ML20198N996
ML20198N996 | |
Person / Time | |
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Site: | Farley |
Issue date: | 12/29/1997 |
From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
To: | |
Shared Package | |
ML20198N914 | List: |
References | |
50-348-97-14, 50-364-97-14, NUDOCS 9801210292 | |
Download: ML20198N996 (36) | |
See also: IR 05000348/1997014
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- U.S.-NUCLEAR REGULATORY COMMISSION.(NRC); i
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-REGION II ,
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Docket Nos: - 50-348 and 50-364' ,
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License Nost NPF-2 and NPF 8' '
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' Report No: _50-34d/97-14 and 50-364/97-l'4-
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'Licenseci -Southern Nuclear Operating Company (SNC) ,
Facility: Farley Nuclear! Plant (FNP) ' Units ~1 and 2
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~ Locat'an: .7388 North State Highway 95
Columbia. AL 36319- :
Dates: l0ctober-19_through November'29. 1997
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Inspectors: T. Ross. Senior Resident Inspector (SRI)
J Bartley. Resident-Inspector (RI)
R. Caldwell. RI:
G. Kuzo.. Region II.- Health Physics Inspector _ _
(Sections R1.1. R1.2. R1.3. R1.4.-R1.5, R3.1. -
-R8.1,.R8.2. and:R8.3)
N. Merriweather. Region II, Reactor Inspector
.(Section E8.1)
Approved by: J. Johnson. Director
Division of Reactor Projects
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EXECUTIVE SUMMARY
Farley NLlear Power Plant. Units 1 and 2
NRC fnspection Report 50-348/97 14. 50 364/97-14
This integrated inspection included aspects of licensee operations,
engineering, maintenance, and plant support. The report covers a 6-week
period of onsite resident inspector inspections.
Doerations
e Operator attrntiveness to main control board (MCB) annunciator alarms
and response to changing plant conditions were pronpt. Management's
persistent efforts to reduce the number of MCB deficiencies and achieve
" blackboard" remained evident. Operating crews demonstrated a high
level of awareness of plant conditions and ongoing activities. Shift
supervisor command and control functions and operations management
oversight ware evident (Section 01.1).
e Overall material conditions for Unit 1 and Unit 2 structures. systems
and components (SSCs) were good. However, physical and material
conditions of the service water intake structure (SWIS), especially the
lower level, have degraded (Section 02.1).
- Safety system walkdowns and tours verified that accessible portions of
selected systems were adequately maintained and operational
(Section 02.2).
- Safety tagging activities were correct and met procedural requirements
(Section 02.3).
e A non cited violation (NCV) was identified for inadequate implementation
of the cold weather protection procedures. In addition, an Operations
supervior and management on day shift were not well-informed about the
progress of the procedures (Section 02.7).
Maintenance
o Maintenance and surveillance testing activities were generally conducted
in a thorough and competent manner by qualified individuals in
accordance with plant procedures and work instructions (Section M1.1),
e A NCV was identified for maintenance technicians failing to sign off
steps in " Continuous Use" procedures as they were accomplished
(Section M1.1).
- The 1-2A Diesel Generator maintenance outage was performed oy well
qualified and knowledgeable personnel. Corrective action efforts were
thorough. Post maintenance testing was satisfactorily comp hted
(Section M1.2).
Enclosure 2
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e A violation was identified for failure to take adequate corrective
actions to maintain the main steam valve room cork seal flooding barrier
(Section M8.1).
- Licensee corrective actions to date to address multiple pre-action
s)rinkler system failures identified in 1996 have been comprehensive.
taorough and generally successful. An additional corrective action plan
has been initiated to resolve the small number of remaining failures
(Section M8.2).
- A non cited violation was issued for failure to follov; work control
.rocedures
, which resulted in inoperability of automatic turbine building
isolation (Section M8.4).
Enaineerinq
e Licensee management met with the NRC in Rockville. Maryland to discuss
currer.t progress and schedules c' .he Steam Generator Replacement
Projects fcr the Unit I during Spring 2000 and Unit 2 during Spring
2001. During the meeting the licensee provided a comprehensive summary
presentation of its schedule. scope of work, organization, proposed
licensing submittals, and engineering plans (Section El.1).
- A violation was identified for lack of tornado missile protection for
the Turbira-Driven Auxiliary feedwater (TDAFW) pump vent stack.
(Section E8.1)
Plant Support
e Radiological controls. area postings and container 16 oles were
maintained in accordance wit 1 Technical Specification (TS) and
10 CFR 20. Anpendix J requirements. Improvements were noted for
Radiological Controlled Area housekee)ing and cleanliness and for
Radiological Work Permit practices. Revisions to local area radiation
survey map for the Unit 1 SFP area were timely. For UlRF14 outage,
ALARA program activites were implemented in accordance with approved
procedures. Actual UlRF14 outage dose expenditure exceeded original
estimates and resulted from an increased scope of steam generator
maintenance activities (Section R1.1).
e Worker deep dose equivalent (DDE) and shallow dose equivalent (SDE)
exposures resulting from aersonnel contamination events and work
activities during the UlR 14 outage were evaluated properly and were
within 20 CFR 20.1201 limits (Section Rl.2).
e (.antrols for minimizing workers' internal exposure were effective
(Section Rl.3).
- Surveillance requirements for the inoperable U1 RE-60B monitor were
completed in accordance with approved procedures (Section R1.4).
Enclosure 2
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e Licensee program guidance for transportation of radioactive waste and
materials met 10 CFR 71.5 and recently revised DOT 49 CFR Parts 100-179
requirements. Transportation program guidance was implemented
effectively (Section RI.5).
- Records for <ietermining workers' prior yearly occupational exposures and
granting extensions to administrative exposure limits were established
in accordance with 10 CFR Part 20. Subpart L requirements and
administrative procedures (Section RJ.1).
- A NCV was identified for Failure to Conduct Compensatory Grab Sampling
for inoperable Unit 2 Containment Atmospheric Radiation Monintoring
System in accordance with TS 3.4.7.1 (Section R8.3).
- Licensee corrective actions for failing to staff the Emergency
0)erations facility (EOF) within the required time frame were prompt and
tlorough. The licensee successfully demonstrated the ability to
activate the alternate EOF (Section Pl.1).
e S urity perconnel observed during the inspection period were attentive
tt their res :sibilities. Site security systems were adequate to
ensure physical protection of the plant (Section 51.1).
- A technician willfully failed to corduct at least three required
inspections, and deliberately falsified at least four checklists. This
non repetitive, licensee-identified and corrected violation was
identified as a NCV (Section P8).
Enclosure 2
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Report Details
Sumary of Plant Status
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Unit 1 operated continuously at 100% power for the entire inspection period. '
Unit 2 operated continuously at 100% power for the entire inspection period.
I. Operations
01 Conduct of Operations
01.1 Routine Observations of Control Room Doerations
a. Insoection Scoce (71707)
Inspectors conducted frequent inspections of ongoing plant operationc in
the Main Control Room (MCR) to verify proper staffing. operator ,
attentiveness. adherence to approved operating procedures,
communications, and command and control of operator activities.
Inspectors reviewed operator logs and Technical S)ecification (TS)
Limiting Conditions of Operation (LCO) tracking sleets, walked down the
Main Control Boards (MCBs), and interviewed members of the operating
shift crews to verify operational safety and compliance with TSs. The
inspectors frequently attended morning plant status meetings and shift
turnover n' tings to maintain awareness of overall facility operations,
maintenaru act. . ities, and recent plant evolutions. Horning reports
and Occurrence Reports (OR) were reviewed on a routine basis to assure
that the licensee properly tracked. reported, and resolved potential
operational safety concerns.
b. Observations and Findinas
Overall control and awareness of plant conditions during the inspection
period remained a strength. Inspectors observed that the Unit 1 MCB
annunciators and Balance of Plant (BOP) and emergency )ower board (EPB)
alarm panels were frequently " blackboard." However, tie Unit 2 MCBs and
B0P panels continued to have some persistent annunciators lighted for
known equipment problems. Management efforts to maintain MCB
deficiencies at low levels continued. The combined MCB deficiencies on
Unit I and Unit 2 have dropped below 10. the lowest level in several
years. Most of the deficiencies involved non-safety related
instrumentation or equipment, and none resulted in a TS LCO.
0)erator attentiveness to MCB annunciator alarms and response to
clanging plant conditions were prompt and effective. Interviews with
members of the operating crew verified that they were consistently aware
of plant conditions and ongoing activities. Operator knowledge was very
good. Operator logs were of sufficient detail and scope. Shift
staffing was verified to be in compliance with procedural and TS
requirements. Pre-shift briefings of the operating crews by the shift
supervisors (SS) were generally concise, informative. and provided
Enclosure 2 >
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operators with shift direction and priorities. Shift turnovers were
'omplished in an orderly m:nner, following a board walkdown by the off going
m a on coming operators and SSs.
Routine reactivity manipulations by the o)erators (i.e., boron
dilutions of the reactor coolant system (RCS)) were observed by
the inspectors. The operators notified the applicable SS prior to
each manipulation, as required by procedure.
c. Conclusions
Control Room professionalism and communications remained good
Operatingcrewdemeanor,teamworkandconductwerebusiness-like
and effective. Unnecessary activities were kept out of the
" Controls Area." Unit SS command and control, and operations
management oversight were evident.
0)erator attentiveness to MCB annunciator alarms and response to
clanging plant conditions were prompt. Management's efforts to achieve
- blackboard" conditions and reduce the number of HCB deficiencies
remained evident. The operating crew consistently demonstrated a high
level of awareness of existing plant conditions and ongoing plant
activities.
