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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217K9401999-10-0606 October 1999 Submits Safeguards Event Log for Calendar Quarter Ending 990930,IAW 10CFR73.71.No Safeguards Events Occurred ML20210R9181999-08-13013 August 1999 Forwards Insp Rept 50-409/99-02 on 990726-28.No Violations Noted ML20210F3651999-07-0909 July 1999 Submits Safeguards Event Log for Calendar Quarter Ending 990630,IAW 10CFR73.71 & LACBWR Security Plan ML20196D5161999-06-21021 June 1999 Discusses Rev 19 to Various Portions of Lacrosse Boiling Water Reactor Emergency Plan Submitted Under Provisions of 10CFR50.54(q).NRC Initial Review of Changes Will Be Subject to Insp to Confirm No Decrease in Effectiveness of Plan ML20207G1991999-06-0303 June 1999 Informs of Reorganization in NRR Ofc,Effective 990328. Reorganization Chart Encl ML20206R9211999-05-10010 May 1999 Forwards Annual Financial Rept & Certified Financial Statements for DPC for Years 1998 & 1997,IAW 10CFR50.71(b). Util Will Forward 1998 Annual Rept as Soon as Rept Is Completed ML20206H6771999-05-0505 May 1999 Forwards Insp Rept 50-409/99-01 on 990414-16.No Violation Noted.Overall Performance During Decommissioning/Safe Storage Activities Was Good ML20206J3671999-04-30030 April 1999 Forwards Rev 13 to QA Program Description, IAW 10CFR50.54(a)(3) & 50.4(b)(7).Changes in Rev 13 Listed ML20205R4261999-04-0808 April 1999 Submits Ltr for Calendar Quarter Ending 990331 IAW 10CFR73.71, Reporting of Safeguards Events. No Safeguards Events Occurred During Quarter ML20204F8291999-03-0909 March 1999 Forwards Annual Rept on Status of Decommissioning Funding for La Crosse Boiling Water Reactor,Iaw 10CFR50.75(f)(1) ML20207C2661999-02-19019 February 1999 Forwards Radioactive Effluent Rept & Radiological Monitoring Rept for 1998 for Lacbwr. Lacbwr,Pcp & ODCM, Encl ML20207A9431999-02-11011 February 1999 Forwards Revised Pages to LACBWR Decommissioning Plan. Each Page with Change Will Have Bar in right-hand Margin to Designate Location of Change ML20198E4371998-12-17017 December 1998 Forwards Insp Rept 50-409/98-05 on 981207-10.No Violations Noted.Activities in Areas of Facility Mgt & Control,Spent Fuel Safety & Radiological Safety Were Examined ML20196A8921998-11-23023 November 1998 Forwards Rev 12 to LACBWR QA Program Description ML20155H4221998-11-0303 November 1998 Ack Receipt of Re Insp Rept 50-409/98-02,in Response to Transmitting Predecisional EC Summary & Exercise of Enforcement Discretion Re Compliance with Maint Rule ML20154K0191998-10-13013 October 1998 Forwards Insp Rept 50-409/98-04 on 980921-22.No Violations Noted ML20154P4351998-10-13013 October 1998 Responds to Re Insp Rept 50-409/98-02 & Refers to C/As Taken to Bring LACBWR Into Compliance with Maint Rule IR 05000409/19980021998-09-17017 September 1998 Discusses Predecisional Enforcement Conference Held on 980630 Re Insp Rept 50-409/98-02 & Exercise of Enforcement Discretion.Two Apparent Violations,Involving Failure to Implement Key Aspects of Maintenace Rule,Identified ML20151Z6501998-09-17017 September 1998 Discusses Predecisional Enforcement Conference Held on 980630 Re Insp Rept 50-409/98-02 & Exercise of Enforcement Discretion.Two Apparent Violations,Involving Failure to Implement Key Aspects of Maintenace Rule,Identified ML20153F7431998-09-14014 September 1998 Informs That Changes Made in Rev 12 Are Adminstrative in Nature & Do Not Result in Reduction in Commitment to Safety & Reliably Operate LACBWR in Safstor Condition,Per 980909 Telcon with NRC ML20237D8861998-08-21021 August 1998 Advises That Rev 18 to Portions of Emergency Plan Do Not Decrease Effectiveness of Plan & Plan Continues to Meet Relevant Stds of 10CFR50.47(b) & Therefore,Nrc Approval Not Required ML20237B9181998-08-17017 August 1998 Forwards Insp Rept 50-409/98-03 on 980811-12.No Violations Were Noted.Insp Included Review of Physical Security Plan for LACBWR ML20236W8111998-08-0303 August 1998 Forwards Summary of Decommissioning Insp Plan for Oct 1998 - Apr 1999,for Info.Plan Will Be Updated Approx Twice Yearly & May Be Revised at Any Time Based on Future Insp Findings, Events & Resource Availability ML20237E2631998-07-15015 July 1998 Forwards Rev 12 to QA Program Description. Page Change Locations Indicated by Bold Bar in right-hand Margin ML20236K7091998-07-0606 July 1998 Forwards Official Transcript Proceedings from 980513,public Meeting Held in Viroqua,Wi on Decommissioning of Lacrosse Boiling Water Reactor.Pen & Ink Changes Made to Original Transcript to Correct Errors & to Clarify Abbreviations ML20249A8331998-06-15015 June 1998 Expresses Appreciation for Support Provided for Recent Meeting Held at Viroqua High School - Middle School Complex on Decommissioning of Lacrosse Boiling Water Reactor ML20248M0461998-06-0909 June 1998 Expresses Appreciation for Support Provided for Recent Public Meeting Held at Viroqua High School on Decommissioning of LACBWR ML20216B9311998-05-0707 May 1998 Forwards Insp Rept 50-409/98-01 on 980420-0423.No Violations Noted ML20217K7121998-03-27027 March 1998 Forwards Rev 18 to LACBWR Emergency Plan.Bar Lines in right- Hand Margins Note Changes.Description of Each Change & Reason for Change Is Included as Cover Pages to Plan Rev ML20203K2041998-02-27027 February 1998 Forwards Summary of Decommissioning Insp Plan for Remainder of FY1998.Plan