ML20138J666

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Insp Repts 50-348/97-03 & 50-364/97-03 on 970216-0329. Violations Noted.Major Areas Inspected:Licensee Operations, Engineering,Maint & Plant Support,Including Health Physics
ML20138J666
Person / Time
Site: Farley  Southern Nuclear icon.png
Issue date: 04/28/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20138J621 List:
References
50-348-97-03, 50-348-97-3, 50-364-97-03, 50-364-97-3, NUDOCS 9705080289
Download: ML20138J666 (20)


See also: IR 05000348/1997003

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U.S. NUCLEAR REGULATORY COMMISSION (NRC)

REGION II

Docket Nos: 50-348 and 50-364

License Nos: NPF-2 and NPF-8 l

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Report No: 50-348/97-03 and 50-364/97-03

Licensee: Southern Nuclear Operating Company. Inc.

Facility: Farley Nuclear Plant (FNP). Units 1 and 2

Location: 7388 North State Highway 95

Columbia. AL 36319

Dates: February 16 through March 29. 1997

Inspectors: T. Ross. Senior Resident Inspector

J. Bartley, Resident Inspector

R. Caldwell. Resident Inspector (In training)

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l Approved by: P. Skinner. Chief. Projects Branch 2

l Division of Reactor Projects

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Enclosure 2

9705080289 970429

PDR ADOCK 05000348

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EXECUTIVE SUMMARY

Farley Nuclear Power Plant. Units 1 and 2

NRC Inspection Report 50-348/97-03, 50-364/97-03

This integrated inspection included aspects of licensee operations,

engineering. maintenance, and plant support. The report covers a 6-week

period of resident inspections.

Doerations

e Operations personnel performed well while maintaining plant coriditions >

during Unit 1 and 2 at steady state full power operation. The Unit 1

shutdown. cooldown, and draindown was generally well controlled

(Sections 01.1 and 01.3).

  • Unit 1 defueling activities were generally well controlled (Section

01.2).

e A violation was identified for multiple instances of failing to follow

procedure (Sections 01.3 and 01.4).

e A non-cited violation was identified for Nuclear Instrumentation System

(NIS) power range channels exceeding the Technical Specifications (TS)

limiting safety system setpoint (Section 01.5).

e Housekeeping and physical conditions were generally adequate, although

certain areas were poor. Licensee efforts to improve targeted areas was

evident. However, overall efforts to improve plant appearances

proceeded very slowly. (Section 02.1).

e Operator overtime was adequately controlled and the records were

thorough (Sectiori 06.1).

e Licensee efforts to identify. resolve, and prevent problems remained

effective (Section 07.1).

e The Nuclear Operations Review Board (NORB) meeting fulfilled the minimum

requirements of TS 6.5.2. However, no declining or adverse trends were

identified and no recommendations were made for improving plant safety

or the effectiveness of Safety Audit and Engineering Review (SAER) group

audits (Section 07.2).

Maintenance

o Maintenance and surveillance testing activities were generally conducted

in a thorough and competent manner by qualified individuals in

accordance with plant procedures and work instructions (Sections M1.1.

M1.2, M1.3. M1.4. and M1.5).

e The SAER Maintenance Rule audit was indepth and comprehensive (Section

M7.1).

Enclosure 2

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e Licensee's corrective actions for procedural compliance failures have

not been fully effective (Sections M8.1 and 01.4).

Engineerina

e Engineers and operators conducting the Unit 1 spent fuel inventory were

knowledgeable and followed their procedures (Section E1.1).

e An Engineering Sup] ort meeting focused awareness on recent procedure

implementation pro]lems (Section E4).

Plant Suncort

e Health Physics control over the radiologically controlled area, and the

work activities conducted within it. was good. Some contaminated areas

we,' cramped and physically restricted removal of anit-contamination

clothing (Section R2.1).

e Security activities continued to be performed in a conscientious and l

capable manner, assuring the physical protection of protected and vital

areas (Section 51.1). j

Enclosure 2

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l Report Details

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Summary of Plant Status (

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Unit 1 operated at 100% power until March 15. 1997, when the unit was shutdown

! for its 14th refueling outage (U1RF14) after 313 days of continuous operation.

j U1RF14 is scheduled to be completed in 55 days.  ;

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Unit 2 operated continuously at 100% power for the entire inspection period.

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j I. Operations

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! 01 Conduct of Operations  :

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01.1 Routine Observations of Control Room Doerations

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j a. Insoection Scoce (Insoection Procedure (IP) 71707)

{ Inspectors conducted frequent inspections of ongoing plant operations in

the Main Control Room (MCR) to verify proper staffing, operator

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attentiveness, adherence to approved operating procedures,

communications, and command and control of operator activities.

Inspectors reviewed operator logs and Technical Specifications (TS)

4 Limiting Condition of 03eration (LCO) tracking sheets, walked down the

Main Control Boards (MC3), and interviewed members of the operating

shift crew to verify operational safety and compliance with TSs. The

inspectors attended the morning plant status meetings to maintain I

i awareness of overall facility operations, maintenance activities, and '

] recent incidents. Morning reports and Occurrence Reports (ors) were  !

