ML20151J351

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Ack Receipt of 880408 & 28 Ltrs Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-482/87-32
ML20151J351
Person / Time
Site: Wolf Creek Wolf Creek Nuclear Operating Corporation icon.png
Issue date: 07/18/1988
From: Callan L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To: Withers B
WOLF CREEK NUCLEAR OPERATING CORP.
References
NUDOCS 8808020231
Download: ML20151J351 (2)


See also: IR 05000482/1987032

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In Reply Refer To: g lg g

Docket: STN 50-482

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Wolf Creek Nuclear Operating Corporation

ATTN: Bart D. Withers

President and Chief Executive Officer

P.O. Box 411

Burlington, Kansas 66839

Gentlernen:

Thank you for your letters of April 8 and April 28, 1988, in response to

our the NRC letter of February 8,1988. This letter acknowledges receipt of

ycJr response to our Safety Systen. Outage Modificetions Inspection (NRC Report

No. 50-482/87-32). We will review the irnplementation of your corrective

actions during a future inspection to detennine that full cortpliance has been

achieved and will be raintained.

Sincerely.

On$3} Db d Q

L J. CALLAN

L. J. Callan, Director

Division of Reactor Projects

cc:

Wolf Creek Nuclear Operating Corporation

ATTN: Otto Maynard, Manager

of Licenst 1

P,0, Box 411

Burlington, Kansas 66839

Wolf Creek Nuclear Operating Corporation

ATTN: Gary Boyer, Plant Manager

P.O. Box 411

Burlington, Kansas 66839

Kansas Corporation Comission

ATTN: Robert D. Elliott, Chief Engineer

Fourth Floor, Docking State Office Building

Topeka, Kansas C6612-1571

Kansas Radiation Control Program Director

RIV:DRP/A C R /A D:DR

ATHowell DDCharrberlain LJCallan

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Wolf Creck Nuclear Operating -2-

Corporation

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Myron karman, ELD, MhBB (1)

RRI R. D. Martin, RA

SectionChief(ORP/A) ORP

RPB-DRSS 8. DeFayette, R!!!

RIV File Callaway, Rill

MIS System RSTS Operator

Project Engineer, DRP/A G. F. Sanborn, E0

Lisa Shea, RM/ALF P. O'Connor, NRR Project Manager

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W$LF CREEK NUCLEAR OPERATING CORPORATION

John.A.

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V. S. Nuclese Regulatory Commission - - -

ATTN: Document Control Desk

Washington, D. C. 20555

,

Reference Letter dated Februsry 8, 1988 from D. M. Crutchfield,

NRC to B. D. Vithars, VCNOC

Subject: D3chet No. 50-482: Inspection Report 50-492/87032-

Safety Systems Outage Modifications Inspectier

Gentlemen

The purpose of this letter is to establish the revised sum itts1 dste for

the response to Inspection Report 50-482/87032 concerning the Safety Systems

Outage Modifications Inspection (SSOMI) conducted at Wolf Creek Generatire

Statior. ksed on discussions with the NR0 Project Manager for Volf Croek

Genorating Station, Volf Creek Nuclear Operating Corporation (VONOC) will

respond to the subject nspection Report on or before April 29, 1998.

The Reference transmitted the SSOMI Inspection Repart and requested a

response to the concerns identified in the Inspection Report. Due to the

length and complex nature of the SSONI Insp<ition Report, VON 00 verbs 11y

requested and receisoi an extension for su Mitting the repsonse to this

Inspection Report.

If you have any questions concerning this matter, please contact me or

Mr. O. L. Maynard of my stsff.

Very truly yours,

t h 1

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.Tohn A. Miley

Vice President

Engineering & Technical Services

JAB /jad

cc B. L. M rt19tt (NRC)

D. M. Crutchfield (NRC)

R. D. Msrtin (NRC)

P. V. O'Connor (NRC), 2

PO Ni 411 i B.svym a 66839 > Fhv4 (316) 364 6831

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April 28, 1988

WM 86-0113 i

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U. S. *iuclear Regulatory Commission

ATTN: Document Cantrol Desk

Vashington. P C. 20555

1

i Reference: 1.etter dated February 8 1986 frota D. M. C r ut ch f i e ltt .

NRC to B. D. Withers, WCNOC

i Subject: Docket No. 50 '.82: Response to Safety Systems

Outage Modifications 1.woection Report 50-482/87032

i,e n c l ern e n :

'

Attached is Wolf Creek Nuclear Operating Corporation's response to the

l Safety Systens Outage Modiiteations Inspection Report transmitted in the

l Referene*. The response provides a description of programmatic and

organizational enhancements made at 'lolf Creek Generating Station subsequent l

l

to the inapection as well as detailel respanses to the spec i fi c findings.

If you hsve any questions concerning this natter. please co1 tact me or

j Mr. O. L. Maynar.1 of my staff.

I

i Very truly yours. ,

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I Bart D. Withers t

i President and i

! Chief E ucutive Ofilter [

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RESPONSE TO

SAFETY SYSTEMS OUTAGE MODIFICATIONS

INSPECTION REPORT

(50-482/87-032)

APRIL 28, 1988

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W$LF CREEK

NUCLEAR OPERATING CORPORATION

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  • INDEE TO SS(MI ITINS L

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] SECTION I - OVERALL CONCLUSIONS fAfg1

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INTRODUCTION 1

MANAGD(ENT CONTROLS 1 i

, ENGINEERING SUPPORT AND EVALUATIONS 2

) CORRECTIVE ACTIONS 3

SUMARY 3

JECTION II

I

l DESIGN AND PROCURDfENT INSPECTION ITDtS

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2.2.2.1 PMR 2024: BATTERY CNARGER AC ALAPM SETPOINT 1

2.1.2.2 PMR 899: ACC'.MULATOR LEVEL TRANSMITTERS 4

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2.1.2.3 PMR 2167: ELECTRICAL EQUIPMENT ROOM No. 1403 CHILLER 6

2.1.2.4 PMR 1634: REACTOR COOLANT DRAIN TANK ISOLATION VALVE 8 .

'

2.1.2.5 PMR 1613
VALVE LEAK 0FF CONTIGURATIONS 11

2.1.2.6 PMR 2109: FEEDWATER VALVE REPLACDiENT * '

2.1.2.7 PMR 2206: AUXILIARY BUILDING FIRE DETECTION SYSTDt 13  !

2.1.2.8 PMR 2222: CONTAINMENT COOLING FAN DAMAGE 16 l

i 2.1.2.9 APPENDIX J LEAK TEST REQUIRDiENTS 18  !

I 2.1.2.10 BATTERY DISCHARGE OF OCTOBER 15, 1987 20 I

! 2.1.2.11 RATTERY SIZING CALCULATION E-3 22  !

l 2.1.2.12 BATTERY PERFORMANCE TEST 24 l

l 2.1.2.13 DC SYSTEM LOV VOLTAGE ALARMS 26 '

2.1.2.14 DIESEL GENERATOR BREAKER OPERATION 27

.

INSTALLATION AND TESTING INSPECTION ITDfS

3.1.2.1 PMR 2262: MARATHON TERMINAL BLOCK REPLACDtENT *

3.1.2.2 PMR 1722: VALVE MOTOR-OPERATOR TESTING 29

3.1.2.3 PMR 1883: HARDLINE SPLICE REPLACDiENT * l

1.1.2.4 PMR 2018: ASCO SOLENOID VALVE REPLACD(ENT 33  !

3.1.2.5 PMR 2329: RAYCHEM SPLICES 36

I 3.1.2.6 PMR 1628: ESV BUILDING CABLE REPLACD(ENT 39

4

3.1.2.7 CONTAINMENT PRESSURE TRANSMITTERS 41

! 3.1.2.8 SAFETY EVALUATIONS * f

3.1.2.9 TECHNICAL SPECIFICATION TESTS 43 t

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! 3.2.2.1 TDiPORARY MODIFICATION TM0 37-120 GK 45

l CLAMPED OPEN CRVIS DAMPER f

1 3.2.2.2 PMR 2106: PRESSURIZER SPRAY VALVE BONNET REPAIR 49  !

l 3.2.2.3 PMR 2084: CCW PIPE VALL THINNING 34

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j 3.2.2.4 PMR 2116: VALVES EF-V090. EF V038. EF.HV47. AND 59

, EF.HV48 HARD SURFACING [

l 3.2.2.5 PMR 1903: REPAIR OF ESV LEAKAGE /VALL THINNING j

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i 3.2.2.6 PMR 0904: ESSENTIAL SERVICE VATER CHECK VALVES 62

{ 3.2.2.7 PMR 1363: CHARGING PUMP CONTROL VALVE CAVITATION 63

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3.2.2.8 SAFETY ANALYSIS REVIEV * i

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j 3.2.2.9 PRESSURIZER SAFETY VALVE TESTING 65  !

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}' *Since no concerns or weaknesses were identified in the Inspection Report. l

l VCNOC has not responded to these items.

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SECTION I

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o Section I

Page 1 of 3

April 28, 1988

01TFRALL CONCLUQlMS,

i INTRODt/CTION

During the second refueling outage at Wolf Creek Generating Station, a Safety

Systems Outage Modifications InJpection (SSOHI) was conducted by the NRC's

Office of Nuclear Reactor Regulation, The SSOMI was completed in two

portions. The first portion dealing with Design and Procurement was conducted

on November 2-13, 1987, while the second portion dealing with Installation and

Testing was conducted on November 9-20,1987.

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The SSOMI identified both strengths and weaknesses in the modification

activities that were performed at Volf Creek Generating Station (VCGS). These

findings were documented and transmitted to Wolf Creek Nuclear Operating

Corporation (VCHOC) in NRC Inspection Report 50-482/87032. This Inspection

j Report stated that, 'The modification activities inspected by the SS0MI team

during the Wolf Creek outage, including procedures, installed equipment and

materials, and workmanship by crafts, were generally in accordance with NRC

requirements and licensee commitments'. In addition, specific strength were

noted related to, '

...the acquisition and control of equipment and materials,

the trend analysis of quality findings and reported deficiencies, and

worknanship by maintenance personnel * .

l The Executive Su= mary of the Inspection Report also identified weaknesses in

i the general areas of Management Controls Engineering Support and Evaluations,

i and Corrective Actions. Each of these areas is specifically addressed in

] Section I of VCNOC's response to the Inspection Report. Section II of VCNOC's

! response presente a detailed response to each of the SSCMI team findings

categorized as either a weakness or concern.

It should be noted that findings categorized as strengths hsve been omitted

from Section II. Each finding in Section II is presented with a Restatement

of the Finding, a General Discussion of the Finding, a Response to the

Finding, Actions Taken, and Conclusions based on the Finding.

MANAGD4ENT CONTROLS

As stated in URC Inspection Report 87-032, Safety Systems Outage Hodification

Inspection. ' modification activities inspected by the SSCHI team during the i

Wolf Creek outage, including procedures, installed equipment and materials,

and workasnship by crafts, were generally in accordt'ce with NRC requirements  !

and licensee connitments' . However, as a result or w'CNOC management concern )

with regard to the significant operational events that occurred during VCGS's (

second refueling outage and individual issues identified by the NRC, VCNOC has  ;

, instituted several organizational enhancements to alleviate any perceived '

weaknesses in VCN00's overall management control.

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In order to more closely control day to day work activities during outages. (

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the Outage Manager will report to the Plant Manager rather than the

Vice-President Nuclear Opetations. The Outage Manager's function and

authority will be clearly reflected in Administrative Procedures. The Outage

Manager will have a support staff consisting of Scheduling personnel and two

Senior Technical personvel.

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Page 2 of 3

April 28, 1988

As an improvement to the Maintenance Organization, Maintenance has been

combined with Facilities and Modifications ta form an organization titled

Maintenance and Modifications. This organizational change combines all

maintenance activities under a single manager and creates a large skilled

labor pool to be used on any maintenance or modifics. tion task. In context

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with this change, significant management attention has been focused on ,

assuring that unneceriary levels of supervision have been eliminated and

establishing more direct management control in all work activities within

Maintenance and Hodifications.

In additior, to theso organizational enhancaments, VCNCC Management formally

restated to all personnel the importance of strict adherence to written

procedures during the performance of work activities, testing, equipment

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repair, and plant modifications. This is being reinforced by mandatory

pru-work briefings. Daily management meetings have been established to ensure

1 direct management control and supervision of all ongoing work activities.

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To eahance corcur.ications and provide more managtment involvement in

day-to-day activities, the daily planning meeting has been restructured to

focus more on problems and corrective actions than on work status. The

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meeting is attended primarily by management persor.nel to provide the necessary  ;

level of authority to resolve problems and take necessary corrective actions. l

The meeting is normally attended by one or more of the Corporate Officers to

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provide senior management support,

j The above organizational modifications and programatic enhancements will  ;

strengthen the performance of WCNOC and subsequently VCGS. These actions >

should minimite the potential for operational or management weaknesses during

future outages at VCGS. The individual examples identified in this section ,

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are fully discussed in other sections of this response to NRC Inspection i

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Report 50-482/87032.  ;

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ENGINEERINO SUPPORT AND EVALUATIONS l

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i NRC Inspection Report 50-462/87032 made the statement that. 'The engineering ;

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support provided for a number of recent modifications and maintenance  ;

. activities was found to be inaccurate or lacking in thoroughness.'. ,

The Inspection Report also stated that, 'The SSCMI team found that modified !

designs were traceable to the original design bases and regulatory

! requirements, that correct design information was utilized, and that

applicable design controls were iuple: rented. ' It should be noted that the

activities discusseo as engineering scpport in the Inspection Report include ,

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activities which are performed by different organizations within WCNOC and not ,

just the design engineering group. Engineering sopport for day-to day I

operational and maintenance activities is performed by various groups under

the Plant Staff. Engineering support for modifications and other design

activities are performed by Nuclear Plant Engineering (NPE). ,

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The organizational enhancements and increased m.anagement involvement discussed l

in the Management Controls section of this response will improve the support  !

activities being performed by the enginee_ing groups. The interaction between

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organizations in the dr.ily management notings will help to focus efforts into

] a singlo direction so that each organization is aware of what is required to

accomplish any given task. In addition, these meetings ensure that individual

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Page 3 of 3

April 28, 1988

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work assignments are being performed by the organization with the proper

experience and expertise to accomplish the task in the most effective manner. t

WCNOC believes that with this strong foundation in the design area along with

enhancements made because of events during the second refueling outage and

items identified by the $50MI team, the weaknesses identified by the SSCHI

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inspection in the engineering support and evaluations area will not reoccur at

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Volf Creek Generating Station.

CORRECTIVE ACTIONS  !

NRC Inspection Rep 0rt 87-332 idtntified several examples which indicate

weakness involving the adequacy of corrective actions for identified

l deficiencies, including the identification of root causes, evaluation of

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related areas for similar deficiencies, and actions to prevent recurrence. It

should be noted that an earlier NRC Inspection concerning corrective action i

j was conducted during the periods May 18 22, and June 2-3, 1987. Upon t

l receiving this NRC Inspection Report. 87 011, on November 3, 1987 VCNOC took ,

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steps to enhance the corrective action program as documented in letter WH l

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88 0028, dated January 29, 1988. An integrated corrective action program in t

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the form of a VCU0C General Procedure. KGP.1210, ' Corrective Action for

Progracmatic and Implementation Deficiencies', has been developed. The

! procedure establishes a standardized method for all VCNOC organizations to

document tnd respond to progracnatic or implementation quality problems. i

During a VCNCC Quality Department audit conducted between December, 1987 and  !

February, 1988, concerning the implementation of this procedure, several i

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inconsistencies were identified in the methods variouJ organizations were

using to implement the proceiural requirements. This has resulted in a g

complete review of KGP-1210. The procedure is currently being revised to (

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provida plant personnel with a more usable explanation of determination of

root causes. It is expected that the revision to KGP-1210 should be

tw91emented by June 1, 1988. A training program is currently under I

development to provide direction to the peruonnel responsible for i

implementation of the revised FGP 1210. In addition, a seminar by EG&G on

' Accident Investigation', is schedu14d to be conducted at the Volf Creek l

Generating Station during Hay, 1988. The above noted revisaon to KGP-1210  :

and training will serve to strengthen the overall corrective action program of [

VCNOC.  ;

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StHuARY

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VCNOC believes the actions described above in conjunction with the specific

actions described in Section II of this response fully address the weaknesses

identified by the SSCHI Inspection Report. It is acknowledged that during the

SSOMI review of modification activitias and significant operational events {,

several specific weaknesses were identified, however, VCNOC believes chat the l

overall organization and program enhancements described above will serve to [

optimize the present and future operation of VCGS. [

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SECTION II

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Page 1 of 70  !

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1 2.1.2.1 PHE 2024: BATTERY CEARGER AC ALARM SETPOINT

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FINDING

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Thie PHR changed the battery charger AC input alarm setpoints to eliminate [

spurious AC alarms and was required because of previous changes to the AC i

system made it.1985 by PMR IMS which reduced the AC input voltage at selected }

safety related and non-safety related battery chargors. PMR 2024 indicated r

that the cause of spurious AC undervoltage alarms was an incorrect voltage [

transformation ratio assumed in the original system Relay Setting Calculation

) (H.12). A review of the latest revision to this calculation indicated that

k the transformation ratio was corrected in April 1983. The correct voltage  !

l transformation ratios were indicated for nine of the eleven battery chargers  !

! on Relay setting Tabulation Drawing E.11028(Q) issued in June 1984, however

] the new relay settings had not been added at that time.

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The SSOHI team reviewed Bechtel Voltage calculation (8 8). which was the basis

l of PMR 1345, searching for other possible reasons for the spurious

j undervoltage clarms. The impedance data used as a calculational input for one t

! of the safety reined load unter transformers was based upon General Electric (

i test data. however this impedance value did not agree with the transformer's t

l nameplate data. Engineering Department personnel indicated that although the [

q test data used in the calculation was not specific to the equipment installed i

! at Wolf Creek Generating Station (WCGS), the error accounted for a calculated  !

voltage error of lese than two percent. The STOMI team considered that the  !

failure to identify the error in the 3echtel Voltage Calculation is indicative  :

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of a weakness in engineering evaluations. [

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) CENERAL DIFCUSSION OF FINDING:

puring the review of PMR 2024 TMR 1345 system relay calculation N 12

l vn1tage calculation 8 8 and relay setting Tabulations (Dr& wings E.11027 and

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i E 11028(Q)) The S$0HI team identified two distinct concerns

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! 1. Corrections made in June 1983 to Calcula', ions H.12 and 8 13 concerning

3 battery charger low AC input voltage alarms and potential transformer

l ratios, were only partially incorporated into relay setting tabulations

j E 11027 and E 11028(Q) during the June, 1984 rev;sion to those

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documents.

2. The impedance data used in Calculatten 3 8 for one of the load center  ;

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transformers was based on the manufacturers test data which does not

agree with the transformer naceplate.

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I RESPONSE TO THE FINDING:

1. The corrections made in the subject calculations identified a lower  ;

j setpoint value for the battery charger low AC input voltage. It is j

l important to note that the purpose of the alarm is to alert the Control

l Roca operators to low AC input voltage on the battery chargers. The

i original setting provided for proper monitoring of the electrical

] distribution system at Wolf Creek Generation Station. It is good

engineering practice to not eliminate the conservatism in the system

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Page 2 of 70

April 28. 1988

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j design setting on the sole basis that a revision to a design esiculation

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identifies additional available margin. Therefore at the time of the

calculation revision, the new setpoints calculated did act need to be

incorporated into the setpoint documents for Wolf Creek. Only after the

ala rms became frequent due to the implementation of PHR 1345. which

optimized the transformer saps for the Wolf Creek Electrical

Distribution System. did a need arise to reduce the alarm setting to the

value identified in the previously revised design calculation.

] It is true that for tem of the eleven battery charger control power

, transformers, the subject setpoint document listed the wrong

] transformation ratios. These two chargers were added as design

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enhancements during 1982. The oversight was corrected promptly when

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discovated but did not affect the conservatism of the alarm setpoint.

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2. The transformer manufacturers test data and certified test data report

which were used as a basis for the subject Voltage Calculation B.8 are

a judged to be kccurate as issued. The subject certified test data

i report reflects the actual results of a performance test on the

1 installed equipment as certified by the manufacturer. It is noteworthy

! that the equipment serial number recorded on the test data and to

! which the referenced calculation refers, also matches the serial number

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stamped on the transformer nameplate. Therefore, the test data and

i calculation are applicable and specific to th: transformer installed at

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Volf Creek. In addition, at the time the transformer was procured. the

nameplate was not required to reflect the values recorded on the

certified test report (reference ANSI C57.12.80 1973) and therefore,

only reflected the design impecance value. It was, in more recent

revisions, that the applicable industry standards for transformers (501

KVA and larger) required that tne actual test data be reflected on the

nameplate.