Will Be Updated Approx Twice Each Yr & May Be Revised Any Time Based on Future Insp Findings,Events, Resource Availabilty,Etc ML20202J4261998-02-16016 February 1998 Forwards Revised LACBWR Decommissioning Plan & Revised LACBWR Initial Site Characterization Survey for Safstor. Both Documents Revised Jan 1998 ML20202J0381998-02-10010 February 1998 Forwards Revised LACBWR Decommissioning Plan. Each Page W/Change Will Have Bar in right-hand Margin to Designate Location of Change ML20199A9351998-01-19019 January 1998 Forwards Insp Rept 50-409/97-01 on 971209-11 & 980107.No Violations Noted.Activities in Areas of Facility Mgt, Decommissioning Support,Spent Fuel Safety & Radiological Safety Were Examined During Insp ML20199J4111997-11-21021 November 1997 Informs That NRC Regional Oversight Responsibilities for LACBWR Has Been Transferred to Region III Div of Nuclear Matls Safety.Effective 971105 D Nelson Became Region III Point of Contact for Routine LACBWR Insp Matters ML20198R9721997-10-24024 October 1997 Forwards Changes to Physical Security Plan,Contingency Plan & Guard Force Training & Qualification Plan.Encl Withheld ML20149G1311997-07-10010 July 1997 Submits Ltr Re Quarterly Submittal of Safeguards Events Log for Quarter Ending 970630.No Safeguards Events During Past Quarter ML20148S9131997-07-0303 July 1997 Forwards Annual Financial Rept & Certified Financial Statements for Dairyland Power Cooperative for 1996 & 1995 ML20141H5581997-05-20020 May 1997 Discusses Change in Ofc as of 970520.Project Mgt for Facility BWR Will Be Assumed by Pw Harris.Site Visit Will Be Arranged Convenient to Both Staff & Scheduled Activities ML20141B7521997-05-0909 May 1997 Forwards TS Re Changes to LACBWR Controlling Documents ML20138H8011997-04-29029 April 1997 Forwards Corrected Page to Safety Evaluation,Issued by NRC, by Ltr Dtd 970425.W/o Ltr ML20138B6821997-04-25025 April 1997 Forwards Corrected Page 8 of SE for Amend 69 to La Crosse Boiling Water Reactor License ML20138A6431997-04-15015 April 1997 Forwards Rev 11 to LACBWR QA Program Description ML20137R7651997-04-11011 April 1997 Forwards Safety Evaluation Approving Changes to QAP Description ML20138B7261997-04-10010 April 1997 Submits Ltr for Calendar Quarter Ending 970331,IAW 10CFR73.71 & LACBWR Security Plan ML20134H1841997-01-31031 January 1997 Submits Quarterly Safeguards Event Log Re License DPR-45 ML20133A3721996-12-16016 December 1996 Forwards Rev 17 to LACBWR Emergency Plan ML20132F8601996-12-10010 December 1996 Forwards Revised LACBWR Decommissioning Plan. Each Page W/ Change Will Have Bar in right-hand Margin to Designate Location of Change ML20134M2421996-11-0505 November 1996 Forwards Rev 11 to QA Program Description, Clarifying Section I, Organization Paragraph 7.d Revised to Assure Majority of SRC Members Be Degreed Individuals ML20149F2461994-08-0202 August 1994 Ack Receipt of 10CFR50.54(a) Submittal Dtd 940620,which Incorporates Changes in Quality Assurance Program Description ML20058P1281993-12-0909 December 1993 Forwards Changes to Physical Security Plan,Contingency Plan & Guard Force Training & Qualification Plan.Encls Withheld (Ref 10CFR2.790(d)) 1999-08-13
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217K9401999-10-0606 October 1999 Submits Safeguards Event Log for Calendar Quarter Ending 990930,IAW 10CFR73.71.No Safeguards Events Occurred ML20210F3651999-07-0909 July 1999 Submits Safeguards Event Log for Calendar Quarter Ending 990630,IAW 10CFR73.71 & LACBWR Security Plan ML20206R9211999-05-10010 May 1999 Forwards Annual Financial Rept & Certified Financial Statements for DPC for Years 1998 & 1997,IAW 10CFR50.71(b). Util Will Forward 1998 Annual Rept as Soon as Rept Is Completed ML20206J3671999-04-30030 April 1999 Forwards Rev 13 to QA Program Description, IAW 10CFR50.54(a)(3) & 50.4(b)(7).Changes in Rev 13 Listed ML20205R4261999-04-0808 April 1999 Submits Ltr for Calendar Quarter Ending 990331 IAW 10CFR73.71, Reporting of Safeguards Events. No Safeguards Events Occurred During Quarter ML20204F8291999-03-0909 March 1999 Forwards Annual Rept on Status of Decommissioning Funding for La Crosse Boiling Water Reactor,Iaw 10CFR50.75(f)(1) ML20207C2661999-02-19019 February 1999 Forwards Radioactive Effluent Rept & Radiological Monitoring Rept for 1998 for Lacbwr. Lacbwr,Pcp & ODCM, Encl ML20207A9431999-02-11011 February 1999 Forwards Revised Pages to LACBWR Decommissioning Plan. Each Page with Change Will Have Bar in right-hand Margin to Designate Location of Change ML20196A8921998-11-23023 November 1998 Forwards Rev 12 to LACBWR QA Program Description ML20154P4351998-10-13013 October 1998 Responds to Re Insp Rept 50-409/98-02 & Refers to C/As Taken to Bring LACBWR Into Compliance with Maint Rule ML20153F7431998-09-14014 September 1998 Informs That Changes Made in Rev 12 Are Adminstrative in Nature & Do Not Result in Reduction in Commitment to Safety & Reliably Operate LACBWR in Safstor Condition,Per 980909 Telcon with NRC ML20237E2631998-07-15015 July 1998 Forwards Rev 12 to QA Program Description. Page Change Locations Indicated by Bold Bar in right-hand Margin ML20217K7121998-03-27027 March 1998 Forwards Rev 18 to LACBWR Emergency Plan.Bar Lines in right- Hand Margins Note Changes.Description of Each Change & Reason for Change Is Included as Cover Pages to Plan Rev ML20202J4261998-02-16016 February 1998 Forwards Revised