R. JenR-Date Signed Accompanying Person 1 J.f. Epperson Approved by:

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A. F. Vibson, Section Chief, FFMS Branch Date Signed SUMMARY Inspection on September 25-28, 1979 Areas Inspected This routine, unannounced inspection involved 28 inspector-hours onsite in the areas of radioactive effluent releases, effluent records and reports, effluent control procedures, solid radwaste, followup on noncompliance and inspector identified items, and followup on IE Bulletins, Circulars, and Information Notice Results Of the six areas inspected, no apparent items of noncompliance or deviations were identified in five areas; one apparent item of noncompliance was found in one area [Infraction:

Inadequate radwaste operating procedures (79-22-01)].

No apparent deviations were foun g3

DETAILS Persons Contacted Licensee Employees

  • R. B. Starkey, Plant Manager
  • D. S. Crocker, E&RC Supervisor
  • W. L. MacCready, Engineer, E&RC J. A. Eaddy, Senior Generation Specialist, E&RC W. T. Ritchie, RC&T Foreman J. Sawyer, Engineering Technician Other licensee employees contacted included one operato *Attended exit interview Exit Interview The inspection scope and findings were summarized on September 28, 1979 with those persons indicated in Paragraph 1 above. With regard to the item of noncompliance, the Plant Manager acknowledged the requirement for written procedures for all radwaste activities, and stated that the development and upgrading of such procedures would receive prompt attentio.

Licensee Action on Previous Inspection Findings (Closed) (78-23-05) Open Item:

Plant modification to preclude access to high radiation area during fuel transfer. Based on a discussion with the E&RC Supervisor, an inspector determined that a panel had been installed to prevent opening the gate by reaching through from outside, and the locking mechanism was now working properly. The inspector had no further question (Closed) (78-28-02) Open Item:

Implementing instructions for effluents. A new set of procedures has been developed. This item is close (Details, paragraph 5)

(Closed) 79-01-01) Open Item: Radiation monitor correlation progra P.T. 29.1, "Radiation Monitor Correlation Program", was approved April 20, 1979. This item is close (Details, paragraph 12)

(Closed) (79-01-02) Open Item: Liquid effluent monitor setpoints. Standing Order No. 4, "Radiation Monitor Setpoints", has been revised to reduce RMS-18 setpoint to a minimum value when no release is in progress. The inspector has no further question (Closed) (79-14-03) Deficiency:

10 CFR 19 notice not posted. An inspector observed that the notices were mounted in more permanent fixtures, as stated in CP&L's response of August 22, 1979, and had no further question.

4. Unresolved Items Unresolved items were not identified during this inspectio.

Efl1eunt Release Procedures The licensee has expanded and combined various Health Physics and Environ mental Surveillance Procedures into a new set of Environmental Surveillance (ES) procedures related to effluent release and accountability, as follows:

ES-2:

"Effluent and Waste Disposal Report" ES-3:

"Liquid Waste Release" ES-4 "Gaseous Effluent Accountability" Although these procedures had not been reviewed by PNSC nor approved by the Plant Manager at the time of this inspection, the inspector's preliminary review indicated that the procedures adequately address sampling, analysis, approval, documentation, and accountability associated with effluent release The inspector offered some comments for improvement of the procedures which were acknowledged by the E&RC Supervisor. The inspector also reviewed recent changes to Operating Procedure OP-35, "Waste Disposal-Gas", and had no question.