M c WsION:

1. The $$CMI team identkfied that there were two incorrect non.1E battery

potential transformer ratios on the applica'le o Relay Setting Tabulation

drawing. However, these errors are not considered reflective of general

engineering weakness and were corrected when discovered. The item

concerning the lack of incorporation of the revised calculation into

the applicable Relay Setting Tabulation for the battery chargers is not

considered a deficiency. The fact that the input voltage lov alarm

retpoint was 94! ton a 480 volt base) instead of the 902 value,

determined by the design calculation is considered conservative. These

types of rargins are not utiliaed unless necessary in order to maintain

the carimum safety margin for protection systems at Volf Cregk Generating

Station. This approach deconstrates a strength in engineering

evaluations, and therefore, requires no further action.

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Page 3 of 70 ,

l April 28. 1988

i 2. The $$ CHI team item concerning engineering's failure to identify an

apparent error in Voltage Calculation B.8 due to data inconsistencies i'

between transformer nameplate data and certified vendor test reporte

I does not constitute a deficiency. The subject Calculstion. 38 as well

i as the cited certified vendor test report data, at. considered correct ,

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and applicable to the trantformer installed. At the time the transformer [

was procured, the nameplate was not required to reflect the values

recorded on the certified test report (reference ANSI C57.12.40 1973) and i

4 therefore, only reflected the design impedance value. It was. in more

1 recent revisions. that the applicable industry standards for transformers .

(301 KVA and larger) required that the actual test data be refiscted on  !

the nameplate. Therefore, no further action is required and no revision  !

to these documents or the transformer nameplate is required. l

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Section II

Page 4 of 70

April 28, 1988

2.1.2.2 FMR 899: ACCUMUI.ATOR LEVEL TRAN8MITTFIS

FINDING

This PKK replaced Accumulator Tank Barton level transmitters with Rtsemount

level transmitters and relocated them to the side of the tank us.ng the

existing sensor taps. The $$CMI team identified the following discrepancies

with this PMR

a. The new sensor connections to the reference leg were five feet higher,

which provided an additions 1 41.36 cubic feet of water in the tank at the

minimum level setpoint than designed. As a result, a sraller volume of

nitrogen gas remainwd in the Accumulator Tank to provide for water

injection into the primary system in the event of a LOCA. The Technical

Specifications required that a minimum of 818 cubic feet of water be

I

injected from the tank into the primary system in the event of a LOCA.

l The actual tank pressure required with the new volume of water was not

determined. The dasign nitrogen gas pressure of 585 peig had some

allowance for conservatism, however this allowance was also unknown.

b. A root cause analysis for changiag the level transmittera was not

provided. Although a significant amount of data existed te stify the

change, this data had not been formally communicated within e e company.

In addition, the Q. list, which lists all safety related equipment in the

plant, was not revised as required.

The failure to evaluate the change in nitrogen gas pressure required for

Accumulator Tank injection, including calculation of the root cause for the

modification is a weakness in the engineering area.

ctNEPAL DISCUSSION OF FINDINO:

a. The design modification stipulated in FMR 899 called for utilization of

the same tank taps. stanopipe taps, and diaphragm seal locations as the

original installation. The replacement Rosemount transmitters were

relocated to a lover elevation than the Bartons (approximately 5 feet to

17 feet difference depending on transmitter) and are now placed at the

f midpoint between the diaphragm seals rather than above the upper seal,

b. Many letters were written as a result of the Barton instrument problems

identified at VCGS. The responsible engineer's correspondence file on the

subject was turned over to the SSCMI team for review. Although this file

did not contain all the project correspondence, it did include the minutes

of a meeting held at Volf Creek on January 25 1984, with representatives

in attendance from KGLE (including the Project Director). Union Electric.

Vestinghouse. !TT Barton, and Nuclear Projects Incorporated. During this

meeting. KGLElUE failures were discussed, including failure modes. and

acticn plans were established.

A review of the FMR package indicates that Q. List Change Notices were part

of the package and were referenced on the Modification Document Form

(KGF.6). Neither the $$CMI team nor the responsible engineer located the

Change Notices in the copy of the package provided to the SSCMI team.

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RESPONSE TO TifE FINDING [

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a. Since the tap connections and diaphragm seal locations were unchanged, the {

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original tank level setpoint calculations remain valid. The replacement

of a transmitter as well as its relocation from above the upper diaphragm f

seal to the seal midpoint would result in the need for calibration. This  !

was performed by Instrumentation and Controls personnel for PHR 899 in

accordance with STS IC-908A ' Channel Calibration Accumulator Level [

Tsensmitters'. These actions result in the tank watvr content remaining  ;

the same as prior to the modificat2on and being within the Technica1

Specification l

bounds. No engineering reanalysis of the effect of r

increased water content was necessary. l

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b. The January 25,

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1984 meeting minutes and other correspondence such as a

January 27, 1984 le*.ter from John Ba;1cy of the Wolf Creek project to (

Kent Brown. KG63 Vice. President (subject Barton Transmitter problems  ;

and intended soluttens) clearly show that ransgement and the project }

as a whole was being informed of the Barton transmitter problem. j

During discussions between the $50HI team and the responsible engineer.

it was z.entioned that Q. List change documents did not exist for the newly ,

installed tracimitters. The responsible engineer could not remember (

generating such documents and thus acknowledged the co9cern. A review of ,

the FMR package was undertaken a,; a result of this finding revealed that  !

the Q-List Change Notices did exist.  !

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00NCt.USION:  ;

a. No changes were made to the system which would require a new analysis.

VCNOC does not consider this item to be a deficiency.

b. VCNOC believes that the project. including upper management. was aware

of the problem with Barton transmitters. and that existing documents j

indicate that a root cause determination was sought as a part of [

resolving the issue. The FMR package does contain an appropriate Q. List [

Change Notice. i

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April 28, 1980

2.1.2.3 Pte 21671 ELECTRICAL FOUTIMENT ROOH NO. 1403 CHILLER

FINDINot

This FMR added additional cooling to Electrical Equipment Room No. 1403 and

installed a room temperr.ture iridicator controller and an automatic chiller

water control valve. ?!C 185 and TV 185, respectively. A Field Change Request

(TCR) was subsequently issued to delete TIC 185 and TV 125 and to add a manual

globe valve. V150. Tgeshangerequiredtheoperatortomanuallycontrolthe

Ecom temperature to 75 F 3,4"F by adjusting valve V150. This installation of  ;

a manual valve was inadequate because a tuperature indicator was not provided

to measure the temperature of Room 1603, the TS surveillance procedures did

not include this room for periodic surveillance and the room was not required

to be monitored for gnvironmental conditions. In addition, the basis for the

acceptability of 75 T was not addressed. The failure to evaluate the effect

of the FCR change on the PMR anc the failure to document the basis for the

design change is an example of a general weakness in the engineering area.

GENTRAL DISCUS,5 ION OF FINMNG t, l

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In Item 2.1.2.3 the S$ CHI teau determined that the installation of a manual

valve (via an FCR) was inadaquate because a temposature indicator was not

provided to measure the temperature of Room 140). the surveillance

procedures did not include this room for periodic surveillance and the room  ;

was not required to be monitored for er.vironmental conditio is. Inagdition '

the $$ CHI team advised that the basis for the acceptability of 75 F room i

temperature was not addressed in the FMR. The $$0MI Team indicated that [

failure to evaluate the effect of the TCR change on the iMR and the failure l

to document the basic for the design change is an example of general r

l veakness in the engineering area, i

RgSPONSE to THF FINDING

l

FMR 2167 was revised, as requested by TCR 02167 F.009 because of natorial [

unavailability. to allow the temporary replacement of the three way flow i

control valve GL.TV.185 with a e.anual globe valve. The disposition of the  !

subject TCR stated that the aforementioned globe valve 'shall' be replaced k

with the three.vay flow centson valve upcn availability. Although the  ;

three vay valve has been received but not yet installed. THR 2167 hse been

i revised and reissued to pcovide for the installation of the three.vay

valve. Additionally, in the interim the disposition stated that the room [

l temperature was to be frequently nonitored and the globe valve adjusted to

e.aintain the room design temperature. T h '. s was to be acceeplished. >

once the unit had been placed in service, by the Auxiliary luilding operator  !

,

at least once per shift 6nd documented per ACM 02 030 'bading Sheets and

l Shift Round Instructions Checklist'. At the t iu of the SSCMI. the l

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additional fan coil unit had not been placM in service. This revision to the ,

I design package demonstrates not a weakness in engineering, rather, an (

l engineering strength. Additionally. an installed temperature indicator is not l

varranted for the temporary use of the globe ealve. l

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The Techn(cal Specification surveillance requirements do not address the  !

area temperature monitoring f nr the roarn, because this roem is considered a  !

mild environment as defined in USAR Page 3.11(3).29. [

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April 28, 1988  ;

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The air handling unit ( SGLO2) for the room and its associated power and

control are not safety related as there are no safety design based

associated with the system. The additional f an.'cott unit SGL20 was added to

operate An parallel with the original $GLO2 unit to provide increased

neoling capability for tha room. The reason that the design change was  !

assued, was to provide for th: installation of a room cooler that would j

provide cool air in the vicinity of the non-safety related, yet temperature  !

sensitive. Full Length Pod Control Cabinet. An evaluatien of the cooling .

load for the room was conducted as well as for the heat sensitive rull

Length Rod Control Caninet. The Engineering evaluation included the review  !

of existing supplier documentation for the cabinet. and the performance of a

calculation to deternine the cooling capacity requitad of the new unit.

The basis for the design change van documented or, ~ m- PHR cover sheet form.

with further supporting documentation (i.e.

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c3.ulations. suppliar

documentation) existing as backup information, testinghouse documentation l

provided inforg.ation that the preferred temperature would be l

spgroxingtely 77 F. but not to exceed 30-104, ambient F. This was the basis for the  !

75 F 1 5 F design temperature. l

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CONCLUSION:

The disposition stated that the room temperature was to be frequently j

monitored and the globe valve adjusted t4 maintain the room design l

temperature. At the time of the $$0MI. the additional fan coil unit had not

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been placed in service. Since the unit his been pieced in service the room

temperature has been read by the Auxiliary Building Operator at least once per  ;

shift and documented per ADH 02 030 ' Reading Sheets and Shift Round [

Instructions checklist *. ,

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As demonstrated in the discussion above, the effect of the TCE change was [

evaluated and the basis for the design change was documented. VCNOC does not

consider this item to be a deficiency, i

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April 28, 1988

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2.1.2.4 PMR 1634: REACTOR COOLANT DRAIN TANK ISOLATION VALVE

! FINDING:

This PMR installed an isolation valve upstream of relief valve H-7160 to

simplify inspection and repair of the relief valve. Previously, repair or

replacement of the relief valve required a plant shutdown. The following

, discrepancies were identified

a. The Results Engineering Group issued Temporary Modification 86-24-4B in

,

March 1986, to gag Reactor Coolant Drain Tank relief valve HBV-7160. The

1

10 CFR 50.09 Safety Evaluation performed indicated that this modification

,

did not affect th: tank's overpressure protection because the tank was

'

protected by relief valve HBV-7169. Although valve HBV-7169 had a larger

spring to acccmmodate a higher set pressure, the evaluation indicated that

the setpoint was below the design pressure of the relief tank and

therefore provided adequate overpressure protection. However, the Safety

Evaluation did not evaluate the required flow rate, the relative flow

rates of the two valves at 110I of the tank design pressure (110 psi) and

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the differences in configuration. Therefore, the evaluation did no.

demonstrate the second relief valve provided equivalent or adequate

protection for the tank.

{ b. The new isolation valve added by PMR 1634 had less flow area than the

relief valve inlet, contrary to cht' tequirements of Paragraph UG-135,

, Appendix M. Section VIII, of the ASME Boiler and Pressure Vessel Code

Division 1-1974. An analysis to verify that the isolation valve would not

reduce the capacity of the relief valve was not performed.

c. In addition, instrumentation was not installed at the isolation valve

location to enable appropriate emergency actions if the tank was

] overpressurized.

The failure of the safety evaluation to demonstrate enat the second relief

valve provided adequate overpressure protection for the drain tank and to

verify that the isolation valve would not reduce the capacity of the installed

relief valve is an example of a general weakness in the engineering aree.

GENERAL DISCUSSION OF FINDTNG:

a. The SSOMI team felt that the 10CFR50.59 Safety Evaluation did not

demonstrate that the second relief valve off of the Reactor Coolant

Drain Tank (RCTT provided equivalent or adequate protection for the

tank, as the r taf valve that was gagged. The RCDT is an ASME Code

Section VIII tat with a working pressure of 100 psig. This tank has

two relief valves off of it, one set at 100 psig and the other at 25

psig. The 25 psig set relief valve is the only relief valve which ir

required by design for providing overpressure protection. The 25 pseg

relief valve was gagged by the subject Temporary Hodification Order. The

associated 10CFR50.59 Safety Evaluation lacked sufficient documentation

that the system bases for ths two relief valv2s with different setpoints

was underscood. The system consequences of gagging the 25 psig relief

was not discussed. Thc evaluation did not document how relief valves

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April 28, 1988

considered identical but not exactly alike provided the same

overpressure protection and relief capacity for the RCDT.

b. The SSOMI team determined that the new isolation valve added by PMR 1634

had less flow area than the relief valve inlet, contrary to the

requirements of Paragraph UG-135, Appendix M.Section VIII, of the ASME

Boiler and Pressure Vessel Code Division I-1974. The SSOMI team indicated

that failure to verify that the isolation valve would not reduce the

capacity of the installed relief valve is an example of a general weakness

, in the engineering area.

c. In addition, the SSOMI team indicated that instrumentation was not

installed at the isolation valve location to enable appropriate emergency

actions if the tank was overpressurized.

RESPONSE TO THE FINDING:

,

a. The Safety Evaluation clearly stated that the two relief valves were

supplied by the same manufacturer and are identical in size, style,

type, assembly number, and material specifications. Additionally,

it stated that the ASME code relief requirements for the tank were

maintained. The evaluation did not state that after full accumulation of

the relief valve, the relief capacity is a function of the valves' orifice

size and that the orifice sizes of the two valves were identical. The

root cause of this finding is an inadequately documented review to support

the subsequent evaluation conclusions.

b. During the design orocess of PMR 1634, a review of ASME B&PV Code, Section

VIII, Paragraph UG-135 and Appendix M was made. Engineering made the

interpretation that ' full area stop valve' meant and was intended to mean

that the isolation valve between a pressure vessel and its pressure

relieving device was to be of the identical line size as the piping and

relief valve. Subsequent to the concern expressed by the NRC, Engineering

discovered that an interpretation had been made by the ASME

(Interpretation VIII-1-83-338) for the definition of a ' full area stop

valve' that confirmed that the minimum flow area within the stop valve be

at least equal the inlet area of the pressure relief device. The incended

stop valve had a minimum flow area of 2.64 square inches versus 3.14

square inches for the pressure relief valve. A technical evaluation of

the stop valve to be utilized indicated that no actual reduction in

capacity of the pressure reducing device would occur (i.e., design

function would not have been effected).

c. Engineering recognizes that isolation of HBV-7160 is not a recommended

mode of operation with the RCDT in service, but that maintenance

activities for HBV-7160, if necessary, are not possible without a means of

isolation. The RCDT is an unfired pressure vessels thus, it is

pressurized only from external sources. If HBV-7160 is removed from the

RCDT as a means of overpressure protection, then administrative action

would be required to remove the sources of pressure from entering the

RCDT, or ensure that HBV-7169 is available to the RCDT, ands comply with

the Code requirement that an ruthorized person monitor and restore the

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Page 10 of 70

April 28, 1988

stop valve to a locked open status. Permanent local instrumentation for

monitoring an activity as infrequent as postulated above is not considered

warranted.

ACTIONS WHICH HAVE BEEN OR WILL BE TAKEN:

a. In the two years since this evaluation, significant experience and

progran development has occurred. The Results Engineering 10CFR50.59

guidance has been augmented to include in each Safety Evaluation the

design bases or function of a component and fully describe how this

component and its system are affected by the change or modification.

Relief valves which appear indentical and hr.ve different setpoints

have different springs, but at full accumulation are, in fact, identical.

This should be documented when identical relief valves are discussed.

b..c.

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Subsequent to the review of the ASME Code Interpretation VIII-1-83-338,

PMR 1634 was withdrawn from implementation status. Based on current

system performance without the modification, this de ign change is not

i presently deemed necessary.

CONCLUSION:

a. The system was restored on December 9, 1986. WCNOC considers this

, item closed.

b. c.

Even if the proposed modification had been implemented, the

modification would not have effected the original relief capacity of the

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valve. Subsequent to the review of the ASME Code Interpretation

VIII-1-83-338 PMR 1634 was withdrawn from implementation status. Based on

current system performance without the modiffestion, this design change is

not presently deemed necessary,

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April 28, 1988

2.*.2.5 PMR 1613: VALVE LEAKOFF CONFIGURATIONS

FINDING:

This PMR redesigned the leakoff configuration for valves BG-HV8146, BB-8074

A,B,C, and D. BB-8055 BG-LC459 and BG-LCV460. The PMR added flexible hoses

and a shutoff valve on the leakoff lines of each of these valves. Since these

valves were subject to Reactor Coolant System (RCS) pressure and temperature,

the flexible hoses could have been pressurized if the valve packing leaked

with the leakoff isolation valves closed. The manufacturer's rated pressure

for the flexible hoses is less than RCS pressure, therefore the flexible hoses

are subject to failure. The failure to adequately evaluate this modification

is an example of a general weakness in the engineering area.

GENERAL DISCUSSION OF FINDING:

PMR 1613 r3 designed the valve stem packing leakoff configurations for valves

BG-HV8146 BB-8074A,B,C and D. BB-8085 (not 8055), BG-LCV459 and BG-LCV460.

This PMR added flexible metal hose and a shutoff valve on the valve stem

packing leakoff lines of each of these valves.

Since these valves are subject to Reactor Coolant System (RCS) pressure and

temperature, the flexible metal hoses can be pressurized to the same RCS

pressure if the valve packing leaked and the leakoff isolation valves are

closed. The area of concern identified by the SSOMI team in the subject PMR

is the fact that the manufacturer's rated pressure for the flexible hoses is

less than RCS pressure, therefore the flexible hoses are subject to failure.

RESPONSE TO THE FINDING:

Valves BB-8074A,B.C and D are 3 inch, manually operated, normally open, gate

valves located in the RTD bypass loops. Valve BB-8085 is a 3 inch, manually

operated, locked open gate valve located in the RCS letdown line (reference

USAR Figure 5.1-1). Valves BG-LCV-459 and BG-LCV-460 are 3 inch air operated

level control valves also in the RCS letdown line Valve BG-HV-8146 is a 3'

air operated globe valve in the centrifugal pump discharge line to RCS loop 1

ccid leg (reference USAR Figure 9.3-8).

These valves are on lines which have a design pressure of 2^85 psig and a

design temperature of 650 F. The normal operating pressure and temperature

are approximately 2235 psig and 5880F. The flexible motal hoses selected for

use are Swagelok models SS-6HO-6-L6 or SS-6H0-1-6-L6 with a SS 3/8' T X 3/8'

NPT adaptor fitting.

The Swagelok catalog sheet for flexible metal hose connector identifies that

the maximum working pressure rating at 70 F for these models of hoses is 1610

psig. Using the recommended derating factor of 0.74 at 600 F, the maximum

working pressure is approximately 1190 psig. If the shutoff valve downstream

of a given flexible metal hose is closed, the flexible metal hose would be

subject to the same operating pressure ( 2235 psig) and temperature ( * 588

F) as the main valves, assuming leakage of the primary packing and no leakage

from the secondary packing to containment atmosphere.

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April 28, 1988

WCNOC does not consider this item to be a deficiency. The basis for the WCNOC

position is as follows:

1. The purpose of the shutoff v41ve is to preclude packing leakoff from

other valves connected to the common header from back-flowing into the

packing chamber of the valve curing maintenance. Tha subject valves

(BB-8074AD,BB-8085 BG-HV-8146, BG-LCV459 and BG-LCV460) have backseats.

The maintenance manuals for these valves require that prior to working on

the packing chamber, the packing chamber be isolated from the main

pressure by the use of backseat. Therefore, during the maintenance of

the subject valves when the leakoff shutoff valves are isolated the

flexible metal hoses will not be subject to RCS pressure.

