ML20133F692

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Insp Repts 50-348/96-13 & 50-364/96-13 on 961013-1123. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support
ML20133F692
Person / Time
Site: Farley  Southern Nuclear icon.png
Issue date: 12/23/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20133F684 List:
References
50-348-96-13, 50-364-96-13, NUDOCS 9701140327
Download: ML20133F692 (52)


See also: IR 05000348/1996013

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l U.S. NUCLEAR REGULATORY COMMISSION (NRC)

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REGION II

l- Docket Nos: 50-348 and 50-364

( License Nos: NPF-2 and NPF-8

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Report No: 50-348/96-13 and 50-364/96-13

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Licensee: Southern Nuclear Operating Company (SNC). Inc.

Facility: Farley Nuclear Plant (FNP) Units 1 and 2

. Location: 7388 North State Highway 95

! Columbia. AL 36319

l Dates: October 13 - November 23, 1996

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Inspectors: T. Ross. Senior Resident Inspector

i J. Bartley, Resident Inspector

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J. Blake Reactor Inspector (Sections M1.2 and

M1.3)

M. Ernstes. Operator Licensing Examiner

(Sections 02.2 and 02.3)

E. Girard. Reactor Inspector (Section E8)

G. Kuzo. Senior Radiation Specialist (Sections

R1.1 R1.2. R2.2. R3. R6. and R7)

N. Merriweather. Reactor Inspector (Section

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El.1)

W. Miller. Reactor Inspector (Sections F2 F3.

FS. F6 F7. and F8)

Approved by: P. Skinner. Chief. Projects Branch 2

Division of Reactor Projects

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! Enclosure 2

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9701140327 961223

PDR ADOCK 05000348

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EXECUTIVE SUMMARY

, Farley Nuclear Power Plant. Units 1 And 2

l NRC Inspection Report 50-348/96-13, 50-364/96-13

This integrated inspection included aspects of licensee operations,

engineering maintenance, and plant support. The report covers a 6-week

period of resident and regional inspections.

I Ocerations

e Operations performed well in controlling plant conditions during Unit I

steady state full power operation and Unit 2 shutdown. The conduct of

l Operations personnel and management was consistently in compliance with

j procedures ar.d regulatory requirements (Section 01).

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e Shift operators remained very attentive to plant conditions, and were

quite knowledgeable of plant status and ongoing activities. However,

the shift superintendent needs to consistently ensure that distracting

activities in main control room (MCR) are kept to a minimum (Section

l 01.1).

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i e The defueling and refueling of Unit 2 was accomplished in a )rofessional

i and competent manner: although, there was a considerable num)er of minor

i instances where foreign objects were found in P.he reactor cavity and-

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spent fuel pool (SFP) (Section 01.2).

e Operators responded well to a Unit 2 solid plant pressure transient

(Section 01.4).

l e Overall housekeeping and abysical conditions were generally just

adequate. However, houseceeping in the Unit 2 radiologically controlled

area (RCA) (especially the piping penetration rooms, decontamination

room, and new fuel storage area) was considerably improved over previous

outages (Section 02.1).

e Safety system walkdowns verified selected systems were properly aligned

and capable of fulfilling their design function (Sections 02.2 and

02.3).

e An unresolved item was identified concerning the interpretation of

technical specification (TS) requirements for penetration room

filtration (PRF) system operability requirements (Section 02.6).

j e Licensee efforts to identify. resolve, and prevent problems remained

effective (Section 07.1).

e Conduct of Nuclear Operations Review Board met TS requirements and

appeared thorough (Section 07.2).

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Enclosure 2

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Maintenance

e Maintenance and surveillance testing activities were routinely conducted

in a thorough and competent manner by well qualified individuals in  ;

accordance with plant procedures and work instructions (Section M1.1).

e Unit 2 service water system code boundary valve replacement activities

appeared to be conducted in a manner consistent with the licensee's  ;

quality programs. and reflected the licensee's understanding of the

relative risk importance of this system (Section M1.2).

e The original scope of steam generator (SG) inspections, and subsequent

expanded scope, demonstrated the licensee's apparently conservative

approach to determining the structural integrity of the Unit 2 SGs

(Section M1.3).

e Several major maintenance, modification, testing, and inspection

activities were well planned and implemented during the Unit 2 refueling

outage (Section M1.4. 5. 6, 8. and 11).

e A poor maintenance work practice resulted in the entry of foreign

material into the Unit 2 reactor coolant pump seal injection system

(Section M1.10).

Enaineerina

e Design change packages and plant modifications were developed and

accom)lished in an acceptable manner (Section El.1 and 2). Engineering

and t1e maintenance craft interfaced well during modification work

(Section El.1 and applicable M1 sections).

e An unresolved item was identified regarding a design issue associated

with the Unit 1 and 2 SG common tap for steam flow and water level not

meeting IEEE-279 (Section E1.3).

e The Unit 2 control rod test and evaluation program pursuant to NRC

Bulletin 96-01 was comprehensive and satisfactorily verified control rod

operability (Section E1.4)

e The remaining open commitments for Generic Letter 89-10 were completed

satisfactorily (Section E8).

Plant Suocort

e In general, radiation work permit (RWP) guidance was adequate for

routine RCA and the Unit 2 eleventh refueling outage (U2RF11)

activities. Except for one individual, all personal exposures were less

than administrative limits and were within 10 CFR Part 20 limits. A

Enclosure 2

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violation was identified for two examples of inadequate implementation

of RWP dressout requirements (Section R1.1).

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o The "As Low As Reasonably Achievable" program guidance and

implementation were acceptable, with no negative trends identified

(Section R1.2).  ;

e Health Physics (HP) control over the RCA. and the work activities

conducted within it, were good. Material condition and housekeeping in  !

the Unit 2 RCA. considering ongoing outage activities, were much better

than in the past (Section R2.1).

e No significant concerns were identified regarding radiation monitoring

system (RMS) operability or supplied breathing air equipment (Section

R2.2).

e Abnormal effluent releases have increased (Section R3).

e The HP organization and staffing provided ap3ropriate radiation

protection coverage of routine and outage jo) evolutions (Section R6).

e Proposed audits of refueling outage radiation protection activities were

adequate: the planned use of outside auditors to assist was considered a

program enhancement (Section R7).

  • Security activities continued to be performed in a conscientious and

capable manner assuring the physical protection of protected and vital

areas (Section S1.1).

e A violation was identified for failing to search a vehicle prior to  ;

entering the protected area (Section S8.1),

o The number of outstanding fire protection system work requests was high.

Corrective maintenance on degraded fire protection systems was being  !

accomplished in a timely manner. Corrective actions have been effective  :

in improving fire pump reliability. However, the root cause analyses of

frequent automatic pre-action sprinkler system failures has not been

effective. A program weakness was identified in that these sprinkler

systems were not being maintained in their normal design configuration.

Daily fire protection status reports were considered a positive means of

identifying degraded fire protection systems and implementing the

appropriate compensatory measures (Section F2.1).

  • Surveillance tests of fire protection systems and features met the

requirements of the Updated Final Safety Analysis Report (UFSAR) or

evaluations had been provided to justify the deviations (Section F2.2).

e Fire protection program implementing procedures met the intent of the

NRC guidelines and requirements. Procedure implementation and general

Enclosure 2

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housekeeping related to the control of combustibles within the plant

were satisfactory (Section F3).

e Fire brigade organization and training met the facility's procedure

requirements and performance of the fire brigade during a drill was good

(Section F5).

e Coordination and oversight of the facility's fire protection program met

UFSAR commitments. Responsible personnel worked together as a team,

along with coordination by the Fire Marshall, to implement the site fire

protection program (Section F6).

e Audits and assessments of the fire protection program were thorough with

corrective actions taken on major discrepancies in a timely manner. l

However, resolution on recommendations and comments to enhance the fire

protection program were not timely (Section F7).

e Evaluations of fire protection related Information Notices (IN) were

appropriate and the recuired corrective actions had been completed. l

except for IN 93-41 anc IN 95-36 (Section F8).

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Enclosure 2

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Reoort Details

Summary of Plant Status

Unit 1 oaerated continuously at 100% power for the entire inspection period.

On Novem)er 22 the unit achieved 200 days of continuous operation.

' Unit 2 remained shutdown for its eleventh refueling outage during the entire

inspection period. The original 48 day refueling outage was extended to 64

days due to unexpected increase in repair scope of SG U-tubes. On October 23.

the reactor core was defueled, and on November 21. the reactor core was

reloaded. Restart was scheduled for December 14, 1996.

I. Operations

01 Conduct of Operations

01.1 Routine Observations of Control Room Goerations

a. Insoection Scooe (Insoection Procedure (IP) 71707)

Resident inspectors and a regional inspector (during the week of

November 4 - 8. 1996) conducted frequent inspections of ongoing plant

operations in the MCR to verify proper staffing, operator attentiveness.

adherence to approved operating procedures, communications, and command

and control of operator activities. The inspectors also regularly

reviewed o)erator logs and TS Limiting Condition of Operation (LCO)

tracking sleets, walked down the MCBs. and interviewed members of the

operating shift crew to verify operational safety and compliance with

TS. The inspectors attended daily plant status meetings to maintain

awareness of overall facility operations, maintenance activities, and

recent incidents. Morning reports and Occurrence Reports (OR) were

reviewed on a routine basis to assure that potential safety concerns

were properly reported and resolved.

b. Observations. Findinas and Conclusions

Overall control and awareness of plant conditions during the inspection

period were excellent. During tours of the MCR. the inspectors observed

that the Unit 1 MCBs were frequently in a " blackboard" condition.

Whereas. the EPB had one persistent annunciator alarm and Unit 2 outage

conditions resulted in numerous annunciator alarms. Aggressive efforts

to reduce MCB deficiencies to very low levels were effective. The

combined number of MCB deficiencies have been reduced to less than half

the number that was existing earlier this year.

Operator attentiveness and response to plant conditions was generally

very good; however, on occasion certain distractions were observed.

Although access to the MCR was regulated for 0)erations business only,

some crews allowed personnel not assigned to t1e MCR to linger and

discuss non-work related issues for up to 10 minutes. At times both

reactor operators for Unit 1, which was at 100% power, had their backs

Enclosure 2

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to the MCB. engaged in non-work related conversation with the Shift '

Supervisor (SS) and personnel not assigned to the MCR. Interviews with

the operators indicated that they were aware of plant conditions and the

status of on-going activities. Even though no adverse consequences

resulted from these few lapses in attentiveness. this practice may not l

be conducive to maintaining the record of exemplary operator response to '

slowly developing transients documented in previous reports during this

cycle.

01.2 Unit 2 Defuelina and Refuelina Ooerations

a. Insoection Scooe (IP 60710)

Resident inspectors observed defueling activities on October 22. during-

the. day and night shifts. The ins)ectors also observed refueling

o)erations during the aeriod Novem)er 19 through 21. Activities were

03 served in the MCR S P. and containment.

b. Observations and Findinas

All defueling and refueling activities observed by the resident

inspectors were performed in a well controlled and methodical manner in

accordance with (IAW) FNP-2-UOP-4.1. Controlling Procedure For

Refueling..and FP-APR-R11. Westinghouse Refueling Manual. The  !

inspectors observed the refueling pre-job brief on November 15. 1996.

The brief was thorough and covered the necessary information and

)rocedural requirements. No significant incidents occurred during fuel

landling and all fuel assemblies were landed in their appropriate

locations. However, the licensee and an inspector identified a.

considerable number of minor instances of foreign materials entering the

Unit 2 SFP and reactor cavity: SFP - key card, electrical pigtail,

strips of adhesive tape and clear plastic, and a tie wrap: Reactor

Cavity - small rubber bulb hammer, and a three inch diameter aluminum

disk. The ins)ector discussed the numerous foreign material intrusion

aroblems with :NP management. Although all such materials appear to

1 ave been located'and removed, responsible management was evaluating the

adequacy of foreign material controls .

c. Conclusion

The inspectors concluded that fuel handling was accomplished in a

professional and competent manner. Although no significant incidents

occurred, there were some foreign objects found in the SFP and reactor

cavity.

Enclosure 2

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01.3 Unit 2 Cooldown for U2RF11 (IP 71707)

On October 14 and 15. a resident inspector observed the cooldown and

sol'.d plant operation of Unit 2 IAW FNP-2-U0P-2.2. Shutdown Of Unit From

Hot Standby To Cold Shutdown. Cooldown was accomplished in a controlled

and purposeful manner. But, shortly after reactor coolant system (RCS) i

temperature was decreased below 200 degrees Fahrenheit, the licensee ,

delayed further cooldown in order to conduct a seat leak test of the'

residual heat removal (RHR) loop suction valves IAW FNP-2-STP-158, RCS

Pressure Isolation Valve Leak Test. Although this test was previously

planned and evaluated for risk significant consequences, it did require

plant conditions (i.e., isolation of RHR system) contrary to TS 3.4.10.3

for low temperature overpressure protection and certain precaution

statements of U0P-2.2. Also, at this point of U2RF11 reactor core

decay heat was very high. The operating crew did an excellent job

establishing and maintaining unit conditions to support the seat leak ,

tests. Ap3ropriate TS LCOs were entered and tracked. However, the '

ins)ector Jecame concerned that neither UDP-2.2 or STP-158 provided

muc1, if any, guidance to the o)erators on the necessary plant i

conditions and how to control t1em effectively. The resident inspector  !

discussed the lack of guidance with Operations management.

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01.4 Solid Plant Pressure Transient - Unit 2 (IP 71707)

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On October 15. 1996, operators responded to an overpressure and loss of i

RCS inventory transient. The event was apparently caused by a charging

flow' perturbation when charging flow control valve (FCV) 122 went shut.

An o)erator was very prompt in observing the decrease in charging flow

and ] umped open FCV-122. However, charging flow jumped to a) proximately

100 gpm. Thi.s increase in charging flow. in combination wit 1 the

automatically reduced letdown flow, caused RCS 3ressure to spike and '

lift RHR relief valve 02E11V0015A ("A" train) w11ch failed to reseat.

This event resulted in approximately 3000 gallons of RCS fluid being

discharged to the pressurizer relief tank and required securing the

reactor coolant pumps (RCP) due to low RCS pressure. The licensee

conservatively secured all high voltage and low voltage switchyard work

while the 2A RHR train was out of service to repair V0015A (2B emergency

diesel generator (EDG) was tagged out for 18 month outage) and all

penetration work.

The inspectors observed the licensee's recovery actions which included

stabilizing the plant and removal and bench testing of 02E11V0015A. The

inspectors concluded: 1) the operating crew performed well in

identifying the condition and stabilizing the plant: 2) the licensee

staff maintained good control and took conservative actions; and 3) the

investigation into the cause of the event was thorough.

