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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217H4661999-10-18018 October 1999 Forwards Changes to EPIPs IAW 10CFR50.54(q) & 10CFR50,App E, Section V.Details of Changes Encl ML20216J8241999-09-30030 September 1999 Notifies of Removal of NRC Headquarters & Region III Offices from Controlled Copy Distribution of Certain CE Documents. Specific Documents,Associated Controlled Copy Numbers & NRC Location Affected Are Shown on Attachment to Ltr ML20211G1221999-08-27027 August 1999 Forwards fitness-for-duty Program Performance Data for Each of Comm Ed Nuclear Power Stations & Corporate Support Employees within Scope of Rule for six-month Period Ending 990630,IAW 10CFR26.71(d) ML20210N5651999-08-0606 August 1999 Forwards Rev 8 to Nuclear Generating Stations Emergency Plan, for Plants.With Summary of Changes ML20210L1061999-08-0202 August 1999 Forwards Insp Rept 50-010/99-13 on 990702-27.No Violations Noted.Insp Examined Activities in Areas of Facility Management & Control & Radiological Safety ML20210M9131999-08-0202 August 1999 Forwards Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for Fys 2000 & 2001 for Comed ML20210D2961999-07-20020 July 1999 Forwards Corrected Info for DNPS Unit 3 MOR for June 1999. Year-to Date Forced Outage Hours Should Have Read 70 Hours Instead of 0 on Page 8.Error Also Affected Cumulative Forced Outage Hours Which Should Have Been 24,761 ML20210B7071999-07-16016 July 1999 Responds to Requesting Review & Approval of Three Proposed Changes to Ceco QA TR,CE-1A Per 10CFR50.54(a)(3) & 10CFR50.4(b)(7) ML20196J9061999-07-0101 July 1999 Provides Evidence That Util Maintains Guarantee of Payment of Deferred Premiums in Amount of $10 Million for Each of Thirteen Reactors,Per 10CFR140.21 ML20196J9131999-07-0101 July 1999 Submits Status of Nuclear Property Insurance Currently Maintained for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR50.54(w)(3) ML20209B8241999-06-30030 June 1999 Forwards Five 3.5 Inch Computer Diskettes Containing Revised Annual Dose Repts for 1994 Through 1998 for Individuals Receiving Neutron Dose Not Previously Included in Reported Total Effective Dose Equivalent Values.Without Diskettes ML20196K3231999-06-30030 June 1999 Informs That Effective 990703,NRC Project Management Responsibility for Dresden,Unit 1 Station Will Be Transferred to P Ray ML20196D3491999-06-18018 June 1999 Forwards Insp Repts 50-237/99-08 & 50-249/99-08 on 990408-0521.Four Non-Cited Violations Noted.Maint on safety- Related Emergency CR Not Performed Well.Low Impact Issues Re Communications Present in Operations,Maint & Security ML20212J0541999-06-17017 June 1999 Responds to Requesting That NRC Staff ...Allow BWR Plants Identified to Defer Weld Overlay Exams Until March 2001 or Until Completion of NRC Staff Review & Approval of Proposed Generic Rept,Whichever Comes First ML20195E3451999-06-0707 June 1999 Forwards 3.5 Inch Computer Diskette Containing Revised File Format for Annual Dose Rept for 1998,per 990520 Telcon Request from Nrc.Each Station Data Is Preceded by Header Record,Which Provides Info Necessary to Identify Data ML20195D6351999-06-0404 June 1999 Notifies NRC of Actions That Has Been Taken in Accordance with 10CFR26, Fitness for Duty Programs ML20207G2571999-06-0303 June 1999 Informs That Effective 990328,NRC Ofc of NRR Underwent Reorganization.Within Framework of Reorganization,Division of Licensing Project Management Created ML20195B2301999-05-19019 May 1999 Requests Approval of Proposed Changes to QA Topical Rept CE-1-A,rev 66a.Attachment a Describes Changes,Reason for Change & Basis for Concluding That Revised QAP Incorporating Proposed Changes Continues to Satisfy 10CFR50AppB ML20206Q3111999-05-18018 May 1999 Final Response to FOIA Request for Documents.Forwards App a Records Being Released in Entirety ML20206P2431999-05-13013 May 1999 Forwards Insp Rept 50-010/99-09 on 990325-0506.Two Violations of NRC Requirements Occurred & Being Treated as non-cited Violations Consistent with App C of Enforcement Policy ML20206F5381999-04-30030 April 1999 Forwards Magnetic Tape Containing Annual Dose Repts for 1998 for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR20.2206(c).Without Magnetic Tape ML20206B1501999-04-22022 April 1999 Forwards 1998 Occupational Radiation Exposure for Dresden Nuclear Power Station,Units 1,2 & 3. Rept Was Revised to Rept Only Individual Radiation Exposures Greater than 100 Mrem ML20206B2471999-04-20020 April 1999 Informs That SE Kuczynski Has Been Transferred to Position No Longer Requiring SRO License.Cancel License SOP-31030-1, Effective 990412 ML20205K5521999-04-0202 April 1999 Forwards Partially Withheld Security Insp Repts 50-010/99-07,50-237/99-07 & 50-249/99-07 on 990308-12.Two non-cited Violations Identified Involving Failure of Security Personnel to Implement Required Measures ML20205K5841999-03-31031 March 1999 Submits Rept on Status of Decommissioning Funding for Reactors Owned by Comm Ed.Attachment 1 Contains Amount of Decommissioning Funds Estimated to Be Required Pursuant to 10CFR50.75(b) & (C) ML20196K7001999-03-31031 March 1999 Forwards Dresden Nuclear Power Station,Units 1,2 & 3 Radioactive Effluent Release Rept,Jan-Dec 1998. ODCM Was Submitted by Ltr in Accordance with Dresden TS 6.9.A.4 of Dresden Tech Specs Section 6.14.A.3 ML20205D7231999-03-26026 March 1999 Informs That Region III Emergency Preparedness Inspector Will Be Provided Copy of Comed Exercise Manual for 990526 Annual Exercise at DNPS ML20205B4241999-03-23023 March 1999 Provides Results of drive-in Drill Conducted on 990208,as Well as Augmentation Phone Drills Conducted Since 981015,as Committed to in Util ML20207L7141999-03-0808 March 1999 Discusses Transmitting Changes Identified as Rev 59 to Security Plan for Dresden Nuclear Power Station,Units 1,2 & 3.Staff Determined That No NRC Approval Required in Accordance with 10CFR50.54(p) ML20207D6831999-03-0101 March 1999 Forwards fitness-for-duty Program Performance Data for Each Comed Nuclear Power Station & Corporate Support Employees for Six Month Period Ending 981231,per 10CFR26.71(d) ML20207E0931999-02-26026 February 1999 