2. The subject valve packing leakoff connections tie into a 2' header which

discharges to Reactor Coolant Drain Tank THB09 via line HB-056-HCD-3'

(reference USAE Figare 11.2 1.3 The reactor Coolant Drain Tank has an

internal design pressure of 100 psig and a design temperature of 250 F

(referente USAR Table 11.2-1). Line HB-060-HCD-2' connected to line

HB-056-HCD-3' is provided with a relief valve Hb-7160 set at 25 psig.

The disposition to EER 86-XX-46 stated that the shutoff valves on the

valve leakoff connections are to be maintained normally in the open

position. Therefore, during the normal plant operation when the shutoff

valves are open the flexible metal hoses will not be subject to RCS

pressure. In fact, during normal plant operation, the pressure in these

flexible metal hoses is expected to be less than 25 psig.

3. It should be nogedthatthe nominal burst pressure for thess flexible

metal hoseg at 70 F is 6440 psig. Using a recommended derating factor of

0.74 at 60 F, the nominal burst pressure is 4765 psig (reference Swagelok

Catalog Sheet). At the normal RCS pressure of 2235 psig, there is still

a safety margin of 2 available.

CONCLUSION:

Based on the above discussion, WCNOC does not consider this item to be a

deficiency.

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April 28, 1988

2.1.2.7 PMR 2206: AUXILIARY BUILDING FIltE DETECTION SYSTEM

.

F2 1I,NG:

This PMR revised the fire detection system in the Auxiliary Building and

installed 3-hour fire resistant material on a hatch. The revisions were

issued in response to additional combustible material loading as a result of

the installation of a tool storsge area and an anti-contamination clothing

storage area in the basement of the Auxiliary B' 31 ding. The increased

combustible loading deviates from the commitments of the USAR, as indicatea

below.

a. USAR Page 9.4-2, indicated that Fixed Vater Suppression Systems were

installed in areas with a high fire or loss potential. No fixed system

was installed in the areas in question.

b. USAR Table 9.5.1-2 stated that an automatic pre-action sprinkler system

was installed to protect cable trays in the Auxiliary Building at

elevation 1974'-0' and that vertical cable chases were protected with an

automatic wet pipe system. Uncovered cable trays containing the power

cables for the 'A' and 'B' Auxiliary Foed Pumps pass vertically through

one of the areas in question with less than 20 feet separation between the

combustible material and no sprinkler system provided.

c. USAR Table 9.5A-1 indicates that safety related systems are isolated or

separated from combustible materials: the USAR also indicates that these

systems are separated when practical. The installation of the two storage

areas in close proximity to safety related systems violates this

guideline.

The SSOHI team was concerned that combustible loading in the Auxiliary

Building was increased without implementation of the commitments of the U54R.

GENERAL DISCUSSION OF FINDING:

,

PMR 2206 revised the fire detection system in the Auxiliary Building (Area

5) and installed 3-hour resistant material on a hatch that connected

areas at elevations 1974' and 1988'. The revisions were issued in response

i to additional combustible material loading in the vicinity. Engineering

Evaluation Request 87-21-04 requested an evaluation of the additional fire

loading as the amount and location of these combustible materials were

deemed necessary to support plant operatien and maintenance activities. The

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SSOMI team was concerned that comoustible loading in the Auxiliary

Building was increased without implementation of the commitments of the

USAR.

RESPONSE TO THE FINDING:

a. Page 9.5 2 of Rev. O of the USAR includes Power Generation Design Basis

Fcur, which states that fixed water suppression systems are installed as

required in areas with a high fire or loss potential. Further, criteria

for determining the need for these systems is in substantial compliance

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April 28, 1988

with the American Nuclear Insurers (ANI) * Basic Fire Protection for

Nuclear Power Plants' (March 1976). It should be noted that this design

basis is not a safety design basis.

The area in question. Rooms 1128 and 1129, maintain a relatively low fire

or risk potential as the increase in the fire loading from the additional

combustible materials does not substantially increase the risk or loss

potential from an exposure fire. This conclusion was based, in part, on

the fact that proper storage of combustibles (e.g. NFPA-30 rated

containers, metal shelving, and bins) and housekeeping controls would be

maintained.

b. The subject area is relatively uncongested which promotes effective fire

fighting ability. In general, sprinklers are located to provide corridor '

bay coverage where concentrations of cable trays occur. Typically,

sprays are provided where two or more stacks of trays are present with

two or more trays in each stack. Also considered are the congestion in

the area and the height of the trays above the floor. In the case of the

subject area, the cable tray concentration and loading is minimal, and

as such does not warrant sprinkler coverage.

In Appendix 9.5B, Fire Hazards Analyses of Rev. O of the USAR, paragraph

two of Section A.1.7.2 Safe Shutdown Capability addresses the issue of

both motor driven auxiliary feedwater pumps' power cables being located

in Room 1128. The principal rationale set forth in the analysis is that

the turbine driven auxiliary feedwater pump is not affected by a fire in

this area and will be available to bring the plant to a safe shutdown.

Other supportive information is provided in USAR section A.1.7.2 (second

paragraph), such as the distance between the cables being nineteen feet,

no other safe shutdown equipment, trays, or exposed conduits are located

in the room, traffic to other areas of the plant cannot pass through the

room, and transient combustibles are limited to those required for pump

maintenance.

c. The reference to USAR Table 9.5A-1 is taken out of context. The section

that is being referred to is under Section D, General Guidelines for

Plant Protection. The WCGS Summary of Compliance with Appendix A of ITRC

Branch Technical Position (BTP) APCSB 9.5-1 for item D.2.a is that

safety related systems are isolated or separated from combustible

materials, where practical. Where this is not practical, special

protection is provided to prevent failure of both safe shutdown trains

by a single fire. Also, reference is made to the Fire Hazards Analysis,

Appendix 9.5B.

The need for fixed water suppression systems is considered not required

for the subject plant modification. Since, the Turbine Driven Auxiliary

Feedwater pump is unaffected by a fire in this area and the PMR provides

additional fire protection afforded by the installation of 3. hour-rated

fire resistant material to the floor hatch between Rooms 1207 and 1129

and the installation of fire detectors, therefore a fixed water

suppression system is not warranted.

The establishment of a separate storage facility outside of the

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April 28, 1988

Auxiliary Building was not considered practical. As discussed in Item b

above, the turbine driven auxiliary feedwater pump is not affected by a

fire in this area. The tarbine dri,en auxiliary feedwater pump is

considered to be the redundant safe.cy related train for a fire in this

area, and thus protection is affo ved in the event of a single fire.

The subject storage aram i; actually not in close proximity to the

required turbine driven auxiliary feedwater pump train. The storage

area is basically twice removed by two separate three-hour barriers from

the turbine driven auxiliary feedwater pump train, and thus safe

shutdown is assured.

  • CONCLUSION:

Although tho initial placement of combustibles in this area was not fully in ,

accordance with USAR discussions, the design modification meets or exceeds all

USAR commitments. The PMR design ensures that the turbine driven auxiliary

feedwater pump train is protected and isolated from a fire in this area.

WCNOC does not consider this item to be a deficiency.

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April 28, 1988

2.1.2.8 PMR 2222: CONTAINMENT COOLTNG FAN DAMAGE

FINDING:

This PMR implemented corrective actions following the failure of a fan blade

in Containment Fan Cooler (CFC) SGN01B. The failure damaged the cooling unit

and required er.tering a TS LLniting Condition for Ope ation (LCO) Action

Statement. The cause of ;he failure was determined to be loosening of the nut

which held the fan blade to the hub of the fan rotor. Subsequent inspection

revealed four other loose nuts on the CFC SGN01B. In addition, the licensee

determined that a similar failure which was attributed to loosening of the

blade nuts had previously occurred at another facility. The licensee

instituted an inspection procedure to verify the tightness of the nuto during g

each refueling outage, but did not investigate and determine the root cause of

the failure. Possible causes for these failures are insufficient torque on

the nuts to produce the required preload, excessive torque causing

overstressing of the blade shafts, inadequate blade shaft size or strength and

excessive vibration. The failure to investigate the root caure of these

failures is an example of a general weakness in angineering evaluations.

GENERAL DISCUSSION 3F FINDING:

In Item 2.1.2.8 the SSOMI team determined that the root cause investigation of

the fan blade failure in Containment Cooler SGN01B was insufficient and that

the failure to fully investigate the root cause of the event to be a general

weakness in the engineering evaluation.

  • iPONSE TO THE FINDING:

. :. the investigation performed of the fan blade failure, visual examinations

of the blades and examinations of the blade threaded connections by the

magnetic particle method were conducted. Due to the nature of the failure of

the broken blade, which was broken transversely across the threaded root

portion, and the fact that no cracks were found in like areas of the remaining

fan blades, it was concluded that inherent material deficiencies or the

existence of overstressed conditions were unlikely root causes. The nature of

the blade failure and the subsequent damage incurred to the remainder of the

fan made it difficult, if not impossible, to distinguish if the contact of the

fan blade tip to the shroud housing occurred prior to or after the fracture of

the blade root. This key aspect prevented determining whether the fan blade

root nut loosened or deficient fan blade material was the root cause of the

fan blade failure.

Based on the above and the isolated instance of a fan failure at another

facility of similar design (Hydrogen Hixing Fan manufactured by Joy

Manufacturing) from which very little information could be derived, it was

concluded that the root cause of the event could not conclusively be

determined. Effective prevention of another such type of failure by

inspections of blade tip angles, torque checks or the blade attachment nuts,

and lubrication of the motor bearings of other like vanaxial fans and

continued monitoring was deemed most appropriate.

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Page 17 cf 70

April 28, 1988

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ACTIONS WHICH HAVE BEEN OR WILL BE TAKEN:

Lubrication of the motor bearings, inspection of the blade tip angles eted

torque checks of the blade attachment nuts is completed at each refueling

'

outage as required by the Preventive Hair.tenance Data Base Program.

Verification of acceptable vibration levels are also conducted in like  ;

fashion. '

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CONCLUSION

?

Based on the above discussion. WCNOC does not consider this item to be a

deficiency.

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Section II

Page 18 of 70

April 28, 1988

2.1.2.9 APPENDIX,J LEAK TEST REQUIREMENTS

FINDING:

PMR's 1143 and 2109 required the encapsulation of hinge pins for feedwater

valves due to leakage. The SSOMI team determined that 10 CFR 50, Appendix J

required leak testing had not been performed on these valves. The licensee

indicated that the Steam Generators and attached secondary systems inside

containment were closed systems and that for all accident conditions, the

secondary pressure was higher than containment pressure. Therefore leak

testing of the valves was not required. The SSOMI team questioned whether the

Steam Generator System was required to be maintained pressurized in the ovent

of a design basis accident and whether the instruments, instrument lines and '

appurtenances on the Steam Generators and other secondary systems were

adequately protected in the event of a high energy line break. Further action

is necessary to clarify the containment boundary and leak testing requirements

with respect to the secondary systems, the assumed condition of the secondary

systems during a design basis accident, and the design of the secondary

systems with respect to high energy line breaks. This general concern has

been previously identified at other plants and is under roview by NRR. There

were no further concerns identified with respect to these PHRs.

GENERAL DISCUSSION OF FINDING:

During the review of PMRs 1143 and 2109, the :iSOMI Team identified that

10CFR50, Appendix J required leak testing had not been performed on the

associated valves. The team questioned the containment boundary and leak

testing requirements with respect to the secondary systems, the assumed

condition of the secondary systems during a dtsign basis accident and the

design of the secondary systems with respect to high energy line breaks.

RESPONSE TO THE FINDING:

The valves associated with the above identified PMR's are Feedwater Isolation

Check Valves AE-V-120, AE-V-121. AE-V-122 and AE-V-123 and Feedwater Chemical

Addition Isolation Valves AE-V-128 AE-V-129, AE-V-130 and AE-V-131. These

valves arc associated with the Main Feedwater Line Penetrations P5, P6, P7 and

P8,

As discussed in Safety Evaluation Seven, in USAR Section 6.2.4.3, the

containment penetrations associated with the steam generators are not subject

to GDC-57, since the containment barrier integrity is not breached. The

boundary or barrier against fission product leakage to the environment is the

inside of the steam generator tubes, the outside of the steam generator shell,

and the outside of the lines emanating from the steam generator shell side.

USAR Figure 6.2.4-2 shows the steam generator and associated secondary systems

that serve as a barrier to the release of radioactivity pose.-LOCA. USAR

Figure 6.2.4-1 Sheets 5, 6, 7 and 8 show the configuration of the subject

ponstrations.

As indicated in USAR Section 6.2.6.3, Containment Isolation Valve Leakage Rate

Tests (Type C tests), the valves associated with the piping systems connected

to the secondary side of the steam generators isolate the steam generatorJ and

are not considered containment isolation valves and are, therefore, not leak

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Section II

Page 19 of 70

April 28, 1988

tested. All portions of the secondary side of the steam generators are

considered an extension of the containment. The above identified USAR Section

further elabotates and specifically excludes penetrations PS, P6, P7 and P8

from Type C testing. As shown on USAR Figure 6.2.4-2, the water level in all

steam generators is maintained above the tubes following a LOCA to preclude

the entrance of the containment atmosphere into the secondary side of the

steam generators. As discussed in USAR Section 6.2.6.1.1, following the

containment stabilization period of the Type A Test (ILRT), the secondary side

of the steam generators are vented outside of the containment to ensure the

most conservative test configuration during the ILRT.

The high energy line pipe break locations and types of brecks are identified

in USAR Figures 3.6-1 and 3.6-3. The stress results that were utilized to

determine the break types and locations are provided in USAR Table 3.6-3. The

high-energy pipe break effects analyses criteria and results are provided in

USAR Table 3.6-4. The results of the analysis demonstrate that the for all

postulated breaks, including the design basis LOCA, containment intqgrity is

maintained and no essential systems are impacted.

CONCLUSION:

As discussed above, the subject valves and associated penetrations have

previously been identified in the USAR as being exempt from local leak rate

testing. In addition, their configuration and compliance with 10CFR50,

Appendix J requirements, relative to Type A Te* ting, (ILRT) have also been

previously provided in the above identified USAR Sections.

The high enargy line break evaluation and supportive existing USAR information

has been identified for clarification as requested. The Safety Evaluation

Reports, NUREG-0830 and NUREG-0881, describe, in Sections 3.6.1, 3.6.2, 6.2.3,

and 6.2.5, the staffs recognition and acceptance of the above identified

information.

.

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Page 20 of 70

April 28, 1988

l 1 2.10 dATTERY DISCHARGE OF OCTOBER 13. 1987

FINDING:

During maintenan e of the Division E Vital Bus NB02 on October 15, 1987, both

Station Batteries ware subjected to a deep discharge resulting in a loss of

both vital buses. The root causes of the discharge are being reviewed by

Region IV and will be addressed in separate correspondence. As part of this

inspection, the SSOMI team reviewed the adequacy of the battery capacity and

associated design calculations.

The maintenance which deenergized the bus was expected to last less than 30

hours. Based upon the nominal ampere-hour capacity of battery NK14

Operations personnel performed a calculation and estimated that the battery

would provide 50 hours5.787037e-4 days <br />0.0139 hours <br />8.267196e-5 weeks <br />1.9025e-5 months <br /> of service with a 35 ampere load. The S30MI team found

that the basis for the estimate that the batteries would provide 50 hours5.787037e-4 days <br />0.0139 hours <br />8.267196e-5 weeks <br />1.9025e-5 months <br /> of

service van inadequate. The licensee indicated that the estimate was made by

dividing the b.ttery rating of 1650 ampere-hours by 50 hours5.787037e-4 days <br />0.0139 hours <br />8.267196e-5 weeks <br />1.9025e-5 months <br /> which yielded a

permtasible d scharge rate of 35 ampt However, the sctual load on the

battery during the discharge was recorded in the control room each shift as 70

amperes. Battery Sizing Calculation E3, indicates that steady state loads of

220 and 100 amperes would result in discharge rates of 20 amperes per positivo

plate (APPP) and 16 APPP for Batteries NK12 and NK14 respectively. The

battery cell characteristic curve indicates that the battery capacity would

provide 10-hours of service at these discharge rates. Based on Calculation

E-3 and the cell characteristic curve, the SSOHI team calculated that a 70

ampere load would have resulted in a discharge time of 35 hours4.050926e-4 days <br />0.00972 hours <br />5.787037e-5 weeks <br />1.33175e-5 months <br />.

In addition, the SSOMI team noted that during removal of the NB02 Vital aus

from service, system operating procedures SYS NB331/4 and SYS NB331/5 were not

utilized. These procedures specified the requirements and precautions for

system operation ar.d isolation and specified a maximum discharge time of 200

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minutes. The licensee subsequently indicated that operational procedures are

not routinely used for removing and returning equipment to service. The

failure to utilize the appropriate operational procedures and incorporate the

l precautiens and requirements of these procedures for the removal and return of

equipment from service in accordance with the requirements of the Technical

Specifications and 10 CFR 50, Appendix A, is considered to be a weakness. The

SbcMI team considers that, If the operations Department had complied with the

procedural requirements, or had used the battery sizing calculations provided

by Engineering, or had consulted with Engineering, the deep discharge and

resulting loss of both vital buses would not have occurred. j

l

The battery discharges occurred on October 15, 1987. Following these events, i

the batteries' conditions were not recorded prior to recharging. Based upon

tha results of the earlier October 7, 1987, performance discharge test on

battery NK12 discussed in Section 2.1.2.12 of this report, and the fact that

the unplanned discharges went deeper than the performance test, at Isast cell

32, and probably other cells, reversed polarity during the unplanned

discharges.

The failure to provide adequate controls for the removal from service of a

safety system which resulted in a loss of the Station Batteries is a weakness.

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Section II

Page 21 of 70

April 28, 1988

In addition, the failure to involve the Engineering Department, either through

the use of system procedures or by consultation during the battery discharges,

is a significant weakness.

GENERAL DISCUSSION OF FINDING:

Station procedures were not utilized to remove Vital Bus NB02 from service and

there was a failure to provide temporary power to Station Batteries NK12 and

NK14. Additionally, enginevring was not utilized to perform discharge

calculations.

RESPONSE TO THE FINDING:

.

The root cause of these events has been attributed to cognitive personnel

error by Operations, Maintenance and Outage management personnel in failing to

plan for th capability to provide temporary power supplies to the batteries

if the NB02 outage was extended. Preparations to supply the ba*.teries with

alternate power were in progress when the Low Voltage Alarms verw received,

however, the task was not completed prior to discharge of the batteries. This

situation existed because prior to this event, station policy was to utilize

work request procedures and tag out procedures to control plant equipment

during outage work. Also, implementation of the temporary modification to

bring in alternate power to the bus was too time consuming.

As a result of the battery discharges, an evaluation of the batteries was

performed. This evaluation concluded that all of the batteries were

capable of performing their design function based on a review of the

specific gravity, voltage, electrolyte level, and electrolyte temperature

for each cell.

ACTIONS WHICH HAVE BEEN OR VILL BE TAKEN:

Programmatic changes have been incorporated which require either the use of

existing procedures or developaent of a new procedure to take equipment out of

service and to restoro equipment to service. Prior to this tim 9. the work

request procedure and the clearance order procedure were used to control

these work activities.

By Septembet 1, 1986, a specific procedure will be prepared which will provido

instructions for deenergizing a vital bus with requirements for powering

Station Batteries from an n1 ternate source. The preparation of this procedure

, and its use will preclude future similar oc .erences.

Plant and Nuclear Plant Engineering procedures have been changed to enhance

the use of engineering talent and skills. These procedure modifications

enanges should result in proper personnel involvement in a specific problem

area.

The events described above were addressed in Programmatic Deficiency Report

(PDR) OP-87-81 and Licensee Event Report (LER)87-049. The implementation of

the corrective action will resolve the concern identified by the SSOMI team.

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Section II

Page 22 of 70

April 28, 1988

2.1.2.11 BATTERY SIZING CALCULATION E-3

FINDING:

Bechtel Calculation E-3, 'Cisss 1E Battery System,' Rev. O, dated January 12,

1987, was reviewec by the SSOMI team and tho following discrepancies were

identified:

a. The calculation assumed a constant load on the DC System based upon a full

load rating of the 7.5 KVA for the Battery Inverter. However, in

calculating the DC current, the DC voltage was taken at the nominal 125

VDC level. Because inverters try to deliver a constant KVA load, as the

battery voltage decreases during a discharge the current drawn by the

inverter from the battery will increase. These errors would add "

approximately 10% to 15Z to the required battery size.

b. The input data did not document the cell characteristics used by the

computerized calculation.

c. The calculation did not consider the minimum cell temperature permitted by

the Technical Specification.

The battery sizes selected for batteries NK11 and NK13 are 25% and 42% larger

than the calculated required size. The errors noted above can be enveloped by

the existing battery and there are no safety concerns with th9 installed size

of the batteries. The inadequacies identified in the battery sizing

calculation are symptomatic of a general weakness noted by the team in

engineering calculations.