02 Operational Status of Facilities and Equipment
02.1 General Tours of Specific Safety Related Areas (71707)
General tours of safety-related areas were performed by the inspectors
throughout both units to examine the physical condition of plant
equipment and structures. and to verify that safety systems were
properly aligned. These general walkdowns included the accessible
portions of safety-related structures. systems, and components (SSC).
Overall material conditions for Unit I and Unit 2 SSCs were good.
Almost all plant areas were clear of trash and debris. Minor equipment
and housekeeping problems identified by the inspectors during their
routine tours were reported to the responsible SS and/or maintenance
department for resolution. Tnese problems included improper storage of
combustible materials, minor boric acid leaks and/or deposits unsecured
items located near safety-related equipment, corroded components, etc.
None of the problems constituted a significant safety or compliance
issue. Two such findings identified by the inspectors during routine
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plant tours included the following:
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Physical and material conditions of the service water intake
structure (SWIS), especially the lower level, have degraded
Enclosure 2
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considerably since past efforts to improve this area. Specific
inspector observations included: 1) multiple roof leaks (upper
and lower levels) that resulted in flooding of floor spaces. 2)
service water system (SWS) pump discharge pipe exhibits surface
rust where it penetrates the floor 3) corrosion and pitting of
SWS discharge piping was still evident inside the penetration of
the north wall of SWIS, and 4) physical and material conditions of
the lower level have degraded appreciably - soiled floors, spider
webs system leaks with associated wet floors, and painted over
rust on many system components (especially SWS strainers).
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A minor electro hydraulic control (EHC) fluid leak (1 to 2
drops / minute) from the 28 intercept valve, identified by
Deficiency Resort (DR) 547529, appeared to have gotten worse.
Also, the leac was being captured by adsorbents that were
saturated. resulting in a floor spill. Aside from a slipping
hazard, the use of adsorbents was not consistent with the Material
Safety Data Sheet (MSDS) for Fyrquei, which recommended using
inert material to absorb leaks / spills.
On November 20. 1997, an inspector accompanied a system operator (50) on
a watchstation tour of the Diesel Generator (DG) Building, which
included: all the DG rooms, the switchgear rooms, the fuel oil storage
tank rooms. Unit 1 circulating water pump area, and the Unit 1 and
Unit 2 reactor make up water storage tank (RMWST). The 50 was
knowledgeable of the multiple DG systems and conscientiously completed
his logs. However the 50's attention was focused on taking logs and
did not specifically look for any unt,Jected equipment or material
condition problems.
'12 2 Biweekly Inspections of Safety Systems (71707)
The inspectors verified the operability of the following selected safety
systems and/or equipment:
- Unit 1 spent fuel pool cooling and purification system. Trains A
and B
- Unit 2 spent fuel pool cooling and purification system. Trains A
and B
e Unit 2 auxiliary feed water (AFW) system
Accessible sortions of these systems were verified to be properly
aligned. T1e inspectors also observed that they were adequately
maintained and in good operating condition. The inspectors did not
identifv :ioy issues that adversely affected system operability. Minor
defidencies were loted and discussed with the appropriate shift
sepervisor.
Enclosure 2
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02.3 Verification of Safety Tanaina
a. Inspection Scope (717021
The inspectors verified that selected tagouts were implemented in
accordance with procedural requirements. The inspectors reviewed and
walked down selected components tagged by the following tag orders
(10s):
e TO# 97-2018 1. Incore Detection System
e TO# 97-2726 1. Condensate Storage Tank (CST) Freeze Protection
e TO# 96 2121-1. RMWST Oegas System
o TO# 97-1118-1. RMWST System
e TO# 97-2'73 2. Incore vetection Panel
e TO# 97-2514 1, lA Component Cooling Water (CCW) Pump
e TO# 97 2582 2, Train A SWS Strainer
e TO# 97-2586-2, 2A Residual Heat Removal (RHR) Pum)
e TO# 97-2574-1, Unit 1 Containment Purge and Mini-) urge
e TO# 97-2620-1, lA SWS Pump
e TO# 97-2710 1, lA SWS Pump
b. Observ.ations and findinas
The inspectors verified that the components identified on the tag orders
were pioperly taoged. The iden+ifications were correct and the tags
wereconspicuousTyplaced,anddiJnotobscurecontrolroompanel
indications. The administrative aspects of filling out the tagging
order forms were complete and correct. The tags placed were adequace
for personnel safety and equipment protection,
C. Conclusion
The inspectors concluded that the reviewed safety tagging activities
were correct and met the procedural requirements. The administrative
aspects of the tagging orders were complete and accurate. The tags
placed were adequate for personnel safety and equipment protection.
02.4 TS LCO Trackinn (71707)
The inspectors routinely reviewed the TS LC0 tracking sheets filled out
by the shift foremen. All tracking sheets for Units 1 and 2 reviewed by
the inspectors were consistent with plant conditions and TS
requirements.
02.5 Doeration of Dual Function Containment Isolation Valves (Temocrary
inspection (11) 2515/136)
A list of all containment isolation valves (CIVs) was provided by
Updated Final Safety Analysis Report (UFSAR) Table 6.2-31. Containment
Isolation Valve Information. In Table 6.2-31. duai function CIVs were
Enclosure 2
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identified as those CIVs whose post-loss of coolant accident (LOCA)
position was specified as "Open." These dual function valves were !
verified with the licensee and no differences were noted. The inspector !
- also verified that all dual function CIVs can be operated from a switch -!
in the MCR. either from the MCBs or the BDP panels. However, in the '
presence of a Containment Spray (CS) or Safety injection (SI) signal, i
these valves will automatically reopen if the operator tries to close !
them. Once the CS and SI signals are reset, then the dual function CIVs :
can be closed from the MCR and will remain closed. l
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All dual function CIVs can be closed from the MCR once the CS and SI
signals are reset. However, the licensee has no specific procedural ,
guidance for resetting the CS or SI signal in the presence of a valid
demand. Current emergency response procedures only address resetting CS
and Si signals once the termination criteria are met. The inspector
discussed this arocedure deficiency with plant management. By the
, conclusion of t11s inspection period, management telieved it to be a !
generic issue and had chosen to pursue resolution through the
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Westinghouse Owners Group.
02f Sg11mic Event in South Alabama (71707) ;
On October 24. 1997. the National Earthquake Information Center reported i
that an earthquake had occurred in southern Alabama at 7:35 a.m. Central
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Daylight Time (CDT). The magnitude of the earthquake was measured at
4.9 on the Richter scale, and its epicenter was located about 120 miles
due west of the plant near Brewton, Alabama. Plant prsonnel did not i
notice any ground movement. Also, a subsequent walkdown of the site
seismic instrumentation revealed no indication that the earthquake
tremors had been detected. Resident inspector tours verified that
selected seismic detectors appeared operational and there was no
evidence of earthquake damage. ,
02.7 Cold Weather Preoaritions (71714) :
a. Inspection Scone
from November 15 through November 18. the plant experienced several
, consecutive days where the daily low temperatures dropped below
freezing. The lowest temperatures observed were approximately 28
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degrees Fahrenheit (?F) during the early morning hours before sunrise.
The inspectors reviewed abnormal operating procedure FNP-0-A0P-21.0.
" Severe Weather." Revision (Rev.) 13. toured freeze protection systems
around the plant, and. interviewed responsible personnel.
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b. Observations and Findinas
During this inspection a number of findings were identified, including:
e Operators did not log entry into FNP 0 A0P-21.0 for temperatures
at or below 33 *F.
e Step 11.0 of FNP-0 A0P-21.0 " Extreme Cold Weather Contingencies."
states that Appendix I will be performed as necessary if
tem)eratures are forecast to be at or below 33 F within the next
24 lours. The inspectors discovered that major
Appendix I were still incomplete on Novemberand 17.some
portions of
were not
complete by the end of this report period. In particular, system
operators had not checked the status of freeze protection system
(i.e. , heat tracing) monitor lights during their roundt.. Also,
the maintenance department personnel had not com)leted their
inspections and functiorial testing of the plant leat tracing
systems in accordance with electrical maintenance procedure
FNP-1-EMP-1383.01. " Freeze Protection Inspections." Rev. 5. After
discussions with the acting Operations Manager. S0s were directed
to perform tours of the plant heat tracing circuits per item 2 of
FNP 0 A0P-21.0 Appendix 1. Discussions with the acting
Maintenance Manager revealed that the schedule for completing
EMP-1383.01 would be on or around December 5.
e Tours by the inspectors, and later the 50s, identified numerous
heat tracing indicator lights that were not lighted during cold
weather. These circuits were intended to actuate at or below
40 *F. Between both units there were about 200 heat tracing
circuit indicator lights, of which almost one half were not
lighted during subfreezing temperatures. However, of the
approximately 100 non-functioning indicator lights, about one
111rd of these were partially shielded from the environment and
may nct have experienced suf ficiently low temperatures,
e Operations supervision and management on dayshift were not well-
informed about the progress of FNP 0-A0P-21.0 implementation.
- Even though the latest revision to Appendix I that added Tables 1
through 7 was a considerable improvement over the previous
revision, an inspector noticed that the tabular location lists of
the heat tracing circuits and indicator lights of EMP-1383.01 and
FNP-0-A0P-21.0 were not consistent.
