ML20196F127

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Insp Rept 50-416/98-13 on 980920-1031.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support
ML20196F127
Person / Time
Site: Grand Gulf 
Issue date: 12/01/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20196F105 List:
References
50-416-98-13, NUDOCS 9812040206
Download: ML20196F127 (26)


See also: IR 05000416/1998013

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ENCLOSURE 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket No.:

50-416.

License No.:

NPF-29

Report No.:

50-416/98-13-

Licensee:

Entergy Operations, Inc.

Facility:

Grand Gulf Nuclear Station

Location:

Waterloo Road

Port Gibson, Mississippi 39150

Dates:

September 20 through October 31,1998

Inspector (s):

Jennifer Dixon-Herrity, Senior Resident inspector

Peter Alter, Resident Inspector

George Replogie, Senior Resident inspector, River Bend

Paula Goldberg, Reactor Inspector

Approved By:

Joseph Tapia, Chief, Project Branch A

Attachment:

Supplemental Information

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9812040206 981201

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ADOCK 05000416

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EXECUTIVE SUMMARY

Grand Gulf Nuclear Station

NRC inspection Report 50-416/98-13

This inspection included aspects of licensee operations, maintenance, engineering, and plant

support. The report covers a 6-week period of resident inspection.

Operations

The control room staff continued to exhibit effective communications, a high level of

operator knowledge, and very good oversight. Scheduled work in the switchyard was

well planned and controlled, appropriately addressing the risk associated with the task

(Section 01.3).

With two exceptions, plant equipment was maintained in good material condition and

housekeeping was found to be good. The inspectors identified that fasteners and

temporary restraining cables required as a corrective action for a previously identified

deficiency with grating in containment had not been installed following the refueling

outage. This was identified as a violation for the failure to take corrective actions for a

known deficiency. The practice of staging plastic sheeting and similar lighter materials

in a safety-related room was identified as a poor housekeeping practice (Section O2.1).

Maintenance

The seven maintenance and testing activities observed were properly performed

(Section M1).

The combustible gas control system was in good material condition and aligned to

satisfy Technical Specification requirements (Section M2.1).

Enaineerina

Engineering actions taken in the operability determination of the reactor core isolation

cooling discharge to residual heat removal check valve were acceptable; however, the

documentation of the issue did not quantify the leakage through the valve

(Section E1.1).

The engineering evaluations prior to and after the event involving the near drop of a

heavy load over the reactor were inadequate. Engineering personnel did not have a full

understanding of the requirements of NUREG-0612 or Grand Gulf's commitments to

comply with NUREG-0612. The engineering screening for this evaluation was

inadequate and was a missed opportunity to identify Updated Final Safety Analysis

Report (UFSAR) requirements and the need to perform a safety evaluation. This was

identified as an example of failing to follow procedures. Three additional examples of a

violation for failure to follow procedures were identified. The examples included the

failure to perform a safety evaluation for a heavy lift and a safety evaluation applicability

review for the procedure to perform the heavy lift, failure to ensure that adequate special

lift procedures were developed, and failure to coordinate the heavy lift with the control

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room supervision (Section E8.6).

The inspectors concluded that the root cause analysis report conducted for the event

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involving the near loss of a heavy load over the reactor was less than adequate. The

conclusions reached were narrowly focused and did not comply with the definitions

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provided in the corrective action program. The report failed to identify the f ailure of

personnel to follow procedures or the failure of enginee. ring personnel to understand

regulatory requirements that were in place. Both of these failures contributed to the

event and would have to be corrected to prevent recurrence (Section E8.6.5).

Plant Support

With one exception, observed activities involving radiological controls were well

performed. The inspectors identified one poor posting practice where the posting

around a high contamination area did not meet the licensee's documented guidance

(Section R1,1).

Routine reactor coolant chemistry and dose equivalent iodine sampling and analysis

were completed proficiently and in accordance with the procedures (Section R4.1).

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Report Details

Summarv of Plant Status

The plant operated at 100 percent power until October 21,1998, when operators lowered

power to 48 percent as a result of the trip of circulating Pump A. After conducting repairs, the

plant was returned to 100 percent power on October 22,1998, and operated at that level the

remainder of the inspection period.

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l.' Operations

01

Conduct of Operations

01.1 General Comments (71707)

The inspectors performed control room observations to ascertain operator knowledge

and performance. Operators exhibited good three-way communications and peer

review. Operations shift turnovers and briefings were thorough and conducted

professionally. Operators were knowledgeable of the status of equipment, and

applicable Technical Specification limiting conditions for operations were appropriately

documented.

01.2 Work in the Switchyard

a.

Inspection Scope (71707)

The inspectors reviewed the licensee's planned work in the switchyard and toured the

switchyard to determine the effect the work had on offsite power sources.

b.

Observations and Findings

The switchyard work planned consisted of the removal of two 500 Kva breakers the

licensee had installed for a future offsite power line and to support Unit 2 and the

replacement of the breakers with bus work. The licensee decided to remove the

breakers because of the high cost of maintenance and abandonment of the plans to add

a third 500 Kva offsite power source or to complete Unit 2. The plans the licensee

developed for removal of the breakers were detailed and thorough. The work

coordinator provided daily status on the project to the control room and at the morning

meeting. The licensee had areas in the switchyard roped off to control traffic and lower

the risk of the work being performed. The equipment in the switchyard was in good

material condition.

During the removal of the second breaker, the inspectors noted that work was

scheduled to be conducted on the Division 3 diesel generator's foundation. The task

consisted of removing tack welds from foundation floor plates to allow access under the

diesel generator. During the turnover in the control room and discussions at the

morning maintenance planning meeting, supervisory personnel stressed that fire

protection personnel were to be involved in the preparation and conduct of the work in

the vicinity of the diesel due to the grinding work that was going to occur. The

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inspectors questioned whether the licensee had considered the level of risk with

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personnel working in the vicinity of the diesel and personnel working in the switchyard.

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The assistant to the operations superintendent explained that this had been specifically

considered during the plant safety review committee meeting where the 10 CFR 50.59 screening for the task was reviewed. The work in the switchyard could occur as

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long as the diesels were functional. The inspectors considered the task, toured the

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diesels where the work was to occur, and determined that the increase in risk would not

be great due to the limited controls and equipment that could be affected in the area

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where the work was occurring.

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The inspectors reviewed the 10 CFR 50.59 screening and the standing order developed

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to support the planned work. Both of these documents were accurate and appropriately

addressed the tasks. Control room personnel had the authority to stop work in the

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switchyard if necessary. This option was taken on October 7 and 28,1998, due to the

concern identified with the reactor core isolation cooling check valve and approaching

bad weather on the first date and due to perturbations on the grid on the second. No

risk significant work was planned or performed during removal of the breakers.

O1.3 Conclusions for Conduct of Operations

The control room staff continued to exhibit effective communications, a high level of

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operator knowledge, and very good oversight. Scheduled work in the switchyard was

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well planned and controlled, appropriately addressing the risk associated with the task.

O2

Operational Status of Facilities and Equipment

O2.1

Plant Tours

a.

