IR 05000348/1988029

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Insp Repts 50-348/88-29 & 50-364/88-29 on 881011-1110.No Violations or Deviations Noted.Major Areas Inspected:Review of Operational Safety Verification,Monthly Surveillance Observation,Info Meeting W/Officials & Emergency Exercise
ML20196A225
Person / Time
Site: Farley  Southern Nuclear icon.png
Issue date: 11/23/1988
From: Dance H, Maxwell G, Miller W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20196A205 List:
References
50-348-88-29, 50-364-88-29, NUDOCS 8812050290
Download: ML20196A225 (8)


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UNITED STATFS 3'

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NUCLEAR REGULATORY COMMISSION

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REGION il o,

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int MARIE TTA ST.. N.W.

g ATLANTA. GEORGIA 30323

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Report Nos.: 50-348/88-29 and 50-364/88-29 Licensee:

Alabama Power Company 600 North 18th Street Birmingham, AL 36291 Docket Nos.:

50-348 and 50-364 License Nos.:

NPF-2 and NPF-8 Facility name:

Farley 1 and 2 Inspoetion Conducted: October 11 - November 10, 1988

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Inspection at Fa ley site fear Dothan, Alabama Inspectors:

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Approved by:

4. C. Dance, Section Chief D'a te S'i g n ed Division of Reactor Projects SUMMARY Scope:

This routine on-site inspection involved a review of operational safety verification, monthly surveillance observation, montnly maintenance observation, information meeting with local officials, emergency exercise, and previous inspection findings, and followup of events.

Results: Within the areus inspected, no violations or deviations were identified.

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REP;RT DETAILS 1.

Licensee Employees Contacted D. N< Morey, General Manager R. D. Hill, Assistant General Manager - Plant Operations

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L. M. Stinson, Assistant General Plant Manager - Plant Support J. K. Osterholtz, Operations Manager C. D. Nesbitt, Technical Manager

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R. G. Berryhill, Systems Performance and Planning Manager J. J. Thomas, Maintenance Manager C. L. Buck, Plant Modifications Manager

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L. W. Enfinger, Administrative Manager L. S. Williams, Training Manager J. E. Odom, Operations Unit Supervisor B. W. Vanlandingham, Operations Unit Supervisor R. Swift, Operations Unit Supervisor - Administrative T. H. Esteve, Outage Planning Supervisor A. M. Davidson, Daily Planning Supervisor i

J. B. Hudspeth, Document Control Supervisor L. K. Jones, Material Supervisor R. H. Marlow, Technical Supervisor

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T. W. Cherry, I & C Supervisor H. R. Garland, Mechanical Maintenance Supervisor B. R. Yance, Electrical Maintenance.ipervisor M. W. Mitchell, Health Physics Su.

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R. H. Graham, Security Supervisor F. G. Watford, Fire Marshall Scott Fulmer, Supervisor, Safety Audit Engineering Review i

Other licensee employees contacted included, technicians, operations personnel, maintenance and I&C personnel, security force members, and office personnel.

Acronyms and abbreviations used throughout this report are listed in the last paragraph.

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2.

Operational Safety Verification (71707, 92700)

i The inspectors conducted routine plant tours during this inspection period i

to verify that the licensee's requirements and commitments were being

implemented. These tours were performed to verify that: systems, valves, and breakers required for safe plant operations were in their correct

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position; fire protection equipment, spare equipment and materials were

being maintained and stored properly; plant operators were aware of the current plant status; plant operations personnel were documenting the status of out-of-service equipment; security and health physics controls were being implemented as required by procedures; there were no undocumented cases of unusual fluid leaks, piping vibration, abnormal hanger or seismic restraint movements; all reviewed equioment requiring calibration was current; and general housekeeping was satisfactory.

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Tours of the plant included review of site documentation and interviews with plant personnel. The inspectors reviewed the control room operators'

logs, tag out logs, chemistry and health physics logs, and c:ntrol board:

and panels.

During these tours the inspectors noted that the operators

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ar9 eared to be alert, aware of changing plant conditions and manipulated piant controls properly.