Although the weather was not cold enough for a long enough period of
time to represent a significant problem, licensee implementation of
FNP-0-A0P-21.0 was considered poor, especially in light of the problems
experienced during the previous year. (Refer to Non-Cited Violation
(NCV) 50-348, 364/96-15-02. Inadequate Procedural Guidance For Freeze
Protection. of Inspection Report (IR) 50-348. 364/96-15.) For the
Enclosure 2
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freeze protection program this year. the procedural guidance was
adequate. The inspectors identified that licensee personnel failed to
adequately implement FNP-0-A0P-21.0. Appendix 1. as required by TS 6.8.1.a. This constituted a violation of minor significance and is
identified as NCV 50 348. 364/97-14-01. Inadaquate Implementation of
Cold Water Protection Program, consistent with Section IV of the NRC
c. Conclusions
Licensee efforts to implement its cold weather protection procedures
prior to subfreezing temperatures were not timely and operations
supervision and management on day shift were not well-informed about the
progress of the procedures. Non Cited Violation 50-348, 364/97-14-01.
Inadequate implementation of Cold Weather Protection Procedures. was
identi fied.
06 Operations Organization and Administration
06.1 Peer Review by World Association of Nuclear Operators (71707 and 40500)
One of the inspectors reviewed the World Association of Nuclear
Operators (WAND) Interim Report dated September 16. 1997. regarding the
peer review conducted onsite during the month of July 1997. The
inspector concluded that the WANO report did not identify any important
safety issues which would require NRC follow-up action. Furthermore,
the WANO findings did not warrant a significant reassessment of NRC
perspectives regarding licensee performance.
11. Maintenance
M1 Conduct of Maintenance
M1.1 General Comments
a. Insnection Scope (61726 and 62707)
The inspectors observed and reviewed portions of various licensee
corrective and preventive maintenance activities and witnessed routine
surveillance testing to determine conformance with plant procedures,
work instructions. industry codes and standards. Technical
S)ecifications (TSs), and regulatory requirements. The inspectors
o) served all or portions of the following maintenance and surveillance
activities, as identified by their associated work order (WO). work
authorization (WA), maintenance procedure, or surveillance test
procedure (STP):
e FNP-2-FSP-63.05. " Visual Inspection of Penetration Fire Barriers"
- FNP-2-STP-11.6. " Residual Heat Removal Valves Inservice Test"
Enclosure 2
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e FNP-0-lMP-226.13. "1-2A EDG Load Stability Test"
e FNP-0-STP-26.08. Revision (Rev.) 12. " Control Room Train B
Ventilation Operability Test"
e FNP-1-STP-20.2 Rev. 8 " Penetration Room Filtration System Train
A(B) Monthly Operability Test"
e FNP-0-EMP-1370.01, Rev. 4. * Cable Termination. Splicing, and
Repair"
e FNP-1-MP-42.0, Rev 8. " Maintenance of Byron Jackson Service Water
Pumps (01P16P001A, 8. C. D. E)"
e FNP-0-EMP-1530.01. Rev. 8. " General Motor Maintenance"
e FNP-0 EMP-1701.01. Rev. 5. " Electrical Equipment Condition Test"
e WA# W00486998, SW Train 'B' Low Pressure Alarm Pressure Switch
e FNP-0-IMP-425.3. Rev 4. " Pressure Actuated Switches (Generic)"
e FNP-2-STP-914. Rev. 5, " Auxiliary Building Battery Charger Load
Test"
e FNP-2 EMP-1341.06, Rev. 5. " Auxiliary Building Battery Charger
Inspection"
e FNP 2-STP 73.1. Rev. 2. " Hot Shutdown Panel Operability
Verification"
e FNP-1-EMP-1383.01. Rev. 5. " Freeze Protection Inspection"
e FNP-0 FSP-57. Rev. 3. " Low Pressure CO2 Systems"
e FNP 0-STP-26.0A. Rev. 11. "Controi Room Train A Ventilation
Operability Test"
e FNP-1-STP-16.1 Rev. 30. " Containment Spray Pump 1A Inservice
Test"
e WO# W000486924. 2A RHR Pump Motor Maintenance and Supply Breaker
Megger Test
e FNP-0-ETP-3616. Rev. 11. " Monthly Surveillance Fiax Map Data
Collection" for Unit 1
e FNP-2-STP 201.18. Rev. 34. " Reactor Coolant System TE412Bl.
TE41282. TE41283 and TE412D Functional Test"
e FNP-0-STP-80.6. Rev.12. " Diesel Generator 1-2A 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> Load Test"
e WO# M97007636. Unit 2 Power Range Channel NI-42 Isolatior
Amplifier Replacement
e FNP-2-STP 22.2. Rev.10. "2B Motor-driven Auxiliary feedwater Pump
Quarterly inservice Test"
b. Observations and Findinos
All observed maintenance work and surveillance testing was performed in
accordance with work instructions, procedures, and applicable clearance
controls. In general, safety-related maintenance and surveillance
testing evolutions were well-planned and executed. Responsible
personncl demonstrated familiarity with administrative and radiological
controls, Surveillance tests of safety-related equipment were
consistently performed in a deliberate step-by-step manner by personnel
in close communication with the Main Control Room (MCR). Overall,
operators, technicians, and craftsman were observed to be knowledgeable.
Enclosure 2
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experienced, and well-trained for the tasks performed. However, the
inspectors observed the following four instances where personnel were
not signing off procedure steps as they were completed:
e On November 19, 1997, the ins)ectors observed a limited portion of
WA #492443 to calibrate 02E23)lC3532 per FNP 0-lMP-401.2. " Fisher
4150 and 4160 Controller Calibration (Generic)." Rev. 7. The
ins)ectors reviewed the work package and noted that, although the
tecinicians were on step 7.3, they had not signed off the steps
which were already completed, including the sign-off for meeting
the initial conditions. IMP-401.2 was designated as a " Continuous
Use" procedure. One of the procedure usage requirements for a
" Continuous Use" procedure, as stated on the procedure cover page,
was that " Work permitting, each step is to be signed off as
complete before proceeding to the next step." The inspectors
reviewed the procedure and did not identify any work conditions
which would preclude signing off the completed steps as they were
performed. The inspectors did not identify any problems nor
indications that the steps which were not signed off had not been
performed.
- On November 21, 1997, the inspectors observed part of
WA# W00486998. SW Train B Low Pressure Alarm Pressure Switch, per
FNP-0 IMP-425.3 Rev. 4. " Pressure Actuated Switches (Generic)"
for 02P16PS0503 in Unit 2 valve box #1. FNP-0-IMP-425.3 was
defined as a " Continuous Use" procedure. The Confined Space Entry
Sheet was satisfactorily completed. Work was in progress and the
inspectors observed that the procedure steps were not being
initialed as they were accomplished. The inspectors also observed
that WA# W00486947 for TPNS 02P16PS0502 was already completed, but
only the iritial condition step had been signed off. Workers were
knowledgeable of the job and familiar with the requirement to sign
off the steps as they were performed. However, they stated that
they had concentrated on the tasks at hand and had forgotten to
ensure that the steps were properly signed off.
- During the 1-2A Diesel Generator outage, the ins)ectors reviewed
the work package and associated procedures for t1e ongoing job.
During this review, the inspectors identified several minor
administrative discrepancies, including procedure steps that were
complete but not as yet signed off in the MP-14.1 " Continuous Use"
procedure,
e On November 26, 1997 the ins)ectors observed portions of the 1A
SWS pump motor replacement. )uring the review, the inspectors
identified several steps of the EMP-1370.01 data sheet for
termination of the pump motor that were complete, but not signed
off as required by a " Continuous Use" procedure.
Enclosure 2
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These observations were brought to the attention of maintenance :
management who then discussed them with the various maintenance teams,
stressing the requirement to sign off steps as accomplished for
" Continuous Use" procedures. Additionally, maintenance personnel ;
provided feedback to management concerning the quality and expectations
of procedures.
1
Failure to initial procedure steps as they are performed, before
proceeding to the next step, is contrary to the procedure usage
requirements stamped on " Continuous Use" procedures. This requirement
ensures that critical procedure steps are performed in a deliberate and '
methodical step by step manner. Since no procedure ste)s were missed or
performed out of sequence, the safety significance of t1e observed
examples was minor. As such, this failure to follow 3rocedure <
constituted a violation of minor significance and is aeing treated as-3 -
NCV consistent with Section IV of the NRC Enforcement Policy. This is
identified as NCV 50 348. 364/97-14 02. Failure To Sign Off Steps For
Continuous Use Procedures as They Are Performed.
c. Conclusions
Maintenance and surveillance testing activities were generally conducted
in a thorough and competent mar.ner fiy qualified individuals in
accordance with plant procedures and work instructions. A NCV was
identified for maintenance technicians failing to sign-off steps in
" Continuous Use" procedures as they were accomplished.
M1.2 1-2A Diesel Generator 18 Month Outane
a. Insoection Scone (62707)
The inspectors reviewed the work aackages and observed portions of the
1-2A Emergency Diesel Generator (EDG) 18-month outage, which included:
lobe oil heat exchanger tube bundle replacement; jacket water heat
exchanger tube bundle replacement; fuel injector replacement: exhaust
system repair and replacement: and various other 18-month inspections.
b. Observations and Findinas
Overall work was performed well. with maintenance supervision constantly
on station to oversee work activities and review the work status.
Workers were diligent in maintaining foreign material exclus;9n covers
over oyen components. The licensee continued its practice of having a
COLTECi vendor representative on-site during major EDG outages, witch
aided in rapid resolution of technical issues.
The 1-2A EDG equipment outage progressed without significant difficulty.-
One of the initial equipment problems targeted for repair was the
exhaust system which had several leaks that actually made the EDG room
uninhabitable for extended periods due to fumes. During mainteriance it '
Enclosure 2 .
h
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.
