ML20236J702

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Insp Repts 50-348/98-03 & 50-364/98-03 on 980412-0530.No Violations Noted.Major Areas Inspected:Licensee Operations, Engineering,Maint & Plant Support
ML20236J702
Person / Time
Site: Farley  Southern Nuclear icon.png
Issue date: 07/01/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20236J684 List:
References
50-348-98-03, 50-348-98-3, 50-364-98-03, 50-364-98-3, NUDOCS 9807080315
Download: ML20236J702 (49)


See also: IR 05000348/1998003

Text

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l U.S. NUCLEAR REGULATORY COMMISSION (NRC)

i REGION II

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Docket Nos: 50-348 and 50-364

License Nos: NPF-2 and NPF-8

Report No: 50-348/98-03 and 50-364/98-03

Licensee: Southern Nuclear Operating Company (SNC)

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. Facility: Farley Nuclear Plant (FNP). Units 1 and 2

Location: 7388 North State Highway 95

Columbia. AL.36319

Dates: April 12 through May 30. 1998

Inspectors: T. Ross. Senior Resident Inspector

J. Bartley Resid?nt Inspector

R. Caldwell Resident Inspector

J. Zimmerman. NRR Project Manager

W. Kleinsorge. Senior Reactor Inspector

(Section M1.5)

G. Kuzo. Senior Radiation Specialist

(Sections'R1. R2. R3 R7 and R8)

L. Stratton. Physical Security Specialist

(Sections S2. S3. 54, and S8)

W. Sartor. Senior Radiation Specialist

(Sections P2. P3. P5. P6 P7. and P8)

J. Kreh. Radiation Specialist (Sections P2. P3.

P5. P6. P7. and P8)

Approved by: L. R. Plisco.. Director

Division of Reactor Projects

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Enclosure 2

9907090315 990701 .

PDR ADOCK 05000349  !

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I Notice of Violation 3

The NRC has concluded that information regarding the reason for Violation C.

! the corrective actions taken'and planned to correct the violation and prevent

l- recurrence and the date when full compliance was achieved is already

l adequately addressed on the docket in LER 97-10-01. However.-you are required

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to submit a written statement or explanation pursuant to-10 CFR 2.201 if the

description therein does not accurately reflect your. corrective actions or

, your position. In that- case, or.if you choose to respond. clearly-mark your i

response as a." Reply to a. Notice of Violation.'" and send it to the U.S.

Nuclear Regulatory Commission. ATTN: Document Control Desk. Washington. D.C.

-20555 with a copy to the-Regional Administrator. Region II and a copy to the

NRC. Resident Inspector at the Farley Nuclear Plant within 30 days of the date

of:the letter transmitting.this Notice of Violation (Notice).

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If you contest this enforcement action, you should also provide a copy of your 1

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response-to the Director. Office of Enforcement. United States Nuclear-

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Regulatory Commission. Washington DC 20555-0001.

Because your res)onse will be placed in the NRC Public Document Room-(PDR). to

the extent- possi ale, it should not include any' personal privacy. 3roprietary. 4

- or safeguards information so that it can be placed in the PDR wit 1out

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i. redaction. However. if you find it necessary to include such information, you

should clearly indicate the specific information that you desire not to be

placed in the PDR. and provide the legal basis to support your request for

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withholding the information from the public.

Dated at Atlanta, Georgia

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this 1st day of' July 1998

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Enclosure 1

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EXECUTIVE SUMMARY

l Farley Nuclear Power Plant. Units 1 and 2

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NRC Inspection Report 50-348/98-03. 50-364/98-03 l

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This integrated inspection included aspects of licensee operations.

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engineering. maintenance, and plant support. The report covers a 7-week

period of onsite resident inspector inspection and announced inspections by

regional inspectors.

Operations

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e Control Room professionalism and communications remained good. l

Operating crew demeanor, team work and conduct were professional and  !

effective. Operator attentiveness to Main Control Board (MCB) i

annunciator alarms and response to changing plant conditions were  ;

prompt. The operating crew consistently demonstrated a high level of '

awareness of existing plant conditions and ongoing plant activities.

(Section 01.1)

e The inspectors concluded that the licensee adequately prepared for and

then satisfactorily conducted Unit 2 midloop operations. (Section 01.3)

e The Unit 2 cycle 13 initial approach to criticality and restart were

well-briefed. deliberate, and conservative. The reactor core performed

within its design parameters. (Sections 01.5 and 01.6)

e The Unit 2 power ascension for Cycle 13. following the )ower uprate, was

conducted in a safe and controlled manner. The unit aclieved full power

without a significant personnel incident or equipment problem.

(Section 01.7)

Maintenance

o Maintenance and surveillance testing activities were generally conducted

in a thorough and competent manner by qualified individuals in

accordance with plant procedures and work instructions. Close

coordination was maintained with the main control room during

surveillance testing activities. (Section M1.1)

e The corrective actions for the March 28 and May 12 rod drop events were

not thorough, but the corrective actions follcwing the May 15. 1998

event appeared to be comprehensive and effective, pending completion of

the licensee's root cause determination. (Section M1.4) '

e A non-cited violation was identified for the licensee's failure to

report a manual reactor trip in a timely manner. (Section M1.4)

e Inservice Inspection (ISI) activities were conducted in accordance with

procedures and regulatory requirements. (Section M1.5)

Enclosure 2

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e The Inservice Inspection / Nondestructive Examination (ISI/NDE) program

lacked procedure qualification of high temperature liquid penetrant

examination. (Section M1.5)

Enaineerina l

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e The inspectors concluded that the licensee had established suitable

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programmatic guidance to ensure that the regulatory requirements of

10 CFR 50.59 would be met by the various onsite and offsite  ;

organizations. However, the inspectors did identify several

programmatic deficiencies and inconsistencies. Training of safety

evaluation preparers and reviewers was adequate. (Section E1.1)

e Changes, tests and experiments were properly screened for 10 CFR 50.59  !

applicability, and adequately evaluated to ensure an unreviewed safety

question (US0) did not exist. Personnel preparing and reviewing safety

evaluatinos were qualified. However, the documentation that addressed

the US0 criteria in several safety evaluations lacked specificity and I

thoroughness. Furthermore, very few of the safety evaluation forms

provided any direct evidence of a cross-disciplinary review.

(Section El.1)

e A violation was issued to the licensee because the original safety

assessment for LER 97-10 was inadequate. In addition, the ability to l

safely shutdown and cooldown the plant from the HSDP was determined to l

have been in a degraded condition for about 12 years. This issue

remains under NRC review and was identified as an apparent violation.

(Section E8.1)

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e A violation of 10 CFR Part 50. Appendix B. Criterion XVI. Corrective  ;

Action was identified. The licensee identified three conditions adverse '

to quality of Control Room Ventilation System Functional System Design ,

(FSD) Open Items, which were either inadvertently or inappropriately 1

closed and not corrected. (Section E8.5)

Plant Suonort

e A weakness in exposure controls and poor communications contributed to

the licensee exceeding its budgeted dose for the removal of Tri-Nuclear

equipment and filters from the U2 lower reactor cavity due. '

(Section R1.1)

e For U2 Refueling Outage 12 (U2RF12) activities, dose ex

exceeded original estimates due to expanded work scope,penditure

unexpected

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Residual Heat Removal (RHR) system maintenance problems, and elevated U2 -

Spent Fuel Pool dose rates. (Section R1.2)  !

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e Worker Shallow Dose Equivalent (SDE) exposures resulting from personnel;

contamination events and work activities during the U2RF12 activities

were evaluated properly and were.within 10 CFR 20.1201 linits.

'(Section R1.2)

e Controls for minimizing workers' internal exposure during U2RF12

activities were effective. (Section R1.3)

e Respiratory protection training, fit tests, medical qualifications, and

equipment status met 10 CFR 20.1703 requirements. (Section R1.4)

e Plant personnel observed working in the radiologically-controlled area

(RCA) generally demonstrated appropriate knowledge and application of

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radiological control practices. (Section R2.1)

e The evaluated Radiation Monitor System (RMS) equipment was installed

properly and the reviewed detector calibrations and functional tests

were conducted in accordance with and met procedural. 10 CFR Part 20.

and Offsite Dose Calculation Manual (0DCM) requirements. (Section R2.2)

-e For 1997. program activities to control. monitor and document liquid and

airborne radionuclides concentrations in effluents and in the offsite

. environment were implemented effectively. No significant environmental

impact was identified. Projected. offsite doses to the maximally exposed

individual were a small fraction of ODCM and'40 CFR 290 specified j

limits. (Section R3.1)

e Extensive delays in returning a community particulate air sampler to

service and lack of corrective actions to prevent recurrence was

~ identified as 'a program weakness. (Section R3.1)

'e The licensee Health Physics (HP) and Dosimetry (DOS) observation program

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continued to be im)lemented effectively and contributed to the reduced

personnel errors o) served for U2RF12 activities. (Section R7.1)

e. Emer :y Response Facilities (ERFs) were well-equipped and

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opf ct onally ready to support an emergency response. Emergency

respuose personnel were adequately trained and responded appropriately

to a scheduled drill. (Sections P2.1 and P5.1)

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.e . Changes to the Emergency Plan were made in accordance with

L 10 CFR 50.54(q). The emergency declaration on March 8. 1998. was made

'in accordance with the. Emergency Plan. (Section P3.1)

e~ The 1996 and 1997 Emergency. Preparedness'(EP) program audits met the

10 CFR 50.54(t) requirement for an annual independent audit of the EP

. prc; ram. (Section P7.1)

Enclosure 2

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e Security personn ? activities observed during the inspection period were

performed well. . te security systems and barriers were adequate to

ensure physical p;stection of the plant and complied with the Physical i

Security Plan. (Section S1.1)  !

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e The failure to include a documented process in access control procedures l

for contractors to timely inform the Security Department of terminated

individuals contributed to a violation for failuce follow procedure to l

immediately terminate eight individuals' unescorted access.

(Section S2.1)

e The licensee had in place a sound strategy that was capable of l

protecting vital equipment from acts intended to cause a significant  :

release of radioactivity. (Section S4.1)  !

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Enclosure 2

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ReDort Details

Summary of Plant Status.

Unit 1 operated continuously at 100% rated thermal power (RTP) for the entire

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inspection period, with the exccption of several hours on May 21, when power

} was reduced to approximately 65%. due to a Steam Generator Feedwater Pump

L trip. The unit reached 360 days of continuous operation as of May 30,

surpassing the previous Unit 1 record of 357 continuous power' operation days.

Unit 2 was.in a refueling outage for most' of the inspection period. On

. May 15. operators attempted to restart Unit 2. However, the unit was manually

tripped due to a:dro ped rod. After making repairs- Unit 2 was returned to

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criticality on May 1 . The unit achieved 100% RTP on May 24 and continued to

operate at this level through the end of the. inspection period.

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I. Operations

101 Conduct'of Operations l

01'.1 Routine Observations of Control Room Ooerations (71707 and 40500)

Following the guidance provided in Inspection Procedures (IPs) 71707 and

40500, the inspectors conducted frequent inspections of routine plant

operations.

The inspectors observed that control room professionalism and

communications remained good. Operating crew demeanor, team work-and

conduct were professional'and effective. Operator attentiveness to Main-

Control Board (MCB) annunciator alarms and response to changing plant

. conditions were prompt. The operating crew consistently demonstrated a

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high level of awareness of. existing plant conditions and ongoing plant i

activities.

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The inspectors routinely reviewed the. Technical Specification (TS) y

Limiting Conditions for Operation (LCO) tracking sheets filled out by j

the Shift Foreman (SF). All tracking sheets for Units 1 and 2 reviewed {

by the inspectors were consistent with plant conditions and TS '

requirements. .

01.2._ Unit 2 Refuelina (60710) j

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The resident inspectors observed Unit 2 refueling activities from the j

Main Control Room (MCR)'and containment on April 27, 1998. .The  !

,,' refueling was conducted in accordance with FP-APR-R12. " Refueling .)

~ Procedure J.M. Farley Unit 2. Cycle XII - XIII Refueling." Revision  !

(Rev.) 0. Refueling activities observed were~ performed in a i

y well-controlled and methodical manner in accordance with procedures. '

Communications between the various stations were clear and concise.

Personnel.were familiar with the procedure ~and knowledgeable of the

process and systems. No significant incidents occurred during_ fuel _

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. handling and all observed fuel a'semblies s were landed in their

' appropriate locations. The inspector concluded that fuel handling was

accomplished in a professional and competent manner.

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01.3 Unit 2 Mid-loco Doerations

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'a, Insoection Scooe (71707)-

The inspectors observed licensee preparations _ for establishing midloop

conditions on Unit'2 in accordance with FNP-2-UDP-4.3. "Mid-loop

Operations." Rev.'8. .The ins)ector reviewed FNP-2-UOP-4.3.

FNP-2-STP-18.4. " Containment iid-Loop and/or Refueling Integrity

Verification and Containment Closure." Rev.17. and. Generic Letter .

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88-17, " Loss of Decay Heat Removal." and verified selected portions of

.FNP-2-UOP-4.3. Section 2.0. Initial Conditions. The inspectors also

performed MCR observations during midloop conditions to verify

compliance with FNP-2-UOP-4.3.

b. Observations a Findinas

The inspectors interviewed Operations and Training supervisors and

determined that the operating crews.had been.provided basic midloop

training during the first training cycle.- In addition, the crew

scheduled to' initiate mid-loop conditions was to receive a detailed

pre-evolution briefi.ng prior.to going into mid-loop operations.

The inspectors reviewed several procedures that were needed for mid-loop

operation and found them to contain adecuate information and appropriate

detail to satisfy the concerns expressec in Generic Letter 88-17.

The inspectors observed MCR operations during mid-loop conditions that

were established and maintained from May 3 through May 5. All required

reactor vessel level indications were functioning properly and closely

monitored by the operators. No significant problems were identified by

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the inspectors.

c. Conclusions

The inspectors concluded that the licensee adequately prepared for and

then satisfactorily conducted Unit 2 mid-loop operations.

