ML19332C631

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Undated & Unsigned Insp Rept 50-416/89-23 on 890826-0930. Violation Noted.Major Areas Inspected:Operational Safety Verification,Maint & Surveillance Observations,Licensed Operator Training,Action on Previous Insp Findings & ROs
ML19332C631
Person / Time
Site: Grand Gulf Entergy icon.png
Issue date: 10/27/1989
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML19332C627 List:
References
50-416-89-23, NUDOCS 8911280364
Download: ML19332C631 (13)


See also: IR 05000416/1989023

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UNITED STATES

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NUCLEAR REGULATORY COMMISSION

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REGION 11

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101 MARIETTA ET., N.W.

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ATLANTA, GEORGLA 30323

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Report No.:

50-416/89-23

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Licensee: System Energy Resources, Inc.

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Jackson, MS 39205

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Docket No.: 50-416

License No.: NPF-29

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Facility Name: Grand Gulf

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Inspection Conducted: August 26 - September 30, 1989

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Inspectors:

H. D. Christensen, Senior Resident Inspection

Date Signed

P

J. L. Mathis, Resident Inspector

Date Signed

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Approved by'

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F. 5. Cantrell _ Chief

Date 51gned

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Projects Section IB

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Reactor Projects Branch 1

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Division of Reactor Projects

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SUMMARY

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scope:

The resident inspectors conducted a rout'<ne inspection in the area:

operational safety verification, maintenaire observation, surveillance

observation, licensed operator training, action on previous inspection

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findings, meeting with local officials, and- renortable occurrences.

The

-inspectors conducted backshift inspections nn September 4,12, and 15,1989.

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Results*

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Within the ar2as inspected-orie violation with three examples was identified:

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Failure to follow procedures which resulted in the closure of the instrument

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air cross-tie valve, a half scram on reactor protection system division II,

and the inadvertent isolation of the reactor water cleanup system, paragraph 3.

This violation appears to be due to a leck of attention to detail by the

operations and I&C departments.

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REPORT DETAILS

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Persons Contacted

Licensee Employees

J. G. Cesare. Director, Nuclear Licensing

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W. T. Cottle, Vice President of Nuclear Operations

M. L. Crawford, Manager, Nuclear Licensing

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D. G. Cupstid, Manager, Plant Modifications and Construction

  • L. F. Daughtery, Compliance Supervisor

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. J. P. Dinnette, Manager. Plent Maintenance

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S. M. Feith, Director. Quality Programs

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  • C

R. Hutchinson, GGNS General Manager

f. K. Mangan, Director, Plant Projects and Support

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R. H. McAnulty Electrical Superintendent

A. S. McCurdy Technical Asst., Plant Operations Manager

  • L. B. Moulder, Operations Superintendent

W. R. Patterson, Technical Asst., General Manager

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  • J. C. Roberts, Manager, Plant & System Engineering

G. Smith, Superintendent, Chemistry

  • S. F. Tanner, Manager. Quality Services

L. G. Temple, I & C Superintendent

T. G. Tinney, Mech 6nical Superintendent

F. W. Titus, Director, Nuclear Plant Engineering

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M. J. Wright, Manager, Plant Support

  • J. W. Yelverton. Mana5er, Plant Operations
  • G. Zinke, Superintendent, Plant Licensing

Other licensee employees contacted included technicians, operators.

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security force members, and office persennel.

  • Attended exit interview

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2.

Plant Status

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The plant began and ended the inspection period in mode one, power

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operations.

Additionally, the site conducted the annual emergency

exercise on September 27, 1989.

The exercise results will be documented

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in NRC inspection report 50-416/89-25.

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3.

Operational Safety (71707)

The inspectors were cognizant of the overall plant status, and of any

significant safety matters related to plant operations.

Daily discussions

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were held with plant management and various members of the plant operating

staff.

The inspectors made frequent visits to the control room.

Observations included the verification of instrument readings, setp91nts

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and recordings, status of operating systems, tags and clearances on

equipment controis and switches, annunciator alarss, adherence to limiting

conditions for operation, temporary alterations in effect, daily journals

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and data sheet entries, control room manning, and access controls.

This

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inspection activity included numerous informal discussions with operators

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and their supervisors,

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On a weekly basis selected engineered safety feature (ESF) systems were

confirmed operable.

The confirmation was made by verifying that

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accessible valve flow path alignrent was correct, power supply breaker and

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fuse status was correct and instrumentation was operational.

