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Category:INSPECTION REPORT
MONTHYEARML25024A0262025-01-24024 January 2025 Notification of Comprehensive Engineering Team Inspection (05000416/2025010) and Request for Information IR 05000416/20243022025-01-22022 January 2025 NRC Initial Operator Licensing Examination Approval 05000416 2024302 IR 05000416/20244032024-12-18018 December 2024 Cyber Security Inspection Report 05000416/2024403 (Cover Letter) IR 05000416/20240032024-11-0606 November 2024 Integrated Inspection Report 05000416/2024003 IR 05000416/20240022024-10-29029 October 2024 Revised Grand Gulf Nuclear Station - Integrated Inspection Report 05000416/2024002 IR 05000416/20240112024-10-16016 October 2024 – Fire Protection Team Inspection Report 05000416/2024011 IR 05000416/20240122024-09-17017 September 2024 License Renewal Post Approval Phase 2 Inspection Report 05000416/2024012 IR 05000416/20244022024-09-0909 September 2024 Security Baseline Inspection Report 05000416/2024402 IR 05000416/20240052024-08-21021 August 2024 Updated Inspection Plan for Grand Gulf Nuclear Station (Report 05000416/2024005) ML24207A0792024-07-29029 July 2024 Integrated Inspection Report 05000416/2024002 IR 05000416/20240102024-06-27027 June 2024 Biennial Problem Identification and Resolution Inspection Report 05000416/2024010 IR 05000416/20240012024-05-0202 May 2024 Integrated Inspection Report 05000416 2024001 IR 05000416/20220042024-03-19019 March 2024 – Amended Integrated Inspection Report 05000416/2022004 and Exercise of Enforcement Discretion IR 05000416/20230062024-02-28028 February 2024 Annual Assessment Letter for Grand Gulf Nuclear Station - Report 05000416/2023006 IR 05000416/20233012024-02-26026 February 2024 NRC Examination Report 05000416-2023301 IR 05000416/20230042024-01-25025 January 2024 Integrated Inspection Report 5000416/2023004 IR 05000416/20234012024-01-18018 January 2024 Cyber Security Inspection Report 05000416/2023401 (Public) IR 05000416/20243012024-01-16016 January 2024 NRC Initial Operator Licensing Examination Approval 05000416/2024301 IR 05000416/20234032023-11-13013 November 2023 Security Baseline Inspection Report 05000416/2023403 Cover Letter IR 05000416/20230032023-11-0808 November 2023 Integrated Inspection Report 05000416/2023003 IR 05000416/20230052023-08-21021 August 2023 Updated Inspection Plan for Grand Gulf Nuclear Station (Report 05000416/2023005) IR 05000416/20230022023-08-0808 August 2023 Integrated Inspection Report 05000416/2023002 and Independent Spent Fuel Storage Installation Inspection Report 07200050/2023001 IR 05000416/20234042023-08-0707 August 2023 Material Control and Accounting Program Inspection Report 05000416/2023404 IR 05000416/20230912023-07-28028 July 2023 Final Significance Determination of a Green Finding and Notice of Violation; NRC Inspection Report 05000416/2023091 IR 05000416/20230902023-06-27027 June 2023 Public Meeting Notice: Grand Gulf Nuclear Station, Dated IR 05000416/2023090 - Preliminary White Finding Choice Letter ML23122A1632023-05-18018 May 2023 NRC Inspection Report 05000416/2023090 and Preliminary White Finding IR 05000416/20234022023-05-17017 May 2023 Security Baseline Inspection Report 05000416/2023402 IR 05000416/20230012023-05-10010 May 2023 Notice of Violation; Integrated Inspection Report 05000416/2023001 and NRC Investigation Report 4-2022-004 ML23110A8002023-05-10010 May 2023 Notice of Violation; Integrated Inspection Report 05000416/2023001 and NRC Investigation Report 4-2022-004 IR 05000416/20230112023-03-0808 March 2023 Design Basis Assurance Inspection Report 05000416/2023011 IR 05000416/20220062023-03-0101 March 2023 Annual Assessment Letter for Grand Gulf Nuclear Station Report 05000416/2022006 ML23026A0952023-02-0101 February 2023 Integrated Inspection Report 05000416/2022004 IR 05000416/20224022023-01-17017 January 2023 Security Baseline Inspection Report 05000416/2022402 (Cover Letter) IR 05000415/20223012022-12-19019 December 2022 NRC Examination Report 05000415/2022301 IR 05000416/20220032022-11-0303 November 2022 Integrated Inspection Report 05000416/2022003 IR 05000416/20224032022-11-0101 November 2022 Security Baseline Inspection Report 05000416 2022403 (Cover Letter Only) IR 05000416/20220132022-10-24024 October 2022 Revised Grand Gulf Nuclear Station Design Basis Assurance Inspection Report 05000416/2022013 IR 05000416/20220502022-10-20020 October 2022 Special Inspection Reactive Report 05000416/2022050 ML22280A0292022-10-11011 October 2022 Design Basis Assurance Inspection (Programs) Inspection Report 05000416/2022013 IR 05000416/20223012022-09-30030 September 2022 NRC Initial Operator Licensing Examination Approval 05000416/2022301 IR 05000416/20220052022-08-18018 August 2022 Updated Inspection Plan for Grand Gulf Nuclear Station (Report 05000416/2022005) IR 05000416/20220022022-08-11011 August 2022 Integrated Inspection Report 05000416/2022002 IR 05000416/20220112022-06-0606 June 2022 Biennial Problem Identification and Resolution Inspection Report 05000416/2022011 IR 05000416/20220012022-05-0909 May 2022 Integrated Inspection Report 05000416/2022001 IR 05000416/20220122022-04-20020 April 2022 License Renewal Phase 1 NRC Inspection Report 05000416/2022012 IR 05000416/20210062022-03-0202 March 2022 Annual Assessment Letter for Grand Gulf Nuclear Station (Report 05000416/2021006) IR 05000416/20210042022-02-0808 February 2022 Integrated Inspection Report 05000416/2021004 IR 05000416/20214202022-02-0707 February 2022 Cover Letter for Grand Nuclear Station, Unit 1 Security Baseline Inspection Report 05000416/2021420 IR 05000416/20200132022-02-0303 February 2022 Amended - Grand Gulf Nuclear Station - Triennial Fire Protection Inspection Report 05000416/2020013 and Notice of Violation ML22011A0992022-01-14014 January 2022 IR 2021012 EOI CO3 2025-01-24
[Table view] Category:NRC-GENERATED
MONTHYEARIR 05000416/19990121999-09-29029 September 1999 Insp Rept 50-416/99-12 on 990725-0904.Violations Noted.Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000416/19990111999-09-28028 September 1999 Insp Rept 50-416/99-11 on 990830-0903.No Violations Noted. Major Areas Inspected:Solid Radioactive Waste Management Program,Radioactive Matl Transportation Program,Facilities & Equipment,Staff Knowledge & Performance & Staff Training IR 05000416/19990141999-09-27027 September 1999 Insp Rept 50-416/99-14 on 990830-0903.No Violations Noted. Major Areas Inspected:Implementation of Liquid & Gaseous Radioactive Waste Effluent Mgt Program & Status of Effluent Radiation Monitors & Counting Room Instruments IR 05000416/19990151999-09-13013 September 1999 Partially Withheld Insp Rept 50-416/99-15 on 990816-20. Noncited Violation Noted.Major Areas Inspected:Licensee Physical Security Program,Personnel Access Control,Access Authorization & Protected Area Detection Aids IR 05000416/19990101999-08-24024 August 1999 Insp Rept 50-416/99-10 on 990809-13.No Violations Noted. Major Areas Inspected:Licensed Operator Requalification Program IR 05000416/19990091999-08-0909 August 1999 Insp Rept 50-416/99-09 on 990613-0724.No Violations Noted. Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000416/19990031999-07-30030 July 1999 Insp Rept 50-416/99-03 on 990405-08 & 0510-11.No Violations Identified.Major Areas Inspected:Corrective Action Program Implementation IR 05000416/19990071999-07-23023 July 1999 Insp Rept 50-416/99-07 on 990622-25.Violations Noted.Major Areas Inspected:Announced Insp of Licensee Performance & Capabilities During full-scale,biennial Exercise of Emergency Plan & Implementing Procedures Performed IR 05000416/19990081999-07-15015 July 1999 Insp Rept 50-416/99-08 on 990502-0612.Violations Noted.Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000416/19990051999-06-27027 June 1999 Insp Rept 50-416/99-05 on 990321-0501.Violations Identified, Being Treated as non-cited Violations.Major Areas Inspected: Aspects of Licensee Operations,Maint,Engineering & Plant Support IR 05000416/19990061999-05-21021 May 1999 Insp Rept 50-416/99-06 on 990419-23.No Violations Noted. Major Areas Inspected:Licensee Implementation of NRC Approved Fire Protection Program IR 05000416/19990021999-05-18018 May 1999 Insp Rept 50-416/99-02 on 990222-26 & 0308-12.Non-cited Violations Noted.Major Areas Inspected:Engineering IR 05000416/19990041999-04-23023 April 1999 Insp Rept 50-416/99-04 on 990131-0320.Violations Noted. Major Areas Inspected:Operation,Maintenance,Engineering & Plant Support IR 05000416/19990011999-02-26026 February 1999 Insp Rept 50-416/99-01 on 990201-05.Violations Noted. Major Areas Inspected:Plant Support.Violation of TS 5.7.2 Identified for Failure to Control Locked High Radiation Area Around Spent Fuel Pool Cooling & Cleanup HX IR 05000416/19980151999-01-20020 January 1999 Insp Rept 50-416/98-15 on 981101-1212.No Violations Noted. Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Suuport IR 05000416/19980161998-12-24024 December 1998 Insp Rept 50-416/98-16 on 981207-11.Violations Noted.Major Areas Inspected:Operational Status of Licensee Emergency Preparedness Program Was Conducted ML20196F1271998-12-0101 December 1998 Insp Rept 50-416/98-13 on 980920-1031.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000416/19980141998-11-27027 November 1998 Insp Rept 50-416/98-14 on 981026-30.No Violations Noted. Major Areas Inspected:Exposure Controls,Controls of Radioactive Matls & Contamination,Surveying & Monitoring & Quality Assurance Oversight of Radiation Protection Program IR 05000416/19980111998-10-14014 October 1998 Insp Rept 50-416/98-11 on 980809-0919.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000416/19980121998-09-15015 September 1998 Insp Rept 50-416/98-12 on 980817-20.No Violations Noted. Major Areas Inspected:Training,Qualifications,Quality Assurance Oversight,Facilities & Equipment & Annual Reports IR 05000416/19980031998-09-0909 September 1998 Insp Rept 50-416/98-03 Cancelled IR 05000416/19980091998-08-31031 August 1998 Insp Rept 50-416/98-09 on 980628-0808.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000416/19980101998-08-26026 August 1998 Insp Rept 50-416/98-10 on 980803-07.No Violations Noted. Major Areas Inspected:Licensee Physical Security Program IR 05000416/19980081998-07-14014 July 1998 Insp Rept 50-416/98-08 on 980517-0627.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000416/19980071998-06-0202 June 1998 Insp Rept 50-416/98-07 on 980518-21.No Violations Noted. Major Areas Inspected:Access Authorization,Alarm Stations, Communications,Access Control of Packages & Vehicles, Assessment Aids & Mgt Support IR 05000416/19980051998-05-28028 May 1998 Insp Rept 50-416/98-05 on 980405-0516.Violations Noted.Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000416/19980061998-05-19019 May 1998 Insp Rept 50-416/98-06 on 980427-0501.No Violations Noted. Major Areas Inspected:Radiation Protection Activities in Support of 1998 Refueling Outage IR 05000416/19980041998-05-0505 May 1998 Insp Rept 50-416/98-04 on 980414-16.No Violations Noted. Major Areas Inspected:Maint & Plant Support IR 05000416/19983011998-04-16016 April 1998 Insp Rept 50-416/98-301 on 980330-0403.No Violations Noted. Major Areas Inspected:Competency of Reactor Operator & Eight Senior Applicants for Issuance of OLs at Grand Gulf Nuclear Station IR 05000416/19980021998-04-15015 April 1998 Insp Rept 50-416/98-02 on 980222-0404.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000416/19980011998-03-0404 March 1998 Insp Rept 50-416/98-01 on 980111-0221.No Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000416/19970221997-12-15015 December 1997 Insp Rept 50-416/97-22 on 971130-980110.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering IR 05000416/19970211997-12-0505 December 1997 Insp Rept 50-416/97-21 on 971019-1129.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000416/19970181997-11-25025 November 1997 Insp Rept 50-416/97-18 on 970804-22.Violations Noted.Major Areas Inspected:Operations & Maint.Nrc IP 40500 Used to Evaluate Licensee Effectiveness in Identifying,Resolving & Preventing Issues That Degrade Quality of Plant Operations IR 05000416/19970201997-10-31031 October 1997 Insp Rept 50-416/97-20 on 970907-1018.Violations Noted.Major Areas Inspected:Operations,Maint & Plant Support Re Emergency Post Accident Sampling Sys Drill IR 05000416/19970161997-10-23023 October 1997 Insp Rept 50-416/97-16 on 970929-1003.No Violations Noted. Major Areas Inspected:Review of Licensed Operator Requalification Program Following Guidelines in IP 71001 IR 05000416/19970151997-10-0909 October 1997 Insp Rept 50-416/97-15 on 970916-19.Three Weaknesses Noted During Exercise.Major Areas Inspected:Licensee Performance & Capabilities During full-scale,biennial Exercise of Emergency Plan & Implementing Procedures IR 05000416/19970071997-10-0101 October 1997 Informs That Insp Rept 50-416/97-07 Has Been Cancelled & There Will Be No Insp Issued for This Rept Number IR 05000416/19970171997-09-0505 September 1997 Insp Rept 50-416/97-17 on 970804-08.No Violation Noted.Major Areas Inspected:Implementation of Solid Radwaste Mgt & Radioactive Matls Transportation Programs IR 05000416/19970131997-08-0606 August 1997 Partially Withheld Insp Rept 50-416/97-13 on 970714-18 (Ref 10CFR73.21).Violations Noted.Major Areas Inspected: Licensee Physical Security Program,Including Review of Records,Repts,Testing,Maint & Assessment Aids IR 05000416/19970141997-08-0505 August 1997 Insp Rept 50-416/97-14 on 970714-17.Violations Noted. Major Areas Inspected:Plant Support & Program to Maintain Occupational Exposures ALARA & Training & Qualifications of Members of Radiation Protection Organization IR 05000416/19970091997-07-16016 July 1997 Insp Rept 50-416/97-09 on 970623-27.No Violations Noted. Major Areas Inspected:Emergency Plan & Implementing Procedures,Emergency Facilities & Equipment,Organization & Mgt Control,Training & Audits IR 05000416/19970101997-07-0202 July 1997 Insp Rept 50-416/97-10 on 970602-05.No Violations Noted. Major Areas Inspected:Plant Support Including Liquid & Gaseous Radwaste Effluent Mgt Program,Radiological Environ Program & Meteorological Monitoring Program IR 05000416/19970111997-06-25025 June 1997 Partially Withheld Insp Rept 50-416/97-11 on 970602-06 (Ref 10CFR73.21).No Violations Noted.Major Areas Inspected: Licensee Physical Security Program,Including Records,Repts, Testing & Maint,Vital Area Barriers & Security Audit IR 05000416/19970051997-05-29029 May 1997 Insp Rept 50-416/97-05 on 970310-27.Violations Noted.Major Areas Inspected:Licensee Operations & Engineering Procedures IR 05000416/19970061997-05-27027 May 1997 Insp Rept 50-416/97-06 on 970323-0510.Violations Noted.Major Areas Inspected:Licensee Operations,Including Emergency Procedure,Maint,Engineering & Plant Support ML20140E6411997-04-24024 April 1997 Insp Rept 50-416/97-03 on 970209-0322.Violations Noted.Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support Activities IR 05000416/19960211997-02-25025 February 1997 Insp Rept 50-416/96-21 on 961221-970208.No Violations Noted. Major Areas Inspected:Operations,Maintenance,Surveillance, Engineering & Plant Support IR 05000416/19970021997-02-19019 February 1997 Insp Rept 50-416/97-02 on 970203-07.No Violations Noted. Major Areas Inspected:External & Internal Exposure Control Programs,Calibration of Portable Radiation Protection Instrumentation & Whole Body Counting Equipment IR 05000416/19960201997-01-0808 January 1997 Insp Rept 50-416/96-20 on 961110-1221.No Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support 1999-09-29
[Table view] Category:INSPECTION REPORT