Informs That Region III EP Inspectors Will Be Provided One Copy of Exercise Evaluation Objectives for 990526 Annual Exercise at Dresden Station as Enclosure to Ltr for Review. Proprietary Encl Withheld ML20203G3631999-02-10010 February 1999 Forwards Insp Rept 50-010/99-02 on 981218-990129.No Violations Noted.During Insp,Activities in Area of Facility Mgt & Control,Decommissioning Support Activities & Radiological Safety Were Examined ML20203F2541999-02-10010 February 1999 Informs That Beginning 990216,DE Hills Will Be Chief of Operations Branch Which Includes Operator Licensing Function ML20203C7001999-02-0202 February 1999 Informs That Mhb Technical Associates No Longer Wishes to Receive Us Region III Docket Info Re Comed Nuclear Facilities.Please Remove Following Listing from Service List ML20202G0621999-01-25025 January 1999 Forwards 1998 Revs to Commitments Rept Made in Docketed Correspondence for Dresden Nuclear Power Station ML20199F3291999-01-14014 January 1999 Ack Receipt of Ltr Dtd 981230,transmitting Changes Identified as Rev 59 to Plant Security Plan,Submitted Under Provisions of 10CFR50.54(p) ML20199E0201999-01-12012 January 1999 Forwards Change to Bases of Dnps,Unit 1 TS Section 3.10, Fuel Handling & Storage. Change Eliminates Reference to Initiation of Generating Station EP Action That Is Incorrect & Not Part of Reason for Min FSP Water Level TS ML20199C8851999-01-11011 January 1999 Forwards Monthly Operating Repts for Dec 1998 for Dnps,Units 1,2 & 3,as Required by TS 6.9.A.5.Year-to-date Generator Hours for Unit 2 for Oct 1998 & Nov 1998 Corrected in Rept ML20206P7411999-01-0707 January 1999 Informs of Delay in Implementation of Strategic Reform Initiative Action Steps.Util Mgt Now Preceeding to Implement Succession Planning Steps for Corporate Ofc & Expects Completion of Action Steps 2 & 3 by 990128 ML20198N7691998-12-30030 December 1998 Forwards Rev 59 to Security Plan for Dresden Nuclear Power Station,In Accordance with 10CFR50.4(b)(4).Rev Withheld ML20198A2511998-12-10010 December 1998 Ack Receipt of ,Which Transmitted Changes Identified as Rev 58 to Plant Security Plan,Per 10CFR50.54(p).No NRC Approval Is Required ML20198A2531998-12-10010 December 1998 Ack Receipt of Which Transmitted Changes Identified as Rev 57 to Plant Security Plan,Per 10CFR50.54(p).No NRC Approval Is Required ML20196E2371998-11-27027 November 1998 Discusses Licensee ,Requesting That Agreement in Be Changed to Reflect Latest NRC Conditions Requiring Licensees to Notify NRC of Transfer of Assets to Affiliates Imposed in Connection with Approval of Transfer ML20196B5871998-11-20020 November 1998 Requests That Svc List for All NRC Correspondence Re Any of Six Comed Nuclear Stations Be Modified Per Attached List.All Other Names Previously Listed Should Be Removed ML20196A4121998-11-19019 November 1998 Forwards Safety Evaluation Accepting Proposed Changes to QA TR CE-1-A,Rev 66,by ,As Modified by Ltrs & 1027.Proposed QA Tr,Rev 66 Continues to Comply with Criteria of 10CFR50,App B ML20195J4271998-11-13013 November 1998 Forwards Insp Repts 50-010/98-18,50-237/98-27 & 50-249/98-27 on 981013-16 & Notice of Violation.Mgt Activities Were Focused Toward Maintaining Effective Security Program ML20195E6451998-11-12012 November 1998 Provides Results of drive-in Drill Conducted on 981007,as Well as Augmentation Phone Drill Conducted on 980917 ML20195F3461998-11-10010 November 1998 Forwards Rev 58 of DNPS Security Plan,Including Listed Changes,Iaw 10CFR50.4(b)(4).Encl Withheld Ref 10CFR73.21 ML20155D2701998-10-27027 October 1998 Forwards Changed Pages from 980423 Submittal Providing Addl Info Marked with Revision Bars & Revised Pages to QA Topical Rept Section 18,for Review ML20154P9051998-10-20020 October 1998 Ack Receipt of 980821 Submittal,Per 10CFR50.54(a),requesting Review & Approval of Proposed Changes That Reduce Commitments in QA TR,CE-1-A.Util Should Refrain from Implementing Subj Changes Until Formal Notification Given 1999-09-30
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217H4661999-10-18018 October 1999 Forwards Changes to EPIPs IAW 10CFR50.54(q) & 10CFR50,App E, Section V.Details of Changes Encl ML20216J8241999-09-30030 September 1999 Notifies of Removal of NRC Headquarters & Region III Offices from Controlled Copy Distribution of Certain CE Documents. Specific Documents,Associated Controlled Copy Numbers & NRC Location Affected Are Shown on Attachment to Ltr ML20211G1221999-08-27027 August 1999 Forwards fitness-for-duty Program Performance Data for Each of Comm Ed Nuclear Power Stations & Corporate Support Employees within Scope of Rule for six-month Period Ending 990630,IAW 10CFR26.71(d) ML20210N5651999-08-0606 August 1999 Forwards Rev 8 to Nuclear Generating Stations Emergency Plan, for Plants.With Summary of Changes ML20210M9131999-08-0202 August 1999 Forwards Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for Fys 2000 & 2001 for Comed ML20210D2961999-07-20020 July 1999 Forwards Corrected Info for DNPS Unit 3 MOR for June 1999. Year-to Date Forced Outage Hours Should Have Read 70 Hours Instead of 0 on Page 8.Error Also Affected Cumulative Forced Outage Hours Which Should Have Been 24,761 ML20196J9061999-07-0101 July 1999 Provides Evidence That Util Maintains Guarantee of Payment of Deferred Premiums in Amount of $10 Million for Each of Thirteen Reactors,Per 10CFR140.21 ML20196J9131999-07-0101 July 1999 Submits Status of Nuclear Property Insurance Currently Maintained for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR50.54(w)(3) ML20209B8241999-06-30030 June 1999 Forwards Five 3.5 Inch Computer Diskettes Containing Revised Annual Dose Repts for 1994 Through 1998 for Individuals Receiving Neutron Dose Not Previously Included in Reported Total Effective Dose Equivalent Values.Without Diskettes ML20195E3451999-06-0707 June 1999 Forwards 3.5 Inch Computer Diskette Containing Revised File Format for Annual Dose Rept for 1998,per 990520 Telcon Request from Nrc.Each Station Data Is Preceded by Header Record,Which Provides Info Necessary to Identify Data ML20195D6351999-06-0404 June 1999 Notifies NRC of Actions That Has Been Taken in Accordance with 10CFR26, Fitness