The

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tollowing systems were verified operable: LPCS, HPCS, and SLCS

General plant tours were conducted on a wcekly basis. Portions of the

control building, turbine building, auxiliary building and outside areas

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were visited.

The observations included safety related tagout

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verifications, shift turnovers, sampling programs, housekeeping and

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general plant conditions, the status of fire protection equipment, control

of activities in progress, problem identification systems, and containment

1 solation and the readiness of the onsite emergency response facilities.

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The inspectors observed health physics management involvement and

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awareness of significant plant activities, and observed plant radiation

controls.

Periodically the inspectors verified the adequacy of physical

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security control.

The inspectors reviewed safety related tagout, 892192 (water box vents) to

ensure that the tagout was properly prepared, and performed. Additionally,

the inspectors verified that the tagged components were in the required

position.

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The inspectors have noted that senior plant management makes routine tours

to the plant and the control room.

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The inspector toured the Local Public Document Room for Grand Gulf located

at the Hinds Junior College library near Raymond, Mississippi.

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The inspectors reviewed the activities associated with the events listed

below.

On September 9,1989, during performance of corrective maintenance on

Unit 1 instrunent air compressor, the compressor began to surge and

instrument air header pressure dropped from 125 psig to 90 psig. Unit 2

instrument air compressor was in service to provide instrument air

pressure.

The operators investigated the low air pressure and determined

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that the Unit 2 compressor was unable to supp)ly air to the Unit I air

header because the cross-tie valve (P53F013

was shut.

Further

investigation determined that valve F013 had been closed during the

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past midshift while hanging a Unit 2 instrument air compressor tagout.

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This tagout did not include the cross-tie valve (P63-F013) and the

operator did not inform the shift superintendent or log the valve

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repositioning.

Additionally, the repositioning was contrary to system

operating instruction 04-1-01-P53-1, Instrument Air System, normal

position. . The service air system was available to provide a backup air

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supply if the instrument air header pressure had dropped to 85 psig. The

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licensee has taken the following corrective actions:

The valve position

indication was verified to be operablo

5 warning label was placed next to

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the valve switch and the individual o + ounselled.

The failure to follow

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the requirements of S01 04-1-01-P53-2, is a violation of TS 6.8.1, which

states that written procedures shall be estchlished, implemented and

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maintained. This is example one of violation 89-23-01.

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On September 22, 1909, the reactor recirculation post accident sampling

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valve, B33-F127, motor operator breaker tripped and the motor burned up.

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The licensee notified the resident inspectors that the reactor recircula-

tion post accident sample point was inoperable as required by a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />

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notification comitment.

The motor operator was replaced and the valve

successfully passed the required LLRT on September 24, 1989.

On September 26, 1989, during the perfomance of surveillance

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06-0P-ID75-M-0001, attachment IV. Standby Diese) Generator II, the synchroniza-

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tion control circuit failed.

The 6 amp control fuse had blown. The fuse

was replaced and the surveillance successfully completed.

This failure

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was classified as a non-valid failure.

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On September 26, 1989, the unit received a half scram on division 11 RPS.

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This was caused by an I&C technician performing weekly APRM surveillance

06-IC-1C51-W-0006.

The technician took APRM flow card 'H' test switch to

test when he should have taken AP9fi 'D' test switch to test. A human

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performance evaluation (HPES) was initiated and individual was counselled.

This is the second example of failure to follow procedure and inattention

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to detail, violation 89-23-01.

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On September 29, 1989, during the perfotinance of surveillance

06-lC-1E31-A-1002, Main Steam Line Tunnel, RCIC Steam Pipe Tunnel and RCIC

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Equipment Room High Temperature /High Differential Tenperature Calibration,

an operator inadvertently placed the RWCU isolation bypass switch to the

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" normal" position.

This action resulted in a RWCU isolation.

The

procedure required the RCIC isolation bypass switch be placed in " bypass",

however, the operator repositioned the wrong switch. This is the third

example of failure to fu110w procedure and inattention to detail,

violation 89-23-01.

4.

MaintenanceObservation(62703)

During the reporting period, the inspectors observed portions of the

maintenance activities listed below.

The observations included a review

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of the MW0s and other related documents for adequacy;

dherence to

procedure, proper tagouts, technical specifications, quali 4 controls, and

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radiological controls; observation of work and/or retesting, and specified

retest requirements.

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MWO

DESCRIPTION

EL792

Inspection and calibration of 480

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volts breaker (RFPT B AC Main Oil Pump).

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E95428

Investigate / lower float voltage for

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IE 3 battery bank.

