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{{Adams | |||
| number = ML20207T577 | |||
| issue date = 03/04/1987 | |||
| title = Insp Repts 50-348/87-02 & 50-364/87-02 on 870111-0210. Violation Noted:Failure to Adhere to Approved Procedures During Replacement & Cleaning of Diesel Generator Lube Oil Strainer Elements | |||
| author name = Bonser B, Bradford W, Dance H | |||
| author affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) | |||
| addressee name = | |||
| addressee affiliation = | |||
| docket = 05000348, 05000364 | |||
| license number = | |||
| contact person = | |||
| document report number = 50-348-87-02, 50-348-87-2, 50-364-87-02, 50-364-87-2, NUDOCS 8703240147 | |||
| package number = ML20207T563 | |||
| document type = INSPECTION REPORT, NRC-GENERATED, INSPECTION REPORT, UTILITY, TEXT-INSPECTION & AUDIT & I&E CIRCULARS | |||
| page count = 12 | |||
}} | |||
See also: [[see also::IR 05000348/1987002]] | |||
=Text= | |||
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UNITED STATES - | |||
'p# P K f 7pg'o NUCLEAR REGULATORY, COMMISSION | |||
~ | |||
p [ n REGloN il | |||
g' j 101 M ARIETTA STREET.N.W. | |||
*- '* ATLANTA. GEORGI A 30323 | |||
\..../ | |||
Report Nos.: 50-348/87-02 and 50-364/87-02 | |||
-Licensee: Alabama Power Company - | |||
'600 North 18th Street | |||
Birmingham, AL 35291 | |||
Docket Nos.: 50-348 and 50-364 License Nos.: NPF-2 and NPF-8 | |||
Facility Name: Farley 1 and 2 | |||
Inspection Conducted: January 11 - February 10, 1987 | |||
Inspection at Fa'rley site near Dothan, Alabama | |||
Inspec ' ors: - It' M 7/Y I7 | |||
Date Signed | |||
y W . H. W Bradford | |||
W BT | |||
/ 19 A6k | |||
. Bonse | |||
g/dn | |||
Date Sig ed | |||
Approved by:N | |||
41. C. DanctA | |||
[W | |||
, Section Chief | |||
3 b | |||
Odte Signed | |||
Division of Reactor Projects | |||
SUMMARY | |||
Scope: This routine, onsite inspection included: monthly surveillance observa- | |||
tion, monthly maintenance observation, operational safety verification, engi- | |||
neered safety system inspection, licensee event reports, and onsite follow up | |||
of events. | |||
Results: One violation was identified in that approved procedures were not | |||
adhered to during replacement and cleaning of diesel generator lube oil | |||
strainer elements. | |||
8703240147 870313 | |||
PDR ADOCK 05000348 | |||
G PDR | |||
- i | |||
_- | |||
* | |||
. | |||
. | |||
, | |||
REPORT DETAILS | |||
:1. Licensee Employees Contacted: | |||
J. D. Woodard, General Plant Manager | |||
' | |||
D. N. Morey,. Assistant General Plant Manager ' | |||
_ | |||
W. D. Shipman, Assistant General Plant Manager 'o | |||
'' | |||
R. D. Hill, Operations Manager | |||
C. D. Nesbitt, Technical Manager | |||
R. G. Berryhill, Systems Performance and Planning Manager | |||
L. A. Ward, Maintenance Manager | |||
L. W. Enfinger, Administrative Manager .i | |||
B. Moore, Operations Supervisor | |||
J. E. Odom,. Operations Unit Supervisor | |||
B. W.'Vanland.ingham, Operations Unit Supervisor | |||
T. H. Esteve, Planning Supervisor *- | |||
J. B. Hudspeth, Document Control Supervisor | |||
L. K. Jones, Material Supervisor | |||
R. H. Marlow, Technical Supervisor | |||
L. M. Stinson, Plant Modification Manager | |||
J. K. Osterholtz, Supervisor, Safety Audit Engineeri.,g Review i | |||
Other licensee employees contacted included technicians, operations | |||
personnel, maintenance and I&C personnel, security force members, and | |||
office personnel. | |||
2. Exit Interview | |||
The inspection - scope and findings were summarized during management | |||
interviews throughout the report period and on February 12, 1987, with the | |||
general plant manager and selected members of his staff. The inspection | |||
findings were discussed in detail. One violation is discussed.in parag- | |||
raph 6. The licensee did not identify as proprietary any material | |||
reviewed by the inspector during this inspection. | |||
3. Licensee Action on Previous Enforcement Matters (92702) | |||
Not inspected. | |||
4. Monthly Surveillance Observation (61726) | |||
The inspectors observed and reviewed Technical Specification required | |||
surveillance testing and verified that testing was performed in accordance | |||
with adequate procedures; that test instrumentation was calibrated; that | |||
limiting conditions were met; that test results met acceptance criteria | |||
and were reviewed by personnel other than the individual directing the | |||
test; that any deficiencies identified during the testing were properly | |||
reviewed and resolved by appropriate management personnel; and that | |||
personnel conducting the tests were qualified. The inspector witnessed / | |||
reviewed portions of the following test activities: | |||
_ _ | |||
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1 | |||
9- FNP-2-STP 61.0 .- Reactor Coolant Pump and.RHR Loop Operability | |||
/i/erification. ', | |||
1- | |||
Notor Driven Auxiliary Feedwater Pump Check Valves ' | |||
~FNP-2-STP 22.12 - | |||
L | |||
Flow Verification. | |||
~ | |||
3r FNP-2-STP 27.1 - | |||
A. C. Source Verification. , | |||
t | |||
. | |||
, | |||
FNP-2-STP 27.3 - | |||
Auxiliary and Service Water Building DC | |||
Distribution; ~ | |||
( | |||
\ | |||
FNP-1-STP 227.5B - Radiation Monitor R24A Containment Purge and | |||
Exhaust Isolation Functional Test. t | |||
FNP-2-STP'35.0 - | |||