Inspection Scope (71707)

The inspectors routinely toured the accessible portions of the plant containing safety

and risk significant structures, systems, and components.

b.

Observations and Findinas

The inspectors found that plant equipment was maintained in good material condition

and that plant housekeeping was good with two exceptions On October 14,1998, while

touring the containment, the inspectors noted that six grat'ngs on the * boat dock" on the

114-foot 6-inch elevation were not fastened to the support structure. The inspectors

recalled that this had been a concern prior to the refueling outage and discussed the

concern with the shift superintendent. The shif t superintendent had personnel check on

the concern and verified that no fasteners had been installed in the gratings the

inspectors questioned. The superintendent documented the concern in Condition

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Report 1998-0014-04. The immediate corrective actions taken included fastening down

the grating, inspecting the grating in the containment to verify that there was no other

loose grating, and requesting that engineering evaluate the impact of the grating on

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equipment. Licensee personnel identified three additional discrepancies during the

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inspection in containment, but all other gratings were found to be fastened in place by at

least one fastener.

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Tl e inspectors reviewed the history of the concern. The licensee identified in Condition

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Report 1998-0014-01 on January 14,1998, that not all grating was fastened down.

During the engineering evaluation that occurred as a result of this deficiency, the

licensee identified that grating Sections 77,78,86,87,88,89,90,91,92,93, and 94, all

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sections of gratings on the boat dock, needed additional restraints. The existing grating

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clips capacity was not sufficient to hold the grating in place during a suppression pool

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swell event, opening up the possibility that equipment in the area could be damaged if

the gratings came loose and became missiles. Until a permanent change could be

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made, the licensee installed temporary cables to fasten the gratings to the supporting

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structure below.

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The inspectors found grating Sections 77,78,91,92,93, and 94 unsecured. During the

licensee's inspection, the licensee determined that none of the temporary cables had

been installed following the refueling outage that ended May 21,1998. The engineering

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evaluation completed on January 22,1998, found that there was no safety-related

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equipment in the vicinity that would be damaged by the grating. However, the

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inspectors noted that the full toroid suppression pool suction strainer had been installed

during the recent refueling outage and that the strainer ran under the boat dock, so -

there was now potential for safety-related equipment to be damaged. The licensee

reported this concern to the agency via a 10 CFR 50.72 report and planned to submit a

licensee event report (LER). The inspectors toured the containment and verified the

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temporary cables were installed to secure the gratings in place. The inspectors

identified the failure of the licensee to reinstall the temporary cable restraints previously

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installed to address an identified deficiency with the grating as a violation of

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10 CFR Part 50, Appendix B, Criterion XVI (Violation 50-416/9813-01). The inspectors

found that the immediate corrective actions taken to address the deficiency and the

corrective actions planned were thorough and should prevent recurrence.

On October 23,1998, while touring the auxiliary building, the inspectors noted that

personnel who had been cleaning the alternate decay heat removal system heat

exchangers had left equipment staged in the residual heat removal Train C room. In

addition to heavy buckets of tools and a mop bucket, personnel had left a large sheet of

plastic, rubber boots, and an empty plastic bucket. The inspectors were concemed that

the lighter plastic items would have the potential to block the drains during a flooding

situation. The inspectors noted that this concern was previously discussed as a poor

housekeeping practice in NRC Inspection Report 50-416/98-09. The inspectors

discussed the concern with the plant supervisor and the supervisor had the items

removed.

c.

Conclusions

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With two exceptions, plant equipment was maintained in good material condition and

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housekeeping was found to be good. The inspectors identified that fasteners and

temporary restraining cables required as a corrective action for a previously identified

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deficiency with grating in containment had not been installed following the refueling

outage. This was identified as a violation for the failure to take corrective actions for a

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' known deficiency. The practice of storing or staging plastic sheeting or similar lighter

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materials in a safety-related room was identified as a poor housekeeping practice.

11. Maintenance

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M1

Conduct of Maintenance

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M1.1 General Maintenance Comments

a.

Insoection Scope (62707)

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The inspectors observed portions of maintenance activities, as specified by the following

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work orders:

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209951

VOTES testing of high pressure core spray outboard test return to

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the condensate storage tank, Valve 1E22-F010

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214721

Troubleshooting of reactor core isolation cooling discharge to

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residual heat removal check Valve 1E51-F065

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214820

Troubleshooting of control rod drive water flow oscillations

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215253

Standby liquid control Train A postmaintenance test

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b.

Observations and Findinos

The inspectors found the performance of this work to be satisfactory. All work observed

was conducted in accordance with the instructions and procedures provided in the work

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packages. The technicians performing the tasks were knowledgeable of the equipment

and used good work practices.

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M1.2 General Surveillance Comments

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a.

Insoection Scope (61726)

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The inspectors observed portions of the following surveillances:

06-IC-1E61-O-1004, Containment and Drywell Hydrogen Analyzer Calibration

06-OP-SP64-W-0001, Fire Pump Weekly Operability Test

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06-OP-1E61-O-0003, Drywell Purge System Operability

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b.

Observations and Findinas

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The inspectors noted that the test procedures provided clear guidance and properly

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implemented Technical Specification requirements. Measuring and test equipment was

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verified to be within its current calibration cycle. As necessary, instrumentation was

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removed from service, applicable limiting conditions for operation were entered, and the

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instrumentation was properly returned to service. The operators and technicians were

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very knowledgeable and qualified. As-found test data was within the tolerance

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established for the equipment. Personnelinvolved demonstrated good communications

and attention to detail.

M1.3 Conclusions on Conduct of Maintenance

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The seven maintenance and testing activities observed were properly performed.

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M2

Maintenance and Material Condition of Facilities and Equipment

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M2.1 Enaineered Safety Feature System Walkdown

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a.

Inspection Scope (71707)

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The inspectors performed detailed system walkdowns of the accessible portions of

Combustible Gas Control System. The inspectors verified proper valve, controi board,

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and electrical alignment in accordance with Procedure 04-1-01-E61-1, " Combustible

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Gas Control System," Revision 30, and Piping and Instrument Diagram M-1091,

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" Combustible Gas Control Systems Unit 1," Revision 27.

b.

Observations and Findinas

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The inspectors found that the postaccident hydrogen analyzers, hydrogen recombiners,

containment purge, and drywell vacuum relief and purge subsystems of the combustible

gas control system were properly aligned to assure system operability in accordance

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with the applicable procedure and drawing. The alignment satisfied Technical

Specifications and UFSAR requirements. Major components were properly labeled,

lubricated, and free of identifiable leakage.

c.

Conclusions

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The combustible gas control system was in good material condition and aligned to

satisfy Technical Specification requirements.

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lit. Enaineerina

E1

Conduct of Engineering

E1.1

Enaineerina Evaluation of the Reactor Core isolation Coolina Check Valve

a.

Inspection Scoce (37551)

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The inspectors observed design and system engineering support of the test to verify

reactor core isolation cooling discharge to residual heat removal check

Valve 1E51-F065 closure and to determine actual valve leakage.

b.