EL1860

Inspection and testing of ITE SKY power

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circuit breaker.

195269

Troubleshoot A recirculation flow control

valve.

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IP5228

FHA pool exhaust recorder calibration.

IN3524

Calibrate turbo oil pressure indicator

(R015A)

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M1062A

Clean PSW side of TBCW beat exchanger.

MA5510

Replace rupture disc on HPCS/RCIC test

return.

M95457

Replace packing to SLCS Pump "B".

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On August 23, 1989, the semi-annual ADS air sample was taken.

The test

results indicated three parameters were out of specification for the

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instrument air supply to ADS. The parameters were total hydrocarbons, dew

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point, and particle count.

NNCR 0270-89 was generated and the evaluation

determined that the condensable hydrocarbons and particle size are within

specification.

However, the dew point was considered to be out of

specification.

A number of actions were recommended to correct the dew

point an evaluation stated that the present dew point should not result in

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moisture condensation in the instrument air system through the month of

November 1989.

The review of corrective action and resolution of the

instrument air dew point out of specification will be an inspector follow

up item 89-23-02.

On September 22, 1989, during troubleshooting of Rosemount trip unit,

1QE22N656, (MWO 195509) 18C technicians discovered air in the sensing

lines.

The technicians vented the high side of the transmitter.

Upon

completion of venting, the shift superintendent performed a functional

test to verify the minimum flow valve was operable.

The functional test

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was performed per S01 04-1-01-E22-1, section 5.2.

At approximately

1:45 a.m. the HPCS pump was started and flow was directed from the CST to

the CST test return.

Valves E22F010 and E22F011 were throttled to

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approximately 30 percent open and the N656 trip unit was verified to

operate properly.

At approximately 1:50, the HPCS pump was secured and

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returned to standby.

Approximately 45 minutes later the auxiliary

building operator reported that the rupture disk on the HPCS/RCIC test

return line was in alam indicating the ruptured disk had blown.

MWO

M95510 was eenerated to inspect / replace the rupture disc.

Upon

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inspecting, IAC found the rupture disc intact but the alarm strip was

broken.

The technician replaced the alarm strip on the rupture disc

indication circuit.

The licensee is investigating what caused the alarm

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strip to break.

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No violations or deviations were identified.

5.

SurveillanceObservation(61726)

The inspectors observed the performance of portions of the surveillances

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listed below.

The observation included a review of the procedure for

technical adequacy, conformance to technical specifications and LCOs;

verification of test instrument calibration; observation of all or part of

the actual surveillances; removal and return to service of the system or

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component; and review of the data for acceptability based upon the

acceptance criteria.

06-IC-IC51-V-003, Revision 26, Source Range Monitor Channel B Calibration.

06-IC-SD17-A-1019, Revision 23, Offgas & Radwaste Building Yentilation

Calibration.

06-IC-1E12-M-005, Revision 24,ContainmentPressure(CTMTSpray)

Functional Test.

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08-S-03-128. Revision 3. Germanian System Calibration.

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06-IC-1E12-M-0002, Revision 25, Containment Spray Time Delay Calibration

and Functional Test,

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No violations or deviations were identified.

6.

LicensedOperatorTraining(41701)

The inspector reviewed procedures and interviewed the operation staff to

assure that controls were adequate to prevent non-licensed or non-

qualified licensed operators from willfully or inadvertently assuming

responsibility for licensed operator duties. Administrative Procedure

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01-S-06-2, Revision 23, Corduct of Operation, designates the operations

superintendent or his designee to verify that the licensee is current in

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the requalification training program.

1he inspector interviewed three

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shift superintendents to ensure they were able to determine the status of

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each of the on-watch operators who were standing a licensed required

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watch.

The shift superinter, dents depend on the operation superintendent

or.his designee to inform them if a licensed operator has failed his

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requalification examination.

Procedure 01-S-06-2, Conduct of Operation,

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states that the training superintendent will noti #y the operations

superintendent per memorandum if an individual does not successfully pass

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requalification training.

The operations superintendent will make

arrangements to remove that individual from licensed duties in a

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reasonable amount of time, i.e., not to exceed seven days from the date of

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notification.

Although it is not proceduralized the training superinten-

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dent calls the operations superintendent or his designee upon notification

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that :n individual failed his requalification examination so that the

individual can be removed from standing shift until he successfully passes

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the requalification examination.

In addition to procedure 01-5-06-2, the

- inspector reviewed the following procedures:

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01-S-04-1, Revision 10

Licensed Operators Training at.d Qualifi-

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cations Program.