GENERAL DISCUSSION OF FINDTNG:

Station batteries NK12 and NK14 were subjected to a deep discharge due to

extended loss of power to their chargers. As a part of their invostigation,

the SSOMI Team examined the adequacy of the battery capacity and associated

Bechtel design Calculation E-3, Rev. O, dated January 12, 1981. (The subject

SSOMI report refers to Bechtel Calculation E-3, Rev. O, dated January 12,

1987. This is in error. The referenced calculation revision is dated January

12, 1981).

RESPONSE TO THE FINDING:

a. The load profile used in calculation E-3 included continuous and momentary

loads that are conservatively assumed to be constant during the design

batia duty cycle. Since the total load on the subject batteries consists

of mostly constant resistance types of loads (e.g., control panel

indication lights, control circuits, instrumentation and emergency

lights), the above assumption is considered conservative as the resistive

load currents decrease under low voltage conditions.

It should also be noted that, as verified by Westinghouse, the inverter

vendor, the subject inverter draws 58 amps at 135VDC, approximately 62

amps at 125VDC and 70 seps at 305VDO. Therefore, the use of 68 amps as a

steady state load over the entire 200 minute profile is conservative and

acceptable since this value approximately equals the maximum current draw

_ _ _ _ _ _ _ _ _ - _ - _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ - _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _________________ _

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Section II

Page 23 of 70

April 25, 1988

.

which occurs only at 105VDC, for a short duration near the extreme end of

the discharge profile.

b. The computer program software was itself an independent and controlled

standard program of the Architect Engineer which contains the subject

, data for the batteries used at Wolf Creek Generating Station. The

y' standard computer program inherently contains the applicable battery cell

characteristico, therefore these characteristics are not provided as user l

entered data every time the computer program is used. It is indicated on

page 10 of tne subject calculation, that the correct battery type and

manufacturer was, in fact, selected and recorded on the calculation.

c. The capacities of the subject batteries have been evaluated and previously l

aiscussed with the NRC (Safety Evaluation Reports, NUREG-0881 (Wolf r

i Creek), April. 1982 and NUREG-0830, October, 1981 (Callaway), Section i

i 8.3.2.2) with regard to temperature performance and other factors, The l

subject batteries are sizej in excess of 50 percent of the initial battery  !

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capacity (i.e., are 50% oversized) thus enveloping the requirements for

l temperature, voltage and specific gravity fluctuation, as well as the l

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replacement criterion of 80 percent. The subject batteries meet IEEE  ;

Standards for battery sizing and are acceptable. This item was  !

specifically discussed with the SSOMI team in order to document that l

2 minimum cr.11 temperatures were evaluated by WCNOC prior to fuel load for i

Cycle III. i

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CONCLUSION: l

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The battery sizes installed are adequately designed and provide more than the

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required capacity. It is not felt that the above observations are indicative

or representative of a general weakness in engineering calculations.

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Section II

Page 24 of 70

April 28, 1980

2.1.2.12 BATTERY PERFORMANCE TEST

FINDING:

In order to evaluate the battery discharge of October 15, 1987, the SSOHI team

reviewed the performance test performed for Battery NK12. The purpose of the

performance test was to demonstrate the actual capacity of the battery

compared to the manufacturer's published rating.

Performance Test STS MS 022, performed on Battery NK12 on October 7,1987, was

interrupted prior to the completion of tt.e test to jumper out Battery Cell No.

32. This cell had dropped 80 millivolts in 10 minutes to 1.692 volts. The

SSOMI team estimated that the battery would have teached its test limit in

less than 1/2 hour if the cell had not been jumped. The test was restarted

approximately 6 1/2 hours later. When the test was restarted the battery

voltage had increased to a voltag' which existed two hours before the test had

been stopped. As a result of the failure to recognize that the battery would

recover lost capacity during the extended outage, the performance test

incorrectly showed that the battery had a capacity of 138.75Z. The SSOMI team

calculated that if the performance test had been left to continue until

completion, the battery capacity would have been calculated at 125I. While

the battery has less capacity than the assumed by the licensee as a result of

the performance test, the battery has 50! more capacity than that required by

the test acceptance criteria. The failure to adequately test and evaluate the

results of the battery performance testing is considered to be indicative of a

general vsakness in engineering evaluations.

GENERAL LISCUSSION OF FINDING:

This item concerns the jumpering of a weak cell (132) during the October 2,

1987 performance discharge test of battery NK12. The finding concerns the

time taken to jumper the weak cell, approximately 6-1/2 hours, and the

battery capacity obtained from the test.

The procedure used in performance of this test, STS MT-022, was written

to incorporate the requirements in the Technical Specifications, and the

recommendations in the Gould Manual and IEEE 450. Step 6.4(4) of IEEE 450 states 'if an individual cell is approaching reversal of its polarity

(plus 1 volt or less), but the terminal voltage has not yet reached its test

limit, the test should continue with a jumper across the weak cell'.

RESPONSE TO THE FINDING:

There are two reasons which can be attributed to tha performance teat

being stopped for approximately 6-1/2 hours. The procedure did not specify a

maximum allowable time for interrupting the test. In addition, although

jumper cabler had been prepared prior to the test, the availability of

the jumper cables was not checked immediately prior to the start of the test-

Maintenance personnel did not recognize the time sensitivity of this while new

jumper cables were being made.

The Gould ibnual does not address performance or duty cycle testing. IER

450 lists recommendations for the performance and duty cycle tests, but

does not identify the maximum allowable time for interrupting a test. As

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l Page 25 of 70

! April 28, 1988

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addressed in IEEE 450 Step 6.4(4), the jumper could be placed directly across

the cell, which would short the cell and completely discharge it, or the

test could be stopped and that cell disconnected from the battery replacing it

with a jumper. Since IEEE 450 states a cell is approaching reversal at plus 1

volt or less, a determination was made when writing the procedure to ,

disconnect the cell from the battery to keep it from being completely

discharged.

,

Gould was contacted after the test was performed as to their recommendation

for jumpering a cell, and a maximum test interruption time. Gould indicated '

they would accept either method for jumpering a cell, and if we choose to

jumper a cell that a test interruption of approximately 15 minutes should not

effect the battery capacity value obtained from the test.

ACTIONS WHICH HAVE BEEN OR VILL BE TAKEN

Procedure STS MT-022 will be revised to incorporate the Gould recommendation

of 15 minutes, as the maximum time allowed to interrupt the test. Due to +

this 15 minute time limit, another step will be added to the STS to have I

the jumper cables cleaned and ready to install prior to starting the test.

These changes will be completed prior to July 1, 1988.

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The battery capacity, listed in Step 5.2.5 of STS HT-022 performed on October

2, 1987 will be corrected to show a capacity of 120.72. This value was  :

the proven capacity at the time the test was stopped. A Fluke meter had been  !

installed to monitor cell #32, and Maintenance Engineering was present during ,

I the test interruption. The voltage of cell 132 dropped quickly, with only a

i few minutes between the 1.692 volt reading and the 1.080 volt reading when l

l the test breaker was opened. If the test had continued after cell #32 was  !

jumpered (in the recoemended 15 minutes), the test would have continued  !

for a very short period before it would have been stopped again to jumper  :

cells #38 and #50. l

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CONCLUSION:

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A revision will be made to the applicable procedure by July 1, 1988 to !

incorporate the resolution of the finding and prevent recurrence. Training '

for personnel in conducting and evaluating battery capacity testing will be

i developed and implemented for personnel prior to the next performance of STS  !

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Hl-022.  !

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April 28, 1988

2.1.2.13 DC SYSTDI LOW VOLTAGE ALARMS

IJNDING: ,

In order to evaluate the battery discharge of October 15, 1987, the SSOHI team

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reviewed the alarms associated with the DC System to ensure that the design of

the alarm setpoints were adequate. A review of the DC System alarms detailed

on Relay Setting Drawing E-11028(Q indicated that four DC undervoltage alarms

existed in each Battery System. These alarms should have provided sufficient

Jrning to prevent the DC System low voltages experienced on October 15, 1987.

.

GENERAL DISCUSSI0F OF FINtING:

Station procedures were not utilized to remove Vital Buss NB02 from service

l and there was a failure to provide temporary power to Station Batteries NK12

i and NK14.

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l RESPONSE TO THE FINDING:

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There are four DC undervoltage alarms for each battery system. Each battery

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system consists of a 125 VDC battery bank, a battery charger and associated i

equipment. The charger DC undervoltage alarm indicates the loss of a battery

charger at 123 VDC. The DC switchboard bus undervoltage alarm indicates low

DC voltage at 112.5 VDC. The distribution switchboard undervoltage alarm

, indicates a loss of the DC distribution panel at approximately 86 VDC. Each

of these alarms displays in the
ontrol room through an NK system trouble
window which will reflash for each alarm. The inverter DC undervoittge alarm

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indicates the loss of DC input to the inverter at 82.5 VDC. This alarm

j displays in the control room through an inverter undervoltage window. These t

alarms provide the control room with indication of a loss of DC system

function, but are not generally anticipatory in nature. During the October

15, 1987 event, undervoltage alarms came in at approximatvly the same time as

the initial Engineered Safety Features Actuations (i.e., Control Room l

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i Ventilaticn Isolation Signal. Containment Purge Isolation Signal and Fuel

l Building Isolation Signal).

l ACTIONS WHICH HAVE BREN OR VILL BE TAKEN

By September 1, 1988, a procedure vill be prepared which will provide i

instructions for doenergizing a electrisal safety related division with ,

requirements for powering Station Batteries from an alternate source. l

FONCLUSION:

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Implementation of the corrective action will resolve the concern idsntifieo by l

the SSOHI team.

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April 28, 1988 i

2.1.2.14 DIF ,

EINDINGt  ;

The SSOMI team reviewed the design of the closing circuit for the Emergency

Diesel Generator (EDG) output breakers, NB0111 and NB0211, and concluded that j

the design is inadequate, in that the ' anti-pumping' logic prevents the '

breakers'from closing onto a cleared, deenergized bus. In the event that both  ;

the normal and alternate 4160 VAC Vital Bus feeder breakers,NB0109 and NB0112, i

are open and the CDG mode switch is in the ' auto' position, the ' anti-pumping'

relay will be energized continuously, thus preventing the EDG output breaker

from closing. Operator action is required to cycle the EDG mode switch at the

local station in arder to clear the ' anti-pumping' logic and close the EDG

output breaker to reenergize the 4160 VAC Vital Bus.

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The requirement for manual operator action appears to represent an unanalyzed

condition, in that the deenergized 4160 VAC Vital Bus cannot be energized i

automatically by the EDG in this condition. This design deficiency was  !

discussed in a conference call between the licensee and NRC Region IV  ;

canagement on December 8, 1987, and will be reviewed by NRC Region IV. The

inability of the EDG output breaker to automatically close onto e cleared. [

deenergized bus is considered *.a be a design weakness.  ;

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GENERAL DISCUSSION OF FINDING:

The SSOMI team review of the design of the closing circuit for the Emergency

Diesel Generator (EDG) output breakers concluded that the ' anti-pumping' logic

of the diesel breaker prevents the breaker from reclosing onto a deenergized

bus after a manual trip is initiated from the Main Control Room. Operator  ;

action is required to cycle the EDG mode switch at the local station in order

to reset the ' anti-pumping' logic and permit reclosure of the EDG output

breaker. The inability of the EDG output breaker to directly reclose on to a

cleared, deenergized bus was considered by SSOHI to be a design weakness.

I

7ESPONSE TO THE FINDINGt

The above concern is related to the reclosing feature (m4nual or auto) of the  !

subject breaker after a manual trip when offsite power is not available and

when power is being supplied by the diesel generator prior to the subject  :

manual trip. It was found that the stated condition resulted from manual

l

interruption, via the Control Room breaker hand switch, of the as designed <

fully automatic sequence for diesel start, loading and restoration of  !

essential AC power under loss of offsite power conditions. e

!

As originally designed, the diesel generator is normally in the standby mode

whereby, on loss of offsite power, it will automatically start and its output

breaker will automstically close on to a cleared, deenergized bus, consistent

with its design intent. No manual actuation or intervention is required for

pettormance of this function. Tripping the output breaker and subsequently

attempting to manually reclose it from the thin Control Room was not the

original design intent, nor is it intended under future designs, that such

interruption be entertained under the stated loss of offsite power conditions.

A meeting was held with NRC, VCNOC and representatives of Bechtel (VCGS A/E)

te discuss the existing design and operatio. of the breaker. The relationship

I

!

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Section II

Page 28 of 70

April 28, 1988

of the design to Regulatory requirements and considerations for modificaties

to the existing dcsign were also discussed.

The dasign was in compliance with relevant Regulatory requirements and that

the existing design operates correctly under the relevant normal and design

basis accident scenarios. However, after discussion with the NRC, it was

concluded that it would be beneficial to have suitable provisions to allow

reset of the circuit and allow resultant breaker reclosurs from the Main

control Room. This capability would allow for more timely recovery should

intentional or inadvertent manual trip of the diesel output breaker occur

under loss of offsite power conditions.

ACTIONS WHICH HAVE BEEN OR VILL BE TAKEN:  ;

Based on review of the subject control circuit and its design features, it was

concluded that the subject diesel generator ureaker was not designed to be

tripped and reclosed nanually from the Main Control Room under the stated

conditions. The entire diesel generator start and loading sequence (including

breaker closure) and power restoration is designed for automatic operation

without manual intervention. However, upon subsequent discussion with the

NRC, it was agreed that a design change providing the operator, in the Main

Control Room, with a capability to teclose the diesel generator breaker on a

deenergized bus would be a beneficial enhancement. Wolf C-eek has procured

the necessary materials and is ready to implement the modification.

CONCLUSION:

The proposed design change will enhance the capability for manual control from

the Main Control Rcom to reclose the diesel generator breaker if manually

tripped during a loss of ot'fsite power event.

,

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Section II

Page 29 of 70

April 28, 1988

!

3.1.2.2 PMR 1722: VALVE HOTOR-OPERATot TESTING f

l FINDINGr

:
Th!.s PXR performed valve motor operator testing and torque and limit switch  !

O settings in response to NRC Inspection and Enforcement (IEE) Bulletin 85-03, i

J regardine torque and limit switch settings in valve motor operators. In [

. addition internal operator wiring was modified to distribute the limit switch  !

j and indi;ation contacts to different rotors.

! The SMR. PHR changes, drawings, calculations, and WR packages for several l

1 affected valves were reviewed. Operators for the five motor operated valves  !

!

(HOVs) identified below were inspected for conformance to design requirements l

l and proper workmanship.

i ,

'

Valve Number Function

i

BB-HV8000A Pressuriser Block Valve

BB-HV80005 Pressurizer Block Valve

AL-HV031 ESW to Motor Driven AFW Pump A

AL-HV030 ESV to Hotor Driven AFW Pump B

EM-HV8923B SI Pump B Suction Isolation

The following discrepancies were identified

a. Deficiencies were identified in two of the valve operators. The spare

conductors of the control cable in each Pressurizer block valve, which are

located inside containment, were not properly protected to prevent

possible interference with the operation of the valve. Bechtel Detail

Drawing E-11013, required spare conductors of safety related cables in the

Reactor Building to be protected with Raychem end caps. Contrary to this

requirement, the spare conductor in Valve BB-HV8000A was unprotected, and

the spare conductor in Valve BB-HV80005 had been originally protected with

tape which subsequently became unraveled. Drawing E-11013 allows the use

of tape for protection of conductors outside, but not inside, the Reactor

Building. In addition, insulation damage was noted on several conductors

of the control cable in Valve BB-HV8000A. Based on these findings. WR

4954-87 was written for Valve BB HV8000A and WR 4953-87 was written for

Valve BB-HV80008 to correct the deficiencies and to evaluate the

insulation damage,

b. A concern was identified in the complexity of drawings required to

identify the wiring configuration for conduct and verification of

maintenance and modifications of the mytor operated valves (HOVs). As

many as seven different drawings and wiring lists were required to fully

inspect the wiring configuration of each MOV reviewed. For example, the

drawings required to inspect Valve AL-1:VU30 included a design schematic, a

vendor wiring diagram which also included a partial schematic, two field

wiring lists, and three design change documents. Other valves had wiring

changes required by the vendor that were specified in writing by vendor

change requests, but were not indicated on the vendor viring drawings.

Differing conventions for identifying the wire termination points on

wiring diagrams were also ident!fied. In some instances, wiring diagrams

identified field wire terminations, and in others tne internal wire

designations duplicated field wire designations.

_ _ _ _ _ - _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _

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Section II

Page 30 of 70

April 28, 1988

The difficulty 4.n using the large number of inconsistent drawings to make

changes to wiring had been previously identified by the station Electrical

Maintenance Department. Engineering Evaluation Request (EER) 8 6-EH-0 3

described the problem of multiple drawings and inadequate cross

referencing between plant and vendor drawings. The SSCHI team was

concerned that, although the EER was approved and submitted on July 18,

1986, an evaluation or disposition for the EER had not been made.

EER 87-KC-08 was written to correct a vendor wiring drawing that used the

same wire numbers twice. The engineering evaluation rejected the

recommended drawing change on the basis that a review of four related

design drawings indieeted the viring was inadequate. The EER response

referenced Bechtel Specification E-01016 ' Electrical As-Built Drawing

Criteria.' Note N. as the reason for not correcting the wiring drawing.

Note N states that internal vendor wiring inconsistencies which do not

affect the circuit electrically or functionally will not be incorporated

into the as-built drawings. The SSCHI team considered that this

resolution was inadequate because as-built wiring drawings are routinely

used for maintenance and modification activities.

4

Except for the discrepancies in the Pressurizer Relief Valves d. :ussed in

d

Section 3.1.2.2.a. the workmanship observed was good. The fact that few

l problems have been identified in motor operators is attributed to the

diligence of the maintenance craft and engineers and is considered a strength.

GENERAL DISCUSSION OF FINDING:

a. During field walkdown with the inspectors to check the actuator wiring

installed in accordance with PHR 01842 (not 01722 as referenced), it was

found that spare conductors were not isolated correctly. It was also

noted that several conductors of cable 11BBG39AG were abraded and

needed to be checked for insulation damage within valve actuator

BB-HV8000A.

b. EER 87-KC-08 identified an anomaly on a vendor wiring diagram, involving

the duplication of vendor wire numbers. It was recommended that one set

j of the duplicated wire numbers be revised to preclude confusion.

The SSOHI team concern dealt with what was termed 'the complexity of

drawings required to identify the wiring configuration for conduct and

verification of maintenance and modifications of the motor operated

valves (HOVs)'. The design documents used on PHR 1722 were of the

stundard format and consisted of:

a I

a) Schematic drawings (E-03's) - drawings used to show the valve

operator's internal e*ectrical configuration and its interface with

other systems and components,

b) Internal wiring diagrams - vendor supplied internal wiring

configuration for each valve. Represents vendor provided or vendor

side wiring.

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Section II

Page 31 of 70

April 28, 1988

c) External wiring diagrams - drawings or listed information that shows

the configuration of external cables, their associated wires and

termination points. Wires installed external to the equipment which

are needed to fit or configure that equipment into the overall

schems are considered as field wires or jumpers. The termination

list ar.d jumper 110t are included in this category.

When any electrical modification is made, the possibility exists that at

least one, and in many ceaes all three of the above documents will be

revised by either Assuing a document revision on a document change

notice. Due to time constraints, a needed revision of the modification

documents associated vith valve AL-HV030 was accomplished by issuing

three document change notices.

RESPONSE TO THI 7INDING:

a. The use of tape within the Reactor Building is not a design approved

means to isolate or protect spare conductors. The root cause is

recognized to be a lack of attention to the specific details by

electricians, QC, and Maintenance Engineering personnel. The

abrasten on conductors was due to original installation methods.

b. The general description, specifications and details for vendor equipment

are provided in vendor instruction manuals. It is necessary that this

information be reviewed prior to routine maintenance or modification

activities.

The instruction manual for the equipment shown on the subject vendor

wiring diagram includes information that eliminates the confusion

i regarding tht duplicate wire numbers. Thersfore, note N on Bechtel

Drawing E-01016, ' Electrical As-Built Drawing Criteria', applies to the

identified anomaly and no drawing revision is required. Therefore, the

disposition is adequate and WCNOC does not considsr this item to be a

deficiency,

i The electrical design documents used for plant modifications are based on

i the system utilized by the Architect / Engineer (A/E) for the original

.

plant design. Each document type is used to convey its portion of the

l

'

total picture. Once an individual bucomes familiar with the scheme used.

the system is not ' difficult'. With regard to what the inspector

described as ' inconsistent drawings *, it must be recognized that the

above three document types were consistent with respect to one another

for any particular operator. However, due to the fact that each vendor's

internal wiring diagrams are different and site installation

characteristics for each operator may be d.fferent (e.g. slack in field

s run cables,, it is possible that the set of electrical design documenta

for a particular operator may be different (or 'not consistent') with

those of another operatcr.