Observations and Findinas

On October 6,1998, during performance of full stroke testing of reactor core isolation

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cooling injection shutoff Valve 1E51-Fn13, control room operators observed unusual

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flow and pressure indications which lead them to question whether there was leakage

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through Valve 1E51-F065. The operators declared the system inoperable and entered

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Technical Specification 3.4.6 for increased leakage across the check valve. Plans to

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address the concern were developed promptly during a meeting held early in the

morning. Engineering personnel developed a one time test instruction to verify actual

leakage through Valve 1E51-F065.

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The test performed and the subsequent operability recommendation enabled the

operations shift superintendent to determine that Valve 1E51-F065 complied with

Technical Specification 3.4.6 for reactor coolant system pressure isolation valve -

leakage. The superintendent declared the valve operable and returned the reactor core

isolation cooling system to service.

The inspectors reviewed the test results prepared by engineering personnel. The first

portion of the test measured the pressure that had developed between

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Valves 1E51-F065 and 1E51-F013 in approximately 18 hours2.083333e-4 days <br />0.005 hours <br />2.97619e-5 weeks <br />6.849e-6 months <br /> since operators closed

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Valve 1E511-F013. During that period,1100 psig had developed, indicating that

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Valve 1E51 F065 did leak over time. The second part of the test verified that

Valve 1E51-F065 closed by opening Valve 1E51-F013 and other valves in the lineup

and verifying a maximum pressure was not exceeded. The pressure in this case was

O psig, showing that the valve was in the closed position. Last, engineers measured the

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pressure between Valves 1E51-F065 and 1E51-F013 after closing the latter to see if

there was an increase in pressure. Pressure was recorded for a 10-minute interval and

there was a O psig increase. The engineers used this information to determine that

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there was no leakage through the valve and that the valve was within the Technical

Specification one gpm limit.

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The inspectors questioned whether the leakage indicated in the first part of the test,

where 1100 psig built up over an approximate 18-hour period, had been quantified. The

engineering supervisor explained that the last test performed was similar to the

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Technical Specification required local leak rate test that was conducted on the valve

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during outages; however, pressure was used as an indicator rather than actual leakage.

The supervisor also explained that Valve 1E51-065 had not had any identified leakage

during the localleak rate tests performed since startup. The system engineer explained

that no calculations had been performed to quantify the leakage over the 18-hour

period. However, they had set up a computer program to check what leakage into the

system would have to occur to allow a buildup of 1100 psig, and that amount, with the

system fully vented, was one pint. With trapped air, the amount of leakage would be

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greater; however, the 10-minute test indicated that there was little leakage when the

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pressure differential was maintained.

c.

Conclusions

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Engineering actions taken in the operability determination of the reactor core isolation

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cooling discharge to residual heat removal check valve were acceptable; however, the

documentation of the issue did not quantify the leakage through the valve.

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E8

Miscellaneous Engineering lasues (92903)

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E8.1

(Open) insoection Followuo item 50-416/9603-01: Review long-term justification for

- methodology and assumed valve factors. The inspectors noted that the licensee

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performed differential pressure testing for two additional valves from the 150 lb. Powell

Gate Valve GA1 group and two additional valves from the 600/900 lb. Powell Gate Valve

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group during Refueling Outage 9. The inspectors reviewed the test data. The test data

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from the 150 lb. GA1 group indicated valve factors of 0.522 and 0.422 for the two 4-inch

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valves tested. For the 600/900 lb. Powell Gate Valve group tests, the licensee

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determined that the valve factors were 0.455 for the 12-inch valve and 0.471 for the

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18-inch valve. The licensee's preliminary review of the test data indicated that the

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bounding valve factors of 0.62 for the 150 lb. valves and of 0.50 for the 600/900 lb.

valves were acceptable. The licensee stated that the differential pressure test data was

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being evaluated and would be documented in Engineering Report 0048-98. The

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licensee had not completed their analysis of the test data using uncertainties. The

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inspectors concluded that the licensee was making progress in determining valve

factors. This item will remain open pending NRC review of the final analysis which will

be documented in Engineering Report 0048-98.

E8.2 (Closed) Inspection Followuo item 50-416/9611-01: Review of the UFSAR description

of safety relief valve logic. The inspectors reviewed Engineering Response 97/0313,

Revision 0, which installed a capacitor in the feedback circuit of the comparator which

provided the trip function of the trip unit. The capacitor functioned to provide the

comparator feedback circuit with a time delay to prevent spurious signals from sealing in

the trip unit. The licensee found that the capacitor had no affect on the trip unit's ability

to react and trip due to a true pressure signal. The modification involved the installation

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of _a safety-related capacitor on each of the safety relief valve low-low set trip units. The

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inspectors determined that the licensee's corrective actions were adequate to avoid

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additional spurious openings of the safety relief valves.

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The inspectors reviewed the GE Safety Analysis Report, which identified the number of

safety relief valves that could open at the same time. The Safety Analysis Report

discussed two adjacent valves opening as one of the cases. The report stated that the

probability of the combination of two adjacent valves opening would be very low, since

the valves that have the same setpoints are uniformly distributed around the

suppression pool. It further stated that the containment structural design requirements

of two adjacent valves opening were satisfied under the asymmetric condition, and

subsequent analysis was not necessary for the multitude of other more probable

asymmetric load cases. The inspectors found that the Safety Analysis Report also

discussed two symmetric cases for containment loads. The cases were 8 automatic

depressurization system valves opening and all 20 of the valves opening. The licensee

stated that the 6 valves that opened were symmetrically located around the suppression

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pool and were bounded by the analysis (of all 20 valves opening or the 8 automatic

depressurization valves opening).

In addition, the licensee stated that the Safety Analysis Report was based on

reestablishing pressure to normal operating pressure for the analysis. If there was an

initiallift of all 20 of the safety relief valves followed by an inadvertent lift of 6 valves, the

pressure during the second lif t would be significantly lower; therefore, the forces would

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be lower also. The inspectors reviewed the UFSAR drawing of the layout of the 20

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safety relief valves and found that each safety relief valve had its own tailpiece, which

prevented the valves from discharging into a common header which would increase

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loading. The inspectors concluded that the case of the six safety relief valves

inadvertently opening was bounded by existing analysis.

E8.3

(Closed) U.nresolved item 50-416/9705-02: Lack of leak tests for nonsafety-related to

safety-reated system interface valves. The inspectors reviewed Program

Plan GGNS-M-189.1," Pump and Valve Inservice Testing Program," Revision 8. The

inspectors noted that the 13 nonsafety-related boundary valves were in the inservice

testing program. A telephone conference was held with the licensee, the inspectors,

and the NRC Program Office on September 21,1998, to discuss this unresolved item.

The position of the NRC Program Office was that, since the licensee determined that a

total system leakage limit, rather than a valve specific leakage limit, was appropriate,

ASME Section IX, Category A, testing did not apply and the licensee was appropriately

testing the boundary valves.

E8.4

(Closed) Violation 50-416/9705-06: Test control deficiencies. The inspectors reviewed

the licensee's June 30,1997, response to the violation. For the first example of the

violation, the licensee stated that they believed that their surveillance procedures were in

compliance with 10 CFR Part 50, Appendix B, Criterion XI. In addition, the licensee

stated that the incorporation of the limits was viewed as an appropriate enhancement.