Enclosure 2

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! 01.5 Larae Service Water Soill In Unit 2 Containment (IP 71707)

On November 15. during return to service of Unit 2 containment coolers.

Operations failed to 3revent a 7000 gallon spill of service water (SW)

into containment on t1e 155 foot elevation. The spill eventually *

flooded the containment basement level (105 foot elevation) to about six

inches deep. Subsequent investigation by the licensee, as documented in

occurence report (OR) 2-96-351. determined that Operations had directed

contract pipefitters to loosen SW flanges to the A & B containment

coolers on October 25. The loosened flanges were needed as vent paths

to expedite draining both coolers. However. Operations failed to

control the physical status of these containment coolers via tagorder or

other a)plicable documentation. Consequently, when the time came to

refill )oth coolers, the operating crew was unaware of the loosened

flanges prior to reintroducing SW to the containment coolers. But even

with inadequate configuration control. Operations missed an opportunity

to identify the situation or minimize the spill by not walking down the

coolers prior to refill or monitoring the refill operation in

containment. Nobody was contaminated and no' plant equipment was damaged

during the spill although SG work on 105 foot level was halted until

cleanup was completed. Work on the lower level was recorrmenced the next

day.

02 Operational Status of Facilities and Equipment

02.1 General Tours of Soecific Safety-related Areas (IP 71707)

General tours of FNP specific safety-related areas were performed by the

resident inspectors to examine the physical conditions of plant

equipment and structures, and to verify that safety systems appeared

properly aligned. Limited walkdowns of a more detailed nature of the

accessible portions of safety-related structures, systems and components

were also performed in the following specific areas:

e Unit 1 and 2 SFP and SFP cooling systems

e Unit 2 containment

<e Unit 2 turbine-driven auxiliary feedwater (TDAFW) pump rooms

e Unit 2 motor-driven auxiliary feedwater pump rooms

e Unit 1 and 2 component cooling water (CCW) pump and heat exchanger

(HX) ronms

e Unit 1 and 2 hot shutdown panels

e Unit 1 and 2 vital 4160 volt alternating current switchgear rooms,

trains A and B

e Unit 1 and 2 aiping penetration room (PPR) on 100 foot elevation

e Unit 1 and 2 JPR on 121 foot elevation

e Unit 1 and 2 vital 125 volt direct current switchgear and battery

charger rooms, trains A and B

e Unit 1 penetration room filtration system (PRF)

e Unit 1 primary sample room and radiochemistry lab

o Unit 1 and 2 RHR HX rooms

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Enclosure 2

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e Unit 2 RHR pump rooms

e Unit 2 containment spray pump rooms

e Unit 2 main steam (MS) valve room

Service water intake structure (SWIS), including SW system pumps

and switchgear

e Unit 1 and 2 turbine building

e Unit 2 charging pump rooms

e Unit 1 and 2 boric acid pump and mixing tank rooms

Overall material conditions and housekeeping for both units were

generally adequate. Minor equipment condition and housekeeping problems

identified by the inspectors were reported to the responsible SS and/or

maintenance department for resolution. The physical appearance of the

floor level in Unit 1 and 2 PPRs at the 121 foot elevation, and Unit 1

PPR at the 100 foot elevation, continue to look well worn with some

random debris and discarded tools / material. Unit 1 was beginning to

show the effects of less attention due to Unit 2 outage. However the

inspectors noticed that Unit 2 housekeeping in the PPRs looked much

better than during past outages. This was a remarkable achievement when

considering the SW system William Powell gate valve replacements being

accomplished in the 121 foot PPR elevation. Management attention to

this area was very evident. Also, the accumulation of outage solid

radioactive waste (radwaste) in the decontamination room and 155 foot

elevation RCA spaces and hallways (especially the new fuel storage area)

was considerably improved over previous outages.

02.2 Biweekly Insoections of Safety Systems (IP 71707)

A regional inspector used IP 71707 to verify the operability of the

following selected safety system.s:

e Unit 1 CCW

e Unit 1 and 2 SFP cooling

The inspector used portions of FNP-1-SOP-23.0A. Com)onent Cooling Water

System. Revision 3. and walked down all the accessi]le valves and

components of both trains of the Unit 1 CCW system. The inspector did

not identify any immediate, safety significant problems that could

adversely affect CCW system operability.

The inspector walked down accessible valves and components for both

trains of the Unit 1 and Unit 2 SFP cooling system. The inspector did

not identify any immediate, safety significant problems that cou'd

adversely affect SFP cooling system operability. The inspector iound

that overall material conditions of equi) ment was adequate. Some minor

housekeeping, material condition, and la)eling discrepancies were

discussed with the licensee for correction. Examples of these

discrepancies were:

Enclosure 2

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The inspector found the position indicator for valve 01G31V007.

" Demineralized Water to SFP Isolation." lying on the floor beneath

the valve.

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The casing vent for the 2A SFP pump was leaking excessively

, despite the isolation valve being closed and the line capped.

l There was a collection bag under the line, and the area

l immediately around the pump was designated as a contamination

area. However, the bag was full and leaking on the pump housing.

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The hand wheel on the skimmer pump casing drain valve. 02G31V039,

appeared to have been stepped on. bending the valve stem.

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An unauthorized operator aid was noted above the Unit 2 SFP to

refueling water storage tank (RWST) isolation valve 02G31V021B.

"Open 1 1/2 turns for 100 gpm" was written in pencil on the wall.

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The sample line below Unit 1 SFP cooling sample valve.-01G31V011A

was plugged with a boron buildup.

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An inactive red hold tag was found on the SFP purification outlet

j to refueling cavity (N1031V021A). (See paragraph 02.5)

! 02.3 Enaineered Safeauards Feature System Walkdown

l a. Insoection Scoce (IP 71707)

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The ins]ector performed a detailed walkdown of the accessible portions

of the Jnit 1 and Unit 2 hydrogen recombiners and the Unit 1 and Unit 2

post accident hydrogen analyzers (PAHA). The inspector also used

portions of FNP-1-EEP-1. Loss of Reactor or Secondary Coolant. Revision

15, in order to walkdown the equipment as it would be used in an

accident situation.

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l b. Observations. Findinas and Conclusions

l The inspector found that overall material conditions of equipment was

l adequate with the exception of a concern with the 2A hydrogen

recombiner. A conduit leading to the 2A hydrogen recombiner had pulled

away from the connector exposing the wires within. This could affect

the operability of the recombiners if the wires were exposed to post-

loss of coolant accident atmospheric conditions. Some minor

housekeeping, material condition, and labeling discrepancies were

discussed with the licensee for correction. Examples of these

discrepancies were:

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pencil labels on the Unit 2 PAHAs.

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no warning signs on the Unit 1 hydrogen sample lines to alert

personnel to the exposed heat tracing as on Unit 2.

! Enclosure 2

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Other than the broken conduit, none of these discrepancies were

significant enough to adversely affect the operability or operation of  ;

j hydrogen recombiners and PAHA equipment.

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02.4 Containment Tours - Unit 2 (IP 71707)

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l Resident inspectors toured Unit 2 containment on several occasions

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during the outage. The initial tour. conducted two days after the unit

l shutdown, only identified one oil spot from a snubber leak. No RCS or

l other fluid system leaks were identified. However, the inspectors were

l concerned about trash and loose tools / equipment which was already

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accumulating in containment. This concern was discussed with plant

management at the exit meeting for Inspection Report (IR) 50-348.

364/96-09.

02.5 Tao Orders (IP 71707)

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During the course of routine resident inspections, portions of the

following tag-orders (TO) and associated equipment clearance tags were

examined by the inspectors:

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e TO# 96-1911-2: 2B CCW HX

e TO# 96-1971-1: 1B CCW HX

l' e TO# 94-0791: SFP purification

e TO# 96-2911-2: 2B RHR pump

l All tags and T0s examined by the inspectors were properly executed and

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implemented, with certain exceptions. During the walkdown of valves

! associated with Unit 1 SFP cooling a red hold tag associated with TO

l #94-0791 was observed on SFP purification outlet to refueling cavity

isolation valve (N1G31V021A). Review of the Unit 1 TO log revealed that

l this T0 was no longer active. The tag had been initialed as cleared on

l March 20, 1994. Due to the large amount of time since the T0 had been

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cleared, it could not be determined if the tagging official had ensured

all tags had been removed. i

After determining that the tag was hanging in error, the operating crew

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removed the tag from the valve handwheel. The valve was in its required

position. OR 1-96-338 adequately addressed this issue. The inspector

verified that none of the other tags associated with this T0 were still

hanging.

Also during the ins)ection period two ors (2-96-308 and 2-96-375) were

written regarding t1e loss of control over a 2B SG manhole cover hold

tag and a nitrogen hose hold tag and caution tag on tygon hose running

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through penetration 90. Licensee and contractor investigations were in

! progress.

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Enclosure 2

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l 02.6 Technical Soecifications Comoliance (IP 71707)

A resident inspector, while performing MCR observation on November 19.

1996. overheard operators discussing a possible TS compliance issue

I which occurred on October 30, 1996. The inspector discussed the issue

with the operators and reviewed the Unit 2 MCR log entries for October

E 30.

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I On October 30. the licensee was moving fuel in the SFP. The 2A startup

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transformer (normal power supply to the "A" train safety busses) and the

4 1-2A EDG (emergency power supply for "A" train safety busses) were out  !

of service (00S) for outage work. At approximately 10:22 am, the '

i licensee commenced performance of FNP-2-STP-20.2. Penetration Room

j Filtration System Train A (B) Monthly Operability Test, on "B" train.

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The lineup for this surveillance test procedure (STP) required isolating

the "B" train PRF system suction from the SFP. AT this time, the "A"

i train PRF was running on its alternate power supply (i.e. 2B startup

i transformer). The night shift operators reviewed TS 3.9.13 and 3.7.8,

and at 7:59 pm decided that they did not meet the TS requirements to

1 move loads over the SFP. The operators informed the SS at 8:20 pm. The

movement of loads over the SFP was terminated and Operations management

I was notified. The Operations manager reviewed the situation and

concluded TS requirements were met. The handling of loads over the SFP

, was recommenced at 9
23 pm.

! The inspectors independently reviewed TS 3.9.13 and 3.7.8 and determined i

j that train A PRF was inoperable from October 29 through November 2 while

the "A" train normal and emergency power supplies were 00S.

. Furthermore, on October 30. the "B" train PRF to the SFP was rendered

l inoperable by shutting the "B" train PRF suction to perform STP-20.2.

i The inspectors met with plant management to discuss the issue, and

i participated in various conference calls with the SNC corporate office.

i After considerable discussion licensee management continued to disagree

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with the inspector's and operating crew's interpretation of TS

requirements. To resolve this issue, the licensee subsequently

i documented their position in a letter to the NRC dated November 27

1 1996. requesting a formal TS interpretation. Until the NRC responds to

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the SNC letter, this issue is identified as Unresolved Item (URI) 50-

364/96-13-01. PRF Operability Requirements for SFP.

. 07 Quality Assurance in Operations 4

07.1 Effectiveness of Licensee Control in IdentifYina. Resolvina. and

Preventina Problems (IP 71707 and 40500).

The resident inspectors scanned all ors initiated, and approved by the

operations manager during the inspection period to ensure that plant

incidents that effect or could potentially effect safety were properly

documented and processed IAW FNP-0-AP-30. " Preparation and Processing of

Enclosure 2

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Incident Reports Certain selected ors were reviewed in detail as

part of the routine inspection program.

Overall, the inspectors concluded the licensee's program for identifying

and resolving problems rtmained effective, and was being accomplished l

IAW AP-30. Plant personnel and management exhibited an appropriate '

threshold for identifying problems, initiating ors. and assigning formal '

root cause teams. Each new OR received prompt attention and was l

regularly discussed by management in the morning status / plan of the day

meeting. Direct derivations and formal root cause analyses continued to I

be conducted by experienced plant staff in a rigorous and thorough

manner. The results of these efforts were almost always effective at

preventing recurrent problems.

The following ors were reviewed and corrective actions were verified:

o 2-96-301. MOV 3318A found open

e 2-96-346, 2A RHR motor wouldn't rotate while bumping for rotations l

(refer to paragraph M1.6 for more details) l

e 2-96-309. Wiring discrepancies during solid state protection

system walkdown

07.2 Nuclear Ooerations Review Board (NORB)(IP 40500)

TS 6.5.2 defines the function. composition. responsibilities, and

authority of NORB. A resident inspector monitored the NORB conducted on

November 15. 1996. The inspector observed good discussions on problem i

areas. The inspector also verified that the NORB met TS requirements

for members.

08 Miscellaneous Operations Issues (IP 92901) .

l

08.1 (Closed) Licensee Event Report (LER) 348/95-10 Actuation of Engineered

Safety Feature Equipment Due to Loss of Main Feedwater i

This event was discussed in IR 50-348. 364/95-19. No new issues were

revealed by the LER.

JI. Maintenance

M1 Conduct of Maintenance ,

,

M1.1 General Comments

,

Inspectors observed and reviewed portions of various licensee corrective

and preventative maintenance activities, and witnessed routine

surveillance testing. to determine conformance with plant procedures. l

work instructions, industry codes and standards. TS and regulatory

requirements.

Enclosure 2

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, a. Insoection Scooe (IP 61726. 62703 and 62707)

} The resident inspectors and a regional inspector observed all or

i portions of the following maintenance and surveillance activities, as

identified by their associated work order (WO). work authorization (WA).

or STP:

'

e FNP-1-STP-23.1: 1A CCW Pump Quarterly Inservice Test (IST)

e FNP-0-STP-80.17: Diesel Generator 2C Operability Test

e- FNP-2-STP-40.3: Phase A Isolation-Test

e FNP-2-STP-627: Local Leak Rate Test of Containment Penetrations

e WA# 120102: Unit 2 Fuel 0xide Measurement

e FNP-2-STP-40.1: B2F Sequencer Operability Test and B2F B2H

Sequencer Load Shedding Circuit Test

e FNP-2-ETP-4411: 28 Residual Heat Removal / Low Head Safety

Injection Pump Curve Development Test

e FNP-2-STP-228.1: Nuclear Instrumentation System Source Range N31

Calibration and Functional Test

e WO# M96004427: 2A Charging Pump Seal Repair

e FNP-2-STP-40.7: Emergency Core Cooling System Branch Line Flow

Test

e WO#00079621: Relug 2B RHR Pump

b. Observations. Findinas and Conclusions

All of the aforementioned maintenance work and surveillance testing

observed by the inspectors were performed IAW work instructions,

procedures, and applicable clearance controls. No adverse findings were

identified. Safety-related maintenance and surveillance testing

evolutions were well planned and executed. Responsible personnel

demonstrated familiarity with administrative and radiological controls.

Surveillance tests of safety-related equipment were consistently

performed in a deliberate step-by-step manner by personnel in close

communication with the MCR. Overall, craftsmen and technicians appeared

knowledgeable, experienced, and well trained for the tasks they

performed.