Reactor Coolant System Pressure and Temperature | |||
Limits Verification. | |||
FNP-2-UOP 1.1 - Startup of Unit from Cold Shutdown to Hot Standby. | |||
's | |||
TNP-2-UOP 1.1A 2 ~ Mode 4' Surveillance Check List. t | |||
Y' y, 1 | |||
No violatibns or deviations were identified.- | |||
s - | |||
~ | |||
'5. Monthly Maintenance Observation (62703) | |||
Station ' maintenance activities of safety-related systems anc' componehts | |||
were observed / reviewed to ascertain that they were conducted in accordance | |||
4 | |||
with approved propadures, regulatory guides, industry codes and standtirds, | |||
4 and were in conformance with technical specifications. 1 | |||
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, | |||
* | |||
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ys The following items were considered during the review: limiting condi- | |||
, | |||
tions for operations aere met while components or systems were removed | |||
S ' | |||
from service; approYsis were obtained prior to initiating the work;- | |||
, j' activities were accomplished using approved procedures and were inspected | |||
i | |||
# - | |||
as applicable; functional testing and/or calibrations were performed prior | |||
to returning components or systems to service; quality control records a | |||
'' | |||
were maintained; activities were accomplished by qualified personnel; | |||
parts and materials were properly certified; radiological controls were | |||
implemented; and fire prevention controls were implemented. Work requestss' | |||
were reviewed to determine the status of outstanding jobs to assure that ' | |||
priority was assigned to safety-related equipment maintenance which may L' | |||
affect system performance. The following maintenance activities were y | |||
observed /rev,iewed: \ | |||
s, . | |||
I | |||
. Unit 2 Excess Letdown Isolation Valve HV 8154 (MWR 145214) | |||
, e ? | |||
. | |||
'28 Steam Generator Manway Cover Repair (MWR 151257[9 . | |||
! . 5 \ 2C W esel Cenerator Maintenance Outage / Lube Oil Strainers and j | |||
1, , | |||
Starting Air. PCN's | |||
- | |||
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d | |||
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- 3' | |||
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- | |||
. 10 and'1A Inverters | |||
<-m' . . | |||
Unit 2~ Plant Vent Stack Monitor Pump - R21 (MWR 145663). | |||
. FNP-0'-MP-28.109 Siemens-Allis 4.16 KV Circuit Breaker PM's | |||
No viola'tions:or deviations were identified. | |||
~ | |||
6. (Operational Safety Verification (71707) | |||
' | |||
' | |||
.The inspectors observed control room operations,_ reviewed applicable logs | |||
and conducted discussions with control; room operators during-.the report: | |||
period. The inspectors verified the operability . of selected emergency | |||
rysta:as, reviewed tagout' records, and' vert fied proper return to service of | |||
a1%3ed ' components. Tours of the auxiliary building, diesel building,- | |||
turme . building and service water structure were conducted to observe | |||
plact equipment conditions, including fluid leaks and excessive vibra- | |||
- tions. De inspector verified compliance' with selected ' Limiting Conditions | |||
~ { | |||
- _ . for. 0pem sons )(LCO) iand results of . selected surveillance tests. The | |||
verifications' were accomplished by direct _ observation- of monitoring | |||
instrumentation, . valve positions, switch positions,. accessible hydraulic | |||
y snubbers; and review of completed logs, records, and chemistry results. | |||
>The licensee's- compliance with LCO action statements were reviewed as | |||
~ | |||
events occurred. | |||
The inspectors routinely attended meetings with certain licensee manage- | |||
: ment and observed various shift turnovers between shift supervisor, shift | |||
foremen and licensed operators. -These meetings and discussions provided a | |||
daily status of plant operations, maintenance, and testing activities in | |||
progress, as well as discussions of significant problems. | |||
'The inspector verified by observation and interviews with security force - | |||
' members that measures taken to - assure the physical protection of the | |||
. facility met current requirements. Ar'eas inspected included the organiza- | |||
' | |||
. tion of the security force; the establishment and maintenance of gates, | |||
doors, and. isolation zones; that access control and badging were proper; | |||
and procedures were followed. | |||
! ' On February 2,1987, while running IC diesel generator (DG) for normal | |||
surveillance, the DG building System Operator (S0) noticed while taking | |||
his ' logs that lube oil strainer differential pressure- (DP) was out of | |||
specification high. The-IC #G strainer DP was 16 psid and the specifi- | |||
' cation is-15 psid. The IC DG was shutdown to change lube oil strainers in | |||
accordance with FNP-0-SOP 38.2 " Changing and Cleaning Lube Oil Strainer On | |||
a D/G." During the process of cleaning the IC DG strainer elements the | |||
~1icensee noticed that the strainer elements had numbers stamped on them | |||
~ | |||
. inappropriate for the 1C DG. S0P 38.2 step 4.3.3 specifies that 1C and 2C | |||
DG's (Fairbanks - Morse) shall use strainer element number 200G (a 74 | |||
micron cylinder) and the 1-2A, 1B and 2B DG's (Colt - Pielstick) shall use | |||
C | |||
'&' | |||