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01-S-04-14. Revision 16. Training Records.

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01-S-04-2, Revision 7. Licensed Operator Requalification Training.

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02-5-01-7, Revision 2, Operations Personnel Qualifications.

The above procedures address the notification requirement for individuals

who fail the requalification exams or physical test. The inspector

reviewed the procedures to assure that they provided for an in-depth

defense against both unintentional and willful assumption of a licensed

watch station by an unlicensed or unqualified individual.

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Procedure 01-S-06-2, Revision 23, step 6.2.2.t states," The shift

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superintendent is responsible for training and assessment of assigned crew

members in the perfomance of plant operating procedures and operator

license requirements, and ensuring operators are pursuing their requalifica-

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tions."

Procedure 01-S-04-2 Licensed Operator Requalification Training,

Revision 7. section 6.9.3 states that the operations training supervisor

shall notify operations management when an individual fails to maintain

current or valid status in the requalification training program.

He shall

notify operations management of completion of any assigned accelerated

retraining program. In the procedures reviewed, no requirements existed

that hold the licened operator responsible for reporting disqualifing

conditions to management.

The inspector determined the names of two licensed operators who had

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failed the annual requalification exam in the recent past.

Control room

watch records were reviewed to determine that neither of these individuals

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stood a licensed watch during the time they were disqualified.

In

addition, the control room watch standing verification records were

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reviewed to ascertain whether persons required by administrative

prccedures recorded their qualification watchs.

Procedure 01-S-06-2,

Conduct of Operation should be corrected to indicate that failure of

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requalification' training requires that the individual be removed from

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licensec duties as soon as a replacement can be assigned.

This is

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identified as an inspector followup item (89-23-03).

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7.

ReportableOccurrences(90712&92700)

The event reports listed below were reviewed to determine if the

information provided met the NRC reporting requirements.

The determina-

tion included adequacy of event description and corrective action taken or

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planned, existence of potential generic problems and the relative safety

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significance of each event. Additional inplant reviews and discussions

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with plant personnel as appropriate were conducted for the reports

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indicated by an asterisk. The event reports were reviewed using the

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guidence of the general policy and procedure for NRC enforcement actions,

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regarding licensee identified violations.

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During the inspection period, two LER's were issued.

LER 89-012, Reactor scram due to condenser expansion joint failure,

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LER 89-013, MSIV failed to close due to extruded elastomer seat material.

Both events were documented in NRC Inspection Report 89-19.

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(Closed) LER 88-007, Failure to take the reouired action in technical

specification for inoperable radiation monitor on the standby service

water system.

The licensee revised the log sheets to provide a separate

list of items which can effect technical specification operability.

This

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item is closed.

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(Closed) LER 89-01, Power interruption to ESF bus causes secondary

containment isolation.

The event was discussed in NRC Inspection Report

B9-12, paragraph 8.

No other actions were required. This item is closed.

(Closed) LER 89-04, Shutdown cooling pump trip due to logic power supply

disturbance.

The event is discussed in NRC Inspection Report 89-14

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Paragraph 3.

No other corrective actions were required.

This item is

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closed.

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(Closed) LER 89-011, Missed chemistry surveillence due to personnel error,

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This event was documented in NRC Inspection Report 89-19, paragraph 5.

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The LER will be administrative 1y closed, and the corrective actions

trocked under violation 89-19-01.

No violations or deviations were identified.

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Action on Previous Inspection Findings

(92701,92702)

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(Closed)TI 2515/95, Inspection for Verification of BWR Recirculation Pump

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Trip Multi-Plant Action Item C-02.

The licensee has installed ATWS

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recirculation pump trips.

The trip functions are reactor vessel water

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level and reactor vessel pressure level.

The instrument setpoints and

trip system operability are covered under TS.

This item is closed.

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(Closed) Inspector Followup Item 89-13-03, Develop and implement a program

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to routinely monitor valve performance.

All valves that are required to

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be tested in response to Bulletin 85-03 are scheduled for continued

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monitoring by the maintenance planning and scheduling system.

This item

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is closed.

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(Closed) Inspector Followup Item 88-08-02, Review the evaluation of the

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loose parts monitor alarm.

An engineering evaluation was perforned to

determine the cause of the loose parts alarm.

The evaluation stated the

source was the recirculation loop 8 discharge gate valve (01833F0678). A

radiograph of the valve was perfomed during RFO-3, and no loose parts

were detected.