The inspectors reviewed Condition Report 1997-0623, dated June 23,1997. The

condition report addressed whether there was a need to revise the standby service

water (SSW) and the high pressure core spray surveillance procedures to verify that the

pump capabilities to remove heat loads were being met. The licensee concluded that,

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since there was no explicit surveiliance requirement in the Technical Specifications to

verify the heat removal capabilities of equipment supported by the SSW and high

pressure core spray systems, the surveillance procedures would not be revised. In

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addition, the licensee stated that an explicit SSW and high pressure core spray service

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water loop analytical flow rate limit was not clearly specified in the accident analyses for

the assumed heat removal capabilities of the interfacing equipment. Furthermore, the

licensee concluded that the analytical flow rate limit alone would not assure the plant

was operated within the assumptions of the accident analyses, since heat transfer rates

were based on the degree of fouling in the heat exchangers as well as the pump flow

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rates. Based on these reasons, the licensee decided not to revise the surveillance

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procedures. The inspectors reviewed Condition Report 1997-0266, dated

May 15,1997. The inspectors noted that the licensee committed to revising the

hydraulic model calculations to incorporate the 10 percent flow degradation margin

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allowed by ASME Section XI. This would allow the lower limit flow values from the

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inservice test program to match the hydraulic models. The inspectors deterrnined that

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the first exampl-e of the violation was closed.

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For the second example of the violation, the inspectors reviewed Procedures 17-S-06-

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22," Performance and System Engineering Procedure SSW A Performance,"

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Revision 4, and Technical Change Notice 2; 17-S-06-23, "SSW B Performance,"

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Revision 5, and Technical Change Notice 5; and 17-S-06-24, "SSW C Performance,"

Revision 2. The inspectors determined that the procedures were revised to include

revised data sheets and to add notes and precautions to clarify desired and minimum

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flow values. The inspectors noted that the acceptance limits for design values for

required minimum heat transfer rates from Engineering Standard GGNS-MS-39.0 were

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included on the data sheets. The inspectors concluded that acceptance criteria had

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been incorporated into the surveillance procedures. The inspectors determined that the

second example of the violation was closed.

The inspectors reviewed Calculation MC-Q1P41-97036," Determination of Fuel Pool

Cooling and Cleanup Heat Exchanger Capability," Revision 0, and noted that the

calculation superseded previous calculations. The purpose of the calculation was to

determine the thermal performance capability of the fuel pool cooling and cleanup heat

exchangers under various operating conditions using appropriate fouling levels for the

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heat exchangers. The inspectors reviewed Program Plan GGNS-M-189.1,". Pump and

Valve Inservice Testing Program," Revision 8, and found that the fuel pool cooling and

cleanup pumps and valves were in the inservice testing program. The inspectors

reviewed Calculation MC-Q1P41-97035,"SSW Heat Exchanger Thermal Performance

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Instrument Uncertainty," Revision 1, which was prepared to validate the current

instrument uncertainty evaluation methodology. The inspectors reviewed

Standard GGNS-MS-39.0, " Mechanical Standard for Thermal Performance Testing of

Safety-Related SSW Heat Exchangers." The inspectors determined that the standard

was revised to incorporate the latest plant practices concerning thermal performance

instrumentation requirements and error measurement, evaluation, application, and the

most conservative design requirements for the fuel pool cooling heat exchangers. The

inspectors noted that the maximum heat duty design value for the heat exchangers was

revised. The inspectors concluded that the licensee had completed all of the corrective

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actions committed to in their June 30,1997, response to the violation. The inspectors

determined that the third example of the violation was closed.

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In the licensee's June 30,1997, response letter to the fourth example of the violation,

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the licensee committed to the same corrective actions as the third example to the

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violation. Therefore, the inspectors concluded that the fourth example of the violation

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was closed.

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E8.5 (Closed) Unresolved item 50-416/9705-07: Further review of licensee basis of current

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flood calculation. The inspectors reviewed Calculation CC-01Y23-91015," Probable

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Maximum Precipitation Site Drainage - Water Level and Duration in Area East and West

of Unit 1 Power Block for a 6 Hour Probable Maximum Precipitation Storm." The

purpose of the calculation was to determine the water level versus time history for areas

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surrounding the Unit 1 power block, including the SSW buildings, for a 6-hour storm

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event. The inspectors found that the maximum water levels during peak flows for the

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SSW pump houses were 132.54-feet for the west house and 132.84-feet for the east

house. The inspectors noted that maximum water levels during flooding were lower

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than the 133-foot floor level of the pump houses.

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The inspectors reviewed Supplemental Safety Evaluation Report 6. The NRC reviewed

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the licensee's request to delete Technical Specification 3/4.7.10 and add a requirement

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for an embankment stability verification program in Technical Specification 6.0. The

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change would have relaxed the limiting condition for operation for the specification that

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ensured that Culvert 1 on the plant site would not be blocked. In addition, while the

present specification required action to verify slope stability and clean the culvert, with

an allowed blockage of 15 percent of its own sectional area, the proposed specification

would not require this until the blockage was 45 percent. While the NRC staff

concluded that the change from a specification to a program was not acceptable, the

staff also concluded that the percent blockage for Culvert 1 could be changed from 15 to

45 percent. The NRC staff performed a preliminary analysis and determined that, with

the culvert 100 percent blocked, the flood elevation would reach 134 feet or 1 foot above

the pump house floor level. Due to the 134-foot flood level with the culvert 100 percent

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blocked, the NRC sta'f determined that the Technical Specification remained in effect

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with a maximum culvert blockage of 45 percent. The inspectors reviewed Calculation C-

A-634.0," Probable Maximum Precipitation Site Drainage - Culvert #1 and Subarea

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Hydrographs to Assess the Blockage of Culvert # 1," Revision 1. The inspectors found

that with 45 percent blockage of Culvert 1, the water level would be 132.8-feet, which

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was lower than the floor elevation of the pump house.

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The inspectors reviewed Engineering Request 97/0460, dated August 28,1997, which

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was a design modification that installed 71/2-inch high toe plates completely around the

SSW pumps. The modification was done to ensure that leakage from the pumps,

valves, or roof hatches would not propagate toward the floor mounted e!ectrical

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equipment. In addition, the inspectors reviewed Engineering Request 97/0244, dated

March 18,1997. This engineering request described the problem with the missing

pump seals. The inspectors noted that the engineering request was dispositioned to

rework the seals to assure that the pump bases were sealed. The inspectors walked

down the SSW pump rooms and found that the modification was fully implemented and

the pump bases were sealed. The inspectors observed that, although the pump bases

were resealed, they were no longer necessary since the pumps were completely

enclosed by the toe plates installed by the modification.