, | |||
-: | |||
t | |||
. | |||
. | |||
4 | |||
strainer element number 2140 (a 40. micron cylinder). Upon further | |||
. investigation- the licensee found incorrect strainer elements in other | |||
DG's. The 1-2A DG had one 2140 strainer element and one 200G. strainer | |||
element installed. 1B DG had two 200G strainer elements installed. 2B DG | |||
had.two 2140 strainer elements installed - both correct; the 2C DG had two | |||
2140 strainer elements and one 200G strainer element installed. A check | |||
by the licensee of some recently completed SOP-38.2 procedures showed that | |||
step 4.3.3 verification of proper strainer element part numbers had been | |||
initialed as complete. | |||
Strainer elements bearing incorrect part numbers were installed in DG lube | |||
oil strainers and strainer element numbers were not verified subsequently | |||
dur.ing cleaning. This is a violation for failure to follow an approved | |||
procedure (348/364-87-02-01). | |||
~The licensee has taken prompt corrective action to prevent reoccurrence of | |||
these errors by changing the procedure to make it clearer .where the | |||
numbers are located on the strainer elements and counseling operators to- | |||
more carefully follow procedures. Also, the licensee has received corre- | |||
spondence from Colt Industries indicating that use of the incorrect | |||
strainers should not be an immediate safety concern on the 1-2A, 1B and 28 | |||
DG's but bearings should be checked during the next diesel maintenance | |||
outage. There is no safety concern on the IC and 2C DG's since they use | |||
the larger mesh strainer. | |||
7. Licensee Event Reports (92700) | |||
The following Licensee Event Reports (LERs) were reviewed ir potential | |||
generic problems to determine trends, to determine wheths.- information | |||
included in the report meets the NRC reporting requirements and to | |||
consider whether the corrective action discussed in the report appears | |||
appropriate. Licensee action, with respect to selected reports, were | |||
reviewed to verify that the event had been reviewed and evaluated by the | |||
licensee as required by the Technical' Specification; that corrective | |||
action was taken by the licensee; and that safety limits, limiting safety | |||
setting and LCOs were no exceeded. The inspector examined selected | |||
incidents' reports, logs and records and interviewed selected personnel. | |||
The following reports are considered closed: | |||
Unit I | |||
LER-83-09 - RHR pump inadvertently secured due to misinterpretation | |||
of instructions. | |||
LER-86-18 - Missed fire watches, personnel error. | |||
LER-86-20 - Special Report: Opening of RCS Pressure Relief Valve. | |||
LER-86-21 - | |||
Special Report: Containment Equipment Hatch non-Functional | |||
as Fire Barrier Longer Than Seven Days. | |||
, . | |||
. | |||
. | |||
5 | |||
, | |||
LER-86-22: | |||
- | |||
Mode change performed with RHR system automatic isolation | |||
capability inoperable (personnel errors). | |||
Unit II | |||
LER-83-11 - | |||
600 volt loud center declared inoperable due to procedural | |||
inadequacy. | |||
-The inspectors had no further questions. | |||
8. -Follow up of_ Plant Events (93702) | |||
On January 13,' 1987 at 7:13 a.m. Unit 'l was ramped down +.o 20%' power and | |||
the generator taken off-line to repair a leaking turbine interface valve. | |||
The valve was replaced and the unit returned to power operation at 2:45 | |||
p.m. | |||
On January 22, 1987 the reactor tripped due to high flux rate as indicated | |||
by nuclear instrumentation channels N41 and N42. The 1A inverter which | |||
supplies power to N41 failed while N42 was in test for surveillance. This- | |||
resulted in a two out of four coincidence for a high flux rate trip. The | |||
testing on N42 was completed and N42 was returned to service. The backup | |||
power supply for N41 was placed in service and the unit returned to power | |||
operation on January 23, 1987. | |||
Unit 2 returned to power operation on January 24, 2987 following a short | |||
maintenance outage. | |||
9. Engineered Safety Systems Inspection-(71710) | |||
The inspector performed a system inspection of the diesel generators. | |||
This inspection included the engine starting air system, engine jacket | |||
cooling water system, service water system alignment in the diesel | |||
generator building. diesel generator building fire protection and detec- | |||
; | |||
tion system, diesei generator building ventilation system, electrical | |||
i switch gear alignment, annunciator response procedures, operating proce- | |||
i dures, operator logs and housekeeping. | |||
l | |||
The systems were assessed to be operable in accordance with the Technical | |||
; Specifications, appropriate drawings, procedures, and the Final Safety | |||
' | |||
Analysis Report. | |||
No violations or deviations were identified. | |||
: | |||
t | |||
i | |||
i | |||
t. . | |||
. | |||
. | |||
6 | |||
10. Enforcement Conference Summary | |||
On February 10, 1987, an Enforcement Conference was held in the offices.of | |||
Region II to discuss the events surrounding the defeat of the- Residual | |||
Heat Removal (RHR) system automatic isolation feature. | |||
' | |||
Mr. L. A. Reyes opened the meeting by reviewing the NRC concerns. | |||
Mr. R. P. Mcdonald gave his introductory statement and Mr. J. D. Woodard | |||