for Duty Programs ML20195B2301999-05-19019 May 1999 Requests Approval of Proposed Changes to QA Topical Rept CE-1-A,rev 66a.Attachment a Describes Changes,Reason for Change & Basis for Concluding That Revised QAP Incorporating Proposed Changes Continues to Satisfy 10CFR50AppB ML20206F5381999-04-30030 April 1999 Forwards Magnetic Tape Containing Annual Dose Repts for 1998 for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR20.2206(c).Without Magnetic Tape ML20206B1501999-04-22022 April 1999 Forwards 1998 Occupational Radiation Exposure for Dresden Nuclear Power Station,Units 1,2 & 3. Rept Was Revised to Rept Only Individual Radiation Exposures Greater than 100 Mrem ML20206B2471999-04-20020 April 1999 Informs That SE Kuczynski Has Been Transferred to Position No Longer Requiring SRO License.Cancel License SOP-31030-1, Effective 990412 ML20196K7001999-03-31031 March 1999 Forwards Dresden Nuclear Power Station,Units 1,2 & 3 Radioactive Effluent Release Rept,Jan-Dec 1998. ODCM Was Submitted by Ltr in Accordance with Dresden TS 6.9.A.4 of Dresden Tech Specs Section 6.14.A.3 ML20205K5841999-03-31031 March 1999 Submits Rept on Status of Decommissioning Funding for Reactors Owned by Comm Ed.Attachment 1 Contains Amount of Decommissioning Funds Estimated to Be Required Pursuant to 10CFR50.75(b) & (C) ML20205D7231999-03-26026 March 1999 Informs That Region III Emergency Preparedness Inspector Will Be Provided Copy of Comed Exercise Manual for 990526 Annual Exercise at DNPS ML20205B4241999-03-23023 March 1999 Provides Results of drive-in Drill Conducted on 990208,as Well as Augmentation Phone Drills Conducted Since 981015,as Committed to in Util ML20207D6831999-03-0101 March 1999 Forwards fitness-for-duty Program Performance Data for Each Comed Nuclear Power Station & Corporate Support Employees for Six Month Period Ending 981231,per 10CFR26.71(d) ML20207E0931999-02-26026 February 1999 Informs That Region III EP Inspectors Will Be Provided One Copy of Exercise Evaluation Objectives for 990526 Annual Exercise at Dresden Station as Enclosure to Ltr for Review. Proprietary Encl Withheld ML20203C7001999-02-0202 February 1999 Informs That Mhb Technical Associates No Longer Wishes to Receive Us Region III Docket Info Re Comed Nuclear Facilities.Please Remove Following Listing from Service List ML20202G0621999-01-25025 January 1999 Forwards 1998 Revs to Commitments Rept Made in Docketed Correspondence for Dresden Nuclear Power Station ML20199E0201999-01-12012 January 1999 Forwards Change to Bases of Dnps,Unit 1 TS Section 3.10, Fuel Handling & Storage. Change Eliminates Reference to Initiation of Generating Station EP Action That Is Incorrect & Not Part of Reason for Min FSP Water Level TS ML20199C8851999-01-11011 January 1999 Forwards Monthly Operating Repts for Dec 1998 for Dnps,Units 1,2 & 3,as Required by TS 6.9.A.5.Year-to-date Generator Hours for Unit 2 for Oct 1998 & Nov 1998 Corrected in Rept ML20206P7411999-01-0707 January 1999 Informs of Delay in Implementation of Strategic Reform Initiative Action Steps.Util Mgt Now Preceeding to Implement Succession Planning Steps for Corporate Ofc & Expects Completion of Action Steps 2 & 3 by 990128 ML20198N7691998-12-30030 December 1998 Forwards Rev 59 to Security Plan for Dresden Nuclear Power Station,In Accordance with 10CFR50.4(b)(4).Rev Withheld ML20196B5871998-11-20020 November 1998 Requests That Svc List for All NRC Correspondence Re Any of Six Comed Nuclear Stations Be Modified Per Attached List.All Other Names Previously Listed Should Be Removed ML20195E6451998-11-12012 November 1998 Provides Results of drive-in Drill Conducted on 981007,as Well as Augmentation Phone Drill Conducted on 980917 ML20195F3461998-11-10010 November 1998 Forwards Rev 58 of DNPS Security Plan,Including Listed Changes,Iaw 10CFR50.4(b)(4).Encl Withheld Ref 10CFR73.21 ML20155D2701998-10-27027 October 1998 Forwards Changed Pages from 980423 Submittal Providing Addl Info Marked with Revision Bars & Revised Pages to QA Topical Rept Section 18,for Review ML20154M4291998-10-15015 October 1998 Forwards 1998 Third Quarter 10CFR50.59 Rept of Completed Changes,Tests & Experiments.Completed SEs Compared to Previous Quarterly Repts as Docketed ML20154J4951998-10-0707 October 1998 Forwards Revised Security Plans for CE Listed Nuclear Power Stations,Per 10CFR50.4(b)(4).Changes Do Not Decrease Effectiveness of Station Security Plans.Encl Withheld ML20151Y5101998-09-11011 September 1998 Provides Results of drive-in-drill Conducted on 980804 & Augmentation Phone Drills Conducted Between 980601 & 0831 ML20151Y2931998-09-0909 September 1998 Notifies NRC of Results of Feasiblity Study of Seismically Qualified or Verified Path to Obtain Water from Ultimate Heat Sink & Deliver It to Shell of Isolation Condenser for Each Unit ML20238F7571998-08-28028 August 1998 Forwards fitness-for-duty Program Performance Data for Each of Util Nuclear Power Stations for Six Month Period Ending 980630 ML20237D9771998-08-21021 August 1998 Forwards Proposed Changes to Quality Assurance Topical Rept (QATR) CE-1-A,rev 66,modifying Ref Submittal & Clarifying Certain Changes to QATR Proposed in Util .Page A-1, 6 of 6 of Incoming Submittal Not Included ML20237A8611998-08-0707 August 1998 Requests Approval of Enclosed Qualified Unit 1 Supervisor Initial & Continuing Training Program, Which Ensures That Qualifications of Personnel Are Commensurate W/Tasks to Be Performed & Conditions Requiring Response ML20237A8871998-08-0707 August 1998 Documents Completion of Util Action Items Discussed at 980529 Meeting W/Nrc.Updated Proposal to Consolidate Near Site Emergency Operations Facilities Into Single Central Emergency Operations Facility,Provided ML20236W1311998-07-27027 July 1998 Forwards Response to NRC Re Violations Noted in Insp Repts 50-010/98-15,50-237/98-18 & 50-249/98-18, Respectively.Encl Withheld ML20236T7241998-07-24024 July 1998 Forwards Revised Epips,Including CEPIP-2000 Series Table of Contents & Rev 7 to CEPIP-2121-01, Augmentation Caller Instructions ML20236R2531998-07-16016 July 1998 Summarizes Results of drive-in Drill as Well as Preceeding call-in Drills Conducted Between Each drive-in