! reviewed on a routine basis to assure that the licensee properly

reported and resolved potential safety concerns,

j b. Observations. Findinas and Conclusions

j Overall control and awareness of plant conditions during the inspection

period remained adequate. Inspectors observed that the Unit 1 MCBs.

4 prior to U1RF14, were in a " blackboard" condition on several occasions.

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Whereas, the Emergency Power Board and Unit 2 MCBs consistently had two

, or more persistent annunciators in alarm. Efforts to maintain MCB

deficiencies at low levels were not as effective as in the past. The

4 combined number of MCB deficiencies increased to 25, which is higher

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than normally observed. Operator response to changing plant conditions

remained very good. Interviews with the operating crew indicated that

they were aware of plant conditions and activities. Pre-shift briefs of

1 the operating crews by the shift supervisors (SS) were generally concise

and informative.

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On March 14. 1997, the inspector observed the Unit 1 crew's response to

low charging flows through the charging flow control valve FCV-122. The

1 crew's actions were logical, well thought out, and accomplished in

i accordance with (IAW) plant procedures.

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01.2 Unit 1 Defuelina (IP 60710)

On March 23, 1997, the inspectors observed defueling activities. The

inspectors observed fuel handling evolutions in the MCR containment,

and Spent Fuel Pool (SFP). Fuel handling was typically well controlled

and conducted IAW Unit Operating Procedure (UOP) FNP-1-UOP-4.1.

" Controlling Procedure For Refueling." FP-ALA-R14. "J.M. FARLEY XIV - XV

Refueling." Revision 0, and Engineering Test Procedure (ETP) FNP-0-ETP-

3636. " Fuel Assembly Visual Inspection During Core Unload." Revision 8.

Personnel performing activities were knowledgeable. Records were

complete and communications between stations was effective.

01.3 Unit 1 Shutdown. Cooldown and Draindown for UlRF14

On March 15 and 17. 1997, inspectors observed portions of Unit 1

cooldown to Mode 5 IAW FNP-1-U0P-2.2. " Shutdown of Unit from Hot Standby

to Cold Shutdown." Revision 45, and subsequent draindown IAW Standard

Operating Procedure (SOP) FNP-1-SOP-1.6. " Draining of Reactor Coolant

System to Reactor Vessel Flange." Revision 24. An inspector also

reviewed the official completed copy of FNP-1-UDP-2.1 " Shutdown of Unit

from Minimum Load to Hot Standby." Revision 31 to verify all applicable

procedural steps had been signed off. Both the cooldown and draindown

evolutions were performed in a methodical, step-by step manner IAW

procedural instructions, except for one instance. Unit 1 operators

entered Mode 4 without ensuring the breakers for certain motor-operated

valves (MOV) were opened as required by UDP-2.2 (see section 01.4

below).

01.4 Failure To Follow Procedures

During the report period, the licensee and inspectors identified several

examples of plant personnel failure to follow procedure. The examples

are as follows:

e On February 27. 1997, an inspector observed that an i

Instrumentation and Controls (I&C) technician only performed the  :

calibration check once for each of the two IB Emergency Diesel '

Generator (EDG) fuel oil day tank room float switches. The

preventative maintenance (PM) data sheets WOO 470336/7

specifically required the level check to be repeated three times

per switch. The inspector asked the I&C technician, during

conduct of this PM activity, whether it was appropriate to deviate

from the explicit instructions on the PM data sheets. The I&C

technician continued to perform calibration checks contrary to the

PM data sheets. This change to the PM was not approved as

required by FNP-0-GMP-1, " Preventative Maintenance Procedure".

Revision 17. Both float switches were verified to be within

required tolerance at least for the one time they were checked.

Maintenance management was notified of the observation.

Enclosure 2

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e On February 27, 1997, the licensee discovered that numerous

checklists for verifying emergency equi) ment and supplies were not

being performed at the frequencies esta)lished by Emergency Plan

Implementing Procedure (EIP) FNP-0-EIP-16.0 " Emergency Equipment

and Supplies." Revision 31. Following a quality assurance audit

by the. Safety Audit and Engineering Review (SAER) group. an

Emergency Planning (EP) technician stated that he had falsified

many of the EP-16.0 checklists. He stated that this had been

going on for several years. The EP technician stated that he.had

performed the checklists on occasion, but not on the prescribed

frequency. See report section P3.1 for discussion of licensee

corrective actions,

e On March 15. 1997, during initial cooldown for U1RF14 IAW UDP-2.2,

a Unit 1 operator recognized that the power supply breakers for

MOVs 8706A and 8706B (RHR pump discharge to charging pump

suctions) were not opened prior to entering Mode 4 (i.e. RCS

temperature below 350 degrees F). TS 4.5.3.2 requires MOVs 8706A

and B to be closed with their breakers locked open when in Mode 4

for overpressure protection. This TS requirement is reflected in

the " Caution" statement before step 5.21 of UOP-2.2. Operators

failed to recognize this TS and procedural recuirement until after

Unit 1 RCS temperature was reduced below 350 cegrees. The

applicable breakers were opened and locked about six minutes after

entering Mode 4. Both MOVs were closed and remained closed during_.

the Mode 3 to Mode 4 transition. The licensee initiated OR #1-97-

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e On March 16, 1997, during the performance of step 9 4.2 of .