gave a summary of events. Attachment 1 gives the agenda, system drawings | |||
and applicable technical ~ specifications (TS) that were handed out by the | |||
licensee. | |||
, | |||
In the system description Mr. R. D. Hill provided a detailed description | |||
of the RHR system and the Emergency Core Cooling System (ECCS). He | |||
pointed out that the ECCS capability of the RHR subsystem was never | |||
inoperable throughout this event. The valves that were improperly | |||
jumpered are not utilized in the ECCS subsystem loop. The licensee took | |||
exception to the wording used in inspection report 86-29 which referenced | |||
the ECCS subsystem of being inoperable. They defined the problem in the | |||
RHR system rather than ECCS. Additionally, he stressed that although the | |||
automatic RHR isolation circuit was made inoperable, other system | |||
interlocks which remained operable prevented the opening of the valves at | |||
higher pressure. The licensee also expressed concern to the violation | |||
refering to the lack of 10 CFR 50.59 review. The licensee did not agree | |||
that due to a personnel error of not following procedures that inay fail | |||
to perform a 50.59 review of a safety system modification. | |||
Mr. J. D. Woodard gave his concluding remarks in that they believed the | |||
root cause of the event was caused by personnel error. ' They admitted they | |||
violated TS 3.0.3 and 3.0.4, however the significance of the violation | |||
were minimum because the ECCS subsystem would have perform its intended | |||
function. | |||
Mr. R. P. Mcdonald gave his closing remarks that they take seriously all | |||
issues relating to this event and that they will look at the maintenance | |||
activities to see how they can be improved. | |||
Mr. L. A. Reyes thanked the licensee for a well prepared presentation, | |||
that it was very beneficial to all concern and that the matter will be | |||
further reviewed by the Region. | |||
Alabama Power Company Attendees | |||
R. P. Mcdonald, Senior Vice President | |||
J. D. Woodard, Plant Manager | |||
L. A. Ward, Maintenance Manager | |||
J. M. McGowan, Manager Safety Audit & Enigneering Review | |||
R. D. Hill, Operations Manager | |||
T. W. Cherry, I&C Supervisor | |||
L. M. Stinson, Modifications Manager | |||
. .- . - - - . _. - - . | |||
. . | |||
. - | |||
-, _ | |||
- | |||
' | |||
,. | |||
' | |||
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7 | |||
_ | |||
NRC Attendees | |||
L. A. Reyes, Director, Division of Reactor Projects | |||
G. R. lJenkins, . Director, EICS ' | |||
'H. C. Dance, Section Chief, DRP | |||
E. Reeves,-Project Manager, NRR | |||
F. Jape, Section Chief, DRS | |||
' W. H. Bradford, Senior Resident Inspector, Farley | |||
L. P. Modenos, Project Engineer, DRP- | |||
' L. Trocine, Enforcement Specialist | |||
B. Uryc, Enforcement Specialist- | |||
. | |||
' | |||
~ | |||
p-.,.- n - - - - = -ap.c---+, | |||
. | |||
_. Attachment 1 | |||
. | |||
leC ENEGtCDENT CCMFERENCE | |||
FEBRUARY 10, 1987 | |||
SUBJECT: RHR System Automatic Isolation and Interlock capability defeated | |||
11/17/86 - 11/20/86 | |||
Alahnma Power Company Representatives | |||
R. P. Mcdonald (Pat) Senior Vice President | |||
J. D. Woudard (Jack) General Manager-Nuclear Plant | |||
R. D. Hill (Richard) Manager-operations-Nuclear | |||
L. A. Ward (Lewis) Manager-Maintenance-Nuclear | |||
L. M. Stinson (Mike) Manager-Plant Modification & | |||
Maintenance Support | |||
T. W. Cherry (Ten) Plant Supervisor - | |||
Instrumentation & Controls | |||
AGEM R | |||
I Introductions R. P. Mcdonald | |||
II Summary of Events J. D. Woodard | |||
III System Description / Technical | |||
Specifications R. D. Hill | |||
IV Sequence of Events L. M. Stinson | |||
V Immediate Corrective Action L. A. Ward | |||
VI Analysis of Event / L. A. Ward | |||
Administrative Controls | |||
VII Corrective Action J. D. Woodard | |||
VIII NRC Concerns J. D. Woodard | |||
IX Conclusion J. D. Woodard | |||
X Closing Remarks R. P. Mcdonald | |||
. | |||
" | |||
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9 | |||
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RESIDUAL HEAT REMOVAL SYSTEM | |||
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** | |||
EMERCENCY CORE COOLING SYSTEMS | |||
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3/4.5.2 ECCS SUBSYSTEMS - T | |||
avg > 350*F | |||
.. | |||
LIMITING CONDITION FOR OPERATION | |||
3. 5. 2 | |||
Two independent Emergency Core Cooling System (ECCS) subsystems shall be | |||
OPERABLE with each subsystem comprised of: | |||
l | |||
a. One OPERABLE centrifugal charging pump, | |||
b. One OPERABLE residual heat removal heat exchanger, | |||
c. One OPERABLE residual heat removal pump, and | |||
, | |||
d. | |||
An OPERABLE flow path capable of taking suction from the refueling | |||
water storage tank on a safety injection signal and transferring | |||
suction to the containment sump during the recirculation phase of | |||
operatioa. | |||
. | |||
APPLICABILITY: MODES 1, 2 and 3. | |||
ACTION: | |||
, | |||
a. | |||
. With one ECCS subsystem inoperable, restore the inoperable subsystem | |||
. | |||
'~' to OPERABLE status within 72 hours or be in at least HOT STANDBY | |||
N' within the next 6 hours and in HOT SHUTDOWN within the following | |||
, 6 hours. | |||
b. In the event the ECCS is actuated and injects water into the Reactor | |||
