IR 05000348/1989012

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Insp Repts 50-348/89-12 & 50-364/89-12 on 890511-0610.No Violations or Deviations Noted.Major Areas Inspected: Operational Safety Verification,Monthly Surveillance Observation,Lers & Design Changes & Mods
ML20246B244
Person / Time
Site: Farley  Southern Nuclear icon.png
Issue date: 06/26/1989
From: Cantrell F, Maxwell G, Miller W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20246B241 List:
References
50-348-89-12, 50-364-89-12, NUDOCS 8907070254
Download: ML20246B244 (11)


Text

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  • h.REr Uh?tTED STATES l'

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. NUCLEAR REGULATORY COMMISSION REGION 11 101 MARIETT A STREET, N.W.

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Report Nos.: 50-348/89-12 and 50-364/89-12 Licensee: Alabama Power Company 600 North 18th Street Birmingham, AL 36291 Docket Nos.: 50-348 and 50-364 License Nos.: NPF-2 and NPF-8 Facility name: Farley 1 and 2 Inspection Conducted: May 11 - June 10, 1989 Inspection at Farley site near Dothan, Alabama Inspectors: [ .

I 4[Mh9 D6te S'igned G." F. Maxwell, Se61pWRpident Inspector Y 4 h/$

W. 'H. ~ Miller, Jr., Res5tM tPinspector 6 l24h/

Da'te Signed Approved by: Adt c[ /,[2C/ff$7 F.S.Cantrell,Section'phlef Date Signed

SUMMAP's

, Scope:

This routine onsite inspection involved a review of operational safety i verification, monthTy surveillance observation, monthly maintenance observation, licensee event reports, design changes and modifications, plant startup from refueling, and proper receipt, storage and handling of emergency diesel fuel oi I Results:

i Within the areas inspected, no violations or deviations were identifie l Certain tours were conducted on deep backshift or weekends, these tours were  !

conducted on May 18, June 2 and 10 (deep backshift inspections occur between

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10 p.m. and 5 a.m.).

The licensee has installed in Unit 2 a N-16 gamma detection system on the main steam lines. This is an enhancement to the plant's leak rate monitoring program and improves ability to detect a steam generator tube lea e90627 PDR O ADOCK 05000348 PDC 4

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l REPORT DETAILS L 1. Licensee Employees Contacted l

R. G. Berryhill, Systems Performance and Planning Manager C. L. Buck, Plant Modification Muager l L. W. Enfinger, Administrative Manager R. D. Hill, Assistant General Manager - Plant Operations

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D. ' N. Morey, General Manager - Farley Nuclear Plant C. D. Nesbitt, Technical Manager J. K. Osterholtz, Operations Manager L. M. Stinson, Assistant General Manager - Plant Support J. J. Thomas, Maintenance Manager L. S. Williams, Training Manager Other licensee employees contacted included, technicians, operations personnel, maintenance and I&C personnel, security force members, and office personne Acronyms and abbreviations used throughout this report are listed in the last paragraph.

l- 2. Plant Status Unit 1 Unit 1 operated at approximately 100% reactor power throughout the reporting perio Unit 2 Unit 2 cycle 6-7 refueling outage continued into this reporting perio The unit returned to power operation on May 2 On May 22 at 10:19 a.m. the reactor tripped due to low-low level in the 2A steam generator. Steam generator feed pump 2A tripped when a loosely connected speed pickup / thrust bearing wear cable was bumped. The unit was returned to power operation on May 22 at 11:34 On May 27 at 9:06 a.m. the reactor tripped due to a turbine generator trip from a ground occurring in the exciter. This resulted in the failure of the No. 9 exciter bearin The unit was returned to power operation at 8:21 p.m.-on May 3 . Operational Safety Verification (71707, 92700) Plant Tours The inspectors conducted routine plant tours during this inspection period to verify that the licensee's requirements and commitments

