IR 05000458/1990002

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Ack Receipt of Re Violations Noted in Insp Rept 50-458/90-02
ML20062A897
Person / Time
Site: River Bend Entergy icon.png
Issue date: 10/08/1990
From: Collins S
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To: Deddens J
GULF STATES UTILITIES CO.
References
NUDOCS 9010230209
Download: ML20062A897 (2)


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.In Reply Refer To:

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Docket: 50-458/90-02

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Gulf States Utilities j..

ATTN: James C. Deddens SeniorVicePresident(RBNG)

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P.O. Box 220

St. Francisv111e, Louisiana 70775 Gentlemen:

Thank you for your letter of September 18, 1990,. which provided a revised response to our letter and Notice of Violation dated April 6, 1990. We have reviewed your revised schedule for full compliance and find that it remains responsive to the concerns raised in our Notice of-Violation. We will review the implementation of your corrective actions during a future inspection to N

i determine that full compliance has been achieved and will be maintained.,

Sincerely, OdelnalGigned By:

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Thomas P.Gwynn Samuel J. Collins, Director Division of Reactor Projects l

cc:

Gulf States Utilities ATTH:

J. E. Booker, Manager-Nuclear Industry Relations P.O. Box 2951 Beaumont Texas 77704 Bishop. Cook, Purcell & Reynolds

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ATTN: Mark. Wetterhahn, Esq.

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1401 L Street, N.W..

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Washington, D.C.

20005 i-

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Gulf States Utilities

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ATTN: Les England, Director Nuclear Licensing-P.O. Box 220 St. Francisville Louisiana 70775 RIV:RI:PSS C6 C:PS$h D:DR f

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Gulf States Utilities.

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'Mr. J. David McNeill, III

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William G. Davis Esq.

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Department of Justice.

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- Attorney General's-Office P.O.~ Box 94095 i

Baton Rouge, Louisiana-70804-9095-

H. Anne Plettinger

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L Baton Rouge, Louisiana -70806

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President of West Feliciana E

Police Jury

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P.O. Box 1921 St. Francisville,. Louisiana 70775-

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Cajun Electric Power Coop. Inc.

ATTH: Philip G. Harris 10719 Airline Highway P.O. Box 15540 Baton Rouge, Louisiana 70895 Department of Environmental Quality ATTN: William H. Spell, Administrator Radiation Protection Division P.O.. Box 14690 Baton Rouge, Louisiana. 70898 U.S. Nuclear Regulatory Commission ATTN: Resident Inspector

'P.O. Box 1051 St. Francisville, Louisiana 70775'

U.S~ Nuclear Regulatory Commission

ATTN: Regional Administrator, Region IV 611 Ryan Plaza Drive, Suite 1000 Arlington, Texas 76011

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bec distrib by RIV:-

R. D. Martin Resident Inspector

DRP; Section Chief (DRP/C)

Lisa Shea, RM/ALF Mls System l

DRSS-FRPS RSTS Operator-ProjectEngineer(DRP/C)

RIV File

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L DRS Senior Resident Inspector, Cooper l

Senior Resident. Inspector, Fort Calhoun T. Stetta C. Johnson

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auzr svares urzzzrres coaerawr Alvth 0END 5t Att0N 0-0$f Of 8lCf DDR 220 St fitANCisvtLLt L0utslANA ?O776 ARE A CODI 604 C35 6364 346 4661

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September 18, 1990

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RBG 33596 File Nos. G9.5, G15.4.1 SEP 211990

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U. S. Nuclear Regulatory Commission

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Document Control Desk Washington, D.C.

20555 Gentlemen:

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River Bend Station - Unit 1 Refer to: Region IV Docket No. 50-458/90-02 Pursuant -to 10CFR2.201, this letter revises Gulf States Utilities Company's (G$U) response dated May 7,

1990 to the Notice of Violation for NRC Inspection Report No. 50-458/90-02.

The inspection was conducted by Messrs.

Johnson, Singh and Murphy during the period of January 22 26, 1990 of

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activities authorized by NRC Operating License NPF-47 for River Bend Station-Unit 1(RBS).

This letter is being submitted at this time pursuant to a conversation with Mr. L. Constable today.