. 11
was determined that the exhaust leaks had seriously damaged the engine
cylinder thermocouples. Mc.st of these thermocou)les were repaired, but
some were left for repair during the next 1-2A EXi outage. All the
exhaust system leaks were repaired.
During the return to service of the 1-2A EDG, mechanics discovered that
the #9 fuel injector pump was not operating and several minor fuel oil
leaks were identified on inje_ctors #2 #3. and #12. In addition to
these minor problems, the EDG output breaker would not close from the
EPB handswitch during the )erformance of the 1-2A EDG o>erability test.
The cause was believed to )e a contact in the handswitc1 circuit that
failed to close when the switch was operated. However, the licensee was
unable to repeat the problem and a conclusive root cause determination
was not made. Also, during a maintenance run, the EDG tripped due to
low lube oil pressure. caused by debris buildup in the strainer. The
debris was believed to be from material that was scrapped off the lube
oil heat exchanger during the tube bundle replacement. Each of these
items was corrected prior to declaring the 1-2A EDG operable.
c. Conclusi20
Maintenance work was performed by well-qualified and knowledgeable
personnel. Corrective action efforts were thorough. Post-maintenance
testing was satisfactorily completed.
M6 Maintenance Organization and Administration
M6.1 Schedulino Of On Line Maintenance (62707)
The inspectors reviewed the Unit 1 Equipment Outage Forecast. Rev. O for
December 1 - 7. 1997, issued on November 25, 1997. The inspectors
noticed that the licensee had scheduled FNP 1-STP-73.1. " Hot Shutdown
P6nel Testing." for December 1. 1997. The planning department had
determined that implementation of certain steps of FNP-1-STP-73.1 would
involve significant risk based on risk-achievement worth (RAW) values i
generated by their equipment out-of-service (E005) risk monitor.
Although the vast majority of hot shutdown panel (HSDP) testing had RAW
values well within the bounds established by ACP-52.1. " Guidelines For
Scheduling of On-Line Maintenance." Rev. 4. there were several steps of
FNP-1-STP-73.1 with RAW values over 10-(one as high as 18.6). These
values were calculated even though 0)erations and Planning personnel had
made efforts (i.e., test procedure c,anges) to reduce the potential
rists associated with on-line HSDP testing. The guidelines of ACP-52.1.
Section 4.2. do not currently allow for conducting on-line maintenance
or testing if the RAW value exceeds 10. Concerns regarding HSDP testing >
with high RAW values were also expressed by Operations personnel. The
inspectors discussed this testing with plant management. including
compensatory measures consistent with ACP-52.1. Plant management
decided to reschedule the high risk portions of FNP-1-STP-73.1 until the
next outage.
Enclosure 2
W
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H8 Hiscellaneous Maintenance Issues (90712, 92700 and 92902)
M8.1 (Closed) Licensee Event Reoort (LER) 50-348. 364/97-07: Outside Of
Desian Basis Due To Dearaded Cork Material
On June 22, 1996. December 10. 1996, and April 17. 1997. licensee
personnel identified that some of the self expanding cork sealing
material was missing from the area between the main steam valve room
(MSVR) and containment. On each date. Deficiency Reports (DRs) were
written. The areas identified on April 17 in the MSVR. and the amount
of material missing or degraded:
Unit 1: "B" Bay - 2 in by 20 ft
"C" Bay - 4 in by 6 in
Unit 2: "A" Bay - 4 in by 6 ft
"B" Bay - 4 in by 4 ft
"C" Bay - 4 in by 4 ft
Although the missing cnd degraded cork seal had been previously
identified in 1996. its significance as a flood barrier was not
recognized until after April 17. 1997, due to the questioning attitude
of a licensed senior reactor operator. Initial licensee concerns
regarding the cork seal, used elsewhere in the auxiliary building,
centered around its function as a fire barrier and as a pressure seal
for the penetration room boundary (See Inspection Report (IR) 50-348,
364/97-04). On April 22. the iicensee determined that the missing cork
represented a condition outside the design basis and reported this
condition in LER 50-348. 364/97-007.
The missing cork would allow water from a main feed line break to flood
the lower level equipment roo9 (LLER) which contains the turbine-driven
auxiliary feedwater (TDAFW) pum). thus rendering the TDAFW pump
inoperable. This accident, com)ined with a single failure of a motor-
driven auxiliary feedwater (MDAFW) pump, would leave the plant with only
one operable MDAFW pump. The Condition IV - Limiting Faults accident
analysis of UFSAR Section 15.4.2.2. " Major Rupture of a Main Feedwater
Pipe." assumed that two MDAFW pumps would be necessary to provide
adequate AFW flow. Further analysis of the AFW system requirements for
Main Feedwater (MFW) line breaks was documented in As-Built Notice (ABN)
93 0-0224. This analysis concludeo that one MDAFW pump provided
adequate flow to the intact Steam Generators (SGs) once the faulted SG
was isolated. Thus, if a MFW line break had occurred while the cork
seal was degraded, coincident with a single failure of a MDAFW pump, the
current main feedwater line break accident analysis could not be met.
However prompt operator action (i.e.. to isolate the faulted SG) per
the Emergency Operating Procedures (E0Ps) would mitigate this event by
allowing the single MDAFW pump to provide the required AFW flow to the
intact.SGs.
Enclosure 2
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t
The very low probability of a MFW line break occurring coincident with a t
single failure of a MDAFW pump wa calculated by the licensee to be ,
4.75E-5 Jer reactor year. This numoer was based on all failure modes ,
for the ADAFW pump (including electric power). Furthermore. the plant ,
emergency response procedures (ERPs) provide direct instructions for
isolating a faulted steam generator. An inspector reviewed the ERPs and
determined that the faulted SG coeld be identified and isolated promptly
(i.e.. less than 10 minutes). Once the faulted SG was isolated, the
remaining MDAFW pump would have adequate capacity. Considering the very
low probability. and the o)erators' ability to mitigate this accident.
the inspectors concluded tlat the safety impact of degraded cork in the *
MSVR was minimal.
'
When identified in 1996, it was evident that the missing and degraded
cork sealing material had been in this condition for many years. .
Degradation of the cork seal used throughout the auxiliary building has
been recognized as a problem as early as 1985. Numerous DRs have been
written regarding degradation of the cork seal in the auxiliary
building. However. no comprehensive repairs or periodic inspections
were initiated. The oldest outstanding deficiency report (i.e. DR
211386) was written in March 1990 for degraded cork between the
auxiliary building and containment. This and other DRs were still open
when the issue was identified again regarding the MSVR in April 1997.
The missing and degraded cork seal in the Unit 2 MSVR was specifically
identified on December 10. 1996 (DR 96006033). but was not adequately
addressed until a senior reactor operator questioned the problem when it
was re-identified on April 17. 1997. This issue was also similar to the
licensee's failure to recognize and correct degradation of the cork seal
that maintained the penetration room boundary (PRB) as documented in
IR 50 348, 364/97-04. For the PRB issue. a Predecisional Enforcement
Conference was held, resulting in several severity * vel IV violctions,
one of which was for inadequate corrective action.
'
The following corrective actions were described in LLR 50-348, 364/97-07
and verified by the inspectors:
1) Cork seal repairs on Unit 2 were completed by April 21. 1997.
The Unit I cork seal was replaced with a foam seal prior to
restart from its last refueling outage in June 1997.
2) Maintenance procedure FNP-1/2-MP-29.0. " Visual Inspection Of
Auxiliary To Containment Building Seismic Joint Seal (Main Steam
Valve Pscom)." Rev. D. was developed and issued June 6. 1997 to
inspect the MSVR cork seal every 18 months.
3) Personnel reviewing DRs for operability reviewed
LER 50 348. 364/97-007.
Enclosure 2
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'
4) The entire corrective maintenance backlog was reviewed to
ensure proper prioritization of outstanding DRs/W0s for scheduling ,
work.
Comprehensive inspections of the cork seal have been conducted 1
throughout the auxiliary building and all repair work has been
completed, or scheduled with appropriate compensatory measures in place
(i.e.. fire watches). The licensee is developing additional periodic
cork seal inspection procedures for all auxiliary building areas outside
the MSVR. These procedures are scheduled to be completed by ;
December 19, 1997.
'
10 CFR Part 50. Appendix B. Criterion XVI: Updated Final Safety Analysis
Report. Section 17.2: and the Operations Quality Assurance Policy
Manual. Chapter 16, require that appropriate measures be taken to assure
that conditions adverse to quality are promptly identified and
corrected. Failure to take adequate corrective actions is identified as
violation (VIO) 50-348, 364/97-14-03. Inadequate Corrective Actions for
Maintaining Main Steam Valve Room Cork Seal Flooding Barrier.
M8.2 (Closed) Insoecto Followuo item (IFI) 50-348. 364/96-02-03: Pre-Action
S.prinkler System Failures
in 1996, two incident reports (FNPIRs) were initiated (i.e.. FNPIRs 1-
96 71 and 2-96 78) and a root cause team was assembled to address the
problems associated with multiple pre-action sprinkler s
Although the root cause was not conclusively identified.ystem failures.
the root cause .
team recommended numerous corrective actions that have been implemented. !