Surveillance Test Procedure (STP) FNP-1-STP-158. " Reactor Coolant i

System Pressure Isolation Valve Leak Test." Revision 15. a Unit 1 l

operator noticed a sharp reduction in residual heat removal (RHR)  !

system flow when MOV 8888B. RHR to Reactor Coolant-System (RCS) i

cold leg isolation valve, was shut. As RCS temperature began to

increase, the operator reopened MOV 8888B restoring RHR flow and <

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adequate reactor core decay heat removal. RCS temperature had

remained at approximately 180 degrees F during the incident, i

Operators terminated the test. The licensee initiated an i

investigation (OR #1-97-69). The licensee determined that the

test engineer. failed to restore the initial system valve lineup as I

required by ste) 8.12 of FNP-1-STP-158 after he completed the

check valve bacc leakage of step 9.3. By not restoring the system l

lineup, manual valve 89728 remained closed before commencing the >

next check valve back leakage test in step 9.4. Consequently. RHR ,

flow in one of the three cold leg injection paths was left

isolated. When step 9.4 2 was performed and a second cold leg t

injection path was isolated. RHR flow was aligned to only one cold j

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Enclosure 2

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leg path. This flow was inadequate for decay heat removal.

[ Note. the STP requires isolating one of the three cold leg

injection paths in order to perform the check valve back leakage

test].

The aforementioned examples constitute a violation (VIO) of TS 6.8.1.

which is identified as VIO 50-348. 364/97-03-01. Multiple Examples of i

Failure To Follow Procedure. 4

Although the circumstances and causes were different, other violations

and non-cited violations (NCV) involving personnel failure to follow

procedure were identified during U1RF13. the last Unit 1 refueling

outage (i.e.. VIO 50-348. 364/95-18-05: Multiple Examples Of Inadequate

Procedural Compliance) and during the last 10 months as listed below:

NCV 50-364/96 1.5-01: Operator failed to establish an RCS vent path )

during critical midloop level changes.

VIO 50-348. 364/96-09-01: Multiple valve misalignments by System

o)erators resulted in two letdown transients and rendered the IB

E E inoperable.

VIO 50-3/ '96-07-01: I&C technician adjusted Unit 1 nuclear

instrumentation system (NIS) intermediate range compensating

voltage during inappropriate conditions.

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NCV 50-348, 364/96-04-06; Operations shift foreman made numerous  !

EDG test data log entry errors '

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In each of the above violations, plant personnel failed to follow I

applicable procedural steps and/or guidance due to inadequate attention

to the details of the job being conducted. None of the previous

violations and NCVs have specifically recurred. However, based on the

significant number of problems with failure to follow procedures it is

evident that prior corrective actions have not been completely effective

in preventing reoccurrence of similar problems.

01.5 (Closed) Licensee Event Reoort (LER) 50-364/97-001: Nuclear

Instrumentation System Inaccuracies Below 50% Power

Based on a review of Westinghouse Technical Bulletin ESBU-TB-92-14-R1.

the licensee identified that between January 31 and February 1.1996.

Unit 2 operated in condition prohibited by TS. Technical Specification 3.3.1 required that a minimum of three Nuclear Instrumentation (NI)  !

)ower range (PR) channels be operable. However. between January 31 and l

rebruary 1. two of four PR channels were inoperable while Unit 2 was at l

power due to mis-adjustments made at low power levels. Channels NI-41

and NI-44 were under-adjusted following a low power calorimetric such

that they would not have tripped the reactor on overpower until about

118.5%. The TS limiting safety system setting is less than 110%.

Enclosure 2

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The licensee modified the UDPs to specify reducing the PR high flux high

trip setpoint to 5 85% if PR NIs are adjusted during calorimetrics

performed at less than 50% rated thermal power. The inspectors verified

that the UOPs were revised. The revisions appeared to be adequate to

3revent recurrence. This licensee-identified and corrected violation is

3eing treated as a NCV consistent with Section VII.B.1 of the NRC

Enforcement Policy. This is identified as NCV 50-364/97-03-02.

Misadjusted NIS Power Range Channels Exceed TS Limiting Safety System

Setpoint.