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01.4' Unit 2 Preparation'For Startuo and Mode Chanaes

The' inspectors periodically reviewed FNP-0-SOP-103 " Return to Service

' Checklist." Rev.10. and verified that mode-specific' lists were

up-to-date and complete. The inspectors verified that appropriate .

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'signoffs and reviews were completed for each mode change evolution.

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Enclosure 2

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01.5L Unit'2 Startuo and Initial Criticality

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I a. Insoection Scoce (71711r

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L The inspectors observed initial criticality of Unit 2 for Cycle 13 and

the commencement of zero power' physics testing. The inspectors also

observed thel pre-evolution briefing,

b. Observations and Findinos

On May'15. the inspectors attended the pre-evolution' briefing for Unit 2

Cycle 12 initial criticality and . low power physics testing. Because

L this ~was an infrequently performed evolution, the Engineering Support .

! (ES) manager and test coordinator (i.e. nuclear engineer) conducted the

L . briefing per FNP-0-AP-92. " Infrequently Performed Tests and Evolutions."

Rev: 3. The briefing was attended by all affected parties and was

comprehensive.

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Unit 2 entered Mode 2 on May 15. when' operators began to wittidraw the

control rod shutdown banks. ~An inspector monitored the aaproach to

criticality during withdrawal of the control banks and su) sequent

. Reactor Coolant. System (RCS) boron dilution. .The inspectors verified

.that the-startup was performed in accordance with FNP-2-U0P-1.2.

"Startup of-Unit From Hot-Standby To. Minimum Load." Rev. 39, and

.FNP-2-STP-101. "Zero Power Reactor Physics Testing." Rev. O.

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The' approach to criticality was conducted in a slow, deliberate manner

in strict compliance with procedural instructions. Criticality was

!- achieved within expected bounds of the estimated critical concentration

.~(ECC) and predicted quantity of makeup water needed to dilute the RCS.

All reactivity alterations were precisely controlled and directly-

communicated .to the shift supervisor (SS) prior to implementing any

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^change. The inverse count rate ratio (ICRR) was plotted methodically

l during the entire evolution and reflected control over reactor

reactivity conditions by Operations and ES personnel. Overall. the

Cycle 12 approach to criticality was performed well.

Later that evening during the dynamic rod worth measurement on control

bank *D' with reactor power below the point of adding heat, control rod I

, F10 dropped into the core from approximately 216 ste)s. Operators

manually tripped the reactor and carried out applica)le emergency

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operating procedures. A blown fuse was found on the movable gripper for-

rod F10. The licensee promptly notified the NRC of this event pursuant

to 10 CFR 50.72_(b)(2)(ii). This was the third rod drop event for

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Unitf2 since March 28-(see Section M1.4).

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c. Conclusions

The Unit.2. Cycle 13 initial approach to criticality was all

pre-briefed. deliberate and conservative. The reactor core performed

.within its design parameters.

01.6 Unit 2' Restart and-Low Power Physics Testina

a. Insoection Scoce (71711)

On.May 17. the inspectors observed operators return the reactor to a

critical condition'by-pulling rods and continuing with low power physics.

testing.

b. ' Observations and Findinas

On May 17. after completing repairs to the rod control power cabinets

(see Section M1.4). o)erators recommenced Unit 2 restart. An inspector

monitored the approac1 to criticality during withdrawal of.the control

banks in accordance with FNP-2-UOP-1.2. "Startup of Unit From Hot-

Standby To Minimum Load." Rev. 39. and FNP-2-STP-101. "Zero Power

Reactor Physics. Testing." Rev. O.

The approach to criticality was conducted in a slow, deliberate manner

in strict compliance with procedural instructions. Criticality was

achieved within the expected bounds of the estimated critical position-

(ECP). All reactivity alterations were precisely controlled and

directly communicated to the SS prior'to implementing any change. The

inverse count rate ratio (ICRR) was plotted methodically during the

entire evolution and reflected positive control .over reactor reactivity

conditions by Operations and ES personnel.

, c. Conclu~sions.

Overall. the Unit 2 Cycle 13 restart was well-controlled and the reactor

core responded ~within design expectations.

01.'7 Unit 2 Power Ascension

a.' Insoection Scooe (71707)

From May 17.through 22.~ the inspectors observed portions of the Unit-2

power ascension and operations, as conducted by associated operating

crews in accordance with FNP-2-UOP-3.1. " Power Operations." Rev 38.

g and FNP-2-ETP-4441. " Power Ascension Following Unit U) rate." Rev. O. In

H addition..the inspectors observed FNP-2-IMP-228,11. ~ils Power Range

Channel N44 Current Rescale." Rev. 18. and portions of FNP-2-ETP-4440.

" Steam Generator Water Level Control Test." Rev. O. at the 33%. power

plateau.

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b. Observations and Findinos

The main generator was synchronized to the grid on May 18 and achieved

full. power.on May 24. The Unit 2 power ascension and power operations

were well-controlled and consistent with FNP-2-U0P-3.1 and

FNP-2-ETP-4441 guidance. FNP-2-IMP-228.11 and FNP-2-ETP-4440 were

conducted in a controlled.. step-by-step manner and completed

1 ' satisfactorily.

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c. Conclusions

-The Unit 2 power ascension for Cycle 13. following the power uprate, was

conducted in'a safe and controlled manner. The unit achieved full

power without a significant personnel incident or equipment problem.

02 Operational Status of Facilities and Equipment

02.1 General Tours of Soecific-Safety-Related Areas-(71707)

related areas were performed by the inspectors

General

to observetours of safety condition of plant equipment and structures, and

the physica

to verify that' safety systems were properly maintained and aligned.

Overall material' conditions for Unit 1 and Unit 2 structures systems.

- and. components (E~3) were good, and safety-related system appeared to

be properly aligne1. Minor ecuipment and housekeeping problems

identified by the -inspectors curing their routine tours were reported to

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the responsible 5S anFor maintenarice department for resolution.

02.2 Inspections of Safety ,vstems (71707)

InsSectors walked down the newly installed Unit 2 Trisodium Phosphate

Bascets and recently repaired emergency core cooling system (ECCS)-

containment sump screens to verify operability. Accessible portions of

these safety-related system components were verified to be adequately.

installed and in good cperating condition. The inspectors did not

identify any issues that adversely affected component operability.

02.3' Unit 2 Conta' inment Closecut Walkdown (71707)

.0n May 14. the inspectors toured the inside of Unit 2 containment

shortly after entry into Mode 3. 'The inspectors identified a slight

amount of debris which was removed prior-to unit startup. A few minor

leaks and housekeeping problems were reported to the Unit 2 SS for

action. Overall. the licensee did an adequate.' job in cleaning and

clearing out the containment.

Enclosure 2

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02.4 Verification of Safety Taaaina (71707)

The inspectors verified that selected tagouts were implemented in

accordance with procedural requirements. The inspectors reviewed and

walked down selected devices tagged by the following tag orders (TOs):

e 98-0242-1.1C Coolant Charging Pump Auxiliary Lube Oil Cooling

Pump

e 98-1186-2. 2C Battery Charger

e 93-1843-2. Spent resin sluice pump

e 97-2742-2. Containment Spray Addition Tank

e 98-0467-2. Lower Equipment Room Air Handling Unit

e 97-2458-2. Turbine Driven Auxiliary Feedwater Pump

The inspectors verified that devices identified on the Tag Orders (TOs)

were properly tagged and that the administrative aspects of filling out

the tagging order forms were complete and correct.

The inspectors concluded that the reviewed safety tagging activities

were correct and met the procedural requirements for personnel safety

and equipment protection.

05 Operator Training and Qualification

05.1 Unit 2 Power Vorate License Condition Trainina

On April 29. the NRC issued Amendment No.137 to Facility Operating

License (FDL) No. NPF-2 and Amendment No. 129 to FOL No. NRF-8 for FNP.

Units 1 and 2. respectively. These license amendments authorized SNC to

operate both units of FNP at reactor power levels up to 2775

megawatts-thermal (MWt), which was a power increase from the original

license limit of 2652 Mwt. As part of the license amendments, the NRC

approved certain new license conditions, one of which was that SNC shall

complete classroom and simulator training regarding power uprate for

operations crews on both units prior to the Unit 2 restart (i.e. , before

entering Mode 2) from U2RF12. The Unit 1 reference simulator was also

to be temporarily modified to accommodate the training. On May 5. an

inspector interviewed responsible training instructors and management to

discuss the conduct of operator training pursuant to the new license

conditions.

The inspector reviewed training lesson plan OPS-56202A " Power Uprate."

which addressed power uprate changes to: 1) System and Control

Setpoints. 2) Technical Specifications. 3) Emergency Procedures, and 4)

Accident Analysis.' The inspector also reviewed applicable training

attendance sheets to verify operator attendance for classroom and l

simulator training. Classroom training was held for all licensed

reactor operators (RO).and senior reactor operators (SRO) during January

through April 1998. Simulator training was conducted for the operating

crews between April 22 and May 6,1998. Based upon the interviews and

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document reviews, the ins)ector concluded that the Appendix C license

conditions of Amendments 90s. 137 and 129. which required operator

training prior to Unit 2 restart, were satisfactorily fulfilled.

061 Operations Organization and Administration

I 06.1. Peer Review by World Association of Nuclear Ooerators (WANO) (71707 and i

L- -40500)

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The-inspectors reviewed the Final Report of the "WAN0 Peer Review of

c- Farley Nuclear Plant." conducted onsite during the month of July 1997.

F The inspectors' review of the Interim Report dated September 16. 1997,

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was documented =in inspection report.50-348, 364/97-14. After reviewing

l the. Final Report, the inspector concluded that there were no new safety

,. issues identified which would require NRC follow-up action or.

L reassessment of NRC perspectives regarding licensee performance.

08 Miscellaneous Operations Issues

-08.1Emolovee Concerns Proaram

a. Insoection Scooe (40500) I

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The inspectors performed a review of a sample of Employee Concerns

Program (ECP) files.

b. Observations and Findinas

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The licensee recently dedicated a full-time Jerson to serve as ECP

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' Coordinator to process employee concerns T11s individual was a Shift

Foreman and holds a Senior Reactor Operator (SRO) license. This i

individual has recently begun actively advertising the plant ECP and {

encouraging: people to submit concerns. l

The total concerns for'1995. 1996, and 1997 were 5' Concerns for 1998

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year to date totaled 30. A review of all. ECP packages for 1995. 1996..

and 1997-and 4 ECP packages for 1998 found two that had followup

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commitments. However there was no documentation indicating that these

commitments were. completed.  !

~ 0re concern stated that there were no searches of individuals entering

or exiting the contractor Jarking area. Security had committed to l

review their. procedures. )ue to communications problems, security. '

reviewed the entrance / exit procedures for the wrong area. Consequently.

no actions were taken. ECP 3ersonnel acknowledged the error-when the

inspectors questioned them a)out the dis)osition of this concern. Upon

~

o subsequent' review.. the -licensee stated tlat no actions were recuired

l because searches were conducted prior to entering the protectec area. ,

J A1.so, the licensee had independently implemented random exit searches. '

Enclosure 2 .

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i

The other concern was associated with inconsistent verification of

. controlled. leakage when swapping a charging pump. The licensee had

committed to change the Unit Operating Procedures (UOPs) and the System

~0perating Procedures (SOPS). This commitment was to be entered into an

informal tracking system.for procedure enhancements. The 50P changes

.were entered into the tracking system and incorporated, but the UDP

= changes were not entered. Consequently, these changes were not made.

However, the. licensee planned to incorporate the changes during the next )

revision cycle of the procedure.

c. Conclusions

There has been a significant increase in usage of the Employee Concerns

Program during 1998. For the ECP packages reviewed, one commitment was

not entered into the tracking system.

,3

II. Maintenance

M1 Conduct of Maintenance

M1.1 Maintenance and Surveillance Testina Activities (61726 and 62707)

Using the guidance provided in IP 61726 and IP 62707 the. inspectors

observed and-reviewed portions of selected licensee corrective and

preventive maintenance activities, and routine surveillance testing

including detailed reviews of the following:

"o FNP-2-STP-40.0, " Safety Injection with Loss of Off-Site Power

Test." Rev. 29

'e FNP-2-STP-40.3, " Phase A Isolation Test," Rev. 1

e WA485614. Replace 1A Condensate Pump bearing

e FNP-1-STP-109.1, " Power Range Neutron Flux Channel Calibration "

Rev. 10

e FNP-0-MP-7.3. " Turbine Driven Auxiliary Feedwater Pump Overspeed

Trip Setpoint Checks," Rev. 4

During the observation of FNP-0-MP-7.3, the inspectors noted several

. . unsuccessful attempts to perform the maintenance. Mechanics were unable  !

to adjust the Turbine-Driven Auxiliary Feed Water. (TDAFW) overs)eed trip '

setpoint within the required tolerances. The source of the pro)lem was

p narrowed down to non-equivalent parts that were replaced on the

overspeed trip mechanism during the Unit 2 Refueling Outage 12 (U2RF12).

The licensee. in consultation with the vendor. concluded that a part of

l. the overspeed_ device was " custom fit" at the factory and that the off-

L :the-shelf component would not work. The licensee determined that the

entire overspeed device would be purchased and factory tested in the

future. After the original parts were put back into the overspeed trip

mechanism, a successful test was accomplished the following day.  ;

Enclosure 2

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_mi_._____ __-.____i___--_______----- - - _ -

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7

9

'Other observed maintenance work activities and surveillance testing were

performed in accordance with work instructions, procedures, and

applicable clearance controls. Safety-related maintenance and

surveillance testing evolutions were properly planned and executed.

. Licensee personnel demonstrated familiarity with administrative and

radiological controls, Surveillance tests of safety-related equipment

were consistently performed in a deliberate manner in close

. communication with the Main Control Room (MCR). Overall, operators,

technicians and craftsman were observed to be knowledgeable,

experienced, and trained for the tasks performed.

M1.2 Unit 2 Safety In.iection with Loss Of Offsite Power Test

The inspectors observed the preparations for and performance of

FNP-2-STP-40.0, ~ ~ Safety Injection with Loss of Off-Site Power 1st,"

.Rev. 29C, on April 25. The inspectors also observed portions of the

-follow-up testing on April 29. and reviewed the completed test package.