Coolant System, a Special Raport shall be prepared and submitted to | |||
, | |||
the Commission pursuant to Specification 6.9.2 within 90 days | |||
describing the circumstances of the actuation and tne total accumu- | |||
lated actuation cycles to date. The current value of the usage | |||
factor for each affected safety infection nozzle shall be provided | |||
in this Special Report whenever its value exceeds 0.70. | |||
. | |||
1 . | |||
* | |||
, . | |||
i | |||
;_, - | |||
FARLEY-UNIT 1 3/4 5-3 AMENDMENT NO. 26 | |||
. | |||
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.- | |||
f | |||
EMERGENCY CORE COOLING SYSTEMS % | |||
- | |||
. | |||
.) | |||
SURVEILLANCE REQUIREMENTS | |||
.~ | |||
4,5.2 Each ECC5 subsystem shall be demonstrated CPERABLE: | |||
. | |||
I | |||
a. At least once per 12 hours by verifying that the following valves | |||
- are in the indicated positions with the disconnect device to the valve | |||
operators locked open: | |||
Valve Number . Valve Function Valve Position | |||
s. 8884, 0886 Charging Pump Closed | |||
, | |||
to RCS Hot Leg | |||
. . | |||
SD 2A, 8U 2B Charging Ptap Open* | |||
b. | |||
discharge isolation | |||
. | |||
I c. 3889 RHR te RCS Hot Closed * | |||
Leg Injection . | |||
b. At least once Mr 31 days by verifying that each valve (manual, | |||
power operatzd or automatic) in the flow path that is not locked, | |||
. sealed, or othenvise secured ic position, is in its correct _) | |||
position. | |||
, | |||
' | |||
_, | |||
l c. By a visual inspection which verifies that no loose debris (rags, | |||
trash, clothing, etc.) is present in the containment which could be | |||
transported to the containment sump and cause restriction of the | |||
pump suctions during LOCA conditions. This visual inspection shall | |||
' - | |||
- | |||
be performed: . | |||
- - . | |||
. | |||
1. For all accessible areas of the containment prict to | |||
establishing CONTAINMENT INTEGRITY, and | |||
. 2. Of the areas affected within containment at the completion of | |||
ephcontainmententrywhenCONTAINMENTINTEGRITYis - | |||
o'stablished. . | |||
* | |||
d. At least once per 18 months by: - | |||
m5 1. VeNfying automatic isolation and interlock action of the | |||
RHR system from the Reactor Coolant System when the Reactor | |||
g:)[ , Coolant Systas pressure is between 700 psig and 750 psig. | |||
2. A visual inspection of the containment sump and verifying that | |||
the subsystem suction inlets are not restricted by debris and | |||
that the sump components (trash racks, screens, inner cages) | |||
are properly installed and show no evidence of structural | |||
distress or corrosion. (3 | |||
* | |||
. . | |||
"Will be verified if charging pump 1A is declared inoperable. | |||
- | |||
AMENDMENT NO. 33 | |||
N | |||
* | |||
3/4 5 4 | |||
}} |
Latest revision as of 13:01, 5 December 2021
ML20207T577 | |
Person / Time | |
---|---|
Site: | Farley |
Issue date: | 03/04/1987 |
From: | Brian Bonser, Bradford W, Dance H NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
To: | |
Shared Package | |
ML20207T563 | List: |
References | |
50-348-87-02, 50-348-87-2, 50-364-87-02, 50-364-87-2, NUDOCS 8703240147 | |
Download: ML20207T577 (12) | |
See also: IR 05000348/1987002
Text
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UNITED STATES -
'p# P K f 7pg'o NUCLEAR REGULATORY, COMMISSION
~
p [ n REGloN il
g' j 101 M ARIETTA STREET.N.W.
- - '* ATLANTA. GEORGI A 30323
\..../
Report Nos.: 50-348/87-02 and 50-364/87-02
-Licensee: Alabama Power Company -
'600 North 18th Street
Birmingham, AL 35291
Docket Nos.: 50-348 and 50-364 License Nos.: NPF-2 and NPF-8
Facility Name: Farley 1 and 2
Inspection Conducted: January 11 - February 10, 1987
Inspection at Fa'rley site near Dothan, Alabama
Inspec ' ors: - It' M 7/Y I7
Date Signed
y W . H. W Bradford
W BT
/ 19 A6k
. Bonse
g/dn
Date Sig ed
Approved by:N
41. C. DanctA
[W
, Section Chief
3 b
Odte Signed
Division of Reactor Projects
SUMMARY
Scope: This routine, onsite inspection included: monthly surveillance observa-
tion, monthly maintenance observation, operational safety verification, engi-
neered safety system inspection, licensee event reports, and onsite follow up
of events.
Results: One violation was identified in that approved procedures were not
adhered to during replacement and cleaning of diesel generator lube oil
strainer elements.
8703240147 870313
PDR ADOCK 05000348
G PDR
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REPORT DETAILS
- 1. Licensee Employees Contacted:
J. D. Woodard, General Plant Manager
'
D. N. Morey,. Assistant General Plant Manager '
_
W. D. Shipman, Assistant General Plant Manager 'o
R. D. Hill, Operations Manager
C. D. Nesbitt, Technical Manager
R. G. Berryhill, Systems Performance and Planning Manager
L. A. Ward, Maintenance Manager
L. W. Enfinger, Administrative Manager .i
B. Moore, Operations Supervisor
J. E. Odom,. Operations Unit Supervisor
B. W.'Vanland.ingham, Operations Unit Supervisor
T. H. Esteve, Planning Supervisor *-
J. B. Hudspeth, Document Control Supervisor
L. K. Jones, Material Supervisor
R. H. Marlow, Technical Supervisor
L. M. Stinson, Plant Modification Manager
J. K. Osterholtz, Supervisor, Safety Audit Engineeri.,g Review i
Other licensee employees contacted included technicians, operations
personnel, maintenance and I&C personnel, security force members, and
office personnel.