Drill,As Committed to in 980326 Meeting Between Util & NRC ML20236F8041998-06-29029 June 1998 Forwards Rev 0 to Defueled SAR Dresden Nuclear Power Station Unit 1 Commonwealth Edison Co, Per Requirements of 10CFR50.71(e)(4).Decommissioning Program Plan Is Being Reformatted & Revised Into Defueled SAR SVP-98-170, Advises That AL Misak,License SOP-30832-1,is No Longer Required to Maintain Operator License1998-05-0101 May 1998 Advises That AL Misak,License SOP-30832-1,is No Longer Required to Maintain Operator License ML20247B6521998-04-30030 April 1998 Forwards 1997 Repts for Braidwood,Byron,Dresden,Lasalle,Quad Cities & Zion Nuclear Power Stations.Repts Being Submitted Electronically on Magnetic Tape.W/O Encl ML20217G8841998-04-23023 April 1998 Forwards Proposed Changes to QATR CE 1-A,rev 66.Change Constitutes Major Programmatic Rev to Onsite & Offsite Review Processes as Presently Described in Rept ML20246Q1391998-04-20020 April 1998 Provides Response to Violations Noted in Insp Repts 50-010/98-08,50-237/98-08 & 50-249/98-08.Corrective Actions: Described in Attachment Which Contains Safeguards Matl.Encl Withheld ML20217N3461998-03-31031 March 1998 Provides Basis for Plant Conclusion That Dam Failure Coincident W/Loca Is Beyond Design Basis of Dresden,Units 2 & 3.Licensing Amend Is Not Necessary & Clarifications to UFSAR May Be Made Through Provisions of 10CFR50.59 ML20216H4041998-03-13013 March 1998 Forwards Revs to Byron,Dresden,Lasalle & Zion Station OCDM, Current as of 971231,ODCM Manual & Summary of Changes Included ML20203L2911998-02-27027 February 1998 Provides Revised Schedule for Hazardous Matl Response Drill Described in 971121 Response to Insp Repts 50-010/97-13,50-237/97-13,50-249/97-13 & NOV 1999-09-30
[Table view] Category:UTILITY TO NRC
MONTHYEARML20059F0311990-08-27027 August 1990 Provides Schedule for Completion of Installation of Mods to Plants Reactor Water Level Instrumentation,Per Generic Ltr 84-23.Penetrations Will Be Installed During Outage 13 for Dresden & During Outage 12 for Quad-Cities ML20055H7631990-07-25025 July 1990 Forwards Financial Info Re Decommissioning of Plants ML17202L2861990-07-0202 July 1990 Forwards Dresden II Upper Vessel Contract Variation Review, La Salle II Upper Vessel Fabrication Summary & Quad-Cities II Upper Vessel Fabrication Summary. ML20043D3231990-06-0101 June 1990 Forwards Rev 31 to Security Plan.Rev Withheld (Ref 10CFR73.21) ML20043C8181990-05-30030 May 1990 Forwards Rev 1 to Core Operating Limits Rept,Dresden Station Unit 2,Cycle 12. Rev Reflects MCPR Limit Adjustment for Cycle 12 Due to Number of Reused Channels,Per Discussion of Channel Bow Effects in BWRs in NRC Bulletin 90-002 ML17347B5881990-03-0101 March 1990 Responds to Generic Ltr 90-01, Request for Voluntary Participation in NRC Regulatory Impact Survey. Info Covers Time Spent by Key Power Plant Managers in Responding to Operational Insps & Audits ML15217A1031990-02-28028 February 1990 Forwards Semiannual Radioactive Effluent Release Rept for Jul-Dec 1989 for McGuire Nuclear Station Units 1 & 2 & Revised Process Control Programs & Offsite Dose Calculation Manuals ML18094B3221990-02-28028 February 1990 Forwards Executed Amend 14 to Indemnity Agreement B-74 ML20011F3821990-02-26026 February 1990 Confirms Amount Electronically Transferred to Us Dept of Treasury,Nrc on 900223 for Payment of NRC Review Fees of 10CFR50 Applications & 10CFR55 Svcs Per 10CFR170,for Period of 890101-0617 for Listed Invoices ML20006G0621990-02-22022 February 1990 Forwards Revised Proprietary Pages to DPC-NE-2004, Core Thermal Hydraulic Methodology Using VIPRE-01, Reflecting Minor Methodology Changes Made During Review & Approval Process.Pages Withheld ML20006E9071990-02-16016 February 1990 Discusses Plants Design Control Program.Util Adopted Concept of Design Change Implementation Package (Dcip).Dcip Will Contain or Ref Design Change Notice Prepared Per Approved Procedures ML20006E1441990-02-16016 February 1990 Forwards Suppl to Rev 1 to Updated FSAR for Braidwood Station,Units 1 & 2 & Byron Station,Units 1 & 2,per 881214 & 891214 Submittals ML20006E4201990-02-14014 February 1990 Requests NRC Approval for Use of Alloy 690 Steam Generator Tube Plugs for Facility,Prior to 900301,pending Final ASME Approval of Code Case for Alloy 690 ML20011E6151990-02-12012 February 1990 Forwards Revs 1 to Security Plan & Security Training & Qualification Plan & Rev 2 to Security Contingency Plan. Salem Switchyard Project Delayed.Revs Withheld (Ref 10CFR73.21) ML20011E4991990-02-0606 February 1990 Discusses Liability & Funding Requirements Re NRC Decommissioning Funding Rules & Verifies Understanding of Rules.Ltr from NRC Explaining Liability & Requirements of Rule Requested ML17202G7741990-02-0505 February 1990 Forwards Core Operating Limits Rept,Dresden Station Unit 2,Cycle 12,Rev 0 & Core Operating Limits Rept,Dresden Station Unit 3,Cycle 12,Rev 0. Cycle 12 Startup Expected on 900210 ML20006D6911990-02-0202 February 1990 Provides Alternative Design Solution to Dcrdr Implementation at Facilities.Simpler Design Devised,Using Eyelet Screw Inserted in Switch Nameplate Which Is Identical to Providing Caution Cards in Close Proximity to Switch Handle ML20006C5661990-01-31031 January 1990 Provides Certification Re Implementation of Fitness for Duty Program Per 10CFR26 at Plants ML18153C0951990-01-29029 January 1990 Forwards Response to Generic Ltr 89-13, Svc Water Sys Problems Affecting Safety-Related Equipment. Belief in Appropriateness to Address Generic Ltr 89-13 Concerns within Context of Established Programmatic Improvements Noted ML20011E2521990-01-29029 January 1990 Forwards Proprietary Safety Analysis Physics Parameters & Multidimensional Reactor Transients Methodology. Three Repts Describing EPRI Computer Code Also Encl.Proprietary Rept Withheld (Ref 10CFR2.790) ML20006D6611990-01-29029 January 1990 Advises That 900117 License Amend Request to Remove Certain cycle-specific Parameter Limits from Tech Specs Inadvertently Utilized Outdated Tech Specs Pages.Requests That Tech Specs Changes Made Via Amends 101/83 Be Deleted ML20006C6711990-01-29029 January 1990 Responds to Generic Ltr 89-13, Svc Water