IR 05000261/1979004

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IE Insp Rept 50-261/79-04 on 790213-16.No Noncompliance Noted.Major Areas Inspected:Licensee Event Followup & Plant Operations
ML14175B033
Person / Time
Site: Robinson 
Issue date: 03/15/1979
From: Dance H, Mchenry T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14175B032 List:
References
50-261-79-04, 50-261-79-4, NUDOCS 7905230592
Download: ML14175B033 (4)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, ATLANTA, GEORGIA 30303 Report No.:

50-261/79-04 Licensee:

Carolina Power and Light Company 411 Fayetteville Street Raleigh, North Carolina 27602 Facility Name: H. B. Robinson 2 Docket No.:

50-261 License No.:

DPR-23 Inspection at Robinson Site, Hartsville, South Carolina Inspector:

c T. J. McHenry (

Date gign d Approved by:

i13 (

/j /

H. C. Dance, Section Chief, RONSB Date Signdd SUMMARY Inspection on February 13-16, 1979 Areas Inspected This routine, unannounced inspection involved 34 inspector-hours on-site in the areas of licensee event followup, review of plant operations, independent inspection effort and facility tour Results Of the four areas inspected, no apparent items of noncompliance or deviations were identifie DETAILS 1. Persons Contacted Licensee Employees R. B. Starkey, Jr., Plant Manager

  • C. W. Crawford, Operations Supervisor
  • H. S. Zimmerman, Maintenance Supervisor
  • J. M. Curley, Engineering Supervisor
  • B. W. Garrison, Quality Assurance Supervisor D. S. Crocker, Environmental and Radiation Control Supervisor C, Wright, Engineering Technician M. Page, Engineer W. T. Traylor, Administratice Supervisor F. Bishop, Electrical Engineer Other licensee employees contacted included technicians, operators, and office personne *Attended exit interview 2. Exit Interview The inspection scope and findings were summarized on February 16, 1979 with those persons indicated in Paragraph I above. The inspection activities presented in these details were discusse. Licensee Action on Previous Inspection Findings Not inspecte. Unresolved Items Unresolved items were not identified during this inspectio.

Review of Plant Operations The inspector reviewed the following areas of plant operation to ascertain whether facility operation was in conformance with applicable regulatory requirements and licensee commitments: Operating Logs and Records The inspector reviewed the following operating logs and records to ascertain whether plant operation was in conformance

-2 with Technical Specifications and established licensee requirements:

-Shift Formen logbook January 6-February 14, 1979-Control Room Operator logbook January 13-February 14, 1979-Control Room Hot Operation Datalog January 1-31, 1979-Auxilary Operator-Outside Data log January 1-31, 1979-Auxilary Operator-Inside Data log January 1-31, 1979-Plant Trouble Tickets January 1-February 14, 1979-Equipment Inoperable Report Forms January 1-February 14, 1979 The inspector reviewed the above operating logs to insure that logged data was recorded in sufficient detail to communicated equipment status and properly reviewed by supervisory personne In addition, logs were reviewed to insure that logged information did not conflict with Technical Specification requirement The inspector reviewed the above plant Trouble Tickets and Equipment Inoperable Report Forms to insure that applicable Technical Specifications including reporting requirements were adhered to for inoperable equipmen No problems were identified in this are Facility Tours The inspector conducted several facility tours including accompanying the inside Auxilary Operator during a backshift inspection. Inspection activities in this area included observation to insure that; instrumentation was operating and calibrated as required, radiation controls were established and properly adhered to, fire protection equipment was located as specified and appeared operable. In addition, selected valves, breakers and control switches were verified to be properly assigned as required by Technical Specifications and plant procedure No problems were identified within this are Control Room Operations Control room operations were observed and discussed with control room personnel to assure compliance with Technical Specifications

-3 and plant administrative requirements. Inspection activities in the control room included observation of selected instrumentation to assure plant operation within required limits, observation of surveillance testing and shift turnover to ascertain adherence to procedural and administrative requirements, verification of control room manning in conformance with the requirements of IOCFR50.54(k), and discussions with control room operators pertaining to selected parameters and annunciator No problems in this area were identifie.

Review of Licensee Event Report (LER's)

The inspector reviewed two LER's for consistency with the requirements of Technical Specification Section The inspector examined the licensee's analysis of the event, corrective action taken, and discussed the LER's with licensee's representatives. The following LER's were reviewed: LER 79-01, Containment Personnel Hatch Seal Leakage The inspector reviewed the requirements of Technical Specification 3.6.1, Containment Integrity, to ascertain the affect of the LER on containment integrity. Since the outer containment door seal was operable there was no loss of containment integrity as defined by Technical Specification definition In addition, the reporting requirements of 6.9.2.b.4 excludes containment. The reportability of this occurrence was discussed with the plant manager who stated that this item was reported primarily due to fact that other occurrence involving Penetration Pressurization System (PPS) leakage through valves had been reported in the pas The inspector stated that additional review of the reportability requirements associated with the PPS system would be conducted and future clarification would be provided when available. This LER is close LER 79-02, Inoperable Smoke Detector This LER is closed without comment.