The test was satisfactorily completed with the exception of five valves,

inadvertently omitted due to personnel error, and several relatively

minor exceptions, which were noted and rescheduled.' While recording

' post-test. component']ositions, the licensee identified that five valves

.were not placed in tie required pre-test alignment because.the operator

performing the pretest, lineup ~ missed page 5 of Table 2. The licensee

' initiated.0ccurrence Report (OR) 2-98-162 to evaluate this occurrence.

These. valves, and the known test exceptions. were retested on April 29.

L The inspectors observed the retest and verified that all exceptions from

.the. initial test were included. The test and retests adequately

. verified SI operation with a loss of offsite power.

M1.3 Residual Heat Removal-(RHR) Heat Exchancer head Gasket Replacement

Theilicensee replaced the RHR heat exchanger (HX) head gaskets, under

.

Work Orders (W0s) M00203005 and M00168359. to eliminate small borated

l' water leaks. The job was complicated when seven of the studs which were

threaded through the tube sheet stuck and had to be cut out with

specialized equipment. This significantly delayed completion of work

and resulted in the dose for the job being almost double the budgeted

dose.

'

On May 1. a contractor noted that some of the. studs (one on each HX

l- endbell and multiple studs on the inlet and outlet flanges) did not have

complete thread engagement with the nuts. In most cases, only one or

l two threads were not: engaged. -The American Society of Mechanical

Engineers-(ASME) Code required full thread engagement. The condition

'

L

was missed by the craftsmen. the craftsmen's supervision, and inspection

personnel. The licensee issued OR 2-98-171. evaluated the condition'for

. current plant conditions initiated a formal root cause investigation,

and. installed longer studs where needed for full thread engagement.

' Based on initial calculations, the licensee determined that for the

Enclosure 2

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6

10

current plant conditions (i.e. Modes 5 and 6). the RHR HXs would meet

their intended function with the as-found thread engagement. Therefore,

based on having adequate bolt strength but not meeting the ASME Code,

the licensee considered this to be a degraded but operable condition.

On May 4. an inspector walked down other systems to determine if

'

inadequate thread engagement was a problem on other safety-related

systems. The inspector identified limited examples of potentially

inadequate thread engagement on the 1A Containment Spray pump supply and

discharge flanges.1C CCP discharge flange. and the 2B RHR pump casing.

After the walkdown, the inspector asked the Plant Modifications and

Maintenance Sup) ort (PMMS) manager if licensee 3ersonnel planned to

walkdown any otler safety-related systems for taread engagement

discrepancies. The manager stated that no further system walkdowns were

planned but that he would discuss the issue with senior plant

management. The inspector then presented his walkdown findings to the

licensee for resolution. On May S. the licensee commenced walkdowns to

identify thread engagement problems on other safety-related systems.

Based on the initial calculations for the RHR HX thread engagement and

the as-designed safety margins the inspector concluded that this was

not a significant safety concern. This issue is identified as

IFI 50-348. 364/98-03-01. Inadequate Thread Engagement, pending

inspector review of the licensee's walkdown results and evaluations.

M1.4 Drooned Rod Durina Rod Doerability Testina

a. Jnsoection Scooe (62707)

Inspectors observed control rod troubleshooting and reviewed the

applicable occurrence reports and Licensee Event Report (LER).

associated with the dropped control rods.

b. Observations and Findinas

On Nay 12. control rod K-2 (control bank A) was dropped during rod

operability testing. This was the same rod that dropped on March 28

during a scheduled Unit 2 refueling outage shutdown (refer to IR 98-02)

when a fuse associated with the stationary gripper coil blew. At that

time. the licensee's troubleshooting concluded that there was an

intermittent problem in the rod control power cable that crossed from

the reactor cavity to the reactor head. The suspected cables were

replaced during the outage. However, for the May 12th event, a fuse

associated with the movable gripper was found to be blown. In both

cases, operators manually tripped the subcritical reactor. The licensee

suspended further control rod operability testing and commenced

troubleshooting to identify the problem. Licensee personnel

subsequently concluded that the movable gripper coil fuse had

experienced a late failure due to the prior overcurrent condition that

blew the stationary gripper coil fuse. Maintenance replaced the movable

gripper coil fuse and exercised the bank several times.

Enclosure 2

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11

Following replacement of the fuse, the inspectors observed Instrument

and Control troubleshooting activities (e.g., electrical power current

traces) of each control rod while operators exercised applicable banks.

The. licensee did not report the May 12 event t'o the NRC until May 15.

Failure to re

by 10 CFR 50. port the manual

/2(b)(2)(ii) reactor

constituted trip withinThis

a violation. four non-repetitive.

hours as required

licensee-identified and corrected violation is being treated as a

Non-Cited Violation (NCV). consistent with Section VII.B.1 of the NRC

Enforcement Policy. This is identified as NCV 50-364/98-03-02. Failure

to Report-Manual Reactor Trip in a Timely Manner.

On May 15, another control rod dropped during zero power physics testing

(see Section 01.5). The licensee's NSSS supplier reviewed the event. A

potential concern was identified regarding suitability of fuse types for

the Control Rod Drive Motor Generator sets and the control rod system.

The licensee had on occasion installed a different type of fuse than-

recommended by the vendor, considered to be equivalent by the licensee.

All of the Unit 2 control rod drive fuses (approximately 160) were

.

replaced with the vendor's recommended fuses and the reactor was

restarted. The inspectors will continue to review the root cause

determinations and the associated LERs. The licensee's corrective

actions. appeared to have been successful and the repetitive dropped rod  ;

. problem corrected..pending results of'the on-going Root Cause

Investigation.

c. Conclusions

The corrective actions for the March 28 and May 12 rod drop events were

L

'-

not thorough, but the; corrective actions following the May 15. 1998

event appeared to be comprehensive, pending completion of the licensee's

-root cause determination.

.

A non-cited violation was identified for the licensee's failure to

report a manual reactor trip in'a timely manner.

M1.5- ' Inservice Insoection Unit 2

a. Insoection Scooe (73753)

To evaluate the' licensee's inservice inspection (ISI) program and the 1

. program's implementation ~. the inspectors reviewed procedures observed

work in progress, and reviewed selected records. Observations were i

' compared with applicable procedures the Updated Final Safety Analysis i

Report (UFSAR) and ASME B&PV Code Sections V'and XI, 1989 Edition. No

. Addenda (89NA). l

,

Enclosure 2 'l

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Specific areas examined-included the following observations.: magnetic

particle (MT) examination of Item Nos. APR2-4350-20 and APR1-1300-S35:

manual ultrasonic (UT) examination of Item No. ARP2-4350-20.: visual

(VT-1) examination of Item No. APR1-4303-0V021(B): visual (VT-3)

. examination of: Item No. APR2-4613-SS-12297: and data acquisition

activities associated with eddy current -(ET) examinations of steam

'

'

generator-(S/G) tubing. The. inspectors reviewed selected completed

-

examination reports and_ procedures.

Procedures reviewed included: FNP-0-NDE-100.1.-'" Measuring and Recording

Techniques for NDE: Examinations." Rev. 2.: FNP-0-NDE-100.5 " Liquid

Penetrant Examination (Color Contrast and Fluorescent)." Rev. 4:

FNP-0-NDE-100.11, " Magnetic Particle Examination." Rev. 3:

~FNP-0-NDE-100.21. " Visual Examination VT-1." Rev. 1: FNP-0-NDE-100.22.

" Visual Examination VT-2." Rev. 2: FNP-0-NDE-100.23. " Visual Examination

VT-3." Rev. 2: FNP-0-NDE-100.32. " Qualification of Ultrasonic-

..

Instruments." Rev. 2: FNP-0-NDE-100.31. " Manual Ultrasonic Examination

l . of Full-Penetration Welds (0.200 to 6.0 Inches)." Rev 4. with .TCN 4A:

FNP-0-NDE-100.34._ " Manual Ultrasonic Examination of Welds in Vessels.".

Rev. 6: FNP-0-NDE-100.35. " Ultrasonic Thickness Examination Procedure."

Rev.~1: FNP-0-NDE-100.37. " Manual Ultrasonic Examination of. Reactor

Coolant Pump Flywheels." Rev. 2: FNP-0-NDE-100.38 " Manual Ultrasonic

Examination of Nozzle Inner Radius." Rev. 2: FNP-0-NDE-100.39. " Manual

Ultrasonic Examination of Bolts and Studs Greater than 2 inches in -

Diameter." Rev. 3: FNP-0-NDE-100.40. " Manual Ultrasonic Examination of

Centrifugal Charging Pump Case." Rev.1: and FNP-0-NDE-100.41 " Manual

Ultrasonic Examination of Cast Stainless Steel Pipe Welds," Rev.1. with

.TCN 1A.

The inspectors performed an independent evaluation of indications to

confirm the licensee's ISI examiners * evaluations. In addition, the

-

inspectors conducted an independent VT-3 inspection of the following

su) ports previously examined by the licensee to confirm their.results:

AP11-4301-2HR-R155 and APR2-4619-SS-12459.

1

The inspectors reviewed records for the nondestructive examination (NDE)

personnel and ecuipment utilized to perform ISI examinations. The

records includec : NDE equipment calibration and materials certification

and NDE examiner qualification, certification, and visual acuity.

=The inspectors observed activities associated with insertion and

y expansion of S/G tube sleeves.

b. ' Observations and Findinas

Unit 2 S/G tubing was subjected to ET examination. This examination was

planned to include: -bobbin - 100% full length: + Point rotating pancake

-(RPC) 100%- top of tubesheet (TTS) 3-inches hot leg. 20% TTS 3-inches

cold leg. row 1 U-bends S/G 2A. row 2 U-bends S/G 2C. and all bobbin

indications. For the alternate repair criteria program, the ET.

Enclosure 2

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i

examinations were to include all tube support plate (TSP) bobbin

indications over 2 volts. all dents over 5 volts, and large mixed

residuals (33 in each S/G). Due to finding 2 tubes with indications in

the S/G 2C cold leg TTS + Point. the + Point program was expanded to 100%

of the inservice tubes. Due to finding an outside diameter stress

corrosion cracking (ODSCC) indication at one TSP intersection in S/G 2B.

that had a large mixed residual signal the + Point program was expanded

to look at the next 66 largest residuals. No indications were

identified in the expanded sample of 66.  !

Procedure FNP-0-NDE-100.5. Rev. 4. Appendix A-2. provided step by step

instructions for the performance of PT examinations in the temperature

range 145 F to 325 F using the following Sherwin Doubl-Chek * visible

solvent removable family: KO-17 Penetrant. D-350 Developer. and KO-19

Cleaner. ASME B&PV Code Section V, paragraph T-647 requires procedure

qualification for PT examinations that are to be conducted outside if

the range of 60 F to 125 F. The licensee indicated that at present. (

it did not have any of the high temperature penetrant consumable

materials. The inspectors determined that no examinations had been

conducted in accordance with FNP-0-NDE-100.5. Appendix A-2. The

licensees *s approval and issuance of a PT procedure for examinations

outside of the range of 60 F to 125 F. without first performing a

qualification in accordance with T-647. was considered an inadvertent

omission of the licensee's ISI/NCE programs.

The inspectors observed several personal safety concerns regarding

improperly secured ladders and Jersonnel working more than six feet

above the floor without pro)er land rails or safety harnesses. The

, inspectors reported these o)servations to the licensee who took

immediate corrective actions to address these issues.

ISI examinations observed / reviewed were conducted in accordance with

approved procedures, by qualified and certified examiners ising

certified / calibrated equipment and materials.

c. Conclusion

i

The Inservice Inspection / Nondestructive Examination (ISI/NDE) program  !

lacked procedure qualification of high temperature liquid penetrant j

examination.

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Enclosure 2

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.III. Enaineerina

E1- . Conduct of Engineering

' E1.1' .10 CFR'50.59 Safety Evaluation Proaram And Implementation

a. 'Insoection SCoDe (37001) 'I

I

LBy letter dated December 2, 1997. the licensee submitted Revision

, (Rev.) 14 to'the Updated Final Safety Analysis Report (UFSAR) for the

t , time. period of November 5.1995, to June 4.1997. This letter also

,

included a Summary Report of all changes. tests, and. experiments (CTEs)

L that were completed under the provisions of 10 CFR 50.59 over the same

period. The licensee's December 2 summary included approximately 135 =

changes.  ;

m

k '

The ' inspectors' conducted.a review of the licensee's program for meeting

L , the regulatory requirements of 10.CFR 50.59 and. examined its .

3 implementation. ' The inspectors. reviewed applicable administrative and

controlling procedures, training materials and numerous safety

evaluations.. including associated UFSAR Rev. 14 changes. In addition,

the inspectors attended a meeting by the Plant Operations Review

Committee-(PORC) that included review and approval of several safety _

L evaluations. The inspectors also reviewed recent audits conducted in

the area of 10 CFR'50.59 safety evaluations.

~

?

b. ' Observations and Findinas

Proaram Review

Thetins)ectors reviewed onsite Administrative. Procedure (AP)

'..

FNP-0-A)-88; " Nuclear Safety Evaluations." Revs. 2 and 3. and corporate

Farley. Nuclear Project procedure G0-NG-42. ~50.59 Evaluations." Rev. 4

In addition. -the inspectors reviewed Nuclear Engineering Procedure

(NEP)'8-102, " Preparation Of Safety. Evaluations." Revs. 6 and 7. and

Nuclear Engineering Procedure Instruction (NEPI) 4-0, " Design Change

Packages." Rev. 2. The principal offsite design organizations.

'

Southern Company Services =(SCS) and Bechtel, used NEP 8-102 and NEPI 4-0

, . for conducting safety evaluations of plant design changes. At the time

l-  : of.- the inspection, the licensee was transitioning from using NSAC-125.

H -

" Guidelines For 10 CFR 50.59 Safety Evaluations,~ to NEI 96-07. -

" Guidelines For 10 CFR 50.59 Safety Evaluations," dated September 1997.

