ML20247P495

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Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-458/89-28
ML20247P495
Person / Time
Site: River Bend Entergy icon.png
Issue date: 09/19/1989
From: Milhoan J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To: Deddens J
GULF STATES UTILITIES CO.
References
NUDOCS 8909270187
Download: ML20247P495 (2)


See also: IR 05000458/1989028

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T Gulf States Utilities

E ATTN:: :Mr. James C. Deddensi

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Senior Vice President (RBNG)'.

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P.O.' Box 220-

St'.'Francisville.. Louisiana 70775

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, Gentle' men:

'

Thank you'for your letter of. August 25, 1989, in response to our letter;and

. Notice of, Violation dated' July 28, -1989. 'We have reviewed your reply and find

it responsive to the concerns' raised in our Notice of Violation. We will

review the implementation of your corrective actions'during a future inspection

to determine that full ~ compliance has been achieved and will be maintained.

Sincerely,

,

James L.' Milhoan, Director

Division of, Reactor Projects

CC:'

Gulf States Utilities

ATTN:

J. E. Booker, Manager-

'

River Bend Oversight

'P.O. Box 2951

1

Beaumont, Texas 77704

' Gulf States Utilities

ATTN:

Les England, Director

Nuclear Licensing - RBNG

P.O.~ Box 220'

St. Francisv111e, Louisiana 70775

Louisiana' State University,

Government Documents Department

Louisiana Radiation Control Program Director

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GULF STATES

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August 25, 1989

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File Nos. G9.5, G15.4.1

U. S. Nuclear Regulatory Commission

Document Control Desk

Washington, D.C.

20555

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Gentlemen:

River Bend Station - Unit 1

Refer to: Region IV

___ Docket No. 50-458/89-28

Pursuant to 10CFR2.201,

this letter provides Gulf States Utilities

Company's (GSU) response to the Notice of Violation for NRC Inspection

Report No. 50-458/89-28.

The inspection was performed by Messrs. E.

J. Ford and

W.

B.

Jones during the period June

1-30,

1989 of

activities authorized by NRC Operating License NPF-47 for River Bend

Station - Unit 1.

GSU's response to the violation is provided in the

attachment.

GSU's response to this item is complete.

Should you have any questions, please contact Mr. L. A. England at

(504) 381-4145.

Sincerely,

,f. h /h

J. E. Booker

Manager-River Bend Oversight

River Bend Nuclear Group

JEB/LAE/

MSF/RGW/ch

Attachment

cc: U. S. Nuclear Regulatory Commission

Region IV

611 Ryan Plaza Drive, Suite 1000

Arlington, TX 76011

Senior Resident Inspector

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P.O. Box 1051

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St. Francisville, LA 70775

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UNITED' STATES OF AMERICA

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' NUCLEAR REGUIJLTORY COMMISSION

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' STATE OF LOUISIANA

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PARISH OF NEST FELICIANA

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Docket No. 50-458

'In the-Matter of

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GULF. STATES UTILITIES COMPANY

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(River Bend Station - Unit 1)

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AFFIDAVIT

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J.

.E.

Booker,: being ' duly

sworn,

states

that

he

is

Manager-River

Bend

Oversight .for

Gulf

States

Utilities

Company;

that he is authorized on the part of said company to-

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sign'and file 'with

the

Nuclear

Regul' tory

Commission -the

a

documents' attached' hereto;

that

he

has

read

all

of the

statements contained in such documents

attached

thereto

and

made

.a

part

thereof;

and that all such statements made and

matters set forth therein are true and correct to the best

of

~his knowledge, information and belief.

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[. E. Booker

-Subscribed

and sworn to before me, a Notary Public in and

for the State and ' Parish above

named,

this

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My Commission expires with Life.

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Mr

Notary Public in and for

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West Feliciana Parish, Louisia[na

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ATTACMENT

RESPONSE TO NOTICE OF VIOLATION 50-458/8928-01

LEVEL IV

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REFERENCES

Notice of Violation - Letter from J. L. Milhoan to J. C. Deddens, dated Ju".y

28, 1989.

INADEQUATE SYSTEM CONFIGURATION CONTROL

River Bend Station Technical Specifications,. paragraph 6.8.1.a

requires that

procedures for activities identified in Appendix A of Regulatory Guide 1.33,

Revision

2,.