2. Exit Interview
The inspection - scope and findings were summarized during management
interviews throughout the report period and on February 12, 1987, with the
general plant manager and selected members of his staff. The inspection
findings were discussed in detail. One violation is discussed.in parag-
raph 6. The licensee did not identify as proprietary any material
reviewed by the inspector during this inspection.
3. Licensee Action on Previous Enforcement Matters (92702)
Not inspected.
4. Monthly Surveillance Observation (61726)
The inspectors observed and reviewed Technical Specification required
surveillance testing and verified that testing was performed in accordance
with adequate procedures; that test instrumentation was calibrated; that
limiting conditions were met; that test results met acceptance criteria
and were reviewed by personnel other than the individual directing the
test; that any deficiencies identified during the testing were properly
reviewed and resolved by appropriate management personnel; and that
personnel conducting the tests were qualified. The inspector witnessed /
reviewed portions of the following test activities:
_ _
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9- FNP-2-STP 61.0 .- Reactor Coolant Pump and.RHR Loop Operability
/i/erification. ',
1-
Notor Driven Auxiliary Feedwater Pump Check Valves '
~FNP-2-STP 22.12 -
L
Flow Verification.
~
3r FNP-2-STP 27.1 -
A. C. Source Verification. ,
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FNP-2-STP 27.3 -
Auxiliary and Service Water Building DC
Distribution; ~
(
\
FNP-1-STP 227.5B - Radiation Monitor R24A Containment Purge and
Exhaust Isolation Functional Test. t
FNP-2-STP'35.0 -
Reactor Coolant System Pressure and Temperature
Limits Verification.
FNP-2-UOP 1.1 - Startup of Unit from Cold Shutdown to Hot Standby.
's
TNP-2-UOP 1.1A 2 ~ Mode 4' Surveillance Check List. t
Y' y, 1
No violatibns or deviations were identified.-
s -
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'5. Monthly Maintenance Observation (62703)
Station ' maintenance activities of safety-related systems anc' componehts
were observed / reviewed to ascertain that they were conducted in accordance
4
with approved propadures, regulatory guides, industry codes and standtirds,
4 and were in conformance with technical specifications. 1
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ys The following items were considered during the review: limiting condi-
,
tions for operations aere met while components or systems were removed
S '
from service; approYsis were obtained prior to initiating the work;-
, j' activities were accomplished using approved procedures and were inspected
i
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as applicable; functional testing and/or calibrations were performed prior
to returning components or systems to service; quality control records a
were maintained; activities were accomplished by qualified personnel;
parts and materials were properly certified; radiological controls were
implemented; and fire prevention controls were implemented. Work requestss'
were reviewed to determine the status of outstanding jobs to assure that '
priority was assigned to safety-related equipment maintenance which may L'
affect system performance. The following maintenance activities were y
observed /rev,iewed: \
s, .
I
. Unit 2 Excess Letdown Isolation Valve HV 8154 (MWR 145214)
, e ?
.
'28 Steam Generator Manway Cover Repair (MWR 151257[9 .
! . 5 \ 2C W esel Cenerator Maintenance Outage / Lube Oil Strainers and j
1, ,
Starting Air. PCN's
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. 10 and'1A Inverters
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Unit 2~ Plant Vent Stack Monitor Pump - R21 (MWR 145663).
. FNP-0'-MP-28.109 Siemens-Allis 4.16 KV Circuit Breaker PM's
No viola'tions:or deviations were identified.
~
6. (Operational Safety Verification (71707)
'
'
.The inspectors observed control room operations,_ reviewed applicable logs
and conducted discussions with control; room operators during-.the report:
period. The inspectors verified the operability . of selected emergency
rysta:as, reviewed tagout' records, and' vert fied proper return to service of
a1%3ed ' components. Tours of the auxiliary building, diesel building,-
turme . building and service water structure were conducted to observe
plact equipment conditions, including fluid leaks and excessive vibra-
- tions. De inspector verified compliance' with selected ' Limiting Conditions
~ {
- _ . for. 0pem sons )(LCO) iand results of . selected surveillance tests. The
verifications' were accomplished by direct _ observation- of monitoring
instrumentation, . valve positions, switch positions,. accessible hydraulic
y snubbers; and review of completed logs, records, and chemistry results.
>The licensee's- compliance with LCO action statements were reviewed as
~
events occurred.
The inspectors routinely attended meetings with certain licensee manage-
- ment and observed various shift turnovers between shift supervisor, shift
foremen and licensed operators. -These meetings and discussions provided a
daily status of plant operations, maintenance, and testing activities in
progress, as well as discussions of significant problems.
'The inspector verified by observation and interviews with security force -
' members that measures taken to - assure the physical protection of the
. facility met current requirements. Ar'eas inspected included the organiza-
'
. tion of the security force; the establishment and maintenance of gates,
doors, and. isolation zones; that access control and badging were proper;
and procedures were followed.
! ' On February 2,1987, while running IC diesel generator (DG) for normal
surveillance, the DG building System Operator (S0) noticed while taking
his ' logs that lube oil strainer differential pressure- (DP) was out of
specification high. The-IC #G strainer DP was 16 psid and the specifi-
' cation is-15 psid. The IC DG was shutdown to change lube oil strainers in
accordance with FNP-0-SOP 38.2 " Changing and Cleaning Lube Oil Strainer On
a D/G." During the process of cleaning the IC DG strainer elements the
~1icensee noticed that the strainer elements had numbers stamped on them
~
. inappropriate for the 1C DG. S0P 38.2 step 4.3.3 specifies that 1C and 2C
DG's (Fairbanks - Morse) shall use strainer element number 200G (a 74
micron cylinder) and the 1-2A, 1B and 2B DG's (Colt - Pielstick) shall use
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strainer element number 2140 (a 40. micron cylinder). Upon further
. investigation- the licensee found incorrect strainer elements in other
DG's. The 1-2A DG had one 2140 strainer element and one 200G. strainer
element installed. 1B DG had two 200G strainer elements installed. 2B DG
had.two 2140 strainer elements installed - both correct; the 2C DG had two
2140 strainer elements and one 200G strainer element installed. A check
by the licensee of some recently completed SOP-38.2 procedures showed that
step 4.3.3 verification of proper strainer element part numbers had been
initialed as complete.