Sys Problems Affecting Safety-Related Equipment. Plants Have Established Preventive Maint Program for Intake Structure & Routine Treatment of Svc Water Sys W/Biocide to Control Biofouling ML20006B7961990-01-29029 January 1990 Forwards Summaries of Latest ECCS Evaluation Model Changes ML20006D2431990-01-26026 January 1990 Provides Info Re Emergency Response Organization Exercises for Plants.Exercises & Callouts Would Necessitate Activation of Combined Emergency Operations Facility Approx Eight Times Per Yr,W/Some Being Performed off-hours & Unannounced ML18153C0871990-01-26026 January 1990 Responds to NRC Bulletin 89-003, Potential Loss of Required Shutdown Margin During Refueling Operations. Refueling Procedures to Be Revised & Familiarization Sessions Will Be Conducted Prior to Each Refueling Outage ML18094B2861990-01-26026 January 1990 Forwards Response to Generic Ltr 89-13, Svc Water Problems Affecting Safety-Related Equipment. Aggressive Program of Monitoring,Insp & Matl Replacement Initiated in Advance of Generic Ltr 89-13 Issuance ML19354E6711990-01-24024 January 1990 Requests Approval to Use Alloy 690 Plugs as Alternative to Requirements of 10CFR55(a),codes & Stds for Plants Prior to 900226 ML17347B5451990-01-24024 January 1990 Informs of Plans to Apply ASME Code Case N-356 at Plants to Allow Certification Period to Be Extended to 5 Yrs.Rev to Inservice Insp Programs Will Include Use of Code Case ML19354E4451990-01-22022 January 1990 Submits Update on Status of RHR Sys Iconic Display at Facilities,Per Generic Ltr 88-17 Re Loss of Dhr.Computer Graphics Display Data in Real Time & Reflect Status of Refueling Water Level & RHR Pump Parameters ML19354E4461990-01-22022 January 1990 Forwards Proprietary Rev 1 to DPC-NE-2001, Fuel Mechanical Reload Analysis Methodology for MARK-BW Fuel, Adding Section Re ECCS Analysis Interface Criteria & Making Associated Administrative Changes.Rev Withheld ML20005G7161990-01-20020 January 1990 Forwards Rev 1 to Updated FSAR for Braidwood & Byron Units 1 & 2.Changes in Rev 1 Include Facility & Procedures Which Were in Effect as of 890610.W/o Encl ML20006A8001990-01-19019 January 1990 Forwards Response to NRC 891220 Ltr Re Violations Noted in Plant Insps.Response Withheld (Ref 10CFR73.21) ML16152A9091990-01-18018 January 1990 Forwards Public Version of Rev 33 to Crisis Mgt Implementing Procedure CMIP-1, Recovery Manager & Immediate Staff & Rev 24 to CMIP-2, News Group Plan. W/900131 Release Memo ML18153C0771990-01-17017 January 1990 Forwards North Anna Power Station Emergency Plan Table 5.1, 'Min Staffing Requirements for Emergencies' & Surry... Table 5.1, 'Min Staffing Requirements...', for Approval,Per 10CFR50.54(q),NUREG-0654 & NUREG-0737,Suppl 1 ML20006A2011990-01-16016 January 1990 Responds to NRC Bulletin 89-002 Re Stress Corrosion Cracking of High Hardness Type 410 Stainless Steel in Anchor Darling Swing Check Valves.Eight Subj Valves Identified in Peach Bottom Units 1 & 2 & Will Be Returned to Mfg ML18153C0731990-01-15015 January 1990 Responds to NRC Bulletin 89-002, Stress Corrosion Cracking of High-Hardness Type 410 Stainless Steel Internal Preloaded Bolting in Anchor Darling Model S350W Swing Check Valves or or Valves.... Util Replaced Studs in twenty-five Valves ML20006A8201990-01-10010 January 1990 Forwards Errata to Rev 3 to BAW-1543,Tables 3-20 & E-1 of Master Integrated Reactor Vessel Surveillance Program Reflecting Changes in Insertion Schedule for A5 Capsule for Davis-Besse & Crystal River ML20006B8821990-01-10010 January 1990 Reissued Ltr Correcting Date of Util Ltr to NRC Which Forwarded Updated FSAR for Byron/Braidwood Plants from 881214 to 891214.W/o Updated FSARs ML20005G6431990-01-10010 January 1990 Responds to Generic Ltr 89-21 Re Implementation of USI Requirements,Consisting of Revised Page to 891128 Response, Moving SER Ref from USI A-10 to A-12 for Braidwood ML20005G7601990-01-0404 January 1990 Forwards Public Version of Rev 33 to Crisis Mgt Plan. Privacy Info Should Be Deleted Prior to Placement in Pdr.W/ D Grimsley 900118 Release Memo ML20005F4641990-01-0303 January 1990 Advises That Licensee Implemented 10CFR26 Rule Re fitness-for-duty Program W/One Exception.Util Has Not Completed Background Check for Some of Program Administrators.Checks Expected to Be Completed by 900105 ML18094B2331990-01-0303 January 1990 Certifies Util Implementation of fitness-for-duty Program, Per 10CFR26.Training Element Required by Rule Completed on 891215.Chemical Testing for Required Substances Performed at Min Prescribed cut-off Levels,Except for Marijuana ML18153C0491990-01-0303 January 1990 Advises of Implementation of fitness-for-duty Program Which Complies w/10CFR26.Util Support Objective of Providing Assurances That Nuclear Power Plant Personnel Will Perform Tasks in Reliable & Trustworthy Manner ML17347B5051990-01-0202 January 1990 Certifies That Util Has fitness-for-duty Program Which Meets Requirements of 10CFR26.Util Adopted cut-off Levels Indicated in Encl ML20042D3731990-01-0202 January 1990 Forwards Revised Crisis Mgt Implementing Procedures, Including Rev 32 to CMIP-1,Rev 29 to CMIP-4,Rev 33 to CMIP-5,Rev 38 to CMIP-6,Rev 37 to CMIP-7,Rev 32 to CMIP-9, Rev 1 to CMIP-14 & Rev 30 to CMIP-21 ML17347B4961989-12-28028 December 1989 Responds to Generic Ltr 89-10, Safety-Related Motor- Operated Valve Testing & Surveillance. Util Considering Expansion of Plants to Include Addl safety-related & Position Changeable Valves W/ Emphasis on Maint & Testing ML20042D3381989-12-28028 December 1989 Forwards Response to Generic Ltr 89-10, Safety-Related Motor-Operated Valve Testing & Surveillance. Util Will Comply W/Ltr Recommendations W/Noted Exceptions.Response to Be Completed When Ltr Uncertainties Cleared ML18094B2201989-12-27027 December 1989 Advises of Intent to Provide follow-up Response to Generic Ltr 89-10 by 900831 to Describe Status of Program, Recommendation Exceptions & Any Schedule Adjustments ML18094B2291989-12-27027 December 1989 Requests to Apply ASME Section XI Code Case N-460 to Facilities Re Reduction in Exam Coverage on Class 1 & 2 Welds.Fee Paid ML18153C0261989-12-26026 December 1989 Responds to Generic Ltr 89-10 Re safety-related motor-operated Valve Testing & surveillance.Motor-operated Valve Program Structured to Allow Similar Approach to motor-operated Dampers.Results Will Be Submitted in 30 Days 1990-08-27