MNCR 101-80 disposition states the noise is probebly

caused by rattling of the gate valves internal parts due to the force of

the flow through the valve. This item is closed.

(Closed) Inspector followup Item 87-33-02, Review procedures addressing

independent review for radioactive shipment paper work.

Procedure

08-S-06-21, Laundry Handling and Shipment, was revised to include an

independent review by the health physics supervisor. This item is closed.

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(Closed) Violation 89-16-02, Failure to take adequate corrective action to

prevent RCIC system isolation on high steam line flow.

The licensee

confirmed the violation in a letter dated July 27, 1989.

The following

corrective actions have been completed:

The RCIC steam line differential

pressure transmitter damping pots were restored to the covered valve; and

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procedure 01-5-07-8, Control of Permanent Plant I&C Equipment Calibra-

tions, was revised to include administrative controls on damping settings.

This item is closed.

(Closed) Unresolved Item 88-21-01, Review deficiency taggino system

improvements.

Procedure 01-S-06-38, Maintenance Work Order Deficiency

Tagging System, was revised to better document the deficiency tagging with

the maintenance work order process.

The procedure requires that the

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completed maintenance work order have the deficiency tag attached to the

work package.

Additionally, a review of the deficiency tag program is

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performed monthly. This item is closed.

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(Closed) Inspector Followup Item 87-33-01 Review licensee conmitment to

define the plant radiation energy spectrums and revise dose algorithms to

automatically measure and report whole body doses delivered to the lens of

the eyes from radiation identified in the energy spectrums.

Procedure

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08-S-02-49 Dose Calculations, was implemented to provide a method and

' algorithm to translate Panosonic UD-802 TLD response to deep, shallow and

lens of eye dose equivalents and to post this dose to the personnel

exposure data base.

Additionally, the licensee completed a plant

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radiation field characterization study, Document No.88-511.13-64.

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study conducted measurements of plant radiation fieldst describe the

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energy composition of beta radiation fields; and the photon field

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characteristics. This item is closed.

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(Closed) Inspector Followup Item 89-01-01. Evaluation of torque

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requirements for rosemount transmitters (MNCR 006-89).

The licensee

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completed the evaluation of MNCR 006-89 and determined that use of 3/8

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inch bolts torqued to 250 in-lb does not overstress the fastener or reduce

the clamping force required for the rigid mounting of the transmitter.

This item is closed.

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(Closed) Inspector Followup Item 87-01-01, Review controi room human

factor items identified during inspector walkdown. A minor change package

88/1067 has been issued to correct several increment indicators in the

control room and on the remote shutdown panels.

Minor Change Package

88/1052 was completed to expand the range of the suppression pool level

indicators at the remote shutdown panels.

DCP 87/3501 was completed for

human factor upgrades on panels Q1H13-P601 and P864.

The P870 panel

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indicating lights for the lower containment personnel air lock have been

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corrected. This item is closed.

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(Closed) Violation 87-40-01, Failure to perform a differential pressure

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instrumentation calibration on LPCS and LPCI.

The licensee responded to

the violation in letter dated March 23, 1988.

The following corrective

actions have been completed:

Procedure 03-1-01-2, Power Operations, was

revised to require recording of line break base line dato upon reaching

100% power and forwarding this information to system engineering for

evaluation.

This item is closed.

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(Closed) Inspector Followup Item 89-04-02, RCIC system labeling

differences.

The labels or the S0I have been changed to correct the

labeling differences. This item is closed.

(Closed) Inspector Followup Item 89-04-03, Correct RCIC walkdown

deficiencies.

The identified deficiencies were corrected.

This item is

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closed.

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(Closed) Inspector Followup Item 89-07-01, Correct walkdown deficiencies

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on the fire water pump house.

The identified deficiencies have been

corrected. This item is closed,

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(Closed) Inspector Followup Item 89-07-02, Correct HPCS diesel walkdown

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deficiencies.

The identified deficiencies were corrected.

This item is

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closed.

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(Closed) Violation 88-19-01, Failure to follow Administrative Procedure

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01-S-06-1, Protective Tagging System.

The licensee confirmed the

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violation in a letter dated October 31, 1988.

The following corrective

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actions have been completed:

Training on the event was conducted; a

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standing order on the use of power panel breakers for equipment tag-out

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was issued; caution labels were installed in all ESF power panels; and

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procedures were revised to require additional review and caution

statements. This item is closed,

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(Closed) Inspector Followup Item 87-10-08, Evaluate the numerous values

noted, detemine the appropriate value and revise the SDG fuel oil level-

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requirements. A surveillance control room rounds sheet has been developed

to evaluate technical specification accept criteria for diesel generator

fuel oil levels. This item is closed.