. Revision 2 of FNP-0-AP-88 Rev. 6 of NEP 8-102, and Rev. 2 of NEPI 4-0

were, based on NSAC-125: the other procedures were recent revisions to

4 (endorse NEI 96-07. The: licensee has committed to fully implement

NEI 96-07 by June 30, 1998.

Enclosure 2

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After reviewing the above procedures, the inspectors concluded that the

licensee had established suitable programmatic guidance to ensure that

the regulatory requirements of 10 CFR 50.59 would be met by the various

onsite and offsite organizations. However the inspectors did identify

several program inconsistencies, as described below:

1) The onsite, corporate and design organization transition

from NSAC-125 to NEI 96-07 was poorly coordinated. At the

time of the inspection, onsite personnel were using

FNP-0-AP-88. Rev. 2. based on NSAC-125 (Rev. 3 was approved

but not issued): whereas. corporate project personnel were

using GO-NG-42 based on NEI 96-07 since January 15. 1998.

Also, offsite design organizations were required to use two

guidelines at the same time with one based on NSAC-125

(i.e.. NEPI 4-0) and another based on NEI 96-07 (NEP 8-102.

Rev. 7).

2) Although the offsite design organizations conducted the

majority of all actual safety evaluations (i.e.. addressing

the unreviewed safety question (US0) criteria), the level of

detail of their procedural guidance was minimal compared to

the onsite and corporate project organizations. NEPI 4-0

lacked much of the general and specific guidelines contained

in FNP-0-AP-88 and GO-NG-42. [However, this was previously

recognized by the licensee who was preparing to implement a

new, more detailed instruction PDI 5.8-102. " Preparation of

Safety Evaluations (10 CFR 50.59)." based on NEI 96-07.]

3) Lack of written guidance for addressing the necessity of

reverifying safety evaluations for changes that are not

implemented after many months or years.

4) Conduct of cross-disciplinary 3 reparation / review of safety

evaluations was not addressed )y 10 CFR 50.59 program

procedures. Only FNP-0-AP-1. Rev. 36. " Development. Review,

and Approval of Plant Procedures.' makes any direct

reference to cross-disciplinary reviews of safety

evaluations and even that applies only to the 10 CFR 50.59

screening. Onsite and offsite design change control

procedures were vague and unclear regarding

cross-disciplinary reviews of 10 CFR 50.59 safety

evaluations.

5) Definition and explanation of safety margin in FNP-0-AP-88.

Rev. 2 was inconsistent with NRC Inspection Manual

Part 9900: 10 CFR Guidance issued April 1996 as

~10 CFR 50.59 Interim Guidance on the Requirements Related

to Changes to Facilities. Procedures and Tests (or

Experiments)." and revised in October 1997. [ Note.

Enclosure 2

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16

inspectors did not review NEI 96-07. or licensee NEI 96-07

related procedures, against the NRC interim guidance.]

6) Responsibilities of the Manager, described in FNP-0-AP-88.

Revs. 2 and 3. for approving safety evaluations that do not

pass the 10 CFR 50.59 screening, are not addressed.

10 CFR 50.59 Screenino Process

l

The inspectors reviewed 20 completed safety evaluation forms for CTEs l

that the licensee determined did not satisfy the requirements for '

performing an evaluation of the USQ criteria of 10 CFR 50.59. For these

safety evaluation forms, only Section B. "10 CFR 50.59 Applicability." ,

was filled out, which determined that a 10 CFR 50.59 safety evaluation i

was not required. The 20 CTEs selected were screened for 10 CFR 50.59  !

a) placability during the time period from August 1997 to April 1998.  ;

T1e inspectors did not identify any CTE that was improperly screened for j

10 CFR 50.59 applicability.

1

Safety Evaluations - US0 Criteria

The inspectors selected about two dozen safety evaluations of

safety-significant CTEs that were determined to be 10 CFR 50.59

applicable to verify that each of the individual safety evaluation

preparers / reviewers / approvers were qualified to conduct these

evaluations. The inspectors also selected 17 safety evaluations of

safety-significant CTEs for a detailed review on the completeness and

adequacy of the answers to the US0 criteria of 10 CFR 50.59. All of the

CTEs selected included a variety of systems and different engineering

disciplines. However, they were almost exclusively related to plant

design changes requests for engineering assistance (REAs), and as-built  !

notifications (ABNs). Very few procedure changes ever met the i

10 CFR 50.59 applicability determination. and the licensee rarely I

performed tests and experiments not described in the UFSAR. Of the '

safety evaluations reviewed. the majority were performed by offsite

design organizations. i

Unlike the FNP site and corporate project, the inspectors found that the

offsite design organizations did not maintain any lists of qualified

preparers / reviewers / approvers, but rather relied on the individual l

engineering supervisors and managers to keep track of who was cualified )

in their. areas of responsibility. This practice made it very cifficult  ;

for the inspectors to independently verify the qualifications of  :

personnel from offsite organizations. Consequently, the inspectors had

to rely on licensee assurance that offsite design personnel were

qualified. based on their review of individual personnel files. The

. j

inspectors did verify that FNP site and corporate project personnel were -

qualified to conduct and review the selected safety evaluations. During

this effort. the inspectors also observed that very few of the safety

. evaluation forms provided any evidence of a cross-disciplinary review

Enclosure 2

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_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ . _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _________a

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which was consistent with the lack of pra rammatic guidance in this

area. In response to this observation, the licensee maintained that

cross-disciplinary reviews of safety evaluations would normally. be

covered during the design input review, and verification. However, the

t

inspectors determined that neither NEP 4-1. " Establishing Design Input

Requirements." Rev. 4. for preparing design input records or NEP 4-9.

" Design Verification." Rev. 4. for conducting design verifications

provided any explicit guidance for multi-discipline reviews of safety

evaluations. Consequently, even after reviewing numerous design change

packages (DCPs) associated with the selected safety evaluations and

reflecting on NEP 4-1 and 4-9. the inspectors were unable to conclude

that safety evaluations were s)ecifically receiving multi-discipline

reviews. Failure to perform taese reviews may be a contributing factor

to the lack of necessary detail in safety evaluations as discussed

below.

Of the 17 safety evaluations reviewed in detail for adecuacy and

completeness of their answers. the inspectors did not icentify a CTE

that involved a USQ. However. many of the safety evaluations provided a

minimal or insufficient level of detail in answering the questions to

address the 10 CFR 50.59 US0 criteria. In general, the information

contained in the " Background and Description" portions of Section A.

" Activity Summary." of the safety evaluation form tended to be quite

detailed. Also, the responses to the questions of Section B.

~10 CFR 50.59 Applicability." were suitable. But the answers to the

questions in Section C.~ ~US0 Criteria.~ were typically very summarized

and lacked specificity. For several of the safety evaluations, the

Section C answers were so brief and generalized that. by themselves.

they would have been inadequate. However, in almost all of these cases,

the reader was able to obtain sufficient information from the

description in Section A to satisfy the appropriate question of

Section C. The major problems with this approach were that it made

reviewing the safety evaluation more difficult suggested that the

preparer did not understand the scope of each question, and was

inconsistent with the NSAC-125 and NEI 96-07 guidance for providing

complete and thorough answers to the seven questions addressed by the

descriptive information.

Some particular examples of safety evaluations that provided inadequate

detail in Section C to address the USQ criteria of 10 CFR 50.59. but

where the information could basically be found in Section A. were as

follows:

-

10 CFR 50.59 Evaluation. Rev. 5. for DCP 96-0-9012-2-006:

-

10 CFR 50.59 Evaluation. Rev. 3. for DCP 97-0-9182-0-004:

[

-

10 CFR 50.59 Evaluation for DCP B-97-1-9192-0-003:

-

10 CFR 50.59 Evaluation for ABN 95-0-0589: and.

-

10 CFR 50.59 Evaluation. Rev. 1. for DCP 95-2-8932-1-004.

Enclosure 2

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18

In addition to these safety evaluations. there was an examale where

neither Section A nor the answers to Section C of the 10 C R 50.59

l safety evaluation form provided enough detail to determine that a USQ

did not exist. However, in this instance, the licensee was able to

demonstrate to the inspectors that, even though the safety evaluation

forms lacked the information needed to answer the questions for

i determining a' US0. there was sufficient documented basis in the

associated DCP and/or references listed in Section A to determine that a

USQ did not exist. This example was the 10 CFR 50.59 Evaluation for

DCP 95-2-8932-1-004.

10 CFR 50.59 does not specify the manner in which a safety evaluation j

should be documented. As such, failure to provide sufficiently detailed

answers to the "seven questions" in Section C does not specifically

constitute a noncompliance with 10 CFR 50.59. However, the guidance in

NEP 8-102 clearly states that " the safety evaluation should be written

as a stand-alone [ emphasis added] document with sufficient detail." It

also states that "a thorough description is required because other

personnel reviewing the documentation may not be familiar with the

physical plant." There was nothing in NEP 8-102 (nor FNP-0-AP-88 or

GO-NG-42) to suggest that the answers of Section C could rely upon

information in Section A, the DCP package, or references in order to

address all elements of the subject change that could reasonably affect

a US0 determination. Quite the contrary, program guidance recommended

completeness and specificity. Adequate documentation to address the US0

criteria is considered a weakness in the implementation of the

licensee's 10 CFR 50.59 program.

10 CFR 50.59 Summary Reoort Descriptions

The inspectors compared 13 summary descriptions of CTEs reported to the

NRC pursuant 10 CFR 50.59 in the December 2, 1997. letter to the

description of changes contained in the actual 10 CFR 50.59 safety

evaluations. Inspection report (IR) 96-07 had identified examples in {

the licensee's previous 10 CFR 50.59 report to the NRC that were either {

incomplete, did not clearly identify the nature of the change, or used I

plant-specific acronyms that were not readily recognizable. During this I

review, the inspectors did not identify any of these exam)les and '

concluded that the descriptions of changes contained in t7e most recent

10 CFR 50.59 summary report were complete and adequately described the

change.

UFSAR Chances Resultina From CTEs

The inspectors reviewed ten design changes identified in the

10 CFR 50.59 summary report and compared them to the actual changes

contained in Rev. 14 to the UFSAR. No discrepancies were identified. i

j

Enclosure 2

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- - - . - _ _ _ _ _ - _ _ - _ - _ _ _ _ __

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4

19

Trainina Associated with 10 CFR 50.59 Proaram Activities

The inspectors reviewed the licensee's training program contained in

the Farley Technical Staff and Management document TSM-510. " Nuclear

Safety Evaluations." July 1996, and associated training material used by

the training department. The training material included: (1) personnel

requirements for aerforming 10 CFR 50.59 evaluations: (2) an FSAR

overview: (3) an :SAR search program use: (4) examples of 10 CFR 50.59

evaluations and screening material for 10 CFR 50.59 applicability; (5)

10 CFR 50.59 evaluation guidelines: (6) NSAC-125 and guidan a related to

its use: and (7) administrative procedure FNP-0-AP-88. Rev. 2.

The inspectors also reviewed FNP-98-0067-TRN. " Designation of Qualified

Reviewers." which contains a matrix of personnel that are qualified to

prepare and/or review 50.59 safety evaluations. Individuals were

selected for 10 CFR 50.59 training based on need and department

managers' recommendations. The training department maintained a list of

trained individuals and the next due date for refresher training. The

inspectors verified that those individuals listed in FNP-98-0067-TRN

have maintained their training current. However, the inspectors noted

that the FNP-0-AP-88 requirement that " Personnel who prepare review. )

or approve 10 CFR 50.59 evaluations will be trained every two calendar

years." was inconsistent with the guidance of Technical Staff and

Managers Curriculum Guide for TSM-510. The licensee's actual practice

of retraining conformed most closely with the curriculum guide rather

than FNP-0-AP-88. Although there is no specific 10 CFR 50.59 I

requirement for refresher training, the licensee was informed of the

conflict between TSM-510 and FNP-0-AP-88.

Prior to November 1997. qualifications to perform 10 CFR 50.59 I

evaluations were based on maintaining training current and successful

completion of the one-day course on TSM-510. However, since that time,

individuals that attend the TSM-510 course were given a written multiple

choice exam at the end of the course. Approximately 150 of 300 people

listed in FNP-98-0067-TRN. have taken the written exam. The licensee

has indicated that the remaining individuals will be given a written l

exam when refresher training is taken. '

During the transition to NEI 96-07. Rev. O. " Guidelines for 10 CFR 50.59

'

Safety Evaluations." and the process of revising FNP-0-AP-88, the

training department was also updating associated 10 CFR 50.59 training

material as applicable. In anticipation of the NEI 96-07 transition and

to provide onsite and offsite safety evaluation preparers / reviewers with

more in-depth and comprehensive training. the licensee contracted for a

special one-day training course, primarily duririg the Summer and Fall of

1997. The SNC 10 CFR 50.59 Evaluation Training Program of " Meeting the

10 CFR 50.59 Evaluation Challenge - A Program to Achieve Excellence."

was given to all qualified preparers / reviewers. The inspectors reviewed

f the training manual used and found it to be comprehensive and thorough.

Enclosure 2 ,

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_, _ ._ _ - _ _ _ _ _ _ _ _ -____ - ___-_____-_ - -___ __

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L Audits of'10 CFR 50.59 Proaram Implementation

Very few audits of the 10 CFR 50.59 program and its implementation have

i been performed. Historically, any audits of licensee safety evaluation

activities were typically included as part of broader audits of other

programs'(e.g... design change control). However, an audit of SNC-Farley-

Support-Nuclear Engineering and Licensing was conducted during July 1997

that. included implementation of G0-NG-42. Rev. 3. Although no audit

finding reports were identified, one comment was made regarding lapsed

training-for certain individuals. Also, during the team inspection, a

L

'

site-specific spot audit was in progress "to obtain the status of, as

well as determine.~ the degree of consistency in implementation of

'

NEI 96-07." The inspectors . reviewed the audit report and audit notes

,

associated with these audits. Both audits were of very limited scope

L and detail. The overall paucity of auditing-in this area provided the

inspectors with ' insufficient information to conclude that the licensee's

audit program was effectively assessing conformance with 10 CFR 50 59. .