These corrective actions included system flushes: detailed inspections,
measurements, and cleaning of multimatic valve internals: replacement of
critical mechanical and electrical components; revised surveillance
procedures: and increased surveillance testing. Over the past two
years, the inspectors have observed aspects of these corrective actions
for selected pre-action sprinkler systems. The inspectors reviewed the
completed FNPIRs identified above and a history report of all the
corrective action commitments to confirm that they were completed. The
inspectors also reviewed intracompany memorandum NEL-97-0476, dated
November 17, 1997, that summarized the corrective actions already taken
and established an additional corrective action plan v'th detailed
actions, responsibilities, and a schedule. The inspectors have also
reviewed the history of surveillance test results since August 1996
which demonstrated dramatic reductions in component (e.g.. multimatic
valve - clappers and solenoid valves) failures. However, certain system '
failures have continued to occur that will be addressed as part of the
corrective action plan of NEL 97-0476, scheduled to be finished by
July 31. 1998.
Licensee corrective actions to-date to address multiple pre-action
s)rinkler system failures identified in 1996 have been comprehensive,
tiorough and generally successful. An additional corrective action plan
Enclosure 2
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, .- - -- , , +
.~ - -- . . - .. .- = - . . . . =. - - - . - . - . _
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. 15
,
has been initiated to resolve the small number of remaining failures.
This IFI is considered closed.
'
M8.3 (Closed) LER 50-348. 364/96-01: TS Action Statement Reauirement Not Met
for SSPS Testina
Tne circumstances surrounding this LER and associated corrective actions
were previously inspected and verified (see IR 50-348, 364/96 03. !
'
Section 3.2.c). This LER is considered closed.
M8.4 (Closed) LER 50-348/97 011: Ent y Into TS 3.0.3 Due to the Failure to
follow the Work Control Process >rocedure
a. Insoection Stone (92902)
The inspectors reviewed LER 50 348/97-011 and associated maintenance
,
W0s, Occurrence Reports (ors). LCO Status Sheets. and Training
Attendance Sheets. ,
b. Observations and Findinas
LER 50 348/97-11. documents an event where failure to follow procedure
associated with controlling the work process, caused Unit 1 to enter a
condition prohibited by TS. Technical Specification 3.7.4 requires two
independent Service Water System (SWS) loops be maintained operable.
However, both trains of the automatic isolation capability of the motor
operated valves (MOVs) for supplying service water (SW) to the turbine
building were made inoperable. TS 3.0.3 was entered for 39 minutes,
until operability was restored.
The inspectors reviewed the associated safety assessment and concluded
that it adequately addressed the effects of the SWS inoperability.
During the time that the automatic isolation function was inoperable.
0:>erators were aware of the condition with the SW Motor Operated Valves
(K0Vs). Any turbine building SW leak that could have jeopardized the
heat transfer capability of the SWS or impacted the capability for
running the EDGs would have been identified in a timely manner.
Operators could have manually isolated SW to the turbine building to
ensure adequate SWS flow to safety related systems.
'
Corrective actions taken to resolve the issue and prevent recurrence
were reviewed by the inspectors. Training conce ning the event was
provided to Operations and Maintenance department personnel and they
were instructed on the need to identify and document specific limits for
troubleshooting activities on the work order. This failure to meet the
requirements of TS 3.7.4 is identified as NCV 50-348/97 14-04. Entry
Into TS 3.0.3 Due to the Failure to Follow the Work Control Process
Procedure. consistent with Section VII.B.1 of the NRC Enforcement
Policy.
-
Enclosure 2
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e-w,s-? e---y -v , ,-: ,,
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. 16
c. (pnclusions
A non cited violation was issued for a failure to follow work control
procedures which resulted in inoperability of automatic turbine building
isolation. LER 50-348/97-011 is closed.
III. Enaineerina
El Conduct of Engineering
E1.1 Steam Generator Reolacement Pro.iect (50001 and 37551)
On November 20, 1997. SNC met with the NRC in Rockville Maryland to
discuss current progress and schedules for the Units 1 and 2 Steam
Generator Replacement Projects (SGRPs). A resident inspector attended
the meeting. The existing Westinghouse Model 51 SGs are currently
scheduled to be replaced with the Westinghouse Model 54F design in
S) ring 2000 for Unit 1 and Spring 2001 for Unit 2. During the meeting.
11e licensee provided a comprehensive summary presentation of its
schedule, scope of work, organization, date for proposed licensing
submittals, and engineering plans.
E8 Hiscellaneous Engineering Issues
E8.1 _
( Closed) URL 50 348. 364/97-201-08- Tornado Protection of Turbine.
Driven Aux 1L iary Feed Water (TDAFW) Pumo Vent Stack
The inspectors observed that the safety-related T0AFW pump vent stack
was installed on the roof of the auxiliary building and was not
protected from tornado generated missiles. Updated Final Safety
Analysis Report (UFSAR) Sections 6.5.1. 3.2.1.3. 3.2.1.5. and
Table 3.2-1 state that Auxiliary Feed Water (AFW) system equipment and
piping are identified as Category 1. UFSAR Section 3.5.4 states that
Category I equipment and aiping outside containment are either housed in
Category I structures or )uried underground. The NRC has reviewed this
issue and concluded that the failure to provide tornado missile
protection for the TDAFW pump vent stack, located on the roof of the
Auxiliary Building. is a violation of 10 CFR 50 Appendix B.
Criterion 111. Design Control. This is identified as Violation 50-348.
364/97-14 05. Failure to Provide Tornado Missile Protection for TDAFW
Pump Vent Stack.
Based on the above, the unresolved item is considered closed.
Enclosure 2
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17
IV. olant Support
R1 Radiological Protection and Chemistry Controls
R1,1 Radiological Controls
a. Inspection Scone (83750)
Radiological controls associated with ongoing Unit 1 (U1) and Unit 2
(U2) routine operations were reviewed and evaluated by the inspectors.
Reviewed program areas included general housekeeping and cleanliness,
area postings, radioactive material and waste (radwaste) container
labels. controls for high and loc.ed-high radiation areas, and
procedural.and radiation work permit (RWP) guidance. Established
controls were compared against Updated Final Safety Analysis Report
(UFSAR) details and documented procedural requirements to meet
applicable sections of Technical Specifications (TSs) and
The inspectors made frequent tours of the radiologically controlled
areas (RCAs). The inspectors directly observed worker and Health
Physics (HP) technician performance and discussed results of radiation
and contamination surveys conducted for selected ecuipment and facility
locations. Confirmatory radiation surveys of the L2 Spent Fuel Pool
(SFP) heat exchanger areas and radioactive waste storage the U2 truck
bay area were reviewed ano discussed in detail.
The inspectors discussed and reviewed "As low as Reasonably Achievable"
(ALARA) program implementation, individual worker doses, and dose
expenditures associated with the Unit 1 Refueling 14 (UlRF14) outage job
evolutions.
b. Observations and Findinas
High and locked-high radiation area controls were verified to be
implemented in accordance with TS requirements. Postings for
radiologically controlled areas were proper and in accordance with TS or
10 CFR 20 Subpart J requirements. Containers holding radwaste,
contaminated materials, and equipment were labeled in accordance with
10 CFR 20.1904 requirements. Excluding the U1 SFP heat exchanger area.
radiation survey maps of local areas within the auxiliary building
accurately reflected radiological conditions, For the U1 SFP heat
exchanger and adjacent rooms. the inspectors noted that survey records
maintained at the RCA control point were accurate and indicated recent
changes in radiological conditions for U1 SFP heat exchanger and
adjacent rooms. However. licensee representatives stated that changes
to the survey ma)s posted in the local area were only updated on a bi-
weekly basis. Tie inspectors verified that the subject rooms were
posted and controlled properly but that the identified lack of
timeliness in revising the locally posted map could cause confusion
Enclosure 2
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. 18
regarding the actual radiological conditions within the subject area.
Licensee representatives stated that this concern would be reviewed and .
appropriate actions taken.
From direct observation of work activities, the inspectors verified that
workers followed proper radiological controls specified in selected
RWPs. In addition, the inspectors noted improvements in housekeeping
and cleanliness within the established RCA. Review of licensee data
verified that approximately six percent of the RCA continued to be
considered contaminated floor space. Licensee representatives stated
that continuing decontamination efforts were ongoing to further reduce
the RCA contaminated floor space.
The Farley Nuclear Plant UlRF14 Outage report was reviewed and discussed
with responsible staff. Implementation of ALARA program activities
including initial planning and subsecuent review of lessons learned for
UlRF14 outage activities was verifiec. Dose expenditure for outage
activities, approximately 246 person rem, exceeded the original
projected dose expenditure of 195 person rem. The outage duration
increased from 52 to 81 days as the result of extensive unplanned steam
generator maintenance activities and contributed to the increased dose
expenditure.
c. Conclusions
Radiological controls, area postings and container labels were maintained
in accordance with TS and 10 CFR 20. Appendix J requirements.
Improvements were noted for RCA housekeeping and cleanliness and for RWP
practices.
Revisions to local area radiation survey mn for the U1 SFP area were
timely. '
For U1RF14 outage. ALARA program activities were implemented in
accordance with approved procedures.
Actual UlRF14 outage dose expenditure exceeded original estimates and
resulted from an increased s"pe of steam generator maintenance
activities. ,
R1.2 External Exposure (83750)
a. Inspection Scoo.g
The inspectors discussed and reviewed deep dose equivalent (DDE) and <
shallow dose equivalent (SDE) exposures to workers involved in UlRF14
outage activities. The review included selected workers'
Thermoluminescent 00simeter (TLD) data and personael contaminations.
documented as either Radiation Worker Performance Observations (RWP0s).
