IR 05000458/2019001

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NRC Integrated Inspection Report 05000458/2019001
ML19130A200
Person / Time
Site: River Bend Entergy icon.png
Issue date: 05/10/2019
From: Jason Kozal
Division of Nuclear Materials Safety IV
To: Vercelli S
Entergy Operations
References
IR 2019001
Download: ML19130A200 (25)


Text

May 10, 2019

SUBJECT:

RIVER BEND STATION - NRC INTEGRATED INSPECTION REPORT 05000458/2019001

Dear Mr. Vercelli:

On March 31, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your River Bend Station. On April 24, 2019, the NRC inspectors discussed the results of this inspection with Mr. Kent Scott, General Manager of Plant Operations, and other members of your staff. The results of this inspection are documented in the enclosed report.

NRC inspectors documented two findings of very low safety significance (Green) in this report.

These findings involved violations of NRC requirements.

If you contest the violations or significance of the violations documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the NRC resident inspector at River Bend Station.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the NRC resident inspector at River Bend Station. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Jason W. Kozal, Chief Reactor Projects Branch C

Docket No. 05000458 License No. NPF-47

Enclosure:

Inspection Report 05000458/2019001

Enclosure U.S. NUCLEAR REGULATORY COMMISSION

Inspection Report

Docket Number(s):

05000458

License Number(s):

NPF-47

Report Number(s):

05000458/2019001

Enterprise Identifier: I-2019-001-0009

Licensee:

Entergy Operations, Inc.

Facility:

River Bend Station

Location:

St. Francisville, LA

Inspection Dates:

January 1, 2019 to March 31, 2019

Inspectors:

L. Merker, Senior Resident Inspector (BWR/TL)

B. Parks, Resident Inspector (BWR)

T. DeBey, Resident Inspector (BWR)

Approved By:

Jason W. Kozal

Chief, Reactor Projects Branch C

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a quarterly inspection at River Bend Station in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. Violations and other additional items being considered in the NRCs assessment are summarized in the table below.

List of Findings and Violations

Failure to Maintain Appropriate Surveillance and Maintenance Procedures for the Division III Emergency Diesel Generator Cornerstone Significance Cross-cutting Aspect Report Section Mitigating Systems Green NCV 05000458/2019001-01 Closed

[H.11] -

Challenge the Unknown 71152 The inspectors identified a Green, non-cited violation of 10 CFR Part 50, Appendix B,

Criterion V, Instructions, Procedures, and Drawings, for the licensees failure to prescribe instructions appropriate to the circumstances, including appropriate quantitative or qualitative acceptance criteria, for an activity affecting quality. Specifically, instructions for surveillance and maintenance work on the turbocharger lubricating oil system of the Division III emergency diesel generator, which is an activity affecting quality, did not specify acceptance criterion for the DC lubricating pump motor continuity check nor did they require a post maintenance demonstration that the motor could run. As a result, the Division III emergency diesel generator was declared inoperable on November 28, 2018.

Inadvertent Initiation of Reactor Core Isolation Cooling due to Personnel Error Cornerstone Significance Cross-cutting Aspect Report Section Initiating Events Green NCV 05000458/2019001-02 Closed

[H.5] - Work Management 71153 The inspectors reviewed a self-revealed, Green, non-cited violation of 10 CFR Part 50,

Appendix B, Criterion V, Instructions, Procedures, and Drawings, for the licensees failure to accomplish an activity affecting quality in accordance with a prescribed procedure.

Specifically, while conducting surveillance testing on the reactor core isolation cooling (RCIC)system, technicians installed an incorrect test fixture and caused an inadvertent injection of RCIC into the reactor vessel.