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Design Drawing C-1736B, " Units 1 & 2 SSW Cooling Tower Basin Misc. & Embedded

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Steel Sections & Details," Revision 8, specified that a continuous bead of silicone

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sealant be applied around the bases of the SSW pumps. During the 1997 inspection,

the inspectors discovered that the seal was missing from the SSW pumps. The

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licensee did not know when the seals were deleted. The inspectors concluded that the

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missing seals were not safety significant since the flooding calculations indicated the

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water would never reach the SSW pump room floors. This failure constitutes a violation

of minor significance and is not subject to formal enforcement action.

E8.6 (Closed) Insoection Followup Item 50-416/9805-01: Further review of licensee's

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investigation into the loss of control of heavy lift. In conducting this review, the

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inspectors interviewed personnel involved in the event and the investigation and

reviewed the following documents:

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UFSAR Section 9.1.4.2.2.5, " Compliance with NUREG-0612," and Appendix 9D,

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"GGNS Compliance with NUREG-0612, ' Control of Heavy Loads at Nuclear

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Power Plants'"

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NUREG-0612," Control of Heavy Loads at Nuclear Power Plants"

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ANSI N14.6-1978, "American National Standard for Special Lifting Devices for

Shipping Containers Weighing 10,000 pounds (4500 kg) or more for Nuclear

Materials"

Procedure 07-S-05-300," Control and Use of Cranes and Hoists," Revision 104

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Procedure 07-S-05-310," Operation of Containment Polar Crane," Revision 100

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Procedure 01 S-06-2," Conduct of Operations," Revision 104

Procedure STD-FP-1996 7674,"BWR Shroud Inspection Tooting Installation and

Removal," Revision 2

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Engineering Request 98/0209-000. " Plant Staff requested Design Engineenng to

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evaluate the rigging fixtures for the Theta Drive and the R-Z Drive related to the

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Shroud Inspection Program"

Root Cause Analysis Report " Vendor Shroud Inspection Tool Theta Drive and

Ring Partial Release from Tool Strongback," dated August 11,1998

Entergy Operations, Inc. Grand Gulf Nuclear Station Stand-Alone

Contract NGS00456

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With one exception, the description of the event in NRC Inspection Report 50-416/98-05

was accurate. Upon conducting the investigation, the licensee found that the vendor

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provided incorrect weights for the tool ring and the strong back assembly or special

lifting rig. The ring weighed 1130 lbs in lieu of 850 lbs. and the lifting rig weighed

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360 lbs. in lieu of 640 lbs.

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E8.6.1 Procurement of Vendor Services

The licensee's root cause analysis report identified that the theta drive and ring and the

R-Z drive were used twice at Grand Gulf Nuclear Station, during vendor shroud

inspection work that took place during Refueling Outages 7 and 9. This service was

procured through a contractor on the licensee's quality programs list of contractors with

an Entergy approved Appendix B quality assurance program. The only procedures

specifically required to be reviewed in the contract were the nondestructive examination

procedures. The licensee identified that the failure to require that the vendor support

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procedures be submitted for review and approval in accordance with the work control

procedures was a potential contributing cause to the event.

The licensee completed the installation and removal during both refueling outages

through repetitive tasks, which were allowed to be used through the work control

procedure due to the use of previously approved procedures. In this case, the

procedures were approved through the vendor's quality assurance program. When the

equipment was used during Refueling Outage 7, the total weight of the lif ting device and

the ring was less than 1140 lbs. The UFSAR required that administrative controls be

put in place for lifts that weighed less than 1140 lbs. The licensee met these

requirements in Refueling Outage 7 by administratively limiting the weight and height,

depending on whether secondary containment and standby gas treatment systems were

available.

The equipment was modified after being used during Refueling Outage 7 and at another

site in 1996 as a result of lessons learned. The modifications were completed just prior

to Refueling Outage 9. The modifications resulted in increasing the weight of the theta

drive, ring, and lifting device and the R-Z drive and lifting device to greater than

1140 lbs. (1490 lbs. and 1250 lbs., respectively). UFSAR Appendix 9D, Section 9D.3,

stated that heavy loads (loads greater than 1140 lbs.) that can be handled in

accordance with Section 5.1.1 guidelines of NUREG-0612 are not evaluated for load

drop consequences. Any heavy load not handled in accordance with the Section 5.1.1

guidelines is evaluated to determine that the consequences of it dropping are

acceptable per the criteria of NUREG-0612, Section 5.1.

The inspectors noted that the increase in weight to greater than 1140 lbs. invoked

additional requirements that were not addressed in the procurement contract. However,

the contract was developed and the services procured (February 4,1998) before the

modifications to the equipment were completed (in March). The licensee was not aware

of the increase in weight until receipt of contractor Letter SGRR-ES-98-41, Revision 1,

dated April 3,1998. On approximately April 10,1998, licensee personnel observed that

there had been a weight change in the tool to be used during the shroud inspection.

Letter SGRR-ES-98-41, which documented the weight change and a calculation

performed to determine whether the safety factors of the theta drive and R-Z drive lifting

fixtures met the NUREG-0612 guidelines, was forwarded to design engineering via

Engineering Request 98/0209 for evaluation.

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E8.6.2 Enaineerina Evaluation

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The inspectors reviewed the engineering reply to Engineering Request 98/0209.

Procedure 01-S-17-5, " Engineering Request," Revision 6, Section 6.5.3, states that an

engineering reply provides information obtained from existing reference documents or

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standard engineering practices, or elaborates on or interprets existing information, and

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that the engineering reply cannot be used to control actions in the field.

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In the engineering reply, the engineer determined that the engineer licensing documents

(UFSAR) were not affected and a 10 CFR 50.59 safety evaluation was not required.

The reply directed that the drives be handled such that the load path be by the shortest

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route possible and the height be limited to no more than 6 inches above the 808-foot

10-inch floor or the top of any intervening obstruction that may be mounted or staged on

the refueling floor. The inspectors concluded that the screening was a missed

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opportunity to identify UFSAR requirements and that the engineer failed to adhere to the

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directions for developing an engineering reply in that the reply provided direction to

control actions in the field.

The engineering reply found that both loads were greater than 1140 lbs. and had to be

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treated as heavy loads at Grand Gulf. The engineering reply listed the vendor's

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acceptance criteria and assumptions in the calculations and the safety factors the

vendor calculated. The inspectors found that the evaluation detailed the requirements

for safety factors (the factor of safety may be 5 for the Theta drive lifting fixture, but

must be a minimum of 10 for the R-Z drive) and a chain fall hoist because of the lack of

redundancy, as described in NUREG-0612, Section 5.1.6, which deals with single

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failure-proof handling systems. The licensee was not required to meet these criteria,

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per UFSAR Section 9D.2.2, which states that the objective of NUREG-0612 was met

without the need for further action by Grand Gulf regarding Phase 11 (NUREG-0612,

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Section 5.1.2 through 5.1.6).

NUREG-0612, Section 5.1.1(4), requires that the guidelines of ANSI N14.6-1978,

" Standard for Special Lifting Devices for Shipping Containers Weighing 10,000 pounds

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(4500 kg) or More for Nuclear Materials," apply to all special lifting devices which carry

heavy loads over defined areas. In the case of the lift of the shroud inspection tooling,

the total lift weighed greater than 1140 lbs., although, the load being lifted by the special

lifting device weighed less than 1140 lbs. In the engineering reply, the theta ring

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assembly was conservatively considered to be a heavy load. The licensee determined

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that the speciallifting rig met ANSI N14.6-1978 requirements and the requirements of

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NUREG-0612 based solely on a review of the safety factors.