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were being implemented. Inspec'tions were conducted at various times including week-days, nights, weekends and holidays. These tours were performed to verify that: systems, valves, and breakers required for safe plant operations were in their correct position; fire protection equipment, spare equipment and materials were being maintained and stored properly; plant operators were aware of the current plant status; plant operations personnel were documenting the status of

-- out-of-service equipment; there were no undocumented cases of unusual fluid leaks, piping vibration, abnormal hanger or seismic restraint movements; all reviewed equipment requiring calibration was current; and general housekeeping was satisfactor Tours of the plant included review of site documentation and interviews with plant personnel. The inspectors reviewed the control room operators' logs, tag out logs, chemistry and health physics logs, and control boards and panels. During these tours the inspectors noted that the operators appeared to be alert, aware of changing plant conditions and manipulated plant controls properl The inspectors evaluated operations shift turnovers and attended shift briefing They observed that the briefings and turnover provided sufficient detail for the next shift crew and verified that the staffing met the TS requirement Site security was evaluated-by observing personnel in the protected and vital areas to ensure that these persons had the proper authorization to be in the respective area The inspectors also verified that vital area portals were kept locked and alarmed. The security personnel appeared to be alert.and attentive to their duties and those officers performing personnel and vehicular searches were thorough and systematic. Responses to security alarm conditions appeared to be prompt and adequat Selected activities of the licensee's Radiological Protection Program were reviewed by the inspectors to verify conformance with plant procedures and NRC regulatory requirement. The areas reviewed included: operation and managemer+ of the plant's health physics staff, "ALARA" implementation, hadiation Work Permits (RWPs) for compliance to plant procedures, personnel exposure records, observation of work and personnel in radiation areas to verify compliance to radiation protection procedures, and control of radioactive material I b. Plant Events and Observations (1) Loss of Main Feedwater Flow On May 22 Unit 2 experienced a reactor trip while operating at about l 34% reactor power. The event was reported to the NRC Duty Officer as i required by 10 CFR 50.72. The inspectors evaluated the circumstances ,

l and conditions which existed prior to and following the reactor trip.

l The trip resulted from loss of the "A" steam driven main feedwater

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pump (the B" pump was not running at that time). Loss of this main feedwater' pump allowed steam generator levels to drop to the low-low steam generator reactor trip setpoint. Initial investigation by the i

licensee indicates that the 4iain feedwater pump trip was probably

!. caused by a loose electrical connector associated with the speed l pickup and thrust bearing wear circuit on the turbine end of the pum Housekeeping activities were being conducted in the area near l the loose connector when the pump tripped. It appears that possibly

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someone may have accidentally brushed against the electrical cable which had the loose connector, thus causing an electrical discontinuity to the turbine speed pickup and thrust bearing wear

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circuit; resulting in a pump tri The cable and loose connector l were both tested. 'The tests indicated that the' connector was loose enough to allow circuit discontinuity when the cable was moved. The connector was then properly fastened and the circuit was returned to full servic About an hour after the event occurred the plant was returned to power operation. The licensee documented the event on incident report 2-89-202 in accordance with administrative procedure Ap-30 and is continuing the evaluation.

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(2) Loss of Public Prompt Notification System On May 24, the NRC Duty Officer was notified about a problem which Houston County had experienced with the public notification syste Initially the licensee reported that the off site tone alert radio system was inoperable from 4:00 p.m. on May 23 until 11:45 a.m. on May 24. Further inquiry by the licensee had revealed that this was a mis-communication and that actually the tone alert radio system was probably not inoperable for longer than just a few minutes. Also the licensee reported that from about 1:00 p.m. on May 23 until about 4:00 p.m. on May 24 the off site siren repeater was inoperable, due to damage during a thunderstor The licensee reported the event to the NRC on May 24 at about 11:45 Licensee personnel stated that they were made aware of the inoperable status of the public notification system only minutes before contacting the NRC. The licensee is evaluating the conditions surrounding the notification system inoperable status and the delay by the Houston County officials to promptly report the cond'ition to the license The event was documented by the licensee o'n Incident Report 1-89-201 and is still under evaluatio _