Additional Tracking Items

Type Issue number Title Inspection Procedure Status LER 05000458/2018-007-00 Manual Reactor Scram due to Reactor Recirculation Pump Trip Caused by Transformer Failure 71153 Closed LER 05000458/2018-008-00 Potential Loss of Safety Function and Unanalyzed Condition due to Legacy Design Deficiency in Control Building HVAC 71153 Closed LER 05000458/2018-009-00 Inadvertent Initiation of Reactor Core Isolation Cooling due to Personnel Error 71153 Closed

PLANT STATUS

River Bend Station began the inspection period at rated thermal power. On January 4, 2019, the unit was down powered to 85 percent to conduct a seal repair on main feedwater pump 1A. The unit was returned to rated thermal power on January 7, 2019. On January 12, 2019, the unit was down powered to 70 percent because of an issue with the inboard main steam isolation valve D solenoid pilot valve. The unit was returned to 75 percent power on January 13, 2019. The unit was shut down on March 30, 2019, to begin refueling outage RF-20 and remained shut down for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515, Appendix D, Plant Status, and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

External Flooding Sample (IP Section 03.04) (1 Sample)

The inspectors evaluated the site's readiness to cope with external flooding for the following areas:

  • Control building on January 23, 2019

71111.04 - Equipment Alignment

Partial Walkdown (IP Section 02.01) (3 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Division II 125 VDC system on January 17, 2019
(2) Low pressure core spray system on March 7, 2019
(3) Division I 125 VDC system on March 19, 2019

71111.04S - Equipment Alignment

Complete Walkdown (IP Section 02.02) (1 Sample)

The inspectors evaluated system configurations during a complete walkdown of the high pressure core spray system on January 30, 2019.

71111.05A - Fire Protection (Annual)

Annual Inspection (IP Section 03.02) (1 Sample)

The inspectors evaluated fire brigade performance on January 30, 2019.

71111.05Q - Fire Protection

Quarterly Inspection (IP Section 03.01) (4 Samples)

The inspectors evaluated fire protection program implementation in the following selected areas:

(1) High pressure core spray room, fire areas AB-2/Z-1 and AB-2/Z-2, on January 30, 2019
(2) Standby liquid control area, fire area RC-4/Z-4, on January 31, 2019
(3) Division I, II, and III battery rooms, fire areas C-18, C-19, and C-21, on February 1, 2019
(4) Low pressure core spray pump room, fire area AB-6/Z-1, on March 7, 2019

71111.06 - Flood Protection Measures

Inspection Activities - Internal Flooding (IP Section 02.02a.) (1 Sample)

The inspectors evaluated internal flooding mitigation protections in the:

Inspection Activities - Underground Cables (IP Section 02.02c.) (1 Sample)

The inspectors evaluated cable submergence protection in:

  • Electrical manhole EMH2A on March 14, 2019
  • Electrical manhole EMH103 on March 14, 2019

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

The inspectors observed and evaluated licensed operator performance in the main control room during a reactor power maneuver on January 4, 2019.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

The inspectors observed and evaluated licensed operator requalification training in the simulator on February 12, 2019.

71111.12 - Maintenance Effectiveness

Routine Maintenance Effectiveness Inspection (IP Section 02.01) (3 Samples)

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:

(1) Functional failure review of the high pressure core spray system on March 6, 2019
(2) Functional failure review of containment unit cooler 1A on March 21, 2019
(3) Functional failure review of the Division I emergency diesel generator on March 25, 2019

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the risk assessments for the following planned and emergent work activities:

(1) Yellow risk during surveillance testing of low pressure coolant injection pump A on January 8, 2019
(2) Yellow risk during surveillance testing of reactor core isolation cooling system on January 15, 2019
(3) Yellow risk during inspection of Division I standby service water system on February 8, 2019
(4) Yellow risk during inspection of Division II standby service water system on February 21, 2019

71111.15 - Operability Determinations and Functionality Assessments

Sample Selection (IP Section 02.01) (5 Samples)

The inspectors evaluated the following operability determinations and functionality assessments:

(1) Division I control building air conditioning system after failure of air handling unit 2A to close electrically in the test position on March 4, 2019
(2) Division I residual heat removal heat exchangers following thermal performance testing on March 11, 2019
(3) Containment unit cooler 1A low air flow conditions on March 14, 2019
(4) Division II hydrogen igniters surveillance testing results on March 21, 2019
(5) Division II main steam positive leakage control system after failure of trip unit card on March 25, 2019

71111.19 - Post Maintenance Testing

Post Maintenance Test Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the following post maintenance tests:

(1) Work Order 00514462, SVV-MOV1B Major Actuator Inspection / Div 2, following actuator inspection of main steam line pressure relief isolation valve SVV-MOV1B on February 20, 2019
(2) Work Order 00514461, SWP-MOV503B Major Actuator Inspection / HVR-UC1B, following actuator inspection of containment unit cooler 1B return header inboard containment isolation valve SWP-MOV503B on February 20, 2019
(3) Work Order 52829384, IAS-C2A - Perform 4,000 Hr Inspection, following 4,000 hour0 days <br />0 hours <br />0 weeks <br />0 months <br /> preventive maintenance of instrument air compressor 2A on February 22, 2019
(4) STP-403-0301, Revision 15, Containment Unit Cooler HVR-UC1A Flow Rate Verification, following cooling coil cleaning due to low air flow conditions on March 14, 2019
(5) STP-251-3205, Revision 16, Diesel Fire Pump Operational Test, following system maintenance on fire pump engine 1B on March 18, 2019

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

In Service Testing (IST) (IP Section 03.01)

(1) STP-201-6310, Revision 311, SLC Pump and Valve Operability Test, on January 31, 2019
(2) STP-205-6301, Revision 25, LPCS Pump and Valve Operability Test, on March 7, 2019

Surveillance Testing (IP Section 03.01) (4 Samples)

(1) STP-309-0201, Revision 062, Division I Diesel Generator Operability Test, on January 7, 2019
(2) STP-256-0201, Revision 304, Div I SWP Valve Lineup Verification, on January 10, 2019
(3) STP-051-4504, Revision 301, NSSSS-Reactor Vessel Water Level-Low Low, Level 2; Low Low Low, Level 1, Channel Functional Test (B21-N682D, B21-N681D),on January 23, 2019
(4) STP-203-0201, Revision 308, HPCS Piping Water Fill and Valve Position Verification, on January 29, 2019

71114.06 - Drill Evaluation

Drill and/or Simulator-Based Licensed Operator Requalification Training (IP Section 02.01) (1 Sample)

The inspectors evaluated an emergency preparedness training drill on March 12,

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01)===

(01/01/2018-12/31/2018)

IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 02.02) (1 Sample)

(01/01/2018-12/31/2018)

IE04: Unplanned Scrams with Complications (USwC) Sample (IP Section 02.03) (1 Sample)

(01/01/2018-12/31/2018)

71152 - Problem Identification and Resolution

Annual Follow-up of Selected Issues (IP Section 02.03) (1 Sample)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issue:

71153 - Follow-up of Events and Notices of Enforcement Discretion Event Report (IP Section 03.02)

The inspectors evaluated the following licensee event reports (LERs) which can be accessed at https://lersearch.inl.gov/LERSearchCriteria.aspx:

(1) LER 05000458/2018-007-00, Manual Reactor Scram due to Reactor Recirculation Pump Trip Caused by Transformer Failure on February 1, 2018 (ADAMS Accession: ML18304A436):

The inspectors reviewed this LER and closed it to non-cited violation 05000458/2018012-04 issued in Inspection Report 05000458/2018012 (ADAMS Accession: ML18261A111).

(2) LER 05000458/2018-008-00, Potential Loss of Safety Function and Unanalyzed Condition due to Legacy Design Deficiency in Control Building HVAC on September 25, 2018 (ADAMS Accession: ML18324A744):

The inspectors reviewed this LER and closed it to the licensee-identified violation issued in Inspection Report 05000458/2018003 (ADAMS Accession: ML18313A028).

(3) LER 05000458/2018-009-00, Inadvertent Initiation of Reactor Core Isolation Cooling due to Personnel Error on November 2, 2018 (ADAMS Accession: ML19003A143):

The circumstances surrounding this LER are documented in the Inspection Results section.

INSPECTION RESULTS

Failure to Maintain Appropriate Surveillance and Maintenance Procedures for the Division III Emergency Diesel Generator Cornerstone Significance Cross-cutting Aspect Report Section Mitigating Systems

Green NCV 05000458/2019001-01 Closed

[H.11] -

Challenge the Unknown 71152 The inspectors identified a Green, non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, for the licensees failure to prescribe instructions appropriate to the circumstances, including appropriate quantitative or qualitative acceptance criteria, for an activity affecting quality. Specifically, instructions for surveillance and maintenance work on the turbocharger lubricating oil system of the Division III emergency diesel generator, which is an activity affecting quality, did not specify acceptance criterion for the DC lubricating pump motor continuity check nor did they require a post maintenance demonstration that the motor could run. As a result, the Division III emergency diesel generator was declared inoperable on November 28, 2018.