In addition, see the discussions below regarding certain major

maintenance and testing activities observed by the resident inspectors

and a Region II inspector (Sections M1.2 through M1.11).

M1.2 Service Water Valve Reolacement. Unit 2 (IP 73753)

a. Insoection Scooe

The inspector reviewed SW System valve replacement activities through

inspection of materials: review of procedures and drawings; observation

of work activities; and discussions with craft and engineering

Jersonnel. The activities were inspected for compliance with the Farley

JFSAR and licensee quality requirements. This area of maintenance work

Enclosure 2

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was selected for observation because of the relative importance of the

SW system in the licensee's IPE.

b. Observations and Findinos

The licensee was in the process of replacing carbon steel gate valves

l with stainless steel butterfly valves as the code boundary valves  ;

between the American Society of Mechanical Engineers Class 2 and Class 3 l

portions of the SW system. The change was being made due to corrosion

problems with the carbon steel gate valves. At the time of the

inspection, the valves had been replaced in the train A portions of the

l SW system, and work was in progress for the train B valve replacement.

l In train B, the gate valves had been removed and the piping was being

! prepared for installation of piping and flanges necessary for the

l. installation of the butterfly valves.

i Along with a licensee materials engineer, the inspector conducted an

! inspection of the condition of inside surfaces of piping in the vicinity

, of the valve replacement locations. The piping contained an oxidized

I

coating, several millimeters in thickness, that obscured the inside

surface of the alping. The materials engineer was able to easily remove

! the coating wit 1 a putty knife so that various locations of the inside

surface could be examined.

, The piping inside surfaces were found to contain some small pitting )

l indications, but in general the piping did not appear to have suffered l

'

appreciable wall loss due to corrosion. The ends of the piping which '

had been machined in place, in preparation for welding, were examined to

l' assess the relative depth of the pitting. On the surfaces examined, the

pits appeared to be only a few millimeters in depth, and therefore I

within the corrosion allowance for this piping wall thickness.

During discussions with craft personnel, the inspector was informed that

.

the piping sections examined by the inspector were representative of the .

l piping. conditions noted during the entire modification project. Several l

. of the craft personnel noted that they had ex)ected to find the piping

l in poor condition, and had been impressed wit 1 it's relatively good

l condition, and how easily the pipe ends cleaned up for weld preparation.

The inspector did witness the_ liquid penetrant examination of a weld l

repair in the Class 2 weld preparation for a 6-inch valve (02P16V044BL  ;

The area being repaired was due to removal of a linear indication, '

resulting in a 2.5-inch by 7/8-inch area being ground in the end of the

pipe.

The inspector reviewed two work packages representative of the work

being done: one package for a 12-inch diameter valve and the other for a

6-inch diameter valve. The inspector noted that the work packages were

i set up in a " traveler" format with individual work sheets for each of

the different welding operations required for each valve replacement.

l The work packages appeared to be very complex, but after discussing the

,

Enclosure 2

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jobs with the craft personnel on the scene, it was apparent that they

understood the process and how the job was to be documented.

c. Conclusions

t

l The SW code boundary valve replacement activities appeared to be

'

conducted in a manner consistent with the licensee's quality programs.

The fact that the licensee had a materials engineer assigned to oversee

these replacement activities, along with other work on the SW system.

I was a positive indication that the licensee understood the relative IPE

l

importance of the system.

M1.3 SG Inservice Insoection (ISI). Unit 2 (IP 73753)

a. Insoection Scooe '

The inspector reviewed ISI inspection activities involving the Unit 2 SG

tubing. The review consisted of discussions with licensee and

contractor personnel
review of eddy current and ultrasonic test

! results: and an independent review of a portion of the eddy current,

l bobbin inspection, test data from the "C" SG.

i

l b. Observations and Findinas

l

l Farley 2 is a Westinghouse 3-loop unit with series 51 SGs. Each SG

contains 3388 U-bend tubes made of Inconel 600. The nominal tube

outside diameter is 0.875 inch with a nominal wall thickness of 0.050

inch: the tubes were expanded into the tubesheet using a mechanical

hardroll. process. Unit 2 reached initial criticality in May 1981, and

this outage is the eleventh (11th) refueling outage.

During this refueling outage, the licensee's eddy current plans included

a 100% bobbin coil inspection of all tubes in each SG from the cold leg

side concurrent with a 100% rotating coil inspection of the hot leg tube

sheet. These basic inspections were to be followed by rotating coil

inspections of bobbin coil indications, particularly at hot-leg support

plate intersections and in free spans. The licensee was using the plus-

point probe for the rotating coil inspection for the first time.

As a result of the planned inspections, a significant number of new

indications were detected. Because of these new indications, the

licensee initiated a special program to establish structural integrity

of the "A" SG: this program would then be followed by special programs

on the "B" and "C" SGs. There were five types of inspection findings
that were determined to be " Free Span Structural Integrity Issues" which

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were the focus of the continuing inspection activity in the "A" SG.

These findings are as follows:

Inside Diameter (ID) >180 at or above the Bottom of Roll

. Circ crack: Transition (BRT)

,

j Outside Diameter  :

t Circ crack: >180 at or above the BRT i

3

. Axial cracks: Crack length of >0.4 inches. above the BRT.

!- Axial & Circ Mixed: If no " null" between circ and axial, Indication

! at or above BRT.

!

Free span above roll transition: Plus point indication >2 volts

i In addition to these tubes. 20 Single Axial Indications and Multiple

i Axial Indications with axial crack length >0.3 inches, above the BRT

i were included in the continuing inspections.

There was a total number of 59 tubes included in the additional

inspection activities. The inspection activities included: a repeat of

>

the plus-point-inspection using a slower speed in order to generate more

data points, and ultrasonic examination (UTEC) of all ID cracks in the  ;

. sample (52 of the 59 tubes had ID cracks). 1

4 l

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j The data from the additional plus-point and UTECs were currently.being

1 analyzed to select the appro riate sample tubes for in-situ pressure

i testing and also for tube pu ls

!

l At the time of this inspection, in the "B" SG. fifteen (15) tubes had

i been selected for " slow" plus-)oint and UTEC. UTEC equipment was being

L installed in the "B" SG. In tie "C" SG data analysis from the original

j bobbin and plus-point examinations had just been completed.

! One finding of note, in the "C" SG was a bobbin coil indication at the

first hot leg support. plate on tube No. R34C53. This tube was plugged

'

in October 1990 with an indication that had been confirmed by Rotating

i Pancake Coil (RPC). (This was before the licensee had received approval

. to use a voltage-based alternate plugging criteria, and tubes were

, plugged upon confirmation of an indication by RPC.) The tube remained

i plugged until March 95 when it was unplugged and bobbin coil examination

showed the indication to be 1.89 volts, which was below the plugging

. criteria of 2 volts. During this inspection, bobbin coil examination

measured the indication as 6.73 volts. This is a significant growth

'

i rate for one fuel cycle.

,

j In discussions with the licensee the inspector learned that, while this

one tube (R34C53) is a singular case because of its large ap]arent

~

growth rate, there does appear to be a pattern where tubes tlat have

f Enclosure 2

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been plugged and later returned to service apparently show larger l

indication growth rates than tubes that have remained in service.

Using the contractor's evaluation equipment, the inspector reviewed

bobbin-coil, eddy current data for the following "C" SG tubes:

R34C37: R06C26: R07C35: R46C51: R45C46: R34C53:

R42C54: R45C56: R35C60: R31C60: R27C68: R30C67:

R32C65: R37C64: R41C64: R42C64: R39C65: R40C67:

R33C71; R30C72: R35C74: R35C76: R32C42: R24C78:

R26C77: R23C75.

During this review. the inspector paid particular attention to

indications at the hot leg support plate locations.

The inspector also observed preparations for the UTEC of a sample of "B"

SG tube indications. The preparation work activities were observed via

video monitoring equipment in the contractor's trailer. The UTEC system

was being used to cuantify the lengths and depths of a representative

sam)le of crack incications found using the plus-point eddy current

pro)e. The inspector also reviewed data alots of the nine tubes from

the "A" SG that had been inspected. At t1e time of the inspection the

only indication that had been depth sized by UTEC was a half-inch long,

axial indication located five inches above the top of the tubesheet in

tube R28C26: that indication had been sized as less than 0.020" in

depth.

c. Conclusions

Based on the review of the planned scope of the SG inspection, and the

expanded scope of inspections after significant numbers of indications

were found, the licensee appears to have taken a conservative approach

to determining the structural integrity of the Unit 2 SGs.

M1.4 2B EDG 18 month insoection (IP 62707)

The inspector reviewed the completed work packages and observed limited

portions of the following work on the 2B EDG:

e MP-14.1 18 Month Inspection

e Replacement of Lube Oil HX, Intercooler HX, Jacket Water HX tube

bundles due to inlet tube sheet erosion concerns.

for exhaust baccleakage.

All work was completed per procedure in a professional manner. Post

maintenance testing was completed satisfactorily.

Enclosure 2

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l- M1.5 W0s #96002615. 96002618. and 96002619: Insoection of Charaina Pumo

, Casinas (IP 62707)

'

The resident inspectors reviewed the licensee's inspection of charging

Jump casings.for cracks and boric acid corrosion concerns identified by

i

4RC Information Notice (IN) 94-63. The licensee utilized an ultrasonic

testing (UT) inspection process to inspect the nozzle ends. .This

)rocess was tested using mockups to verify it could detect defects

aetween the cladding and the case as small as 0.09 inches. The

inspectors reviewed the test package and determined it was adequate.

The inspections revealed no indications of cladding cracks in the nozzle

ends.

However, just prior to the outage, a failure of the 2A charging pum)

required removal of the rotating assembly. With the rotating assem)1y

removed, the licensee identified rust stains on the casing clad. UT and

RT testing in areas of rust stain showed no indications of a crack or

wastage of the casing. The licensee videotaped the indications and sent

copies to Westinghouse and Pacific Pumps for further analysis. The

analysis indicated that there were possibly two cracks in the cladding

but there was negligible wastage of the casing. Initial recommendations

were to conduct UT inspections of the casing and nozzles on an increased

frequency. However, as of the end of this re) ort, no formal

recommendations or actions had been taken. T1is will be tracked as

Inspector Followup Item (IFI) 50-364/96-13-02. Increased Frequency Test

Program for Charging Pumps due to Cladding Cracking.

M1.6 Desian Chanae Packaae (DCP) S95-2-8966: Chanaeout of RHR Pumo Imoellers

(IP 62707)

The resident inspector reviewed the DCP and observed work in progress

and the post-modification testing. This DCP was performed to enhance

pump performance at higher flows to provide a larger margin for pump

degradation. The DCP was performed on Unit 1 during the last refueling

outage. Overall work was well controlled. However, rework was required

to relug the motor leads because an incorrect lug / crimp size was used

and the motor ratings required upgrading from 380 to 400 horsepower.

The lugging deficiency was identified on November 11, 1996, when the 2A

RHR pump failed to start during the post-modification testing. On-

investigation the licensee found an open circuit where the lug on the

motor lead had pulled off the wire. The motor leads were 49 strand #6

wires. The original lugs were #4 lugs. Maintenance personnel initially

tried to relug the motor leads using #6 lugs but they were too small.

Maintenance personnel reverted back to the #4 lugs (as used by the

manufacturer) and crim)ed the lugs with a #8 die. The maintenance

personnel found that t1e lugs were not tight enough on the 2B RHR pump

so they recrimped the 2B RHR pump motor leads with a #7 die. They did

not go back and recrimp the lugs on the 2A RHR pump.

Enclosure 2

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i The licensee relugged both RHR pumps using #6 lugs s)ecifically sized

i for 49 strand wire per WO S00079621. An inspector o) served the

i relugging of the 2B RHR pump. The inspector reviewed FNP-0-EMP-1370.01,

Cable Termination. Splicing and Repair. for specific guidance on lugging

criteria. The inspector determined that the procedure only provided

general guidance and relied on skill-of-the-craft for determining lug

i sizing requirements.

!

3 The inspector observed the post-modification testing of the pumps per

i FNP-2-ETP-4411, 2B Residual Heat Removal / Low Head Safety Injection Pump

i Curve Development Test, Revision 0. The inspector reviewed the test

J.

+

prerequisites and procedure and observed the evolution prebrief and

3erformance of the test. The licensee found that the maximum brake

l lorsepower (Bh)) requirement at a runout condition of 4400 gallons per-

minute was higler than expected (between 380 and 390 Bhp). The RHR l

, motors have a 380 Bhp rating. To prevent exceeding the motor ratings

the licensee placed administrative controls on the use of the RHR pumps
until formal evaluations could be completed. The licensee performed a

50.59 evaluation. performed additional testing on the RHR

,

analyzed the impact of the increased loading on the EDGs.As pumps, and

a result

! of the 50.59 evaluation and the related safety evaluation, the licensee

'

was able to uarate the RHR pum) motors to 400 Bhp. The ins)ectors l

observed the 31 ant Operations Review Committee meeting at w1ich the  ;

issue was discussed and reviewed the 50.59 Jackage. The inspectors

i

"

concluded the evaluation was thorough and t1e motor uprate was

adequately justified.

M1.7 FNP-1-STP-24.1: Service Water System Quarterly IST

i a. Insoection Scooe (IP 61726)

i An inspector observed the entire performance of FNP-1-STP-24.1, 1A, 1B,

3 and 1C SW Pump Quarterly IST.

1

! b. Observations and Findinas

4

"

The SW sytem pumps performed as expected. The inspector verified that:

1) all initial conditions and prerequisites were satisfied and 2) test

instrumentation was calibrated and of the proper range. The inspector

j also verified selected data point calculations.

1 c. Conclusions

!

-This IST of the unit 1 Train A SW system pumps, including the swing 1C

pump, was performed IAW the procedure steps of STP-24.1. No

a deficiencies were identified.

..

Enclosure 2

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. M1.8 STP-40.0: Safety In.iection With Loss Of Offsite Power Test - Unit 2 (IP

61726)

,

On November 16. a resident inspector observed the conduct of FNP-2-STP-

40.0. Safety Injection With Loss Of Offsite Power Test. Overall, this

fully integrated, challenging and complex test was very well

orchestrated. No significant procedural problems or performance errors

were identified. All systems and components operated per design during

the test except: 1) minipurge dampers would not reopen: 2) hydraulic

contol valve 603A failed to fully open (due to binding): 3) 2A and 28

RHR pump flows were less than required: and 4) the mini-flow for 2C

charging pum) sprung a serious packing leak. Also, the 2A charging pump

was unavaila]le for the test due to repairs. and the 20 containment

cooler fast speed breaker was put in test.just prior to STP-40.0 due to

its fan rotating in reverse direction. Deficiency Re] orts were written

to address identified equipment problems. 2A and 2B 1HR flow discharge

valve stops were subsequently readjusted and pump flow retested

satisfactorily.