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(Closed) Inspector Followup Item 86-17-01, Review the retest requirements

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to check the local indication is functional following maintenance.

Procedure 01-S-07-2, Test and Retest Control, includes a test matrix which

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specifies retest requirements for valve position indications following

maintenance. This item is closed.

!

(Closed) Unresolved Item 88-12-03

Determine if a safety evaluation per

10 CFR 50.59 should have been performed on inadvertent starts of the

Procedure 06-0P-1P75-M-0001, Standby

diesel auxiliary (lube oil pump.SDG) 11 Functional Test, was revised to require testi

'

Diesel Generator

to detemine if the auxiliary lube oil pump suction check valve is

'

properly seated. The licensee determined that a safety evaluation was not

-required. This item is closed.

(Closed) Violation 87-26-01, Failure to document and evaluate the test

discrepancies during standby liquid control system testing.

The licensee

confirmed the violation in a letter dated November 25, 1987.

The

following corrective actions have been completed, procedures were revised,-

!

a MNCR was generated to investigate the problem, a design change was

issued (DCP-85/4053) to increase system operating pressure and training

was-conducted on procedure changes.

This item is closed.

(Closed) Inspector Followup Item 87-01-06, Permanent action to prevent SRV

lifts during trip unit calibration checks.

The licensee installed DCP

87/0037, SRV Ground Voltage Differential Minimization and DCP 87/0038,

,

Relay Coil EMI Diodes.

These DCPs appear to have fixed the SRV lifting

problems during calibration checks.

This item is closed.

9.

Information Meeting with Local Officials (94600)

The resident inspectors met with Claiborne County Board of Supervisors and

Tensas Parish, La. Policy Jury to inform them of the NRC's mission and the

key NRC personnel associated with the facility.

Both meetings were

beneficial.

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10.

Exit Interview (30703)

The inspection scope and findings were summarized on October 2,1989, with

those persons indicated in paragraph 1 above.

The licensee did not

.

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identify as proprietary any of the materials provided to or reviewed by

the inspectors during this inspection. The licensee had no comment on the

following inspection findings:

Item Number

Description and Reference

Violation 89-23-01

Failure to follow procedures with three

examples:

Mispositioning an instrument air

,

valve; a half scram on division II RPS; and

RWCU isolation.

l

IFI 89-23-02

Review corrective actions on instrument air

dew point.

!

IFI 89-23-03

Revise Procedure 01-S-06-2 to require prompt

,

removal of unqualified operator from duty.

,

10. Acronyms and Initialisms

ADHRS-

Alternate Decay Heat Removal System

ADS

Automatic Depressurization System

-

t

ATWS -

Anticipated Transient Without Scram

APRM -

Average Power Range Monitor

Boiling Water Reactor

BWR

-

Control Rod Drive

CRD

-

Design Change Package

DCP

-

Diesel Generator

DG

-

ECCS -

Emergency Core Cooling System

Engineering Safety Feature

ESF

-

Flow Control Valve

FCV

-

HPCS ~

High Pressure Core Spray

i

Hydraulic Power Unit

HPU

-

Instrumentation and Control

18C

-

Inspector Followup Item

IFI

-

Limiting Condition for Operation

LCO

-

Licensee Event Report

LER

-

LLRT -

Local Leak Rate Test

LPCI -

Low Pressure Core Injection

LPCS -

Low Pressure Core Spray

MNCR -

Material Nonconformance Report

MSIV -

Main Steam Isolation Valve

MWO -

Maintenance Work Order

Nuclear Plant Engineering

- NPE

-

Nuclear Regulatory Commission

NRC

-

Pressure Differential Switch

PDS

-

P&ID -

Piping and Instrument Diagram

Plant Service Water

PSW

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ODR

Quality Deficiency Report

-

RCIC -

Reactor Core Isolation Cooling

RF0

Refueling Outage

-

RHR

Residual Heat Removal

-

RPS

Reactor Protection System

-

RWCU -

Reactor Water Cleanup

.-

RWP

Radiation Work Permit

-

SDG

Standby Diesel Generator

-

SERI -

System Energy Resource Incorporation

SLCS -

Standby Liquid Control System

SOI

System Operating Instruction

-

SRV

Safety Relief Valve

-

Standby Service Water

SSW

-

TCN

Temporary Change Notice

-

TS

Technical Specification

-

. _

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_ _ . . . .

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