Description:

On November 28, 2018, operators in the River Bend Station (RBS) main control room received an alarm, Div III D/G System Trouble, for the Division III high pressure core spray (HPCS) emergency diesel generator. Investigation into the cause of the alarm revealed that both turbocharger lubricating oil pumps had failed, rendering the diesel generator inoperable. The inoperability lasted for about 8.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> while the oil pumps were repaired. Operability of the HPCS system during a loss of offsite power requires operability of its dedicated diesel generator. Since offsite power was available on November 28, 2018, the HPCS system remained operable. The HPCS diesel generator is one of three emergency diesel generators that are required to be operable by RBS Technical Specification 3.8.1. Per RBS Procedure SOP-0052, HPCS Diesel Generator (Sys #309), Revision 58, for Division III (HPCS) diesel generator operation, no planned starts of the engine should be performed without a turbocharger lubricating oil pump operating. The procedure also stated that if both (AC and DC-powered) turbocharger lubricating pumps are out of service, the diesel engine is not available for operation. Lubrication of the diesel engine turbocharger is supplied by an engine-driven pump while the engine is running and an AC electric pump when the engine is stopped. If the AC pump would stop while the engine is not running, a DC electric pump is designed to start so that lubricating oil flow to the turbocharger is maintained. The turbocharger lubrication system has two primary functions:

(1) lubrication of the turbocharger bearings and
(2) cooling of the turbocharger.

Condition Report CR-RBS-2018-06363 documented the loss of turbocharger lubricating oil flow to the HPCS diesel generator that resulted in its inoperability on November 28, 2018.

Troubleshooting by station personnel revealed that one of the two brushes on the DC lubricating pump motor was mispositioned, causing the motor to fail. Questioning from the inspectors revealed that the stations surveillance and maintenance of the DC motor was done on a biennial basis and was not appropriate to detect the mispositioned brush or to verify the ability of the motor to run after the electrical surveillance. Additionally, the licensees work order instructions were not appropriate and did not contain appropriate quantitative or qualitative acceptance criteria. Further inspector questioning revealed that the same instruction inadequacies also existed for the HPCS emergency diesel generator DC motor for the associated circulating oil lubrication system. It is likely that the DC motor was not able to operate from September 18, 2017 (the most recent inspection and preventive maintenance date), until November 28, 2018.

Corrective Actions: The licensee removed the DC motor from the diesel engine, reinstalled the mispositioned brush, returned the motor to the diesel engine, and performed a successful post maintenance test. Other corrective actions that the licensee is considering include performing monthly (vs. biennial) functional testing of the DC oil pump, requiring removal of the DC motor in order to do the brush inspections, improving the DC motor inspection process, sharing the lessons learned from this event, and revising the procedural requirement for declaring the diesel engine inoperable when the turbocharger lubricating oil flow is lost.

Corrective Action Reference: CR-RBS-2018-06363

Performance Assessment:

Performance Deficiency: The failure to prescribe instructions appropriate to the circumstances, including appropriate quantitative or qualitative acceptance criteria, for surveillance and maintenance of the turbocharger lubricating oil system of the Division III (HPCS) emergency diesel generator, resulting in inoperability of the diesel generator, was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor, and therefore a finding, because it was associated with the equipment performance attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, instructions for surveillance and maintenance work on the turbocharger lubricating oil system of the Division III emergency diesel generator, which is an activity affecting quality, did not specify acceptance criterion for the DC lubricating pump motor continuity check nor did they require a post maintenance demonstration that the motor could run. As a result, the Division III emergency diesel generator was declared inoperable on November 28, 2018.

Significance: The inspectors assessed the significance of the finding using NRC Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, Exhibit 2, Mitigating Systems Screening Questions, dated July 1, 2012.

The finding was determined to be of very low safety significance (Green) because it did not represent a deficiency affecting the design or qualification of a mitigating structure, system, or component; did not represent a loss of system and/or function; did not represent an actual loss of function of at least a single train for more than its technical specification allowed outage time or two separate safety systems out-of-service for more than its technical specification allowed outage time; and did not represent an actual loss of function of one or more non-technical specification trains of equipment designated as high safety-significant in accordance with the licensees maintenance rule program for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

Cross-cutting Aspect: The finding had a cross-cutting aspect in the area of human performance, challenge the unknown, because the licensee did not stop when faced with uncertain conditions, and risks were not evaluated and managed before proceeding. Specifically, the licensee did not question the lack of acceptance criterion for the DC lubricating pump motor continuity check or post maintenance demonstration that the motor could run [H.11].