MONTHYEARML25024A0262025-01-24024 January 2025 Notification of Comprehensive Engineering Team Inspection (05000416/2025010) and Request for Information IR 05000416/20243022025-01-22022 January 2025 NRC Initial Operator Licensing Examination Approval 05000416 2024302 IR 05000416/20244032024-12-18018 December 2024 Cyber Security Inspection Report 05000416/2024403 (Cover Letter) IR 05000416/20240032024-11-0606 November 2024 Integrated Inspection Report 05000416/2024003 IR 05000416/20240022024-10-29029 October 2024 Revised Grand Gulf Nuclear Station - Integrated Inspection Report 05000416/2024002 IR 05000416/20240112024-10-16016 October 2024 – Fire Protection Team Inspection Report 05000416/2024011 IR 05000416/20240122024-09-17017 September 2024 License Renewal Post Approval Phase 2 Inspection Report 05000416/2024012 IR 05000416/20244022024-09-0909 September 2024 Security Baseline Inspection Report 05000416/2024402 IR 05000416/20240052024-08-21021 August 2024 Updated Inspection Plan for Grand Gulf Nuclear Station (Report 05000416/2024005) ML24207A0792024-07-29029 July 2024 Integrated Inspection Report 05000416/2024002 IR 05000416/20240102024-06-27027 June 2024 Biennial Problem Identification and Resolution Inspection Report 05000416/2024010 IR 05000416/20240012024-05-0202 May 2024 Integrated Inspection Report 05000416 2024001 IR 05000416/20220042024-03-19019 March 2024 – Amended Integrated Inspection Report 05000416/2022004 and Exercise of Enforcement Discretion IR 05000416/20230062024-02-28028 February 2024 Annual Assessment Letter for Grand Gulf Nuclear Station - Report 05000416/2023006 IR 05000416/20233012024-02-26026 February 2024 NRC Examination Report 05000416-2023301 IR 05000416/20230042024-01-25025 January 2024 Integrated Inspection Report 5000416/2023004 IR 05000416/20234012024-01-18018 January 2024 Cyber Security Inspection Report 05000416/2023401 (Public) IR 05000416/20243012024-01-16016 January 2024 NRC Initial Operator Licensing Examination Approval 05000416/2024301 IR 05000416/20234032023-11-13013 November 2023 Security Baseline Inspection Report 05000416/2023403 Cover Letter IR 05000416/20230032023-11-0808 November 2023 Integrated Inspection Report 05000416/2023003 IR 05000416/20230052023-08-21021 August 2023 Updated Inspection Plan for Grand Gulf Nuclear Station (Report 05000416/2023005) IR 05000416/20230022023-08-0808 August 2023 Integrated Inspection Report 05000416/2023002 and Independent Spent Fuel Storage Installation Inspection Report 07200050/2023001 IR 05000416/20234042023-08-0707 August 2023 Material Control and Accounting Program Inspection Report 05000416/2023404 IR 05000416/20230912023-07-28028 July 2023 Final Significance Determination of a Green Finding and Notice of Violation; NRC Inspection Report 05000416/2023091 IR 05000416/20230902023-06-27027 June 2023 Public Meeting Notice: Grand Gulf Nuclear Station, Dated IR 05000416/2023090 - Preliminary White Finding Choice Letter ML23122A1632023-05-18018 May 2023 NRC Inspection Report 05000416/2023090 and Preliminary White Finding IR 05000416/20234022023-05-17017 May 2023 Security Baseline Inspection Report 05000416/2023402 IR 05000416/20230012023-05-10010 May 2023 Notice of Violation; Integrated Inspection Report 05000416/2023001 and NRC Investigation Report 4-2022-004 ML23110A8002023-05-10010 May 2023 Notice of Violation; Integrated Inspection Report 05000416/2023001 and NRC Investigation Report 4-2022-004 IR 05000416/20230112023-03-0808 March 2023 Design Basis Assurance Inspection Report 05000416/2023011 IR 05000416/20220062023-03-0101 March 2023 Annual Assessment Letter for Grand Gulf Nuclear Station Report 05000416/2022006 ML23026A0952023-02-0101 February 2023 Integrated Inspection Report 05000416/2022004 IR 05000416/20224022023-01-17017 January 2023 Security Baseline Inspection Report 05000416/2022402 (Cover Letter) IR 05000415/20223012022-12-19019 December 2022 NRC Examination Report 05000415/2022301 IR 05000416/20220032022-11-0303 November 2022 Integrated Inspection Report 05000416/2022003 IR 05000416/20224032022-11-0101 November 2022 Security Baseline Inspection Report 05000416 2022403 (Cover Letter Only) IR 05000416/20220132022-10-24024 October 2022 Revised Grand Gulf Nuclear Station Design Basis Assurance Inspection Report 05000416/2022013 IR 05000416/20220502022-10-20020 October 2022 Special Inspection Reactive Report 05000416/2022050 ML22280A0292022-10-11011 October 2022 Design Basis Assurance Inspection (Programs) Inspection Report 05000416/2022013 IR 05000416/20223012022-09-30030 September 2022 NRC Initial Operator Licensing Examination Approval 05000416/2022301 IR 05000416/20220052022-08-18018 August 2022 Updated Inspection Plan for Grand Gulf Nuclear Station (Report 05000416/2022005) IR 05000416/20220022022-08-11011 August 2022 Integrated Inspection Report 05000416/2022002 IR 05000416/20220112022-06-0606 June 2022 Biennial Problem Identification and Resolution Inspection Report 05000416/2022011 IR 05000416/20220012022-05-0909 May 2022 Integrated Inspection Report 05000416/2022001 IR 05000416/20220122022-04-20020 April 2022 License Renewal Phase 1 NRC Inspection Report 05000416/2022012 IR 05000416/20210062022-03-0202 March 2022 Annual Assessment Letter for Grand Gulf Nuclear Station (Report 05000416/2021006) IR 05000416/20210042022-02-0808 February 2022 Integrated Inspection Report 05000416/2021004 IR 05000416/20214202022-02-0707 February 2022 Cover Letter for Grand Nuclear Station, Unit 1 Security Baseline Inspection Report 05000416/2021420 IR 05000416/20200132022-02-0303 February 2022 Amended - Grand Gulf Nuclear Station - Triennial Fire Protection Inspection Report 05000416/2020013 and Notice of Violation ML22011A0992022-01-14014 January 2022 IR 2021012 EOI CO3 2025-01-24
[Table view] Category:UTILITY
MONTHYEARIR 05000416/19900201990-10-30030 October 1990 Insp Rept 50-416/90-20 on 900915-1019.No Violations or Deviations Noted.Major Areas Inspected:Operational Safety Verification,Maint Observation,Surveillance Observation,Esf Sys Walkdown,Preparation for Refueling & Refueling Activity IR 05000416/19900181990-10-12012 October 1990 Insp Rept 50-416/90-18 on 900917-21.No Violations or Deviations Noted.Major Areas Inspected:Pump & Valve Inservice Testing & Followup of Previous Insp Findings IR 05000416/19900161990-10-10010 October 1990 Insp Rept 50-416/90-16 on 900827-31.No Violations or Deviations Noted IR 05000416/19900131990-08-16016 August 1990 Insp Rept 50-416/90-13 on 900709-13.Violation Noted But Not Cited.Major Areas Inspected:Radiation Protection Program in Areas of Internal & External Exposure Controls,Alara,Control of Radioactive Matls & Outage Planning IR 05000416/19900111990-07-0202 July 1990 Insp Rept 50-416/90-11 on 900519-0615.Violation Noted But Not Cited.Major Areas Inspected:Operational Safety Verification,Maint Observation,Surveillance Observation, Installation & Testing of Mods IR 05000416/19900091990-06-0101 June 1990 Insp Rept 50-416/90-09 on 900514-18.No Violations or Deviations Noted.Major Areas Inspected:Emergency Preparedness,Including Corrective Action Tracking Sys, Training & Maint of Select Emergency Kits & Equipment IR 05000416/19900081990-06-0101 June 1990 Insp Rept 50-416/90-08 on 900414-0518.Violations Noted.Major Areas Inspected:Operational Safety Verification,Maint Observation,Surveillance Observation,Surveillance Procedures & Records,Action on Previous Insp Findings & ROs IR 05000416/19900101990-05-25025 May 1990 Insp Rept 50-416/90-10 on 900507-11.No Violations Noted. Major Areas Inspected:Fire Protection/Prevention IR 05000416/19900071990-05-0202 May 1990 Insp Rept 50-416/90-07 on 900416-20.No Violations or Deviations Noted.Major Areas Inspected:Settlement of Category 1 Structures,Flood Protection,Testing of Main Steam Safety Valves & Snubber Surveillance IR 05000416/19900051990-04-30030 April 1990 Insp Rept 50-416/90-05 on 900326-30.Violation Noted Re Failure to Obtain NRC Approval for Disposal of Slightly Contaminated Licensed Matl.Major Areas Inspected:Liquid & Gaseous Radiological Effluents & Plant Chemistry IR 05000416/19900061990-04-26026 April 1990 Insp Rept 50-416/90-06 on 900317-0413.Violations Noted Re Failure to Verify Senior Operator License Application Info. Major Areas Inspected:Safety Verification,Maint Observation, Surveillance Observation & ESF Sys Walkdown IR 05000416/19900041990-04-0606 April 1990 Partially Withheld Insp Rept 50-416/90-04 on 900319-22 (Ref 10CFR2.790(d) & 73.21).No Violations or Deviations Noted. Major Areas Inspected:Physical Security Program for Power Reactors ML20042E1161990-04-0202 April 1990 Insp Rept 50-416/90-03 on 900217-0316.Violations Noted.Major Areas Inspected:Operational Safety Verification,Maint Observation,Surveillance Observation,Qa Program & Action on Previous Insp Findings & ROs IR 05000416/19900021990-03-0202 March 1990 Insp Rept 50-416/90-02 on 900120-0216.No Violations or Deviations Noted.Major Areas Inspected:Operational Safety Verification,Maint & Surveillance Observation,Independent Safety Engineering Group & ROs IR 05000416/19890301990-01-31031 January 1990 Insp Rept 50-416/89-30 on 891216-900119.Violations Noted. Major Areas Inspected:Operational Safety Verification,Maint Observation,Surveillance Observation,Action on Previous Findings & ROs IR 05000416/19900011990-01-23023 January 1990 Insp Rept 50-416/90-01 on 900108-12.No Violations or Deviations Noted.Major Areas Inspected:Core Power Distribution & Thermal Limits,Calibrs of Nuclear Instrumentation & Core Thermal Power IR 05000416/19890291990-01-0404 January 1990 Insp Rept 50-416/89-29 on 891118-1215.Violations Noted.Major Areas Inspected:Operational Safety