Strainer elements bearing incorrect part numbers were installed in DG lube
oil strainers and strainer element numbers were not verified subsequently
dur.ing cleaning. This is a violation for failure to follow an approved
procedure (348/364-87-02-01).
~The licensee has taken prompt corrective action to prevent reoccurrence of
these errors by changing the procedure to make it clearer .where the
numbers are located on the strainer elements and counseling operators to-
more carefully follow procedures. Also, the licensee has received corre-
spondence from Colt Industries indicating that use of the incorrect
strainers should not be an immediate safety concern on the 1-2A, 1B and 28
DG's but bearings should be checked during the next diesel maintenance
outage. There is no safety concern on the IC and 2C DG's since they use
the larger mesh strainer.
7. Licensee Event Reports (92700)
The following Licensee Event Reports (LERs) were reviewed ir potential
generic problems to determine trends, to determine wheths.- information
included in the report meets the NRC reporting requirements and to
consider whether the corrective action discussed in the report appears
appropriate. Licensee action, with respect to selected reports, were
reviewed to verify that the event had been reviewed and evaluated by the
licensee as required by the Technical' Specification; that corrective
action was taken by the licensee; and that safety limits, limiting safety
setting and LCOs were no exceeded. The inspector examined selected
incidents' reports, logs and records and interviewed selected personnel.
The following reports are considered closed:
Unit I
LER-83-09 - RHR pump inadvertently secured due to misinterpretation
of instructions.
LER-86-18 - Missed fire watches, personnel error.
LER-86-20 - Special Report: Opening of RCS Pressure Relief Valve.
LER-86-21 -
Special Report: Containment Equipment Hatch non-Functional
as Fire Barrier Longer Than Seven Days.
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LER-86-22:
-
Mode change performed with RHR system automatic isolation
capability inoperable (personnel errors).
Unit II
LER-83-11 -
600 volt loud center declared inoperable due to procedural
inadequacy.
-The inspectors had no further questions.
8. -Follow up of_ Plant Events (93702)
On January 13,' 1987 at 7:13 a.m. Unit 'l was ramped down +.o 20%' power and
the generator taken off-line to repair a leaking turbine interface valve.
The valve was replaced and the unit returned to power operation at 2:45
p.m.
On January 22, 1987 the reactor tripped due to high flux rate as indicated
by nuclear instrumentation channels N41 and N42. The 1A inverter which
supplies power to N41 failed while N42 was in test for surveillance. This-
resulted in a two out of four coincidence for a high flux rate trip. The
testing on N42 was completed and N42 was returned to service. The backup
power supply for N41 was placed in service and the unit returned to power
operation on January 23, 1987.
Unit 2 returned to power operation on January 24, 2987 following a short
maintenance outage.
9. Engineered Safety Systems Inspection-(71710)
The inspector performed a system inspection of the diesel generators.
This inspection included the engine starting air system, engine jacket
cooling water system, service water system alignment in the diesel
generator building. diesel generator building fire protection and detec-
tion system, diesei generator building ventilation system, electrical
i switch gear alignment, annunciator response procedures, operating proce-
i dures, operator logs and housekeeping.
l
The systems were assessed to be operable in accordance with the Technical
- Specifications, appropriate drawings, procedures, and the Final Safety
'
Analysis Report.
No violations or deviations were identified.
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10. Enforcement Conference Summary
On February 10, 1987, an Enforcement Conference was held in the offices.of
Region II to discuss the events surrounding the defeat of the- Residual
Heat Removal (RHR) system automatic isolation feature.
'
Mr. L. A. Reyes opened the meeting by reviewing the NRC concerns.
Mr. R. P. Mcdonald gave his introductory statement and Mr. J. D. Woodard
gave a summary of events. Attachment 1 gives the agenda, system drawings
and applicable technical ~ specifications (TS) that were handed out by the
licensee.
,
In the system description Mr. R. D. Hill provided a detailed description
of the RHR system and the Emergency Core Cooling System (ECCS). He
pointed out that the ECCS capability of the RHR subsystem was never
inoperable throughout this event. The valves that were improperly
jumpered are not utilized in the ECCS subsystem loop. The licensee took
exception to the wording used in inspection report 86-29 which referenced
the ECCS subsystem of being inoperable. They defined the problem in the
RHR system rather than ECCS. Additionally, he stressed that although the
automatic RHR isolation circuit was made inoperable, other system
interlocks which remained operable prevented the opening of the valves at
higher pressure. The licensee also expressed concern to the violation
refering to the lack of 10 CFR 50.59 review. The licensee did not agree
that due to a personnel error of not following procedures that inay fail
to perform a 50.59 review of a safety system modification.
Mr. J. D. Woodard gave his concluding remarks in that they believed the
root cause of the event was caused by personnel error. ' They admitted they
violated TS 3.0.3 and 3.0.4, however the significance of the violation
were minimum because the ECCS subsystem would have perform its intended
function.
Mr. R. P. Mcdonald gave his closing remarks that they take seriously all
issues relating to this event and that they will look at the maintenance
activities to see how they can be improved.