LACBWR Decommissioning Plan & Revised LACBWR Initial Site Characterization Survey for Safstor. Both Documents Revised Jan 1998 ML20202J0381998-02-10010 February 1998 Forwards Revised LACBWR Decommissioning Plan. Each Page W/Change Will Have Bar in right-hand Margin to Designate Location of Change ML20198R9721997-10-24024 October 1997 Forwards Changes to Physical Security Plan,Contingency Plan & Guard Force Training & Qualification Plan.Encl Withheld ML20149G1311997-07-10010 July 1997 Submits Ltr Re Quarterly Submittal of Safeguards Events Log for Quarter Ending 970630.No Safeguards Events During Past Quarter ML20148S9131997-07-0303 July 1997 Forwards Annual Financial Rept & Certified Financial Statements for Dairyland Power Cooperative for 1996 & 1995 ML20141B7521997-05-0909 May 1997 Forwards TS Re Changes to LACBWR Controlling Documents ML20138H8011997-04-29029 April 1997 Forwards Corrected Page to Safety Evaluation,Issued by NRC, by Ltr Dtd 970425.W/o Ltr ML20138A6431997-04-15015 April 1997 Forwards Rev 11 to LACBWR QA Program Description ML20138B7261997-04-10010 April 1997 Submits Ltr for Calendar Quarter Ending 970331,IAW 10CFR73.71 & LACBWR Security Plan ML20134H1841997-01-31031 January 1997 Submits Quarterly Safeguards Event Log Re License DPR-45 ML20133A3721996-12-16016 December 1996 Forwards Rev 17 to LACBWR Emergency Plan ML20132F8601996-12-10010 December 1996 Forwards Revised LACBWR Decommissioning Plan. Each Page W/ Change Will Have Bar in right-hand Margin to Designate Location of Change ML20134M2421996-11-0505 November 1996 Forwards Rev 11 to QA Program Description, Clarifying Section I, Organization Paragraph 7.d Revised to Assure Majority of SRC Members Be Degreed Individuals ML20058P1281993-12-0909 December 1993 Forwards Changes to Physical Security Plan,Contingency Plan & Guard Force Training & Qualification Plan.Encls Withheld (Ref 10CFR2.790(d)) ML20059G6131993-11-0101 November 1993 Responds to Re Violations Noted in Insp Rept 50-409/93-01 on 930903 & 22 & 24.Corrective Actions: Reassigned Mechanics & Instrument Technician to LACBWR Staff ML20056E2601993-08-12012 August 1993 Forwards Nonproprietary & Proprietary Version of Analysis of Potential Blast Effects on LACBWR Reactor Bldg Due to 16 Inch Natural Gas Pipeline Failure,Suppl Analysis for Fast Closing Valve. Proprietary Version Withheld ML20056E2681993-05-11011 May 1993 Requests That Proprietary Analysis of Potential Blast Effects on LACBWR Reactor Bldg Due to 16 Inch Natural Gas Pipeline Failure,Suppl Analysis for Fast Closing Valve Be Withheld,Per 10CFR2.790(b)(4) ML20128P4611993-02-11011 February 1993 Forwards Rev to Annual Decommissioning Plan,Changing Requirement to Maintain Hourly Meteorological Data Logging for Effluent Release Calculations & Removing Makeup Demineralizer Sys ML20128K5891993-02-0909 February 1993 Forwards Corrected App a to Annual Rept for 1992 - Rept of Changes,Tests & Experiments ML20055H6371990-07-25025 July 1990 Forwards Decommissioning Fund Rept for Plant ML18041A2111989-11-16016 November 1989 Responds to Generic Ltr 89-19 Re Request for Action Re Resolution of USI A-47, Safety Implication of Control Sys in LWR Nuclear Power Plants. Actions or Recommendations in Generic Ltr Will Not Be Performed ML20248C5941989-09-21021 September 1989 Forwards Revised Radioactive Effluent Rept for LACBWR (Jan- June 1989), Incorporating Sr-89/90 & Fe-55 Analysis Data ML20247A1931989-08-22022 August 1989 Forwards Proposed Operator Licensing Exam Schedule Format for FY90 - FY93,in Response to Generic Ltr 89-12 ML20245G0911989-07-27027 July 1989 Advises That Util Already Exempt from 10CFR26, Fitness-for- Duty Program Because of Safstor Status.Request for Exemption Will Not Be Necessary Since License Amended to possession-only License Via Amend 63 ML20246K8411989-07-10010 July 1989 Responds to Generic Ltr 89-06, Task Action Plan Item I.D.2, Spds. All Spent Fuel Transferred from Reactor to Spent Fuel Storage Well & on 870804,License DPR-45 Amended to possess- but-do-not-operate Status ML20246B8371989-06-27027 June 1989 Forwards Endorsements 71,72,73,74,75 & 76 to Nelia Policy NF-217 ML20245A1231989-06-0606 June 1989 Submits Whole Body Dose Estimates & Request for Changes to Tech Specs 6.8.3.1 & 6.8.4 ML20248C2861989-06-0101 June 1989 Responds to Generic Ltr 89-08, Erosion/Corrosion-Induced Pipe Wall Thinning. Generic Ltr Does Not Apply to Plant Since No Sys Operate as High Energy Sys ML20247B3121989-05-0808 May 1989 Responds to NRC Re Conduct of Backfit Process, Informing NRC of Plant Permanent Shutdown in Apr 1987 ML20248F1421989-04-0707 April 1989 Forwards Annual Financial Rept & Certified Financial Statements for 1987 & 1988.W/o Annual Financial Rept ML20246N8041989-03-17017 March 1989 Submits Info Re on-site Property Damage Insurance for License DPR-45 for Period 880919 - 890919 ML20204G9191988-10-13013 October 1988 Requests Immediate Relief from Several Sampling & Analysis Requirements of Radiological Environ Monitoring Program to Check for Prescence of I-131.Tech Spec Changes Encl ML20155A3101988-09-30030 September 1988 Responds to NRC 880707 Request for Addl Info Re Decommissioning Plan.Info Includes Flooding Potential & Protection Requirements,Flood Conditions & Effects of High Water Level on Structures ML20154L3511988-09-0909 September 1988 Forwards Answers to Request for Addl Info Re Decommissioning Plan & Safe Storage Tech Specs.Some Answers Suggest Changes to Either Tech Specs or Decommissioning Plan ML20154J3411988-09-0808 September 1988 Forwards Revs to Security,Training & Qualification & Contingency Plans.Revs Withheld (Ref 10CFR2.790(d)) ML20154E4671988-08-30030 August 1988 Responds to Generic Ltr 88-13, Operator Licensing Exams. NRC Will Require Qualified Individuals to Be in Charge of Control Room & Fuel Handling Operations ML20207D1801988-08-0303 August 1988 Advises That Generic Ltr 88-11 Re Radiation Embrittlement of Reactor Vessel Matls Inapplicable to Facility.Reactor Vessel Will Not Be Subj to Pressurization in Plant Safstor Condition 1999-07-09