Enclosure 2-
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1.e., dispersed contamination less than 5000 disintegration per minute
per 100 square centimeters (dpm/100cm') and specks with less than 100,000
dpm/ probe area, or as personnel contamination events (PCEs) i.e. , 2
dispersed contamination greater than or equal to (a) 5000 dpm/100cm and
specks a 100,000 dpm/ probe area. ,
Dose assessment methods and assumptions, where applicable, were reviewed
for technical adequacy. Dose results were compared against 10 CFR
Part 20 limits,
b. Observations and Findinas
For outage activities, the maximum total effective dose equivalent (TEDE)
was approximately 2386 millirem (mrem) assigned to an Individual involved
in steam generator maintenance activities. For the outage period,
approximately 75 speck and 120 dispersed personnel contaminations were
identified in RWP0 documents. Approximately 14 PCEs were identified,
with only one requiring a skin determination. For the affected
Individual, a not particle located on the upper right forearm resulted in
an assigned shallow dose equivalent of approximately 10.7 rem. Licensee
assumptions and details regarding physical location, length of exposure
and isotopic characteristics of particle were appropriate. The
inspectors noted that all assigned doses were within 10 CFR 20.1201
limits.
c Conclusions
Worker DDE and SDE exposurec resulting from personnel contamination
events and work activities during the U1RF14 outage were evaluated
properly and were within 10 CFR 20.1201 limits
RI.3 internal Exposure (83750)
a. Inspection Scooe
The inspectors discussed program guidance for monitoring and evaluating
)ossible internal exposures. Results of selected investigative whole-
)ody count (WBC) analyses conducted during the U1RF14 outage were
reviewed in detail.
b Observations and Findinas
From review of WBC analysis records of workers' positive radionuclide
intakes, a weakness affecting the accuracy of associated evaluations was
identified. The inspectors noted that farley Nuclear Plant (FNP)
Dosimetry (005) procedure-307. Rev. 20, Operation and Standardization of
the Canberra Nuclear Stand-up Whole Body Counters, dated February 18,
1997, Section (S)4.7.13.2 specified that it,jividuals indicating a
potential intake equal to or greater than 10 millirem (mrem) following
WBC analyses in paper clothing requires (1) initiation of a DGS Form 921.
Enclosure 2
L
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. - 20 !
Investigative Whole Body Count record, and (2) instructing individuals to i
return for another count at the beginning of the next work day. Further. i
the WBC operator was required to ensure that the actual intake date and
time was entered into the computerized system. During the review of WBC
analysis records, the inspectors identified two individuals whose initial 1
WBC analyses data resulted in an assigned committed effective dose ,
equivalent (CEDE) exceeding 10 mrem, but where subsequent WBC analyses
were conducted with improper intake dates and times. That is, for the
workers' WBC analyses conducted subsequent to the initial measurements ,
which initially identified the positive radionuclide intakes. WBC system
operators input the current dates and times rather than the actual intake
dates and times. The inspectors noted that the failure to follow
)rocedures for WBC investigative analyses was a violation of TS 6.8.1.
Juring the week of November 17. 1997. responsible licensee
representatives issued a memorandum to all responsible personnel '
regarding the identified procedural problems and conducted manual
calculations using proper event dates and times for the two impro>er
intake evaluations. No significant changes were identified for tie
calculated CEDES based on the minimal quantities and long effective half-
life of the radionuclides detected. Licensee followup interviews with
responsible technicians identified confusion regarding procedural
directions and requirements for conducting proper intake evaluations
using positive WBC analysis data. Licensee representatives stated that
additional training would be provided and that documentation regarding
intake event dates and times would be evaluated and improved, as *
applicable. The inspectors noted that the failure to follow procedures
constituted a violation of minor safety significance and, consistent with
Section IV of the NRC Enforcement Policy. is identified as Non Cited
Violation (NCV) 50 348. 364/97 14 06: Failure to Follow WBC Analysis
Procedures for EvaluaM on of Workers' Potential Radionuclide Intakes.
The inspectors noted that from March 15 through May 25. 1997, the U1RF14
outage period. approximately 30 investigative WBC analyses were ,
conducted. The analyses were con 6Jcted as a result of specific events,
usually documented in RWP0s, which could cause or indicate potential
radionuclide intakes resulting in internal exposure. The estimated
maximum intake was 309 nanocuries (nr') approximately 7.8 derived air
concentration-hours (DAC hrs), resulting in an assigned CEDE of 20 mrem.
The inspectors verified the 20 mrem CEDE was added to the deep dose
equivalent (DDE) to provide the total effective dose ecuivalent (TEDE)
documented in the individual's official exposure recorcs. No other
- evaluated worker intakes exceeded 10 mrem, i.e. 0,2 percent of the
annual limit of intake (ALI) required to be documented by licensee
procedures.
c. Conclusions
The failure to follow proct;dures for evaluating potential intake of "
radionuclides was identified as NCV: 50-348.364/97-14 06: Failure to
Enclosure 2
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.
c , ,
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. 21
Follow WBC Analysis Procedures for Evaluation of Workers' Potential
Radionuclide Intakes.
Controls for minimizing workers' internal exposure were effective.
RI.4 Radiation Monitoring System (RMS) Operability Issues (84750)
a. Scoce
Status of the Unit 1 (U1) main steam relief and atmospheric steam dumn
discharge radiation monitor B (RE-60B) operability was reviewed and
discussed. The inspectors reviewed and discussed Special Report
97-03-00. U1 Inoperable Radiation Monitor R60-B. and reviewed selected
records regarding implementation of the applicable surveillances and
compensatory sampling required by the TS action statement.
b. Observations
The inspectors verified that, for the inoperable U1 RE-60B monitor,
required surveillances verifying U1 Steam Jet Air Ejector (SJAE) monitor
R-15A operability were conducted in accordance with the applicable
procedures. Backup grab samples were not required for the period
reviewed based on operability of the SJAE monitor during that period,
c. Conclusions
Surveillance requirements for the inoperable U1 RE-60B monitor were
completed in accordance with approved precedures.
R1.5 Radioactive Waste and Material fransportation Activities (86750.
a. Insoection Scoo_e
The inspectors reviewed RCP program activities associated with packaging
and subsequent trancport of radioactive material and waste from the site.
The review evaluated implementation of revised Department of
Transpcrtation (DOT) 49 CFR Parts 100-179 and 10 CFR Fart 71 regulations.
Program implementation based on the completeness and accuracy of shipping
documents associated with recent shipping activities was evaluated.
Procedural guidance detailed in recently revised Farley Nuclear Plant
(FNP) RCP procedures was reviewed and evaluated against anlicable
requirements in the revised 49 CFR Parts 100-179 and 10 C 4 Part 71
regulations.
e FNP-0-RCP-810. Shipment of Radioactive Waste to Barnwell Burial
Site. Rev. 29. issued January 1. 1997.
Enclosure 2
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22
e FNP-0-RCP-811. Shipment of Radioactive Material. Rev. 20, issued
October 28, 1997,
i
1
e FNP-0 RCP-888. Health Physics Radwaste Group Forms. Rev. 12, issued
October 15. 1997.
Records of selected radioactive waste and material shipments made between
June 1. and October 22, 1997, were reviewed and discussed.
b. Observations and Findinas
The licensee's )rocedural guidance met a)plicable regulatory
requirements. Recent revisions to 49 CFR Parts 100-179 and 10 CFR
Part 71 regulations were incorporated into approved procedural revisions. i
Shipping paper data entries were accurate and completed appropriately.
c. Conclusions
Licensee program guidance for transportation of radioactive waste and
materials met 10 CFR 71.5 and ru ently revised DOT 49 CFR Parts 100-179
requirements.
Transportation program guidance was implemented effectively.
R3 RP&C P;ocedures and Documentation (83750)
R3.1 Dose Records
a. Inspection Stog
The inspectors reviewed and evaluated licensee program guidance and
implementation for determination of current-year prior occupational
doses. The inspectors reviewed and discussed NRC Form 4. or equivalent,
records for selected contractor personnel involved in U1RF14 outage
maintenance activities. In addition. implementation of procedural
guidance for extensions to administrative dose limits was evaluated for
individuals involved in selected U1RF14 outage activities.
Licensee program guidance and corres)onding records were compared against
approved procedures and 10 CFR 20 Su)part L requirements, as applicable.
b. Observations and Findino;
The inspectors verified that a)propriate records of current-year prior
occupational doses were availa)le for the selected individuals. Initial
estimates of current-year prior doses assigned for deer, skin, extremity,
and lens of the eye for each individual worker were conservatively based.
Enclosure 2
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All documentation required for granting administrative dose extensions in
accordance with approved procedures was complete and maintained.
c. Conclusions
Records for determining workers' prior yearly occupational exposures and
granting extensions to adeinistrative e cosure limits were established in
accordance with 10 CFR Part 20. Subpart . requirements and administrative
procedures.
R8 Hiscellaneous RP&C Issues i83750, 84750)
R8.1 (Ocen) VIO 50-348. 364/96-10 01: Failure to Construct and Maintain an
"As Bui' t' Samole Line in Accordance with Confiouration Control
Procedures and Drawinas.
This violation addressed differe.. as between the installed "as-built" and ,
the applicable configuration control procedures and drawings for the U1
Post Accident Sampling System Particulate detector (RE-67) sample line.
Completion of corrective actions was verified during system walk-downs.