However, the _ inspectors did note .that routine auditing of 10 CFR 50.59

1 activities were-not specifically required by the audit program as

defined by TS', UFSAR, and Operations Quality Assurance Policy. Manual

(00APM).

c. Conclusion-

The inspectors concluded that the licensee had established: sufficient

programmatic guidance' to ensure .that the regulatory requirements of

10 CFR 50.59 would be met.by the various onsite and offsite

organizations. However, the inspectors did identify several

programmatic deficiencies and inconsistencies. Training of safety

evaluation preparers and reviewers was adequate.

Changes.. tests and experiments were properly screened for 10 CFR 50.59

applicability, and adequately ~ evaluated to ensure an unreviewed safety

. question-.did not exist. Personnel preparing.and reviewing. safety

-'

evaluations were qualified. . However, the documentation that addressed

lthe.US0 criteria in several safety evaluations lacked specificity and

thoroughness. Furthermore, very few of the safety evaluation forms

provided any direct evidence of a cross-disciplinary review.

Licensee audits of the 10 CFR 50.59 program were few in number and very

limited-in scope.and detail.

,

<

Enclosure 2

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E8 Miscellaneous Engineering Issues (IP 92903)

E8.1 (Closed) Unresolved item (URI) 50-348.364/98-01-04. Inadeouate Safety

Assessment For Mis-wired Hot Shutdown Panel MOVs

'

(Closed) Licensee Event Report (LER) 50-348.364/97-10-01. Motor Operated

Valve Local - Remote Control Circuit Wirina Discrepancies

a. Inspection Scope

.

The inspectors reviewed revised LER 97-10-01. applicable Abnormal

Operating Procedures (AOP). licensee's response to a request for

engineering assistance (REA), and conducted walkdowns of the equipment

in question.

b. Observations and Findinas

In May 1997 the licensee discovered that the control power circuitry

for five motor-operated valves (MOVs) were mis-wired. The mis-wired

,

condition defeated the electrical isolation fuse design that ensured

1 that these five MOV's would be operable from the Hot Shutdown Panel

3

(HSDP) during .a fire in the MCR or cable spreading room. The licensee

promptly repaired the improper wiring and submitted LER 97-10 for

operating in a condition outside of the design basis.

As referenced in Section E8.1 of IR 98-02. 10 CFR 50.73(b)(3) requires

the licensee to assess the safety consequences and implications of

reportable events, including the availability of other systems or

components that could have performed the same function as that which had

failed. After reviewing the safety assessment of the original

LER 97-10. the inspectors concluded that the licensee failed to perform

an adequate assessment of the safety consequences and implications of

the mis-wired MOV's during a fire in the MCR or cable spreading rooi.1

that would necessitate implementing the unit-specific A0P-28.1. " Fire or

Inadvertent Fire Protection System Actuation in the Cable Spreading

Room.~ or AOP-28.2 " Fire in the Control Room.~ Furthermore, the

licensee failed to describe availability of other systems, components,

or manual actions to compensate for the loss of MOV functions. Failure

to perform an adequate safety assessment constitutes a violation of

10 CFR 50.73(b)(3) and is identified as VIO 50-348. 364/98-03-04

Inadequate Safety Assessment for Mis-wired Hot Shutdown Panel MOVs.

Based on this violation. URI 50-348.364/98-01-04 is closed. The

licensee revised its original LER, especially the safety assessment, to

provide a better understanding of the risk and safety significance of

the reportable event. Additionally, no new corrective actions for the

event were identified. The inspectors reviewed the revised safety

assessment and concluded it adequately addressed the safety consequences

and implications of the event, as well as, described the availability of

other systems. components. or manual actions to compensate for the loss

of the MOVs.

Enclosure 2

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22

The licensee's revised safety assessment determined the possible adverse

impacts of postulated plant fires in the cable spreading rooms (CSR) and

the main control room (MCR) upon the ability to shutdown and cooldown

the plant considering the mis-wired MOV's. For these limiting fires,

the consequences of inadequate electrical isolation of these five

mis-wired MOVs on the HSDP and MCB are discussed below.

Power Operated Relief Valve (PORV) Block Valves

i

Postulated fires in the MCR and CSR could have resulted in both d

mis-wired PORV block valves becoming inoperable from the HSDP. However.

the licensee concluded that a failed open PORV could be manually

de-energized and thereby closed to re-establish the RCS pressure

boundary. by using procedural guidance previously approved by the NRC in

a SER for an Appendix R exemption. The inspectors verified that this

procedural guidance was available at the Hot Shut Down Panel.

Component Coolina Water (CCW) to Secondary Heat Exchanaer Isolation

Valve MOV 3047 and Refuelina Water Storaae Tank (RWST) to Charaina Pumo

Suction Isolation Level Control Valves (LCVs) 1158 and 115D

The more significant concern identified by the licensee's safety

assessment was the potential that a MCR or CSR fire coincident with a

'

LOSP could have resulted in a LOCA due to loss of cooling to the RCP

seals. [ Loss of cooling to the RCP seals would require a loss of seal

injection and CCW flow to the thermal barrier heat exchangers.]

Under certain fire-induced failure conditions, the centrifugal charging

pump (CCP) suction could be' lost, resulting in possibie vapor binding

and damage to the operating CCP. In addition, a fire-induced s)urious

valve closure could isolate CCW supply flow to the RCP thermal >arrier.

Restoration of CCW flow or charging flow would then recuire manual

actions because of the loss of control of MOV 3047 anc LCV-115B and

LCV-115D. from the HSDP due to blown MCR fuses. According to the

licensee's assessment, the redundant CCPs would have been available to

start-from the HSDP. but only after manually opening the RWST to CCP

suction MOVs (and venting the CCPs, as necessary) to reestablish seal

cooling through seal injection. Similarly. CCW flow could only be

restored by manual operation of MOV 3047. However, these manual

actions, without specific operator training or procedures. would have

significantly delayed restoration of seal flow.

'The inspectors walked down the MCR and CSR wiring for the components of

concern to determine the probability of a fire affecting both the CVCS

(letdown. CCPs. VCT discharge valves) and CCW MOV 3047. The inspectors

found that MOV 3047 and the CVCS were on the same section of the MCB.

,

approximately 12 feet apart. The respective cables dropped vertically

f from the switches through floor penetrations directly to the CSR. The

majority of the cables in that section of the MCB had a braided

stainless steel jacket. There were no vertical separators in the MCB to

Enclosure 2

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23

provide 3hysical isolation. Once in the CSR, the cabling split north

and sout1 to the respective "A" and "B" train cable trays. The

inspectors concluded based on the 3hysical layout, that it would take a

major MCR or CSR fire to affect botl charging flow and MOV 3047 to cause

a loss of RCP seal cooling and subsequent seal LOCA.

During the 12-year period that the affected MOVs were mis-wired, no

fires or other significant' plant events occurred that necessitated

taking control of the MOVs at the HSDP.

The licensee's assessment concluded that it would be extremely unlikely

that a fire of sufficient magnitude to adversely impact components as

described above to occurr. The licensee considered it even more

unlikely that a fire of this magnitude could occur coincident with an

LOSP. A significant' fire in the main control' room was not considered by

the licensee to be a credible event because it is continuously occupied.

)ower. circuits are minimized, and combustibles are limited. The CSRs

lave automatic fire su

combustible. materials.ppression The CSRssystems, fire alarms,

are also equipped withand limited

manually

actuated low pressure carbon dioxide fire suppression systems. The

licensee also considered that the advance of a postulated fire would.not

have been instantaneous- and' components adversely affected by the fire

would not have.been affected simultaneously. 0)erators in the MCR would

have been alerted to component malfunctions eitler through indications,

alarms.-or procedural steps.

The licensee concluded that'while the MOVs were mis-wired, the ability

-to achieve safe shutdown for certain )ostulated plant fires coincident

with a LOSP was degraded. This possi)le loss of capability to shutdown

and cooldown the plant from outside the MCR; as required by 10 CFR 50.

Appendix F is~ identified as an apparent violation. EEI 50-348,

364/98-03 3 HSDP Loss of Function.

In addition to the corrective actions of LER 97-10-00, the licensee

reported in LER 97-10-01 that the Abnormal Operating Procedures for

responding to fires in the CSR or MCR were revised. The revised

)rocedures now require operators (if time allows) to open LCV-115B and

.CV-115D prior to evacuating the control room in order to minimize the

potential for. losing suction to the operating CCP. This action was

considered an enhancement to the procedure by the licensee. These

)rocedure changes were verified by the inspectors. The revised

_ER 97-10-01 is considered closed.

c. Conclusion

- A violation was identified because the original safety assessment for

LER 97-10 did not completely address the safety consequences and

implications of the possible failure of five mis-wirec motor-operated

valves at the Hot. Shutdown Panel during a control room or cable

spreading room. fire. The subsequent supplemental LER did provide

Enclosure 2

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.

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24

sufficient information for an adequate safety assessment of the event.

In addition, an apparent violation was identified due to the I

determination that the licensee's ability to safely shutdown and '

cooldown the plant from the HSDP was in a degraded condition for about

12 years.

E8.2- (Closed) VIO 50-348. 364/97-11-04 Failure to Imolement a Test Proaram j

for Service Testina of the TDAFW Batterv

The licensee responded to this VIO in correspondence dated December 17,

1997 and initiated Corrective Action Report (CAR) 2321. The inspectors l

reviewed the licensee's written response and completed CAR. verified j

implementation of corrective actions, and reviewed the test data for the l

Unit TDAFW battery service test. This VIO is closed.  !

E8.3 (Discussed) VIO 50-348. 364/97-11-03. TDAFW Batterv Installation and

Check Valve Test Deficiencies

The licensee responded to this VIO in correspondence dated December 17,

1997, and initiated CAR 2322. This CAR was not complete at the end of

this inspection period. The inspector verified that the TDAFW Battery

racks were rebuilt per the applicable drawings. This VIO will remain  ;

open pending review of the completed CAR and the check valve test i

deficiencies corrective action.

E8.4 Modification of Penetrations for GL 96-06

The inspectors verified that relief valves were installed in i

Penetration 30. Pressure Relief Tank (PRT) Makeup, and Penetration 31.

Reactor Coolant Drain Tank (RCDT) Drain, per the licensee's letter dated

May 23. 1997, in response to GL 96-06 " Assurance of Equipment

Operability and Containment Integrity During Design-Basis Accident

Conditions."

-EB.5 (Closed) URI 50-348. 364/98-01-05. Failure to Track and Correct

Conditions Adverse to Quality  :

(Closed) IFI 50-348. 364/98-01-06. Control Room Ventilation Testina I

a. Inspection ScoDe (37551)

The inspectors reviewed a variety of tracking list data and closure l'

documentation, interviewed personnel, and walked down the systems.

l

b. Observations and Findinas

The subject of 1.icensee Event Report (LER) 97-13. " Operating Outside the

Design Basis Due to Control Room Exhaust Isolation Dam)ers Not Closed."

originated from Open Item CRV-007, identified during t1e Control Room

Ventilation (CRV) Functional System Description (FSD). Historically.

Enclosure 2

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the plant had operated with the CRV exhaust dampers open. But during a

self-assessment of the CRVS. questions arose regarding the design basis j

requirements for positioning these exhaust dampers and FSD CRV-007 was '

opened. In April 1995, a design evaluation was performed offsite to

address CRV-007. This evaluation concluded that the CRVS emergency

) pressurization system was designed to operate with these dampers shut. ,

lowever, the results of the evaluation were misinterpreted at the site '

and the dampers were procedurally left open. In August 1997. during the

FSAR verification arocess, the open damper position was again questioned

by the licensee. _icensee personnel determined that the plant had

o)erated outside its design basis while the exhaust dampers were open. 1

T1ese dampers were then shut and LER 97-13 was issued (see IR 98-01. l

Section E8.2)  ;

As part of the corrective actions for.LER 50-348. 364/97-13. the

licensee conducted a review of all the closed out "Open Items"

previously identified during the CRV FSD and Safety System i

Self-Assessment (SSSA) and ascertained that 5 of 19 open items had been

'

closed out without any evidence that the recommended corrective actions

were implemented. Responsibility for two of these items (0 pen Items

CRV-010 and CRV-019) had been assigned to the site.

Open Item _ CRV-010 originally identified that some areas surrounding the

main control room (MCR) could be pressurized to greater than 0.125 l

inches water gauge (w.g.), thus allowing unfiltered in-leakage, greater  !

than assumed. into the MCR. Bechtel letter AP-21274, dated June 7.  !

1995, completed the evaluation and identified two s) aces where single l

failures could cause a room adjacent to the MCR to 3e pressurized J

greater than 0.125 inches W.G. This letter provided recommendations to

resolve the concern of over-pressurizing areas next to the Control Room

and thereby not allow greater than assumed unfiltered in-leakage into

.

the MCR. These recommendations were provided to the site from corporate

engineering via a letter (NEL 95-0189). dated July 6. 1995. The Bechtel  ;

letter also recommended closing item CRV-FSD-010. " Control Room

'

Pressurization from Adjacent Areas." and it was removed from the

corporate tracking list. However during this time the o)en item was

also inadvertently removed from the site tracking list. _ater in

November 1997, during the review of completed CRVS FSD, and SSSA Open

Items as a corrective action for LER 97-13. the licensee determined that

no evidence (e.g. revised procedures. etc;) could be found to ascertain

that the recommendations for CRV-FSD-010 had ever been implemented or

dispositioned at the site. This item was subsequently reopened, and the

proposed recommendations were still being evaluated at the end of this

inspection period.

j

'

0)en Item CRV-019 was originally concerned with weaknesses in testing

t1e pressurization system to support the allowable o)en penetrations in

the control room boundary. During the SSSA of the CRV system.

Assessment Observation CRV-MECH-02, dated November 17. 1995 (later

designated as Open Item CRV-019) identified some potential weaknesses in

Enclosure 2

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26

the testing to support MCR allowable open per.etrations calculation. The

response to CRV-MECH-02 (NEL 96-0069. dated February 27, 1996) addressed

several specific issues, but did not look at' the larger issue of MCR

boundary degradation. During corrective actions for LER 97-13. former

"Open Items" from the FSD/SSSA were reviewed to verify adequate closure.