M1.9 WOf 596000458: Unit 2 TDAFW Pumo Governor Valve Stem and Soacer/ Washer

Reolacement (IP 62707)

On October 28. a resident inspector observed implementation of i

modification DCP-2-95-8939 by several mechanics. This DCP replaced the i

Unit 2 TDAFW pump governor valve stem, spacers. and washers based on

problems described by IN 94-66. The concern involved the use of l'

incompatible materials that would cause the stem to bind resulting in

turbine overspeed trips. The DCP and WO directed the installation of

new components made of vendor recommended materials. The inspector

observed the component replacements per approved work instructions and

inde)endently verified material compositions by reviewing applicable

purclase orders.

M1.10 RCP Seal Iniection System Foreian Material Intrusion (IP 62707)

OR 2-96-325 was written to document an investigation into the source and

cause of foreign debris (i.e.. pulverized 0-ring material) discovered in

six of nine RCP seal injection check valves. The seal injection check

valve internals were inspected during U2RF11 due to prior evidence of

debris from seal injection filter 0-ring material (Maintenance Incident

Report 95-02) and a seal injection flow transient during Unit 2 fuel

Cycle 11 (Incident Report 2-96-161). The discovery of additional 0-ring

material downstream of the seal injection filters led to the preliminary

conclusion that a poor work practice used during installation of RCP

seal injection system filters (i.e., failure to lubricate 0-rings per '

manufacturer recommendations) has resulted in the introduction of 0-ring

fragments throughout the seal injection flow path to the RCP seals. The

inspectors will review the licensee's completed OR and applicable safety

evaluation, and verify corrective actions. This issue is identified as

Enclosure 2

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IFI 50-348, 364/96-13-03, Foreign Material From Seal Injection System To I

! RCP Seals.

!

i

M1.11 Reset Motor-Ocerated Valve (MOV) Toraue_5 witches to Hiaher Values

! (IP 62707)

.

l

The NRC ins)ectors reviewed documentation and observed work in progress  !

j to verify tlat the licensee was resetting MOVs IAW a previous commitment '

made to the NRC in response to IR 94-28. The schedule, provided in a

l March 3, 1995, letter from the licensee to the NRC, required 10 Unit 2

i

MOVs to be reset in the current Unit 2 refueling outage. The related

work observed by the inspectors involved resetting MOV 2-32108. The

j- documentation reviewed was selected from a sample of 3 of the 10 valves

i and included: work authorization 451260 for resetting MOV 2-88878 and

, W0s 75880 and 75865 involving activities to replace MOVs 2-3019B and 2-

i 3134 (requiring them to be reset). The inspectors concluded that the

Unit 2 MOV were being reset IAW the licensee's commitment,

f M8 Miscellaneous Maintenance Issues (IP 92902)

i M8.1 (Closed) LER 50-364/95-08: Reactor Trip During DEH Card Changeout

! This event was discussed in IR 50-348, 364/95-20. No new issues were

! revealed by the LER.

!

! III. Enaineerina

l El Conduct of Engineering

j i

j El.1 Desian Chances 'and Plant Modifications i

i I

a. Insoection Scooe (IP 37550)

l The inspector reviewed design changes and plant nomfications that were  !

j being implemented on Unit 2 during the current ref. ting outage to )

-

determine if these activities were being Jerformed ,- / regulatory '

! requirements.1_icensee commitments, and tie design modification

procedure. Walkdowns were also performed in order to inspect the

? implementation of the modification in the field.

b. Observations and Findinos

The licensee had 46 DCPs on the list of plant modifications that had

been approved and scheduled to be worked during the U2RF11. The

inspector reviewed four DCPs as listed below that involved significant

electrical modifications:

DCP 95-0-8816, Provided design to convert the MCR air conditioner units

from water to air cooled units. This modification is being implemented

Enclosure 2

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by the licensee to improve reliability, maintenance and operation of the

MCR air conditioning system.

DCP 95-2-8875, Provided design to delete 13 MCR recorders and associated

wiring on Unit 2. replace four recorders with computer points, replace

three recorders with vertical scale indicators, add a new recorder to

~

monitor SG feedwater pump suction pressure, replace two obsolete MCB j

trend recorders, and add jacks to the moveable incore detector system to

provide for the connection of a portable recorder.

DCP 91-2-7186, Provided design to install interposing relayscin the l

, circuitry for high energy pipe break switches. The current high energy

)ipe break switches are obsolete and the approved re]lacement switches

l lave only one set of contacts instead of two as on t1e existing

switches. The addition of these relays will allow replacement of

existing switches.

DCP 87-2-4592, Provided design to automatically load an instrument air

,

compressor on the EDGs by the engineered safety system or loss of

l

'

offsite power (LOSP) sequencer, block the pressurizer heater backup

group A during sequencing and provide a manual bypass for unblocking. l

The )lant modifications required to be performed by the above DCPs had  ;

not )een completed. The inspector conducted interviews with the i

appropriate assigned engineers to discuss the scope of the modification, ,

work completed and remaining, and testing that would be performed for  !

functional acceptance. The inspector, accompanied by the assigned

engineer, performed walkdowns in the field to examine the work completed ,

on modification DCPs 95-0-8816. 95-2-8875, and 91-2-7186. I

With regard to DCP 95-0-8816. the inspector examined the modifications

of the A and B trains of the MCR air conditioner units. The A train- i

modifications were com)lete and functional. The B train was being

worked this outage. T1e inspector examined the conduit routing for the

new 600 VAC power cable for the B train condenser unit and found it to

be acceptable. The routing was examined from motor control center 1G in

the auxiliary building to the B train condenser unit on top of the

control building. Intermediate routes also included the MCR via

conduit. A revi;w of the UFSAR and RG 1.75. Revision 0, confirmed that

this routing was consistent with the licensee's commitments on RG 1.75.

The inspector concluded that the modifications performed to date

appeared to be acceptable.

l

The inspector examined portions of work performed under DCP 95-2-8875 to

l delete specific MCR recorders. The inspector accompanied by the

assigned engineer, toured the MCR to examine the Unit 2 MCB and the

I recorders that were being removed. While in the MCR the inspector

i observed the craft determinating the Metal Impact Monitoring System

i Recorder. The craft noted that the wires could not be determinated at

both ends because one end was soldered. The craft notified the engineer

l

j Enclosure 2

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who was accompanying the inspector at that time of this problem. A >

short time later, the engineer issued a field change for the wires to be 1

I

determinated at the one end only, taped and spared. - On a subsequent  :

tour of the MCR. the inspector observed that the Metal Impact Monitoring  !

I

Recorder had been removed as recuired by the DCP and the internal wiring -

had been determinated at one enc only, the ends of the wires had been

sealed with tape, and each wire had been labeled. spare. The inspector  :

found the completed work to be acce) table. In regards to this issue.

the inspector found that the craft lad a good questioning attitude and

that engineering interfaced well with the craft to resolve this problem.  ;

'

The inspector held discussions with the licensee regarding the

. instruments that are within the scope of RG 1.97 1 e., Types A. B. and C

-

l

l

and Categories -1 and 2 instruments. These instruments are required by  :

! RG 1.97 to be uniquely identified on MCBs as post accident monitoring

i instruments. The results of these discussions revealed the following

information regarding the licensee's methods for labeling MCR ,

'

,

instruments. An internal Alabama Power Company letter dated December

j 14, 1987, " Marking of Main Control Room Indicators =" indicated that

orange labels were being used as markers of E0 indicators to aide the

operators in identifying those instruments that would be more reliable

under accident conditions. Some time later the orange labels were

removed by the licensee and replaced with name)lates with black

lettering and white backgrounds with "E0" in tie label description. The

licensee's RG 1.97 Compliance Review Report No. A-204866. Revision 4.

dated November 28, 1995, requires that certain instruments be marked as

RG 1.97, but it does not specify how these instruments will be marked or

labeled. The inspector selected four Category 1 indicators from the

Compliance Review Report (i.e.. PI-402A, 402B, 403A. and 403B) and

confirmed in the MCR that they had been marked as "E0" The inspector

also noted that DCP 95-2-8875 3rovides design to delete the Boric Acid

Flow Strip Chart Recorder whic1 is Variable 102 in the RG 1.97

Compliance Review Report. In accordance with the Compliance Re) ort this

variable is not required to be marked on the MCB. Although no RG 1.97

indicators were identified without labels, the inspector had a concern

that the labeling of E0 instruments may not be adequate because there

may be other RG 1.97 instruments that are not E0 that are required to be

labeled.

The licensee acknowledged the inspector's concern regarding RG 1.97

labelling and subsequently conducted a thorough re-review of the issue.

Based on this re-review. SNC issued a letter dated December 5,1996 to

the NRC revising their commitment from using orange bars on the NCBs to

^ the "E0" designator. Furthermore, this letter confirmed that all RG

1.97 required variables specified in their 3revious commitment were

marked "E0." except for MS line 3ressure. R4ST level, and condensate

i storage tank level. But since t1ese instruments were not located in

! harsh environments and are uniquely identified by the plant's emergency

l

response procedures no additional identification is warranted.

4. Enclosure 2

i

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,

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21

The inspector reviewed portions of Revisions 7 and 8 to Design

Calculation E-42 Steady State Diesel Generator Loading Calculation for

LOSP, Safety Injection (SI) and Station Blackout (580). to confirm that

the additional loads ) laced on the EDGs by DCPs 8816 and 4592 had been

properly assessed. T1e inspector found that Revision 8 assessed the

load additions from DCPs 8816 and 4592 and concluded that EDG 1C steady

state load would exceed the continuous rating by less than 5 percent in

some design basis scenarios and SB0 scenarios, but would remain well

below the yearly 2000 hour0.0231 days <br />0.556 hours <br />0.00331 weeks <br />7.61e-4 months <br /> rating of 3100 kilowatts. This was found to

be acceptable. The steady state loading for EDGs 1-2A, 18 and 2B

remained below the continuous rating for all design basis and SB0

events.

Field wod on DCP 91-2-7186 was inspected and found to be acceptable.

The in:;pector reviewed the 50.59 evaluations for the DCPs identified

above to verify that they were adequate and that an unreviewed safety

question did not exist,

c. Conclusion l

The inspector concluded that the design changes and plant modifications

were adequate and the work completed on the above modifications was  ;

acceptable. The craft demonstrated a good questioning attitude during

the removal of the Metal Impact Monitoring Recorder which resulted in a

Field Change to the DCP. Engineering was also timely in providing an

acceptable solution to the problem. I

El.2 DCP S94-2-8752: Reolacement of Service Water System William Powell Gate

Valves (IP 37551)

The inspector reviewed the DC.P. UFSAR requirements for containment

isolation valves. TS requirements, and the valve technical data. The

inspector observed selected portions of the following:

e Removal of the old valves

e Preparation of the pipes

e Installation of the new valves

e Testing and setup of the MOV actuators

e Environmental qualification of MOV actuators

Work was generally performed IAW the DCP and plant requirements. Some

minor deficiencies were noted with foreign material exclusion controls

on the new valves in the laydown area and "As Low as )easonably

Achievable" (ALARA) practices in the work area. These deficiencies were

promptly corrected by the licensee.

Enclosure 2

l

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22

El.3 SG Level Control and Protection System Outside Desian Basis (IP 71707) j

After reviewing Westinghouse issued Nuclear Safety Advisory Letter 96-

004 dated October 8. 1996 the licensee concluded that under certain

conditions the SG level control and protection features for Units 1 and

2 do not meet Section 4.7.3 of IEEE-279 as re

On November 7. SNC promptly notified the NRC, quired

including thebysenior

10 CFR 50.55a(h).

resident inspector, pursuant to 50.72(b)(1)(ii)(B) for a condition

outside the design basis. Unit 1 steam flow channel selector switches

were selected to the channel IV position to eliminate the problem of a I

common tap for the steam flow transmitter and narrow range SG water

level that exist for channel III. Resident inspectors verified selector l

1

switch position and caution tags on steam flow channel switches for Unit

1. Unit 2 has the same design problem but is currently shutdown for

U2RF11. The licensee has declared Unit 1 steam flow and SG water level

protection features operable, and plans to resolve Unit 2 design problem

with a longterm fix prior to startup. Resident inspectors will review ,

the Unit 1 operability determination and continue to follow up on I

licensee longterm corrective actions for Unit 2. This issue is  !

identified as URI 50-348, 364/96-13-04 Common Tap For SG Steam Flow l

Transmitter And SG Narrow Range Water Level System Fails To Meet IEEE- i

279. l

E1.4 Control Rod Test and Evaluation Proaram .

l

On October 12 through 14, 1996, the engineering support group and

Operations conducted FNP-0-ETP-3661. Control Rod Test and Evaluation

Program, in order to accomplish special rod control tests, evaluations

and reporting requirements committed by the SNC response to NRC Bulletin

96-01, Control Rod Insertion Problems. A resident inspector observed

the conduct of ETP-3661. Appendix A. Observation Of Timely Rod Insertion

During Reactor Trip, as documented in NRC IR 50-348, 364/96-09. All

control rods were observed to insert properly. Appendix B. Multiple Rod

Testing Using Automated Measurement System Equipment, and Appendix E,

Control Rod Recoil Verification, were subsequently performed while still

in Mode 3. prior to cooldown for U2RF11, but not observed by the

inspector. The completed test procedure and test results were reviewed

by the inspector and found to be satisfactory. No abnormal control rod

drop characteristics were indicated. Additional control drag testing by

the vendor in the SFP and control rod drop testing using FNP-2-STP-112.

Rod Drop Time Measurement, in Mode 3 was planned during U2RF11 to

complete licensee NRC Bulletin 96-01 commitments.

Enclosure 2

- - - ..- - . - . - - . - . - - - . - - . - .- . - -- ---

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23 i

l E8 Miscellaneous Engineering Issues (92903) ,

!

E8.1 (Closed) IFI 50-348. 364/94-28-01. Evaluation of'Settinas for Cones- I

l Vulcan MOVs 8811A/B and 8812A/B Usina the EPRI PPP Model. ,

This item was opened to track the licensee's completion'of a commitment

to evaluate the settings of seven 14-inch solid wedge Copes-Vulcan gate '

valves using criteria developed in the Electric Power Research Institute

'

l (EPRI) Performance Prediction Program (PPP). The licensee's commitment

l

'

was made in response to an NRC concern regarding the reliability of the

valves' settings. The settings were questioned by the NRC because they

had been based on a method that recuired extensive extrapolation. The

subject valves were employed for RFR sump suction isolation and were

identified 1-8811A. 1(2)-8811B. and 1(2)-8812A/B. Their active safety

function was to open.

l In the current inspection. NRC inspectors reviewed and assessed the

! documented actions which the licensee had taken to meet their

l'

commitment. This review included Calculation SM-90-1653-018. Rev. O. ,

which determined oaening thrust requirements for the seven valves: and a i

letter identified :ile: ENG 15 90-1653. Log: FP 96-0346. which evaluated

the results of the calculation. The inspectors checked a sam)le of the 1

calculation inputs and verified that they were consistent wit 1 values  ;

given in the licensee's UFSAR and design-basis document. They also  !

verified that the licensee's calculation employed criteria developed by

the EPRI PPP and that the calculation had been independently verified by l

a separate organization. Further, the inspectors performed an

independent hand calculation which confirmed the accuracy of a

" cracking" computation included in the licensee's calculation.