02 Operational Status of Facilities and Equipment

02.1 General Tours of Specific Safety-Related Areas (IP 71707)

General tours of safety-related areas were performed by the inspectors

to examine the physical condition of plant equipment and structures, and

to verify that safety systems were properly aligned. These general

walkdowns included the accessible portions of safety-related structures,

systems, and components in the following areas:

e Unit 1 containment

e Unit 1 main steam (MS) valve room

o Unit 1 and 2 Condensate Storage Tank (CSTs)

e Unit 1 and 2 SFP. SFP heat exchangers (HXs), and SFP cooling pump

rcoms

e Unit I and 2 new fuel storage areas

e Unit 1 and 2 aiping penetration rooms (PPR) on 100 foot elevation

e Unit 1 and 2 3 prs on 121 foot elevation

e Unit 1 and 2 electrical penetration rooms and vital motor control

centers (MCCs)

e Unit 1 and 2 penetration room filtration (PRF) systems

e Unit 1 RHR HX room

o Unit 1B RHR pump room

o Unit 1 and 2 control room emergency filtration system (CREFS) and

control room air conditioning system

o Unit 1 and 2 charging pump rooms and hallway

e lurbine building

o EDG building

e Unit 1 and 2 turbine-driven auxiliary feedwater pump rooms

e Unit 1 and 2 motor-driven auxiliary feedwater (MDAFW) pump rooms

e Unit 1 and 2 containment spray pump rooms

e Unit 1 component cooling water pump and HX rooms

e Unit 1 and 2 vital 4160 volt alternating current (VAC) switchgear

and vital 600 VAC load center rooms, trains A and B

General material conditions nd housokeeping for Unit 2 were adequate.

Areas were generally clear ci cr. d debris. However, except for the

121 foot elevation PPR and 2A Charging pump skid, most painted surfaces

of floors and equipment were chip)ed, stained and worn. Unit I

refueling outage activities made lousekeeping a challenge, but efforts

Enclosure 2

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to control the effect of these activities were obvious. Limited efforts

to improve physical appearances plant areas and equipment were ongoing.

Overall efforts to improve plant appearances proceeded slowly. Minor

equipment and housekeeping problems identified by the inspectors during

their routine tours were reported to the responsible SS and/or

maintenance department for resolution. None of these problems

represented operability concerns.

02.2 Biweekly Insoections of Safety Systems (IP 71707)

Inspectors used IP 71707 to verify the operability of the Unit 1 and 2

CSTs. Accessible portions of the systems were verified to be properly

aligned and operable. The inspectors did not identify any significant

issues that adversely affected system operability.

Inspectors re-verified corrective actions for LER 50-348/94-005: Missile

Protection for Condensate Storage Tanks, due to the CST missile

arotection issue identified during a recent NRC Architect and

Engineering Inspection. Specific items verified were:

. The Vacuum degasification valves for each CST were closed and

appropriate hold tags applied.

. The emergency plugging equipment was stationed in the Diesel

Generator Building Carbon Dioxide room. The Maintenance

Department is responsible for installing the plugs, if required.

The inspectors observed that the plugging kit lacked patching

equipment and brought this finding to the attention of the

! licensee. The licensee added appropriate patching materials.

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. A procedure precaution addressing the issue was verified to be

incorporated into Abnormal Operating Procedure (AOP) FNP-0-AOP-

21.0. " Severe Weather." Revision 11.

During the CST system walkdown the inspectors identified numerous loose

and abandoned items (e.g., four sections of 2" X 4" planks about three

feet long, several hand-sized metal ]lates, and a four foot section of

two inch carbon steel pipe) within t1e fenced CST enclosures. These

were identified to the SS. The Inspectors concluded that corrective

actions were implemented.

02.3 Unit 1 Containment Tour

i On March 15. 1997, inspectors toured the Unit 1 containment shortly

after shutdown to Mode 3. Overall, containment looked good. Numerous

small boron leaks were identified from aipe caps. valve packing and body

to bonnet. Several of these leaks had 3een previously identified and

marked by licensee personnel. however many others had not, indicating

that they had not been identified.

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02.4 Taq Orders (IP 71707)

During the course of routine inspections portior.s of the following tag

orders (TO) and associated equipment clearance tag were examined by the

inspectors:

e TO# 97-0729: A Train CREFS recirculation filter unit

e TO# 97-0860-1: A Train PRF System

All tags and TOs examined by the inspectors were properly executed and

implemented.

02.5 TS LCO Trackina (IP 71707)

The inspectors routinely reviewed the TS LCO tracking sheets filled out

by the shift foremen. All tracking sheets for Unit 1 and 2 reviewed by ,

the inspectors were consistent with plant conditions and TS l

requirements. However, the licensee identified several TS compliance '

problems associated with the way the TS are written. These are as  ;

follows:

a) TS Table 3.3-1, Reactor Trip Instrumentation, functional unit 6.B

requires two channels of NIS source range (SR) to be operable

(indication only) prior to entering Mode 3. However NIS SRs are

deenergized at power and are not usually energized until many

minutes after entering Mode 3. Also the applicable surveillance

tests are performed after energizing.

b) TS 4.5.3.2 required certain emergency core cooling system valves

to be closed with their breakers locked open prior to entry into

Mode 4. However, these same valves are required to be operable

for Mode 3 per TS 3.5.2: TS provided no allowance far

transitioning from Mode 3 to 4 without entering a condition

prohibited by TS.

c) TS Table 4.3-1. Reactor Trip System Instrumentation Surveillance

Requirements, functional unit 2.B for NIS PR. neutron flux-low,

requires certain channel calibrations that are not only irrelevant

but can not be performed.