Enforcement:

Violation: Title 10 of the Code of Federal Regulations, Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, requires, in part, that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings of a type appropriate to the circumstances. The instructions, procedures, or drawings shall include appropriate quantitative or qualitative acceptance criteria for determining that important activities have been satisfactorily accomplished.

Contrary to the above, on September 18, 2017, the surveillance and maintenance procedure for the turbocharger lubricating oil system of the Division III emergency diesel generator, which is an activity affecting quality, was not appropriate to the circumstances because it did not include appropriate quantitative or qualitative acceptance criteria for determining that important activities have been satisfactorily accomplished. Specifically, instructions for surveillance and maintenance work on the turbocharger lubricating oil system of the Division III emergency diesel generator, which is an activity affecting quality, did not specify acceptance criterion for the DC lubricating pump motor continuity check nor did they require a post maintenance demonstration that the motor could run. As a result, the Division III emergency diesel generator was declared inoperable on November 28, 2018.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Inadvertent Initiation of Reactor Core Isolation Cooling due to Personnel Error Cornerstone Significance Cross-cutting Aspect Report Section Initiating Events

Green NCV 05000458/2019001-02 Closed

[H.5] - Work Management 71153 The inspectors reviewed a self-revealed, Green, non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, for the licensees failure to accomplish an activity affecting quality in accordance with a prescribed procedure.

Specifically, while conducting surveillance testing on the reactor core isolation cooling (RCIC)system, technicians installed an incorrect test fixture and caused an inadvertent injection of RCIC into the reactor vessel.

Description:

At 3:53 a.m. on November 2, 2018, during performance of surveillance Procedure STP-051-4524, ECCS/RCIC-Reactor Vessel Water Level-Low Low, Level 2; Low Low Low, Level 1; Channel Functional Test (B21-N692E, B21-N691E), Revision 5, RCIC initiated and began injecting water into the reactor vessel. After verifying that the initiation was inadvertent, operators tripped the RCIC turbine in accordance with Procedure AOP-0034, Inadvertent Initiation of an ECCS System or RCIC, Revision 2, and declared RCIC inoperable. Operators subsequently restored RCIC to a normal standby lineup and returned the system to operable status.

Subsequent investigation determined that technicians caused the initiation by installing an incorrect test fixture into the system. Procedure STP-051-4524, Step 7.1.9, instructed technicians to connect a red A/B contact test fixture and Simpson Multimeter to test jack E51A-J1, RCIC LOGIC A TEST. Instead of installing that contact test fixture, technicians installed a green B/C contact test fixture. The installation of the green B/C contact test fixture into jack E51A-J1 satisfied the coincidence logic for RCIC initiation, causing the inadvertent injection into the core.

The licensee conducted a review of the event and identified multiple deficiencies in the area of work management. In an attempt to recover lost time in the work schedule, the nightshift supervisor directed the technicians to perform an unusually high number of surveillance items in one shift. The supervisor assigned the items at the beginning of the shift and proceeded to focus on other plant issues for the remainder of the night, failing to sufficiently engage with and oversee the risk-significant testing that was being carried out. The technicians failed to fill out the required pre-job brief checklist and the peer reviewing technician failed to conduct an adequate peer check prior to the critical step.

Corrective Actions: The licensee restored RCIC to operable status after the event and issued corrective actions to augment supervisory oversight of pre-job briefs and testing evolutions.

Corrective Action Reference: CR-RBS-2018-05854

Performance Assessment:

Performance Deficiency: The failure to accomplish an activity affecting quality in accordance with a prescribed procedure was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor, and therefore a finding, because it was associated with the human performance attribute of the Initiating Events Cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, by failing to properly complete the steps of the surveillance test procedure, the licensee caused an inadvertent RCIC injection into the reactor vessel.

Significance: The inspectors assessed the significance of the finding using NRC Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, Exhibit 1, Initiating Events Screening Questions, dated June 19, 2012. The inspectors determined that the finding was of very low safety significance (Green) because the finding did not cause a reactor trip and the loss of mitigation equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition.