The licensee's evaluation included comparisons of previously determined

valve capabilities with the opening thrust requirements determined in 1

Calculation SM-90-1653-018. These com)arisons showed that the present

capabilities and settings of five of tie seven valves were adequate, as

they exceeded the opening thrust recuirements. However, the comparisons

showed that the other two valves dic not have sufficient reduced voltage

capabilities to provide the opening " cracking" (unseating) force

requirements under worst case design accident conditions. The

capabilities of these two valves were shown to be 0.4 and 6 percent less

than recuired. (Note: The torque switches of the valves had been

.

r bypassec for the unseating or " cracking" portion of the opening stroke,

!

such that the valves' full reduced voltage capabilities were not

i

restricted by torque switch settings.) To su

i

two valves to perform their safety functions,pport the adequacy

the licensee 3rovidedof

a these

rationale that the actual cracking force requirements for t1e Farley

valves were lower than determined in the EPRI PPP calculation. Also.

! they stated that the valves' reduced voltage capabilities were actually

i higher than initially considered. based on the measured stem friction

'

coefficMnts for each of the valves. The inspectors reviewed supporting

licensee data :nd considered it insufficient to support lower cracking

l Enclosure 2

4

4

)

!

. . . _ - . . .

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24

force requirements. However, the inspectors found that the licensee's

test results supported a dynamic stem friction coefficient of 0.18.

Reduced voltage capabilities calculated using this stem friction

coefficient were sufficient to provide the required cracking forces.

The reduced voltage capability calculated by the licensee for the worst

case valve (1-8811A) using this stem friction coefficient exceeded the -

calculated minimum opening thrust requirement by approximately 1

percent. The other six valves had estimated capabilities more than 10

percent greater than required (much greater than 10 percent in most

cases).

The inspectors concluded that the licensee had satisfactorily completed

their commitment for these valves and that this provided additional

support for the capability of the valves to perform their active safety

function. On this basis the IFI was closed. However, the inspectors

noted continued weakness in the licensee's support for the capabilities

of these valves because of the following:

. The EPRI PPP criteria used by the licensee has not yet been

demonstrated to satisfactorily apply to valves manufactured

by Copes-Vulcan.

. Even assuming the EPRI PPP criteria was applicable, the

licensee's data for valve 1-8811A only supported a limited

margin of thrust capability above that required to perform

its safety function.

E8.2 _(Closed) IFI 50-348. 364/94-28-02. Evaluation of Settinas for

Westinghouse Unit 2 MOV 8811A Usina the EPRI PPP Model.

This item was opened to track the licensee's completion of a commitment

to evaluate the thrust setting for a 14-inch Westinghouse flexible wedge

gate valve using criteria developed in the EPRI PPP. The licensee's

commitment was made in response to an NRC concern that the setting was

based on EPRI PPP data but had not been determined IAW the related

criteria which EPRI had under development in the PPP. The subject valve

was omployed for RHR sump suction isolation and was identified 2-8811A.

Its active safety function was to open.

In the current inspection. NRC inspectors reviewed and assessed the

documented actions which the licensee had taken to meet their

commitment. This review included Calculation SM-90-1653-019. Rev. O.

which determined opening thrust requirements for the valve; and a letter

identified File: ENG 15 90-1653. Log: FP 96-0346. which evaluated the

results of the calculation. The inspectors checked a sample of the

calculation inputs and verified that they were consistent with values

given in the licensee's UFSAR and design-basis document. They also

verified that the licensee's calculation employed criteria developed by

the EPRI PPP and that the calculation had been independently verified by

a separate organization.

Enclosure 2

9

.

4

25

The licensee's evaluation com)ared the previously determined valve

capability with the opening t1 rust requirement determined in Calculation

SM-90-1653-019. This comparison showed that the present thrust setting

for the valve was satisfactory, as it exceeded the opening thrust

requirement determined in the calculation.

The inspectors concluded that the licensee had satisfactorily completed

their commitment for this valve and that the results confirmed the

adequacy of the setting used. On this basis the IFI was closed. j

E8.3 (Closed) IFI 50-348. 364/94-28-03. Evaluation of Settinas for Pratt .

Sutterfly MOVs Usina the EPRI PPP Model. l

This item was opened to track the licensee's completion of a commitment

to evaluate the settings for 16 butterfly valves manufactured by Henry

Pratt. The evaluation was to be performed using criteria developed in

the EPRI PPP. The licensee's commitment was made in response to an NRC

'

concern that the licensee did not have any useful diagnostic data to

support the settings used for these butterfly valves. Torc ue l

requirements for the valves had been established using guicance from the

valve manufacturer. The valves were divided into groups. Their

functional names and valve numbers were as follows:

Functional Name Valve Numbers

Turbine Building Service Water 1(2)-0514, 1(2)-0515, 1(2)-

l Isolation Valves 0516. and 1(2)-0517

>

Steam Generator Heat Exchanger and if2)-3149 and 1-3150

Boron Thermal Regenerative Chillers

Service Water Isolation Valves

. . Component Cooling Water Valves to RHR 1(2)-3185A/B

.

Heat Exchanger

1

In the current inspection. NRC inspectors reviewed and assessed the

documented actions which the licensee had taken to meet their

commitment. This review included Calculations SM-90-1653-017, SM-90-

1653-014, SM-90-1653-015, and SM-90-1653-016, which determined the

torque requirements for these valves. Additionally, the inspectors

reviewed the licensee's evaluations of the results of the above

calculation, which were documented in a letter identified File: ENG 15

90-1653. Log: FP 96-0346.

The inspectors checked a sample of the inputs to the calculations and

verified that they were consistent with values given in the licensee's

UFSAR and design-basis document. They also verified that the licensee's

calculation employed criteria developed by the EPRI PPP and that the

calculation had been independently verified by a separate organization.

Enclosure 2

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.. .

26

The licensee's evaluations compared the valves' torque settings with the

l torque requirements determined in the EPRI PPP calculations. This 1

comparison showed that the present torque settings were satisfactory. l

except that the torque settings for the turbine building SW isolation j

l valves were too low in one accident scenario. The torque switches for j

l these valves had been bypassed in the region of concern and the valves J

were capable of performing their safety function. The inspectors found

-

that the licensee had initiated documentation (e.g. W0s 450972, 450973.

450974, and-450975) to reset the torque switches to the higher values

determined by the calculation.

The inspectors concluded that the licensee had satisfactorily completed

their commitment for these valves and that the results showed the valves l

were acceptable for operation. On this basis the IFI was closed.

IV. Plant Sucoort

4

R1 Radiological Protection and Chemistry (RP&C) Controls

i

l R1.1 Radiolooical Controls I

i

a. Insoection Scooe (IP 83750) l

The inspectors discussed planning and observed implementation of

,

selected RWP requirements associated with the following routine tasks

l and U2RF11 outage job evolutions,

o RWP 096-0081. Waste Processing, Revision (Rev.) 0, effective

January 1, 1996.

e RWP 296-0154, Special Plant Maintenance. All Work Associated with

i Primary Steam Generator Manway and Diaphragm Removal and

Installation in Containment. Refueling, Rev. O, effective October

1. 1996.

e RWP 296-0161. Refueling, Rev. 0. effective October 1, 1996.

e RWP 296-0196, Special Plant Maintenance. Work Associated with the

l Boron Injection Tank (BIT) Removal, Rev. O, effective October 1.

l 1996.

e RWP 296-0198. Special Plant Maintenance Work Associated with

Replacement of Service Water Isolation Valves & Actuators to

Containment Coolers 2A, 2B, 2C, 2D and the Reactor Coolant Pump

Motor Air Coolers, Rev. O. effective September 24, 1996.

l e RWP 296-0199, Special Plant Maintenance. Work Associated with

,

Replacement of Service Water Isolation Valves & Actuators to

. Containment Coolers 2A. 28. 2C. 2D and the Reactor Coolant Pump

Motor Air Coolers Rev. 0, effective October 1, 1996.

Enclosure 2

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Job planning and pre-job briefings were discussed and evaluated for

selected RWP guidance. In addition, the inspectors observed licensee

radiation surveys conducted adjacent to the transfer canal outside of

containment and reviewed the adequacy of auxiliary building controls and

postings in place during transfer of irradiated fuel.

The inspectors made frequent tours of the RCA. and reviewed and

discussed specific procedural guidance, selected survey results and

postings. The site dose expenditure and dose expenditure for selected l

U2RF11 tasks were reviewed and discussed with HP supervisors and  ;

technicians. l

In addition. FNP OR Number 96-227 dated October 7. 1996, documenting

details of a worker who exceeded plant administrative quarterly dose

limits and an associated discrepancy between his thermoluminescent

dosimeter (TLD) and digital alarming dosimeter (DAD) monitoring results

were reviewed and discussed. The status of licensee followup actions

regarding the event were discussed in detail.

b. Observations and Findinas

Excluding two identified events involving BIT system maintenance and

laundry 3rocessing, all work activities observed were conducted IAW the

establisled RWP requirements. Initial reviews and surveys to establish

controls and postings were IAW FNP-0-RCP-4 Refueling Survey. Rev. 13a.

dated October 21, 1996. Administrative and physical controls, and

established postings within the auxiliary building during movement of

irradiated fuel were verified to be adequate based on measured dose

rates.

TS 6.11 requires, in part, that procedures for personnel radiation

protection be prepared consistent with the requirements of 10 CFR Part

20 and be approved, maintained and adhered to for all operations

involving personnel radiation exposure. Procedure FNP-0-M-001. Health

Physics Manual. Rev. 12. effective July 14. 1996. Section (S) 6.4

requires any entry into the RCA to be governed by a RWP. During tours

of the RCA during the week of October 21, 1996, the inspectors

identified the following issues.

e On October 22, 1996, a worker performing maintenance on the BIT

recirculation pump equipment located adjacent to the auxiliary

building 100 foot elevation batching crea, was observed kneeling

and crawling within an area posted as " contaminated" without the

required coverall dressout specified by RWP-096-0196. Special

Plant Maintenance, effective October 1. 1996.

e On October 24. 1996, a HP support worker was observed operating

the automated laundry monitor (ALM) without proper gloves and shoe

covers as required by RWP-096-0081. Waste Processing. Rev. O.

effective January 1, 1996.

Enclosure 2

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28

Initial corrective actions for the identified RWP compliance concerns

included work stoppage, counseling of individuals involved and

subsequent discussions with supervisors. None of the involved

individuals were found to be contaminated during RCA exit surveys. For

the BIT maintenance work issue, the inspectors requested the licensee to

conduct contamination surveys within the posted contaminated area where

the work was observed on the auxiliary building 100 foot elevation.

Licensee survey results indicated contamination levels (beta / gamma) were

less that 200 disintegrations per minute per 100 square centimeters, j

Discussions with HP staff indicated that the area was posted as a

contaminated area due to the potential for release of contamination from

within the BIT equipment during the maintenance activities. The

licensee initiated FNP OR Nos. 96-1002 and 96-1003 for the identified  !

RWP compliance concerns. On October 25. 1996, licensee representatives {

informed the inspectors that preliminary review indicated that observed )

improper dressout observed for the ALM operations resulted from i

misinterpretation of RWP requirements by the responsible supervisor of

the involved worker.

On October 25, 1996, the inspectors attended and observed a pre-job

briefing associated with removal of the SG manway diaphragms.  !

Meaningful discussions between HP and maintenance staff were noted i

regarding changes to previous storage practices following diaphragm i

removal. Previous use of large shielded containers were discontinued i

with new storage to be provided using drums containing water for

shielding. The use of the water filled drums improved dose reduction

efforts and reduced safety concerns associated with movement of the  ;

large containers within containment. From subsequent discussions with i

licensee representatives regarding this change, the inspectors noted I

that although evaluated, the licensee had evaluated the change in i

storage methods qualitatively, a detailed evaluation of the dose i

reduction effect using the new water filled drums was not documented. i

The ins)ectors reviewed and evaluated licensee actions associated with

FNP OR io. 96-27. dated October 7, 1996. The report documented an HP ,

support individual's dose as measured by TLD of 1122 millirem (mrem)

which exceeded the established administrative quarterly limit of '

1000 mrem. Licensee followup also identified a significant difference,

a] proximately 44 percent, between the TLD and the DADS used to monitor 1

tie worker's dose for the quarter. On average. TLD to DAD monitoring

result comparisons were less than five percent. The worker was excluded

from further RCA entries and an investigation initiated. Review of the

individual's daily DAD entries, indicated maximum potential for exposure

to elevated dose rates occurred on September 6 and 10. 1996, during

placement of spent filters in High Integrity Containers in a Radwaste

exclusion area. General license followup included interviews of all

personnel involved and review of radiation control 3ractices associated

with the subject filter placement: verification of JAD calibrations and

calibrator operation, and confirmation of TLD readings; and

determination and evaluation of filter isotopic data and energy response

Enclosure 2

.

.

29

of personnel monitoring equipment. The licensee had assigned the

subject individual the 1126 mrem exposure resulting in a year-to-date

(YTD) total effective dose equivalent (TEDE) exposure of 1160 mrem. At

the end of the onsite inspection, no definite causes for the observed

differences between TLD and DAD quarterly dose results were identified

and licensee evaluations were continuing.

As of October 24. 1996, maximum TEDE results 1160 and 806 mrem, were

reported for two individuals involved with handling spent filters within

the radwaste facilities in September 1996. Extremity shallow dose

exposure results of 5762 and 5414 mrem were reported for these

individuals. For the outage activities reviewed, the maximum individual

dose, i.e.. deep dose equivalent, of 300 mrem was documented for a

contractor involved with eddy current testing.

. c. Conclusions

In general. RWP guidance was adequate for routine RCA and U2RF11 outage

activities. Documentation of detailed dose reduction efforts and

calculations 'should be improved. Excluding one individual, all personal

exposures were less than administrative limits and all individuals were

within regulatory limits. Licensee review and followup actions for a

worker exceeding quarterly administrative dose limits were adequate.

Two examples of inadequate implementation of RWP dressout requirements

were observed. These examples were identified as Violation (VIO) 50-

348.364/96-13-05. Failure to Follow Radiation Work Permit For Use of

Proper Protective Clothing .