Verification,Maint & Surveillance Observations & Evaluation of Licensee self-assessment Capability IR 05000416/19890281989-12-13013 December 1989 Insp Rept 50-416/89-28 on 891021-1117.Violations Noted. Major Areas Inspected:Operational Safety Verification,Maint & Surveillance Observation,Cold Weather Preparations,Action on Previous Insp Findings & ROs IR 05000416/19890271989-11-17017 November 1989 Insp Rept 50-416/89-27 on 890931-1020.No Violations or Deviations Noted.Major Areas Inspected:Operational Safety Verification,Maint Observation,Surveillance Observation,Esf Sys Walkdown & Action on Previous Insp Findings IR 05000416/19890241989-11-0303 November 1989 Partially Withheld Insp Rept 50-416/89-24 on 890918-22 (Ref 10CFR2.790(d) & 73.21).One Noncited Violation Noted.Major Areas Inspected:Security Plan & Implementing Procedures,Mgt Effectiveness,Records & Repts & Access Controls IR 05000416/19890251989-11-0303 November 1989 Insp Rept 50-416/89-25 on 890926-29.No Violations or Deviations Noted.Exercise Weakness Noted.Major Areas Inspected:Observation & Evaluation of Annual Emergency Exercise,Including Objectives & Scenario Events IR 05000416/19890231989-11-0101 November 1989 Corrected Insp Rept 50-416/89-23 on 890826-0930.Major Areas Inspected:Operational Safety Verification,Maint Observation, Surveillance Observation,Licensed Operator Training,Action on Previous Insp Findings & Meeting W/Local Officials ML19332C6311989-10-27027 October 1989 Undated & Unsigned Insp Rept 50-416/89-23 on 890826-0930. Violation Noted.Major Areas Inspected:Operational Safety Verification,Maint & Surveillance Observations,Licensed Operator Training,Action on Previous Insp Findings & ROs IR 05000416/19890211989-09-29029 September 1989 Insp Rept 50-416/89-21 on 890828-0901.Violations Noted.Major Areas Inspected:Emergency Preparedness,Including Maint of Select Emergency Kits & Equipment,Organizational Changes, Training & Independent Audits IR 05000416/19890181989-08-0101 August 1989 Insp Rept 50-416/89-18 on 890710-14.No Violations or Deviations Noted.Major Areas Inspected:Occupational Exposure,Shipping & Transportation & Licensee Action on Previous Insp Findings IR 05000416/19890171989-07-28028 July 1989 Insp Rept 50-416/89-17 on 890617-0714.Violations Noted.Major Areas Inspected:Operational Safety Verification,Maint Observation,Surveillance Observation,Esf Sys Walkdown,Action on Previous Insp Findings & Reportable Occurrences ML20246B2801989-06-27027 June 1989 Insp Rept 50-416/89-16 on 890520-0616.Violations Noted.Major Areas Inspected:Operational Safety Verification,Maint Observation,Surveillance Observation,Esf Sys Walkdown, 10CFR21 Procedures & Action on Previous Insp Findings IR 05000416/19890151989-06-20020 June 1989 Insp Rept 50-416/89-15 on 890530-0602.No Violations Noted. Major Areas Inspected:Onsite Followup of Facilities Recirculation Sys Pump Shaft Crack IR 05000416/19890131989-06-0505 June 1989 Insp Rept 50-416/89-13 on 890417-21.No Violations or Deviations Noted.Major Areas Inspected:Pump & Valve Inservice Testing,Ie Bulletin Followup & Followup on Previous Insp Findings ML20245F5471989-06-0505 June 1989 Insp Rept 50-416/89-14 on 890415-0519.Violations Noted.Major Areas Inspected:Operational Safety Verification,Maint Observation,Surveillance Observation,Esf Sys Walkdown,Test Piping Support & Restraint Sys & Startup from Refueling ML20244E0571989-05-24024 May 1989 Insp Rept 50-416/89-08 on 890327-31 & 0419-21.Major Areas Inspected:Radiological Controls During Present Refueling Outage & follow-up on Employee Safety Concerns & Allegations IR 05000416/19890091989-05-16016 May 1989 Partially Withheld Insp Rept 50-416/89-09 on 890417-21 (Ref 10CFR2.790(d) & 10CFR73.21).No Violations Noted.Major Areas Inspected:Security Plan & Implementing Procedures,Security Audit Program,Records & Repts,Testing & Maint,Locks & Keys IR 05000416/19890121989-04-28028 April 1989 Insp Rept 50-416/89-12 on 890318-0414.Violation Noted.Major Areas Inspected:Operational Safety Verification,Maint Observation,Surveillance Observation,Installation,Testing of Mods,Outage Organization & Reportable Occurrences IR 05000416/19890111989-04-26026 April 1989 Insp Rept 50-416/89-11 on 890410-14.No Violations or Deviations Noted.Major Areas Inspected:Inservice Insp, Including Review of Procedures,Nrc Bulletin 87-001,Generic Ltr 88-01,Info Notices 88-003 & 89-001 & Feedwater Valves ML20246H7501989-04-26026 April 1989 Insp Rept 50-416/89-10 on 890327-31.No Violations or Deviations Noted.Major Areas Inspected:Piping Sys Procedures & Calculations IR 05000416/19890071989-04-10010 April 1989 Insp Rept 50-416/89-07 on 890218-0317.No Violations or Deviations Noted.Major Areas Inspected:Operational Safety Verification,Maint & Surveillance Observation,Esf Sys Walkdown & Other Areas ML20247E7441989-03-16016 March 1989 Insp Rept 50-416/89-04 on 890114-0217.Violation Noted.Major Areas Inspected:Operational Safety Verification,Maint Observation,Surveillance Observation,Procedures & Records & Preparation for Refueling IR 05000416/19890061989-03-13013 March 1989 Insp Rept 50-416/89-06 on 890221-24.No Violations or Deviations Noted.Major Areas Inspected:Radiation Protection for Unit Refueling Outage Scheduled for 890318 IR 05000416/19890051989-03-0808 March 1989 Partially Withheld Insp Repts 50-416/89-05 & 50-417/89-05 on 890131-0201 (Ref 10CFR2.790(d) & 73.21).No Violations or Deviations Noted.Major Areas Inspected:Mgt Support,Security Program Plans & Protected Area Barriers IR 05000416/19880271989-02-27027 February 1989 Corrected Page 4 to Insp Rept 50-416/88-27 IR 05000416/19890011989-02-13013 February 1989 Insp Rept 50-416/89-01 on 890109-13.No Violations or Deviations Noted.Major Areas Inspected:Design Control,Design Changes & Mods IR 05000416/19890031989-02-10010 February 1989 Insp Rept 50-416/89-03 on 890110-12.Violations Noted.Major Areas Inspected:Alert & Notification Sys,Training of Offsite Support Agency Personnel Assigned to Sys Monitoring & Operation & Review of Emergency Preparedness Procedures IR 05000416/19890021989-02-0808 February 1989 Insp Rept 50-416/89-02 on 890124-27.No Violations or Deviations Noted.Major Areas Inspected:Assessment of Compliance W/Nrc Bulletin 88-007, Power Oscillations in Bwrs IR 05000416/19880231988-11-0404 November 1988 Insp Rept 50-416/88-23 on 880924-1020.No Violations or Deviations Noted.Major Areas Inspected:Operation Safety Verification Radiological Protection & Physical Security Verification,Maint Observation & ESF Sys Walkdown IR 05000416/19880201988-11-0202 November 1988 Insp Rept 50-416/88-20 on 881003-06.No Violations or Deviations Noted.Major Areas Inspected:Annual Radiological Emergency Response Exercise IR 05000416/19880191988-10-0505 October 1988 Insp Rept 50-416/88-19 on 880820-0923.Violations Noted.Major Areas Inspected:Operational Safety Verification,Maint & Surveillance Observation,Ros,Operating Reactor Events & Followup & Unresolved Items IR 05000416/19880161988-08-29029 August 1988 Partially Withheld Insp Rept 50-416/88-16 on 880725-29.No Violations Noted.Major Areas Inspected:Security Plan & Implementation Procedure,Security Program Audit,Records & Repts,Testing & Maint & Access control-personnel IR 05000416/19880171988-08-26026 August 1988 Insp Rept 50-416/88-17 on 880716-0819.No Violations or Deviations Noted.Major Areas Inspected:Licensee Action on Previous Enforcement Matters,Maint & Surveillance Observations,Operational Safety Verification & ESF Sys IR 05000416/19880181988-08-25025 August 1988 Insp Rept 50-416/88-18 on 880808-12.No Violations or Deviations Noted.Major Areas Inspected:Areas of Fire Protection/Prevention.Strengths in Implementation of Fire Protection Program Listed IR 05000416/19880151988-08-10010 August 1988 Insp Rept 50-416/88-15 on 880718-22.No Violations or Deviations Noted.Major Areas Inspected:Previously Identified Findings in Area of Environ Qualification of Electrical Equipment Important to Safety 1990-08-16
[Table view] Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS
MONTHYEARIR 05000416/19990121999-09-29029 September 1999 Insp Rept 50-416/99-12 on 990725-0904.Violations Noted.Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000416/19990111999-09-28028 September 1999 Insp Rept 50-416/99-11 on 990830-0903.No Violations Noted. Major Areas Inspected:Solid Radioactive Waste Management Program,Radioactive Matl Transportation Program,Facilities & Equipment,Staff Knowledge & Performance & Staff Training IR 05000416/19990141999-09-27027 September 1999 Insp Rept 50-416/99-14 on 990830-0903.No Violations Noted. Major Areas Inspected:Implementation of Liquid & Gaseous Radioactive Waste Effluent Mgt Program & Status of Effluent Radiation Monitors & Counting Room Instruments IR 05000416/19990151999-09-13013 September 1999 Partially Withheld Insp Rept 50-416/99-15 on 990816-20. Noncited Violation Noted.Major Areas Inspected:Licensee Physical Security Program,Personnel Access Control,Access Authorization & Protected Area Detection Aids IR 05000416/19990101999-08-24024 August 1999 Insp Rept 50-416/99-10 on 990809-13.No Violations Noted. Major Areas Inspected:Licensed Operator Requalification Program IR 05000416/19990091999-08-0909 August 1999 Insp Rept 50-416/99-09 on 990613-0724.No Violations Noted. Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000416/19990031999-07-30030 July 1999 Insp Rept 50-416/99-03 on 990405-08 & 0510-11.No Violations Identified.Major Areas Inspected:Corrective Action Program Implementation IR 05000416/19990071999-07-23023 July 1999 Insp Rept 50-416/99-07 on 990622-25.Violations Noted.Major Areas Inspected:Announced Insp of Licensee Performance & Capabilities During full-scale,biennial Exercise of Emergency Plan & Implementing Procedures Performed IR 05000416/19990081999-07-15015 July 1999 Insp Rept 50-416/99-08 on 990502-0612.Violations Noted.Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000416/19990051999-06-27027 June 1999 Insp Rept 50-416/99-05 on 990321-0501.Violations Identified, Being Treated as non-cited Violations.Major Areas Inspected: Aspects of Licensee Operations,Maint,Engineering & Plant Support IR 05000416/19990061999-05-21021 May 1999 Insp Rept 50-416/99-06 on 990419-23.No Violations Noted. Major Areas Inspected:Licensee Implementation of NRC Approved Fire Protection Program IR 05000416/19990021999-05-18018 May 1999 Insp Rept 50-416/99-02 on 990222-26 & 0308-12.Non-cited Violations Noted.Major Areas Inspected:Engineering IR 05000416/19990041999-04-23023 April 1999 Insp Rept 50-416/99-04 on 990131-0320.Violations Noted. Major Areas Inspected:Operation,Maintenance,Engineering & Plant Support IR 05000416/19990011999-02-26026 February 1999 Insp Rept 50-416/99-01 on 990201-05.Violations Noted. Major Areas Inspected:Plant Support.Violation of TS 5.7.2 Identified for Failure to Control Locked High Radiation Area Around Spent Fuel Pool Cooling & Cleanup HX ML20207E0881999-02-26026 February 1999 Notice of Violation from Insp on 990201-05.Violation Noted: on 990201,NRC Inspectors Identified That Area with Dose Rates Greater than 1000 M/H Not Provided with Locked or Continously Guarded Doors to Prevent Unauthorized Entry IR 05000416/19980151999-01-20020 January 1999 Insp Rept 50-416/98-15 on 981101-1212.No Violations Noted. Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Suuport PNO-IV-99-005, on 990113,Grand Gulf Operators Commenced Unit Shutdown,From 100 Percent Power,Due to One or More Apparently Degraded Current Transformers Located in Safety Related Div I,4.16 Kv Switchgear.State of Ms Informed1999-01-13013 January 1999 PNO-IV-99-005:on 990113,Grand Gulf Operators Commenced Unit Shutdown,From 100 Percent Power,Due to One or More Apparently Degraded Current Transformers Located in Safety Related Div I,4.16 Kv Switchgear.State of Ms Informed ML20198L7711998-12-24024 December 1998 Notice of Violation from Insp on 981207-11.Violation Noted: on 950630,licensee Made Change to Emergency Plan Without Commission Approval IR 05000416/19980161998-12-24024 December 1998 Insp Rept 50-416/98-16 on 981207-11.Violations Noted.Major Areas Inspected:Operational Status of Licensee Emergency Preparedness Program Was Conducted ML20196F1271998-12-0101 December 1998 Insp Rept 50-416/98-13 on 980920-1031.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20196F1141998-12-0101 December 1998 Notice of Violation from Insp on 980920-1031.Violation Noted:From 980521 Through 981015,conditions Adverse to Quality Identified in Condition Rept 1998-0014 Not Promptly Corrected IR 05000416/19980141998-11-27027 November 1998 Insp Rept 50-416/98-14 on 981026-30.No Violations Noted. Major Areas Inspected:Exposure Controls,Controls of Radioactive Matls & Contamination,Surveying & Monitoring & Quality Assurance Oversight of Radiation Protection Program IR 05000416/19980111998-10-14014 October 1998 Insp Rept 50-416/98-11 on 980809-0919.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000416/19980121998-09-15015 September 1998 Insp Rept 50-416/98-12 on 980817-20.No Violations Noted. Major Areas Inspected:Training,Qualifications,Quality Assurance Oversight,Facilities & Equipment & Annual Reports IR 05000416/19980031998-09-0909 September 1998 Insp Rept 50-416/98-03 Cancelled IR 05000416/19980091998-08-31031 August 1998 Insp Rept 50-416/98-09 on 980628-0808.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000416/19980101998-08-26026 August 1998 Insp Rept 50-416/98-10 on 980803-07.No Violations Noted. Major Areas Inspected:Licensee Physical Security Program IR 05000416/19980081998-07-14014 July 1998 Insp Rept 50-416/98-08 on 980517-0627.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000416/19980071998-06-0202 June 1998 Insp Rept 50-416/98-07 on 980518-21.No Violations Noted. Major Areas Inspected:Access Authorization,Alarm Stations, Communications,Access Control of Packages & Vehicles, Assessment Aids & Mgt Support IR 05000416/19980051998-05-28028 May 1998 Insp Rept 50-416/98-05 on 980405-0516.Violations Noted.Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support ML20248E7501998-05-28028 May 1998 Notice of Violation from Insp on 980405-0516.Violation Noted:On 980421,inspectors Found Back Doors on Diesel Generator Control Cabinet 1H22-p400 in Div 1 Standby Diesel Generator Room Standing Wide Open & Unattended IR 05000416/19980061998-05-19019 May 1998 Insp Rept 50-416/98-06 on 980427-0501.No Violations Noted. Major Areas Inspected:Radiation Protection Activities in Support of 1998 Refueling Outage IR 05000416/19980041998-05-0505 May 1998 Insp Rept 50-416/98-04 on 980414-16.No Violations Noted. Major Areas Inspected:Maint & Plant Support IR 05000416/19983011998-04-16016 April 1998 Insp Rept 50-416/98-301 on 980330-0403.No Violations Noted. Major Areas Inspected:Competency of Reactor Operator & Eight Senior Applicants for Issuance of OLs at Grand Gulf Nuclear Station IR 05000416/19980021998-04-15015 April 1998 Insp Rept 50-416/98-02 on 980222-0404.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000416/19980011998-03-0404 March 1998 Insp Rept 50-416/98-01 on 980111-0221.No Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000416/19970221997-12-15015 December 1997 Insp Rept 50-416/97-22 on 971130-980110.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering IR 05000416/19970211997-12-0505 December 1997 Insp Rept 50-416/97-21 on 971019-1129.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20199L9411997-11-25025 November 1997 Notice of Violation from Insp on 970804-22.Violation Noted: on or About Period of 970117-29,approved FP Program as Described in UFSAR Was Not Fully Implemented.Emergency Light 1T92S222A Was Not Capable of Performing Function IR 05000416/19970181997-11-25025 November 1997 Insp Rept 50-416/97-18 on 970804-22.Violations Noted.Major Areas Inspected:Operations & Maint.Nrc IP 40500 Used to Evaluate Licensee Effectiveness in Identifying,Resolving & Preventing Issues That Degrade Quality of Plant Operations IR 05000416/19970201997-10-31031 October 1997 Insp Rept 50-416/97-20 on 970907-1018.Violations Noted.Major Areas Inspected:Operations,Maint & Plant Support Re Emergency Post Accident Sampling Sys Drill ML20198Q0291997-10-31031 October 1997 Notice of Violation from Insp on 970907-1018.Violation Noted:As of 971011,security Patrols Had Not Reported Dark Areas in Temporary Covered Maint Work Area in Protected Area IR 05000416/19970161997-10-23023 October 1997 Insp Rept 50-416/97-16 on 970929-1003.No Violations Noted. Major Areas Inspected:Review of Licensed Operator Requalification Program Following Guidelines in IP 71001 IR 05000416/19970151997-10-0909 October 1997 Insp Rept 50-416/97-15 on 970916-19.Three Weaknesses Noted During Exercise.Major Areas Inspected:Licensee Performance & Capabilities During full-scale,biennial Exercise of Emergency Plan & Implementing Procedures IR 05000416/19970071997-10-0101 