The inspectors evaluated operations shift

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turnovers and attended shift briefings. They observed that the briefings

and turnovers provided sufficient detail for the next shift crew and verified that the staffing met the TS requirements.

i Sito security was evaluated by observing personnel in the protected and vital areas to ensure that these persons had the proper authorization to be in the respective areas. The inspectors also verified that vital area portals were kept locked and alarmed. The security personnel appeared to be alert and attentive to their duties and those efficers performing

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personnel and vehicular searches were thorough and systematic. Resperses to security alarm conditions appeared to be prompt and adequate.

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Selected activities of the licensee's Radiological Protection Program

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were reviewed by the inspectors to verify conformance with plant procedures and NRC regulatory requirement.

The areas reviewed included:

operation and management of the plant's health physics staff, "ALARA" l

implementation, Radiation Work Permits (RWPs) for compliance to plant

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procedures, personnel exposure records, observation of work and personnel in radiation areas to verify compliance to radiation protection procedures, and control of radioactive materials.

No discrepancies were

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noten.

On October 21 while operating at 100% reactor power a Unit 1 reactor trip occurred.

The trip was reported to the NRC in accordan:e with 10 CFR 50.72, 10 CFR 50.73 and site administrative procedure FNP-0-AP-16 Conduct of Operation. The licensee has documented the event and is evaluating the facts and circumstances surrounding the trip.

The inspectcrs reviewed the preliminary Licensee Event Report data, interviewed responsible operations and maintenance personnel and noted the following:

Reactor trip occurred after the main turbine throttle valves closed.

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i Throttle valves closed while maintenance personnel were conducting

maintenance activities on the main turbine over-speed protection

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computer circuit.

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Maintenance activities were non-safety related and were authorized by maintenance work request MWR 186751.

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Authorized maintenance activities required a test card to be inserted

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i into the turbine speed control card rack. Records indicate that when

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computer's universal input output buss.

This resulted in a signal being generated to cause the turbine main throttle valves to close.

When maintenance personnel re-enacted the work functions which preceded the turbine trip, they discovered that the test card had a switch located near the outer front edge of the card.

If the card was grasped in the mid front position while inserting, it is likely that the test switch could have been momentarily re positioned. An analysis of the speed control circuitry indicates that momentarily flipping this test switch to the "simulate" position while pushing the card into place could cause a false trip signal to be injected into the speed control circuit.

Following the reactor trip all of the required equipment started and the plant was maintained in a safe shutdown condition until the cause of the trip was 6.sessed by operations personnel.

The plant was returned to power operation on October 22.

The inspectors have reviewed the licensee's evaluation of this trip and have no further questions at this time.

The inspectors reviewed the medical records of two shift supervisors and four reactor operators which have an NRC senior reactor operator or reactor operator license. The scope of this audit was to verify that the medical examinations satisfied the requirement of 10 CFR 55 and that each operator's medical records were up to date. Of the records reviewed no discrepancies were identified.

On October 19 Unit 2 experienced excessive vibration on the butterfly valve which is used for isolating the service water flow through the 2C component cooling water heat exchanger. A maintenance work request

'MWR-185161) was initiated to authorize the necessary maintenance to repair the valve.

Maintenance personnel inspected the operator on the valve (Q2p16V0007C) and found the lever to be worn and the pin located in the thrust collar was sheared. Authorized repairs were made, the valve operator was tested and the valve was returned to service.

3.

Monthly Surveillance Observation (61726)

The inspectors witnessed the licensee conducting maintenance surveillance test activities on safety related systems and components to verify that the licensee performed the activities in accordance with TS and licensee requirements. Those observations included witnessing selected portions of each surveillance, review of the surveillance procedures to ensure that administrative controls and tagging procedures were in force, determining that approval was obtained prior to conducting the surveillance test and the individuals conducting the test were qualified in accordance with plant-approved procedures. Other observations included ascertaining that test instrumentation used was calibrated, data collected was within the

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specified requirements of TS, any identified discrepancies were properly noted, and the systems were correctly returned to service. The following specific activities were observed:

1-STP-5.0 Full Length Control Rod Operability Test 1-STP-9 RCS Leakage Test 2-STP-9 RCS Leakage Test 2-STP-11.10 RHR Pump 2B Monthly Operability Test 2-STP-20.2 Penetration Room Filtration System Train B Operability Test 1-STP-23.1 CCW Pump 1A Quarterly IST 1-STP-23.7 CCW System Flow Path Verification Test 2-STP-33.0B Solid State Protection System Train B Operability Test 1-STP-33.0A Solid State Protection System Train A Operability Test 1-STP-33.1A Safeguards Test Cabinet Train A Functional Test 0-STP-52.1 Diesel Fire Pump 1A Operability Test 2-STP-80.1 OG 28 Operability Test 0-STP-80.2 DG 2C Operability Test 2-STP-80.6 DG 2B 24 Hour Run 1-STP-129 Low Pressure CO2 System Test 1-STP-223.3A Hydrogen Recombiner 1A Calibration 2-STP-228.6A Nuclear Instrumentation Power Range Calibration and Functional Test 2-STP-607.1 Containment Air Lock Leakage Test 1-$0P-23.0 Train B CCW Surge Tank Feed and Bleed 1-SOP-23.0B Shift SW from CCW Train A to CCW Train B 1-ETP 3616 Flux Map Testing 4.

Monthly Maintenance Observation (62703)

The inspectors reviewed the licensee's maintenance activities to verity the following: maintenance personnel were obtaining the appropriate tag out and clearance approvals prior to commencing work activities, correct documentation was available for all requested parts and material prior to use, procedures were available for all requested parts and material prior to use, procedures were available and adequate for the work being conducted, maintenance personnel performing work activities were qualified to accomplish these tasks, no maintenance activities reviewed were violating any limiting conditions for operation during the specific evolutions, the required QA/QC reviews and QC hold points were implemented, post-maintenance testing activities were completed, and eo' Ipment was properly returned to service af ter the completion of work activities. Activities reviewed included:

WR 150780 Inspect Terminal Strips in MCC IT For Proper Installation MWR 151349 Replace Broken Hinge Support On Fire Damper 1-119.09 MWR 179066 Installation of Support for level Switch to Reactor Make-up Water Tank

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WR 180914 Replace Head Gasket on Diesel Engine Fire Pump No 2 MWR 180983 Remove and Replace Relief Valve to Unit 1 Train B CCW Room Cooler 1-GMP-52.1 Weekly Battery Checks WA 70094 Tendon Inspection:

ETP-4202 Tendon Grease Inspection (Tendon V-59)

WA 85775 Inspection of Unit 1 Train B CCW Room Cooler WA 85778 Inspection DG 1B in accordance with:

MP-12.3 Diesel Air Start System MP-14.6 Model PC-2V Diesel Engine Quarterly Inspection WA 85791 Inspection of Unit 2 Train A CCW Room Cooler i

WA 92355 Inspect DG 1B While Operating For Oil / Water Leaks and Correct if Possibie 5.

Information Meeting With Local Officials (94600)

On October 14 the inspectors visited and met the staff of the Houston County Emergency Management Ager.cy in Dothan, Alabama.

A brief description of the NRC organization and its relationship to the operation of the Farley Plant was given to the Emergency Management Agency staff.

The inspectors also toured the Emergency Operations Complex.

The meeting was beneficial in that the resident inspectors learned more about the organization and function of the Emergency Management Agency and were able to provide information about the NRC's normal responsibilities and duties in the event of an emergency.

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6.

Emergency Exercise of 1988 (82301)

The resident inspectors participated as team members in the NRC evaluation of the Farley Emergency Exercise which was conducted on November 2,1988.

The 1988 Emergency Exercise consisted of a simulated seismic event which caused a loss of the

"A" train emergency 4160V buses.

The loss of electrical power in conjunction with initial charging pump and CCW pump configuration resulted in a loss of RCP seal cooling.

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after the seismic event, the RCP seals failed causing a loss of reactor l

coolant accident and an Alert classification. An aftershock at 9:15 a.m.

t resulted in a CROM rupture and subsequent declaration of a Site Area Emergency.

At 10:30 a.m. another af tershock lead to the failure of the personnel hatch and leakage from containment to the environment.