The licensee identified that the response to close out this issue did

not address the boundary degradation issue (NEL 97-0526. dated

December 19. 1997) and recommended that periodic testing be accomplished

to assure that the MCR penetration opening allowance was conservative.

On February 2. 1998, the licensee established an administrative Limiting

Condition of Operation (LCO) that prevented additional breaches in the

control room boundary. However, on March 5. 1998, corporate engineering

sent an evaluation (NEL 98-0088) to the site which recommended against

testing to validate the pressurization performance, but did state that

the plant may want to consider adding a test to determine boundary

degradation. In addition, the letter re-issued a Bechtel letter which

confirmed that the 21.21 scuare inch opening was conservative. At that

time the restriction on adcitional boundary breaches was lifted.

However, no additional boundary breaches were required. After

discussions with the licensee. Engineering Support conducted a test on

March 25. 1998. for the CRV system that included air flow data. The

licensee's calculation determined that only 10 square inches of opening

could be allowed and still maintain the required MCR over-pressure. The

licensee re-instituted an administrative LCO to prevent CR boundary

breaches greater than the new calculated area. On April 21. 1998, the

licensee added a temporary change to FNP-0-AP-16. " Conduct of Operations

-Operations Group." Rev. 27, which removed the 21.21 square inch

administrative limit and referenced a data sheet in the Plant Curve

Book. which is updated quarterly to reflect the boundary degradation of

- the control room.

Until this time, the testing being done did not verify that the control

room minimum pressure could be maintained with a 21.21 square inch

opening, the licensee's administrative limit.

An inspector's review of the most recent surveillences. FNP-0-STP-26.2.

" Control Room Pressurization / Filtration Operability Test" for 'A' and

  • B' Trains." Rev. 12. indicated that the system can maintain the minimum

control room pressure in its current condition and that the licensee is

cognizant of the need to maintain the control room boundary integrity.

- Open Items CRV-007. CRV-010. and CRV-019 were conditions adverse to  ;

quality that were not adequately corrected. In each of the three i

previously described cases, the licensee had originally identified a l

deficiency and then either inadvertently or inappropriately closed it v

out. The licensee then re-identified the items and either has taken or i

is completing corrective actions on the individual issues. Failure to  !

adequately correct conditions adverse to quality is identified as i

VIO 50-348. 364/98-03-06. Inadequate Corrective Actions for MCR 1

l

Enclosure 2

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~ Ventilation System. ' Also, the inspectors expressed concern to the

licensee that FSD open items for systems in addition to the CRVS may

have been closed with inadequate corrective actions. By the end of this 1

inspection period, the licensee had not reviewed or reverified the

adequacy of the corrective actions closed out for other FSD systems.

l

l

c. Conclusiq01

P

- A violation of 10 CFR Part 50. Appendix B Criterion XVI, Corrective

Action was identified. The licensee identified three conditions adverse

to quality of Control Room Ventilation System Functional System Design

-(FSD) Open Items, which were either inadvertently or inappropriately

. . closed and not corrected.

IV. Plant Sucoort

R1 Radiological Protection and Chemistry (RP&C) Controls (83750, 84750,

86750)

RI.1 Radiological Controls (83750)

m

E i a. Insoection Scooe

L Radiological controls associated with ongoing Unit 1 ('U1) routine

l_ ' operations and with Unit 2 Refueling Outage 12 (U2RF12) activities were

< reviewed and evaluated by the inspectors. Reviewed program areas

'

Li included area-cleanliness and housekeeping, area postings. radioactive

o >

material and waste'(radwaste)-container labels. high and locked-high

radiation area controls, and procedural and radiation work permit (RWP)

implementation. The inspectors made frequent tours of the

U

Radiologically Controlled Areas (RCAs) and directly observed worker and

Health Physics Technician (HPT) performance during selected tasks. l

, Established Radiation Protection (RP) program guidance and

!

'

implementation were compared against commitments detailed in the Updated

Final Safety Analysis Report (UFSAR). and in procedural. Technical

l Specification (TS), and 10 CFR Part 20 requirements.

L

"

b '. 0 observations and Findinas-

High.and locked high radiation area controls were' established and

L. maintained in accordance with TS requirements. Area postings and

4 container labels were proper for the radiological conditions and met

procedural. TS, or 10 CFR 20 Subpart J requirements. Improvements were

"

noted in labels provided for containers of radioactive materials.-

Contamination and radiation surveys were conducted in accordance with

procedural requirements. Radiation and contamination survey results met

established regulatory and procedural limits.

1

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On April 29, 1998, the inspectors observed work activities and HP

practices associated with removal of Tri-Nuclear equipment and filters

from the lower reactor cavity conducted in accordance with Specific RWP

No. 298-2491. Revision (Rev.) 1. During completion of the task., a

remote handling-tool was damaged causing the dose expenditure to

escalate to approximately 985 millirem (mrem), exceeded the budgeted

dose-of 900 mrem. The following poor radiological practices, job

. planning weaknesses, and communication issues were identified and

discussed with licensee representatives:

. Mock-u) training was not provided for removing the spent filters

from t1e vacuum system and for transferring the material to the

Unit 2 drumming room. Design differences between the previous and

current vacuum system model, which now required a specific

alignment of the filters within their housi.ngs for proper removal,

was not identified. Improper alignment during the initial . attempt-

'

to remove a filter from the vacuum system resulted in excess force -

being applied and the remote handling device being damaged.

  • Methods and controls to limit personnel exposure were minimally

effective. ' Plans for use of an extension tool while transferring

the filters in containment was abandoned after problems were

' identified during removal of the initial filter from the vacuum

system: extensive exposure time was required to manually tie and

untie ropes to bags used to hoist the eight vacuum system filters

from the lower to-the upper cavity area: and on several occasions.

workers entered designated exclusion areas during transfer of the

filters. Also. when a supplemental teledose monitor.'provided to

a Health Physics Technician (HPT) handling a spent filter alarmed

as a result of an improper dose rate alarm setting. the individual

returned to transfer an~ additional filter prior to change-out of

the alarming unit.

.. Planning and communication weaknesses were identified during a

post-job briefing and from followup discussions with participating

operations, maintenance HPT and "As Low As Reasonably Achievable"

(ALARA) staff. For example, maintenance workers were

knowledgeable of general area dose rates associated with the

filters, but were not fully aware of the significant hazard from

the filter contact dose rates and the importance of using remote

tools in handling the filters. Furthermore, previous maintenance

staff-safety concerns regarding use of the remote tool to remove

the filters from the vacuum equipment and potential contamination

concerns from ropes used to suspend the vacuum equipment in the

cavity were not' incorporated into planning for the current task..

p

1

Enclosure 2

'

w__=_-___ _ _ - _

- _ _ - - - - _ - - _ _ _ - _ - _ - - _ _ _ _ _ _ - - -

. - -

.- .

.; ..

29-

c. ' Conclusions

Radiological controls were established and maintained in accordance with-

. procedural.-TS and 10 CFR 20 Appendix J requirements.

A weakness in exposure controls and poor communications contributed to

-the licensee exceeding its budgeted dose.for the removal of Tri-Nuclear

equipment and filters from the U2 lower reactor cavity due.

R1.2 External Exoosure (83750)

a. Insoection Scooe

The inspectors discussed and reviewed deep dose equivalent (DDE) and

shallow dase equivalent (SDE) exposures to workers involved in U2RF12

activities. Personnel contaminations, documented as personnel

contamination events (PCEs), i.e.. dispersed contamination greater than

or equal to.(a) 5000 disintegrations 2

per minute per 100 square

centimeters (dpm/100cm ) and specks = 100000 dpm/ probe. areas, were

reviewed and discussed.

Dose assessment methods and assumptions, where applicable, were reviewed

.for technical adequacy. : Dose results were, compared against 10 CFR

Part 20. limits,

b. Observations and Findinas

Estimated dose data, as measured by Digital Alarming Dosimeter (DAD) for

U2RF12 activities, were reviewed and discussed with responsible staff.

-As of April- 30, 1998, dose expenditure.for outage activities.

approximately 169.064 person-rem, exceeded the original projected dose

expenditure of 155.956 person-rem. The licensee identified problems

with Residual Heat Removal (RHR) pump maintenance activities, expanded

scope of mid-loop valve maintenance, and unexpected elevated dose rates.

in the U2 spent fuel pool (SFP), contributing to the elevated person-rem

expenditures. From review of selected Occurrence Reports and

l

discussions with licensee staff, the inspectors verified that RHR

maintenance and-SFP dose expenditure issues were being reviewed and

evaluated.

As of April 29. 1998, approximately 29 personnel contamination event

!

'

reports were documented with only one event requiring a skin SDE

determination. For the affected individual. a hot particle located on

the u

-(SDE)pper.right forearm

of ap3roximately resulted

7.76 rem. in an assigned

Licensee assumptions shallowand dose details equivalent

regarding p1ysical: location.' length of. exposure and isotopic

characteristics of particle were appropriate. The inspectors noted that

all assigned doses were within 10 CFR 20.1201 limits.

I

Enclosure 2 I

? l

.-

L___-_-______-__ -

-

.

-.

. .

'

- . ..

' - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - -

- __ . _ _ _ - _ _ - _ --. . _ _ . _ _ .

. .

,

l.

30

c. Conclusions

For U2RF12 activities, dose expenditure exceeded original estimates due

to expanded work scope, unexpected maintenance problems, and elevated U2

spent fuel ' pool dose rates.

Worker SDE_ exposures resulting from personnel contamination events and

work activities during the U2RF12 activities were evaluated properly and

were within 10 CFR 20.1201 limits.

R1.3 Internal Exoosure (83750)

a. Insoection Sccoe

Results of selected investigative whole-body count (WBC) analyses

conducted during the U2RF12 outage 'were reviewed in detail.

b. Observations and Findinas

From review of WBC analysis records of workers' positive radionuclides

intakes, the inspectors identified one individual whose initial WBC

analyses data resulted in an assigned committed effective dose

equivalent (CEDE) exceeding 10 mrem. The inspectors noted that as of

April 29,1998, approximately 12 investigative WBC analyses were

conducted as a result of specific events, usually documented in

-Radiation Worker Performance Observations, which could cause or indicate

potential radionuclides intakes resulting in internal exposure. The

estimated maximum iiltake was approximately 158 nanocuries (nC1). >

resulting in an assigned CEDE of 12 mrem. The ins)ectors verified that

the 12 mrem CEDE was added to the DDE to provide t1e total effective

dose equivalent (TEDE) documented in the individual's official exposure

records. No other evaluated worker intakes exceeded 10 mrem. i.e. 0.2

percent of the annual limit of intake (ALI) required to be documented by

licensee procedures.

c. Conclusions

Controls for minimizing workers' internal exposure during U2RF12

activities were effective.

R1.4 Respiratory Protection (83750)

a. .Insoection Scone

Respiratory protection program implementation for U2RF12 activities was

reviewed and evaluated. The review verified training, fit testing, and

medical qualifications for selected licensee and contractor personnel

who were supplied and used respiratory protection equipment.

Enclosure 2

_ _ - _ _ _ _ - . _ _ __. _

. ._ ._ _ _ _ _ - _ _ _ _ - _ _ _ _ _ _ - _ _ _ _ _ _ _

i

.

!

L

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31

Licensee activities were reviewed and evaluated against procedural and

10 CFR 20.1703 requirements.

L b. Observations and Findinas

Workers using respiratory protective equipment during U2RF12, were fit

tested. medically qualified, and trained in accordance with procedural l

requirements. l

l

c. Conclusions ,

,

Respiratory protection program implementation for U2RF12 activities met -

established procedural and 10 CFR 20.1703 requirements.

R2 Status of Radiological Protection and Chemistry Controls Facilities and

Equipment

R2.1 Radiologically Controlled Area (RCA). Units 1 and 2 (71750) i

Overall cleanliness of the RCA remained good. Plant personnel observed

working in the RCA generally demonstrated appropriate knowledge and

application of radiological control practices. Health physics

technicians generally provided positive control and support of work

activities in the RCA.

R2.2 Radiation Monitorino Systems I

a. Scope

Design and calibration issues were reviewed and discussed for selected

Radiation Monitoring System (RMS) sampling equipment and detectors.  ;

Design issues for the RE-29B. Plant Vent Post-Accident Vent monitor were '

reviewed. Calibration activities for the U2 Containment High Range

Monitor (CHRM) RE-27A were observed and resultant calibration data were

reviewed and discussed. In addition, design issues associated with

effluent stream flow pathways for the RE-29B particulate sampler were

reviewed and verified.

Installed equipment was evaluated against recommendations specified in

American National Standards Institute (ANSI) N13.1-1969. American

National Standard Guide to Sampling Airborne Radioactive Materials in '

Nuclear Facilities. Calibration activities were evaluated against

applicable sections of the Updated Final Safety Analysis Re) ort (UFSAR).

Technical Specification (TS), and Offsite Dose Calculation ianual (ODCM)

requirements. In addition, calibration activities to meet a March 14

1983 Order to implement and maintain licensing commitments associated

with Three Mile Island (TMI) Action Item II.F.1 for the CHRMs special

calibrations were reviewed.

t

Enclosure 2

,

L_____

- _ _ . _ _ _ _ .

,1 ,

<

.

32

b. Observations and Findinas

.The installed U1 RE-298 RMS sample line flow path was found to be

acceptable. The U2 CHRMs electronic calibrations and functional tests

and isotopic calibration checks were conducted in accordance with

Surveillance Test Procedure FNP-2-STP-227.18. "In-Containment High Range

Radiation Area Monitor R-27A." Rev. 9. and Radiation Control and

Protection (RC&P) Procedure FNP-2-RCP-272. " Isotopic Calibration Check ,

of the Unit 2 Containment High Range Area Monitors." Rev. 3. The

calibrations were conducted by electronic signal substitution for all

range decades above 10 Roentgens per hour (R/hr). No regulatory issues

were identified for the test and calibration data reviewed.

c. Conclusions

The evaluated RMS equipment was installed properly and the reviewed

detector calibrations and functional tests were conducted in accordance

with and met procedural. 10 CFR Part 20. and ODCM requirements.