R1.2 Imolementation of the ALARA Proaram

a. Insoection Scoce (IP 83750 and 84750)

The licensee's ALARA program guidance and implementation associated with

the current outage activities were discussed and reviewed. In addition. 1

selected radiation control performance indicators were reviewed and

discussed with licensee representatives.

b. Observations and Findinos

For 1996 which included a single refueling outage, licensee

representatives established a dose goal of 250 rem. This dose

expenditure for the site is similar to the 251 rem expended in 1994,

also single outage year. As of October 23. 1996, the licensee YTD dose

expenditure was documented as 10.503 rem compared to a predicted

exposure of 43.925 rem. The difference was expected, in part, as a

result of delays in the outage schedule.

The amount of contaminated floor space, excluding containment and

exclusion areas, was repcrted as less than or equal to approximately

eight percent since 1994. As of September 27, 1996. licensee listed 5.5

Enclosure 2

a

.

  • . .

30

percent of floor space as contaminated, a slight decrease from 5.7

percent reported in Jan 26, 1996. Similar values. 5.26 and 8.38 3ercent

were reported for April and July 1995 respectively. For 1994, t1e

licensee reported contaminated floor space ranging from 6.0'to 8.2

percent.

For 1996, only one personnel contamination event (PCE). defined as

contamination levels exceeding 5000 disintegrations per minute, was I

reported. For single and dual outage years of 1994 and 1995, the

licensee listed 55 and 74 PCEs, respectively. The majority of PCEs were

identified for contractors and were associated with poor work practices.

The inspector reviewed ALARA initiatives conducted during the U2RF11

outage IAW the long-term exposure reduction program outlined in FNP

Exposure Reduction Plan, dated May 1993. The inspector discussed and

verified implementation of the following ALARA program items including

cobalt reduction, crud trap flushing, early boration, elevated pH and

boron / lithium management, improved ALARA training and awareness, remote

personnel monitoring, robotics and selected SG maintenance enhancements.

The licensee had suspended the zinc injection program since the U2RF9

outage but was expected to resume its implementation during the current

outage.

c. Conclusions

Implementation of established ALARA program activities was verified. No

significant negative trends were observed for the performance indicators

reviewed.

R2 Status of (RP&C) Facilities and Equipment 1

R2.1 Tours of the Unit 1 and 2 Radioloaically Controlled Areas (IP 71750)

During the course of the inspection period the resident ins)ectors

conducted numerous tours of the auxiliary building RCA for Jnits 1 and

2. In general. HP control over the RCA and the work activities

conducted within it, were good. Material condition and housekeeping in

the Unit 1 and 2 RCA considering ongoing outage activities, were much

better maintained than in the past (see Section 02.1).

R2.2 General walkdowns of radiation monitorina systems

a. Insoection Scooe (IP 83750 and 84750)

The inspectors reviewed and evaluated general housekeeping and verified,

where applicable, operability of selected process and effluent RMS

detectors, electronics, sampling lines and flow meters. The following

RMS samplers or detectors, i.e. radiation elements (REs), and associated

equipment were included in the walkdowns: Unit 1 (U1) containment

atmosphere particulate (RE-11) and gas (RE-12): U1 turbine building

Enclosure 2

. _ _ _ _ . _ _ _ . _ . . . _ _ . _ _ _ . _ _ . _ _ _ _ . _ _ - _ _ _ . _ ,

.

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31

ventilation exhaust normal range (RE-15): U1 & U2 plant vent gas (R-

298) and particulate (RE-29A): MCR air supply (RE-35A&B): and U1 & U2

. post accident sampling system airborne particulate (RE-67).

In addition, the inspectors reviewed and discussed program guidance and

testing of air to ensure service air compressor system supplied Grade D

respirable air for use, as applicable, during U2RF11' job evolutions.

,

b. Observations and Findinas

,

In general. housekeeping practices associated with RMS detectors and

equipment were improved relative to conditions observed for the period

of August 12-16. and 26-30. 1996 and documented in-IR 50-348. 364/96-10.

dated September 27, 1996. Only two examples of poor housekeeping

L practices associated with the RMS equipment skids or sample locations

l were noted during equipment walkdowns conducted on October 25, 1996.

The examples included unsecured equipment stored within the U1 plant

vent particulate (RE-29A) sampler area and excess filter pa)ers being

stored within the U1 Plant Vent sampler cabinet (RE-29B). _icensee

l representatives stated that the identified concerns would be corrected

in a timely manner.

The inspectors also verified that the service air compressor system was

tested to certify supplied breathing-air as Grade D for potential use

l

during outage activities. Licensee representatives collected Unit 2

'

containment breathing system air samples on October 15, 1996. IAW FNP 2- l

RCP-112. Sampling of Service Air to Meet Respiratory Limits, dated  ;

September 9. 1996. Sample-results verified that the U2 containment air

quality exceeded the established limits for Grade D air based on the

Compressed Gas Commodity Specification G7.1.1973.

c. Conclusions

Overall. no significant concerns were identified for RMS operability and

for certification of the supplied breathing air equipment. Licensee

tests verified that the service air compressor system supplied Grade D ]

respirable air IAW 10 CFR 20. Appendix A requirements.

R3 RP&C Procedures and Documentation l

a. Insoection Scooe (IP 83750)

Records of the previous 1996 YTD occupational radiation doses for

approximately 20 contractors hired specifically for U2RF11 outage tasks  !

were reviewed and discussed with licensee staff. l

L

i

The inspectors also reviewed selected effluent release data. In

i particular the inspectors reviewed and discussed abnormal effluent

i releases documented for the period 1994 through October 21, 1996.

3 Enclosure 2

i-  !

I

i

4

- , , . , , . . - . - . , . . _ . , . - . .n _. .,-~r.-, , _ _ _ , .

,,

. _ _ . . _ _ _ _ _ . _ _ . _ _ . _ _ __ _ . _ _ __

i .'

'

l-

l

32

b. Observations and Findinas *

The inspectors verified that all contractor persennel had provided a

signed u)-to-date NRC Form 4, or equivalent ar;or to conducting initial

work witlin the RCA. Further the licensee lad received, or was in the

l process of obtaining reports of each individual's 3revious 1996 dose

L equivalents from the most recent employers for worc involving radiation

I

exposure.

l For 1994 no abnormal effluent releases were identified. In 1995 only

one abnormal effluent release associated a small U1 primary to secondary

, leak and the venting of the atmospheric relief valves following a U1

l -reactor trip was identified and evaluated. The event as documented in

'

chemistry incident report (CIR) 1-95-009. resulted in a increase-in

offsite dose. For 1995, dose estimates from all effluents were a

t fraction of a percent of the allowable offsite dose calculation manual

(0DCM) limits. As of October 21. 1996, three abnormal effluent releases

'

were reported and documented in CIRs-1-96-19. 1-96-30, and 1-96-33. The ,

inspector noted that CIR 1-96-19 documented and calculated a negligible ,

dose effect from required surveillance testing of the U1 TDAFW Jump

during a small primary to secondary leak. The two remaining CIls

l identified a continuous leak of effluents containing tritium through the

l U1 MS line atmospheric relief valve. Effects of the leak were to be

l documented in the 1996 annual effluent report,

c. Conclusions

l Licensee records of previous dose estimates for outage contractors were

being completed IAW 10 CFR 20.2104 requirements. Documentation

regarding effluent releases was prepared IAW ODCM requirements and

demonstrated release data verified offsite doses were small fraction of

a percent of the allowed limits. The number of abnormal releases have

increased since 1994, mainly, as a result of U1 primary to secondary

leakage associated with required or inadvertent ecuipment operation, or

maintenance problems. These abnormal releases hac a negligible

contribution to offsite doses.

!

l R6 RP&C Organization and Administration

i

a. Insoection Scooe (IP 83750)

!

l Recent changes to the HP organization and staffing levels for the U2RF11

outage relative to the 1995 U2RF10 were reviewed and discussed. From

facility tours and observations of work in progress the inspectors

evaluated staffing adequacy and proficiency of the HP technicians

providing job coverage.

I

Enclosure 2

- - - - -

,. -

. .

. . - - - - . - - _ . - - - - _ - - - - -- . _ . - , - - - -

t .

'

4-

i-

33

4

I

b. Observations and Findinas >

The HP organization and permanent staff for routine operations have

remained relatively stable. Since a previous U2 refueling outage in

-

1995, the only organizational change involved combining the plant health

i physicist and radwaste supervisor positions and elimination of a

! permanent HP technician position. Currently, the permanent HP staff

included a HP superintendent, a HP su3ervisor, health

>

physicists /radwaste su)ervisor, five iP foremen and 33 senior

technicians. During t1e current outage, the licensee sup)1emented the

i- staff with approximately 50 contract HP 3ersonnel and 21 iP and ,

J

chemistry staff members from Vogtle and latch Nuclear Plants. Overall. I

'

j the numbers of non-permanent HP personnel employed during the current

i outage decreased by approximately 15 technicians, approximately ten

junior and five (senior) HP technicians since the previous U2RF10

outage. I

! No concerns regarding job coverage nor HP technician proficiency were

l identified during observation of fuel movement. RHR pump maintenance,

i and SW valve replacement activities.

c. Conclusions  !

! No concerns were identified for the current organization. The amount of

j job coverage and proficiency of HP technicians were considered adequate

for the early outage tasks observed. j

.

l R7 Quality Assurance in RP&C Activities

1

R7.1 Licensee Self-Assessment Activities

a. Insoection Scooe (IP 84750)

The inspectors reviewed and discussed the detailed plans for audits

scheduled to be conducted during the U2RF11 outage. The following audit

plans were reviewed in detail.

e Safety Audit and Engineering Review (SAER) Audit Report No. 96-

0A/41-1 Refueling Outage Activities

e SAER Report No. 96-PRM/23-1. Primary Vendor Services Audit

e SAER Report No. 96-FL/27. Fuel Loading

e SAER Report 96-PRTP/32. Post Refueling Test Program

In addition, supplemental audit staffing was reviewed and discussed.

.

Enclosure 2

_. _ _ _ . . _ . . _ _ _ _ _ __ _ _ _ . . _ _ _ _ . _ _

< .

,

t

34

'

b. Observations and Findinas

Review of the audit plan details verified that radiological 3rotection

issues were included in the SAER evaluations scheduled for t1e current

outage. Audit plan details included, in part, observation and

'

verification of radiological work controls for routine outage activities

and radiography practices internal exposure controls, housekeeping and

cleanliness, personal qualifications and certifications, and

verification of completion of Standard Test Procedures conducted during

the outage. From review of audit plans and discussions with SAER

auditors, the inspectors determined that specific job evolutions to be

reviewed included radiological controls associated with U2 fuel

movement, SG maintenance and SW valve replacement activities. The

inspectors directly observed auditors conducting radiological work

practice observations for auxiliary building SW valve replacement and U2

containment fuel movement activities.

An additional outside auditor with senior reactor operator (SRO)

experience was scheduled to assist the FNP SAER group during the current

outage, In addition, SAER management stated that in response to

concerns addressed in NRC IR 50-348/96-10, 364/96-10 dated September 27,

1996, an individual from the Vogtle Nuclear Plant with extensive

chemistry and radiation arotection experience was scheduled to

participate in a future RP&C audit in early 1997.

,

l

c. Conclusions

No concerns were noted for ongoing and proposed audits of radiation

control and chemistry activities. The scheduling of outside auditors to

assist in review and evaluation of RP&C. program areas was considered a

program enhancement.

R8 Miscellaneous RP&C Controls Issues (92904)

R8.1 (Closed) LER 50-348. 364/95-06: Licensed Material Shicoed to Incorrect

Destination by Common Carrier

This LER was a minor issue and was closed.

S1 Conduct of Security and Safeguards Activities

S1.1 Routine Observations of Plant Security Measures (IP 71750)

During routine inspection activities, resident inspectors verified that

portions of site security program plans were being properly implemented.

This was evidenced by: 3 roper display of picture badges by plant

personnel: appropriate cey carding of vital area doors; adequate

stationing / tours of security personnel: proper searching of

packages / personnel at the primary access point and service water intake

structure; and adequacy of compensatory measures (i.e., posting of

Enclosure 2

.

35

guards) during disablement of vital area barriers. Security activities

observed during the inspection period were well performed and appeared l

adequate to ensure physical protection of the plant. Guards were

observed to be alert and attentive while stationed at disabled doors and  !

access covers to critical underground equipment (e.g., SW system valve

boxes). Posted positions were manned with frequent relief.

S8 Miscellaneous Security and Safeguar,ds Issues (IP 71750) l

S8.1 (Closed) URI 50-348. 364/96-09-05: Failure to Search Contractor Trailer

Prior to Entry Into the Protected Area (PA)

On October 10, 1996, a resident inspector observed security guards

escort a Westinghouse sludge lance trailer into the PA that was not

searched. The trailer was posted as a RCA. A security guard outside

the PA gate did search the truck, cab, and driver prior to entering the

PA. After subsequent review of licensee corrective actions, and

interviews with responsible individuals and su ervision, the inspector

concluded that this instance constituted a vio ation of the FNP Security l

Plan, section 4.4.2 that requires searching all vehicles. materials and

packages prior to entering the PA. with certain exceptions established

as Categories I - IV. Categories I and III would allow certain types of

materials or packages to enter the PA without being searched as long as l

they were under continuous direct observation, or positive controls were ,

put in place, respectively. Categories II and IV did not apply to this '

situation. Also it was the inspectors judgement that the RCA boundary

around the trailer did not constitute a personnel hazard per Category

II. The other categories did not apply to this situation.

Security guards did not search the Westinghouse sludge lance trailer

prior to entering the PA. and subsequently relinquished direct

observation of the trailer without establishing positive control. A

search was not conducted until the following day on October 11. Upon

notification of the problem, immediate corrective actions were taken by

the Security Chief to promptly and effectively address the problem. By

the end of the IR period, longterm corrective actions were still being

pursued that should considerably improve effectiveness of future PA

searches. Good coordination was evident by the Security Chief with

other FNP departments and outside sources in developing a new permanent

policy. This issue is identified as VIO 50-348, 364/96-13-06. Failure

To Search Truck Trailer Prior To Entering Protected Area, and closes

this URI.

Enclosure 2

. . - . - - . . - . _ _ _ - - . - . - . _ . _ - - . - - . - _ - .

,

.

t . .;

~

1

j 36

j F2 Status of Fire Protection Facilities and' Equipment

F2.1 Doerability of Fire Protection Facilities and Eauioment

'

i

l

a. Insoection Scoce (IP 64704)

The inspectors reviewed the open maintenance W0s, maintenance history.

and incident reports on the ' facilities . fire protection systems and
features, and inspected these items to determine the performance trends
and the material conditions of this equipment.

b. Observations and Findinas

i- Maintenance Observations:

As of November 12. 1996, the total number of open maintenance work '

requests related to the fire protection systems and features was 81. *

l These work requests were grouped as follows:

5  :

j Kaowool Fire Barriers 38 i

Fire Protection Water Systems 34 ,

'

.