October 1997 Informs That Insp Rept 50-416/97-07 Has Been Cancelled & There Will Be No Insp Issued for This Rept Number ML20216J2081997-09-12012 September 1997 Notice of Violation from Insp on 970803-0906.Violation Noted:As of 970811,duplex Filter Selection Levers for HPCS & Div 1 Standby DGs Were in Both Position Such That Two Strainers/Filters Were Selected IR 05000416/19970171997-09-0505 September 1997 Insp Rept 50-416/97-17 on 970804-08.No Violation Noted.Major Areas Inspected:Implementation of Solid Radwaste Mgt & Radioactive Matls Transportation Programs ML20210N0761997-08-19019 August 1997 Notice of Violation from Insp on 970622-0802.Violation Noted:On 970630,inspectors Identified Extension Ladder Supported on safety-related Cable Tray & No Engineering Evaluation Had Been Completed ML20216A8411997-08-0606 August 1997 Notice of Violation from Insp on 970714-18.Violation Noted: on 970717,compensatory Measures Not Implemented at Two Trailers within Protected Area Where Lighting Did Not Meet Required 0.2 Footcandles IR 05000416/19970131997-08-0606 August 1997 Partially Withheld Insp Rept 50-416/97-13 on 970714-18 (Ref 10CFR73.21).Violations Noted.Major Areas Inspected: Licensee Physical Security Program,Including Review of Records,Repts,Testing,Maint & Assessment Aids 1999-09-29
[Table view] |
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Report Nos.:
50-416/85-44 and 50-417/85-08
- Licensee: Mississippi Power and Light Company-Jackson, MS.39205 Docket Nos.:
50-416 and 50-417 License Nos.:
NPF-29 and CPPR-119
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' Facility Name: Grand Gulf Nuclear Station
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Inspection Conducted: Dec mber 2-13, 1985 Inspector:
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. E. A. King Accompanying Personnel:
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T. P. Lynch
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G. Simonds G. Wehmann J
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. M. Will Approved by:
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' T. R. Decker, Section Chief
' Date Signed Emergency Preparedness Section Division of Reactor Safety SUMMARY Scope: This routine, announced inspection involved 212 inspector-hours onsite in the area of the annual emergency preparedness exercise.
Results:
No violations or deviations were identified; however, four exercise weaknesses were identified, namely:
failure to follow followup notification
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message procedure (paragraph 8);
failure to conduct Emergency Operations i
Facility (EOF) Air Sampling per procedure (paragraph 10.d.1);
failure to make timely and consistently accurate assessments (paragraph 10.d.4);
f ailure to follow offsite radiological monitoring procedures (paragraph 11).
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REPORT DETAILS
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Persons Contacted Licensee Employees
- 0. D. Kingsley, Jr., Vice President, Nuclear Operations
- L. F. Dale, Director, Licensing and Safety
- J. G. Cesare, Manager, Nuclear Operations-
E. Cross, Site Director
- P. B. Benedict, Emergency Planning Coordinator
- J. Moore, Vice President Corporate Communications
- T. Cloninger, Vice President, Nuclear Engineering and Support
- V. Parrish, Chemistry / Radiation Superintendent
- G. O. Smith, Supervisor, Environmental Services
- J. Vincelli, Radiation Control Supervisor-
-*C. Brown, Health Physics Supervisor
- J. G. Hurley, Emergency Planning Specialist Other licensee employees contacted included engineers, technicians, operators, mechanics, security force members, and office personnel.
Other Organizations
- G. O. Smith, Tenera (Emergency Planning Consultant)
"M. Hill, Enercon Services (Emergency Planning Consultant)
- D. Schneck, Tenera (Emergency Planning Consultant)
NRC Resident Inspector
- Attended Special Meeting (NRC Region II, December 13,1985)
- Attended both exit interview and Special Meeting (NRC Region II, December 13,1985)
2.
Exit Interview (30703)
The inspection scope and findings were summarized on December 4,1985, with those persons indicated in Paragraph 1 above. The inspector described the areas inspected and discussed in detail the inspection findings listed herein. The licensee did not identify as proprietary any oof the materials provided to or reviewed by the inspector during this inspection.
As a consequence of the exercise findings, the licensee requested a meeting with the NRC, licensee management representatives eet with NRC Regional management on December 13, 1985, to review the-findings and discuss planned corrective actions and the scheduied completion thereof.
The licensee
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committed to submit a letter to the NRC documenting the corrective actions defined, including training, remedial drills, and schedules.
3.
Licensee Action on Previous Enforcement Matters
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(Closed) Violation 50-416/85-15-01, 50-417/85-15-01:
Failure to Train Offsite Firefighters. Inspection of training records and related documents, including attendance rosters, disclosed that the subject requirements were met during the 1985 calendar year.
The corrective action was consistent with the commitments defined in the licensee's letter of July 3, 1985.
4.
Exercise Scenario (82301)
The scenario for the emergency exercise was reviewed to assure that provisions were made to test the integrated capability and a major portion of the basic elements defined in the licensee's emergency plan and organization pursuant to 10 CFR 50.47(b)(14), Paragraph IV.F of Appendix E to 10 CFR 50, and specific criteria defined in Section II.N of NUREG-0654, Revision 1.
The scenario was reviewed in advance of the scheduled exercise and was discussed in detail with licensee representatives on November 26, 1985, and December 2, 1935.
The scenario developed for this exercise was detailed, and designed to fully exercise the onsite emergency organization.
It appeared, however, that the scenario was exceedingly rigid and placed severe demands on the response organization.
These demands were particularly noticeable in the following instances:
(1) challenging the Operations
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Support Center's (OSC) capability to provide and deploy required investigative and repair teams; (2) the diverse source terms generated in response to the States of Mississippi and Louisiana exercise requirements; (3) delay in Control Room staff initiating response to the reported simulated sequence of events.
Notwithstanding the above, the scenario was consistent with the intent of the cited regulatory requirement and guidance.
The licensee made a large commitment to training and personnel through the use of controllers, evaluators, and required personnel participating in the exercise. Note, however, that training weaknesses were identified in the areas of dose assessment and offsite radiological monitoring at. discussed in paragraphs 10.d.4 and 11, respectively.
No violations or deviations were identified.
5.
Assignment of Responsibility (83201)
This area was c5 served to assure that primary responsibilities for emergency response by the licensee were established, and that adequate staff was available to respond to an emergency pursuant to 10 CFR 50.47(b)(1),
Paragraph IV. A of Appendix E to 10 CFR 50, and specific criteria defined in Section II.A of NUREG-0654, Revision 1.
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The inspector observed that specific emergency assignments were made for the licensee's emergency response organization, and that adequate staff was available to respond to the simulated emergency.
The initial response organization was augmented by designated licensee representatives; however, based on the scenario scope and conditions, long term or continuous staffing of the emergency response organization was not required.
Discussions with licensee representatives indicated that sufficient technical personnel were available to provide for continuous staffing of the augmerted emergency organization if needed.
The inspector also observed activation, staffing, and operation of the emergency organization in the Technical Support Center (TSC), Operations Support Center (OSC), and Emergency Operations Facility (EOF).