[Table view] Category:UTILITY TO NRC
MONTHYEARML20055H6371990-07-25025 July 1990 Forwards Decommissioning Fund Rept for Plant ML18041A2111989-11-16016 November 1989 Responds to Generic Ltr 89-19 Re Request for Action Re Resolution of USI A-47, Safety Implication of Control Sys in LWR Nuclear Power Plants. Actions or Recommendations in Generic Ltr Will Not Be Performed ML20248C5941989-09-21021 September 1989 Forwards Revised Radioactive Effluent Rept for LACBWR (Jan- June 1989), Incorporating Sr-89/90 & Fe-55 Analysis Data ML20247A1931989-08-22022 August 1989 Forwards Proposed Operator Licensing Exam Schedule Format for FY90 - FY93,in Response to Generic Ltr 89-12 ML20245G0911989-07-27027 July 1989 Advises That Util Already Exempt from 10CFR26, Fitness-for- Duty Program Because of Safstor Status.Request for Exemption Will Not Be Necessary Since License Amended to possession-only License Via Amend 63 ML20246K8411989-07-10010 July 1989 Responds to Generic Ltr 89-06, Task Action Plan Item I.D.2, Spds. All Spent Fuel Transferred from Reactor to Spent Fuel Storage Well & on 870804,License DPR-45 Amended to possess- but-do-not-operate Status ML20246B8371989-06-27027 June 1989 Forwards Endorsements 71,72,73,74,75 & 76 to Nelia Policy NF-217 ML20245A1231989-06-0606 June 1989 Submits Whole Body Dose Estimates & Request for Changes to Tech Specs 6.8.3.1 & 6.8.4 ML20248C2861989-06-0101 June 1989 Responds to Generic Ltr 89-08, Erosion/Corrosion-Induced Pipe Wall Thinning. Generic Ltr Does Not Apply to Plant Since No Sys Operate as High Energy Sys ML20247B3121989-05-0808 May 1989 Responds to NRC Re Conduct of Backfit Process, Informing NRC of Plant Permanent Shutdown in Apr 1987 ML20248F1421989-04-0707 April 1989 Forwards Annual Financial Rept & Certified Financial Statements for 1987 & 1988.W/o Annual Financial Rept ML20246N8041989-03-17017 March 1989 Submits Info Re on-site Property Damage Insurance for License DPR-45 for Period 880919 - 890919 ML20204G9191988-10-13013 October 1988 Requests Immediate Relief from Several Sampling & Analysis Requirements of Radiological Environ Monitoring Program to Check for Prescence of I-131.Tech Spec Changes Encl ML20155A3101988-09-30030 September 1988 Responds to NRC 880707 Request for Addl Info Re Decommissioning Plan.Info Includes Flooding Potential & Protection Requirements,Flood Conditions & Effects of High Water Level on Structures ML20154L3511988-09-0909 September 1988 Forwards Answers to Request for Addl Info Re Decommissioning Plan & Safe Storage Tech Specs.Some Answers Suggest Changes to Either Tech Specs or Decommissioning Plan ML20154J3411988-09-0808 September 1988 Forwards Revs to Security,Training & Qualification & Contingency Plans.Revs Withheld (Ref 10CFR2.790(d)) ML20154E4671988-08-30030 August 1988 Responds to Generic Ltr 88-13, Operator Licensing Exams. NRC Will Require Qualified Individuals to Be in Charge of Control Room & Fuel Handling Operations ML20207D1801988-08-0303 August 1988 Advises That Generic Ltr 88-11 Re Radiation Embrittlement of Reactor Vessel Matls Inapplicable to Facility.Reactor Vessel Will Not Be Subj to Pressurization in Plant Safstor Condition ML20151Q5001988-07-29029 July 1988 Responds to NRC Bulletin 88-008, Thermal Stresses in Piping Connected to Rcs ML20151E8791988-07-18018 July 1988 Requests Revised Submittal of Deadline of 881001 to Facilitate Review of Questions Re Decommissioning Plan. Partial Submittal Will Be Made as Soon as Possible ML20151D4161988-07-15015 July 1988 Responds to NRC Bulletin 87-002,Suppls 1 & 2, Fastener Testing to Determine Conformance W/Applicable Matl Specs. Fastener Purchases Will Be Monitored Through Procurement Control & Receipt Insp Processes ML20196J2371988-06-22022 June 1988 Responds to NRC Re Violations Noted in Insp Rept 50-409/88-06.Semiannual Whole Body Counts Required by Procedure But Not by Regulation ML20196J1391988-06-22022 June 1988 Responds to NRC Bulletin 88-005 & Suppl 1 to Bulletin Re Nonconforming Matls Supplied by Piping Suppliers,Inc.Review of Procurement Documents Indicated That No Procurement Made W/Piping Suppliers,Inc ML20155E3431988-06-0606 June 1988 Responds to NRC Bulletin 88-004, Potential Safety-Related Pump Loss. Demineralized Water Transfer Sys Has Potential for dead-heading of One Pump,But Sys Not safety-related.No Actions Planned in Response to Bulletin ML20154J3291988-05-18018 May 1988 Forwards Change to Rev 10 to Emergency Plan Section 3.8.1, Radiological Protection of Onsite Personnel, Per 880511 Request.Change Describes Conditions for Precautionary Onsite Sheltering & Control Room Ventilation Isolation ML20154F9581988-05-16016 May 1988 Responds to NRC Bulletin 85-003,Suppl 