Revisions to the original response-are denoted in the attachment by change bars in the margin.

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Should you have any questions, please contact Mr.

L.

A.

England at (504)381-4145.

Sincerely, f

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W.

. Odell Manager-Oversight River Bend Nuclear Grcup Attachment cc:

'U. S. Nuclear Regulatory Comiss16n

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Region IV j

611 Ryan Plaza Drive Suite 1000

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Arlington TX 76011 i

Senior Resident Inspector Post Office Box 1051 St. Francisville LA 70775-9&ieWo//o ?W-

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'i UNITED STATES OF AMERICA

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NUCLEAR REGULA'!ORY COMMISSION STATE OF IDUISIANA

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PARISH OF WEST FELICIANA

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Docket No. 50-458

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In the Matter of

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GULF STATES (ITILITIES COMPANY

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(River Bend Station - Unit 1)

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AFFIDAVIT

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W. H. Odell, being duly sworn, states that he is a Manager

- Oversight for Gulf States Utilities Company; that he is authorized on the part of said company to sign and file with the Nuclear Regulatory Commission the documents attached hereto; and that all such documents are true and correct to the best of his knowledge, information and. belief.

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W.

H. Odell

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Subscribed and sworn to before me, a Notary Public in and for the State and Parish above named, this /8A day of

/M1d-mlHA 1990.

My Commission expires with Life.

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0AllLLOYL 0. ANAAOY Claudia F.

Hurst Notary Public.in and for West Feliciana Parish, Louisiana

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ATTACWENT

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REPLY TO NOTICE OF VIOLATION 50-458/9002-02 (SEVERITY LEVEL III)

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REFERENCES Response to Violation - Letter from J. C. Deddens to U. S. NRC, dated May 7,

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1990.

Notice of Violation - Letter from S. J. Collins to J. C. Deddens, dated April 6, 1990.

Enforcement Conference Summary - Letter from S. J. Collins to J. C.

Deddens, i

dated March 26, 1990.

Notice of Enforcement Conference - Dated March 6,1990.

Inspection Report

Letter from

S.

J.

Collins to J. C. Deddens, dated

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February 26, 1990.

Licensee Event Report No.89-036 - Letter from J. E.

Booker to NRC, dated

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November 16, 1989, Rev. I dated January 31, 1990.

VIOLATION

Operating License NPF-47

Section C.10., states that GSU shall comply with

the requirements of the fire protection program as specified in " Attachment

4."

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Attachment

to

Operating License NPF-47,

" Fire Protection Program

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Requirements," states that GSU shall implement and maintain

in effect all

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provisions of the approved fire protection program as described in the Final

Safety Analysis Report for the facility through Amendment 22 and as approved

in the SER dated May 1984 and Supplement 3 dated August 1985 subject to

Provisions 2 and 3 below (which are not applicable here).

Tables 2 and 5 of GSU design specification 240.201,

" Fire Analysis and

Evaluation Criteria and Evaluation Method Including Results and Conclusions

for 10 CFR 50, Appendix R Fire Hazards Analysis," part of the approved fire

protection program described above,

list motor-operated valves for which

electrical powgr is assumed to be removed during plant operations.

Contrary to the above, from November 1985 to October 1989, GSU did not

implement and maintain in effect all

provisions of the approved fire

protection program in that when River Bend Station was operating during this

period, electrical

power had not been removed from 19 motor-operated valves

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listed in Tables 2 and 5 of design specification 240.201 as having power

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removed during plant operations.

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REASON FOR THE VIOLATION

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Of the nineteen valves assumed in the FHA to have electrical power removed,

four were listed in the Final

Safety Analysis Report (FSAR),

Section

9A.2.1.2, as high/ low pressure interface valves.

These four valves, plus two

additional valves associated with steam condensing mode of residual heat

removal

(RHR), did have power removed during initial startup.

Two of these

valves, IE12*MOVF009 and 1E12*MOVF040, were subsequently reenergized.

VALVE 1E12*MOVF009

Valves 1E12*MOVF009 and IE12*M0VF008 are the containment isolation valves for

the RHR shutdown cooling mode suction line.

This is a high/ low pressure

interface between the recirculation system and the RHR shutdown cooling mode

piping.