With regard to the SSOMI team's consents on dispositioning Engineerina

Evaluation Requent (EER) 86 EM-03, Nuclear Plant Engineering is

addressing the concerns reflected in the EER se part of the werk scope of

FMR's 1722, 1842, 2071, 2073 and 2076.

1

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. Section II

Page 32 of 70

April 28, 1908

ACTIONS WHICH HAVE BEEN OR VILL BE TAKEN:

a. Work Request 14953-87 installed an appropriate end cap on the spare

conductors in BB-HV8000B. Work Request 14954-87 installed approved end

caps on the spares in valve BB-HV8000A. Work Request 14954-87 also

reworked the abraded conductor insulation in accordan:e with the criteria

defined in E-11013.

Maintenance Engineers were reminded of the Raychem end cap criteria

for spare conductors within the containment, and measures were taken to

prevent further conductor degradation by installing protective

sleeving on the abraded conductors.

CONCLUSION:

a. This item does not point to a significant program breakdown. The

improper isolation of spare conductors is not a major defect. The

abrasion noted is a result of previous incorrect installation and the

problems were resolved expediently when identified.

b. WCNOC realizes that the wiectrical design document format may be somewhat

confusing to an individual who is unfamiliar with the A/E's system.

Hove.rer, the system does work and provides the information needed to

support plant operations. Although a ' standard' approach is desirable

and is used where possible, differences in vendor drawings and field

installation configurations do cause variations in the method used to

achieve the same end results.

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Section II

Page 33 of 70

'

April 28, 1988

3.1.2.4 PME 2018: ASCO SOLENOID VALVE REPLACI! MENT

i

FINDING:

[

This PHR replaced twelve safety related, seismic Category I, environmentally

qualified. Asco solenoid valves on air operated valves in the Reactor Coolant

System, Chemical and Volums Control System, Residual Heat Removat System. High  ;

Pressure Core Injection System, and Liquid Radiological Vaste System. The  ;

modifscation was initiated as a result of shorting of electrical wiring within  !

the solenoid housing aused by limited space within the housing, splicing of l

pigtail leads, and Raychem sleeving o' wires with damaged insulation. The PHR

replaced solenoid vrives using slectrical pigtails with solenoid valves using -

terminals. ,

The PMR, VRs. procedures and docunentation associated with the installation

[

were reviewed. A field inspection was conducted on three solenoid L

'

installations that had been completed at the time of the inspection. The

Installations were inspected against the assembly and mounting detail drawings ,

and work instructions in V:ts that implemented the PHR. Solenoid valve serial j

numbers were verified against material requirements for the valves that were i

inspected. The fc11owing concerns were identified:  ;

t

a. The 10 CFR 50.59 Lafety Evaluation was inadequate in that the seismic and (

environmental equivalency of the solenoid valves being installed was not j

documented. The written evaluation described only the improvement in j

safety because the leads would not short out in the new model solenoids. l

l

The safety evaluation for changes involving substitution of components

would normally be expected to reference equivalency or superiority in i

form, fit, function, materials, mounting, and qualification, which woald [

equate the change to a quality level at least consistent with the  ;

originolly analyzed design. i

b. The air supply line for the ASCO solenoid valve EJ-HCV88908 had inadequate

seismic support between the solenoid valve and the polar crane wall. The l

supply line had approximately eight feet of rigid and hard copper tubing r

that did not havo support. The unsuppo.ted tubP4 cont %ined both an  !

unsupported drain valve and the solenoid air isolat h <alve. r

i

c. 'h e 3/8-inch diameter stainless stwel air tubing for the Asco solenoid  !

alve serving Valve EJ-HCV88905 had one loose tubing support between the  !

Asco solenoid valve and the air operator.

d. Work Request 1042-87 which replaced Asco solenoid Valve EM HV8881 had one [

instance of enclear work instructions. Step 26 required recording the t

valve serial number without reference to which valve. Consultation with

the personnel who had written the work instructions and performed the work -

was required to ascertain that the serial number recorded was for the l

valve which had been removed. In this case, ;he unclear instructions did

not affect sc.fety, f

F

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Section II

Page 34 of 70 .

4

April 28. 1938

L

REFERAL DISCUSSION OF FINRIPGr

a. SSOMI team review of PHR 02018 Asco Solanoid Valys Replacement identified I

l a concern with the 10CFR50.59 Safety Evaluation. The identified concern

is an isolated case that was an omission in the preparation of the i

j 10CFR50.59 faiety Evt.luation because the solenoids utilized in the design

>

were procured earlier as replacement parts to the appropriace technical j

i and quality requiremer.ts. i

l b. The air supply line for ASCO Solenoid Valve EJ-HCV-88905 appeared to be l

sustalled with inadequate seismic supports. Approximately eight feet of i

,

rigid and hard copper tubing were not seismically supported, as well as a i

drain valve and the solenoid air b olation valve.

l c. During field walkdown of valve EJ.HCV88908 a loose 5/8' air line j

i was identified.  ;

1

.

4 d. Work Request #1042-87 written for valve Di-HV8851 contained a confusing 7

) step for the recording of a valve serie.1 number. j

1 i

1

RESPONSE TO THE FINDING i

i

l a. The new model solenoids were originally procured as replaca'ents for the

! solenoid valves. The spare parts had been purchased in accordance with  ;

'

the original Westinghouse Purchass Order which included seismic and  ;

i environmental qualification requirements. In addition, the Haterial

l Received Report (HRR) includes a certificate of conformance documenting

'

the compliance with Westinghouse Purchase Order and the applicable Codes [

j and Standards. Based on this discussion, the seismic and environmental i

considered during the  !

equivalency

~

of the replacement parts were '

! procurement process: therefore, no hardware deficiency has been

i identified. However, reference to this equivalency should have been

j documented on the 10CFR50.59 Safety Evaluation.

i

l b. The Instrument Air System at WCGS, of which the subject tubing is a part,

f is non-safety related and non-seismic. The copper tubing in question is '

.

) designed to ANSI B31.1, and the branch line feeding the solenoid on Valve

i

EJ.HCV.88905 is field routed and supported in accordance with t

)

Specification 10466.H 203. Appendix X. In the event of the fsilure of l

I this air supply tubing, the valve will return to its fail-safe mode.

i Trom the standpoint of !!/1 considerations the subject tubing was  !

reexamined by an engineering walkdown subsequent to the $50HI Review. The  :

l valkdown confirmed that no adverne II/I condition exists with the mbject [

)

installation and no !!/I considerations need be made for the sub9ct r

) tubing installation. l

c. The cause of the loose air lir.e support is unknown. [

t

t

i

, d. The root cause of the confusing work instruction on valve Dt-HV8881 was  !

j the lack of adequate review of work instructions by the maintenance [

r

1 lead electrical engineer.

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Section II

Page 35 of 70 l

April 28, 1988

ACTIONS WHICH HAVE BEEN OR VILL BE TAKEN

c. The loose air line support was tightened in accordance with Work Request

  1. 4802-87.

d. Step 36 was an informa tion only item for maintenance. It was not a

requirement of the installation, therefore no corrective action to correct

the intent of the step was taken. Work instructions are currently being

reviewed in a much more attentive manner prior to issue in attempt to

ninimize confusing items in the future.

CONCLUSION:

a. VCNOC scknowledges that the 10CFR50.59 Safety Evaluation for PMR 2018

Asco Solenoid Valve Replacement should have identified the reference to

equivalency and suitability of the repiscement solenoids. In order to

preclude further omissions of this nature, the subject deficiency will be

brought to the attention of those personnel performing safety evaluations

through reviev of the SSCHI team audit findings and the VCNOC response.

No further action is warranted at this time,

b. As discussed above, the subject installation does not require additional

seismic or II/I consideration, and as such WCNOC does not consider this

,

item to be a deficiency.

c. The identification of the loose air line st'pport was corrected on WR

  1. 4802-87.

d. WCNOC acknowledges that confusing work .nstructions existed. Current

plans for more detailed reviews. word processing capability, and the

normal recognition of experience will minirize these type of problems.

These improvements will be implemented by September 1, 1988.

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Section II

Page 36 of 70

April 28, 1988

3.1.2.5 PMR 2329: RAYCif?N SPL'@

FINDING:

This PHR did not require field work and was used to document the disposition

of 38 deficient Raychem splices identified in VR 4443-87 that were to be

dispositioned 'use-as-ds'. The Raychem splices were not installed in

accardance with the Raychem instructions in that overlaps were less than the

required two inch minimum and bend radii were less than the required five

times the outside diameter. The PMR had been approved based on Wyle Nuclear

Environmental Qualification Test Report No. 17859-02P, Revision A. The Wyle

test report qualified seven Byron and Braidwood Generating Station specific

configurations and thirteen Zion Generating Station specific configuratjans

with overlaps as little as 1/2 inch and bend radii of 1.2 times the outside

diameter.

The PMR, the VR which documented the 38 splices and the Wyle test report were

reviewed. In addition, the Nuclear Plant Engineering (NPE) personnel who

conducted the engineering evaluation and the Instrument Maintenance (IM)

personnel who had participated in the original walkdevn of the splices were

interviewed. The following concerns were identified:

a. The PKR did not contain an evaluation or documentation which indicated

that the WCGS design LOCA environment is equivalent to or less than severe

than the design LOCA environment that was used as a basis for the Wyle

testing. Evaluation and documentatica of the LOCA conditions is required

to establish a basis for use of the Wyle test report at WCGS.

b. VR 4443-87 documented the recommended disposition of 'use-as-is' for the

38 splices. The WR listed the splices and stated that all splices, as a

group, had seal lengths of greater than 1/2 inch but less than two inches,

and that the minimum bend radius was less than five times the shrink tube

outtr diameter. The VR did not document the configuration of each

individual splice or provide measured bend radii or overlaps. The EER

disposition that accepted the splices for 'use-as-is,' based on the Wyle

test report, s*.ated that the splices with bend radii as lit'.le as 1.2

times the outside diameter of the splice were tested. It also <cated that

the tested splices had bend radii more severe than the splics.s identified

at VCGS. However, documentation that each splice has a bend radius

greater th:n the bend radius tested by Wyle (stated as 1.2 times the

outside diameter) was not available.

The Vyle test report covered tests of tventy Raychem splices with

different configurations, tubing sizes and wire types. Only one splice

tested was of a configuration similar to the 38 deficient splices at WCGS.

The SSOMI team considered that the confirmation of each of the deficient

splices at VCGS should be documented to confirm that the results of the

Wyle tests are applicable.

c. The Vyle test report documented that the Raychem tubing was bent while it

was heated. The VCGS splices were performed in accordance with vendor

instructions which allowed the splices to cool befote bending. Bending

the cooled Raychem tubing is less conservative because of the reduced

pliability of the tubing at lower temperatures.

.

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Section II

Page 37 of 70

April 28, 1988

l

During a previous NRC Environmental Qualification (EQ) team inspection,

questions were raised reearding the lack of documentation for sizes and

lengths of machine screva used in Raychem splices. The maximum working

di aeter of Raychem tubing would be exceeded if the machine screw used to

connect the terminal lugs were too long. Following the EQ inspection, an

Engineering Evaluation Request was initiated by the licensee to establish the

acceptance criteria for conducting field measurements of tubing diameter to

insure that maximum Raychem working diameters were not exceeded. At the time

of the SSOMI inspJction, WR 4943-87 and other similar WRs were in process to

, inspect all suspect splices. The SSOMI team concluded that the WR appeared to

adequately verify and correct Raychem problems associated with exceeding the

maximum working diameter, but did not add ess the concerns discusseo above

regarding the applicability of the Wyle test report. The failure to

adequately document and evaluate the eng4neering disposition of the

nenconforming splices is a weakness in the engineerin5 area.

GENERAL DISCUSSION OF FINDING:

a. The concern was that PMR 2329 did not contain an evaluation or

documentation to show that the parameters of Wyle test report No.

17859-02P enveloped the WCGS environmental conditions.

b. The NRC was concerned that Work Request (WR) #4443-87 gave a 'use-as-is'

disposition for 38 kaychem splices with seal lengths of greater than 1/2

inch but less than 2 inches and bend radii less than five times the splice

outer diameter without specific documentation of the configuration of each

splice.

c. The Raychem splice was bent while heated in the Wyle Labs test report

(17859-02P) versus bending while cool for the WCGS splices. The NRC

considers the bending of cooled splices to be less conservative.

RESPONSE TO THE FINDING:

a. PHR 2329 did not contain the evaluation of Wyle Test Report No. 17859-02P

because Environmental Qualification Work Packages (EQWP's), not MR's,

are used at WCGS to document environmental qualification analysis.

An applicability review of the test report was performed prior to the

release of the PMR as stated in the Engineering Disposition to WR i4443 87

which was attached to the PMR. However, this revies was not formally

documented prior to the release of the PMR and included in EQWP-E-01013.

The documented review is required to be included in the appropriate EQWP

by Nuclear Plant Engineering Procedure KPN-D-313.

b. Only two of the 38 splices had seal length less than two inches. WR

14214-87, which is referenced in VR #4443-87, documents the seal length

for each splice. Instru=entation and Controls personnel verified verbally

to Nuclear Plant Engineering (NPE) that the bend radii of the splices were

not less than 1.2 times the outside diameter of the splice, however, this

phone conversation was not documented. While documentation of the bend

radius of each splice should have been provided, the lack of documentation

would not impact the 'use-as-is' disposition. Confirmation that the bend

_ _ _ _ _ _ _ _ _ _ - _ _ - _ _

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. Section II

Page 38 of 70

April 28, 1988

radii were greater than 1.2 times 0.D. allowed the use of only one test

report (No. 17859-02P) to address the deficiencies.

It should be noted that another Wyle Labs test report (No. 17859-02B),

which waa reviewed and determined applicable to WCGS, successfully tested

a Raychem splice which was bent back on itself with essentially zero bend

radius. The test parameters of this report bounds the WCGS conditions.

This report was subsequently included in the Equipment Qualification Work

Package.

c. The vendor irstructions state that the tubing is not to be flexed until

after cooling to the point it is comfortable to touch. This would prevent

thinning of the tubing at the point of bending. Since the splices tested

by Wyle were bent while heated, the testing indicates that acceptable

qualification exists even if thinning may have occurred. In addition, the

splice which was successfully tested with essentially zero bend radius in

Wyle test No. 17869-02B was bent while cooled.

ACTIONS WHICH HAVE BEEN OR VILL BE TAKEN

Verbal information utilized for dispositions, will te subsequently documented

and included with the appropriate documents prior to formal closeout of the

document.

CONCLUSION:

l

a. While it is true that the evaluation is not in the PMR, the performance

and documentation of qualification test evaluations is addressed by NPE

procedures. The results of these evaluations are in the EQVP's and are

nt. required to be included in PHR's. This is not considered to be

a deficiency.

b. Subsequent to this disposition. It was decided that all 38 splices should

be replaced with splites completed strictly in accordance with the Raychem

installation instructions. This replacement has been completed.

The NRC concern is partially addressed in that all the specific splice

seal lengths were provided in WR #4214-87. While the bend radius for each

splice should have been provided, inclusion of this information would not

have changed the original 'use-as-is' disposition,

c. The concern regarding bending of the splices while heated or cooled is not

considered significant in t!at successful qualification tests have been

performed for splices bent both while cool and while heated.

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

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Section II

Page 39 of 70

April 28, 1988

3.1.2.6 PMR 1828: ESV BUILDING CABLE REPLACDfENT

IJUDING:

This PMR replaced cables routed to the Emeraency Service Water (ESW) building

based upon the need for additional circuits at the ESW structure and the

identification of several failures in existing cables. Cable failures were

discovered during the performance of surveillance testing in which circuit

breakers failed to trip open on a non safety related load shed signal during

Safety Injection actuation. Investigation by the licensee resulted in the

identification of grounded and open circuit conditions in a number of cables

which had been pulled through the duct bank system from the Main Power Block

to the ESW building. Subsequent evaluation of the failed : ables identified

damage in the form of cuts and nicks in the insulation and jackets of these

cables. This damage was assumed to hr.ve occurred during the initial cable

pull. Consequently, this PMR was issued to pull new cables to the ESW

building.

,

Although the licensee perforced an evaluation of the damaged cables, an

additional evaluation to determine the root cause of the failurcs in the

original safety related cables routed to the ESW building was not performed.

The SSOMI team noted that banding material had been found in a duct bank

associated with some of the damaged cables and was considered by the licensee

to be the cause of the failures to the cables in that duct bank. However, the

root cause for cable failures in redundant trains and cables associated with

other duct banks has not been determiaed. The SSOMI team was concerned that

the conditions associated with the original cable pulls were not evaluated to

provide assurance that the cable failures were not the result of a generic

condition.

GENERAL DISCUSSION OF FINDING:

The SSOHI team identified a concern with PMR 1828, ESW Building Cable

Replacement, that the root cause for control cable failures had not been

determined. The SSOMI team was concerned that an evaluation was not performed

to eliminate the possibility of a generic condition affecting the opposite

train.

RESPONSE TO THE FINDINGt

The original revision of PMR 1828 provided a design for replacement of control

cables in both safety related trains. After removal of the damaged train A

control cables information was available to justify revision of the PMR to

exclude the other train of control cables. The justification for concluding

i that the failures were not indicative of a generic condition involved the

following facets:

(1) During the design development of FMR 1828 detailed cable pulling

calculations were performed in order to add the maxinum number of

l spare control cables possible. These calculations represented a

l limiting case (more severe than the original design) which

established that the original ductbank design (e.g. distance between

manholes, slope of the ducts, etc.) provided for a safe pulling

l

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. _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ ___ _ _ _ _

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e Seition II

Page 40 of 70

April 28, 1988

length for the original control cable installed. Therefore, the

ductbank design was eliminated as a potential root cause for th6

control cabla failures.

(2) A review of the number of control cable failures and their physical

routing within the ductbank was accomplished. This review revealed

that seven conductors had failed in the A train and one conductor had

failed in the B train. In addition, the A train conductors had the

'

same physical routing within the ductbank.

(3) An evaluation of the damaged cables removed during the train A cable

pull revealed damage to the outer jackets as well as conductor

insulation damage at various locations. Based on discussions as well

as visual observations of the cable (exposed copper was not

corroded), some of the damage to the cable occurred during removal

from the ductbank. However, some damage cccurred prior to removal

'

based en visual observation of copper corrosion found on the exposed

conductor (in one case the conductor had completely corroded away).

This damage is judsed to be the leading contributor to the control

cable failures that probably occurred during the initial

installation.

(4) The available spare control cables were assessed for future

contingencies. In order to maximize the available spare conductors,

auxiliary relays wcre added to train B control circuits to provide

4 two additional train B control conductors.

i

-

(5) The fact that only one control cable has failed in train B provides

evidence that the contcol cables were not damar,ed during installation

as indicated by the large number of faili,res in train A. This

conclosion is based on the premise that cables that have a common

failure mode should have approxJmately the same averrge time to

failure under the same conditions. Therefore, if any other control

cables in train B are affected, additional failures in train B should

have been identified.

1

Based on these considerations,. adequate justification s;isted to craciude that

, the failure mechanisms were isolated to train /. only. Br.s ed on this

j conclusion. PHR 1828 was revised to eliminate ths train B control cable

i replacement.

CONCLUSION:

VCNOC believes that adequate justification exists to conclude that the control

cable failures were not indicative of a generic condition affecting the

opposite train. It is tras that the justification was not assembled as a part

of the subject FMR and, therefore, not readily available for the SSOMI team

involved with the installation and testing inspection.

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Section II

Page 41 of 70

April 28, 1988

3.1.2.7 CONTAINMENT PRESSURE TRANSMITTERS

FINDING:

During plant inspections associated with other modifications, it was noted

that the connection box cover for Containment Pressure Transmitter PT-934, was

missing one of two screws. Maintenance or modifications were not in progress

'

on the transmitters. A field inspection of the other pressure transmitters

identified the following discrepancies.

PT.934 - Missing 1 of 2 connection box screws.

PT-935 - No discrepancies noted.

PT-936 - Missing 1 of 2 connection box screws.

PT-937 - Missing 1 of 2 connection box screws.

PT-938 - No discrepancies noted.

PT-939 - Missing 1 of 2 connection box screws.

The licensee indicated that the missing cover screws may have been left out

during a Raychem splice inspection. These discrepancies indicated a lack of

attention to detail in maintenance and modification activities but were

considered to be minor in nature.