1, Motor-Operated Valve Common Mode Failures During Plant Transients Due to Improper Switch Settings. No Addl safety-related motor- Operated Valves Found ML20154D5871988-05-10010 May 1988 Submits Info Re Level & Sources of Onsite Property Damage Insurance,Per 10CFR50.54(w).Effective Dates of Primary Coverage Are 870919-880919 ML20154P7371988-04-29029 April 1988 Responds to NRC Re Violations Noted in Insp Rept 50-409/88-03.Corrective Actions:Operations Review Committee Meeting Convened to Discuss Implications of Event.Individual Counseled Re Attention to Duty ML20151U0351988-04-28028 April 1988 Forwards Rev 2 to Plant Physical Security,Guard Force Training & Safeguards Contingency Plans.Encls Withheld (Ref 10CFR2.790(d)) ML20151M7871988-04-18018 April 1988 Forwards Annual Financial Rept & Cetified Financial Statements for 1986 & 1987.Annual Rept for 1987 Will Be Forwarded as Soon as Possible ML20151M8251988-04-15015 April 1988 Responds to 880128 & 0219 Requests for Addl Info Re Plant Emergency Plan & Forwards Rev 10 to Plan.Map of LACBWR Site Defining Emergency Planning Zone Will Be Added to Emergency Plan as Figure A-2 on Page A-15 ML20151B2131988-03-28028 March 1988 Forwards Revised Rev 5 to QA Program Description for possession-only Condition.Revised Pages Reflect Recent Organizational Change ML20148H0511988-03-28028 March 1988 Forwards Revs to Amended Security,Guard Force Training & Qualification & Safeguards Contingency Plans Submitted on 870924.Encls Withheld (Ref 10CFR2.790) ML20196H3531988-02-25025 February 1988 Responds to NRC Bulletin 88-001, Defects in Westinghouse Circuit Breakers. No Westinghouse Ds Series Circuit Breakers Installed at Facility ML20149N0351988-02-22022 February 1988 Forwards Revised Pages to 870930 Application for Amend to License DPR-45 ML20149J1261988-02-16016 February 1988 Responds to Generic Ltr 88-02 Re Isap Ii.Participation in Program Would Not Further Interests of Util,Since Facility Permanently Shut Down on 870430 & Defueling Completed on 870611 ML20234C3601987-12-21021 December 1987 Forwards Rev 5 to Facility QA Program Description.Analyses Show That No Postulated Accident Would Result in Release Exceeding 10CFR100 Limits,In Present Plant Condition ML20147A8031987-12-21021 December 1987 Forwards Decommissioning Plan & Suppl to Environ Rept for Facility post-operating License Stage,For Review.Proposed Tech Specs for Safstor Period Will Be Submitted Separately. Fee Paid ML20236X8671987-11-30030 November 1987 Forwards 870929 Application Fee for Review of Emergency Plan Rev,In Response to from Diggs to Taylor ML20236M4541987-11-0505 November 1987 Discusses Review of Surveillance Testing Performed Due to 870430 Plant Shutdown.Performance of Listed Tests No Longer Required by Tech Specs Terminated ML20236J8301987-10-30030 October 1987 Confirms That Util Not Required to Pay Annual Fee for Power Reactor OLs or Seek Renewal of Exemption Reducing Amount of Such Fee,Per Issuance of Amend 56 to License DPR-45 on 870804 ML20236J4471987-10-30030 October 1987 Forwards Application Fee for Amend to License DPR-45, Inadvertently Omitted from ML20235X0991987-10-12012 October 1987 Forwards Payment in Amount of $25,000 in Response to 870224 Notice of Violation & Proposed Imposition of Civil Penalty ML20235R1541987-10-0101 October 1987 Provides Supplemental Info Re Requesting Exemption from Requirements to Conduct Annual Emergency Preparedness Exercise.Util Plans to Conduct Exercise within 180 Days After NRC Approval of 870930 Rev ML20235R0161987-09-29029 September 1987 Forwards Emergency Plan Rev,Reflecting Current Status of LACBWR Facility for NRC Approval.Technical Rept,Justifing Proposed Emergency Planning Zone Boundary,Encl ML20235S3321987-09-29029 September 1987 Informs That La Crosse BWR Permanently Shutdown on 870430. Reactor Defuelling Completed on 870611.Listed Active Licensing Actions No Longer Necessary ML20235H4791987-09-24024 September 1987 Forwards Changes to Physical Security,Security Guard Force Training & Qualification & Safeguards Contingency Plans.Fee Paid.Changes Withheld (Ref 10CFR73.21) ML20234E3641987-09-0909 September 1987 Submits Response to IE Bulletin 87-001, Thinning of Pipe Walls in Nuclear Power Plants, Dtd 870709.Formal Insp Program Not Necessary for Continued Safe Fuel Storage at Facility Due to Permanent Termination of Plant Operations ML20238C5201987-09-0202 September 1987 Forwards Endorsements 68 & 69 to Nelia Policy NF-217 ML20238F7371987-09-0101 September 1987 Requests Exemption from 10CFR50,App E Requirement to Conduct Annual Emergency Preparedness Exercise & Requirements to Prepare & Distribute Info Brochure to Residents within 5-mile Epz.Requirements Unnecessary 1990-07-25
[Table view] |
Text
' e +W* . ,-
D DA/RYLAND COOPERAT/VE . p.O box 817 ~ . 2615 EAST AV SOUTH
- LA CROSSE. Wl_SCONSIN 54601 (608) 788 4 000 -
June 3, 1985 In re; ly, please refer to LAC-10934 DPCKET NO. 50-409 Director'of Nuclear Reactor Regualtion Attn: Mr. John Zwolinski-Operating Reactors Branch #5 Division'of Operating Reactors U. ' S. Nuclear Regulatory Commission Washington, DC 20555
SUBJECT:
DAIRYLAND POWER COOPERATIVE LA CROSSE BOILING WATER REACTOR (LACBWR) s PROVISIONAL OPERATING LICENSE NO. DPR-45 GENERIC ITEM B-24, CONTAINMENT PURGING / VENTING DURING NORMAL OPERATIONS
References:
(1) NRC Letter, Crutchfield to Linder, dated April 30, 1985.