I

R3 Radiation Protection and Chemistry Documentation (84750)  !

R3.1 Radiological Effluent and Environmental Monitorina Reports l

a. Insoection Scone l

l

Data and conclusions documented in the 1997 Annual Radiological  !

Environmental Operating Report and the 1997 Annual Radioactive Effluent  !

Release Report were reviewed and discussed. The contents and l

conclusions of the reports were evaluated against the applicable '

sections (SS) of TSs 6.8 and 6.9.1. and S 7 of the Offsite Dose i

Calculation Manual (0DCM).

b. Observations and Findinas

The inspectors verified that the 1997 Radiological Environmental

Operating Report was prepared and submitted in accordance with TS and

ODCM requirements. Based on trend data for radionuclides concentrations  !

in offsite environmental matrices at control and indicator stations, no '

discernible offsite effects or trends were demonstrated from plant

effluent discharges to the environment. The licensee properly

determined the controlling receptor to evaluate the maximum dose to a

member of the public beyond the site boundary based on releases and

current land-use census data. From review of the 1997 environmental

monitoring program sam) ling deviations required by ODCM Section 7.1.2.4. l

the inspectors noted t1at community airborne particulate monitoring

,

station number (No.) 1108 was inoperable from approximately November 18.

1997, through January 27. 1998, due to construction at the electric

substation which supplied power to the equipment.. Farley Nuclear Plant

(FNP) Occurrence Report No. 973135. generated in response to finding the

! power off on November 25, 1997. initially documented that power would be

4

l Enclosure 2

I

'

. _ _ _ _ _ . . . _

_ - _____ - -_-____ _ _ -

.- .

.

33

interrupted for approximately two weeks. but an attached note indicated

that as of January 13. 1998. power had not been restored to the sampling

equipment. Corrective actions to 3revent recurrence, such as the use of

portable samplers or securing anotler source of electrical power within

the immediate vicinity was not addressed. The inspectors identified the

lack of detailed corrective actions to prevent recurrence of the

l extensive out-of-service condition due to a known power supply

l interruption. extending past the original two-week estimate, as an

environmental monitoring program weakness.

The 1997 Annual Radioactive Effluent Release Reports was submitted in

accordance with TS and ODCM requirements. For the raport period,

calculated offsite doses from liquid and gaseous effluent releases were

a small fraction of the ODCM limits.

c. _ Conclusions

for 1997, program activities to control, monitor and document liquid and

airborne radionuclides concentrations in effluents and in the offsite

environment were implemented effectively. No significant environmental

impact was identified. Projected offsite doses to the maximally exposed

individual were a small fraction of ODCM and 40 CFR 190 specified

limits.

Extensive delays in returning a community particulate air sampler to

service and lack of corrective actions to prevent recurrence was

identified as a program weakness.

R7 Quality Assurance in RP&C Activities

R7.1 Licensee Self-Assessment Activities (83750. 84750. 86750)

a Insoection Scooe

The ins)ectors reviewed implementation and status of the licensee's

Health 3hysics Observation program. Program implementation and results

were evaluated against commitments initially documented in an

October 25, 1996 licensee response to a Notice of Violation regarding

improper dosimetry use.

b. Observations and Findinas

The inspectors noted that observations of both Health Physics (HP) and

Dosimetry (DOS) practices continued. The observed data were assessed

for the most current 1000 observations made and sorted into 26 separate

ty)es of poor practices or issues. Each identified item was

subsequently assigned to one of twenty-three separate work groups.

Results routinely were presented to upper management and workers. For

identified error rates exceeding five and fifteen percent of the HP and

DOS practices observed. Occurrence Reports were initiated and additional

Enclosure 2

.

__

_ _ - _ _ _ _ _ _ _ - _ _ _ _ - _ _ _ _ - _ _ _ _ _ - _ _ _ . _ _ _ _ _ _ _ . _ _ - _ - _ _ _

.

.

...

,

34

l

L co'rrective' actions taken. From review of the licensee weekly

!

observation trend data for the U2RF12 outage, the inspectors noted that

the percent errors for both HP and DOS issues were reduced by

approximately 50 percent- relative to weekly data collected during the

I 3revious. Unit.1 Refueling Outage 14 (U1RF14) activities. For the

!

J2RF12 the majority of identified ~ issues were associated with incorrect

radioactive material . handling, violation of HP boundaries, spread of

contamination..and incorrect dress out;

- c. Conclusions-

The licensee HP and' DOS observation program continued to be implemented

effectively and contributed to the reduced personnel errors observed for

-U2RF12 activities.

R8. Miscellaneous RP&C Issues (83750, 84750)

R8.1 (C1osed) IFT 50-348.364/98-01-07: Review Licensee Actions ~ to Imoro've

Radioactive Material Container Label Effectiveness.

'In response to. inconsistencies and poor practices noticed for .

<

radioactive material container label types and information required by

10 CFR 20.1501; the licensee had assigned a senior HPT responsibility to

'

review and provide oversight. of the subject program area. Based on

improvements-in the radioactive material. container labeling program

activities-noted during the current inspection. period, this item is

closed'.

~ P2 Status of Emergency Preparedness (EP) Facilities, Equipment, and

Resources

- P2.1 Facilitv Insoection

a2 Insoection'Scoce (82701)

The inspectors examined the licensee's emergency response facilities

'(ERFs) and equipment to assess their adequacy and to determine whether

they were maintained in a state of operational readiness as specified in

the Farley Emergency Plan.

..

- b. Observations and Findinas

The' inspectors toured the Control Room. Technical Support Center (TSC).

Operational Support Center (OSC). Emergency Operations Facility (EOF),

and the alternate E0F. Selected equipment, supplies, and communications

L systems within these facilities were inspected. All tested equipment

r and systems were found to be in operable condition. The facilities were

L well-maintained.

b '

L Enclosure 2

. .

-_-_----._----_____-_.-___.__.-._-__--l _ _ _ . _ _ _ . _ _ _ . - - - _ . - _ _ . _ . - . - - _ . _ . . _ _ - - - - - - . - - . _ - . . - _ . _ ._ . - _ . . - - - - - _ _ _ - _ _ . . - - - - . . . - \

-

. .

..

,

35

c. Conclusions

.ERFs were well-equipped and operationally ready to support _an emergency..

P3- Emergency ~ Preparedness (EP) Procedures and Documentation

P3.1 Emeraency Plan

a. Insoection Scoce=(82701)

'The' inspectors reviewed recent revisions to the Emergency Plan to

' determine whether' changes were made in accordance with 10-CFR 50.54(q).

and )lan implementation. In addition..the implementation'of the plan of

' Marc 1 8. 1998. was reviewed.

,

-b. Observations ~and Findinas

The current revision of-the Emergency Plan was administrative in nature.

.The Emergency Plan was implemented'on March 8.1998, with a Notification-

-

of-Unusual Event (NOUE) due to high river water level. There was a

partial TSC activation and review of documentation revealed that the

requi. red notifications were completed in a timely manner,

c. -Conclusions

Changes to the Emergency Plan were made in-accordance with

. -The NOUE on March'8. 1998..was made in accordance with

~10 CFR 50.54(q)1an.

the Emergency P

P5 Staff Training and Qualification in EP.

P5.1 Trainina of Emeroency Resoonse Personnel

a. Insoection Scooe (82701)

The inspectors evaluated the training program for the Emergency Response

. Organization (ERO): through review of program documentation and

observation of licensee training' functions.

.

'

b. Observations and Findinas-

-The licensee conducted a program of periodic integrated response drills

~

'(typically six per- year)' to enhance the training for ERO personnel. In

an effort to gauge:the effectiveness of the emergency res)onse training

pr gram, the inspectors observed a previously scheduled ERO training

dr ll.on May_21. ERO personnel- activated the ERFs in a timely manner

and responded capably ~to the simulated emergency, which included event

classifications e f Alert. Site Area Emergency. and General Emergency.

Minor problems wdh the ER0's . response efforts. were identified by

licensee drill monitors for corrective action. The inspectors. also

Enclosure 2

L _ . -_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

D

p

...

. .-

.

36

L

lL ' observed an E0F tabletop drill on May 19 involving real-time setup of-

o

the- facility.and a round; table discussion of staff functions and -

interfaces,

c. Conclusions

The conduct of regular integrated drills enhanced the quality of ER0-

.

training. Drill monitors effectively identified response problems for

L. corrective actions. 'ERO personnel were adequately trained and responded

l- appropriately to a simulated event.

_P6- EP Organization and Administration

P6.1 EP Proaram Organization

i

'

a. Insoection Scooe (82701)

The inspectors reviewed this area to determine if changes in personnel

had occurred which could adversely affect the management and

implementation of the EP program.

[ b. ' Observations and Findinas

The organization of the EP program was reviewed and discussed with

L. -- -licensee management representatives. Two changes to the EP' organization

were noted. .The position of Emergency Planning Technician was.

reassigned in' September 1997-to an individual who had 3reviously been a

member of the radiation protection group at Farley. T11s individual's

3 professional development included a one-week training course in EP in

Jecember 1997.

A new Emergency Management Director for Houston. County was recently

aapointed. According to licensee management representatives, this

clange had not had a negative impact upon the working relationship

between the licensee and Houston County. The inspectors were informed

~

that no other significant changes in management )ersonnel for offsite

interface / support agencies had occurred during tie past two years.

c. Conclusions:

. No degradation had occurred in the EP program since the previous

inspection.

1

.. ,

Enclosure 2

L.

1

_ _ . _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ . _ _ _ _ _ _ _ _ _ - _ _ . - - _ _ - _ _ _ _ _ - . - _ _ _ _ _ _

__

,

.

.

37

P7 Quality Assurance in EP Activities

P7.1 10 CFR 50.54(t) Audit of Emeraency Preparedness Proaram

a. Insnection Scone (82701)

The inspectors reviewed this area to assess the quality of the required

annual audit of the emergency preparedness program, and to verify that

the audit met the requirements of 10 CFR 50.54(t).

b. Observations and Findinas

The inspectors reviewed documentation associated with the following EP

program audits conducted by the licensee's Quality Assurance (0A) group:

e Safety Audit and Engineering Review (SAER) Audit of Farley Nuclear

Plant-Emergency Planning Report No. 97-EP/16.

e SAER Audit of Farley Nuclear Plant-Emergency Planning

Report No. 96-EP/16-1.

The audits were thorough and independent, and the nature of the j

identified issues indicated inclusive understanding of the EP area by

the auditors. The audits provided evidence of the licensee's ability to J

l

self-identify emergency preparedness program issues.

c. Conclusions

The 1996 and 1997 EP program audits met the 10 CFR 50.54(t) requirement 3

for an annual independent audit of the EP program.

P7.2 Effectiveness of Licensee's Corrective Action Proaram for EP Issues

a. Insoection Scope (82701) <

The inspectors reviewed this area to evaluate the licensee's program for

identifying, tracking, and resolving problems in emergency preparedness.

b. Observations and Findinas

The licensee formally identified and tracked EP issues by means of the

" Emergency Planning Punchlist." The licensee's list of open EP items is

used to track all substantive findings, including many improvement items

derived from drill critiques and carried at the lowest priority.

Although the punchlist was maintained by the Emergency Planning

Coordinator and was not integrated with any plant-wide tracking system,

it was periodically distributed for updating by the assigned group for

each item. This method was effective for resolving identified EP

I

deficiencies and issues.

Enclosure 2

_ _ __

__ _ _ , _ .

,

-

.

38

c. [pnclusions

The licensee's program for identifying, tracking, and.resolv'ng problems

in EP was effective.

P8 Miscellaneous EP Issues

P8.1 (Closed) Insoector Follow-uo Item (IFI) 50-348. 364/96-14-01: Exercise

Weakness--Significant Emeraency Information Was Not Communicated to the

Acorooriate Emeraency Manaaer in a Timely Manner.

This exercise weakness from the 1996 full-participation exercise was

identified because significant emergency information was not

communicated to the appropriate emergency manager in a timely manner.

.The training drill observed by the inspectors on May 21, 1998. provided

the opportunity for the inspectors to focus on the transfer of emergency

information from the interim Emergency Director (ED) in the simulator to

the ED in the TSC. and later from the ED to the Recovery Manager in the

Enrgency Operations Facility. In all cases, the transfer of

inform:.ition was done clearly with repeat-backs to assure understanding,

and it was done timely. This item is closed.

51 Conduct of Security and Safeguards Activities

S1.1 Routine Observations of Plant Security Measures (71750)

The inspectors verified that selected portions of site security program

plans were being adequately implemented. Disabled vital area doors were

properly maned and controlled. Security personnel activities observed

during the inspection period were performed well. Site security systems

were adequately maintained and functional to ensure the physical

protection of the plant. However, the inspectors did identify two minor

instances in which Security personnel were not attentive to equipment

3roblems that adversely im) acted effectiveness of physical security

Jarriers: 1) Inoperative iCR door card reader green light (contrary to

alant policy egress was allowed without verifying green light) and 2)

1roken door latch on bullet hardened door outside PAP (door was blocked

open, rather than disabling latch and leaving door shut. Although not

specifically addressed by the Physical Security Plan (PSP), these

barriers were in a degraded condition without compensatory measures in

place. Once notified Security promptly resolved each instance.

Enclosure 2

l

l . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ -

_ --_- -_-----

,

.

A

39

S2 Status of Security Facilities and Equipment

S2.1 .P_rotected and Vital Area Access Control

a. Insoection Scope (81700)

i The inspectors reviewed the PSP to determine if the licensee's access

i

control program for personnel and packages met the commitments specified

therein.

b. Observations and Findinos

On April 21. the inspectors observed a reliability test conducted at the

Primary Access Portal (PAP). A disabled weapon was placed inside a

lunch cooler that was carried by a licensee individual with unescorted

access. The search officer immediately discovered the weapon and

detained the individual. The officer located in the final access

control booth appropriately locked the protected area turnstiles and

summoned assistance.

The inspectors reviewed records for 17 favorably terminated individuals

with respect to the licensee s action to remove unescorted access.

Procedure FNP-0-SP-11. ~Badgire Procedures." Rev.13. required that

changes in personnel access require'aents caused by termination of

employees will be reported immediately to the Security Site Manager.