5

l C0're

Fi Doors 2  :

Fire Pumps 1

Fire Detection System l

1 i

i 81  ;

i

All except five of these work requests were issued in 1996. The work

requests issued prior to 1996 were minor repairs which did not affect

the operability of these systems. The Kaowool work requests involved a

j number of recently identified discrepancies. Work was in process to

-

correct these issues.

There was not a backlog of open work requests.

l

l Fire Protection Related Incident Reoorts: .

'

!

i The licensee initiated 54 incident reports from January 1. 1993 through

October 31. 1996. on fire protection related items, such as fire pumps. -

l automatic sprinkler systems, fire detection system. CO2 systems, fire

barriers, and fire watch activities. These incident reports were as

.

follows:

! Fire Protection System / Feature Number Percent

!

l

j Fire Pumps 14 25.8  !

Fire Watch 9 16.4

j Sprinkler and Fire Hose Systems 9 16.4

Fire Alarm System 8 14.6

CO2 Systems 8 14.6

1 Enclosure 2

a

.

$

_

. _ _ _ _ _ _ _ . _ - . . _ _ _ _ _ . . _ _ _ . _ . _ _ . _ _ . . _ _ . _ . . _.

,

.

t , i

i'

1

- '
37

'

i Personnel Errors 4 7.1

i Fire Barriers 2 3.5

4

Fire Doors _1 B  :

.

Totals 55 100.0

i Incident reports related to the recent Kaowool problems where not  :

included in this list.

s

Most of the abnormal occurrences, exceat for the Kaowool problems. -

l during this period were related to pro)lems with the fire pumps, fire l

4

watches and water suppression systems. .

i

l

i Fire Protec' tion System Ooerability:

!

,

A review of the Fire Protection portion of the Plant's Daily Status

Report for November 12, 1996 indicated the following components or

systems were out of service:

l

j Fire Protection System Unit 1 Unit 2

i

,

i Kaowool Fire Barriers 49 24

i Fire Doors 8 16

Fire Barrier Penetrations 3 6

Automatic Sprinkler Systems 1 12

Fire Hose Stations 0 1
Fire Detection System 1 2

The inspector considered the number of fire protection systems out of 1

i service to be excessive. However, this high number was attributed to i

the current Unit 2 refueling outage and the repairs in process for the i

} Kaowool fire barrier discrepancies Appropriate compensatory measures

j had been implemented for the equipment which was out of service.  ;

i

The status report provided the licensee with a good means of identifying

j out of service fire protection equipment to assure that appropriate

compensatory measures were implemented.

] During the plant tours. the inspector noted that the maintenance and

'

material condition of the fire protection equipment were satisfactory,

exce)t for a significant number of pre-action automatic sprinkler valves

whic1 were set wet. These valves are designed to be maintained in the

i close position and activate to the open position by signal from the

associated fire or smoke detection system. When these valves are
- maintained in the tripped or open position, the water flow alarms to

j these systems are placed out of service and sprinkler system actuation

1 would not be transmitted by the alarm system. This increases the

possibility of water damage to plant equi) ment in the event of

inadvertent actuation of these systems. _eaving the pre-action valves

in the tripped position for appreciable long periods of time has been a

!

} Enclosure 2

I

i

>

- ,, , - _ . _

- _= -

-

~, . >

  • .

.

38

normal practice at Farley for several years. This is identified as a

program weakness.

In March 1996, as documented by NRC IR Nos. 50-348, 364/96-02 and 96-07.

multiple failures occurred during the routine operability testing of the

pre-action automatic sprinkler system valves. Approximately 9 of the 27 1

pre-action system valves installed to provide fire protection for safety

related areas failed to operate automatically upon an actuation signal

from the fire detection system, i.e. the valves would not operate from

the normally closed to the open water flow position. The licensee  !

implemented additional preventive maintenance measures for these valves.

contacted the vendor for assistance and scheduled an accelerated

surveillance testing program. The surveillance testing of these valves

was changed from 18 months to two months. Prior to the August 1996

scheduled tests, two valves failed to operate 2n August 12 following an

l inadvertent action of the fire alarm panel. On August 22. during

l performance of the two month accelerated surveillance testing

- activities, one additional valve failed to operate either manually or-

automatically. The licensee assembled a root cause team and continued

to work with the vendor to determine the cause of these failures. One

of the failed valves was sent to the vendor's test laboratory for

further evaluation. The results of this evaluation were not available

at the conclusion of this inspection. The vendor was scheduled to

]articipate during the next surveillance testing of these valves in

)ecember 1996. The reliability of these valves is considered

questionable until the licensee identifies the cause of these failures

and implements appropriate corrective action to resolve the problem.

This issue is being tracked as IFI 50-348, 364/96-02-03, Pre-action

sprinkler system failures.

j From January 1993 through October 1996, multiple failures of the diesel l

-

engine driven fire Jumps to start on demand were identified or diesel l

engines had to be slut down due to operability problems. Exam)les of-

these problems included: inoperable electrical selector switcles,

! electrical starter switch, engine starter, engine batteries leaking

! engine coolant hose connector, ruptured coolant hose connector, and

i leaking oil from the lubrication system. The inspector reviewed

approximately 14 incident reports which had been issued on the diesel

driven fire pumps.

To establish a high confidence level on the operability of these pumps,

the automatic start surveillance test for the diesel driven pumps was

changed in May 1995 from monthly to every two weeks and the frequency of

the functional and capacity tests was changed from 18 months to

annually. The last recorded failure of a diesel driven fire pump was

September 26, 1995. The licensee )rovided the inspector with trending

, information which indicated that t1e performance of the two diesel

l driven fire pumps in the 18 months prior to November 1996 had improved

j as follows:

i I

! Enclosure 2

. . ., __ _ _ . - - -

._ _ __ _ _ _ _ _ _ -._ _ . _ _ _ _ . _ _ _ _ _ _ . _ . _

<

.

,

e

39

Diesel Driven Fire Pump 1 Three start failures in previous 228

demands for a reliability of 98.7%

Diesel Driven Fire Pump 2 No start failures in previous 195 demands 1

for a reliability of 100%

!

1

The licensee's program to establish a high level of confidence in the '

i

operability of these pumps was considered pro-active.

The licensee informed the inspector that replacement parts for the

station fire alarm control panels were no longer manufactured and were

becoming difficult to obtain. The existing system was operable but due

to the lack of replacement parts, future reliability may be a problem.

c. Conclusions

The number of outstanding work requests related to the fire protection

systems was high. However, there was not a backlog of outstanding W0s.

Corrective maintenance on degraded fire protection systems was being

acccmplished in a timely manner. The fire pumps and automatic sprinkler

systems sustained reliability problems during the past two years due to

.a number of operational failures. The licensee had taken positive

corrective action initiatives to resolve these concerns. This action

was effective for the fire pumps but currently has not been effective on

the resolution of the problems with the automatic sprinkler systems.  !

Leaving the 3re-action valves in the tripped position for long

'

of time has )een a normal practice at Farley for several years.This periods

is

identified as a program weakness.

Replacement parts for the site fire alarm system were difficult to

locate. The system was operable but reliability may decline due to lack

of readily available replacement parts.

The daily fire protection status report was considered a positive means

of identifying degraded fire protection systems and to implement the

appropriate compensatory measures for inoperable systems.

F2.2 Surveillance of Fire Protection Features and Eauioment <

.

a. Insoection Scooe (IP 64704)

The inspectors reviewed the surveillances and tests scheduled for the

various fire protection systems and features to determine compliance

with UFSAR Section 9B Attachment C.

b. Observations and Findinas

Available documentation or cross reference material was not available to

indicate that'all of the tests and inspections listed by UFSAR Section

9B Attachment C had been incorporated into cppropriate plant

Enclosure 2

. -. . .. . .

.- - _ . - . - . . - . - - . - ~ . -. - - - . - _ - -

,

'

'

'

- .  !

,

.

i

  1. '

40

!

l surveillance procedures. Therefore, the inspector selected 18 fire

i protection inspection and surveillance requirements from the UFSAR to

verify that these items had been incorporated into the surveillance

procedures. It was noted that the operability test of the automatic

fire and smoke detectors did not meet the frequency listed by the UFSAR.

b UFSAR Section 98.C.1.1.2 requires accessible smoke detectors to be ,

demonstrated operable once per six months. The licensee had recently

, changed this test requirement. The new test requirement was to

demonstrate fire and smoke detector operability once per two years.

The licensee provided two 10 CFR 50.59 Evaluation Reports. Diesel

i Building Fire Detector Surveillance Frequency Revision dated September

i 24, 1996, and Change for Frequency of Smoke Detector Testing dated

i November 21, 1995. These evaluations used past satisfactory test

a

results and the bench test, sensitivity calibration and enhanced

cleaning and maintenance program performed on each detector every two l

years as justification for changing the test frequency. In addition,

the evaluation indicated that trending of the detector test program and

,

failures were to be monitored. If the failure rate increased, the two

-year test frequency would be adjusted accordingly to ensure that

i adequate reliability of the fire detection system was maintained.

.

Tharefore, the justification provided to change the testing frequency

from six months to two years was appropriate.

. c. Conclusion

,  ;

.

The surveillance and tests of the fire protection systems and features

met the frequencies specified by UFSAR Section 9B A)pendix C except for

the functional operability test of the fire and smote detector

instrumentation. The frequency of these tests was recently changed from

six months to two years. The evaluation performed by the licensee to

justify this change was appropriate.

.

l F3 Fire Protection Procedures and Documentation

.

a. Insoection Scooe (IP 64704)

a

'

The following Station Administration Procedure and Fire Protection

Procedures were reviewed for compliance with the NRC requirements and

guidelines:

-

FNP-0-A0P-29.0 Revision 13. Plant Fires

-

FNP-0-EIP-13. Revision 14. Fire Emergencies

-

FNP-0-EIP-3401. Revision 3. Transient Fire Load Analysis

,

-

FNP-0-AP-35. Revision 20. General Housekeeping and Cleanliness

Control

4

Enclosure 2

.

,

--

. . - _ _ _ _ _ _ _ . ~ . _ . _ _ . _ . - . _ _ _ . _ . - . _ _ . _ .

. .

-

L

41

-

FNP-0-AP-36. Revision 12. Fire Surveillance Procedures and

Inspections ,

-

' FNP-0-AP-37. Revision ll, Fire Brigade Organization

-

FNP-0-AP-38. Revision 10 Use of Open Flame

-

FNP-0-AP-39. Revision 12. Fire Patrols and Watches.

-

FNP-0-AP-45, Revision 15. Training Plan

Appendix P. Fire Brigade Training Program

Appendix 0 Fire Brigade Retraining Program *

-

FNP-0-AP-63. Revision 5, Conduct of Operations. Engineering

L Support Department. Section 2.1.4 Fire Protection Program ,

l Plant tours were performed to assess procedure compliance.

l

b. Observations and Findinas

The above procedures established the administrative guidance used to

implement the fire protection program at Farley and included the

requirements for the control of combustibles, ignition sources and fire

l brigade organization and training. The procedures met the intent of the

l NRC reauirements.

-

l The operability, surveillance and test requirements for the fire

protection systems and features had been removed from the TSs and

incorporated into UFSAR Section 9B Attachment C. These requirements met

, the requirements for the fire protection features which were formerly in

! the TSs. except for the testing of the fire detection system as

! discussed in Section F2.2. However, an appropriate evaluation had been

l provided to justify this change.

i

The inspector performed plant tours and noted that the general

l housekeeping related to the control of combustibles within the plant and

l implementation of the other fire prevention procedure requirements were

l satisfactory.

l

L c. Conclusions

l

, The fire protection program implementing procedure met the intent of the

l NRC guidelines and requirements. Implementation of the fire protection

l and prevention procedures and the general housekeeping for control of

l combustibles within the plant were satisfactory.

,

l'

! Enclosure 2

. - . .-

_ __

,

.

' .

,

42

F5 - Fire Protection Staff Training and Qualification

a. Insoection Scooe (IP 64704)

The inspector reviewed the fire brigade organization and training for

compliance with the facility's fire protection program and the NRC

guidelines and requirements and witnessed a fire brigade drill.

b. Observations and Findinas

The organization and-training requirements for the Farley plant fire

brigade were established by Procedure FNP-0-AP-37, Fire Brigade

Organization, Revision 11. The fire brigade for each operational shift

was composed of a fire brigade leader (operations shift foreman) and

three brigade members (non-licensed system operators) from operations

and one brigade member from security. The fire brigade leader was l

normally a licensed SRO. Each fire brigade member was required to '

receive initial, quarterly and annual fire fighting related training and

satisfactorily com)lete an annual medical evaluation to certify

participation in tie fire brigade. There were a total of 104 operations

personnel and 24 security personnel on the plant's fire brigade. j

The inspector reviewed the Training Department's training summary  ;

records and verified -that the training for the fire brigade personnel  ;

was up to date. A minimum of six drills were performed each quarter. and i

scheduled such that each fire brigade member attended at least two

~ drills per year. Most of the fire brigade drills had been unannounced

drills.

On November 13 the inspector witnessed a fire brigade drill involving a

simulated fire at the fire pumps' diesel fuel tank and fire pump house.

The fire brigade leader and four fire brigade members responded in full

fire fighting turnout gear. Personnel from HP and operations also ,

responded to the drill. The action by-the brigade met the established ,

drill objectives, except for some minor problems encountered with self

However, additional e

contained breathing apparatus.available if this equipment had actually been

was conducted with the fire brigade members following the drill.

c. Conclusions i

The fire brigade organization and training met the facility's procedure

requirements and the performance by the fire brigade to a drill during

this inspection was good.  ;

.

Enclosure 2

'

.

'

.

.

43

F6 Fire Protection Organization and Administration

a. Insoection Scope (IP 64704)

The licensee's management and administration of the facility's fire

protection program were reviewed for compliance with the commitments to

the NRC and to current NRC guidelines

b. Observations and Findinas

The Plant Operations Assistant General Manager was designated as the

onsite manager responsible for the administration and implementation of

the fire protection program. The daily control of the fire protection

]rogram was assigned to the station Fire Marshal who reported to the

Engineering Support Supervisor under the management of the Engineering

Support Manager and the Plant Support Assistant General Manager.