CENERAL DISCI)J' YON OF FINDING:

The inspection team found one of two connection box cover screws on several

of the containment pressure transmitters missing. Although the inspection

report admittoi this to be minor in nature, it concludes that the missing

screws indicate an overall lack of attention to detail in performing

maintenance or modifications.

RESPONSE TO THE FINDING:

Although the actual reason for the missing screws could not be determined, it

is most likely that at some time during construction, startup or commercial

operation the cover screws were lost. It is possible that because personnel

were aware that the covers servad no direct safety function such as

environmental sealing or steam impingement protection and because one screw

adequately holds the cover in place, efforts we-e not made to obtain

replacement screws.

ACTIONS WHICH HAVE BEEN OR VILL BE TAKEN:

When Instrumentation and Controls was notified of the missing screws,

replacement screve were immediately obtained and installed. The SSOMI

Inspection report has been discussed in a monthly shop meeting with emphasis

placed en workmanship requiring attention to detail and has been routed as

required reading.

_ _ _ _ _ . .

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. Section II

Page 42 of 70

April 28, 1988

CONCLUSION:

The impact of the missing screws is considered minor in nature, however,

workmanship and attention to detail has been emphasized in monthly shop

meetings. No further specific action is considered necessary.

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! Page 43 of 70

April 28, 1988

3.1.2.9 TECIDTICAL SPECIFICATION TESTS

FINDING:

The SSOHI team monitored the performance of Technical Specification

Surveillance Tests (STS) STS IC-280A, ' Analog Channel QP Test Ctrl Rm

Detection Train A,' and STS IC-433, ' Channel Calibration HIS Post Accident

Monitoring N61,' to ensure that they were performed in accordance with the

requirements of the listed test procedures and were administratively

controlled by procedure ADM 02-300, ' Surveillance Testing.' STS IC-280A

verified the operability of the Chlorine Detection Control Room Ventilation

Isolation System and STS10-433 calibrated the Post Accident Monitoring

Huclear Instrumentation System (NIS).

The performance of STS IC-280A was in accordance with requirements. Test

personnel were knowledgeable and appeared qualified to accomplish test

objectives. However, several weaknesses were observed in the test

instructions of STS IC-433. A lack of detail in some sections of the

procedure resulted in confusion on the part of the Test Technician. For

l

example, a note to Section 6.3.1.3.1 incorrectly referenced ' sero power' as a

prerequisite for bypassing certain steps of the procedure. This note should

'

I have referenced a Nuclear Instrumentation System (NIS) Source Range level. In

I

addition. Sections 6.3.2.2.2 and 6.3.2.3.2.1 specified test equipment

connections which could not be accomplished without removal of the appropriate

solid state circuit card. The removal and reinstallation of the circuit card

and any subsequent requirement for equipment warm up were not detailed in the

, procedure. Consequently, interpretation on the part of test personnel was

( required in order to accomplish the test objectives. As a result of these

discrepancies, the test perfornance was suspended until the procedure was

revised.

The S50MI team was unable to determine the extent of this concern because of

the limited sample of tests and test procedures available for review. The

test personnel were knowledgeable and this test could have been accomplished

through application of the skills and experience which they possessed.

However, the SSOMI team was concerned that detailed and accurate test

instructions were not provided to ensure that test objectives and applicable

TS requirements are fulfilled in approved surveillance procedures.

GENERAL DISCUSSION OF FINDINO:

During the pe rf ormance of STS-IC-433 the inspector identified what he

considered several weaknesses in the test instructions. The term 'Zero

Power * vas considered in.dequate because nuclear instrumentation system

was not specifically mentioned as the source reading to determine 'Zero

Power". Additionally, two paragraphs identified test point connections

that required circuit card removal to gain access to them. The procedure

did not specify removal and reinstallation of the circuit card.

_ _ _ _ _ _ _ _ _ _ _ _ ____ ______

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Section II  !

Page 44 of 70 l

April 28, 1988

,

RESPONSE TO THE FINDING

The procedure was initially developed directly from instructions contained in

the controlled technjcal manual by personnel very familiar with the ,

equipment. The manual instructions assume that the performer has the drawings l

In the manual readily available. It is possible that when the procedure

was previously performed the technicians had the manual with them to aid in

physically locating specified test points.

ACTIONS WHICH HAVE BEEN OR VILL BE TAKEN:

'

The test was suspended to allow the test performer tire to research and

change the procedure. Temporary procedure change (TPC) MA 87-481 was written

to clarify the steps in question. Follow.fng TFC approval the test was

satisfactorily completed. An ongoing review of procedures is providing a high

level of confidence that test objectives and Technical specifications are met.

CONCLUSION:

,

The inspection report states that 'The test personnel were knowledgeable and  :

this test could have been accomplished through application of the skills and

experience which they possessed.' The actioria taken bf the test performera

when questions were encountered were proper. Thn test was stopped,

'

clarification was obtained, and the procedure was enhanced prior to

continuing. This is considered to be a normal par *. of improving procedure t

instructions as a result of experience. The weaknesses found in STS10-433 '

did not compromise the valid performance of the test. No further action is

considered necessary.

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Section II

Page 45 of 70

April 28, 1988

3.2.2.1 TEMPORARY MODIFICATION TMO 87-120 CK: CidhPED OPEN CRJIS D3MPFR

FINDING:

This modification clamped the Train A Control Room Emergency Ventilation

System supply damper in the open, actuated position in response to several

failures of the actuating linkage'. The SSOHI team determined that the

licensee had not adequately determined whether the system remained operable

and capable of pressurizing the centrol roem as required by TS 3/4.7.6.

TS 3/4.7.6, ' Plant Systems - Control Room Emergency Ventilation System,'

requires that the Control Room Ventilation Isolation System (CRVIS) be

operable in all modes and capable of pressurizing the control room to 0.25

inches of water (gauge) upon detection of radiation or toxic gas in the air

intakes. In addition, Section 3.1 of the USAR and 10 CFR 50, Appendix A.

require that safety systems be designed tc automatically protect againct

single failures of passive and active components. The system configuration

entsblished by the temporary modification provided a bypass path for supply

air to the centrol room if the Train A fan failed to automatically start on a

CRVIS initiation signal. Upon CRVIS actuation, the Traic B CRVIS fan would

start and discharge air to the fan discharge plenum, however the clamped open

Train A damper would permit backflow through the idle Train A CRVIS fan and

bypass the control room. In this configuration, the CRVIS would not be able

to provide the required positive pressure in the control room, assuming the

single failure of Train A CRVIS fan. Additionally, the licensee had not

performed a calculation or a functional test to demonstrate tha ability of the

Train B CRVIS to maintain the tequired control room pressure in this degraded

mode.

Additional concerns associated with this temporary mocification were noted as

follows: -

I

a. The licensee failed to recognize the requirement for the safety system to  !

'

remain operable with a single failure without operator action. In order

to ensure the operability of the CRVIS, the temporary modification

required an operator to remove the clamp from the failed CRVIS damper.

l

Although these actions would pe rmit Train A to be isolated upon fan

i failure and therefore satisfy the single failure design of the system, the

l need for operator action to meet the single failure design of a safety

system does not conform to the requirements of 10 CFR 50, Appendix A.

b. Even though the operator actions did not meet single failure design

requirements, the specified operator actions would not be sufficiently

responsive when considering the design requirement of the CRVIS to

maintain a positive prcssure in the control room in the event of radiation

or gas in the air intakes. The emergency instructions require the

operator to don a self-contained breathing apparatus, go to the damper,

climb a ladder to the blocked damper, remove the clamp and manually ensure

that the damper has closed. Furthermore, the SSOHI inspector noted that

these instructions would have been difficult to implement in an emergency

because they were not found in the Alarm Response Procedure as normally

expected, but were included as an addendum to the temporary modification.

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Section II

Page 46 of 70

April 28, 1988

c. Despite having performed repeated Safety Evaluations on this and other

CRVIS dampers which were sLailarly clamped open, the licensee failed to

recognize that additional testing or calculations vera necessary to verify

that the system remained operable with the temporary modification

implemented.

d. Appropriate corrective action in preventing rupeated damper fs' lures was

not taken Five CRVIS damper failures were experienced during the period

of June 25 to November 3, 1987. As a result, replacement operating gear

to repair the broken train A CRVIS supply damper was not available.

Appropriate corrective actions require a consideration of past defects and

noncompliances in basic components important to safety, VCGS Procedure

'

ADH 01-033, ' Instructions Describing Reportability Review and

Documentation of Licensee Event Reports and Defect Deficiencies,' Rev. 16

specified evaluation and reporting requirements pursuant to 10 CFR 21.

The licensee had not identified the above failures as potentially

reportable nor evaluated the failures per the above procedure.

GENERAL DISCUSSION OF FINDING:

a..b..c.

The SSCHI team stated that the 10CFR50.59 Safety Evaluation did not

adequately de te rmine if the CRVIS damper blocked in its safeguards

position by the subject modification impaired the operability of the

CRVIS function in fulfillment of the systems safety function.

Additionally, they stated that the temporary change introduced a stated

compromise of the single failure criteria which is not in accordance

with the general design criteria for nuclear power plants.

The Technical Specifications require two independent Control Room

Emergency Ventilation Systems to be operable in all HODES. The ACTION

statement during HODES 5 and 6 states that with both Control Room

E=ergency Ventilation Systems inoperable suspend all operations

involving core alterations or positive reactivity changes.

RESPONSE TO THE FINDING:

a. b..c.

In the USAR Chapter 15 analysis, the bounding worst single failure has

been ascertained to be the failure of the filtration fan in one of the two

filtration system trains. Operator action is required to isolate the

train with the failed filtration fan. At the same time, one train of the

control room pressurization system will also be isolated. Prior to

i s e'.a tion , a potential pathway exists allowing air from the control

building to enter the control room, bypassing the control room filtration

filters. After isolation, one control room pressurization fan and one

'

control room filtration fan operate for the duration of the accident. No

bypass pathways then exist for unfiltered air to enter the control room.

.

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Section II

Page 47 of 70

April 28, 1988

Blocking the subject damper open in its safeguards position did not put

the system in a condition outside of previous analysis nor create a

different type of accident nor increase the probability or passibility

of a malfunction from previous analysis. Safety Evaluation Three

of USAR Section 6.4.4 for the Control Room Ventilation System states that

"no single failure will coepromise the systems safety functions.' In

view of the inherent design aspects of the system, the denial of the

damper to go closed upon occurrence of an active failure does not put

the system outside of previous analyzed system failures since other

limiting failures exist.

The subject dampers are closed by their motor operators when the air

conditioning units fan motor is deenergized. They do not have a spring

returnt hence, the damper failure mode is 'as is'. Clamping these

dcmpers open would place them in their safeguards position where they

could fulfill their intended CRVIS safety function. A single failure per

10CFR$0 Appendix A means an occurrence which results in the loss of

i

the capability of a component to perform its intended safety function. -

Clamping the damper (s) open does not compromise the CRVIS safety

function. The designated operator action was not essential, but wonid

have placed the system in a censervative tested configuration.

d. Defect Deficiency Report 87-122 was initiated on November 17, 1987, as a

'

result the SSOMI team concern about performing a 10 CFR Part 21

reportability evaluation of mechanical problems associated with damper

GK-D-084 and its actuator GK-H2-40A. A review of the maintenance work

requests for dampers / actuators GK-D-080/GK-H2-29A, GK-D-081/GK-HZ.0290

GK-D-084/GK-HZ-40A, GK-D-085/GK-H2-40B was conducted. *his review

identified that the actuators wr:e reworked during 1984 with some

machining being conducted on the cmaplings. In 1085, CK-HZ-40A ard B were

replaced due to the actuators being jammed. In 1987, failures of

GK-H2-29A. 40A and 40B, occuteed which required replacecent of the

actuators. Discussions with a vendor representative indicated that these

failures could be attributed to a misalignment of the coupling and the

saddle because of previous maintenance and the method of clamping the

dampers when blocking them open or closed. The vendor has subsequently

provided appropriate tolerances and coupling clearances to ensure proper

coupling alignment. WCNOC concluded that this deficiency was not

reportable pursuant to 10 CFR Part 21.

The appropriate tolerances and coupling clearances were obtained and an

alignment jig was fabricated to assist in alignment of the saddle and the

coupling. Three of the above dampers were realigned. The fourth danper

was inspected and determined to be within the tolerances provided.

CONCLUSI0?h

a..b..c.

The 10CFR50.59 Safety Evaluation was not deficient in its analysis of the

subj2ct change. The condition described in thu evaluation was bounded by

the analysis presented in Chapter 15 of the Updated Safety Analysis

Report. Damper replacement parts were installed and the CRVIS system was

restored on November 26. 1987.

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Cection II

Page 48 of 70

April 28, 1988

d. As discussed above, VCNOC believes the cause of the repetitive damper

problems during 1987 have been identified and corrected

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Section II I

I Page 49 of 70 I

April 28, 1988 i

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3 3.2.2.2 PMR 2106: PRESSURIIEE SPRAY VALVE BONNET REFaIR

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FINDING:

-  ?

This PHR involved the installation of gland plugs or set screws in four j

'

injection holes as permanent modification to the Pressuriser Spray Valve. The  ;

four injection holes were drilled in the bonnet of the Pressuriser Spray Valve  ;

! in order to provide an injection path for a liquid sealant (Furmanite) which  ;

] was used to repair the body-to-bonnet steam leak. j

i

i The engineering disposition of Engineering Evaluation Request (EER) 85-XX-37,

'

i which requested that NPE approve the use of certain sesling corgounds in

temporary repair procedures at the discretion of the Maintenance

i Superintendent, previously approved the repair of leaking mechanical joints in

piping components such as flanges, valve packing, and bolted valve bonnets by i

l the use of sealant injection, provided that the sealant chemistry I

"

requirements, application procedure, and system limitations specified in the ,

engineering disposition were followed. The disposition approved the generic l

!

use of liquii sealing compounds such as Furmanite and authorized drilling

i holes into pressure tcta N ng parts of ASME Code Class I components in order

l to facilitate the repair process.

!

WR 00101-87 and associated revisions, the vendor work request and procedure,  !

the engineering disposition to PMR 2106 and other associated documentation  !

l vhich were a part of the work package were reviewed. The following concerns i

were identified:

(

) a. Section 3.2, ' Bolted Connection,' of the application procedure, which was (

i detailed in the engineering disposition to EER 85-XX-37 and used to repair  ;

the Pressurizer Spray Valve, was act verified to meet the ASME Code t

j requirements. The Justification of Engineering Resolution for EER [

i 85-XX-37 indicated that the disposition ensured that Code requirements I

i were not violated. NPE subsequently indicated that the requirements cited l

l in the Justification of Engineering Resolution were obtained from the  !

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Vendor and not from the ASME Code as indicated. When requested by the [

SSOHI team, the licensee could not demonstrate that the tequireswnts  !

j provided by the vendor met the Code requirements. (

'

)

b. The SSCHI team considered that the 10 CFR 50.59 Safety Evaluation of EER l

!' 85-XX-37 was inadequate, in that it did not identify that drilling holes  ;

into pressure retaining parts of ASME Class I components involved changes

' the facility. Although the Safety evaluation performed for VR

to  !

00101-87 Rev. 3, correctly determined that the holes drilled in the f

] pressurized bonnet were a change to the facility, the explanation given i

, for determining whether this instance involved an unreviewed safety

j question was inadequate because it failed to address the safety ,

} significance of the modification to the Pressuriser Spray Valve using EER

i 85-XX-37.

i

! c. The engineering disposition to EER 85-XX-37 required the sealing compound

injection pressure to be calculated so as to limit the injection pressure f

-

and thereby limit the stress on the flange bolts. Documentation of these j

calculations was not available. Additionally. the maximum pressure used ,

to inject the sealant compound in the body-to-bonnet area of the (

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Section II

Page 50 of 70

April 28, 1988

Pressurizer Spray Valve was not recorded. Because the maximum pressure

was not calculated and records did not exist to demonstrate the pressure

used, the flange bolt stresses could have been exceeded for the

Pressurizer Spray Valve during the injection process.

d. A Safety Evaluation was not performed for the vendor work procedure to

repair the Pressurizer Spray Valve by sealant injection as required. ADH

07-100 requires that a 10 CFR $0.5.' Safety Evaluation be completed for all

procedures reviewed by the Plant Safety Review Committee (PSRC),

GENERAL DISCUSSION OF FINDING:

a. During the review of PMR 2106, the SSOHI team determined that the

Engineering Disposition to EER 85-XX-37 was not verified to meet the ASME

Code requirements.

b. During the review of PMR 2106, the SSOHI team determined that the Safety

Evaluation associated with EER 85-XX-37 was inadequate in that it did not

identify that drilling holes into pressure retaining parts of ASME Class 1

components involved changes in the facility. Also, the SSOHI team

determined that the Safety Evaluation performed for WR 00101-87, Rev. 3

was inadequate in that it failed to address the safety significance of the

modification to the Pressurizer Spray Valve using EER 85-XX-37.

c.,d.

The repair of the pressurizer spray valve (PMR 2106) was a SSOHI team

audit item. The content of the PMR was a repair instruction on holes

drilled into the packing box of the pressurizer spray valve to stop a

body-to-bonnet leak by the use of '?urmanite'. The PMR issued was not

implemented and was cancel!.ed. A replacement of the valve packing box

was performed instead. .

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During the investigation, two concerns were expressed in the peocedures  :

for allowing Furmanite to inject the valve.

1) Documenting the injection pressure of the Furmanite compound.

2) No Safety Evaluation was performed on the Vendor Procedure

used to implement the vendor work plan.

RESPONSE TO THE FINDILQ1

a. The disposition to EER 85-XX-37 provided generic guidelines to facilitate

temporary on-line sealing of leaking components. This disposition was

used for the temporary on-line sealing of the packing box flange on valve

BB-PCV-455B and applied the guidelines set forth in Section 3.2, ' Bolted

i Connection *, of the subject disposition.

The disposition to EER 85-XX-37 also identified systems which come into

contact with p-imary fluid and required approval from WCNOC Management i

prior to performing sealant injection on these systems. However, the

disposition does not clearly identify the Code (s) to which the

requirements for drilling holes into ' Bolted Connections * comply with and

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Section II

Page 51 of 70

April 28, 1988

did not include provisions to verify code compliance for specific

components to which these generic guidelines would be applied.

Work Request 700101-87, Rev. 3 requested an engineering evaluation of a

proposed permanent repair to the temporary injection holes. The

engineering disposition to VR #00101-87 Rev. 3 required that the

injection holes made on valve BB-PCV-455B during the temporary on-line

sealing process be permanently weld repaired in accordance with the

Section XI repair and replacement program.

b. 1. The Safety Evaluation issued with EER 85-XX-37 did not identify a

change in the facility as described in the safety analysis report. As

indicated on the Safety Evaluation, this evaluation ' addresses only

the suitability of the sealant materials, the injection procedures and

the effect of the procedure on thi sealed components'. As previously

discussed in the response to SSOMI item 3.2.2.2.a. the disposition to

EER 85-XX-37 provided generic guidelines to facilitate temporary

on-line sealing of leaking components and did not apply to any

specific component.

2. Vork Request 00101-87, Rev. 3, requested an engineering evaluation of

a proposed permanent repair to valve BB-PCV-455B which had previously

been sealed on-line by Furr.anite. The proposed repair involved using

gland plugo or cet screws to seal the injection holes made during the

on-line sealing process.

After review of the specific request to provide a pormanent repair

using gland plugs or set screws. Engineering determined that the

injection holes would need to be volded pcr ASMI Section XI

Repair / Replacement Program. The engineering disposition and

associated Safety Evaluations performed address only the specific

repair request in WR 00101-87, Rev. 3. Therefore, the Safety

Evaluation provided for the disposition to WR 00101-87 Rev. 3, which,

as discussed above, has as its scope only the permanent repair of the

temporary injection holes, and is considered adequate within the

confines of the scope of the final permanent repair. The subject

safety Evaluation was not intended to address the alteration

(temporary) made to the pressurizer spray valve to facilitate on line

sealing.

c. An Engineering Evaluation Request, (EER 85-XX-37), disposition was

used in preparing and planning the injection of the pressurizer spray

valve. The disposition gave generic criteria to be met when using

Furmanite to inject a component to stop leakage. The disposition

required that the injection pressure should be limited suen that when

the injection pressure times the beating area of the sealant plus the

system operating pressure times the area subjected to system pressure

shall not exceed 1.1 times the flange bolt allowable stress. This

formula is used to figure injection pressures. This value has been

recalculated and the injection pressure specified (4500 psi) was a

conservative number.