The FSAR required one of the pair to have electrical power removed.

Meeting this requirement of the FSAR also met the assumption for power

removal in the FHA.

In Supplement 3 to the Safety Evaluation Report for River Bend Station,

August 1985, and a GSU letter dated August 6, 1985, a commitment was made to

add a keylock switch in the control circuitry of IE12*MOVF008 to " lock out

(block) control of the valve (E12*F008) from both the control

room and the

remote shutdown panel." The switch was to be installed in the motor control

center (MCC) located in the auxiliary building and was not to disable the

valve position indication in the control room or the remote shutdown panels.

Modification request (MR) 85-0956 was initiated and installed in November

1985 to add the keylock switch to the control circuitry for 1E12*MOVF008.

Both valves were then energized.

During the design for the MR, the engineer

perceived concerns with locating the switch in the auxiliary building at the

MCC.

There were no keylock switches available that could be qualified for

the harsh post accident environment in this area. There was also a concern

about operator access to the switch during a post accident environment. Due

to these concerns, the keylock switch was relocated to the remote shutdown

panel in the control building.

In this location, the keylock switch provided

easy operator access yet still prevented inadvertent opening of IE12*MOVF008

during a transfer of control

from the main control room to the remote

shutdown panel.

The design in the MR and the 10CFR50.59 safety evaluation failed to recognize

the concerns associated with fire exposure and subsequent spurious actuation

of both the IE12*MOVF008 and 1E12*MOVF009 velves. With the keylock switch

located in the remote shutdown panel and the manner in which it was installed

in the control, circuitry, a single fire in either the remote shutdown panel

or the main c6ntroT room could cause spurious actuation of both valves. With

the electrical power restored to both valves after the MR, the assumptions in

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the FHA were violated.

An inadequate design analysis for MR 85-0956 is considered to be the root

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cause for violating the assumptions of the FHA as related to 1E12*M0VF009.

Several factors contributed to the inadequate design analysis. An inadequate

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depth of investigation as part of the design development failed to reveal the

FHA assumptions.

A lack of familiarity with the FHA and no formal training

in the requirements of the FHA on the part of individual

system engineers

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contributed to this oversight of the FHA. Coupled with this was a deviation

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from the modification procedure.

The modification procedure required a fire

protection checklist to be completed if fire protection issues were affected.

The fire protection checklist was not prepared, and no review by the design

fire protection engineer was performed.

The lack in depth of documentation

in the methods and assumptions used in the FHA contributed not only in the

initial oversight but also in the delay in discovery of the problem.

The

lack of maturity in the engineering organization during the trans.. ion of

responsibility from the architect / engineer to GSV also contributed to the

oversight.

At the time of installation of the MR,

fire

protection

engineering responsibility was divided among GSV Nuclear Plant Engineering,

GSV Technical Staff, the architect / engineer design office, and the architect /

engineer Site Engineering Group.

VALVE 1E12*M0VF040

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Valves 1E12*MOVF040 and 1E12*M0VF049 are the system interface isolation

valves between the RHR system and the radwaste system.

This is considered a

high/ low pressure interface only during the steam condensing mode of RHR. A

license condition prohibits use of the steam condensing mode of RHR at River

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Bend Station.

Due to this, Engineering Evaluation and Assistance Request

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(EEAR) 87E-0216 was

initiated in May 1987 to evaluate

re-energizing

IE12*MOVF040 since it is not a high/ low pressure interface valve with steam

condensing mode of RHR disabled.

The EEAR was answered in June 1987 with the

required changes to the FSAR and operating procedures to allow energizing the

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valve.

Included in these operational procedure changes was a revision to

A0P-0031,

" Shutdown from Outside the Main Control Room". This revision

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required verification that 1E12*M0VF040 was in the closed position if the 'A'

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division of RHR was in shutdown cooling prior to transfer of control from the

main control room to the remote shutdown room.

Although subsequent reviews for separation showed that this situation was

acceptable, the FHA was not revised at the time to delete the assumption of

removing power on this valve.

It is not clear that the FHA and its

assumptions were considered in the evaluation process.

The oversight

associated with EEAR 87E0216 can be attributed to the same root causes as

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associated with MR 85-0956.