Most of the surveillance ins)ections and tests corrective and

preventive maintenance for t1e fire protection systems and features were

provided by a designated maintenance team composed of three mechanical.

three electrical, and one I&C maintenance craft personnel, and two

system operators (non-licensed operators). This maintenance team worked

primarily on fire protection systems and other plant support systems

such as heating and ventilation components and was under the supervision

of the Maintenance Manager. The Fire Marshal reviewed all completed

surveillance and test 3rocedures and coordinated the maintenance work

activities to assure tlat appropriate inspections, tests and maintenance

were performed. Engineering technical support was provided as needed

from the engineering personnel on site and from the corporate office

staff in Birmingham. Alabama.

The responsibility for the fire brigade training was assigned to a fire

brigade training instructor in the Training Department.

There did not appear to be a formal program for trending fire protection

condition reports and performance of fire protection system te. sting.

However. periodic informal interface between the Fire Marshal and

various personnel assigned fire protection related functions was being

made to coordinate the implementation of the fire protection program.

c. Conclusions

The coordination and oversight of the facility's fire protection program

met the licensee's commitments to the NRC in the UFSAR. The personnel

assigned various fire protectico related functions were working together

as a team and with coordination by the Fire Marshal to implement the

fire protection program at the site.

Enclosure 2

-_ _ __ .. ._ _ . _ . . ___ . _ _ _ . - . _m.__ ._. _ _ _ _ _ . _ . _ _ . _

,

  • .

44  :

F7 Quality Assurance in Fire Protection Activities

a. Insoection Scooe (IP 64704)

The following quality assurance (0A) audit reports were reviewed:  ;

,

Audit dated 8/24/89 Station Fire Protection Annual / Triennial

Audit 1

Audit dated 5/30/90 Station Fire Protection Annual Audit

i

Audit dated 8/3/92 Station Fire Protection

Annual / Biannual / Triennial Audit

Audit dated 3/30/93 Station Fire Protection Annual / Triennial

Audit

Audit dated 5/17/94 Station Fire Protection Biannual Audit

Audit dated 8/19/94 Station Fire Protection Annual Audit

Audit dated 8/10/95 Station Fire Pr c'J

Annual / Biannual /Trienn.ai Audit

Audit dated 7/22/96 Station Fire Protection Annual Audit

b. Observations and Findinos

These audits were thorough and identified a number of findings.

recommendations and comments for program enhancements. A different

independent fire protection specialist was provided for each of the

audits. This provided different perspectives of the fire protection

program. The corrective actions taken on each of the audit findings,

recommended enhancements and comments from each 0A report were reviewed

by the inspector. The corrective actions for major discrepancies or

findings were found to have been completed in a timely manner. However,

action on the recommendations and comments which were made to enhance

the program were not addressed in a timely manner. Three of five

enhancement items in the 1993 audit, three of five in the 1995 audit and

two of five from the 1996 audits had not been completed. A formal

program was only provided to track the completion of the corrective

actions for major discrepancies.

c. Conclusions

The audits and assessments of the facility's fire protection program

were thorough and corrective actions were taken in a timely manner to

resolve major identified discrepancies. However, resolution on

recommendations and comments to enhance the fire protection program was

not timely.

Enclosure 2

. . - - . - . . = - - - - - - - - - - - - - . - . - - . ~ -. .-.. - . -

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45

i

j F8 Miscellaneous Fire Protection. Issues (IP 92904)

.

F8.1. Fire Protection Related NRC ins

} a. Insoection ScoDe

3

!

The inspector reviewed the licensee's evaluation for the following NRC

,

ins:

!

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IN 92-18. Potential Loss of Shutdown Capacity During a Control

Room Fire

]

j -

IN 92-28. Inadequate Fire Suppression System Testing

,

-

IN 93-41. One Hour Fire Endurance Tests Results for Thermal

i Ceramics, 3M Company FS-195 and 3M Company Interam e-50 Fire

Barrier Systems

IN 94-28. Potential Problems with Fire Barrier Penetration Seals

-

-

j -

IN 94-31. Potential Failure of WILCO LEXAN-Type HN-4-L. Fire Hose

i Nozzles

I

l

.

IN 94-58. Reactor Coolant Pump Lube Oil Fire

!

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IN 95-36. Emergency Lighting

b. Observations and Findinas

l

i The evaluations for these ins were. appropriate and the appropriate

actions had been completed, except for IN 93-41 and IN 95-36.

IN 93-41. One Hour Fire Endurance Tests Results for Fire Barrier Systems

l

~

A review of the licensee's evaluation of the Kaowool one hour fire

, barriers installed at Farley found that these barriers did not meet the

!

'

NRC guidelines of Generic Letter 86-10 Su]plement 1. The princi)le

deviations from the NRC guidelines were: (aowool was not tested Jy an

j independent laboratory in an approved large scale furnace, temperature

measured on the external raceway exceeded 165 C [ tested raceways were

l approximately 426 C]. cable was damaged oy the fire tests, tested

'

configurations did not match in plant installations, and fire barriers

! were not subjected to a hose stream test after the fire test.

. Therefore, the adequacy of the installed fire barriers at Farley is

, being reevaluated by the NRC. This issue was previously identified as

! URI 50-348, 364/96-09-08 and remains open pending completion of the

NRC's reevaluation.

!

4

Enclosure 2

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IN 95-36. Emeraency Liahtina

The licensee was reevaluating this IN due to recent problems with the

Appendix R. 8-hour emergency lighting units. The licensee's

reevaluation of this IN will be reviewed during a subsequent NRC

inspection.

l

c. Conclusions

The evaluations and the actions taken on the reviewed ins were

appropriate, except for IN 93-41. An URI was identified for IN 93-41

concerning the adequacy of the one hour Kaowool fire barriers. The

licensee was reevaluating IN 95-36 for applicability at Farley.

V. Manaaement Meetinas and Other Areas

X1 Review of UFSAR Commitments

A recent discovery of a licensee o)erating their facility in a manner

contrary to the UFSAR description lighlighted the need for a special

focused review that compares plant practices, procedures and/or

parameters to the UFSAR descriptions. While performing the inspections

discussed in this report, the inspector reviewed the applicable portions

of the UFSAR that related to the areas inspected. The inspectors

verified that the UFSAR wording was consistent with observed plant

practices, procedures and/or parameters. Only one exception was

identified, as follows:

e UFSAR Appendix 3K, High Energy Line Break (Outside Containment),

provides no description of the pressure differential switch high

detectors identified in TS 3.3.3.7 for High Energy Line Break

(HELB) Isolation Sensors. Inspection followup of the licensee

resolution of this omission is identified as IFI 50-348, 364/96-

13-07. Certain HELB Isolation Sensors Not Described In UFSAR.

X2 Exit Meeting Summary

The resident inspectors presented the inspection results to members of

licensee management on November 27. 1996, after the end of the i

inspection period. The licensee acknowledged the findings presented. - i

The resident inspectors asked the licensee whether any materials

examined during the inspection should be considered proprietary. No

proprietary information was identified.

Enclosure 2

I

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.m%.- p .y ,. . a

<--eq~ay w , w,-, --

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l 47

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PARTIAL' LIST OF PERSONS CONTACTED ,

!

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l Licensee

.

W. Bayne. Chemistry / Environmental Superintendent

R. Coleman Maintenance Manager

S. Fulmer. Technical Manager

H. Garland. Assistant Maintenance Manager

D. Grissette. Operations Manager

R. Hill, General Manager - Farley Nuclear Plant

R. Martin. Su)erintendent Operations Support

M. Mitchell, iealth Physics Superintendent

R. Monk. Engineering Support Supervisor - Equipment Evaluation

C. Nesbit. Assistant General Manager - Support

J. Odom. Superintendent Unit 1 Operations

l J. Powell. Superintendent Unit 2 Operations

l L. Stinson. Assistant General Manager - Plant Operations

l

J. Thomas. Engineering Support Manager

-

B. Yance. Plant Modifications and Maintenance Support Manager

W. Warren. Engineering Support Supervisor - Performance Review

l G. Waymire. Safety Audit and Engineering Review Site Supervisor

1

l NRC

J. Zimmerman Project Manager - Farley Nuclear Plant j

INSPECTION PROCEDURES USED I

!  ;

l IP 37550: Engineering

IP 37551: Onsite Engineering

IP 40500: Effectiveness of Licensee Controls in Identifying. Resolving, and l

Preventing Problems  !

IP 60710: Refueling Activities '

IP 61726: Surveillance Observations i

l IP 62703: Maintenance Observations  !

l .IP 62707: Maintenance Observations

IP 64704: Fire Protection / Prevention Program

IP 71707: Plant Operations

IP 71750: Plant Support Activities

IP 73753: Inservice Ins)ection '

IP 83750: Occupational Radiation Exposure

IP 84750: Radioactive Waste Treatment. and Effluent and Environmental

Monitoring

IP 92901: Followup - Operations

i IP 92902: Followup - Maintenance

'

IP 92903: Followup - Engineering

IP 92904: Followup - Plant Support

i

Enclosure 2

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_m ._- -- - _, _ _ - . _ _ , - - . - - -m,. _, . _ _ _ , ,,

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! 48

i ITEMS OPENED, CLOSED, AND DISCUSSED

?

! Ooened  :

i .

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T.ygg Item Number

_ Status Description and Reference

! URI 50-364/96-13-01 Open PRF Operability Requirements for SFP

(Section 02.6). i

'

IFI 50-364/96-13-02 Open Increased Frequency Test Program for

Charging Pumps due to Cladding

l Cracking (Section M1.5).

3

IFI 50-348. 364/96-13-03 Open - Foreign Material From Seal . Injection

System To RCP Seals (Section M1.10).

URI 50-348, 364/96-13-04 Open Common Tap For SG Steam Flow

, Transmitter And SG Narrow Range

Water Level System Fails To Meet

j IEEE-279 (Section E1.3).

,

VIO 50-348, 364/96-13-05 Open Failure to Follow Radiation Work

{ Permit For Use of Proper Protective

j Clothing (Section R1.1).

) VIO 50-348, 364/96-13-06 Open Failure To Search Truck Trailer

j Prior To Entering Protected Area

(Section S8.1).

IFI 50-348, 364/96-13-07 Open Certain HELB Isolation Sensors Not

Described In UFSAR (Section X1). i

\

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Closed

l Tygg Item Number Status Descriotion and Reference

?

LER 50-348/95-10 Closed Actuation of Engineered Safety

, Feature Equipment Due to Loss of

3 Main Feedwater (Section 08.1).  ;

LER 50-364/95-08 Closed Reactor Trip During DEH Card

j Changeout (Section M8.1).  !

1

1 IFI 50-348, 364/94-28-01 Closed Evaluation of Settings for Copes-

Vulcan MOVs 8811A/8 and 8812A/8

Using the EPRI PPP Model (Section

, E8.1).

!

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Enclosure 2 i

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,. _ _ , _ _ _ _ ____._._ _ _._ _ - -----._ - -.

y

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49

IFI 50-348, 364/94-28-02 Closed Evaluation of Settings for  ;

4

Westinghouse Unit 2 MOV 8811A Using '

] the EPRI PPP Model (Section E8.2).

,

j IFI 50-348, 364/94-28-03 Closed Evaluation of Settings for Pratt-

4 Butterfly MOVs 'Using the EPRI PPP

j.

Model (Section E8.3).

! LER 50-348, 364/95-06 Closed Licensed Material Ship)ed to

! Incorrect Destination ]y Common

! Carrier (Section R8.1).

i URI 50-348. 364/96-09-05 Closed Failure to Search Contractor Trailer

Prior to Entry Into the Protected-

Area (Section S8.1).

1

,

Discussed

!-

i 1322 Item Number Status pescriotion and Reference

!

' 50-348, 364/96-02-03

IFI Open Pre-action sprinkler system failures

l

4

(Section F2.1).

h

i URI 50-348, 364/96-09-08 Open Adequacy of Kaowool qualification

j tests to scope installed

-

,

configurations (Section F8.1). '

i

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i: Enclosure 2

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50

LIST OF ACRONYMS USED

ALARA As low As Reasonably Achievable

ALM Automated u undry Monitor

Bhp Brake Horsepower

BIT Boron Injection Tank

BRT Bottom of Rolled Transition

CCW Component Cooling Water

CFR Code of Federal Regulations

CIR Chemistry Incident Report

CO, Carbon Dioxide

DAD Digital Alarming Dosimeter

DCP Design Change Package

EDG Emergency Diesel Generator

EPB Emergency Power Board

EPRI Electric Power Research Institute

E0 Environmentally Qualified

ETP Engineering Test Procedure

FCV Flow Control Valve

FNP Farley Nuclear Plant

HELB High Energy Line Break l

HP Health Physics I

HX Heat Exchanger  !

IAW In Accordance With

ID Inside Diameter

IFI Inspector Followup Item l

Information Notice

'

IN

IP Inspection Procedure

IPE Individual Plant Examination

IR Inspection Report

ISI Inservice Inspection

IST Inservice Test

LCO Limiting Condition for Operation

LER Licensee Event Report

LOSP Loss of Offsite Power i

MCB Main Control Board

MCR Main Control Room

MOV Motor Operated Valve

mrem millirem

MS Main Steam

NORB Nuclear Operations Review Board

NRC U.S. Nuclear Regulatory Commission

ODCM Offsite Dose Calculation Manual

00S Out of Service

OR Occurrence Report

PA Protected Area

PAHA Post-Accident Hydrogen Analyzers

PCE Personnel Contamination Event

PDR Public Document Room

. pH The negative logarithm of the hydrogen concentration.

Enclosure 2

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PPP Performance Prediction Program

PPR Piping Penetration Room

PRF Penetration Room Filtration

OA Quality Assurance i

Radwaste Radioactive Waste  !

RCA Radiologically Controlled Area

RCP Reactor Coolant Pump

RCS Reactor Coolant System

RE Radiation Element

RG Regulatory Guide

RHR Residual Heat Removal

RMS Radiation Monitoring System

RP&C Radiological Protection and Chemistry

RPC Rotating Pancake Coil i

RWP Radiation Work Permit l

RWST Refueling Water Storage Tank l

RxxCxx SG tube location (e.g. R20C26 - Row 20 Column 26) l

SAER Safety Audit and Engineering Review

SB0 Station Blackout

SFP Spent Fuel Pool

SG Steam Generator

SI Safety Injection

SNC Southern Nuclear Operating Company

SOP System Operating Procedure

SRO Senior Reactor Operator

SS Shift Supervisor

STP Surveillance Test Procedure

SW Service Water

TDAFW Turbine Driven Auxiliary Feedwater

TEDE Total Effective Dose Equivalent

TLD Thermoluminescent Dosimeter

TO Tag Order

TS Technical Specifications

U2RF11 Unit 2 eleventh refueling outage

UFSAR Updated Final Safety Analysis Report

UOP Unit Operating Procedure

URI Unresolved Item

UT Ultrasonic Testing

UTEC Ultrasonic Examination

VIO Violation

WO Work Order

YTD Year-to-Date

)

4

Enclosure 2

1

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