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. Commonwealth Edison One First National Plaza. Chicago. lilinois Address Reply to: Post Office Box 767 Chicago, lihnois 60690 February 25, 1980 Mr. T. A. Ippolito, Chief Operating Reactors - Branch 3 Division of Operating Reactors U.S. Nuclear Regulatory Commission Washington, DC 20555
Subject:
Dresden Station Unit 3 Feedwater Nozzle /Sparger and CRD Return Line Nozzle Inspection Programs NRC Docket No. 5D-249
References:
(a) G.A. Abrell letter to D.L. Ziemann dated September 22, 1976 (b) G.A. Abrell letter to D.L. Ziemann dated October 18, 1976 (c) M.S. Turbak letter to D.K. Davis dated November 28, 1977 (d) M.S. Turbak letter to Mr. Lear dated May 15, 1978 (e) General Electric Report, NEDE-21821 dated March 1978, " Boiling Water Reactor Feedwater Nozzle /Sparger Final Report" (f) M.S. Turbak letter to D.K. Davis dated June 23, 1977
Dear Mr. Ippolito:
The purpose of this letter is to provide the feedwater nozzle and the control rod drive (CRD) return nozzle inspection programs to be implemented on Dresden Unit 3 during the present refueling outage. Justification for these programs is provided below, along with the long-term plan for the modification of the feedwater nozzles on this unit.
Feedwater Nozzle Program I. Feedwater Nozzle /Sparger Inspections The feedwater nozzle /sparger inspection program for Dresden Unit 3 will consist of the following:
- 1. Examination of the visible portions of the four spargers using underwater television equipment, h$
0 0 R l
Commonwealth Edison Mr. T. A. Ippolito February 22, 1980 Page 2
- 2. Ultrasonic examination of the inner blend radius and bore of the four nozzles using Procedures NOT-C-24 and NDT-C-25.
- 3. Ultrasonic examination of the four feedwater nozzle safe ends and safe end welds.
- 4. Acceptance criteria for the ultrasonic examination shall be identical to that defined in Reference (a), i.e.:
- a. The calibration piece shall be a duplicate (same material and geometry) of the actual feedwater nozzle and the adjoining section of the vessel wall and associated weld.
- b. Instrument calibration shall be performed by setting the response of an 8 mm deep notch in the blend radius and bore of the duplicate nozzle to 80% of full screen height (FSH).
- c. The examination shall be conducted at a sensitivity equal to the calibration sensitivity plus an additional 6 db in accordance with ASME Code, Article I-5112 of Section XI.
- d. All relevant indications with an amplitude greater than or equal to either 50% of the reference reflector (8 mm notch) or 10% FSH above the clad roll noise level shall be recorded and evaluated. This evaluation shall be in accordance with the methods defined in Reference (b).
All evaluations will be made at calibration sensitivity.
- e. If a relevant indication is evaluated as 80% FSH or more at calibration sensitivity, a dye penetrant examination will be made of the area containing the indication.
II. Justification for the Proposed Feedwater Nozzle /Sparger Inspection Program On February 2, 1980 Dresden Unit 3 began its third refueling outage following the installation of the interference fit, forged-T, feedwater spargers. The spargers were installed during the 1975 refueling outage occurring on D-3. A complete dye penetrant examination was performed prior to the installation of the new spargers. All indications found were removed by grinding leaving no linear indications. A reexamination of these nozzles was performed in September 1976, during the following refueling outage on that
CommonweaHh Edison Mr. T. A. Ippolito February 22, 1980 Page 3 unit. An external ultrasonic examination cas performed of the inner blend radius and the nozzle bore using CECO. procedures NDC-C-24 and NDT-C-25. As reported in reference (b) no significant indications were found. The unit had accumulated 14 startup/ shutdown (SU/DS) cycles.
During the Winter 1978 refueling outage another inspection was performed on the feedwater nozzles. The unit had accumulated 29 SU/SD cycles since the original repair in 1975.
The inspection as defined in reference (c) included an ultrasonic examination of the nozzle bore and inner radius of all four nozzles, again using CECO. procedures NDT-C-24 and NDT-C-25. Two reportable indications (Reference (d)) less than 80% full screen height were found in the nozzle bore area of two nozzles. These indications were verified to be the same indications that were found during the fall outage in 1976. It was concluded that these two small indications were cladding discontinuities.
The CECO. ultrasonic testing procedures used for examination of the feedwater nozzles has been demonstrated to be capable of detecting flaws ) 4 mm in depth. However, for the purpose of thevessel examination, the procedure requires that an 8 mm notch be used as a calibration reference, which ensures the detection of flaws 5 8 mm in depth. The maximum crack, therefore, which might remain after an ultrasonic examination, would be < 8 mm in depth. General Electric has had similar experience with their ultrasonic testing technique as reported in reference (e).
Crack growth curves developed by General Electric and CECO. were formulated assuming leakage flow past the thermal sleeve of the feedwater sparger as was the characteristic of the loose fit spargers. General Electric formulated a curve assuming a generic SU/SD cycle which was later found to be much more severe than the actual operating conditions. This was determined (Reference (f)) while reviewing operating data on Dresden 2 & 3 and Quad-Cities 1 & 2 for the purpose of constructing a plant unique cycle for the CECO. units. It is evident upon comparison of the two curves that the G.E. curve is much more prohibitive towards accumulating SU/SD cycles and continuing unit operation. An 8 mm crack would grow to critical flaw size after 43 SU/SD cycles using the G.E. curve, whereas it would take 68 cycles using the CECO. curve.