ANSI N14.6-1978 calls out five design criteria, in addition to the safety factors. It also

identifies eight different design considerations. Among these are considering the

problems related to the environment in which the device will operate, ensuring that

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positive locking mechanisms are provided for load-carrying components that could

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become disengaged, and providing a method of retrievalin case of unintentional

disengagement for devices used in pools. In addition to these requirements, design

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considerations to minimize decontamination, the coatings to be used, method of

f abrication, inspection, acceptance testing, maintenance, and assurance of continued

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compliance with the standard were addressed. The inspectors determined that these

criteria were not evaluated or even questioned prior to determining that the vendor

supplied rigging fixture was approved for use.

The inspectors discussed this concern with the engineering supervisor responsible for

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the evaluation. The supervisor explained that not all the requirements of ANSI N14.6-

1978Property "ANSI code" (as page type) with input value "ANSI N14.6-</br></br>1978" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process. were applicable because the load on the lifting rig was less than 1140 lbs. The

inspectors were concerned that the acceptance criteria selected by the engineer were

not identified in an approved procedure or in the design basis and were not approved for

use. In not providing acceptance criteria to evaluate the speciallifting device, evaluating

it in accordance with ANSI N14.6-1978, or providing compensatory measures to address

the lack of evaluation, the inspectors concluded that the licensee jeopardized the

defense-in-depth developed through use of NUREG-0612. The engineering supervisor

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acknowledged that the evaluation was not at the level normally expected by engineering

management. The failure to follow the instructions in Procedure 01-S-17-5 for the

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screening and development of the response to the engineering request was identifiea as

the first example of a violation of 10 CFR Dart 50, Appendix B, Criterion V

(Violation 50-416/9813-02).

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The licensee's root cause analysis report stated that system engineering reviewed the

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engineering reply, the vendor's procedure for the installation and removal of the tooling,

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and Procedures 07-S-05-300 and 07-S-05-310 on April 17,1998, in order to ensure

understanding of the reply and compliance with procedural requirements. This review

was only documented in the root cause analysis report. Based on the direction provided

in the reply and the three procedures, system engineering determined that respective

requirements were met for lift and installation of the vendor shroud inspection tool. The

inspectors considered this an additional missed opportunity to identify discrepancies

with meeting the regulatory requirements and site procedures.

In a subsequent clarification for the evaluation, design engineering addressed the

question "Was the Theta Drive Lifting Rig evaluated for full compliance with

NUREG-0612 and ANSI N14.6-1978 as a special lifting device?" Engineering found that

the device was not a special lifting device because it was not required to carry 1140 lbs.

Engineering personnel failed to question the absence of acceptance criteria for the

lifting device or the weak point created in the defense-in-depth approach. The vendor

did not submit additional information to demonstrate compliance with the other sections

of ANSI N14.6-1978. Engineering personnel found through discussions held during the

investigation that the lifting rig was designed to meet other applicable provisions of

ANSI N14.6-1978. Engineering personnel never requested this information prior to the

event nor evaluated the information further beyond the discussions held. At the close of

the clarification, engineering personnel concluded that the lifting rig was designed and

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tested in a manner consistent with the Grand Gulf commitments to NUREG-0612 and

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ANSI N14.6-1978. The inspectors concluded that the evaluations prior to and after the

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event were inadequate and that engineering personnel did not have a full understanding

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of the requirements of NUREG-0612 or Grand Gulf's commitments to comply with

NUREG-0612.

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E8.6.3 Procedures

The areas required to be satisfied by NUREG-0612 included: (1) safe load path,

(2) procedures for load handling operations for heavy loads, (3) training and qualification

of crane operators, (4) special lifting rigs, (5) lif ting devices that are not specially

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designed, (6) inspection, testing and maintenance guidance for the cranes, and

(7) design guidance fcr the crane. Procedure 07-S-05-300 specifically addressed a

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number of these areas, including the training of operators, inspections and pre-

operation checks for the cranes, and general directions for lifting loads. The procedure

referred to Procedure 07-S-05-310 for overall guidance, but required that loads in

excess of 1140 lbs. have special lift procedures and be handled in accordance with

Section 5.1.1 of NUREG-0612.

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Procedure 07-S-05-310 required that nonstandard heavy loads be directed by the refuel

floor manager or his designee who will have overall responsibility for safe handling of

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the load and that all Safety Class 1 loads have a speciallift procedure. The procedure

)

referred to a list of standard heavy loads in Attachment 1. Attachment I contained a

Zonal Load Restriction Chart which required that loads greater than 1140 lbs. not be

carried over fuelin the reactor cavity without a safety evaluation. In addition, this

procedure defined the different safety classes which Grand Gulf has been approved to

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use in place of safe load paths. The procedure stated that the procedural actions were

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included in the maintenance instructions for each heavy lift, based on the safety class

assignments for the heavy load.

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The inspectors determined that the licensee met the first, third, sixth, and seventh areas

addressed in NUREG-0612, Section 5.1.1, through the two procedures addressed

above. The requirement to have a special lift procedure should have met the second

area. In this case, the procedure was prepared by the vendor and the licensee did not

require that the speciallift procedure be reviewed. Procedure STD-FP-1996 7674 did

not limit the time and the height the load was carried over the area of concern,

contained no inspection requirements or acceptance criteria to be met prior to

movement of the load, and did not address special precautions as required by the

UFSAR and .NUREG-0612. The procedure was a generic procedure developed by the

vendor for use of the vendor's equipment and not reviewed or approved by the licensee

to verify that it met the licensee's regulatory requirements for heavy lifts. The failure to

ensure that a procedure appropriate to the circumstances was used during the heavy lift

was identified as a second example of a failure to meet 10 CFR Part 50, Appendix B,

Criterion V (Violation 50-416/9813-02).

The inspectors questioned whether a safety evaluation had been completed in

accordance with the requirement in Procedure 07-S-05-310, Attachment I, or in

accordance with the requirement in Procedure 01-S-06-24," Safety and Environmental

Evaluations," Revision 103. Section 6.3.1 of this procedure requires that new

procedures with the potential for adversely affecting environment and operation of

structures or components in the UFSAR be reviewed for safety evaluation applicability.

In this case, the installation and removal of heavy test equipment in the reactor had the

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potential to affect the reactor and the fuelif the equipment were dropped. The licensee

explained that no safety evaluation had been done. The failure to perform the

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procedurally required review for safety evaluation applicability was identified as a third

example of a violation of 10 CFR Part 50, Appendix B, Criterion V

(Violation 50-416/9813-02).