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Section II

Page $2 of 70

April 28, 1988

A second part of this concern was that the injection pressure was not

recorded. There was no requirement in the work package Instruction

Checklist to record the injection pressure.

d. At the time of the injection of the valve, there were no I

procedural requirements to process a Safety Evaluation (10 CTR 50.59) for

' Vendor Procedures'. At this time there are no procedural requirements i

to process a safety Evaluation for ' Vendor Procedures'. Howeywr,

PSRC review of these procedures is required. '

} ACTIONS VMICH HAVE BEEN OR VILL BE TAKEN l

'

!

a. The guidelines provided in the disposition to EER 85-XX-37 for temporary

r

! on line sealing were intended to be generic guidelir.es only and did not

'

apply to any specific component (s). Th!s disposition will be withdrawn '

and modified to mandate provisions for verification of Code compliance }

'

! prior to applying the generic guidelines for temporary on line sealing of

specific components. This corrective action shall be accomplished prior  ;

to June 1. 1988.  !

I

b. As indicated in the response to SSOMI item 3.2.2.2.a. EER 85-XX-37 is l

being withdrawn and will be modified to mandate provisions for Code

j compliance verification prior to performing any temporary on-line sealing *

l'

of specific components. The assoc!sted Safety Evaluation will be provided

with the modified EER dispositi?n.  ;

CONCLUSTON: l

f i

s. VCNOC agrees with the SSOMI teams observation that the guidelines outlined l

l in the dispositien to EER 35-XX-37 were not verified to meet ASHI Codo

requirements for all components. t

r

As indicated above, these generic guidelines were not applicable to i

specific components. Therefore, the previous disposition is being  !

!

withdrawn for revision to indicate that application of the guidelinis

'

needs to be verified for compliance with the applicable design Code of the .

j specific application prior to implementation.  !

!

l It should be noted that the ASHE code neither allows nor disallows

temporary drilling of components for the purpose of on-line sealing.

Verification of Code Compliance in these cases needs to consider the ,

effect of this type of temporary condition, i.e. drilling holes into I

component parts, on the original design (structural) basis of the subject ,

component,

f

r

In a letter dated January 25, 1988, from L. C. Shao. Director Division of

Engineering & Systems Technology. USKRC. to J. L. Milhoan. Director <

Division of Reactor Safety. Region IV. USNRC. concerning the use of h

sealing fluids on primary pressure boundary ccaponents the NRC evaluated  !

the concern identified at WCGS. The NRC stated that. 'In conclusion. l

temporary on-line leak sealing of components is an acceptabic alternative [

to an unscheduled plant shutdown to effect a permanent repair provided  !

!

,

1

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Section II

, Page 53 of 70

April 28, 1988

i

that the applicable guidelines are met and the Quality t.ssurance measures ,

are followed for proper selection, procursuent end opplication of

sealants'.

h. As discussed above, VCNOC ecknowledges the SSOMI team concern regarding

the safety Evaluation associated with EER 85-XX-37. ,

i

The SSOHI team concern regarding the adequacy of the Safety 5 valuation i

provided with work request WR 00101-87 Rev. 3 is not consiuered to be a

a deficiency. As discussed above the subject work request and associsted

safety evaluation was limited in scope to only address a final permanent

repair.

c.,d.

,

Although not documented, the injection pressure specified 4500 psi, was ,

proven to be a conservative number. Also, there was no requirement to

doc'iment the actual injection pressure but QC accepted the pressure that

was used. Baced on these two facts, no corrective action is necessary

for item 4.2.2.3.c.

l

l A Safety Evaluation is presently not required for Vendor Procedures. The

Work Controls Task Force is reviewing the Vendor Vork Plan Procedure (ADH

i 01-043). This procedure will be revised by August 31, 1988, to require l

t

safety evaluations to b) performed for vendor procedures. Due to the

i procedural requirements and actions being taken, no further corrective

! action is required.

,

!

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,

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f

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- _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ __ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

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Section II

Page 54 of 70

April 28, 1988

3.2.2.3 PMW j084: CCV PIPE VALL THINNING

,

FINDING:

This PMR involved application of a weld overlay on a Component Cooling Vater

(CCV) line servicing the Train A Residual Heat Removal (RHR) Heat Exchanger in

order to repair a pipe section downstream of Valve EJ-V033. The licensee's

ultrasonic examinction of the piping section determined that the pipe section

was below minimum will thickness. Although subsequent ultrasonic ex4minations

dete rmined that these results were erroneous because laminar inclusions

(acceptable conditions), rather than the wall inner diameter, were being

identified, the SSOMI tuam identified the following concerns:

a. The licensee did not declare Train A of the CCV and RHR systems inoperable

per TS after identifying that the piping was below minimum wall thickness.

The licensee subsequently issued a guidance memorandum on July 29, 1987,

directing the plant operators to consider system as inoperable if

requirements for minimum piping wall thickness were violated. The general

matter of the licensee's handling of these and other similar operability

matters was subject of an NRC:NRR-licensee meeting in NRC headquarters on

November 17, 1987.

b. The riping was repaired without being isolated and drained of water, even

though the test results showed wall thinning down to nearly 1/16 inch

(about 22 percent nominal). Although Velding Procedures WPS1-0000,

'ASME/ ANSI General Requirements,' Rev. 2, permitted welding under these

i

conditions, the SSOMI team considered that the procedure represented a l

high risk of wall burn through, threatened system pressure boundary

integrity, and therefore represented a unconservative repair procedure.

c. Major changes in the work instructions for veld overlay repairs on the

EJ-V033 piping were implemented by Revision 2 to VR 0702-87 but were nct

incorporated into the revised ASME Section XI work instructiont 4-

required by Section 9.3.6.1 uf ACM 01-036, 'VCGS ASME Section XI Repair

and Replacement Prograv.' Rev. 2. ADM 01-036 required that work packages

contain complete and concise work instructions to accomplish repairs and .

provided guidance for content. Revision 2 to the VR fmplemented changes l

in the basic repair procedure and included requirements for in-service  !

leak testing and radiography. The existing work instruction was annotated ,

to delete all existing steps by Revision 2, but replacement work steps I

were not provided. Additionally, the repairs were compiled without craft

or QC signoff of the revised work instructions.

d. The post modification leak testing of the piping was not accomplished as

rsquired by procedure until two months following completion of the work.  !

e. During the review of this FMR, the SSOMI team also noted that ASME

required radiography was incorrectly deferred by the engineering

disposition of Corrective Work Request (CVR) 0702-87, Rev. 1, for about

six months. 10 CFR 50.55a(g)(5)(iii) requires NRC notification when

conf o rmance with certain code requirements is impractical. The licensee

did not initially notify the NRC when the radiography was deferred.

1

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.. . . .

Section II

Page 55 of 70

April 28, 1988

Following identification of similar oversights by the NRC Resident

Inspectors, the licensee submitted a Code Relief Request for the

radiography of PHR 2084 repairs on August 24, 1987.

GENERAL DISCUSSION OF FINDING:

a.

The NRC states that at the time the ultrasonic testing determined that

there was a below minimum wall condition on a pipe section downstream of

valve EJ.V033, plant operators should have declared Train A of the CCW and

RER systems inoperable. VCNOC did not initially declare Train A of the

CCW and RHR systems inoperable, since when it was initially determined

that the CCW and RHR piping was below the code mininum wall thickness

allowed for new pipe, the Plant Staff was not aware that this condition

represented a potential noncompliance that needed to be expeditiously

i evaluated by Engineering to determine whether or not the as-found pipe

1

thickness was sufficient to maintain maximum design basis stress below the

q code allowable stresses.

b. The piping section. SA-106Gr8 Carbon Steel Pipe. 0.375' nominal wall

thickness, was repaired utilizint an external weld overlay which extended

i around the entire circumference of the pipe. This weld repair was

j performed without the piping section being drained of water, even though

the ultrasonic examination indicated that the piping had localized areas

] of wall thinning as thin as .086*. Although the applicable velding

procedures pe rmitted welding under these conditions, the SSCHI team

j considered that the procedure represented a high risk of wall burn

through, tarentened systen pressure boundary inttausty, and therefore

'

represented a unconservative repair procedure,

c. Revision 2 to Vork Request 00702-87 deleted all previous work

instructions, implemented changes to the basic repair procedure, includen

requirements for inservice leak testing, and deferred the required

radiographic examination until the next refueling outage. Complete and

concise work instructions were not developed and incorporated into the

revised ASHI Section XI work instructions as required by the applicable

V7NOC procedure. Subsequently the repair was completed without craft

signoffs of the revised work instructions.

!

d. The required post modification leak testing of the piping was not

accomplished until two months following completion of the work,

e. Because the intent of the veld overlay was to re?torv the nominal pipe

wall thickness to .375 inches and this repsir exceeded the lessor of 3/8

inch or lot of section vall thickness, radiograph = of the repaired area in

accordance with the ASHI BLPV Code. Section '; ;. Subsection ND was

required. However, further review of the repair process revealed that

1. the area of repair would contain an irregular surface on the

interior of the pipe due to postulated erosion.

2. the repair was to be conducted with the pipe filled with water.

These two factors were judged to take examination by the radiography

method difficult to interpret with meaningful results because of the

m ,

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Section II

Page 56 of 70

April 28, 1988

d

irregular surface and that the water would induce diminished sensitivity.

In lieu of radiography, Engineering determined that surface examination of  !

'

each veld deposit layer and adjacent heat affected sono by the liquid

penetrant or magnetic particle method would provide adequate assurance of

the suitability of service by the repair weldment until the Code required <

,

examination or suitable raterial replacement could be performed,  !

RESPONSE TO THE FINDING:  !

a r

1 a. When it was initially determined that the CCV and RHR piping was below

the code minimum wall thickness allowed for new pipe, the Plant Staff was

'

not aware that this condition represented a potential noncompliance that

needed t.o be evaluated by Engineering to determine whether or not the

'

as-found pipe thickness was sufficient to maintain maximum design basis

stress below the code allowable stresses. Therefore, the time between

] initially discovery and subsequent declaration of the EJ piping as

inoperable was inappropriately long.

i

j Although the November 17, 1987, meeting discussed in the finding is not a

j major issue for this item, it should be noted that the meeting was held at

a the request of VCNOC and the primary subject of the nesting was the VCHOC

pipe wall u.spection ;,rogra= and the results obtained to that date.

]

] b. VCNOC personnel considered the following factors whon developing this ,

'

repair procedure and concluded that this repair could be performed with an '

acceptable level of risk.

1) Pressure / temperature of portion of system being repaired. This !

'

a portion o: the CCV/RHR .ystem had been removed frem service and

! allowed to cool ts ambient temperature. The system head i

pressure, not system operating pressure, was present during the ,

j repair operation.

{

l 2) To minimize the possibility of wall burn through, the first veld

layer was deposited utilizing the Gas Tungsten Arc Velding i

process, maintaining as low amperage as possible, while remaining '
within the Velding Precedure Specification limitations, to localize

1

and reduce heat input. Additional weld metal was deposited utilizing

the Shielded Metal Arc Velding process, increasing amperage and/or

electrode diameter with subsequent layers.  ;

) 3) Previous experience of WCNOC personnel had been that had the velder

' burned through* the pipe wall it would create minor leakage, and  ;

'

j not a serioue pipe failure.

i

. 4) VCNOC personnel performing the repair, were in constant contact

2

with the control room to initiate system isolation and drain down

,

if the welder ' burned through' the pipe. ,

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Section II

Page 57 of 70

April 23, 1988

i c. The applicable procedures for work requests and ASME Section XI Packages

4 contain different requirements for the devel',,pment and revision of work

instructions. Personnel failed to follow correct procedural

requirements for development and revision of the ASME Section XI Package

work instructions. per ADM 01 036.

d. het modification testing for this repair consisted of an ultrasonic

thickness examination, radiogrisphic examination and a leak test at

normal operating temperature ar.d pressure. However, due to the assumed

,

internal damage to the pipe from cavitation erosion, it was determined

'

that obtaining code acceptable radiographs, and their subsequent

interpretation, would be extremely difficult, if not impossible. Based

on this assumption, the radiographic examination was deferred until the

next refueling outage.

The work instructions for post modifiestion testing did not clearly

define the timeliness of the required testing. Subsequently, upon

completion of the ultrasor.ic thickness examinations the work package was

incorrectly placed in a ' hold' file for completion of testing during an

4

upcoming refueling outage prior to performing the required leak testing.

e. The reason for deferring that radiographic examination without prior NRC

notification was a failure to recognize the applicability of 10 CFR

I 50.55a(g)(5)(iii) to post maintenance testing. The requirements were

interpreted to be applicable only to inservice testing and not post

j maintenance testing.

l ACTIONS VHICH HAVE BEEN OR VILL BE TAKENt

a. Procedure requirements ensure that engineering is promptly notified of

wall thinnir g concerns, and that engineering evaluations are completed

j promptly to support operability determinations. These procedures will

, minimize the time period for identifying equipment which is in an

inoperable condition.

c. WCNOC Maintenance / Modification personnel, are developing a standardized

, work package preparation program which will place all work instructions

in a word processing program for producing step by step work instructions

on a standardized format. This program will be developed and

implemented by August 31, 1988.

'

d. The required post modification leak test has been performed.

'

.

Maintenance Engineers have been cautioned to follow up with tiecly review

and completion of NDE requirements and subsequent post modification tests.

e. Upon notification from the NRC that deferring post maintenance testirg

seguirements of AEME Ccde Class 1, 2, and 3 components was governed by the

requirements of 10 CFR 50.55a(g)(5)(iii). VCNOC requested and received, on

June 23, 1987, temporary relief from ASME Section XI in order to defer the

radiography required by the Code. On June 30, 1997. (not August 24. 1987

as stated in the report) a formal request for relief alonr. with the

Technical Justification for the pipe section downstream of valve EJ-V033

,

was submitted to the NRC.

_ _ _ _ _ _ - _ _- _ _ _

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1 Section II

"

Page 58 of 70

April 28. 1988

l

CONCLUSION:

<

a. Subsequent to the determination that the EJ piping could potentia 11v

exceed Code allowable stress for a worst caso design basis event, it was

declared inoperable. The timeliness in requesting the evaluation and

making that determination was inappropriately long. Procedure

requirements ensure that engineering is promptly notified of wall thinning

] concerns, and that engineering evaluations are completed promptly to

support operability determinations. These procedures will minimits the

'

, time period for identifying equipment which is in an inoperable condition.

b. In conclusion. VCNOC personnel determined that performing this weld

l repair with ' stagnant' water in the system could be satisfactorily

accomplished without putting the system or plant in jeopardy,

c. The completion of the standardized work package preparation program w!11

1 resolve this concern.

!

d. Typically the required post modification testing is performed as

soon as possible upon completion of work, therefore timeliness of

testing is not normally specified. Eovever, in this case where a

.

'

deferment of the radiographic examination was being performed, the leak

test should have been specified to be performed when the system was

returned to normal operating temperature and pressure.

J

Clearly, deferment of a required post modification radiographic

j examination is an unusual deviation from normal operating procedures. In

future instances when requirements are deferred, the timeliness of all

J testing will be clearly specified in the work instructions.

e. At the time of the deferment of the radiography for piping downstream of

valve EJ.V033. VCNOC did not recognize the requirement of 10 CTR 50.55a to

notify the 4mmission for this case. Since VCN0C is now aware of this

]

requirec*et, the Commission is being notified of cases in which post

j maintenance testing for ASMI components is going to be deferred.

4

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Section II

Page 39 of 70

April 28, 1988

3.2.2.4 PMR 2116: VAT,VES EF-V090. EF-V058. EF-ifV47 AND EF-ifV48 HARD

SURFACIPO

FINDING:

This PHR involved the final repairs of Essential Service Water (ESV) system

piping, including EF.V090 piping downstream of Valve EF-V058 on the opposite

train. Additionally, this modification involved replacement of a carbon steel

24' X 16' bell reducer with a stainless steel replacement more resistant tc

erosion and corrosion. Adjacent piping was also hard surfaced with either

stainless steel or stellite veld overlays. The PHR, associated VR packages

and in progress welding and fitup of a new piping bell reducer at EF-Vn58 were

reviewed. On November 12, 1987, during the $50HI inspection, work on the

above VRs ano all safety related pipe fitting and walding activity conducted

by the Haintenance Department were suspended by QA Work Hold Agreement 123.

The Work Hold Agreement, issued jointly by the QA and Maintenance Departments,

cited for fourteen Conditions Adverse to Quality involving PHR 2116 as ths

basis for the work suspension. These included improper piping cutouts,

marginal or inadequate pipit 4g fitups, failure to temporarily cupport piping

for spool remeval, out of tolerance spool fabrication, bypassed QC hold

points, improper veld buildups and overlays, and others. This work hold

followed a previous QC requested work stoppage.

Maintenance and QC Department management indicated that the problems

associated with PHR 2216 were caused by the Maintenance Department's lack of

experience in major pipe fitting nodifications. Previously, such vork was

perf o rmed by contractors under the direction of the Facilities and

Hodifications (F&M) Department. This sedification was transferred to FEH on

November 13, 1987, and work resumed following review and revision of work

,

instructions on November 14, 1987.

No concerns were identified with respect to this work. However, the SSOHI

team's review of testing requirements identified that the hydrostatic test

instructions for replacement of ESV piping downstream of Valve EF-V58, did not

consider possible overpressurlastion of adjacent systems, the testing

pressurized a portion of the ESV system to 220 psig and required a test relief

valve set at 239 psig. The procedure provided a single valve isolation for

thirteen heat exchangers served by the piping. No provisions were included to

ensure that the adjacent components were aligned such that test boundary valve

leekage will be vented to atmosphere or the untested portion of the system.

The SSCHI team was concerned that the test boundary valve leakage without

component protection could result in pressurisation of the heat exchangers in

excess of the pressures allowable under ASHE Section XI.

CENERAL DISCUSSION OF FINDING:

The SSCHI team finding concerning the Hydrostatic Test performed downstream

of valve EF.V038 per Vork Request $2931 87 is outlined in 3 items:

1) Instructions issued with the test package did not consider the

possibility of overpressurizing adjacent ASHE systems.

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Section II

Page 60 of 70

April 28, 1988

2) The valve lineup for the test provided only single valve isolation

for thirteen ASMI heat exchangers. Test instructions did not provide a

means of venting possible leakage past single isolation boundary

valves to atmosphere or to the untested portion of the system.

3) Soundary valve leakage may have subjected several ASME heat exchangers

to pressures er.ceeding ASME Sectiot. XI allowances.

RFSPONSE TO THE FINDING:

Subsequent to ths finding. F.evision 5 to Vork Request 2931 47 added several

open valves to the lineup to permit venting boundary valve leakage into the

untested portion of the EF System.

Valves ET.V33? and EF.V227 open to the atmosphere, provided overpressure

protection to heat exchangers in some adjacent systems as follows:

SGL11A was isolated from the bydrostatic test by boundary valve EF.V057.

On the inlet side of this heat exchanger, valve EF.V056 was open with

valve EF.V227 vented to atmosphere.

SGK04A was isolated from the hydrostatic test by boundary valve EF.V040.

On the inlet side valve EF.V039 was open with valve EF.V227 vented to

atmosphere.

SGG04A was isoleted from the hydrostrtic test by boundary valve EF.V147.

On the inlet side of this unit. valve EF.V146 was open and EF.V227 vented

to atmosphere.

SGL15A was isolated from the hydrostatic test by valve EF.V042. On

the vs.it inlet side, valve ET.V041 was open. Valve ET.V227 was vented to

the atmosphere.

SGF02A was ivolated frem the hydrostatic test by valve ET.YO48. On its

inlet side, valve EF.V047 was open with ET.V227 vented to the atmosphere.

SGL12A was isolated from the hydrostatic test by valve EF.V030. i

Upstream from this unit valve EF.V029 was open with EF.V227 vented to the

atmosphere.

SGLO9A was isolated from the hydrostatic test by valve EF.V033. On the

inlet side. Valve EF.V032 was open, and EF.V227 vented to atmosphere.

SGL13A was isolated from the hydrostatic test by valve ET.V036. On the

inlet side of this unit. valve ET.V035 was open. ET.V227 vented to

accosphere.

SGL10A was isolated from the hydrostatic test by valve EF.V038. Upstream.

Valve EF.V037 was open with valve EF.V227 vented to atmosphere.

Clearance Order 87 1228.EF shows valve EF.V272 open and valve ET.V332 open

to atmosphere, providing added protection against overpressuriaation for the

heat exchangers listed above.

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Section II

Page 61 of 70

April 28. 1988

The outlet from heat exchanger EEG01A was isolated by valve EF-HV59. Also,

valve EF-VOS8 was removed during the test. Note that with EF-V058 removed.

line EG-208HBC 16 is open at the flanged end of pipe spool EF03 5006. This

provided a vent to a tmos phere preventing accidental pressurization of the

EEG01A shell side in case of boundary valve leakage.