Radioactive Effluent Releases - Liquid Based on a review of all liquid waste release permits (LWRP) for January and February 1979, a spot check of other LWRP's from March through June 1979, and selected tests of data consistency between composite analysis results, monthly summary reports, and Semi-Annual Effluent Reports, an inspector determined that no liquid releases had exceeded the limits of Technical Specification 3.9.1 over the period July 1978 through June 197 The January and February LWRP's were checked in detail for calcu lational errors and for proper review and approval in accordance with plant procedures. Three uncorrected errors were identified on the LWRP's checked. Many potential errors had been prevented by the licensee's internal review and check program. Two LWRP's were found without the RC&T Foreman's approval as required by procedure. None of the mistakes identified appeared to have a significant impact on the total activity released or technical specification adherence. The inspector stated that much progress had been made in reduction of errors through the internal checks, but that continued emphasis on attention to detail would be required. Licensee management acknow ledged the inspector's commen During discussions of processing and release of liquid radwaste, a licensee representative said that the waste evaporator was now operating at a capacity of about 4 gpm compared with the previous capacity of 11-12 gpm. This reduction resulted from recent coating of the evaporator tubes with insulation material used in the major plant modification

-3 for fire prevention/control. The insulation material was inadvertently introduced into the radwaste system by contract workers washing out buckets in decontamination sink.

Radioactive Effluent Releases -

Gaseous Based on the review of Semi-Annual Effluent Reports for last half, 1978, and first half, 1979; gaseous waste release permits (GWRP) for January-June 1979; and selected tests of data consistency between monthly summary reports and Semi-Annual Effluent Reports, an inspector determined that no gaseous releases had exceeded the limits of Technical Specification 3.9.2 over the period July 1978 through June 197 Detailed checks were made of 36 out of a total of 127 GWRP's for the first six months of 1979. All required reviews and approvals appeared to be in order. Two uncorrected errors were identified on the GWRP's reviewed; neither appeared to have a significant impact on the net result The inspector's comments on attention to detail, discussed in paragraph 6.b, were applied to GWRP's as wel The second half, 1978 Semi-Annual Effluent Report identified an abnormal gaseous release which occurred October 26, 1978. An inspector discussed the event with licensee representatives and reviewed POE:

78-2. The event involved the release of containment air through the purge inlet valves due to an error by an operator in training. A GWRP had been prepared and approved for a containment pressure relief. The total release time through the purge inlet valves was about 30 seconds before it was manually stopped by the licensed operator. A GWRP was completed after the release for accountability purposes. Based on a review of the data, an inspector concluded that no technical specifi cation release limits were exceede.

Records and Reports of Radioactive Effluents Semi-Annual Effluent Reports for July - December 1978, and January June 1979, were reviewed for mistakes, anomalous results, trends, et No problems were identifie Based on reviews of waste release permits, monthly summary reports, and composite analyses results, the inspector had no questions regarding the adequate maintenance of effluent record.

Solid Radioactive Waste An inspector reviewed solid waste processing operations by discussions with licensee representatives and during a plant tour. The plant's originally installed equipment for solidification of spent resin and evaporator bottoms never operated satisfactorily. The method currently used for disposal of spent resin involves sluicing the resin to a

V-4 contractor supplied cask outside the auxiliary building, dewatering, and shipping to a licensed burial facility. The method used for disposal of evaporator concentrates (bottoms) involves pumping the slurry to the waste drumming room and manually mixing the slurry with cement into 55-gallon drums; the drums are subsequently shipped by truck for burial. The inspector reviewed Operating Procedure OP-36,

"Drumming Station". This procedure, last revised in 1974, provides operating instructions for the originally installed solidification system, with an added section (1973) on manual evaporator concentrate drumming. Since the procedure has not been revised since the instal lation of a new, larger waste evaporator in about December 1977, all references to the waste evaporator feed tank piping and valve lineups are apparently obsolete. There is no approved procedure for the connection, filling, dewatering, or precautionary measures needed for the transfer and packaging of spent resin. The inspector identified the lack of management approved procedures for these important radwaste evolutions associated with evaporator bottoms and spent resin as noncompliance with Technical Specification 6. (79-22-01) The inspector also noted that both IE Information Notice 79-09, March 30, 1979, and IE Bulletin 79-19, August 10, 1979, addressed the need for management approved procedures and instructions for radwaste related activities. Licensee management acknowledged the inspector's comments and stated that prompt attention would be given to the required procedure IE Bulletin 79-19, "Packaging of Low-Level Radioactive Waste for Transport and Burial" An inspector reviewed CP&L's response, dated September 21, 1979, to this Bulletin and had the following comments:

(1) The response stated that the official copies of DOT and NRC regulations and the waste burial facility license are maintained by the Health Physics Unit at the Harris Energy and Environmental Center. The inspector stated that these documents should be available at the plant because this is the origination point for shipments that are prepared by plant personnel. The Plant Manager concurred and stated that copies of the documents will be maintained at the plan (2) The response stated:

"We currently have management-approved, detailed instructions and operating procedures to be used by all personnel involved in the transfer, packaging, and transport of low-level radiactive materials." As discussed in paragraph above, significant transfer and packaging operations are being conducted without such procedures. Region II's concern with this discrepancy is addressed in the letter transmitting this inspection repor (3) The actions discussed in the response pertaining to training and audits will be reviewed during a later inspection. (79-22-02)

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10. IE Information Notices IN 79-07, "Rupture of Radwaste Tanks" The licensee's evaluation indicated that the radwaste concentrates holding tank has an atmospheric pressure rating (hydro-tested at 25 psig) and is heated to prevent the crystallization of waste concentrate The evaluation stated that there is no inspection program for the tank or its piping, but that any pressurization of the tank would be thor oughly reviewed before being implemented. The inspector had no further question IN 79-08, "Interconnection of Contaminated Systems with Service Air Systems Used as the Source of Breathing Air" H.B. Robinson Plant uses instrument air, rather than service air, for air supplied breathing apparatus. Instrument air is used to operate diaphragm type valves in the CVCS and radwaste system An engineering review concluded that a double failure of both a valve diaphragm and air regulator would be required to permit contamination of the instrument air. Weekly sampling of the instrument air for radioactivity has been incorporated into procedure HP-1. The inspector had no further question IN 79-09, "Spill of Radioactively Contaminated Resin" An inspector reviewed the licensee's written evaluation and discussed the resin transfer operation with the E&RC Supervisor. Contaminated resin are transfered from the drumming room to an outside dewatering cask using a metallic base rubber high pressure hose furnished by the contractor. Resin is moved through the lines to the cask by pressurizing the spent resin storage tank with nitrogen. The cask is vented and there are no flow restrictions to cause pressurization of the hose or couplings. The most likely means for a resin spill is to overfill the dewatering cask. The E&RC Supervisor said that during resin transfer, nearby storm drains are covered and communications are established between Operations and RC&T personnel. The inspector stated that these precautions should be detailed in the procedures discussed in paragraph 9.a above. The inspector had no further questions regarding this Information Notic.

IE Circulars IE Circular 79-09, "Occurrences of Split or Punctured Regulator Diaphragms in Certain Self-Contained Breathing Apparatus" By review of an internal memorandum and discussion with licensee representatives, an inspector determined that all plant Scott Air Paks have been inspected by an independent vender, plant personnel have been trained by Scott Aviation on the proper methods of inspection and repair, and all Scott Air Paks are inspected monthly by plant personne The inspector had no further question IE Circular 79-15, "Bursting of High Pressure Hose and Malfunction of Relief Valve and "O"-Ring in Certain Self-Contained Breathing Apparatus" This circular described problems associated with Surviv Air breathing apparatus. A licensee representative stated that H. B. Robinson plant does not use that type SCBA. The inspector had no further question.

Correlation of Radiation Monitors An inspector reviewed the first completed P. T. 29.1, "Radiation Monitor Correlation Program", based on data obtained during June-August, 197 These results were of limited value because most of the process and effluent monitor readings were below the statistically significant minimum detectable activity. The E&RC Supervisor said that he planned to perform the P. quarterly for about one year and then evaluate what deletions or changes should be made. The inspector had no further questions.