The licensee intends to address these TS problems in their upcoming

submittal incorporating the improved standard TS. In addition, the

licensee conducted a comprehensive review of all TS requirements

uniquely associated with decreasing Mode changes. The licensee will

issue applicable LERs which the inspectors will review.

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06 Operations Organization and Administration

06.1 Administrative Control of Goerator Overtime (IP 71707)

The requirements for control of operator overtime are contained in TS 6.2.2. The inspector interviewed two shift clerks and reviewed several

randomly selected operator overtime records for the period December 1

through 31. 1996. The inspector did not identify any discreaancies with

the control of operator overtime. The inspector concluded t1at the

o)erator overtime was adequately controlled and the records were

tlorough.

07 Quality Assurance in Operations

07.1 Effectiveness of Licensee Control in Identifyina. Resolvina. and

Preventina Problems (IP 71707 and 40500)

The inspectors briefly reviewed all newly initiated ors and completed

ors approved during the inspection period to ensure that plant incidents

which affect or could potentially affect safety were properly documented

and processed IAW Administrative Procedure (AP) FNP-0-AP-30.

" Preparation and Processing of Incident Reports." Revision 22 Selected

ors were reviewed in detail.

The inspectors concluded that the licensee's program for identifying and

resolving problems remained effective and was being accomplished IAW

FNP-0-AP-30. Plant personnel and management exhibited an appropriate

threshold for identifying problems. initiating ors. and assigning formal

root cause determinations. Each new OR received prompt attention and

was discussed in the morning status / plan of the day meeting. The

l Operations manager continued to pursue the OR backlog with other

j managers and reduce the number.

Inspectors reviewed the following ors for accuracy completeness and

reportability, and adequacy of corrective actions:

. OR #1-97-035: Inadequate Emergency Response Procedures associated

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l . OR #1-97-039: Auxiliary Feedwater FCV solenoid missing mounting

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screws

These ors were processed properly with one exception. The corrective

l actions specified in OR #1-97-035 were not completely implemented in

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that two operations personnel (a reactor operator and SS) assumed their

onsnift duties prior to reviewing Event Specific Procedure ESP-1.3.

" Transfer To Cold Leg Recirculation." procedure changes. Inspectors

identified this discrepancy to Operations management. The inspector

considered this a minor isolated occurrence.

Enclosure 2

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07.2 Nuclear Operations Review f.oard

a. Ecpag i

On March 20. 1997, inspectors monitored the quarterly meeting of the

Nuclear Operations Review Boarsi (NORB) via telephone. TS 6.5.2

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establishes the requirements ol' the NORB. TS 6.5.2.7 lists nine topics

which are required to be reviewed by the NORB.

b. Observations and Findings ,

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The NORB reviewed the topics prescribed by TS 6 5.2.7 in 30 minutes.

Overall, the NORB appeared to meet the minimum requirements of TS 6.5.2

mgarding attendance, quorum, and areas covered However, only a couple

of the NORB members actively participated. Mcinbers asked few questions.

Participation of several members was limited to signifying assent to the

. standard "NORB Recommendation Guide" stateents drafted by the NORB

secretary. No independent comments, conclusions, or recommendations

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were heard by the inspectors from the vanous NORB members. No

declining or adverse trends were identitied: no recommendations for

improving plant safety or effectiveness of SAER audits were made; all i

areas reviewed were adequate with no areas of weakness or proposed i

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In general, the meeting was quite perfunctory. Subsecuent to the

meeting, the NORB Vice Chairman did not reveal any adcitional insights

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except that NORB members are encouraged to review the meeting material

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and ask questions before the meeting. The Vice Chairman acknowledged

that this particular meeting was probably shorter and less dynamic than

most. However, the inspector considered this NORB meeting very similar

to one observed on February 21, 1996.

II. Maintenance

M1 Conduct of Maintenance

M1.1 General Comments

a. Inspection Stone (IP 61726 and 62707)

Inspectors observed and reviewed portions of various licensee corrective

and preventive maintenance activities, and witnessed routine

surveillance testing to determine conformance with plant procedures,

work instructions, industry codes and standards TSs. and regulatory

requirements. The inspectors observed all or portions of the following

maintenance and surveillance activities, as identified by their

associated work order (WO), work authorization (WA) or STP:

Enclosure 2

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e WO# 467103: IB MDAFW pump vibration measurements

e WA# 120178: A train CREFS recirculation filter unit and

pressurization unit visual inspections

e WO# S97002116: 1A PRF System Environmental Qualification (E0)