(3) Loose Parts from Unit 2 Turbine Driven Auxiliary Feedwater Pump After performing various startup test following the l! nit 2 refueling outage, the turbine driven auxiliary feedwater pump seized on May 16 due to loose broken metal pieces from the pump diffuser. The pump was disassembled and two fragments from the auxiliary feedwater pump l

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d d diffuser turning vane were not recovere The . fragments were approximately,2 1/4" by 23/32" by 1/4" and 9/16" by 23/32" by 1/4" in

- size and may have entered the discharge piping of the auxiliary feedwater system. The licensee performed evaluations to determine the potential effects of.these loose parts on the feedwater system .

and the.means required to either locate and remove the. loose parts or the results anticipated if the parts could not be located. Procedure 2-EIP-1035, . Turbine. Driven Auxiliary. Feedwater System Flow Test- to Determine Possible Effects from Loose Parts in System,.was issued t perform Eflow tests L and inspect sections . of the ' piping system

- including the flow restrictors for evidence of the loose part However, the. loose parts were not foun Westinghouse performed an evaluation of the problem (Reference No. ES

- 89-1463) and determined-that the presence of these loose objects on the secondary side of the steam generator were not expected to result in an increased probability of a steam generator tube rupture. Also, the safety margin as defined in the TS bases for maintenance of the reactor coolant pressure boundary integrity was not expected to be reduce The inspectors observed the licensee's performance of portions of Procedure 2-ETP-1035 and surveillance tests of the turbine driven auxiliary feedwater pump following repairs. The pump met the TS performance requirements following repairs and the personrel appeared

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to adhere to the inspection 'and test requirements of Procedure

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2-ETP-103 The inspectors also reviewed the ~ evaluations on this problem and had no further questions on this item.

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(4) Loss of Main Turbine Generator Excitation Voltage On May 27 Unit 2 experienced a reactor trip while operating at about 88% reactor power. The-reactor trip resulted from the main turbine generator trippin The turbine trip was caused by loss of excitation voltage for the main generator. The~ licensee evaluated this condition and determined that it appears to have been caused by the number nin>e turbine bearing and the permanent magnet for the exciter becoming excessively hot. This bearing and the exciter permanent magnet were both physically installed on the south end of the main turbine adjacent to the generator excite The inspectors were informed by licensee personnel that the bearing and the exciter permanent magnet became excessively overheated as a result of the static electricity generated while the generator was rotatin The effects of this static charge would not have normally affected the bearing or other adjacent equipment or parts. However, during the most recent Unit 2 outage the main turbine generator had maintenance activities conducted on the exciter end of the generato During that time it appears that an insulator was not installed on one of the bearing lubricating lines which were connected to the number nine bearing. This allowed the static electric'l charge to have a heating affect on the bearing and to the adjacent exciter permanent magne !

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I The bearing and the permanent magnet became damaged by the hea Thus resulting in loss of power to 'the exci cer for the main turbine y generato t i

Following the reactor trip the bearing was replaced, the insulators f were correctly installed on the bearing lubricating lines, the exciter's permanent magnet was repaired, and the turbine generator was returned to servic The licensee reported the event to the NRC Duty Officer and documented it on Incident Report 2-89-203 in accordance with administrative procedure AP-30 and is continuing the evaluatio No violations or deviations were identifie The results of the inspections in this area indicate that the program was effective with respect to meeting the safety objective . Monthly Surveillance Observation (61726)

The inspectors witnessed the licensee conducting maintenance surveillance test activities on safety-related systems and components to verify that the licensee performed the activities in accordance with TS and licensee requirements. These observations included witnessing selected portions of each surveillance, review of the surveillance procedures to ensure that administrative controls and tagging procedures were in force, determining that approval was obtained prior to conducting the surveillance test and the individuals conducting the test were qualified in accordance with plant-approved procedures. Other observations included, ascertaining that test instrumentation used was calibrated, data collected was within the specified requirements of TS, any identified discrepancies were properly noted, and the systems were correctly returned to service. The following specific activities were observed:

2-STP- Full Length Control Rod Operability Test 1-STP- Reactor Coolant System Leak Rate Test 1-STP-1 RHR Pump 1A Quarterly IST 1-STP-22.lfi Turbine Driven Auxiliary Feedwater Pump Quarterly IST 2-STP-22.16 Turbine Driven Auxiliary Feedwater Pump Quarterly IST 2-STP-2 Cycle 7 Shutdown Margin Calculation (TAVG 5470F)

2-50P-37.1C Switching Battery Charger 2B 2-STP-3 Unit 2 Startup TS Verification 2-STP-4 Power Range Functional Test Channel N-44 0-STP-8 Diesel Generator 18 OperebiSity Test 0-STP-8 Diesel Generator 2C Operability Test 2-STP-8 Diesel Generator 2B Operability Test 2-STP-80. bi Diesel Generator "A" Train Loss of Off Site Power Test i

2-STP-80.15 Diesel Generator "B" Train Loss of Off Site Power Test

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0-STP-227.14 Functional Test of Control Room Ventilation Isolation (R-35B)

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Test 2-STP-80.14 conducted May 16 was satisfactory, except the breaker to CCW " swing" pump 2B (breaker BF05) did not close in the test. Pump 2B was aligned to the B train at the time of this test. The licensee checked the jumpers installed for the test to assure correct installation and conducted a retest of this breaker. The breaker closed satisfactorily during the retes The surveillance test of diesel generator 2B on May 15 resulted in an administrative slow start from the use of the air start header No. 2. The diesel started in 10.56 seconds. The maximum TS limit is less than 12 seconds. This engine previously experienced an administrative slow start on the No. I air header during the surveillance conducted on March 15, 1989. Work orders have been issued to investigate and correct the slow start problem . Monthly Maintenance Observation (62703)

The inspectors reviewed the licensee's maintenance activities to verify the following: maintenance personnel were obtaining the appropriate tag out and clearance approvals prior to commencing work activities, correct documentation was available.for all requested parts and material prior to use, procedures were available for all requested parts and material prior to use, procedures were available and adequate. for the work being conducted, maintenance personnel performing work activities were qualified to accomplish these tasks, no maintenance activities reviewed were violating any limiting conditions for operation during the specific evolution, the required QA/QC reviews and QC hold points were implemented, post-maintenance testing activities were completed, and equipment was properly returned to service after the completion of work activitie Activities reviewed included:

MWR 187070 Repair fuel oil leak on No. I cylinder to diesel generator 1 MWR 200040 Disassemble electric motor to circulating water pump 2B, repair oil leak, clean motor and stator and reassembl MWR 2000069 Repair Unit 2 turbine driven auxiliary feedwater pum WA-W00306767 Perform quarterly inspection on diesel generator IB using procedures: MP-1 Diesel Air Start System, and MP-14.6, Model PC2V Dwsel Generator Quarterly Inspectio . Licensee Event Reports (92700, 90714)

The following Lirarsee Event Reports (LERs) were reviewed for potential generic problems to determine trends, to determine whether information included in the reports meet the NRC reporting requirements and to consider whether the corrective action discussed in the reports appear appropriate. The Licensee action was reviewed to verify that the events were reviewed and evaluated by the licensee as required by the technical specifications; that corrective action was taken by the licensee; and that safety limits, limiting sa' ' setting and LCOs were not exceede The

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[ . inspector examined the incident reports, logs and records, and interviewed selected personnel. The following reports are considered closed:

Unit 1 l LER/89-01 Special Report: Fire doors inoperable for more than seven Days l LER/89-02 Special Report: Fire doors inoperable for more than 7 days Unit 2