Comparing the number of SU/SD cycles accumulated on Dresden 3 since the last ultrasonic examination to the empirical crack growth curves, the unit is found to be well within the safe limits of either of the two curves.
i Commonwealth Edison Mr. T. A. Ippolito February 22, 1980 Page 4 Experience accumulated with the new interference fit sparger, however, has pointed out the conservatism even in the CECO. crack growth curves. Figure 1 contains data accumulated by General Electric on crack depth for up to 75 SU/SD cycles with the interference sparger in use. A curve established using the G.E. generic SU/SD cycle is compared to this actual interference fit data. It can be seen that the worst case of the 10 units with the interference fit sparger has a maximum crack depth of 0.2", with only one other unit having a maximum crack depth of 0.1". The remaining eight units, however, had maximum crack depths that were much smaller or nonexistent.
The above data points out the effectiveness of the interference fit sparger in eliminating the leakage flow which is the mechanism initiating the cracking in the feedwater nozzles.
Previous inspections on Dresden Unit 2 and Quad-Cities Unit 2 have confirmed the above trend for plants with interference fit spargers. As reported above, Dresden 2 had cracks less than 1/16" after 33 SU/SD cycles. During the Spring 1978 refueling outage on Quad-Cities Unit 2, a dye penetrant examination was performed on the accessible areas of three nozzles, and the entire bore and inner radius of the fourth nozzle with the sparger removed. The unit had 44 SU/SD cycles since the original repair and sparger installation, and no linear indications were found. Based on the dye penetrant examination, data accumulated by General Electric for the 10 units and on CECO. data for Quad-Cities Unit 2 and Dresden Unit 2, it is our contention that if any cracks exist on Dresden 3, they are no deeper than 0.2" considering that the unit has accumulated 49 SU/SD cycles since the original repair.
Finally, as part of the on-going program to provide a
" final fix" solution to the feedwater nozzle cracking problem, CECO. will install the new G.E. double seal / triple thermal sleeve sparger and will remove the clad from the feedwater nozzles on Dresden Unit 3. This work is scheduled to occur during one of the long outages associated with the Mark I containment work scheduled for the Fall of 1981.
In summary, our technical evaluation of the Dresden Unit 3 feedwater nozzle indicates that:
- 1. All indications on the feedwater nozzle inner radius were removed during the original clad repair and interference fit sparger installation.
- 2. The ultrasonic examination procedures used will insure that any cracks ) 8 mm in depth will be detected.
Commonwealth Edison Mr. T. A. Ippolito February 22, 1980 Page 5
- 3. Conservative crack growth curves still predict that a flaw remaining in the Dresden 3 nozzles subsequent to the previous inspection would be well below the critical flaw size.
- 4. Feedwater nozzle inspection data from GE and CECO. has proven the effectiveness of the interference fit sparger for providing an end to the effects of the thermal cycling on the feedwater nozzles in that after 75 SU/SD cycles, the deeptest crack found to date has been 0.2" (approximately 25 percent of the critical flaw size).
- 5. Dresden Unit 3 has had 49 SU/SD cycles accumulated since the original repair which is well below the threshold for which significant cracking has been observed on units with interference spargers.
On the basis of these facts, it is judged that the inspection program defined above is adequate. Furthermore, as stated, plans have been made to install the new G.E. double seal-triple thermal sleeve sparger and to remove the nozzle cladding on Dresden 3 during the Mark I, Fall 1981, outage.
Considering the above, plus the fact that a dye penetrant examination of the feedwater nozzles could expend approximately 200 man-rem and 10 critical path days of outage time, we feel that a dye penetrant exam is not warranted this outage. An estimated 18 additional SU/SD cycles, determined from D-3 cycle history, will occur prior to the start of the 1981 refueling outage which is still within the limits of experience with the
, interference fit sparger. It is the CECO. position, therefore,
( that the proposed inspection program, even though less stringent than that suggested in NUREG-0312, provides a safe and reliable inspection which would not compromise unit availability.
t CRD Return Line Nozzle Program Status l
As a result of cracking problems occurring with the CRD return line nozzle in BWR reactor vessels, an inspection of the Dresden Unit 3 nozzle was performed during the Fall 1978 refueling outage. As reported in Reference (d), the inspection consisted of an underwater TV camera examination of the thermal sleeve and an external ultrasonic examination of the' inner
, radius and the wall below the nozzle. During the inspection I
the nozzle thermal sleeve retainer ring was found cracked and
+ -
Commonwealth Edison Mr. T. A. Ippolito February 22, 1980 Page 6 the thermal sleeve was subsequently removed. A dye penetrant examination was then performed on the nozzle inner radius and the area below the nozzle. Several linear indications were found all of which were removed by grinding (Reference (d)).
The thermal sleeve was not reinstalled.
An UT of CRD return line welds was also performed. A crack was found on the pipe side heat-affected zone of the pipe to safe-end weld. The section of line between the safe-end and the first 900 elbow including the elbow were replaced.
Data on the CRD nozzle cracking problem has indicated that the cracking found in the BWR vessels has been due to thermal fatigue. A metallurgical analysis of the broken pieces of the retainer ring and the cracked pipe confirmed that thermal fatigue was the failure mechanism. (The same test result occurred when the CRD return nozzle thermal sleeve on 0-2 was analyzed after having been found cracked).
Following the nozzle inspection and repair on Dresden Unit 3, the CRD return line was valved out terminating the 500 -
1000F condensate flow through the return line. Eliminating this cold flow puts an end to the source of thermal cycling which has been determined to be the cracking mechanism.
Based on the above, it is the CECO. position that no further inspection of the CRD return nozzle is warranted.
Cracks that were present wer- removed and the environment that the nozzle will be exposed to will not include the cold condensate flow. However considering the susceptibility of stagnant stainless steel lines to stress corrosion cracking, an augmented inservice inspection will be performed of the stainless steel welds on the reactor vessel side of the inboard valve used for isolation.
Please address any questions you may have concerning this matter to this office.
One (1) signed original and thirty-nine (39) copies of this transmittal are provided for your use.
Very truly yours, i p Robert F. anecek Nuclear Licensing Administrator l
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' 1 Chicago. Ilknois 60690 October 6, 1981 (tel.L)
Mr. Darrell G. Eisenhut., Director Division of Licensing U.S. Nuclear Regulatory Commission Washingt'on, DC- 20555
Subject:
Quad Cities Station Unit 2 Implementation of NUREG-0619 Control Rod Drive Return Line Nozzle Inspections NRC Docket No. 50-265 References'-(a): NUREG-0619, BWR Feedwater Nozzle and Control Rod Drive Return Line Nozzle Cracking, -
November 1980.
(b): R. Janecek letter to D. Eisenhut dated February 23, 1981.
(c): T. Novak letter to J. Abel' dated July 20, 1981.