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e WO#pection

S97002126: 2B PRF System EQ Inspection

e WA# WOO 466705: MCC 1V 600 VAC Breaker Inspections and Cleaning

e Installation of jumpers per FNP-1-SOP-16.1 and Electrical

Maintenance Procedure EMP-1906.01 to override low dilution flow

Steam Generator blowdown isolation

e FNP-1-STP-26.0B: Control Room B Train Ventilation Operability Test .

e FNP-0-ETP-4426 PRF Dirty Filter Data Collection (2A PRF) l

e FNP-0-ETP-3616; Monthly Surveillance Flux Map [ Unit 2] l

e FNP-1-STP-206.2: Post-Accident Containment Water Level 01E11LT l

3594B Loop Calibration i

e FNP-0-ETP-3636: Fuel Assembly Visual Inspection During Core Unload l

[ Unit 1]

b. Observations. Findinas and Conclusions l

All of the maintenance work and surveillance testing observed by the

inspectors was performed IAW work instructions, procedures, and

applicable clearance controls. No adverse findings were identified.

Safety-related maintenance and surveillance testing evolutions were well

planned and executed. Personnel demonstrated familiarity with

administrative and radiological controls. Surveillance tests of safety-

related equi) ment were consistently performed in a deliberate step-by-

step manner Jy personnel in close communication with the MCR. Overall,

operators and technicians appeared knowledgeable, experienced, and well

trained for the tasks they performed.

M1.2 Main Steam Safety Valve lift Testina

On March 11, 12. and 13, 1997, inspectors observed MS safety valve lift

testing and adjustments IAW FNP-1-STP-608.1 " Main Steam Line Safety

Valve Test." Revision 8. and the applicable Furmanite Trevitest

procedure. All lift testing was accomplished by contractors in a well

controlled manner, under the direct constant supervision of plant

maintenance personnel. Activities were well coordinated with the MCR.

M1.3 1C Reactor Coolant Pump Seal Package Inspection and Cleanina

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The inspector observed maintenance activities involving the disassembly,

ins)ection, and cleaning of the 1C Reactor Coolant Pump (RCP) seal

paccage and the reinstallation of the lower seal, including centering

and torquing. This work was performed under WA WOO 467103 using ALA-PMS-

0-120. " Seal Inspection and Replacement." Revision 11. The ins)ector

verified the installation of high temperature 0-rings (Generic _etter

88-20 commitment). Westinghouse personnel were skilled and

knowledgeable.

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M1.4 PRF System Heater Performance Test

On March 5, 1997, the Inspectors observed the performance of FNP-1-STP-

917 " Penetration Room Ventilation System Heater Test." Revision 2. for

the Unit 1A PRF system. This was conducted under WA W00475671. The

required LCO was written and the work was properly authorized. Initial

system conditions were established and the system appeared to operate

adequately. The procedure now requires starting the recirculation fan

first and then the exhaust fan. This prevented HV 3357A from slamming

o)en and shut, which was a recently identified problem in both plants.

T1e plant electricians tested the heaters after Engineering Support (ES)

personnel verified the system was at a full flow of 4887 standard cubic

feet per minute. The electricians identified that phase 'B' power to

the heater was open and an OR was written. The inspector concluded the

procedure was effective in identifying conditions adverse to quality.

M1.5 PRF System Monthly Ooerability Testina

On March 5 and 6, 1997 the inspector observed conduct of FNP-1-STP-20.0,

" Penetration Room Filtration System Train A Quarterly Operability and

Valve In-Service Test," Revision 23. Air Operated Valve 1HV3357A stroke

time exceeded the Stroke Time for Corrective Action but was within the

Maximum Allowable Time. The operator initially timed from when he heard

the air release from the valve to when it repositioned. The SS informed

the operator that the stroke time was to be measured from when valve

movement was first apparent until the valve stopped. The test was

conducted again, but still exceeded the Stroke Time for Corrective

Action. An OR was written by the SS.

On March 6, 1997, the inspector observed STP FNP-2-STP-20.2.

" Penetration Room Filtration System Train A Monthly Operability Test."

Revision 5. The system operated satisfactorily in automatic. However,

when the procedure forced the system into the full recirculation mode,

it did not maintain penetration room vacuum.

Work authorizations and procedures appeared to be properly filled out

and personnel conducting the test were knowledgeable of the test and

plant conditions. The inspector concluded that the tests were conducted

IAW procedures and effectively identified conditions adverse to quality.

!

M7 Quality Assurance in Maintenance Activities i

M7.1 Maintenance Rule Quality Assurance Audit

I

On February 18, 1997, the SAER Maintenance Rule Audit Exit for plant

management was observed. The audit team was experienced and included

expertise from: Maintenance Support - Hatch Project: Project Engineer -

Vogtle Project: Vogtle Senior Engineer; and a Farley Senior Engineer.

The individual from the Hatch Project had recently experienced a NRC

Maintenance Rule Inspection. The team identified several significant

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findings, these included: eight system functions were found classified i

category (a)(1) without performance goals established; some non-safety  !

related systems were not scoped into the program (Heater Drain.