Cross-cutting Aspect: The finding had a cross-cutting aspect in the area of human performance, work management, because the licensee failed to implement a process of planning, controlling, and executing work activities such that nuclear safety was the overriding priority. Specifically, the licensee conducted a risk-significant evolution with inadequate concurrent peer check and insufficient supervisory oversight [H.5].

Enforcement:

Violation: Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, requires, in part, that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings.

Contrary to the above, on November 2, 2018, the licensee failed to accomplish an activity affecting quality in accordance with a prescribed procedure appropriate to the circumstances. Specifically, during surveillance testing of RCIC, which is an activity affecting quality, the licensee violated the surveillance test procedure by installing the wrong test fixture into the system.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On April 24, 2019, the inspector presented the quarterly resident inspector inspection results to Mr. K. Scott, General Manager of Plant Operations, and other members of the licensee staff.

DOCUMENTS REVIEWED

71111.01 - Adverse Weather Protection

Condition Reports (CR-RBS-)

2018-04723

2018-05237

2019-00366

Engineering

Reports

Number

Title

Revision

RBS-CS-15-00008 Fukushima Flooding Integrated Assessment Report

000

RBS-SA-17-00001 2017 Focused Evaluation for External Flooding

000

Procedures

Number

Title

Revision

AOP-0029

Severe Weather Operation

040

OSP-0070

Preparation for Mississippi River Flooding

000

71111.04 - Equipment Alignment

Condition Reports (CR-RBS-)

2016-06474

2017-08540

2018-01305

2018-01850

2018-02155

2018-02517

2018-03476

2018-03786

2018-04582

2018-05038

2018-05510

2018-05862

2019-00125

2019-01052

2019-01519

Procedures

Number

Title

Revision

AOP-0014

Loss of 125 VDC

27

R-STM-0305

DC Distribution

006

SOP-0030

High Pressure Core Spray

034

SOP-0032

Low Pressure Core Spray

25

SOP-0049

25 VDC System (Sys #305)

043

STP-203-0201

HPCS Piping Water Fill and Valve Position Verification

308

STP-203-6501

HPCS Pump and Valve Operability Test

2

71111.05AQ - Fire Protection Annual/Quarterly

Calculation

Number

Title

Revision

G13.18.12.2-022

River Bend Station Combustible Loading

005

Condition Reports (CR-RBS-)

2016-07444

2017-06932

2018-00526

2018-01736

2019-00347

Miscellaneous

Documents

Number

Title

Revision

EN-TQ-125

Fire Brigade Drills

007

EN-TQ-125,

Fire Drill Scenario

007

Procedures

Number

Title

Revision

AB-070-501

LPCS Pump Room Fire Area AB-6/Z-1

004

AB-070-506

HPCS Pump Room Fire Area AB-2/Z-1

004

AB-095-517

HPCS Piping Area Fire Area AB-2/Z-2

004

CB-116-133

Battery 1A Room Fire Area C-18

004

CB-116-134

Battery 1B Room Fire Area C-19

004

CB-116-136

HPCS Battery Room Fire Area C-21

004

RB-141-008

SLC Area Fire Area RC-4/Z-4

003

STP-000-3602

Fire Barrier Visual Inspection

017

71111.06 - Flood Protection Measures

Calculations

Number

Title

Revision

PN-314

Moderate Energy Line Crack Flow Rates

PN-317

Max Flood Elevations for Moderate Energy Line Cracks

in Cat I Structures

Drawings

Number

Title

Revision

210-EB-40A-7

Floor & Equipment Drainage Aux Bldg EL 70-0 SH-1

210-EB-40B-9

Floor & Equipment Drainage Aux Bldg El 70-0 SH-2

210-EB-40C-5

Floor & Equipment Drainage Aux Bldg El 95-9 SH-3

210-EB-40D-7

Floor & Equipment Drainage Aux Bldg El 95-9 SH-4

EE-032J

Arrangement - Manholes Plan and Details

PID-32-09J

Engineering P&I Diagram System 609 Drains - Floor

and Equipment

PID-32-09K

Engineering P&I Diagram System 609 Drains - Floor

and Equipment

Procedure

Number

Title

Revision

EN-DC-346

Cable Reliability Program

Work Orders

2867111

2869316

71111.11 - Licensed Operator Requalification Program and Licensed Operator Performance