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REMAINING VALVES

The remaining thirteen valves that had not had electrical power removed as

assumed in the FHA remained energized due to oversight during the original

preparation of operational

procedures

in 1985.

This oversight was most

probably caused by a lack of awareness by the developers of the procedures of

the FHA and* its assumptions.

The FSAR listed only those valves that were

required to have power removed due to

high/ low

pressure

interface

considerations.

The valves listed in the FSAR were proceduralized to have

power removed but those that were only contained in the FHA were overlooked.

Valve 1821*MOVF019 is not a high/ low pressure interface valve but does

represent a potential

loss of coolant path.

Valve IB21*M0VF019 is an

isolation valve for the main steam drain lines. A fire in the main control

room could cause spurious actuation of this valve and the other valves in

series with this valve.

This would allow reactor coolant to bypass the main

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steam isolation valves directly to the condenser.

Coupled with the Appendix

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R-required assumed loss of offsite power, the condenser could be pressurized

causing the rupture of the air relief diaphragms on the low pressure turbine.

Although of minor safety significance, this would represent an uncontrolled

discharge to the turbine building atmosphere.

CORRECTIVE ACTIONS WHICH HAVE BEEN TAKEN AND THE RESULTS ACHIEVED

The immediate corrective action that was taken in October 1989 upon discovery

of the problem was to remove the electrical power from valves

IE12*M0VF009

and

1821*MOVF019.

Power was removed from these two valves due to

inaccessible locations in the drywell and main steam tunnel.

A fire wa tch

was

initiated for the other valves along their control circuitry until the

separation required by 10CFR50, Appendix R could be verified.

By November

13, 1989, the review for adequate separation for those valves was completed

verifying that the necessary separation did exist. During that time period,

the requirenent for removal of power from 1E12*MOVF009 and IB21*MOVF019 was

verified since adequate separation did not exist-for these potential loss of

coolant paths. Adequate Appendix R separation does not exist in the main

control

room for either valve and does not exist in the remote shutdown room

for IE12*MOVF009.

The verification of divisional separation for thirteen of

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the valves and removal of power for two of the valves, along with the four

valves which have had power removed since 1985, put the plant in a condition

that was

in compliance with the basis of the FHA for these valves.

MR

90-0003 was issued on January 25, 1990 to revise the FHA to reflect the

current status of the valves in the plant.

As pa rt of the corrective action,

Engineering Analysis performed safety

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assessments of the spurious opening of 1821*MOVF021 and 1E12*M0VF009 due to

fires

in the main control room and the remote shutdown panel.

(Note that

IB21*MOVF019 was open with the downstream valve IB21*H0VF021

closed.

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Therefore,

the safety assessment for containment bypass via 1821*MOVF019

focused on the probability of spurious actuation of 1821*H0VF021 due to fire,

to create an open bypass pathway.) Details of these assessments are provided

in the referenced Licensee Event Report.

The probabilistic risk assessment (PRA) for 1821*MOVF021 indicated that the

probability for a steam release from the condenser was approximately 1.9 E-04

over the time the valve was energized.

The radioactivity releases from this

event

were

determined to remain below 10CFR20 and 10CFR100 limits.

Therefore, the safety significance of this event is low.

The PRA for IE12*M0VF009 examined the likelihood of an interfacing system

LOCA and estimated the core damage frequency (CDF) for this event as 5.8E-08.

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This is a factor of 100 below the total CDF of 5.0E-06 for RBS.

Therefore,

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the safety significance of this event is also low.

Due to the heightened awareness of the FHA and the lack of incorporation of

specific requirements associated with the valves, GSU Quality Assurance

Februa ry

7,

1990 a Safety System Functional

performed from January 1

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Inspection (SSFI) of the FHA as related to the energized valves.

The SSFI

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identified several

recommendations for operator actions from the FHA that

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were not reflected in the plant Prefire Strategies. The SSFI also identified

two instances where the necessary electrical jumpers were not available for

potential fire-induced repairs required for equipment necessary to

achieve

cold shutdown.

The affected Prefire Strategies were revised by March 8, 1990, to add the

reconcendations for operator action from the FHA.