, *LER/89/01 TS Ac'4cr Statement Requirement Not Met for Inoperative

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Fire N iection System Due to Personnel Error LER/89-02 Special Report: Fire Doors Inoperable For More Th n 7 Days

  • LER/89-04 Containment Integrity Breach Caused By Personnel Error LER/89-05 Personnel Error Causes of Engineered Safety Feature Equipment LER/89-06 Special Report: Containment Hatches Were Non-functional as Fire Barriers For Longer Than 7 Days
  • NOTE: These LERs are closed since violations 348,364/89-07-01 and 348,364/89-11-01 have been issued on these discrepancies. The licensee's corrective actions on these report's and violations will be reviewed during subsequent NRC inspection No violations or deviations were identified. The results of the ,

inspections in this area indicate that the program was effective with respect to meeting the safety objective . Design Changes and Modifications (37828) - Unit 2 The inspectors evaluated two plant design changes which were implemented during this outage for Unit 2. The details for these modifications were described in the control packages for Plant Change Notices (PCN)

B-87-2-3976 and PCN B-88-2-521 PCN B-87-3976 provided the controls and authorization to allow the installation of a new analog / digital total AFW flow indicator on the Unit 2 main control boar PCN B-88-2-5213 authorized the installation of a new radiation monitoring system in Unit 2 main steam valve room to detect possible primary to secondary leak The inspectors noted that the design change packages contained details that considered: 10 CFR 50.59 applicability; safety evaluation; applicable FSAR sections; codes, standards and regulations; and, equipment environmental qualification requirement The design verifications required various design review Each package provided sufficient verification signatures to show that the reviews were conducte The inspectors observed the installed condition of the auxiliary feedwater q total flow indicator and noted that the new meter has been placed into the !

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surveillance test progra The surveillance which are conducted on it are controlled by STP-209.4, Total Flow Loop Q1N23FI3229 Loop Calibratio )

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The new flow control circuit has the capability of providing an input to the plant safety parameter display console syste The inspectors observed parts of the in process installation and the i completed installation of the secondary main steam valve room leak monitoring system. The inspectors were informed that this system is a -

current industry method used for monitoring possible primary to secondary leaks. The system was designed to detect N-16 gamma radiation that would be present in the event of a steam generator tube lea The system detectors are near each of the main steam generator steam headers before the main steam relief valves. A recorder, indicators and annunciators have been provided to alert the control room operators should a leak be detected by this syste No violations or deviations were identified. The installation of the N-16 gamma secondary system leak detection system is considered an enhancement for the plant leak rate monitoring program. This new system will provide the unit with the ability to rapidly assess a steam generator tube lea . Plant Startup From Refueling (71711) - Unit 2 Following the refueling outage the inspectors observed the licensee implementing the various system lineups required by procedure FNP-2-U0P-1.1P, Startup of Unit from Cold Shutdown to Hot Standby and FNP-2-U0P-1.'c , Startup from Hot Standby to Minimum Load, Completed system lineup checklists were evaluated to verify that the restoration program was being implemente The accessible portions of the Unit 2 high head safety injection system were walked down by the inspectors to verify: valves and electrical breakers were in correct alignment, hangers and supports were made up correctly, major components were properly labeled and lubricated, and no visible leakage existe No violations or deviations were identifie The results of the ;

evaluation of the overall restoration program and the walkdown of the high '

head injection system indicates that the licensee's program was effective in this are . Proper Receipt, Storage and Handling of Emergency Diesel Generator Fuel Oil (TI 2515/100)

Temporary Instruction 2515/100 required followup to verify that the licensee has a program in plece to purchase and store fuel oil that meets the requirement of the techni;al specifications. The inspectors reviewed the licensee's diesel fuel oi? receipt and storage program and verified that the licensee: routinely determined the quality of stored fuel oil by scheduled analysis; can detect degradation of stored fuel quality; routinely monitors and cleans filters, strainers and other components