(2) DPC Letter, Linder to Crutchfield, LAC-9971 dated June 5, 1984.
(3) DPC Letter, Linder to Eisenhut, LAC-7320 dated January 16, 1981.
(4) NRC Letter, Crutchfield to Linder, dated September 20, 1983.
(5) NRC Letter, Crutchfield to Linder, dated December 12,.1980.
(6) DPC Letter, Linder to Crutchfield, LAC-8335 dated June 9,1982.
(7) DPC Letter, Linder to Crutchfield, LAC-10032 dated July 11, 1984.
(8)~. DPC Letter, Linder to Crutchfield, LAC-8546 dated August ' 31, 1982.
Dear.Mr._Zwolinski:
Reference 1-recommended that further study of the plant unique reasons for venting the LACBWR containment be undertaken to determine which plant modifications or changes in operating practices would be most cost-effective in limiting vent or purge system operation. Reference 2 stated that a study of^ purge / vent operations for safety related reasons would be submitted by July 1, 1985. . The necessity of venting the Containment Building (CB) has been re-examined both from a safety and cost standpoint.
There are 3 main reasons the CB as-is needs to be vented. They are accessibility, pressure reduction and leak detection. All are inter-related.
'WPl.6.8 PER'"A8?M 88888!o,
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Mr. John Zwolinski June 3, 1985 Operating Reactors Branch #5 LAC-10934
' CONTAINMENT BUILDING ACCESSIBILITY Containment Building ' accessibility is important at LACBWR. Instead of the drywell/ Reactor Building combination common to other U. S. BWRs, LACBWR has a Containment Building which contains the reactor, the primary system, and auxiliary systems equipment. The Fuel Element Storage Well and its attendent system are also located in the CB. Pumps, valves, filters and instrumentation in systems ranging from the _High Pressure Core Spray System to the Forced Circulation System are contained in the CB. Control rod drive mechanisms including their accumulators and auxiliary systems are in the CB basement.
The Shutdown Condenser, which can provide primary system pressure relief and decay-heat removal during a loss of power or when the reactor is isolated f rom the main condenser, is located inside Containment. The Shutdown Condenser eliminates the need for the relief valves installed in other plants.
The primary system code safety valves have never lif ted to relieve pressure.
Much of the equipment in the containment needs attention during plant operation.
Currently, the auxiliary operator tours the Containment Building twice a shift. ' Some of the instrument readings the operator takes include:
. Reactor Gauge Glass Control Rod Drive Gas Pressure (29)
Control Rod Drive Effluent Temperature (29)
Forced Circulation Pump Leakoff Flow Purification Resin Bed Differential Pressure (2)
Shield Cooling Filter Differential Pressure Seal Injection Supply to Forced Circulation Pump Filter Differential Pressure Seal Injection Supply to Control Rod Drive Filter Differential Pressure Control Rod Drive Effluent Flow Overhead Storage Tank Level Reactor Cavity Radiation Monitor Flow Hydraulic Valve Accumulator System Pressure Hydraulic Valve Accumulator System Level Purification Filter Differential Pressure Fuel. Element Storage Well Filter Differential Pressure The cost of remoting readings if it-is possible - to rewire the existing containment electrical penetration plates was estimated at $400,000 in 1982.
In _ addition to taking readings, the auxiliary operator changes filters, operates the waste water collection system, checks out abnormal control room indications, and performs many other functions. One of the most important is observation. Through the years operators have observed and isolated small leaks. They have detected incipient fires and taken corrective action prior to the occurrence of major problems. The operators have detected trends in equipment performance and provide excellent loose parts detection capability.
Elimination or reduction of entries into the containment would reduce the safety which was designed into the plant with the provision of an accessible Containment Building.
WPl.6.8 Mr. John Zwolinski June 3, 1985 Operating: Reactors Branch #5 LAC-10934 Other plant personnel routinely enter the CB during operation. Health physics technicians _ take daily samples of teactor coolant and periodic samples from other water systems. Shif t Supervisors make periodic tours. . Fire and safety inspections are conducted . routinely. Corrective and preventive maintenance and troub1 shooting are conducted. -Surveillance tests are performed. Many Technical Specification required tests would not be able to be conducted if the CB was not accessible.
While some of- these activities, like instrument readings, could possibly be remoted, others are more difficult or impossible. A remote primary coolant sampling system would have to be installed for use during normal operation.
No system modification, though, can substitute for frequent inspection tours.