The electrical jumpers and

work packages for the repairs necessary to equipment for cold shutdown were

fabricated and staged by January 26, 1990.

An initial review of the FHA by Design Engineering was completed in January

1990 to verify the consistency of the existing design and operational

procedures. This review was done in conjunction with review of the Prefire

Strategies to ensure all actions or plant conditions assumed in the FHA were

contained in the Prefire Strategies or other plant procedures.

No other

inconsistencies other than those already detailed were identified.

In addition to the actions taken to correct the sp;cific condition with the

valves and FHA, additional progrannatic actions have been taken over the last

few years.

In 1987, responsibility for fire protection engineering was

consolidated in Design Engineering.

This minimized the potential for errors

due to confusion over engineering responsibility.

Procedural compliance has

improved throughout River Bend. The need for procedural compliance has been

emphasized

to

all managers and supervisors.

The Design Engineering

supervisors review and evaluate each QA unsatisfactory finding (unsats) and

Quality Assurance Finding Report assigned to Design Engineering.

The results

of those evaluations are discussed in Design Engineering staff meetings to

determine if trends in unsats are developing and to correct those trends

early.

This has resulted in a significant decrease in the number of unsats

generated against Design Engineering documents.

The modification procedure has been revised to require increased depth of

design bases evaluation and documentation.

This will help preclude an

oversight of the FHA and its requirements in the future.

CORRECTIVE ACTIONS WHICH WILL BE TAKEN TO AVOID FURTHER VIOLATIONS

Although the corrective actions that have been taken to date bring the plant

into a state of full compliance with the operating license, additional

corrective actions are necessary to ensure a similar situation does not occur

in the future.

The corrective actions are separated into three areas:

the

FHA and associated procedures, modification requests, and training.

As stated above, an initial review of the FHA has been performed. A final

review and veH fication of the FHA will

be performed by an independent

contractor.

In addition,

the independent contractor is to provide fully

detailed documentation of the design bases and assumptions of the FHA.

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verification of the consistency between the FHA and plant

procedures will be perfonned by the independent contractor.

This will be

followed by another SSFI performed by GSU Quality Engineering to evaluate

implementation and effectiveness as outlined in the FHA.

To ensure that no additional modification requests with similar oversights

exist, a review of MRs engineered from the time GSU assumed control of the

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design modification process to January 20,

1987 will be perfonned.

This

review will be done to ensure that adequate documentation exists for

potential impact on the FHA.

After January 20, 1987,the fire protection

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checklist was required to be completed for all MRs.

If the review of MRs

engineered prior to that date indicates the problem may extend beyond January

20, 1987, the scope of the review will be increased.

In order to increase the general awareness of the Fire Hazards Analysis and

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its requirements, a training program on the FHA is to be developed.

The

training program will be provided to all engineers who perform modification

requests and safety evaluations.

In addition to the engineers, the members

of the Facility Review Committee and appropriate operations personnel will be

given training on the FHA.

The training for the operations personnel will

include the recommended operator actions that are included in the FHA.

In addition to the corrective actions that are being done to prevent a

recurrence, an investigation is being pursued to allow operations to energize

1821*MOVF019 during startup phases of plant, without continuous opera tor

attendance at the valve's MCC.

This investigation is evaluating the amount

of time that would be required to pressurize the condenser and rupture the

air relief diaphragms with the reactor at various power levels and pressures.

These times will be evaluated to determine at what pressure level or power

level adequate time is available for ensuring isolation of the main steam

drain lines

in the event of a main control

room fire.

Until

the

investigation is completed, this valve will remain under current controls.

DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED

As of Ma rch

8,

1990, with the issuance of the revised Prefire Strategies,

River Bend Station was in compliance with the Fire Protection Program as

required by its operating license.

Further corrective actions will be

accomplished per the following schedule:

The contract has been awarded to NUS Corporation for the FHA review and

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documentation,

the proposed schedule requires the work to be complete by

January 15, 1991.

Review of the MRs will be complete by February 28, 1991.

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The follow-up SSFI to evaluate the implementation and effectiveness of

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revised procedures regarding the FHA will be performed by July 1991.

Implementat, ion of the training program will be complete during the second

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quarter 1991'.

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