At each emergency response facility, the required staffing and assignment of responsibility was consistent with the licensee's approved procedures.
No violations or deviations were identified.
6.
Onsite Emergency Organization (82301)
The licensee's onsite emergency organization was observed to assure that the following requirements were implemented pursuant to 10 CFR 50.47(b)(2),
Paragraph IV.A of Appendix E to 10 CFR 50, and specific criteria promulgated in Section II.B of NUREG-0654, Revision 1:
(1) specific definition of responsibilities for emergency response; (2) adequate staffing to assure initial facility accident response in key functional areas at all times; (3) specification of onsite and offsite support organizational interactions.
The inspector observed that the initial onsite emergency organization was adequately defined and that staff was available to fill key functional positions within the emergency organization.
Augmentation of the initial emergency response organization was accomplished through mobilization of off-shift personnel.
The on-duty Shift Supervisor assumed the duties of Emergency Director promptly upon initiation of the simulated emergency and directed the response until relieved by the Station Manager.
Delay in initiation of response was observed, however, because of the detailed definition and treatment of the sequence of accident events.
Required interaction between the licensee's emergency response organization and State and offsite support agencies was adecuate and consistent with the scope of the exercise prior to activation of the Emergency Operation Facility (EOF).
Following activation of the EOF, however, a significant change in implementing required followup notification messages was noted.
This finding is discussed in Paragraph 8, below.
No violations or deviations were identified.
7.
Emergency Classification System (83201)
This area was cbserved to assure that a standard emergency classification
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to 10 CFR 50.47(b)(4), Paragraph IV.C of Appendix E to 10 CFR 50, and specific criteria promulgated in Section II D of NUREG-0654, Revision 1.
An emergency _ action level matrix was used to promptly identify and properly classify the emergency and escalate to more severe emergency classifications
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as the simulated emergency progressed.
Licensee actions in this area were considered adequate.
An inspector observed that the emergency classification system was
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effectively used and was consistent with the Radiological Emergency Plan and Implementing Procedures.
The system appeared to be adequate for the classification. of the simulated accident sequences.
The emergency procedures provided for initial and continuing mitigating actions during _the simulated emergency.
No violations or deviations were identified.
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8.
Notification Methods and Procedures (83201)
This area was observed to assure that procedures were established for notification of State and local response organizations and emergency
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personnel by the licensee, and that the content of initial and followup messages to response organizations was established. _This area was further observed to assure that means to provide early notification to the populace within the plume exposure pathway were established pursuant to 10 CFR 50.47(b)(5), Paragraph IV.D of Appendix E to 10 CFR 50, and specific criteria defined in Section II.E of NUREG-0654.
Prior to activation of the EOF, it was observed that notification methods and procedures were established and consistently used to provide information concerning the simulated emergency conditions.to Federal, State and local response organizations, and to alert the licensee's augmented emergency response organization. Telephone notification of State and local response
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organizations was promptly followed by transmission of hard copies of the notification to these organizations and the licensee's Emergency News Media Center (ENMC).
Following activation and routine operation of the EOF, however, it was observed that the licensee consistently failed to implement followup notification (FUN) messages to the States and offsite agerbies as required by Section 6.1.9 of Emergency Plan Procedure 10-S-01-6, Revision 10 (Notification iof Offsite Agencies and Plant-On-Call Emergency Personnel)l
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The subject procedure required that following activation of: the.Technica
. Support Center (TSC) and E0F, the followup notification form must be filled out and transmitted as new information becomes available, or every 30 minutes whichever comes first. Consistent with this procedure, the EOF Communicator assumes responsibility for all further communications /notifi-cations to offsite agencies. Observations confirmed a delay of 54 minutes in transmission of site boundary thyroid dose data. Other radiological data was typically delayed 35 to 45 minutes prior to transmission of FUN
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Based on the above findings, the licensee was informed that failure to follow the referenced procedure regarding FUN messages constituted an exercise weakness (50-416/85-44-01, 50-417/85-08-01).
The licensee acknowledged the finding. This item was fully discussed during the exercise critique, and was later discussed during a meeting between licensee and NRC Regional management held on December 13, 1985. The licensee committed to implement required corrective action, including additional personnel training.
No violations or deviations were identified.
9.
Emergency Communications (83201)
This area was observed to assure that provisions for prompt communications among principal response organizations and emergency personnel was established and maintained pursuant to 10 CFR 50.47(b)(6), Paragraph IV.E of Appendix E to 10 CFR 50, and specific criteria promulgated in Section II.F of NUREG-0654, Revision 1.
' Communications among the licensee's emergency response facilities and emergency organization were. adequate and consistent with approved Emergency Plan procedures and the scope of the exercise. Communications between the licensee's response organization and the State and local offsite agencies were adequate, except as discussed in Paragraph 8, above.
No violations or deviations were identified.
10.
Emergency Facilities and Equipment (83201)
This area was observed to assure that adequate emergency facilities and equipment to support an emergency response were provided' and maintained pursuant to 10 CFR 50.47(b)(8), Paragraph IV.E of Appendix E to 10 CFR 50, and specific criteria defined in Section II.H of NUREG-0654, Revision 1.
The inspectors observed the activation, staffing, and operation of the.
emergency response facilities and evaluated the equipment provided for emergency use daring the exercise.
a.
Control Room - The inspector observed that following review and analysis of the sequence of accident events, reactor Control Room t
operations personnel acted promptly to initiate required responses to the simulated emergency. Emergency procedures were readily available, routinely followed, and factored into accident assessment ~ and mitigation exercises.
Control Room personnel involvement was essentially limited to those personnel assigned routine and special operational duties.
Effective management of personnel gaining access to the Control Room precluded overcrowding, and maintained an ambient noise levtl required for the orderly conduct of operations under emergency condition.
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The Shif t Supervisor and the Control Room operators were cognizant of their duties, responsibilities, and authorities.
.These personnel demonstrated an understanding of the emergency classification system and the proficient use of specific procedures to determine and declare the proper emergency classification.
It was observed that the voluminous data and information provided as the scenario initial sequence of accident event's and conditions placed extraordinary demands upon the Emergency Director and the Control Room Staff in initiating the exercise in a timely manner. The Control Room staff, however, demonstrated the capability to effectively assess the initial conditions and implement required mitigating actions.
b.
Technical Support Center (TSC) - The TSC was activated and promptly staffed following notification by the Emergency Director of the simulated emergency conditions leading to the Alert classification.
The facility staff appeared to be cognizant of their emergency duties, authorities, and responsibiliti'es. Required operations at the facility proceeded in an orderly manner.
This facility was provided with adequate equipment for support of the assigned staff. TSC security was promptly established.
The independent ventilation system was actuated during tne exercise.
During operation of this facility, radiological habitability was routinely monitored.
Dedicated communicators were assigned to the facility and all required notifications were promptly implemented.
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Status boards were strategically located to facilitate viewing by the TSC staff.
Status boards were frequently updated as required to chronicle changes in plant status, accident assessment and mitigation throughout the exercise.
The inspectors noted that a status board dedicated to trending of simulated plant systems status and engineering data was maintained and updated during the accident sequence.
c.
Operations Support Center (OSC) - The OSC was promptly staffed following activation of the emergency plan by the Emergency Director.
It was observed that teams were promptly assembled, briefed, and prepared for deployment. The OSC Supervisor appeared to be cognizant of his duties and responsibilities. During operation of this facility, radiological habitability was routinely monitored and documented.
It was observed that the OSC could not meet the demands of the exercise scenario. Such demands exceeded the number of augmented personnel and emergency teams routinely available to the facility during emergency conditions.
It was also observed however that the OSC supervisor demonstrated the required ability to discern and select those conditions which warranted priority, and promptly provided the required investigative and repair teams.
The EOF is located in the d.
Emergency Operations Facility (EOF)
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Training Building located approximately is mile from the plant site
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boundary." The facility was adequately equipped and staf fed to support an emergency response.
E0F security was promptly established during facility activation and was maintained throughout the duration of the exercise.
During operation of the facility, radiological habitability was routinely monitored.
Status boards and other related visual aids were strategically located and were readily accessible for viewing by the E0F staff.
Dedicated communicators were assigned to the facility to assure that all required notifications were promptly implemented; however, as discussed in Paragraph 8, above, significant delays in issuance of FUN messages were observed.
Inspection disclosed the following additional findings, namely:
(1) assumption of duties by the EOF Director was definite and firm; (2) staff briefings were frequent and consistent with changes in plant status, and progress in accident assessment and mitigation; (3) communications between the EOF and the other emergency response facilities were effective; (4) engineering and other technical support functions, including the States of Louisiana and Mississippi dose assessment groups, were readily accommodated within the facility.
Interaction among the facility technical groups appeared adequate.
The findings detailed below were also identified.