Additional corrective actions documented in a November 15, 1997. response
to violation (VIO) 50 348/97 08 05, which also aie applicable to this
issue, were reviewed and discussed. Licensee commitments addressing
Radiation Monitoring System (RMS) design control issues included
additional system walk-downs. development of a RMS Functional System
Description (FSD) document and subsequent validation by a Self-initiated
Safety System Assessment (SSSA). From discussion with responsible
licensee representatives and review of the FNP Radiation Monitor Plan and
Radiation Monitor Walk down Issues documents, the inspectors verified
completion of the initial RMS equipment walk-downs and preliminary
evaluations. Identified RMS design issues were discussed and determined
to not affect RMS operability. Additional walk-downs of currently
inaccessible RMS equipment located in both U1 and U2 containments were
planned to be completed during future outages. Licensee representatives
provided a preliminary schedule regarding development of the RMS FSD
document and subsequent validation by a $SSA. Additional RMS design
issues identified by the SSSA are to be corrected. Based on the
completed actions and documented commitments for RMS equipment c:rign
issues, this part of the VIO is closed. However, the parts of this
violation which were addressed in Section El.3 of IR 50-348, 364/96-07
and Section El.2 of IR M 348. 364/96-09 remain open, pending future NRC
review.
Enclosure 2
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. 24
R8.2 (Closed? VIO 50 340/97-10-05: Inadeouate Confiauration Control of 01 RMS
Particu ate Samole Lines.
r
This violation identified concerns retarding differences between the
installed sample lines constructed with flexible stainless steel tubing
having corrugated internal surfaces and the applicable configuration
control-documents for the U1 backup Post-Accident Sampling System plant -
vent airborne particulate sampler (RE-68) and the U1 main stack
particulate sampler (RE-29A). From direct observation of RMS equipment
and review of licensee records, completion of corrective actions i.e.,
installation of the correct sam)le line for the RE-68 nonitor and use of .
'
a backup sampling system (RE-293) for the U1 RE-29A monitor, was
verified. As documented in Section R8.1, additional corrective actions ,
and commitments detailed in the licensee's November 15. 1997, response to
the violtion were reviewed and discussed. Based on the completed
actions and documented commitments. this VIO is closed.
R8.3 (Closed) Licensee Event Reoort (LER) 50-364/97-04-00: Doeratina Outside '
of Technical Soecifications Due to Recuired Containment Grab Samoles Not
3eina Taken.
i
a. _ Inspection Scone
The inspectors reviewed and discussed with responsible personnel.
Licensee Event Report (LER) 50-364/97-04-00 which addressed the failure
to conduct containment atmosphere grab samples as required by TS 3.4.7.1
when both the U2 containment atmosphere particulate (R-11) and gaseous
(R-12) radiation monitoring systems were inoperable from September 10-12.
1997.
The LER and associated licensee's occurrence report were reviewed and
discussed with cognizant licensee re)resentatives. The affected system
was walked down with responsible teclnicians and corrective procedural
revisions were documented in FNP-2-RCP 27. Operation of Unit 2 RE0011/12
and RE0021/22. Rev. 12, issued November 4. 1997, were discussed.
b. Observations and Findinas
The licensee occurrence report concluded that multiple equipment
failures, inadequate procedural guidance, the failure of personnel to
followup properly, and abnormally low radiation monitor readings
contributed to the failure to identify the need for the TS grab sample
surveillances. The inspectors noted that the failure to conduct grab
samples when the U2 R 11 and R-12 radiation monitoring sampling systems
were inoperable was identified as a violation of TS 3.7.4.1. The
. inspectors noted that.the licensee's evaluation considered all potential
causes contributina to the event and specified appropriate corrective
actions. The implementation of proper corrective actions. including
procedural revisions and associated training was verified. Consistent
4 with Section VII of the Enforcement Policy, this issue was identified as
Enclosure 2
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. NC.V 50-364/97-14-07: Failure to Conduct Compensatory Grab Sampling for
Inoperable Unit 2 Contali ont Atmospheric Radiation Monitoring System in
accordance with TS 3.4.7.1.
c. Conclusions
The inspectors identified NCV 50-364/97-14-07: Failure to Conduct.
C'xnpensatory Grab Sampling for Inoperable Unit 2 Containment Atmospheric
I jdiation Monitoring System in accordance with TS 3.4.7.1.
,
, - P1 Cc luct of EP Activities (71750)
Pl.1 Emeraency Plan Exercises
a.Srm
~
The inspectors observed the conduct of multiple emergency plan drills
including two unannounced off hours drills.
-b. e servations and Findinas
On October 30. 1997. resident inspectors participated in an unannounced
off-hours drill of the licensee's emergency plan. The inspectors were
onsite at 3:00 a.m., to observe the start of the drill and the setup of
the Technical Support Center (TSC) and Emergency Operating Facility
(E0F). The TSC and E0F were setup expeditiously and efficiently. The
majority of the licensee staff was able to respond to the site aromptly.
However. two of the required positions for minimum manning of t1e EOF
were not-manned in time. This resulted in the EOF not being staffed and
ready until 95 minutes after declaration of the Alert. 20 minutes more
.than the required time.
The licensee addressed the staffing deficiency promptly. On October 31.
the licensee began briefing all on-call staff to discuss the delay in
manning the EOF and to reiterate the expectations for staff response to
site emergencies. The inspectors observed the first briefing conducted
.on October 31 and concluded that it clearly identified the licensee's
expectations to plant on-call staff.
On-November 18 the inspectors observed the licensee perform another
unannounced off-hours drill to verify the effectiveness of the corrective
-
actions. The ' drill started at 4:30 a.m., and all required positions were
filled within the required times. Specifically, tne EOF was manned and
- ready within'70 minutes of declaring the emergency.
- 0n . November 12. a resident inspector also observed the conduct of an
. announced. emergency plan exercise that involved activation and manning of
lthealternate'[0F. This facility was located at an Alabama Power Com)any
b -(APC) service center in Headland Alabama . The inspector confirmed t1at
_
emergency response. personnel were able.to locate. setup, and fully
.
_
,
Enclosure 2
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activate the alternate EOF. which would be used anytime the onsite E0F is
unavailable, j
c.Concipsions
-Licensee corrective accions for failing tu staff the EOF within the
required time frame were prompt and thorough. The licensee successfully
deconstrated the ability to activate the alternate EOF.
P8 Hiscellaneous Emergency Preparedness (EP) Issues
During a Safety Audit and Engineering Review audit conducted during the
period of November 25, 1996, to February 19, 1997, the licensee
identified inconsistencies in the documentation associated with the
inventory of emergency planning equi) ment. The inconsistencies were
later determined by the licensee to se falsifications of the inventory
checklists. On June 30. 1997, the NRC Office of Investigations (01)
completed an investigation of the apparent failure of an Emergency
Preparedness Technician to perform required equipment inventories and the
associated falsification of inventory checklists. 01 concluded that,
during the period April 1996 through January 1997, the technician failed
to conduct at least three required inspections, and deliberately
falsified at least four checklists. A copy of the synopsis to 01 Report
No. 2-97-005 is attached.
Based on licensee and O! reviews of this issue, a violation of
10 CFR 50.9. Completeness and Accuracy of Information, was identified in
that the deliberate acts of the technician resulted in records that are
required to be maintained by the licensee were not con.piete and accurate
in all material respects. The licensee identified the inconsistencies,
took prompt actions to investigate the issue, completed follow-up actions
'
to ensure that all emergency preparedness equipment was in place and
operable, and took appropriate remedial action. There was no actual
safety consequence as a result of the falsificaticns, and the violation
involved the isolated acts of a low-level individual. Therefore, this
non-repetitive licensee-identified and corrected violation is being
treated as a Non-Cited Violation (NCV). consistent with Section VII,B.1
of the NRC Enforcement Policy. This is identified as NCV 50-348,
364-97-14-08: Falsification of Emergency Planning Checklists Resulted in
inaccurate Records Being Maintained by the Licensee.
SI Conduct of Security and Safeguards Activities (71750)
51.1 Routine Observationc of Plant Security Measures
During routine inspection activities, inspectors verified that portions
of site security program plans were being properly implemented. This was
evidenced by: proper display of picture badges and use of the biometrics
system by plant personnel: appropriate key carding of vital area doors;
adequate stationing / tours in the protected area (PA) by security
Enclosure 2
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personnel: proper searching of packages / personnel at the primary access
point and service water intake structure (SWIS): and adequate performance
of security systems (i.e., video cameras). Security personnel activities
observed during the inspection period were performed well. Site security
systems were adequate to ensure physical protection of the plant.
Inspector tours of the power block and SWIS PA boundaries verified
structural integrity and condition of PA barriers.
F8 Hiscellaneous Fire Protection Issues (IP 71750)
F8.1.(flased)VIO 50-348/96-410-01013: Failure to Assure that Electrical
Cables Associated with Systems Necesjiary to Actueve and Maintain Hot
Shutdown Conditions Were Enclosed in One-Hour Fire Barriers (92904l
The licensee responded to this VIO in correspondence dated December 4
1996 and initiated Corrective Action Reprt (CAR) 2225. An inspector
reviewed the licensee's letter, completed CAR. and implementation of the
corrective actions. The inspector observed portions of the installation
of one of the fire barriers. This was documented in IR 50-348.
364/97-05. The inspector also verified that the remaining fire barriers
were installed. The corrective actions identified in the CAR were
consistent with those identified in LER 50-348/96-006. This VIO is
closed.
F8.2 (Closed) LER 50-348/96-006-00: Kaowool Fire Barriers Not Installed Der
Desian Drawinas (92700)
This LER reported the issue cited in VIO 50-348/96-410-01013. This LER
is closed based on the licensee's completion of corrective actions
described in Section F8.1.