As described above, the lift was conducted through the licensee's work control

,

procedures as a repetitive task. In the root cause analysis evaluation, the licensee

identified that the impact statement on the work package had undergone a number of

changes, but that the affects on design basis and safety evaluation required questions

were answered with "NO." The licensee found that the effectiveness of this barrier was

eliminated by the lack of review of the vendor procedure and the belief that the same

work was done in Refueling Outage 7. Procedure 01-S-07-1," Control of Work on Plant

Equipment and Facilities," Revision 32, Section 6.12.2, required that impact statements

be developed and the work scope clearly identify what the activity will involve, a

programmatic statement identifying special needed attention, effects on the design

basis be identified, and 10 CFR 50.59 application be made.

The impact statement dealt specifically with the performance of the reactor vessel

internals inspection. The work scope did not identify that the work would include a

heavy lift over the reactor vessel. The only reference to procedures in the work

instructions was to approved Westinghouse procedures. No instructions or guidance

were provided for the installation of the equipment. The work package was completed

and approved prior to the arrival of the work instructions for the installation of the shroud

inspection equipment onsite. The inspectors concluded that the inadequate description

of the work and inadequate understanding of the activities that were to occur were a

missed opportunity to apply the regulatory requirements for heavy lifts and to possibly

prevent the event.

E8.6.4 Coordination Between Departments

The inspectors discussed the event with the refuel floor supervisor, a senior reactor

operator, who was on the refueling floor at the time that the event occurred. The

supervisor indicated that, through his review of the engineering evaluation, he thought

that the lift was a light lift, not a heavy lift. The inspectors questioned who was

responsible for the lift. The manager explained that the contractor (the contractor's

refuel floor supervisor) was in charge of the lift.

Procedure 07-S-05-300, Section 6.1.3, requires that all Safety Class 1 lifts on the

208-foot elevation be directed by the refuel floor manager or designee who will have

overall responsibility for safe handling of the load. Procedure 01-S-06-2," Conduct of

Operations," Revision 104, Section 6.7.3, required that the refuel floor supervisor

supervise all refueling activities on the containment and auxiliary building refuel floors,

except core alterations. Section 6.7.6 required that the refuel floor supervisor notify the

shift superintendent before the start of any major evolution. Section 6.7.7 required that

the refuel floor supervisor be present on the 208-foot elevation whenever crane and

hoist activities are conducted and that the supervisor was to supervise all lifting activities

with the containment polar crane. During the root cause analysis investigation, the

licensee found that the shift superintendent was not notified at the start of the heavy lift.

The inspectors discussed this concern with a refuel floor manager who was not onsite at

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the time of the event, but was responsible for the root cause analysis investigation. The

manager explained that there was no definition in the procedure for major evolution and

that operation personnel had been informed of the impending lift at the plan-of-the-day

meeting that occurred early in the morning on the day of the event. The failure to

coordinate with the shift superintendent as required in the procedure was identified as

the fourth example of a violation of 10 CFR Part 50, Appendix B, Criterion V

(Violation 50-416/9813-02).

E8.6.5 Roo. t Cause Analysis Report

The inspectors reviewed the licensee's root cause analysis report. The root causes

identified were that the lifting device was not designed to be used under upset

conditions and that there were no formal controls over system restorations or venting

operations during heavy lifts. Contributing causes identified dealt with: (1) failure to

require review of vendor support procedures, failure to clearly define existing

requirements to review vendor documents, and failure to clearly define the relationship

between heavy loads and lifting devices and the multiple procedures which provided

requirements for lifts on the fuel floor; (2) repetitive tasks did not always meet the quality

requirements in the procedure; and (3) the meaning of positive locking in

ANSI N14.6-1978 was not well defined.

The first root cause identified was attributed to the vendor who supplied the equipment.

Procedure 01-S-03-10, "GGNS Condition Report," defined root cause as the

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fundamental cause(s) that, if corrected, would prevent recurrence of an event or

adverse condition. Designing this lifting device for upset conditions would prevent the

specific event that occurred, but would not prevent other heavy lift events. The

corrective action, having design engineering establish criteria for environmental

consideration and lifting device latching mechanisms and incorporating the criteria in

design documentation procedures, would not address the identified root cause or

prevent recurrence. The problem was that the licensee did not conduct sufficient

engineering review prior to allowing use of the equipment onsite. Changing the design

documentation procedures would not prevent a contractor or vendor from modifying

equipment prior to bringing it onsite or from using unqualified equipment. The licensee

,

already had design requirements in place at the time, but the requirements were not

(

adequately applied. Only one criteria, safety factors, out of a number of requirements

was evaluated. The equipment was not designed in accordance with NUREG-0612

because the load did not meet the criteria of a heavy lift when the equipment was initially

designed. The engineering staff did not question this point or request any evaluation

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which may have been done to qualify the equipment. Had engineering conducted a

thorough, questioning evaluation, questions about the acequacy of the equipment may

have been asked and limitations and precautions for its use put in place.

The second root cause dealt with the lack of controls which should have prevented valvo

manipulations from occurring while a heavy lif t was in progress. The conduct of

operations procedure required that the refuel floor supervisor contact the shift

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superintendent prior to a major evolution. This notification did not occur. The inspectors

questioned whether this f ailure was as a result of an inadequacy within the procedures

or a misunderstanding on the part of personnel as to the seriousness of a heavy lift over

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irradiated fuel. The licensee explained that the term " major evolution" was not defined

and that the refueling floor supervision had informed operations supervision in the plan-

of- the-day meeting that the lift was going to occur at some point that morning. The

inspectors noted that the operations staff in the control room were not given the

opportunity to stop work that changed conditions in the vessel because they were not

notified when the evolution began. The inspectors concluded that the root cause and

corrective action did not accurately reflect the problem because the requirements for

coordination were in place in the plant procedures. Personnel did not adhere to the

requirements.

The inspectors reviewed the first contributing cause and found the f ailure to include the

requirements in the purchase contract was potentially a root cause. if the contract had

detailed the requirements applicable to the lift equipment, the vendor would have had an

opportunity to meet those requirements and prevent the event. If the licensee had

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reviewed the contractor's program to ensure that it met NUREG-0612, there would have

been an additional opportunity to identify problems with the equipment, in this case,

however, the licensee was not aware of the change made to the tooling equipment, so

the contract could not have reflected the additional regulatory requirements. The

inspectors found that the corrective actions identified, changing the contracting program

and enhancing the heavy lift requirements, should address the problem and provide an

opportunity for review in the future, but may not have been effective in preventing the

subject event due to the inability of the licensee to predict the change in the equipment.

The inspectors reviewed the second contributing cause, that the work order did not

provide sufficient detail in the impact statement and the vendor procedure was approved

through approval of the vendor's quality assurance program, not the licensee's review

and approval process. The concern in this case was that a regulatory requirement,

meeting the requirements of NUREG-0612 during heavy load lifts, was not understood

or reflected in the package or in the impact statement. The inspectors noted that this

was the last barrier prior to approval of the package for use. The licensee's corrective

actions included evaluating the use of repetitive tasks to perform nonstandard work and

revising procedures and trair;ing. The inspectors observed that the cause determination

did not include the need for personnel to fully understand the scope of the work and to

accurately reflect the full scope of the work in the impact statement, as required by the

procedure.