On November 2 at approximately 2:50 p.m. during the annual emergency drill the off-site emergency notification sirens at Ashford, Columbia and Gordon were found to be inoperative.

Investigation by the Houston (Alabama)

Emergency Management Agency found that the main actuation panel would not actuate the sirens by using the normal actuation devise.

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repairs were made to the system at 4:45 p.m. on November 2 which permitted I

the system to be operational. Final repairs were completed on November 3 at 11:00 a.m, and the system was fully restored and returned to service.

The system was subsequently tested satisfactorily on November 9.

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On November 3 a joint NRC/ licensee critique was held to discuss the strong points and areas in need of improvements which were identified during the exercise. Refer to NRC Report 348,364/88-30 for additional information on the exercise and critique.

In general the objectives of the 1988 Emergency Exercise were met and the participants'

performance satisfactorily demonstrated that the Emergency Plan Implementing Procedures are adequate to protect the health and safety of the public.

7.

Action on Previous Inspection Findings (92702)

(Closed) Violation 364/88-23-01, Failure to remove charcoal filter units from Unit 2 Penetration Ventilation Equipment Room following changeout.

The licensee's letter of response dated August 15, '2988 indicates the corrective action taken on the violation. This action included retraining the plant staff in the requirements of FNP-0-AP-35, General Plant Housekeeping and Cleanliness Control. The inspectors verified that this training had been accomplished.

This item is closed.

(0 pen) Part 21 348,364/88-03 Gamma-Metrics Cable Assemblies Installed As Part of the Neutron Monitoring System May Possibly Leak.

This item is being evaluated by the licensee.

Appropriate corrective action is scheduled to be accomplished during the next refueling outages, Fall of 1989 for Unit I and Spring of 1989 for Unit 2.

This item remains open and will be reviewed when the corrective actions have been completed.

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Other Activities During this report period the licensee made changes to their site management organization; these changes are as follows:

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Shipman, Assistant General Manager - Plant Operations was re-assigned to a position in the corporate office. He was replaced by R. D. Hill the former Assistant General Manager - Plant Support.

The position vacated by the Site Assistant General Manager - Plant Support was filled by M. Stinson, formerly the Plant Modifications Manager.

This later position was filled by C. Buck.

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Exit Interview The inspection scope and findings were summarized during management interviews throughout the report period and on November 9, with the plant manager and selected members of his staff.

The inspection findings were discussed in detail.

The licensee acknowledged the inspection findings and did not identify as proprietary any material reviewed by the inspection during this inspection.

Licensee was informed that the item discussed in paragraph 7 was closed.

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11. Acronyms and Abbreviations Auxiliary Feedwater AFW

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Abnormal Operating Procedure AOP

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Administrative Procedure AP

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Alabama Power Company APC0

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Code of Federal Regulations CFR

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Component Cooling Water CCW

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Design Change DC

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Deviation Report DR

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Emergency Contingency Procedure ECP

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Emergency Plant Implementing Procedure EIP

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Environmental Qualifications EQ

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Engineered Safety Features ESF

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Engineering Work Request EWR

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Fahrenheit F

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Final Safety Analysis Report FSAR

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Gallons Per Minute GPM

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Inservice Inspection ISI

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Inservice Test IST

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Limiting Condition for Operation LCO

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Licensee Event Report LER

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Motor-Operated Valve MOV

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Motor-0perated Valve Actuation Testing Maintenance Work Request MWR

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Nonconformance Report NCR

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Nuclear Regulatory Commission NRC

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NRC Office of Nuclear Reactor Regulation NRR

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Plant Modifications Department PMD

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Quality Assurance QA

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Quality Control QC

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Radiation Control and Protection Procedure RCP

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Reactor Coolant System RCS

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Residual Heat Removal RHR

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Safety Injection SI

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Safety Audit and Engineering Review SAER

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Steam Generator S/G

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Solid State Protection System SSPS

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Solenoid Operated Valve i

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Surveillance Test Procedure STP

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Service Water SW

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Technical Specification TS

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Technical Support Center TSC

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Work Authorization WA

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