(1) Section 5.2.4.c of Corporate Emergency Plan Procedure (CEPP)
No. 4.9, requires periodic sampling of air in the EOF in the area where the majority of personnel are assembled.
Because of the loud noise made by the sampler, EOF staf f objected and requested that further sampling be deleted. Air sampling was immediately stopped.
During the remainder of the exercise, sampling was simulated.
This finding is classified as an exercise weakness (50-417/85-44-02, 50-417/85-08-02) based on failure to implement air sampling. consistent with procedural requirements and the scope of the exercise.
This finding was fully discussed with the licensee during the exercise critique and the Special Meeting previously referenced.
The licensee acknowledged the finding and committed to implement corrective action.
(2) The Corporate Emergency Plan Procedure (CEPP) No. 4.5 ( Activation and Operation of the Emergency Operations Facility) appears to be inadequate.
It does not provide the requirement to isolate the EOF via actuating the H&V ventilation system should this become necessary during a radiological release.
The requirement to actuate the EOF ventilation system was consistent with the scope of the exercise.
The above procedure will be reviewed during subsequent inspections (IFI 50-416/85-44-03, 50-417/85-03).
This item was discussed in detail during the exercise critique.
The licensee acknowledged this findin (3) Attachment I to procedure EPP No.10-S-01-12 does not provide conversion factors for shutdown times greater than 12.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />.
Shutdown time for the exercise was 384 hours0.00444 days <br />0.107 hours <br />6.349206e-4 weeks <br />1.46112e-4 months <br />.
This finding was fully discussed during the exercise critique and the previously referenced meeting with licensee management on December 13, 1985.
The-licensee acknowledged this finding.
This procedure will be reviewed during subsequent inspections (IFI 50-416/85-44-04,50-417/85-08-04).
(4) The dose assessment group and the function thereof appeared confused and disorganized, and consistently issued questionable dose projections.
For exampla, a radiological assessment message was developed which projected a thyroid dose at the site boundary representing an increase of 100 to 1000 over any value calculated during the preceding hour.
Iterations of this type were consistently repeated during the course of the exercise.
This failure indicates a lack of required training of the subject group and, as such, constituted an exercise weakness (50-416/85-44-05, 50-417/85-08-05). This finding was discussed in detail during the exercise critique, and the previously referenced meeting of December 13, 1985.
The licensee acknowledged this finding and committed to implement required corrective actions including remedial drills.
No violations or deviations were identified regarding emergency response facilities and equipment.
11. Accident Assessment (82301)
This area was observed to assure that adequate methods, systems, and equipment for as'sessing and monitoring actual or potential offsite consequences of a radiological emergency condition were in use as required by 10 CFR 50.47(b)(9), Paragraph IV.B of Appendix E to 10 CFR 50, and specific criteria promulgated in Section 11.1 of NUREG-0654, Revision 1.
The accident assessment p-ogram included assessment of plant systems and status, and the effects of resulting radiological hazards to onsite and offsite personnel. During the exercise, the engineering accident assessment team functioned effectively in analyzing plant status to provide recommendations to the Site Emergency Manager regarding mitigating actions required to reduce damage to plant systems, prevent releases of radioactive materials, and terminate the emergency condition.
Radiological assessment activities involving in plant and offsite monitoring were conducted by licensee radiation monitoring teams. Offsite radiological effluent data was reported to the TSC as appropriate. EOF dose assessments and projections as computed and based on data transmitted by the of f site monitoring group is discussed in Paragraph 10, abov.
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Three offsite radiological monitoring / survey teams were deployed by the licensee during the exercise.
One team, designated the Red team; was evaluated. Observations of this team disclosed the findings detailed below.
a.
Excessive prompting by the assigned controller was observed _throughout the field exercises, b.
Poor contamination practices and controls were observed, namely:
failure to use or simulate use of protective clothing when required; inadequate control precluding sample cross-contamination as stated in Section 5.H of Corporate Emergency Procedure 4.8; failure to survey vehicle; contaminated waste inadequately segregated from clean items.
c.
During plume monitoring, beta / gamma readinga were not taken as required by Emergency Plan Procedure 10-5-01-14 and Corporate Emergency Procedure 4.8.
d.
No source checks were performed on survey / monitoring instruments prior to deployment.
e.
Players did not appear to be familiar with field sample locations, field calculations, and required procedures.
These findings indicated a lack of adequate training and, as such, constituted an exercise weakness (50-416/85-44-06, 50-417/85-08-06).
This finding was discussed in detail at the exercise critique and the Special Meeting previously referenced.
The licensee acknowledged the finding, and committed to implement required corrective action.
No violations or deviations were identified.
12.
Public Education and Information (82301)
This area was observed to assure that information concerning the simulated emergency was made available for dissemination to the public as required by 10 CFR 50.47(b)(7), Paragraph IV.D of Appendix E to 10 CFR 50, and specific criteria promulgated in Section II.G of NUREG-0654, Revision 1.
Information was provided to the media and the public in advance of the exercise.
The information included details on how the public would be notified and the initial actions which should be taken in the event of a radiological emergency. A rumor control program was also in place.
The licensee activated a near site (Port Gibson, Miss.) Emergency News Media Center (ENMC).
The facility was adequately equipped.
Coordination of information between the State and licensee was timely.
Both licensee and State groups worked together effectively in the ENMC.
Written press releases were prepared and issued from the ENMC.
Releases issued were timely, and adequately reflected plant emergency conditions and mitigating actions taken or planned. Corporate and State spokesmen conducted periodic
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press briefings. The briefings were technically accurate and were presented in a manner readily understood by laymen. Visual aids were provided which effectively defined the simulated accident and the local areas within the plume exposure 10 mile EPZ impacted by radiological releases. A conference telephone link was established between the ENMC, Mississippi Emergency Management Agency (MEMA) Operations Center, and the MP&L general of fice during the press briefing. This feature continues to enhance the exchange of news information.
No violations or deviations were identified.
13.
Radiological Exposure Control (82301)
This area was observed to determine that methods for controlling radiological exposures during an emergency were established and implemented for emergency workers, and that such methods included exposure guidelines consistent with EPA recommendations as required by 10 CFR 50.47(b)(11) and specific criteria promulgated in Section II.K of NUREG-0654.
An inspector noted that radiological exposures were controlled throughout the exercise by issuing supplemental dosimeters to emergency workers and by conducting periodic radiological surveys in the emergency response facilities.
Exposure guidelines were in place for various categories of emergency actions, and adequate protective clothing and respiratory protection were available if needed.
No violations or deviations were identified.
14.
Recovery and Reentry Planning (82301)
This area was observed to assure that general plans were made for recovery and reentry as required by 10 CFR 50.47(b)(13), Paragraph IV.H of Appendix E to 10 CFR 50, and specific criteria in Section II.M of NUREG-0654.
The licensee developed general plans and procedures for reentry and recovery which addressed both existing and potential conditions. The plans contained the position / title, authority, and responsioilities of each key individual in the recovery organization.
The plans and criteria addressing deescalation of the emergency were consistent with the scope of the exercise and the scenario developed therefor.
No violations or deviations were identified.
15.
Exercise Critique (82301)
The licensee's critique of the emergency exercise and weaknesses observed during their emergency response were formally presented to licensee management for corrective actions as required by 10 CFR 50.47(b)(14),
Paragraph IV.E of Appendix E to 10 CFR 50 and specific criteria promulgated in Section II.N of NUREG-065 *
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-11 The exercise critique was conducted on December 4, 1985.
Licensee management, key exercise participants, and NRC representatives were present.
The licensee. discussed areas of the exercise which required corrective action and improvements. The inspectors. determined that the critique was comprehensive, and adequately addressed the weaknesses-identified in their
' emergency response during the exercise.
All findings identified herein were discussed in detail with licensee representatives. A meeting of NRC and lice'nsee management was later held in Region II on December 13, 1985, to further discuss the referenced findings and the licensee's commitments to implement required corrective actions including training, retraining and remedial drills, where indicated.
No violations or deviations were identified.
16.
Federal Emergency Management Agency (FEMA) Report (82301)
Reports of FEMA Regions IV and VI evaluation of offsite emergency preparedness will be provided by a separate transmittal.
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17. Public Meetings (82301)
Public critiques of the exercise were held in St. Joseph, Louisiana and Port Gibson, Mississippi. Agencies participating in the critiques included the licensee, States and local support groups, FEMA Regions IV and VI, and the NRC.
18.
Followup Items (92701)
The following items were reviewed:
a.
(Closed)
IFI 50-416/05-04-01:
Failure to recommend protective action consistent with EPP-1-0-S-01-5, Following General Emergency Declaration.
Licensee action regarding the subject finding was observed during this inspection.
This item is closed consistent with observation findings.
b.
(Closed)
Violation 50-416/85-15-01:
Failure to Train Offsite Firefighters.
See Paragraph 3, above.