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The last contributing cause dealt with the details of the positive locking device, which is

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also related to the first root cause, in that the vendor did not consider upset conditions in

the design of the tool. The corrective action was the same as that identified for the first

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contributing cause. The inspectors noted that, prior to the event, licensee engineering

personnel had not considered whether positive locking devices were used or evaluated

whether the design would be effective.

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E8.6.6 Conclusions

The engineering evaluations prior to and after the event involving the near drop of a

heavy load over the reactor were inadequate and engineering personnel did not have a

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full understanding of the requirements of NUREG-0612 or Grand Gulf's commitments to

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comply with NUREG-0612. The engineering screening for this evaluation was

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inadequate and was a missed opportunity to identify UFSAR requirements and the need

to perfc m a safety evaluation. This was identified as an example of failing to follow

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procedures. Three additional examples of a violation for failure to follow procedures

were identified. The examples included the failure to perform a safety evaluation for the

procedure to perform the heavy lift, failure to ensure that adequate special lift

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procedures were developed, and failure to coordinate the heavy lift with the control

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room. The inspectors concluded the root cause analysis report conducted for the event

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involving the near loss of a heavy load over the reactor was less than adequate. The

conclusions reached were narrowly focused and did not comply with the definitions

provided in the corrective action program. The report failed to identify the failure of

personnel to follow procedures or the f ailure of engineering personnel to understand

regulatory requirements that were in place. Both of these failures contributed to the

event and would have to be corrected to prevent recurrence.

E8.7 (Closed) LER 98-003: Core shroud inspection tool theta drive ring became partially

disconnected from its strongback. The inspectors reviewed the voluntary LER

submitted to document the subject event for the interest of the rest of the industry. The

root causes and corrective actions documented were the same as those identified in the

root cause analysis report. The LER did not address the procedure violations identified

in Section E8.6 or provide new information on the event. The inspectors determined

that this LER could be closed due to the discussion in Section E8.6 and the followup

which will be required as a result of the identified violation.

IV. Plant Support

R1

Radiological Protection and Chemistry Controls

R1.1

General Comments (71750)

a.

Inspection Scope (71750)

The inspectors made frequent tours of the radiological controlled area and observed

radiological postings and worker adherence to protective clothing requirements.

b.

Observations and Findinas

Personnel followed radiation protection procedures, locked high radiation doors were

locked, and radiation and contamination areas were properly posted with one exception.

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On October 21,1998, the inspectors noted that a high contamination area posted

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around the refuel floor on the 208-foot elevation of containment was posted so that a 2-

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to 3-foot area was not posted. The refuel bridge support leg was in the center of this

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unposted area. The high contamination area was inside a contamination area and the

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posting changed from the high contamination area to the contamination area at the

refuel bridge support. The inspectors discussed the concern with health physics

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personnel. They explained that the refuel bridge had just been moved to that position to

support modifications being made to it and that the posting had probably been changed

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at that point. The inspectors noted that the space between the rail around the pool and

the post was small, but that one could still get through and not see the posted signs.

The health physics personnel posted the area so that there was no opening. Because

the small space was not posted, the inspectors determined that the posting was an

example of a poor posting practice. The inspectors discussed the concern with the

radiation protection superintendent. He reviewed the area and indicated that part of the

open area was marked with tape. The inspectors reviewed the licensee's guidance on

posting and pointed out that tape alone was only appropriate for small spaces and that

the area posted should be such that equipment was fully in or out of the area to ease

operations. The superintendent acknowledged the concern.

c.

Conclusions

With one exception, observed activities involving radiological controls were well

performed. The inspectors identified one poor posting practice where the posting

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around a high contamination area did not meet the licensee's documented guidance.

R4

Staff Knowledge and Performance

R4.1

Reactor Coolant Samole

a.

Inspection Scope (71750)

The inspectors observed the following to verify that plant chemistry was within Technical

Specifications and procedural limits:

06-CH-1821-0-0002, Reactor Coolant Routine Chemistry

06-CH 1B21-W-0008, Reactor Coolant Dose Equivalent Iodine

=

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b.

Observations and Findinos

On October 7,1998, the inspectors observed reactor coolant routine chemistry and dose

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equivalent iodine sampling and analysis. The technician performing these activities

demonstrated proper concerns for radiological controls and materials handling. The

technician made sure that operations and radiation protection personnel were aware of

the activities being performed. The analyses were performed in accordance with

approved procedures using properly calibrated and standardized laboratory equipment.

The results were entered into the licensee's data tracking system for trending and

analysis. The technician was very knowledgeable of the procedures used and well

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versed on the equipment and analysis techniques used.

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c.

Conclusions

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Routine reactor coolant chemistry and dose equivalent iodine sampling and analysis

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were completed proficiently and in accordtnce with the procedures.

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S1

. Conduct of Security and Safeguards Activities

On a daily basis, the inspectors observed the practices of security personnel and the

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condition of security equipment. Protected and vital area barriers were in good

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condition. The isolation zones were free of obstructions and the protected area

illumination levels were good. The inspectors concluded that the daily security activities

were conducted in a professional manner.

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V. Manaaement Meetinos

X1

Exit Meeting Summary

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The inspectors presented the inspection results to members of licensee management at the

conclusion of the inspection on November 5,1998. The licensee acknowledged the findings

presented.

The inspectors asked the licensee whether any materials examined during the inspection

should be considered proprietary. No proprietary information was identified.

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ATTACHMENT

PARTIAL LIST OF PERSONS CONTACTED

Licensee

C. Bottemiller, Superintendent, Plant Licensing

W. Eaton, Vice President, Grand Gulf Nuclear Station

K. Hughey, Director, Nuclear Safety and Regulatory Affairs

C. Lambert, Director, Design Engineering

J. Roberts, Director, Quality Programs

R. Wilson, Superintendent, Radiation Control

J. Venable, General Manager, Plant Operations

INSPECTION PROCEDURES USED

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IP 37551

Onsite Engineenng

IP 61726

Surveillance Observations

IP 62707

Maintenance Observation

IP 71707

Plant Operations

iP 71750

Plant Support Activities

IP 92903

Followup - Engineering

ITEMS OPENED. CLOSED. AND DISCUSSED

Opened

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50-416/9813-01

VIO

Failure to install temporary restraining cables on floor grating

(Section O2.1).

50-416/9813-02

VIO

Failure to follow procedures resulting in near drop of tool ring

(Section E8.6).

Closed

50-416/9611-01

IFl

Review of the UFSAR description of safety relief va've logic

(Section E8.2).

50-416/9705-02

URI

Lack of leak tests for nonsafety-related to safety-related system

interface valves (Section E8.3).

50-416/9705-06

VIO

Test control deficiencies (Section E8.4).

50-416/9705-07

URI

Further review of licensee basis of current flood calculation

(Section E8.5).

50-416/9805-01

IFl

Further review of licensee's investigation into the loss of control of

heavy lif t (Section E8.6).

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50-416/98-003

LER

Core shroud inspection tool theta drive ring became partially

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disconnected from its strongback (Section E8.7).

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Discussed

50-416/9603-01

IFl

Review long-term justification for methodology and assumed valve

factors (Section E8.1).

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