Extraction Steam. and some structures like the Turbine Building): Some

maintenance rule functions were not monitored as required; and, the

method used to assess out of service equipment did not account for the ,

overall effect on performance of safety functions. The team identified l

several other less significant issues. The results were, in general.  !

accepted by the maintenance rule program owners. The inspector 1

concluded that the audit was indepth and comprehensive with regards to I

the Maintenance Rule implementation.

M8 Miscellaneous Maintenance Issues (IP 92902)

M8.1 (Closed) VIO 50-348.364/95-18-05: Failure To Follow Procedures. Multiple

Examples

Corrective action report No. 348/364-95-18-05 was issued to document the

scope of the violation and implementation of corrective actions. By

letter dated December 19, 1995, the licensee responded to the NRC

providing a description of the reasons Gr the violation and proposed

corrective actions. An inspector review a Lhese documents and

determined that in addition to correcting tne immediate consecuences of j

each of the violation examples, the licensee conducted a broacness '

review of other previous procedural compliance problems. This

licensee's review identified the following procedure performance

weaknesses: 1) not performing a procedural step. 2) not signing off each l

l

step as performed. 3) not performing steps in the designated sequence,

and 4) performing actions not in direct compliance with the procedure.

1 To address these generic concerns in order to prevent recurrence, the

licensee requested site supervision and managers to conduct specific

l training on procedural adherence with all groups emphasizing the

aforementioned procedural performance weaknesses and reinforcing i

management expectations. The inspector verified conduct of this

training by reviewing applicable training attendance sheets and

documentation. This vioiation is considered closed. However, it is

evident that the licensee's corrective actions have not been effective

in preventing recurrence of procedural performance weaknesses (see

report section 01.4).

III. Enaineerina

El Conduct of Engineering (IP 37551)

El.1 Unit 1 SFP Fuel Inventorv

On March 18. 1997, inspectors observed ES engineers and an operator

conducting an inventory of fuel in the Unit 1 SFP prior to core unload

IAW FNP-1-ETP-3634. " Fuel Inventory Verification," Revision 9. The

engineers and operator were knowledgeable and followed their procedure.

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The MCR operating crew was aware of their activities. Except for

certain equipment problems with the underwater lighting. and minor

difficulties in orienting the video camera, the evolution went smoothly.

Subsequent discussions with the res)onsible ES supervisor confirmed that

all fuel assemblies to be verified )y ETP-3634 were accounted for.

E4 Engineering Staff Knowledge And Performance

On March 21, 1997, an inspector attended a meeting of all ES department

personnel to discuss recent procedural compliance problems (i.e.. VIO

97-01-01 and the first example in report Section 01.4 above). Each of

the two responsible test engineers discussed their particular incidents

involving a failure to follow procedures, and subsequent lessons

learned. The associated ES supervisors explained their roles in failing

to prevent the specific incidents. At the end of the meeting the ES

manager reiterated the need for procedural compliance, implementing  !

self-verification, and requesting su) port as necessary. The meeting was .

effective in focusing awareness of t1e pitfalls associated with the l

recent problems to the engineering staff.

]

IV. Plant Sucoort '

R2 Status of Radiological Protection Facilities and Equipment

R2.1 Tours of the Unit 1 and 2 Radioloaically Controlled Areas (RCAs)

(IP 71750)

During the course of the inspection aeriod, the inspectors conducted

tours of the Unit 1 and 2 auxiliary auilding RCAs. In general, health

physics (HP) control over the RCA. and the work activities conducted

within it, were good. However, in Unit 1. some contaminated areas were

cramped and physically restricted. Some of these areas lacked step off

pads. Some were so confined that workers had to remove their anti-

contamination clothing outside the roped off contaminated area (e.g. 1B

charging pump). In another instance, clothing had to be removed while

standing on the step off pad (e.g.. RHR pump rooms). These problems did

not result in any contamination events and were discussed with HP

management.

P3 Emergency Plan Procedures and Documentation

P3.1 Emeroency Eauioment and Sucolies Checklist Verification

On February 27.1997 'an EP technician admitted to falsifying many of 4

the EIP-16.0 " Emergency Equi) ment and Supplies," checklists required to i

be accomplished on a routine ) asis. The licensee initiated OR #97-046 to

track the deficiency. The EP coordinator and plant staff promptly

i

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conducted all EIP-16.0 checklists to confirm EP equipment and supplies

in a proper state of readiness. The licensee identified some

discrepancies. The inspectors determined that the discrepancies would

not have impacted the licensee's emergency response capabilities.

S1 Conduct of Security and Safeguards Activities

S1.1 Routine Observations of Plant Security Measures (IP 71750) ,

!

During routine inspection activities, inspectors verified that portions I

of site security program plans were being pro)erly implemented. This l

was evidenced by: proper display of picture Jadges by plant personnel; l

appropriate key carding of vital area doors; adequate stationing / tours 1

of security personnel; proper searching of Jackages/ personnel at the )

primary access point and service water intate structure. Security

activities observed during the inspection period were performed well and

were adequate to ensure physical protection of the plant.

