IR 05000348/2019001
| ML19130A196 | |
| Person / Time | |
|---|---|
| Site: | Farley |
| Issue date: | 05/10/2019 |
| From: | Alan Blamey NRC/RGN-II/DRP/RPB2 |
| To: | Kharrl C Southern Nuclear Operating Co |
| References | |
| IR 2019001 | |
| Download: ML19130A196 (9) | |
Text
May 10, 2019
SUBJECT:
FARLEY UNITS 1, 2 - NUCLEAR REGULATORY COMMISSION INTEGRATED INSPECTION REPORT 05000348/2019001 AND 05000364/2019001
Dear Mr. Kharrl:
On March 31, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Farley Units 1, 2. On April 23, 2019 the NRC inspectors discussed the results of this inspection with Daniel Komm and other members of your staff. The results of this inspection are documented in the enclosed report.
The NRC inspectors did not identify any finding or violation of more than minor significance.
This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA/
Alan J. Blamey, Chief Reactor Projects Branch 2 Division of Reactor Projects
Docket Nos.: 05000348 and 05000364 License Nos.: NPF-2 and NPF-8
Enclosure:
Inspection Report 05000348/2019001 and 05000364/2019001
Inspection Report
Docket Number(s):
05000348 and 05000364
License Number(s):
Report Number(s):
05000348/2019001 and 05000364/2019001
Enterprise Identifier: I-2019-001-0024
Licensee:
Southern Nuclear Operating Co., Inc.
Facility:
Farley, Units 1 and 2
Location:
Columbia, Alabama
Inspection Dates:
January 1, 2019 to March 31, 2019
Inspectors:
P. Meier, Senior Resident Inspector
K. Miller, Resident Inspector
Approved By:
Alan J. Blamey, Chief
Reactor Projects Branch 2
Division of Reactor Projects
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees
performance by conducting a Quarterly inspection at Farley Units 2 and 1 in accordance with
the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for
overseeing the safe operation of commercial nuclear power reactors. Refer to
https://www.nrc.gov/reactors/operating/oversight.html for more information. Findings and
violations being considered in the NRCs assessment are summarized in the table below.
List of Findings and Violations
No findings were identified.
Additional Tracking Items
None.
PLANT STATUS
Unit 1 began the report period at or near 100 percent rated thermal power (RTP). On February
19, the Unit 1 reactor was shut down to mode 3 to troubleshoot and repair issues with the main
generator hydrogen cooler. Following this work, Unit 1 was returned to mode 1 on February 25
and achieved 100 percent RTP on March 6. Unit 1 stayed at or near 100 percent RTP for the
remainder of the report period.
Unit 2 began the report period at approximately 100 percent RTP and maintained that power
level for the entire report period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in
effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with
their attached revision histories are located on the public website at http://www.nrc.gov/reading-
rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared
complete when the IP requirements most appropriate to the inspection activity were met
consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection
Program - Operations Phase. The inspectors performed plant status activities described in
IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem
Identification and Resolution. The inspectors reviewed selected procedures and records,
observed activities, and interviewed personnel to assess licensee performance and compliance
with Commission rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.01 - Adverse Weather Protection
Seasonal Extreme Weather Sample (IP Section 03.02) (1 Sample)
The inspectors evaluated readiness for seasonal extreme weather conditions prior to the
onset of seasonal cold temperatures from January 29, 2019, to January 30, 2019, for the
following systems (FNP-0-SOP-0.12):
Main Steam Valve Room
Main Feedwater
71111.04 - Equipment Alignment
Partial Walkdown (IP Section 02.01) (3 Samples)
The inspectors evaluated system configurations during partial walkdowns of the following
systems/trains:
(1)
Unit 1 'A' train residual heat removal system while 'B' train was inoperable for testing
on January 3, 2019, (P&ID D-175041).
(2)
Unit 2 'B' train penetration room filtration system while A train was inoperable for a
maintenance outage on February 5, 2019, (P&ID D-205022).
(3)
Unit 1 B train residual heat removal system while A train was inoperable for testing
on February 6, 2019, (P&ID D-205041).
71111.05A - Fire Protection (Annual)
Annual Inspection (IP Section 03.02) (1 Sample)
The inspectors evaluated fire brigade performance on February 13, 2019.
71111.05Q - Fire Protection
Quarterly Inspection (IP Section 03.01) (4 Samples)
The inspectors evaluated fire protection program implementation in the following selected
areas:
(1)
Fire area 1-040, fire zone 318, Unit 1 cable spreading room on March 25 - 28, 2019
(FNP-1-FPP-1.0).
(2)
Fire area 1-034, fire zone 317, Unit 1 penetration room and filtration system
equipment room on March 25 - 28, 2019 (FNP-1-FPP-1.0).
(3)
Fire area 1-041, fire zone 335, train 'A' 4kv / 600v switchgear room on March 25 - 28,
2019 (FNP-1-FPP-1.0).
(4)
Fire area 1-041, fire zone 343, train 'A' 4kv / 600v switchgear room on March 25 - 28,
2019 (FNP-1-FPP-1.0).
71111.06 - Flood Protection Measures
Inspection Activities - Internal Flooding (IP Section 02.02a.) (1 Sample)
The inspectors evaluated internal flooding mitigation protections in the:
Unit 1 residual heat removal system heat exchanger room on March 12, 20192019 (Calc #
BM-99-1932-001, Internal Flood Assessment).
71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)
The inspectors observed and evaluated licensed operator performance in the Control Room
during a Unit 1 down power to address a main generator cooler leak on February 19, 2019.
Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)
The inspectors observed and evaluated Simulator Exam Scenario, 19-1 As-Left Exam, for
crew 5 involving various instrumentation failures, a reactor trip, a spurious safety injection,
and an event notification on January 31, 2019.
71111.12 - Maintenance Effectiveness
Routine Maintenance Effectiveness Inspection (IP Section 02.01) (2 Samples)
The inspectors evaluated the effectiveness of routine maintenance activities associated with
the following equipment and/or safety significant functions:
(1)
U1 main generator hydrogen cooler leak on February 19, 2019 (WO SNC999419).
(2)
Unit 1 and Unit 2 emergency diesel generators (NMP-ES-002, revision 22).
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Risk Assessment and Management Sample (IP Section 03.01) (4 Samples)
The inspectors evaluated the risk assessments for the following planned and emergent work
activities:
(1)
High voltage switchyard high-risk work on January 18, 2019 (NPM-GM-031).
(2)
Unit 2 elevated risk while the 2C emergency diesel generator was out of service for
maintenance on January 22, 2019 (NPM-GM-031).
(3)
Unit 1 and Unit 2 elevated risk while the spent fuel pool cooling, the 2B Emergency
Diesel Generator, and Unit 1 water-based fire suppression and hose stations were
out of service for maintenance on January 28, 2019 (NPM-GM-031).
(4)
Unit 1 main generator hydrogen cooler leak on February 19, 2019 (NPM-GM-031).
71111.15 - Operability Determinations and Functionality Assessments
Sample Selection (IP Section 02.01) (5 Samples)
The inspectors evaluated the following operability determinations and functionality
assessments:
(1)
Cracks on the 2A vital DC battery cells identified on January 13, 2019 (CR
10570713).
(2)
Gas accumulation monitoring on Units 1 and 2 at charging pump suction piping high
points on February 4, 2019 (CR 10578892).
(3)
Unit 1 ('B' train) motor driven auxiliary feedwater pump failure to start from the main
control board following local start surveillance on January 30, 2019 (CR 10576713).
(4)
Unit 2 'B' train emergency diesel generator sequencer logic failed to reset while
testing on January 17, 2019 (CR 10576737).
(5)
Unit 1 and Unit 2 movable incore detector systems and heat flux hot channel factor
and nuclear enthalpy rise hot channel factor (CR 10586445 / 10586321).
71111.18 - Plant Modifications
Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (1
Sample)
The inspectors evaluated the following temporary or permanent modifications:
Unit 1 'A' main steam isolation valve steam leak repair on February 25, 2019 (WO
SNC1001137).
71111.19 - Post Maintenance Testing
Post Maintenance Test Sample (IP Section 03.01) (6 Samples)
The inspectors evaluated the following post maintenance tests:
(1)
After replacement of EL09, feeder circuit breaker, in motor control center 1L on
January 2, 2019 (WO SNC837324).
(2)
'2A' Charging Pump Quarterly Inservice Test, after replacement of the pump mini-flow
check valve, Q2E21V0121A, on January 9, 2019 (WO SNC785642).
(3)
'2C' Emergency Diesel Generator operability test, after completion of a planned
maintenance outage on January 26, 2019 (WO SNC586812).
(4)
Unit 2 'A' battery charger DC voltage sensing board calibrations on February 11, 2019
(WO SNC952450).
(5)
Unit 2 'A' penetration room filtration system suction damper dual indication repair on
February 11 - 15, 2019 (WO SNC997132).
(6)
Unit 2 'C' Charging Pump speed increaser bearing replacement 3/19-3/30 (WO
SNC883382 & WO SNC966089).
71111.22 - Surveillance Testing
The inspectors evaluated the following surveillance tests:
In Service Testing (IST) (IP Section 03.01) (1 Sample)
Unit 1 'C' Charging Pump Inservice test (FNP-1-STP-4.3) on January 2, 2019.
Surveillance Testing (IP Section 03.01) (4 Samples)
(1)
Unit 1 'B' train Residual Heat Removal Pump Quarterly Inservice Test (FNP-1-STP-
11.2), on January 3, 2019.
(2)
Unit 1 Turbine Driven Auxiliary Feedwater Pump quarterly Inservice test (FNP-1-STP-
22.16), on January 10, 2019.
(3)
Unit 1 'B' Train Motor Driven Auxiliary Feedwater Pump surveillance testing from the
hot shutdown panel control station (FNP-1-STP-73.1, Appendix M) on January 31,
2019.
(4)
Unit 2 'B' train sequencer operability test (FNP-2-STP-226.1) on January 17, 2019.
71114.06 - Drill Evaluation
Drill and/or Simulator-Based Licensed Operator Requalification Training (IP Section 02.01) (1 Sample)
The inspectors observed and evaluated a simulator-based licensed operator requalification
involving complications to manually trip the reactor, a spurious safety injection, and an event
notification on January 31, 2019.
OTHER ACTIVITIES - BASELINE
71151 - Performance Indicator Verification
The inspectors verified licensee performance indicators submittals listed below:
IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01) (2 Samples)
(1)
Unit 1 (January 1, 2018 - December 31,2018)
(2)
Unit 2 (January 1, 2018 - December 31,2018)
IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 02.02) (2
Samples)
(1)
Unit 1 (January 1, 2018 - December 31,2018)
(2)
Unit 2 (January 1, 2018 - December 31,2018)
IE04: Unplanned Scrams with Complications (USwC) Sample (IP Section 02.03) (2
Samples)
(1)
Unit 1 (January 1, 2018 - December 31,2018)
(2)
Unit 2 (January 1, 2018 - December 31,2018)
INSPECTION RESULTS
No findings were identified.
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
- On April 23, 2019, the inspector presented the quarterly resident inspector inspection results
to Daniel Komm and other members of the licensee staff.