Mr. L. A. Reyes thanked the licensee for a well prepared presentation,
that it was very beneficial to all concern and that the matter will be
further reviewed by the Region.
Alabama Power Company Attendees
R. P. Mcdonald, Senior Vice President
J. D. Woodard, Plant Manager
L. A. Ward, Maintenance Manager
J. M. McGowan, Manager Safety Audit & Enigneering Review
R. D. Hill, Operations Manager
T. W. Cherry, I&C Supervisor
L. M. Stinson, Modifications Manager
. .- . - - - . _. - - .
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NRC Attendees
L. A. Reyes, Director, Division of Reactor Projects
G. R. lJenkins, . Director, EICS '
'H. C. Dance, Section Chief, DRP
E. Reeves,-Project Manager, NRR
F. Jape, Section Chief, DRS
' W. H. Bradford, Senior Resident Inspector, Farley
L. P. Modenos, Project Engineer, DRP-
' L. Trocine, Enforcement Specialist
B. Uryc, Enforcement Specialist-
.
'
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_. Attachment 1
.
leC ENEGtCDENT CCMFERENCE
FEBRUARY 10, 1987
SUBJECT: RHR System Automatic Isolation and Interlock capability defeated
11/17/86 - 11/20/86
Alahnma Power Company Representatives
R. P. Mcdonald (Pat) Senior Vice President
J. D. Woudard (Jack) General Manager-Nuclear Plant
R. D. Hill (Richard) Manager-operations-Nuclear
L. A. Ward (Lewis) Manager-Maintenance-Nuclear
L. M. Stinson (Mike) Manager-Plant Modification &
Maintenance Support
T. W. Cherry (Ten) Plant Supervisor -
Instrumentation & Controls
AGEM R
I Introductions R. P. Mcdonald
II Summary of Events J. D. Woodard
III System Description / Technical
Specifications R. D. Hill
IV Sequence of Events L. M. Stinson
V Immediate Corrective Action L. A. Ward
VI Analysis of Event / L. A. Ward
Administrative Controls
VII Corrective Action J. D. Woodard
VIII NRC Concerns J. D. Woodard
IX Conclusion J. D. Woodard
X Closing Remarks R. P. Mcdonald
.
"
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9
'
RESIDUAL HEAT REMOVAL SYSTEM
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EMERCENCY CORE COOLING SYSTEMS
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3/4.5.2 ECCS SUBSYSTEMS - T
avg > 350*F
..
LIMITING CONDITION FOR OPERATION
3. 5. 2
Two independent Emergency Core Cooling System (ECCS) subsystems shall be
OPERABLE with each subsystem comprised of:
l
a. One OPERABLE centrifugal charging pump,
b. One OPERABLE residual heat removal heat exchanger,
c. One OPERABLE residual heat removal pump, and
,
d.
An OPERABLE flow path capable of taking suction from the refueling
water storage tank on a safety injection signal and transferring
suction to the containment sump during the recirculation phase of
operatioa.
.
APPLICABILITY: MODES 1, 2 and 3.
ACTION:
,
a.
. With one ECCS subsystem inoperable, restore the inoperable subsystem
.
'~' to OPERABLE status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or be in at least HOT STANDBY
N' within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in HOT SHUTDOWN within the following
, 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />.
b. In the event the ECCS is actuated and injects water into the Reactor
Coolant System, a Special Raport shall be prepared and submitted to
,
the Commission pursuant to Specification 6.9.2 within 90 days
describing the circumstances of the actuation and tne total accumu-
lated actuation cycles to date. The current value of the usage
factor for each affected safety infection nozzle shall be provided
in this Special Report whenever its value exceeds 0.70.
.
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FARLEY-UNIT 1 3/4 5-3 AMENDMENT NO. 26
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EMERGENCY CORE COOLING SYSTEMS %
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SURVEILLANCE REQUIREMENTS
.~
4,5.2 Each ECC5 subsystem shall be demonstrated CPERABLE:
.
I
a. At least once per 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> by verifying that the following valves
- are in the indicated positions with the disconnect device to the valve
operators locked open:
Valve Number . Valve Function Valve Position
s. 8884, 0886 Charging Pump Closed
,
to RCS Hot Leg
. .
SD 2A, 8U 2B Charging Ptap Open*
b.
discharge isolation
.
I c. 3889 RHR te RCS Hot Closed *
Leg Injection .
b. At least once Mr 31 days by verifying that each valve (manual,
power operatzd or automatic) in the flow path that is not locked,
. sealed, or othenvise secured ic position, is in its correct _)
position.
,
'
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l c. By a visual inspection which verifies that no loose debris (rags,
trash, clothing, etc.) is present in the containment which could be
transported to the containment sump and cause restriction of the
pump suctions during LOCA conditions. This visual inspection shall
' -
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be performed: .
- - .
.
1. For all accessible areas of the containment prict to
establishing CONTAINMENT INTEGRITY, and
. 2. Of the areas affected within containment at the completion of
ephcontainmententrywhenCONTAINMENTINTEGRITYis -
o'stablished. .
d. At least once per 18 months by: -
m5 1. VeNfying automatic isolation and interlock action of the
RHR system from the Reactor Coolant System when the Reactor
g:)[ , Coolant Systas pressure is between 700 psig and 750 psig.
2. A visual inspection of the containment sump and verifying that
the subsystem suction inlets are not restricted by debris and
that the sump components (trash racks, screens, inner cages)
are properly installed and show no evidence of structural
distress or corrosion. (3
. .
"Will be verified if charging pump 1A is declared inoperable.
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AMENDMENT NO. 33
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3/4 5 4