F3.3 (Closed) VIO R-348. 364/96-410-02014: Inadecuate Periodic Insoection
Procram for Kaowool One-Hogr Fire Barriers (92904)
The licensee responded to this V10 in correspondence dated December 4
1996, and initiated CAR 2226. The inspectors reviewed the licensee's
letter, completed CAR. and implementation of the corrective actions.
Licensee corrective actions included: 1) updating FNP-0-FSP-43. " Visual
Inspection of Kaowool Wraps." to provide more detailed inspection
guidance and identification of specific wraps to be inspected. 2)
training insaection personnel for required Kaowool configurations, and 3)
reviewir.g otler aspects of the fire protection inspection prograra which
were transferred to maintenance for similar problems. The inspectors
verified that the corrective actions were complete. This VIO is closed.
Enclosure 2
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V; Hanaaement-Heetinas-and Other Areas
- X1-- . Review of Updated Final Safety Analysis Report Commitments . ;
.
'
A recent discovery of a licensee o)erating its facility in a manner ~
' contrary to the UFSAR description lighlighted the need for a special
-focused review that compares plant practices. procedures and/or
parameters to the UFSAR descriptions. While performing the inspections-
discussed in this-report, the inspectors rt. viewed the applicable portions
of the UFSAR that related to the areas inspected. The inspectors
verified that the UFSAR wording was consistent with the observed plant
oractices procedures-and/or parameters.
F X2 : Exit Heeting.Sunnary i
'The inspectors presented the inspection results to members of licensee
management on December 4. 1997; The licensee acknowledged the findings
presented.
The inspectors asked the 1leensee whether any materials examined during .
the inspection should be considered proprietary. No proprietary
information was identified.
PARTIAL LIST OF PERSONS CONTACTED
Licensee
C -Buck. Operations Superintendent - Unit 2 ;
F Coleman. Maintenance Manager
3' C. Collins. Operations Superintendent - Administration
P. . Crone. Engineering Support Performance Supervisor
T. Esteve. Planning & Control Supervisor
R; Fucich. Engineering Support Manager
S. Gates. Administration Manager
D. Gr:ssette. Operations Manager
'P. Harlos. Plant Health Physicist
R. Hill. General Manager
C. Hillman,- Security Chief
R.-Johnson. 0perations Superintendent - Procedures
T. Livingston, Chemistry Superintendent
R. Martin. Maintenance Team Leader
M. Mitchell~, HP Superintendent
-C.-Nesbitt. Assistant Genera 1' Manager Plant Support
W. :Oldfield. Nuclear _0perations Training Supervisor -
C. Reneau. Maintenance Team Leader---Team 5
M, Stinson, Assistant General Manager. Operations -
G. Waymire. Technical ~ Support Manager
R Yance. Plant-Modifications and Maintenance Support Manager
BRC:. .
J.1Zimmerman -NRR~ Project Manager
.=_.
.
Enclosure 2 '
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INSPECTION PROCEDURES (IP) USED
IP:37551:- 1
IP'50001: Onsite Engineering
Steam Generator Rep lacement Inspection- ,
IPL61726: Surveillance Observations- ,
IP 62707:~ - Maintenance Observations- .
>
IP 71707: Plant Operations
'IP'71714i ! Cold-Weather Preparations *
IP 71750: Plant Support Activities '
JIP 83750: Occupational Radiation Exposure
- Radioactive Waste Treatment, and Effluent-and Environmental
IP 84750:-
'
- Monitoring- s
- IP 86750:- - Solid Radioactive Waste Management and Transportation of
- Radioactive Materials ,
IP 90712: In Office Review of Written Reports of Non-Routine Events at:
,
Power Reactor Facilities
~'.- 'IP 92700: Onsite followup of Written Reports = of Non Routine Events at f
Power Reactor Facilities
IP 92901: Followup ~- Operations
IP 92902: Followup - Maintenance !
-IP 92903: Followup - Engineering
-IP-92904: Followup _- Plant Support-
--TI 2515/133: Im31ementation of Revised 49 CFR Parts 100-179 and 10CFR
-
'
)ar+ 71. .
_
TI-2515/136: Operation of Dual Function Containment Isolation Valves
,
ITEMS OPENED, CLOSED, AND DISCUSSED
- Opened
Iygg Item Number Status Descriotion and Reference
NCV 50-348. 364/97-14-01 Open Inadequate-Imolementation of Cold
Weather Protection Procedures
- (Section 02.7)
NCV 50-348, 364/97 14-02 Open Failure To Sign Off= Steps For
Continuous Use Procedures as They Are-
. Performed (Section M1.1)
- VIO 50-348, 364/97-14-03.
_
Open Inadequate Corrective Actions for-
^
Naintaining Main Steam Valve Room Cork -
Seal Flooding Barrier (Section M8.1)-
NCV 50-348/97-14 04- 0 pen Entry Into TS 3.0.3 Due to the Failure 3
to Follow.the' Work Control Process
. Procedure (Section M8.4)
t
Enclosure 2-
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'
- VIO? 50 348.-364/97-14-05- Open !
l Failure _ to Provide: Tornado Missile '
Protection:for TDAFW Pump Vent Stack:
(Section E8.1)
'
,
NCV' 50'-348,' 364/97-14-06'- '
- Open Failure to Follow Wholebody Counting _-
-
(WBC) Analysis Procedures for'.
'
i
Evaluation of Workers' Potential:
Radionuclide Intakes (Paragraph R1.3)
NCV'50-364/97-14-07 Open Failure to Conduct Compensatory Grab; .
Sampling for Inoperable Unit 2- e
' Containment Atmospheric Radiation '
' Monitoring-System in accordance with-
TS 3.4.7.1 (Paragraph R8.3) :
NCV -50-348, 364-97-14-08 Open Falsification of Emergency Planning
Checklists Rcsulted in Inaccurate -
--
Records Being Maintained-by the -
Licensee (Section P8) <
Closed
lypg Item Number. Status -Description and Reference
NCV. 50-348, 364/97-14-_01 Closed Inadequate Implementation of Cold-
Weather Protection Procedures
(Section 02.7)
NCV 50-348, 364/97-14-02 Closed Failure To Sign Off Steps For
Continuous Use Procedures as They Are
Performed (Section M1.1)
.I
NCV' 50-348/97-14-04- Closed Entry Into TS 3.0.3 Due to the Failure
to Follow the Nork Control Process
N cadure (Section M8.4)
LER 50-348, 364/96-01 Closed- TS Action Statement Requirement Not-
.
Met For SSPS Testing (Section M8.3)
u
-LER 50-348/97-11- C W,ed Entry Into TS 3.0.3 Due to the Failure-
, to Follow the Work Control-Process
Procedure (Section M8.4)
IFI 50:348.1364/96-02 03- : Closed Pre-Action Sprinkler System Failures
(Section-M8.2)-
i
LER 50-348, 364/97-07-00- ' Closed
-
- 0utside Of Design Basis _ Due To
Degraded Cork Material (Section M8.1)
l
!
Enclosure-2._
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LURI '50-348,.364/97-201-08 Closed- Tornado Protection of TDAFW-Pump Vent: i
Stack 'Section E8.1)
. ~LER 450 348/96-006-00- -Closed - Kaowool Fire Barriers Not Installed !
- per Design Drawings (Section F8.2)-
' ~ VION 50-348/96-410-01013 Closed Failure to Assure that Electrical
Cables Associated with SystemsL
i -
- Necessary to Achieve and Maintain Hot :
Shutdown Conditions Were Enclosed in -
One-Hour Fire Barriers (Section F8.1)
'
--VIO 50-348,'364/96 410-02014 Closed Inadequate Per. iodic Inspection Program
for Kaowool One-Hour Fire Barriers
(Section F8.3)-
- - -
Failure to FolicW Wholebody Counting; i
NCV 50-348;-364/97-14-06 Closed-
(WBC) Analysis Procedures for i
Evaluatiore of Workers' Potential
Radionuclide Intakes (Paragraph R1.3)
-NCV- 50-364/97-14 07
-
Closed Failure to Conduct Compensatory Grab
Sampling for Inoperable Unit 2
. Containment Atmospheric Radiation-
r Monitoring System in accordance with
TS 3.4.7.1 (Paragraph'R8.3)
NCV 50-348, 364-97-14-08 Closed Falsification of Emergency Planning
Checklists Resulted in Inaccurate
- Records Being Maintained by the
Licensee (Section P8) .
VIO 50-348/97--10-05 Closed Inadequate Configuration Control of U1
-
RMS Particulate Sample Lines
(Section R8.2) ;
LER 50-364/97-04-00 Closed Operating Outside of Technical
E Specifications Due. to Required
Containment Grab Samples Not-Being
>
Taken (Section R8.3)
.
- Discussed-
,
Iygg Item Number Status Descriotion and Reference ,
sVIO:150-348. 364/96-10-01~- Open: Failure to Construct and Maintain an-
"As-Built" Sample Line in Accordance
-
.
with Configuration Control Procedures-
m and Drawings (Section R8.1)
.
i
, Enclosure 2-
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,
.
SYNOPSIS
The Office of Investigations. U.S. Nuclear Regulatory Commission. Region II.
initiated this investigation on March 17, 1997. in order to determine if a
former Emergency Planning (EP) techr.ician at Alabama Powar Company's Joseph m.
Farley Nuclear Plant had failed to conduct required inspections of emergency
equi) ment and supplies, and deliberately falsified EP equipment inspection
checclists.
Based upon the evidence develo)ed in this investigation, it is concluded that,
during the period April 1996 tirough January 1997, the former EP technician
failed to conduct at least three required inspections, and deliberately
falsified at least four checklists.
Case'No. 2-97-005 Attachment