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prone to fouling in the fuel oil system; and reviews and evaluates NRC information on fuel oil problems, i.e., NRC Information Notices and Bulletin In general, the licensee's program was adequate to assure that the fuel oil for the emergency diesel generators met the requirements of the T However, the licensee's program does not include several of the elements addressed in the questionnaire to the temporary instruction. These items were forwarded to NRC Region 11 on May 25,1989 for review. No further followup action on these items is required by the resident inspectors at this tim The residents reviewed a random sample of 19 completed " Certificate of Analysis" on the receipt of diesel fuel oil performed between April 1988 and March 1989. Six of the analyses indicated that the diesel fuel had a heating value less than that specified in the FSAR. FSAR 9.5.4.1 states that the diesel fuel will have a heating value higher than 19,000 Btu /l The deficient sample dates, Btu /lb rating and source from which analyses were taken are as fcllows:

Sample Date Source Description Btu /lb 2-2-89 Vendor truck 125 Tanker 472 18,850 2-2-89 Vendor Truck 80 Tanker 462 18,841 11-30-88 Vendor Truck 72 S-2630-53 18,771

.11-30-88 Vendor Truck 72 S-2630-52 18,814 10-19-88 Vendor Truck 34888 Tanker 2520 18,979 9-21-88 Vendor Truck 80 Tanker 462 18,970 The licensee's preliminary investigation of this finding indicates that in the event of the worst design base accident, which is a dual unit loss of off-site power with a loss of coolant accident in one unit, two large and one small diesel generators will be required. Sufficient fuel will be available from four of the five underground diesel fuel storage tanks to run these three emergency diesels for at least seven days as required by the FSAR. The licensee is continuing the evaluation and stated ir. the exit interview that by August 1, 1989 a copy of any necessary proposed FSAR change with appropriate safety evaluation report will be provided to the resident inspector This is identified as Inspector Followup Item 348,364/89-12-0 No violation were identified in the areas inspecte . Exit Interview The inspection scope and findings were summarized during management interviews throughout the report period and on June 9, with the plant manager and selected members of his staff. The inspection findings were discussed in detail. The licensee acknowledged the inspection findings and did not identify as proprietary any material reviewed by the inspection during this inspection.

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l Licensee was informed that the items discussed in paragraph 6 were close ITEM NUMBER DESCRIPTION AND REFERENCE 348,364/89-12-01 Inspector Followup Item: Further Evaluation-by the Licensee of the Btu /lb Requirements for Emergency Diesel Fuel Oil - Paragraph . Acronyms and Abbreviations j AFW - Auxiliary Feedwater A0P - Abnormal Operating Procedure AP -

Administrative Procedure APC0 - Alabama Power Company CFR - Code of Federal Regulations CCW - Component Cooling Water DC -

Design Change DR -

Deviation Report ECP - Emergency Contingency Procedure EIP - Emergency Plant Implementing Procedure EQ -

Environmental Qualifications ESF -

Engineered Safety Features EWR - Engineering Work Request F -

Fahrenheit GPM -

Gallons Per Minute ISI - Inservice Inspection IST - Inservice Test LCO - Limiting Condition for Operation MOV -

Motor-0perated Valve M0 VATS - Motor-0perated Valve Actuation Testing MWR - Ma'intenance Work Request NCR -

Nonconformance Report #

NRC - Nuclear Regulatory Commission NRR - NRC Office of Nuclear Reactor Regulation PMD - Plant Modifications Department QA - Quality Assurance QC - Quality Control RCP - Radiation Control and Protection Procedure RCS - Reactor Coolant System RHR -

Residual Heat Removal SI - Safety Injection SAER - Safety Audit and Engineering Review S/G - Steam Generator SSPS - Solid State Protection System SOV - Solenoid Operated Valve STP -

Surveillance Test Procedure

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Service Water TS - Technical Specification TSC - Technical Support Center i WA -

Work Authorization j

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