The necessary action will be taken to remove the individuals' name from

access. In addition, procedure FNP-0-AP-42. " Access Control." Rev. 26.

Section 7.5.3. required that individuals' names be removed from the

appropriate access list immediately upon termination of need.

Of the 17 records reviewed the inspector determined that 8 of the

individuals did not have their unesc'orted access removed from the

security computer ranging from 1 to 11 days after the individual had

been terminated. All eight individuals had access to protected and

vital areas: however, no individual accessed those areas after

termination. Security removed access upon notification.

The inspector determined that although procedures did exist.

clarification was needed as to contractors * responsibilities. Neither

procedure had a process in place to ensure that contractor personnel who

no longer needed unescorted access were immediately removed from the

security com) uter. The inspector reviewed a Change Order (CO) for a

contractor w1ich was currently providing work at FNP and found that the

C0 simply stated to follow access procedures.

The failure to immediately report terminations of 8 employees to the

Security Department is identified as Violation 50-348, 50-364/98-03-07.

Failure To Promptly Terminate Security Access.

Enclosure 2

.

__

. _ _ _ _ _ -- _ - - - _ _ _ - _ _ _ _ _ _ _ _ - _ _ _ _ _

, *

.

I-

'

40

l c. Conclusions-

The licensee was a)propriately searching individuals and packages prior

i to entrance into t1e protected area. The failure to include a

,

'

documented process in access control procedures for contractors to

timely inform Security of terminated individuals contributed to a

violation for failure to immediately terminate 8 individuals' unescorted

access.

! S2.2 Protected Area Detection

a. Insoection Scone (81700). a

l

The inspectors evaluated the licensee's protected area detection

capability to determine if provisions of Section 5.3 of the PSP were

met.

b. Observations and Findings

On April 22. the inspectors observed the licensee test two perimeter

zones. Both zones alarmed appropriately. The inspector additionally i

performed a walkdown of the aerimeter and determined that the design. l

placement, and coverage of tie' intrusion detection system met the

'

requirements specified in the PSP.

c. Conclusions  :

A test of two perimeter zones identified that they alarmed

appropriately. A walkdown of the perimeter intrusion detection system

identified that design. placement, and coverage met the requirements of 4

the PSP. l

S2.3 . Protected and Vital Area Barriers

a. Insoection Scooe (81700)  !

Section 3 of the PSP outlined protected and vital area barriers that are

in place at FNP. The inspectors evaluated those barriers to ensure that

the criteria were being met,

b. Observations and Findinas

The inspector performed a walkdown of 3rotected and vital area barriers.

Fences and gates were intact and met tie overall height requirement.

Manholes were appropriately secured and isolation zones were free and

clear to assure a distinct field of vision. Protected area barriers

were separated from vital area barriers.

Enclosure 2

- _ _ _ _ _ _ _ _ _ _ _ _ -_ ._ _ -

_ - - _ _ _ _ _ _ _ _ - - - _ _ - _

-

.

I

41 ,

l

Vital area barriers were appropriately in place and contained no )

openings greater than 96 square inches. Vital c:rea doors were locked I

and alarmed. Access was controlled by a security focce member, card

reader, or the Central / Secondary Alarm Stations. The inspector

accompanied a security officer who performed vital area door checks as

part of his post. All vital area doors were secured and alarmed in the

Central and Secondary Alarm Stations when opened. Vital area

penetration points were secured by locks, alarms, or welded in place.

FNP-0-SP-30. " Declassification of Vital Area / Systems / Equipment." Rev. O.

dated March 11, 1994, was reviewed by the inspector. The licensee

devitalized four valve boxes during Mode 5 of the outage. This

devitalization of equipment met procedural requirements.

c. Conclusions

Protected and vital area barriers were appropriately placed, maintained,

and secured as specified in Section 3 of the PSP. The licensee followed

procedure to devitalize equipment during Mode 5 of the outage. j

S3 Security ana Sifeguards Procedures and Documentation

l

S3.1 Security Procram Plans

a. Insoection Scoce (81700)

To determine if requirements were met, the inspectors reviewed Rev. 8 of

the Training and Qualification Plan, which was subnitted under

10 CFR 50.54(p).

b, Observations and Findinos

Revisions to the Training and Qualification Plan met the requirements of

10 CFR 50.54(p). Administrative changes and clarification statements

were also noted.

c. Conclusions

A revision to the Training and Qualification Plan did not decrease the

effectiveness of the plan and met the requirements of 10 CFR 50.54(p).

l

l

!

I

f Enclosure 2

l

_,

I

.

'

.

42

l S4 Security and Safeguards Staff Knowledge and Performance

S4.1 Resoonse Capabilities

a. Inspection Scooe (81700)

The inspectors reviewed and evaluated the licensee's response force

strategy to determine if the licensee was capable of engaging an

adversary force to preclude penetration of vital area barriers and any

act intended to cause a significant release of radioactivity.

b. Observations and Findinas

The inspector reviewed the Security Response Plan. Rev 5 and drill

critiques for the last two quarters. Three of the four res)onse teams

participated in the drills and the fourth team performed taaletop

exercises. In addition, the inspector discussed with licensee

representatives the current strategy. Target sets established by the

licensee for the 1995 Operational Safeguards Response Evaluation (OSRE)

remained current.

c. Conclusion

The licensee had in place a sound strategy that was capable of

protecting vital equipment from acts intended to cause a significant

release of radioactivity.

S8 Miscellaneous Security and Safeguards Issues

S8.1 Actions on Previous Insoection Findinas (92904)

(Ocen) IFI 50-348. 364/97-02-01: Failure to Provide Locks of

Substantial Strenath to Prevent Tamnerina

The licensee had changed FNP-0-SP-10. " Patrol Procedures." Rev. 16. to

require the motor patrol to physically check the locks every four hours.

once per shi ft. In addition. the locks selected by the licensee were

susceptible to damage by hand tools, creating a possible vulnerability.

The licensee had purchased more substantial locks. However, the

evaluation of the lock covers was still underway. This IFI remains open

pending the completion of the licensee's evaluation.

Enclosure 2

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43.

(Closed)'IFI 50-348; 364/97-13-01
Questionable Planned Biometrics

l  ; Implementation.

'The licensee was installing and testing the use of biometrics for access

. control in the protected areas. The-licensee had determined that the

l

Service Water- Intake Structure (SWIS) a separate protected area, would

ibe controlled by portable biometric units. Procedures were in ) lace to=

process employees from one protected area to the other.. This III is

. closed.

~ S8.-2 Protection of Safeauards Information

a. =Insoection Scooe (81810)

An evaluation of the licensee's program to protect Safeguards

Information-(SGI) under the provision of 10 CFR 73.21 was conducted.

! b. ' Observations and Findinas

.The inspector reviewed and evaluated FNP-0-AP-72. " Protection of

Safeguards Information." and determined that all components of

10 CFR 73.21 were incorporated. The licensee currently-is storing

, Safeguards Information at various locations. The inspector toured all

areas and randomly checked Ge1eral Services Administration-(GSA)

approved safes to ensure that they were locked. In addition, in

Document-Control, the inspector selected non-Safeguards a) proved

. containers and selected files to ensure that'SGI was not )eing stored at

these locations' All.SGI was appropriately stored.

.

Through discussion with licensee representatives, the inspector

determined that SGI was logged transported, and given to only those

individuals with fingerprints.on file and with a need to know.

c. ' Conclusions

Safeguards -Information was appropriately handled and stored as specified d

-in'10 CFR-73.21.

F2 .-Status of Fire Protection Facilities and Equipment

F2.1'-(Oce'n)'URI 50-348; 364/98-01-10: Pre-Action Sorinkler System Failures

-(71750)

On May 19. 1998, a. conference call was held between the resident staff,

~','

.NRR. Plant Farley personnel, and Farley Project personnel in Birmingham

to; discuss the status'of this issue. The licensee reported that an ,

Enclosure 2

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44

equipment problem root cause team had been assembled, including

representation from the nuclear industry. The team had met at the

l- . vendor's site and reviewed the problem. No conclusion concerning the

failure cause had been identified. However, the team continued its

evaluation.

V. Manaaement Meetinas and Other Areas {

X1 Review of Updated Final Safety Analysis Report (UFSAR) Commitments

While performing the inspections discussed in this report. the

inspectors reviewed the applicable portions of the UFSAR that related to 1

the areas inspected. The inspectors verified that the UFSAR wording was I

consistent with the observed plant practices, procedures and/or

parameters. The inspectors identified that FSAR Section 5.2.2.3 stated,

" Pressurizer pressure is sensed by fast response pressure transmitters l

with a time response of better than 0.2 seconds." This is faster than {

the acceptance criteria of 0.23 seconds used by the licensee for testing i

the pressurizer pressure transmitters. This is not safety-significant

because the pressurizer pressure instruments currently installed have

response times faster than 0.2 seconds. This was provided to the

licensee for resolution.

X2 Exit Meeting Summary

i

The inspectors presented the inspection results to members of licensee l

management on June 4 and June 25, 1998, after the end of the inspection I

. period. The licensee acknowledged the findings presented. l

The inspectors asked the licensee whether any materials examined during I

the inspection should be considered proprietary. No proprietary

information was identified.

1

PARTIAL LIST OF PERSONS CONTACTED

Licensee

R. Badham. Supervisor, Safety Audit and Engineering Review (SAER)

P. Crone. Engineering Support (ES) Performance Supervisor

K. Dyer. Security Manager, Farley Nuclear Plant

T. Esteve. Planning & Control Supervisor

R. Fucich ES Manager

S. Fulmer. Plant Training and Emergency Preparations Manager

S. Gates. Administration Manager

D. Grissette. Operations Manager

R. Hill. General Manager

D. Jones. Configuration Management Manager

W. Lee, Emergency Preparedness Coordinator (corporate office)

Enclosure 2

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i

l T. Livingston. Chemistry Superintendent

R. Martin. Maintenance Team Leader

M. Mitchell.'HP Superintendent

C. Nesbitt. Assistant General Manager. Plant Support

W. Oldfield Nuclear Operations Training Supervisor

L. Revels. Assistant Security Manager. FNP

M. Stinson. Assistant General Manager. Operations

R. Vanderbye. Emergency Planning Coordinator

G. Waymire. Technical Support Manager

G. Wilson. SNC Corporate Senior Engineer

R. Winkler. Engineering Group Supervisor. PMMS

B. Yance. Plant Modifications and Maintenance Support Manager ,

1

'

NRC

J. Zimmerman NRR Project Manager

l

l

INSPECTION PP9CEDURES USED

IP 37001: 10 CFR 50.59 Safety Evaluation Program ,

IP 37551: Onsite Engineering  !

IP 40500: Effectiveness of Licensee Controls In Identifying. Resolving and

Preventing Problems

IP 60710: Refueling Activities ',

IP 61726: Surveillance Observations  ;

IP 62707: Maintenance Observations

IP 71707: Plant Operations  !

IP 71711: Plant Startup from Refueling  !

IP 71750: Plant Support Activities

IP 73753: Inservice Inspection .

IP 81700: Physical Security Program for Power Reactors

IP 81810: Control of Safeguards Information l

IP 82701: Operational Status of the Emergency Preparedness Program

IP 83750: Occupational Radiation Exposure

IP 84750: Radioactive Waste Treatment, and Effluent and Environmental

Monitoring

IP 86750: Solid Radioactive Waste Management and Transportation of

Radioactive Materials >

IP 92700: Onsite Follow-up of Written Reports of Nonroutine Events at Power

Reactor Facilities

IP 92903: Followup - Engineering

IP 92904: Followup - Plant Support

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l Enclosure 2

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ITEMS OPENED, CLOSED, AND DISCUSSED

Tyng Item Number Description and Reference

Ooen

IFI 50-348, 364/98-03-01 Inadequate Thread Engagement

(Section M1.3).

IFI 50-364/98-03-03 Rod Control Fuse Failures (Section M1.4).

VIO . 50-348, 364/98-03-04 Inadequate Safety Assessment for Mis-wired

Hot Shutdown Panel MOVs (Section E8.1).

EEI 50-348, 364/98-03-05 HSDP Loss of Function Inadequate Safety

Evaluation (Section E8.1).

VIO 50-348, 364/98-03-06 Inadequate Corrective Actions for MCR

Ventilation System (Section E8.5).

VIO 50-348, 364/98-03-07 Failure to Promptly Terminate Security

Access (Section S2.1).

Closed

i

NCV 50-364/98-03-02 Failure to Report Manual Reactor Trip in a

Timely Manner (Section M1.4).

LER 50-348, 364/97-10-01 Motor Operated Valve Local - Remote

Control Circuit Wiring Discrepancies 1

(Section E8.1).

URI 50-348, 364/98-01-04 Inadequate Safety Assessment for Mis-wired

Hot Shutdown Panel MOVs (Section E8.1).

VIO 50-348, 364/97-11-04 Failure to Implement a Test Program for

Service Testing of the TDAFW Battery

(Section E8.2).

URI 50-348, 364/98-01-05 Failure to Track and Correct Conditions

Adverse to Quality (Section E8.5).

IFI 50-348, 364/98-01-06 Control Room Ventilation Testing

(Section E8.5).

IFI 50-348. 364/98-01-07 Review Licensee Actions to Improve

Radioactive Material Container Label

Effectiveness (Section R8.1).

Enclosure 2

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- IFl 50-348, 364/96-14-01 Exercise Weakness--Significant Emergency

Information Was Not Communicated to the

Appropriate Emergency Manager in a Timely i

Manner (Section P8).

'

IFI 50-348, 364/97-13-01- Questionable Planned Biometrics

Implementation (Section S8.3).

Discussed

VIO 50-348, 364/97-11-03 TDAFW Battery Installation and Check Valve

Test Deficiencies (Section E8.3).

URI 50-348, 364/98-01-10 Pre-Action Sprinkler System Failures

(Section F2.1),

.

'

IFI ~50-348.-364/97-02-01 Failure to Provide Locks of Substantial

Strength to Prevent Tampering

(Section S8.1).

I

Enclosure 2