February 1978, be established, implemented, and maintained.

Paragraph 9 of Regulatory Guide 1.33 requires that maintenance activities

that can affect the performance of safety-related equipment be properly

preplanned and performed in accordance with written procedures, documented

instructions, or drawings appropriate to the circumstances.

Contrary to the above, Administrative Procedure ADM-0028, " Maintenance Work

>.

. Order,". Revision 10, was not appropriate in that it did not require the

maintenance work order (MWO) job plan to provide specific restoration steps

if valve manipulations are performed or that the system be restored in

accordance with the applicable procedure. As a result,18 control rod drive

hydraulic control units were not. verified as being properly aligned following

flush and vent activities authorized by MWO R126315. This condition existed

from June 2-17, 1989.

REASON FOR THE VIOLATION

At approximately 3 a.m. on June 17, 1989 during reactor startup following the

second refueling outage, a reactor operator was dispatched to vent a control

rod drive (CRD) at its respective hydraulic control unit (HCU). The reactor

operator arrived at the CRD location and discovered that a CRD cooling water

isolation valve (HCU 4821-V104) was closed. The Station Operating Procedure

(S0P)-0002,

" Control

Rod Drive Hydraulics", requires this valve to be open.

The last time this SOP was performed and completed was on May 22, 1989.

Further investigation revealed subsequent work on the CRDs after the 50P was

performed. MWO R126315 was work released on May 25, 1989 to flush and vent

various- HCUs including HCU 4821-V104.

The job plan step requiring that

operations verify the valve position per the S0P valve line-up sheet, prior

to returning the system to service was deemed not applicable by the planner

and the job plan did not address any other restoration steps.

The MWO was

completed and signed off on June 2,1989 without any other verification as to

the correct valve lineup.

In conclusion, Gulf States Utilities Company (GSU)

determined the root cause was attributed to two causal factors: personnel

error was made in determining the applicability of the job plan step, which

should have required valve lineup after completed work and a specific

restoration step did not exist at the end of the job plan.

Page 1 of 2

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CORRECTIVE ACTIONS WHICH HAVE BEEN TAKEN AND THE RESULTS ACHIEVED

'

Immediately following- the discovery of the mispositioned

valve,

GSU

- management terminated the plant start-up and operations personnel performed

the S0P-0002 valve lineup. The performance of this lineup did not find any

other HCU valves closed or mispositioned. Operation's management personnel

determined the missing lock wires were also a direct result of the work

performed on MWO R126315. The operations department initiated a revision to

SOP-0002 to improve its format and content.

Based on the evaluation, GSU

decided to proceduralize the flushing of CRDs with required individual

sign-offs for each step.

Currently, each valve on the HCU is identified on

the lineup sheet and requires a first and second verification signature.

This revision eliminates the original generic lineup for CRDs by specifically

identifying valve numbers and providing more clarity'to the sign-offs.

7

CORRECTIVE ACTIONS WHICH WILL BE TAKEN TO AVOID FURTHER VIOLATIONS

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ADM-0028,

" Maintenance Work Order", was revised to resolve the deficient e b

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manipulations

1) shall

delineate

plan to specify steps

requiring ) valve

steps or 2 be performed in_accordance with ADM-0027,

specific restoration

" Protective Tagging",

GMP-0042, " Circuit Testing and Lifted Leads and

- Jumpers" or the appropriate S0P valve lineup sheet.

A 100 percent verification of all- safety-related valves was conducted prior

to commencing the subsequent plant start-up.

This verification involved

approximately 11,700 valves and resulted in finding one additional valve

(LSV*PT21A) closed in the positive valve leakage control

system (PVLCS).

- This valve is required to be open per SOP-0041, " Penetration Valve Leakage

Control System". Since the finding was discovered during corrective action

for the CRD valve and the PVLCS system operability was not affected by the

valve being closed, no further corrective action was appropriate.

In

addition, the procedure revisions now in effect for 50P-0002 and ADM-0028

specifically address the root cause for the mispositioned valve.

.

DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED

GSU is currently in full compliance and all

corrective actions have been

completed.

!

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