Elimination of a means of detecting'ainor problems can result in an increase in plant transients. Such an action is contrary to the recent emphasis in minimizing' plant transients.
If the CB ventilation system was totally isolated, the activity buildup (assuming steady _ state power operation, with coolant activity and leakage similar to normal operation) would result in personnel stay times, without supplied air breathing apparatus, being limited to approxiantely 3.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> per week, after 1 day without venting; 0.9 hour1.041667e-4 days <br />0.0025 hours <br />1.488095e-5 weeks <br />3.4245e-6 months <br /> per week, after 7 days without venting; and 0.7 hour8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> per week af ter 9 or more days without venting. These limited stay times would not permit adequate maintenance or surveillance of
'the plant. Operations personnel alone average approximately 15-20 manhours per week inside the CB. Limiting venting is not consistent with the goal of maintaining personnel exposure As-Low-As-Reasonably-Achievable.
In addition to radiological problems, lack of ventilation leads to high temperatures and humidity inside the CB.
The -containment building air conditioners were sized to provide adequate heat removal while ventilating the containment during operation. Experience in time periods when ventilation was interrupted indicated forced circulation pump cubicles temperatuares as high as 140*F in February. A 5 hour5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> ventilation period dropped the temperature about 3*F. These temperatures are equal to the maximum for summertime operation with ventilation. The higher temperatures expected without ventilation would limit personnel access and lead to ' degradation of the reactor forced circulation pump motors and other equipment. The cost of substantially upgrading air conditioning capability by 50% is approximately $40,000 for the hardware plus installation, rewiring, etc. (1982 estimate)
Upgrading the air conditioning system would have no affect on the quality of air in an isolated containment. Even af ter isolation periods of a day or two due to maintenance, the air seems stale, humid and foul. Therefore, an influx of fresh air would be necessary prior to containment entries if the ventilation dampers were maintained closed.
Not only during normal operation is containment access important. At LACBWR, a rerote shutdown is conducted from inside the CB. Access is thus needed at all - times. 'In case of a fire outside containment, there would not be time to purge the Containment Building prior to entry, even if there was power available to open the CB dampers. In order to meet the applicable portions of WPl.6.8 Mr. John Zwolinski June 3, 1985 Operating Reactors Branch #5 LAC-10934 10 CFR 50 Appendix R, access to the CB must be available at all times.
PRIMARY SYSTEM LEAKAGE DETECTION in addition ~ to eliminating the possibility that a leak would be detected by visual observation, cessation of venting would adversely affect the installed primary system leakage detection systems.
l .The most sensitive system is the reactor cavity leak detection system. The
-reactor lower cavity contains most of the reactor vessel and associated piping. The primary system leak detection sensitivity is based on a measured
- air sweep through the cavity being routed past a monitor. This air is supplied by the plant control air system external to containment.
The reactor cavity leak detection system was installed in March 1969, following the Atomic Energy Commission review of LACBWR's primary leak
. ~ detection capabilities. The system was first described in an Addendum to
' Amendment No. 3 to the Application for Transfer of Provisional Operating Authorization DPRA-6 for LACBWR, dated March 17, 1970. Its usage in detecting 'a small primary leak of less than 2 al/hr was described in Technical
' Report DPC-851-21, "LACBWR Primary Piping and Reactor Vessel Leak Detection System Performance," February, 1971. This system is necessary to meet the requirements of SEP Topic V-5, " Reactor Coolant Pressure Boundary Leakage Detection."
If_the containment building cannot continue venting, air can no longer be introduced into the reactor cavity, since it would pressurize the building.
The sensitivity of the detection system is directly proportional to the air
- flow past the monitor. Therefore, decreasing the air flow would increase the size leak which could be detected. If air is not introduced into the cavity, the area will no longer be pressurized with respect to the remainder of the building. Therefore, leakage into the cavity from other sources, such as the retention tanks, would occur, which would increase the activity the monitor is detecting and mask small leaks. Discontinuation of the air sweep would also decrease the likelihood of the activity generated by a small leak and increase the time for activity , released by any leak to reach the monitor to be detected.
> In addition to the decrease in detection sensitivity resulting from discontinuation of the cavity air sweep, not venting the containment building
- would result in increased background activity, which would further limit the ability to detect small primary leaks.
The increase in background activity would also affect the forced circulation pump (FCP) cubicle monitor leak detection system, limiting its ability to detect leaks. - Another method of leak detection which would be adversely affected ~ i;s the humidity monitoring system. As the humidity in the building increases due to lack of ventilation, the use of dewcells to detect increased leakage would lack sensitivity. Even the indicated accumulation in the
! Retention Tanks is affected by CB venting. The indicated tank level is t affected by building pressure. Therefore, increasing pressure or changes in l pressure as venting is initiated and terminated affect 'the indicated tank level and hence the leakage calculation based on Retention Tank accumulation.
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Mr. John Zwolinski June 3, 1985 Operating Reactors Branch #5 LAC-10934 CONTAINMENT BUILDING PRESSURIZATION When the Containment Building is isolated, building pressure starts increasing. Containment pressures as high as 4-4.5 psig have been observed in the past while the ventilation dampers were closed. The Containment Building high pressure actuation setpoint is set at i 5 psig. Refer to Reference 3 for a discussion of the setpoint. Receipt of a high CB pressure signal starts High Pressure Core Spray Pumps, Alternate Core Spray Pumps, and isolates non-essential CB penetrations to name the most important ef fects. This would result in a design basis cold water injection transient. Therefore, operation at or near the setpoint is not acceptable.
Two of the main sources of air which serve to pressurize the Containment Building when isolated are the reactor cavity leck detection system, discussed earlier, and the air operated valves controllers. The reactor cavity leak detection system employs an approximately 15 SCFM air sweep. The 15 SCFM amounts to 22,000 f t 3/ day and 150,000 ft /3 week. The containment free air volume is approximately 264,000 ft 3.