V. Manaaement Meetinos and Other Areas

X1 Review of Updated Final Safety Analysis Report (UFSAR) Commitments

A recent discovery of a licensee o)erating its facility in a manner

contrary to the UFSAR description lighlighted the need for a special

focused review that compares plant practices, procedures and/or

parameters to the UFSAR descriptions. While performing the inspections

discussed in this report, the inspectors reviewed the applicable

portions of the UFSAR that related to the areas inspected. The

inspectors verified that the UFSAR wording was consistent with the

observed plant practices. procedures and/or parameters.

X2 Exit Meeting Summary

The inspectors presented the inspection results to members of licensee

management on A)ril 2,1997, after the end of the inspection period.

The licensee actnowledged the findings presented.

The inspectors asked the licensee whether any materials examined during

the inspection should be considered proprietary. No proprietary

information was identified.

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PARTIAL LIST OF PERSONS CONTACTED

Licensee i

M. Ajluni. SNC (Corporate) Licensing Manager - Farley Project

B. Bell Maintenance Team Leader

R. Coleman Maintenance Manager

S. Fulmer. Technical Manager

D. Grissette. Operations Manager

R. Hili. General Manager - FNP

C. Hillman Security Chief

R. Martin. Superintendent Operations Support

M. Mitchell. Health Physics Superintendent

C. Nesbit. Assistant General Manager - Support

J. Powell Superintendent Unit 2 Operations i

R. Rogers. Engineering Support Supervisor - Engineering Support )

L. Stinson. Assistant General Manager - Plant Operations 1

J. Thomas. Engineering Support Manager l

G. Waymire. Administrative Manager

NRC

J. Zimmerman. Project Manager - Farley Nuclear Plant i

INSPECTION PROCEDURES USED

IP 37551: Onsite Engineering

IP 40500: Effectiveness of Licensee Controls in Identifying. Resolving, and

Preventing Problems

IP 60710: Refueling Activities

IP 61726: Surveillance Observations

IP 62707: Maintenance Observations

IP 71707: Plant Operations  !

IP 71750: Plant Support Activities l

IP 92902: Followup - Maintenance j

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ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

Iypf Item Number Status Descriotion and Reference

VIO 50-348. 364/97-03-01 Open Multiple Examples of Failure To

Follow Procedures (Section 01.4).

NCV 50-364/9/-03-02 Open Misadjusted NIS Power Range Channels

Exceed TS Limiting Safety System

Setpoint (Section 01.5).

Closed

, Tvoe 11.em Number Status Descriotion and Referencg

VIO 50-348, 364/95-18-05 Closed Failure To Follow Procedures.

Multiple Examples (Section M8.1).

NCV 50-364/97-03-02 Closed Misadjusted NIS Power Range Channels

Exceed TS Limiting Safety System

l Setpoint (Section 01.5).

LER 50-364/97-001 Closed Nuclear Instrumentation System

Inaccuracies Below 50% Power ,

(Section 01.5).

"

LIST OF ACRONYMS USED

AP Administrative Procedure

CFR Code of Federal Regulations

.

'

CREFS Control Room Emergency Filtration System

CST Condensate Storage Tank

EDG Emergency Diesel Generator

EIP Emergency Plan Implementing Procedure

i EP Emergency Plan

EQ Environmental Qualification

ES Engineering Support

ETP Engineering Test Procedure

FNP Farley Nuclear Plant

HP Health Physics

HX Heat Exchanger

I&C Instrumentation and Control

IAW In Accordance With

IP Inspection Procedure

IR Inspection Report

LCO Limiting Condition of Operation

LER Licensee Event Report

MCB Main Control Board

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MCC Motor Control Center

MCR Main Control Room

'

MDAFW Motor Driven Auxiliary Feedwater

MOV Motor Operated Valve

MS Main Steam

NCV Non-Cited Violation

NI Nuclear Instrumentation

'

NIS Nuclear Instrumentation System

NORB Nuclear Operations Review Board

NOV Notice Of Violation

!

NRC U.S. Nuclear Regulatory Commission

OR Occurrence Report
i PDR Public Document Room

PM Preventative Maintenance

PPR Piping Penetration Room

PR Power Range

PRF Penetration Room Filtration

<

RCA Radiologically Controlled Area

RCP Reactor Coolant Pump

RCS Reactor Coolant System

RHR Residual Heat Removal

SAER Safety Audit and Engineering Review

SFP Spent Fuel Pool

SNC Southern Nuclear Company

S0P Standard Operating Procedure

SR Source Range

SS Shift Supervisor

STP Surveillance Test Procedure

TO Tag Order

TS Technical S]ecifications

U1RF13 Unit 1. 13t1 Refueling Outage

U1RF14 Unit 1. 14th Refueling Outage

U2RF11 Unit 2. 11th Refueling Outage

UFSAR Updated Final Safety Analysis Report

UOP Unit Operating Procedure

VAC Volt Alternating Current

VIO Violation

WA Work Authorization

WO Work Order

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