Containment cooler heat exchangers SGN01A and SGN01C were isolated by

valves EF-BY45 EF-HV47, and EF-HV49. Thus these heat exchangers, were

'doublo' isolated from the test boundary after that portion of the line was

filled and vented.

SGK05A and the diesel generator coolers on 'A' train were double isolated

from the hydrostatic test by valves EF-V053. EF-V055 and EF-V273.

ACTIONS WHICH HAVE BEEN OR VILL BE TAKEN

VCNOC believes the finding as stated was correct. Prior to the

hydrostatic test Work Request 2931-87 was revised accordingly, thus ensuring

that the heat exchangers mentioned above would not be pressurized in excess of

ASME Section XI limits.

A revision to the hydro.tatic and pneumatic test procedure HGH.M00C-02 will be

made to add precaution 7.2.4.1 'The test instruction must include provisions

for over pressure protection of systems or components adjacent to single

isolation test boundary valves. Leakage past these single isolation boundary

valves must not subject other systems or components to pressure exceeding ASME

Section XI allevances' . This procedure revision will be completed by July 1

1988.

CONCLUSION:

VCNOC agrees that the subject finding is correct and the corrective actions

taken in response to this finding should preclude ue pressurization of heat

exchangers in excess of the pressures allowed by ASME Section XI.

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Section II

Page 62 of 70

April 28, 1988

3.2.2.6 PMR 0904: ESSENTIAL SERVICE VATER CHECK VALVES

FINDINGt

This pMR installed isolation valves for Essential Service Water (ESV) Check

Valves EF.V0046 and EF.V0076 to improve the maintenance and testing of the

check valves. The PHR added two new gate valves. EF.V0345 and EF.V0346. The

review of the PMR and the associated work packages found that clearance Order

l No. 871061EF, which was used to establish the clearance boundaries for the

work, did not provide correlation between the initials and signatures of the

individuals establishing and verifyleg the boundary as required by 10 CFR 50

Appendix B, Criterion XVII, ' Records' Criterion XVII requires that quality

records shall, as a minimum, identary .Te inspector or data recorder, other

licensee procedures, such as surveillance procedures, typically include a

tabulation which correlates the individual's initials and signatures to permit

positive identification. The SSCHI team considered that the personnel

performing valve lineups should be clearly identified.

CENERAL DISCUSSION OF FINDING:

During an NRC review of Clearar.ce Order 87 1061.EF, which was used to

establish clearance boundaries for implement.ation of PMR 0904, it was fou2d

i that there was no correlation between the initials and signatures of the

individuals establishing and verifying the boundary. The NRC's basis for this

Finding, as stated, is that 10 CFR 50 Appendix B. Criterion XVII ' Records'

! requires that Quality Records shall, as a minimum. identify the inspector or

l data recorder.

RESPONSE TO THE FINDING 1

10 CFR 50 Appendix B, Criterion XVII specifically states Inspection and Test

l Records shall, as a minimum, identify the inspector or data recorder, the type

of observation, the results, the acceptability, and the action taken in

I conjunction with any deficiencies noted.'

l The Clearance Order form is used by operations to establish and document safe

working boundaries for maintenance / modification activities and is not

considered an inspection or ttst record.

l CONCLUSION:

VCNOC does not consider this item to be a deficiency based on the requirements

of 10 CFR 50 Appendix B. Criterion XVII. It should be noted that VCNOC

r.anagement desires and is capable of identifying the individuals establishing

clearance bouadaries. This can be secomplished through a process of

determining the shift in which the clearanec was established and reviewing

operatiens Special order $7, ' Safety Tagging for Persennel Authorized to

Perform Tagging Activities'. This Special Order lists tagging Authorities as

well as individuals authorized to hang and remove tags. In addition, this

Special Order specifies personnel authorized to sign on and off of Clearances.

Additional methods are being reviewed to improve the capability to identify a

specific individual involved in tagging under the safety tagging program.

This review will be ccmpleted by June 1. 1988.

,

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gection II

Page 63 of 70

April 23, 1988

j,32.2.7 FMR 1363: N"IlfG FUMP CONTROL VALVE CAVITATI00f **"I

I l E DIG.L

This PMR replaced the trim in Charging Pump Plow Control Valve 30.PCV121 with

a new design. The former valve tria experienced cavitation damage because of

the high flow and high pressure drop while in service.

VR 4430 86, used to implement PMR 1363 for Valve PCV.121, did not note that

PMRs 1613 and 1635 were performed concurrently. Contrary to Note 9 on Copes

Vulcan Drawing D.283137 which required a total of nine packing rings to be

installed, step 7 of the work package was annotated to indicate that twelve

rings of packing were installed. The licensee indicated that the reason there

were more packing rings installed was because the licensee had implemented

PMRs 1613 and 1633 concurrently with FMR 1363. PMRs 1613 and 1633 removed

packing leakoff piping and lantern rings and replaced braided asbestos packing

with graphite packing. More rings of replacement packing had to be used to

replace the originally installed packing. A review of PMRs 1613 and 1635 by

the $$0MI team found that the installation of the new packing material was

acceptable, and the team noted that a supplemental valve repacking instruction

was attached to the VRs which implemented the requirements of PMR 1635 for

packing replacement. The failure to annotate VR 4430 86 to cross reference

the above PMRs for documentation completeness is considered a weakness.

GEN 11tAL DISCUSSION OF FINDING:

The concern was that in the work instructions for implementing PMR 1363.

reference Vork Request #04430 86, states to repack the valve in accordance

with the technical manual, which states that nine (9) rings of packing needs

to be installed. According to Vork Request #04430 86, twelve (12) rings of

packing were installed. PMR 1633 changing valve packing to a non. asbestos

material, also allowed the removal of the lantern ring. which in turn, made

more room for packing in the stuffing box. The concern expressed by the $50MI

toam was that PMR 1635 was not referenced on Work Request (04430 46.

RESPONSE TO THE FINDIN3:

During the implementation process of PMR 1633, packing is fabricated by

the mechanics using dies and ribben type packing. Numerous valves have

been repacked in the plant with only one known failure. The generic

instruction sheet used for repacking gives a stuffing box dimension. The

number of rings is not considered as important as the inside and outside

diameter of the packing ring. The quantity, as specified on drawings, is

considered more of a purchasing number than application number. For

examples if a valve is repacked and there is room for more packing or not

enough room for the packins as stated by the drawing, the mechanic is going

to pack the valve using good maintenance practices.

It should also be noted that packing is a consumable item and as the

service life of the valve increases, more packing will be installed

depending on valve performance, not the number of packing rings specified on a

drawing.

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Page 64 of 70

April 28, 1988

It should also be recognir.ed that PMR 1635 changed the thought process

of repacking a valve. Asbestos type packing, as specified on most

drawings, is very seldom if ever used.

EqHCLUSION:

Valve SG-FCV121 was repacked on November 11, 1986 on Work Request #52181-86.

The leak off line was removed. (PHR 1613 on October 5, 1987). This PMR has a

requirement that before the leak off line can be removed, the valve aust be

packed with graphoil packing: which was completed by work Request $52181-86.

The valve trim change out was completed on October 9, 1987 per Work Request

  1. 04430-86. All work was performed per the dicection given in their respective

PMR's and by using good maintenance practice. Therefore, it is delt that no

corrective actions or changes to the program need to be performed.

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April 28, 1988

3.2.2.9 PRESSURIZER SAFETY VALVE TESTING  !

FINDING:

The SSOHI team reviewed the ASME Code Section XI testing of the Pressurizer

safety valves. The test procedure and the implementation of the test i

procedure were inadequate because the test procedure did not use the

representative temperature of the valve when installed in the system as

required by TS 3/4.4.2.2. Additionally, because the 'as-left" valve l

temperature was not recorded for valves which were tested and reset, the TS

requirements could not be substantiated.

Three direct acting Code Safety valves made by the Crosby Valve and Gage

Company were installed on the Pressurizer. ASME Section XI Article IWV-3500,

required that the valves be tested on a rotating basis so that each valve is

tested at least once every five years. This five year cycle for valve testing

began with facility consnercial operation.

As a result of NRC Region IV concerns with the adequacy of the testing of the

safety valves, the licensee conducted setpoint testing of the three installed

valves (BB-8010A, BB-8010B, and BB-8010C) during the current outage. The

licensee elected to test the valves by the use of a local bench test becauss

of dissatisfaction with the contractor which had previously tected the Main

Steam safety valves. Th'a pressurizer safety valres were previously tested by

the valve vendor between 1977-1978 and had not exceeded their ASME Code

testing periodicity requirement. Additionally, three spare valves had been

tested in March 1987. The inspector reviewed the detailed test procedures and

data and identified the following concerns.

a. Five of the six valves tested had setpoi .s well beoow the minimu's TS

limit of 2461 psig. Additionally, the 'C( talve setpoint was found to be

below the Pressurizer Power Operated Relief Valves (PORVs) setpoint,

although the licensee indicated that this safety valve had not lifted  :

durlag a prior plant transient which had caused the PORVs to lift.

The valves were bench tested in accordance with a method acceptable by the

ASME Coda, using a low volume, high pressure test rig. The valvus were

variously heated to sinulate ambient installed conditions using eithwr

heat blankets or a ' hot box' equipped with electrical heating elements.

As corrective action ene 'B' and 'C' valves were replaced with spara

safety valves and the 'A' valve was reset and reinstalled.

b. The SSOMI team also noted that the safety valves exhibited greater thc.n

expected setpoint deviation with respect to temperature variations. l

Dia. gnostic testing of the safety valves, pe: Jorce 1 as a result of (

discrepancies identified in the 'B' and 'C' valve testing, indicated thst

the valve setpoint dropped about 0.87 psia por degree Fahrenheit (F)

1;.c rea s e . The diagnostic testing was perforced at various ambient

temperature condit t

a vinging frvm 80 to 17S degrees F and various nnzzle L

rinc settings. D.s nozz1t, ring adjusts the valve litt sensitivity. The ,

licensee performed an informs 1 statistical evaluation of this data and l

founi the temprature setpoint relationship to be linear. A review of the

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Section II

Page 66 of 70

April 20, 1988

Electric Power Research Institute (EPRI) test data for similar valves

found the temperature setpoint shift observed at WCGS to be two or three

times and the maximum inferred from the EPRI data,

c. The temperature conditions used to test the installed valves were

different from the temperature conditions used to test the spare valves.

The installed valves were tested per procedure STS MT-005, ' Pressurizer

Code Safety Valve Operability,' Revision 1, which specified that the

valves be heated to 120 to 200 degrees Fahrenheit (F) to simulate the

ambient condition as required by the TS. The spare safety valves wore

tested by detailed test instructions baaed on the Crosby Vat"- Manual

which specified that the valves be heatad to 120 to 140 - - F.

Additionally, test temperature data was not required nor collectra for the

valves that were tested and reset and the licensee could not substantiate

that the test temperatures represented the "as-insta11ed' valve ambient

conditions as required by TS 3/4.4.2.2.

d. NPE had not been involved in the evaluation of dita nor the determination

of the correct test temperatures. As a result of the SSOMI team concernt,

the Maintenance Department issued EER No. 87-BB-21 on November 16, 1987,

requesting specification of a valve test temperature range which would

satisfy the TS requirements. The disposition to this EER, issued on

November 18, 1987, provided a temperature range of 70 to 120 degrees F and

direction for obtaining temperature measurements. The SSOHI team

considered that the EER disposition was unsatisfactory because the

temperature recommended by NPE did not have a correlation with the actual

installed conditions.

e. Pressurizer safety valves are equipped with guide and adjusting rings

which control the valve blowdown. The ASME Ccde and associated test

requirements assume that guide ring settings established dr. ring vendor

certification testing result in repeatable valve configurations which do

not require periodic testing. Therefore bench testing, which does r.ot

change the ring settings, is allowed even though it does not verify actual

blowduwn perf o rma ncs . During the inspection, the SSOHI team found that

the ring settings for the ""Tre Pressurizer ssfety valves were not set as

required by the manufacturer to ensure a proper valve bleedown

characteristic. Furthermors, the guide rtng position hsd not been

verified on the installed Pressurizer safety valves, and the testing

procedures did not include steps to verify guide ring position wnenover

the Pressurizer safety valves wer* tested.

f. Tne licensee fa116d to eval * ate tha information contained in I&E

Information Notico 66-05, 'Hain Steam Safety Valve 7est Failures and 1.ing

Setting Adjuatments,' and I&S :nformation Notice 06-05, Supplement 1,

which identitled valve performance protlems resulting from impreperty

established guide ring se+ sings. Incorrect ring settings had been found

to re ult an insufficient relief capacity and have possibly contributed to

premC.ure valve operation and'or reseating failures. Although the I&E

Information N7ti;e addressed ibin S tetti safoty valves and not the

Pressurizer safety v11ves, the Prossuriser safety 'alves at VCG5 are

essentially identical in configuration to the Main Steam aafety valves and

whould have been evalusted. t

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April 28, 1988

GENERAL DISCUSSION OF FINDING:

a.,b.,c.,e.

Four maintenance items were identified conaerning the pressurizer safety valve

testing.

1) 3.2.2.9.a - 5 of 6 valves tested below the setpoint.

2) 3.2.2.9.b - Temperature seemed to have more of an impact on setpoint than

would be expected.

3) 3.2.2.9.c - Test temperatures used had no correlation with ambient temper-

atures at the pressurizer.

4) 3.2.2.9.e - The guide ring and blowdown ring settings were not verified.

d. As a result of questions concerning the ambient temperature conditions of

the Pressurizer Code safety valves during power plant operation and the

temperature influence with regard to setpoint acceptance testing,

Engineering was requested to provide the temperatures to be utilized and

where physically on the valve to monitor that temperature during testing.

EER 87-BB-21 was dispositioned providing an ambient temperature range of

70 to 120 F. This temperature range was based on an evaluation of normal

operating containment conditions judged to be reasonably accurate in the

immediate area of the Pressurizer Code Safety valves. Locations for

temperature monitoring on the valves during setpoint testing were also

provided.

f. Although tha Pressurizer Code Jafety valves were not the subject of IEE

Information Notice 86-05, ' Ma i'4 Steam Safety Valve Test Failures and Ring

Setting Adjustmentd' And ILE information Notice 86-05 Supplement 1, ehe

pressurizer code safot; valves are similar and should have been evaluated.

EESSONSE TO THE FINDING _1

a. b., c., e.

1) The three pressurizer code safety valves removed from the system, were

tested using a low volume, high pressure rig, utilizing a heat bir.aket

tv simulate operational ambient temparatures stated in tbc ".utinghouse

equipment specification. The test required the valve to lift (pop)

at 248S 1 1: psi. O'. the three valves cecoved from the pressuri2er, the

first tested witi.8a tolerance and the cther two tested below the

Technical Specification limit. Thtee replacement valves were tested in

a similar fashion with additional criteria, and tva of the m valves

tested out of tolercnce.

Of the two valves removed from the pressurizer that tested low, it was

found that the mechenic who tested these valves believed that when

the valves hissed er chattered indicated the setpoint, as found when

testing relief valves. The mechanic did not know that a safety valve

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P6ge 48 of 70

April 4.8, 1988

would fully lift when test pressure reached its setpoint. Additionally

the test equipment war being improperly used. Further testing of one

of these valves proved that the valve would operate as designed.

The replacement valves were tested with the same low pressure rig, but

were heated with radiant heat in a hot box to a lower temperature more

representative of actual ambient operating temperature. Each valve was

then required to lift two consecutive times in the test range. All

three presaurizer code safety valves were replaced with successfully

tested valves.

2) WCNOC believes that t', 9.87 pound decrease per degree of

temperature is invalid bas d on the inconsistencies in test

parameters, (i.e. method of tempvature control and length of time

to reach equilibrium).

3) The test temperature of 120 - 200 F was taken from the Westinghouse

design specification. The procedure was written with thesa values, during

Start-up of 1.he plant. The spare valves were tested between 120 - 140 P.

This value was not from the technicag manual but a value @osen which

fits within the criteria of 120 - 200 F.

The three valv e s installed were installed utilizing detailed work

instructions rather than procedure, allowing more specific details.

4) If the guide rings are not adjusted during testing, verifications were not

needed. In the case of the spare valves, the guide rings were adjusted

and placed back to what the Crosby Teeting Report specified.

d. The temperature range of 70 -120 F, prov1Nd for setpoint valve testing,

is considered adequate for the folleving reaso.a

1) Containment atmospheric conditions are designed to be maintained less

than 120 F. The location of the Pressurizer Code Safety valves from

the ;,ressurizer (11 f eet) is sufficient to preclude temperatures of

the valve to be excessively greater than that of the general aren.

2) The dominant factor thst may vary the relieving pressure setpoint in

regard to temperature is the relief valve spring. The location of

the spring in respect to the process fluid makes the temperature of

the spring more closely resemble the general area temperai.ure.

3) Subsequent temperature monitoring of the Pressurtzer Code Safety

valves during power operation during March

surface and spring temperatures ranging from 77,1988 to 88gevealed

F. Thisvalve

data

confirms the temperature range provi.tod in the Engineerir g

Jisposition to EER 87-BB-21.

4) Adequate compensation should ce given to operating temperature

conditions during the set pressure tasting of safety relief valves.

The Engineering Disposition to EER 87-BB-21 addresjed ambient

temperature conditions. Inlet pipe temperature conditions should

also be considered as to its applicability or influence on the test

results and the a ceptance of the test. Engineering concluded that

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Page 69 of 70

April 28, 1988

the contribution that the inlet pipe temperature has in relation to

that the spring imposes is negligible,

f. The pressurizer safety relief valves are designed to limit primary system

pressure excursions following anticipated operational and accident

transients. Operability of the safety valves was demonstrated by

prototypical testing and appropriate analysis in accordance with

NUREG-0731 II.D.1. The type of safety valve used at Wolf Creek, Crosby

Model HB-BP-86 6H6, was tested in an EPRI test program.

The ring settings used for the Crosby 6H6 valves at Wolf Creek aprcoximate

those used in a series of EPRI tests on the Crosby 6M6 valve, where

' reference' settings were used. Results from this series of tests are

considered applicable to the plant valves.

The safety valves are required to operate over a range of full pressure

steam, steam-to-water transition, and subcooled water flufJ conditions.

The valves were tested for the range of required conditions in the EPRI

test program. The acceptance of this test program and plant specific

results by the NRC was documented in a letter fro 9 P. O'Connor to B.

Withers, dated August 6, 1987.

ACTIONS WHICH HAVE BEEN OR VILL BE TAKEN:

a.,b.,c.,e.

1) The operability test procedure for the pressurizer code safety valves was

revised January 26, 1988 to reflect the following:

The procedure now includes a statement about the lifting characteristics

of a safety valve, minimizing test pstformance error.

Heating requirements of the valve for testing have been changed to reflect

more accurate representr. tion of actual ambient temperatures. Using

radiant heat, a more evea heat soak is obtained, and lessens thermal

gradients throughout the valve.

The test procedure now requires two successful consecutive pops within

the allowed tolerance. This shoulu verify the accuracy of the set

pressure.

2) None deemed necessary

3) Procedure STS HT-005, has been changed for a heat box to be used rather

than heat blankets. The box supplies a uniform heating source for the

valve, making a consistent temperature across the entire valve. A step

was added to the procedure to record the temperature of the valve at the

time the valve is tested. -

4) Three new safety valves were installed on the pressurizer on Work

Requests 91059-87, 03999-87, and 0430' 57. The guide ring settings were

verified to be correct per Crosby T,.t Data Sheet. The three valves

removed will ts disassembled, inspected, reessembled and tested on Work

Requests 70654-87, 70705-87 and 70655-87. At that time the guide rings

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will be verified as being correct per the Crosby Test 'ata Sheets. The

only time the guide rings need to be verified as be.ng set correctly

is when the rings need changed during the course of work.

CONCLUSION:

a., b., c., e.

Procedure STS MT-005 was first used during Refuel II. Though the

procedure satisfied the requirements of the Technical Specifications, the

methodology was lacking in direction. There has been a complete procedure

rewrite, incorporated on a temporary procedure change, and a permanent

procedure change is being written.

The items of concern expressed on the testing of the pressurizer safety

valve were resolved on Work Requests 191050-87, 104300-87, and #03999-87,

with detailed work instruction. The work instructions were then used to

develop a new procedure and work instructions for performing inspection

and testing of the three removed valves on Work Requests 170654-87, 17070."-87,

and 170655-87.

Temperature data is being taken in the plant at normal operating

pressure and temperature to further define the actual ambient temperatures

that are experienced by the safety valves. This data, when completed and

evaluated, will be incorporated into the procedure.

d.,f.

Based on the above discussions, WCNOC does not consider this item to be a

deficiency.

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