As discussed earlier, considerably more equipment is located in the LACBWR containment than at other plants. These systems contain numerous valves, many of which are air operated. Some of the air operated valves can be modulated, while others are strictly open/close valves. For example, the Shutdown Condenser inlet valves can be modulated, while the ventilation dampers are either full open or full closed.
The I/P converters associated with all the modulated valves have a constant air bleed during normal operation. The bleed rate typically ranges from 0.75-1.25 SCFM depending on the type of relay installed. A bleed rate of 1 SCFM corresponds to about 10,000 f t /3 week / valve. Also, as the valve position is changed, air is bled of f from the operator, depending on whether the valve opens or closes on application of air pressure.
The air operated open/close valve controllers also bleed of f air to the containment as the valve is either opened or closed. Any minor leakage in the air supply system of any valve also serves to increase the containment air mass.
The level control chambers located inside the Containment Building supply a steady bleed of air into the containment atmosphere. Two of these control chambers are used to control the Shutdown Condenser secondary side water level. Bubbler systems are used to measure level in the Overhead Storage Tank (the source of water for HPCS) and the Retention Tanks. These bubblers involve constant air flow.
As can be seen from this discussion, extensive modification would be necessary to eliminate or greatly reduce the air influx into containment during normal operation. Not only would there be a significant cost, there would be an adverse impact on safety and not only from the entensive modification work involved.
Air operated valves have the great advantage over other types of valves in WPl.6.8 _
Mr. John Zwolinski June 3, 1985 Operating Reactors Branch #5 LAC-10934 that they can be installed to fail safe on loss of air. Therefore, during a loss of power event or during a postulated hot short event, air can be shut of f to the containment, (if a loss of air hasn't occurred) and valves fail to their position for achieving safe shutdown and cooldown. This fail-safe feature combined with the modulating ability of air operated valves makes them superior to other types of ' valves, such as motor operated valves, for most non-manual valve uses. Therefore, replacement of the air operated valves would adversely affect safety in addition to being expensive.
The plant does not have an established history of operating with the ventilation dampers and vent header valve isolated. Therefore, it is not known how f ast CB pressure would increase without ventilation. Generally, in the past when the ventilation dampers were closed for any significant amount r of time, the vent header has been used, though it could not adequately ventilate the building. Rough calculations show that with ventilation totally isolated, containment pressure would reach almost 3 psig af ter only I day, assuming air inflow just due to the cavity monitor leak detection system and 15 modulated valves. An increase of 1 psi per 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> shif t has been noticed in the past when the dampers were closed.
In May 1979, the ventilation dampers opened following a reactor vessel hydrostatic test. Containment building pressure was 3 psig since a pump which vented to containment had been used to assist in pressurizing the reactor vessel. The pressure differential when the dampers opened was sufficient to collapse 10 feet of ductwork. This incident demonstrates that limited periodic venting is not a feasible option on a regular basis. Since after only 1 day without venting the pressure in the CB would be 3 psig, venting once a day would essentially cause a repeat of the 1979 incident.
VENTILATION DAMPERS Many actions have been taken to demonstrate and improve the ventilation dampers operability over the last few years. Dynamic flow testing was performed on a prototype in 1979. Based on the tests, the NRC has stated that the dampers have been found operable and fully qualified in References 4 and
- 5. Additional Technical Specifications were submitted in References 6 and 7 per NRC requests. Debris screens were installed in the ventilation ducts in April 1985 to further eliminate the possibility of debris preventing closure of the dampers. The air conditioners and exhaust fan already restricted debris access to the ventilation dampers.
The Containment Building monitor setpoints were reduced to approximately 5 times background. Activity measured above the setpoint causes automatic closure of the ventilation dampers and vent header internal valve. An analysis was performed and submitted in Reference 8 on the activity which could be released following a LOCA prior to ventilation system isolation.
Re-opening of containment isolation valves following automatic closure now requires manual reset of the closure signal. Especially following these improvements and analyses, there is no reason the ventilation system should not be used during normal operation.
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l Mr. John Zwo11nski June 3, 1985 l Operating Reactors Branch #5 LAC-10934 CONCLUSION Both DPC and the NRC agree the Containment Building ventilation dampers are -
fully ' qualified and operable. DPC has performed studies and taken actions to assure their operability if closure is necessary.
-There are substantial reasons to maintain continuous ventilation. As discussed. . they mainly fall in the areas of containment accessibility, leakage
. detection, and containment pressurization. While modifications are possible to eliminate some of the reasons for venting, a significant number remain which involve safety, significant cost, and/or extreme difficulty.
In evaluating a change which is proposed to improve plant safety, any associated adverse affects on plant safety also have to be examined. DPC's evaluation of the expected adverse affects of not ventilating shows they far exceed the benefit of not having to depend on fully operable ventilation dampers closing during an accident situation. The latter is the only benefit of not continuously venting.
The probability of experiencing a situation requiring containment isolation will be increased if the ventilation system is not used. Venting as discussed earlier improves detection of small leaks. Accessibility is important for locating the source of leakage and isolating it, if possible. De tec ting ,
locating and stopping small leaks prevents small leaks from growing into major problems.
Containment accessibility is important to safety, reliability and good operation from the standpoints of equipment. monitoring, operation, testing and maintenance. _ Accessibility is especially important during a fire or other event requiring remote shutdown from outside the control room.
Replacement of air operated valves with valves of another type would adversely affect plant safety. During any accident situation, air operated valves can be relied upon to either fail safe or be able to be failed safe by securing of the air supply. Elimination of this attribute is not acceptable.
DPC believes these adverse affects of stopping or limiting venting far outweigh any benefit. Partial modifications are not available which would allow venting to be limited without imposing the adverse consequences.
If there are any questions, please contact us.
Sincerely yours, DAIRYLAND POWER COOPERATIVE f $f f
/lFiank Linder, General Manager FL:LSG:sks cc: J. G. Keppler Region III NRC Resident Inspector Richard Dudley, LACBWR Project Manager WPl.6.8