Dear Mr. Eisenhut:
In Reference (b), Commonwealth Edison provided our plans for resolving the Control Rod Drive (CRD) return line nozzle cracking problem (described in NUREG-0619) at Dresden Station Units 2 and 3 and Quad Cities Station Units 1 and 2. In the case of Quad Cities Station Unit 2, we indicated that during the current (Fall, 1981) refueling outage a leak rate test would be performed on the valve which has been used to isolate the CRD return line. This will provide an indication of whether or not there had been leakage of cold water to the' nozzle. If the test proves that the valve was leaking, a dye penstrant test (PT) of the return line nozzle as specified in NUREG-0619 would again be performed (a PT examination
- was performed previously in the Spring 1978, outage). If the valve oroves to be leak tight, no further nozzle inspections are deemed
~
necessary betause the crack initiating mechanism (cold water) will have been shown to be absent.
In Reference (c), the NRC staff took issue with our position concerning re-inspection of the CRD return line nozzle.
The major concer61 cited was the possibility that crack indications ,
could be discovered in pre'iously v inspected and ground-out areas <
because flaws had been missed by being " buttered-over" during the -
grinding process. It was then concluded that the return line nozzle ,,
should be reinspected prior to our implementation of a two valve leak detection modification on the return line.
r W
D. G. Eisenhut October 6, 1981 The Commonwealth Edison Company response to this concern and to the other issues raised in Reference (c) will be provided for Dresden Units 2 and 3 and Quad Cities Units 1 and 2 within the time frame requested. However, because Quad Cities Unit 2 is currently shutdown for the Fall 1981, refueling outage, our decision and bases for not re-examining the Quad Cities 2 CRD return nozzle is being provided at this time prior to the Reference (c) requested date.
As committed, the leak rate test on the valve isolating the CRD return line was performed during the current Quad Cities Unit 2 re'ueling outage on September 24, 1981. At a test pressure of 25 psig, no leakage was found through valve 2-0301-74. The test pressure was mutually agreed upon by the Station and the NRC Senior Resident Inspector, based upon a normal operating differential pres-sure of approximately 10 psi across the valve, plus an additional margin for conservatism. Because the valve is leak-tight, no further nozzle PT examinations are deemed necessary. Commonwealth Edison strongly believe: that not performing a PT of the nozzle will provide no degredation of safety margins, and that our present and already committed programs are both adequate and responsive to the concerns of NUREG-0619. Further justification of this position is provided below.
- 1. CRD Return Line Nozzle Thermal Sleeve Removal and PT Examination, 1978 Refuel Outage Diligent efforts were taken in 1978 to assure that the CRD return line nozzle was crack-free so that future PT examinations would not be necessary. The maintenance /
modification procedure governing the thermal sleeve removal and PT examination was explicit and thorough concerning the preparation for and conduct of the PT examination, and required Quality Control and Quality Assurance notification prior to proceeding with PT l
indications grinding. The procedure was prepared by a Maintenance person, and approved by the Master Mechanic, Quality Control Supervisor, Technic 91 Staff Supervisor, Q.A. Inspector and the Assistant Superintendent. The Modification was duly approved and authorized by the Station On-Site Review Committee and the Station Nuclear Engineering Department. A 10 CFR 50.59 Safety Evaluation was performed, and it was concluded that no unreviewed safety questions existed. The PT was performed in accordance with the Commonwealth Edison Company Special Process Procedures Manual. A brief description of the removal and examination follows:
- a. The retainer ring attachment weld was ground out.
- b. The retainer, spring washer, and thermal sleeve were removed. The ring remained in place.
l
D. G. Eisenhut October 6, 1981
- c. The nozzle area was cleaned with alcohol, and stainless steel wire brushes. The oxide coating was cleaned from the nozzle.
- d. An initial PT was performed, and 4 non-relevant indications were identified. The indicatons were adjacent to the three nozzle radius thermal sleeve lugs, in the clad portion of the Reactor vessel. The indications were ground out; 2 were to a depth of three-sixteenths of an inch (3/16) and 2 were to a depth of one-sixteenth of an inch (1/16). No grind-outs were deep enough to penetrate into base metal.
All grind-outs were finished with a 4-to-1 blend.
- e. A final PT was performed after flapper wheel preparation, and the results were acceptable. All PT was performed by a CONAM Inspection Level II, and verified and accepted by the Station Quality Control Supervisor.
The extensive cleaning and PT preparation measures that were taken were unique to this job, and simple grinding was not done for PT preparation. It is very unlikely that flaws were missed by being " buttered-over" during the grinding process. Further assurance that the CRD return nozzle is crack free was provided by subsequent direct visual and underwater TV camera inspection described below.
- 2. Direct Visual Examination, 1980 Refuel Outage On February 15, 1980, a direct visual examination of the nozzle revealed no cracking in the nozzle nor in the vessel apron below the nozzle. The inspection was performed by a qualified Level II visual examiner assigned to Station Quality Control Department.
- 3. Underwater TV Camera Inspection, 1981 Refuel Outage On September 17, 1981, a Reactor vessel internals inspection was completed on Unit 2. An underwater television camera was used. After focusing, the camera was used to inspect the CRD Return Line Nozzle (N-9).
There was not evidence of cracking on the nozzle radius or nozzle apron to an area of about 18 inches below the nozzle. The inspection was performed by a qualified Visual Inspector assigned to the Station Quality Control Department, who has had previous experience in this type of inspection.
. j. .
D. G. Eisenhut October 6, 1981
- 4. A nozzle PT in the current refueling outage would require personnel work inside the Unit 2 Reactor vessel at a location where the projected dose rate will be 27 REM per hour. From an ALARA viewpoint and from a personnel safety consideration, this inspection is not justifiable. The risk of potential overexposure also presents itself, should an event such as a power failure to the Reactor Building Crane occur.
- 5. Lowering the water level in the Reactor vessel with the head removed would be necessary in order for the inspectors to be lowered into the Reactor to do the PT.
This would likely be stopping necessary Torus modification and Drywell Hanger outage work on the outage critical path. This is also an undesirable condition from radiological safety and contamination considerations.
- 6. We plan to close both outboard return line valves (2-0301-74 and 2-0301-94) upon startup of Unit 2 follow-ing refueling, and monitor for leakage during subsequent operation. This will provide further redundant assurance that nozzle degradation will not occur.
In addition to the above, the CRD return line piping inside the drywell has been UT examined during the current outage per our Reference (b) response. More information concerning this inspection and other issues raised in Reference (c) will be provided for Dres-den Unit 2 and 3 and Quad Cities Units 1 and 2 in our next response.
In conclusion, Commonwealth Edison strongly believes that the integrity of the Quad Cities Unit 2 CRD return line nozzle and l piping is being maintained, and that inspections performed to date I
have shown no evidence whatsoever to the contrary. We believe a PT of the nozzle to be unnecessary and potentially hazardous from a radiological and personnel safety standpoint.
Please address any questions you may have concerning this matter to this office.
One (1) signed original and thirty-nine (39) copies of this transmittal are provided for your use.
Very truly yours,
^
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Thomas J; Rausch Nuclear Licensing Administrator Boiling Water Reactors l
cc: Region III Inspector - Q.C.
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