Condition Reports (CR-RBS-)

2018-00225

2018-01263

2018-01576

2018-01690

2018-03330

2018-06304

Miscellaneous

Documents

Number

Title

Revision

EIP-2-0001

User Aid 1

F

RSMS-OOPS-19-

19-1 As Found Evaluation

Procedures

Number

Title

Revision

AOP-0001

Reactor Scram

AOP-0002

Main Turbine and Generator Trips

AOP-0003

Automatic Isolations

AOP-0005

Loss of Main Condenser Vacuum, Trip of Circulating

Water Pump

AOP-0016

Loss of Standby Service Water

AOP-0017

Reactor Pressure Control Malfunctions

AOP-0050

Station Blackout

EN-OP-115

Conduct of Operations

EOP-0001

RPV Control

281

EOP-0002

Primary Containment Control

EOP-0003

Secondary Containment and Radioactive Release

Control

EOP-0004

Contingencies

GOP-0002

Power Decrease/Plant Shutdown

2

GOP-0005

Power Maneuvering

330

SOP-0003

Reactor Recirculation System

315

SOP-0009

Reactor Feedwater System

079

SOP-0035

Reactor Core Isolation Cooling System

SOP-0053

Standby Diesel Generator and Auxiliaries

71111.12 - Maintenance Effectiveness

Condition Reports (CR-RBS-)

2017-04898

2017-07080

2017-07111

2017-07532

2017-07983

2017-08041

2017-08048

2017-08190

2017-08529

2017-08561

2018-00170

2018-00635

2018-01002

2018-01805

2018-01982

2018-01987

2018-02314

2018-02524

2018-03780

2018-03895

2018-04275

2018-04276

2018-04751

2018-04992

2018-05603

2018-05618

2018-05698

2018-05709

2018-05752

2018-05764

2018-05854

2018-05857

2018-05866

2018-05876

2019-00034

2019-00229

2019-00732

2019-00750

2019-00826

2019-01230

2019-01246

2019-01275

2019-01362

2019-01386

2019-01422

2019-01431

2019-01437

Miscellaneous

Document

Number

Title

Date

System Health

Report: 309 and

405

Standby Emergency Diesel Generators - Division I, II, &

III and HVAC

03/19/2019

Procedures

Number

Title

Revision

EN-DC-203

Maintenance Rule Program

EN-DC-204

Maintenance Rule Scope and Basis

EN-DC-205

Maintenance Rule Monitoring

EN-DC-206

Maintenance Rule (a)(1) Process

SOP-0030

High Pressure Core Spray (Sys #203)

SOP-0059

Containment HVAC System (Sys #403)

Work Order 00483043

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Condition Reports (CR-RBS-)

2019-00035

2019-00068

Procedures

Number

Title

Revision

ADM-0096

Risk Management Program Implementation and On-line

Maintenance Risk Assessment

27

EN-OP-119

Protected Equipment Postings

010

EN-WM-104

On Line Risk Assessment

018

Procedures

Number

Title

Revision

STP-207-4536

RCIC Isolation RCIC Steam Line Flow High Channel

Functional Test (E31-N683A, E31-N690A, E51A-K64)

2

STP-207-4539

RCIC Isolation RCIC Steam Supply Pressure Low

Channel Functional Test (E31-N685B)

301

STP-207-4549

RCIC Isolation RCIC RHR Steam Line Flow High

Channel Functional Test (E31-N684B, E31-N691B)

011

Work Orders

2716192

2847802

2847803

2847804

71111.15 - Operability Determinations and Functionality Assessments

Calculation

Number

Title

Revision

G13.18.14.1-037

Residual Heat Removal System Heat Exchanger

Performance Guidance

Condition Reports (CR-RBS-)

2017-01774

2017-04636

2018-06569

2018-06683

2019-00744

2019-00868

2019-00947

2019-01265

2019-01362

2019-01386

2019-01510

Drawings

Number

Title

Revision

ESK-06HVC02

Elementary Diagram 480V Switchgear Control Room Air

Handling Unit ACU2A

GE-793E922A

Main Steam Positive Leakage Control System

Miscellaneous

Documents

Number

Title

Revision

21.432-000-019 RHR Heat Exchanger Calculated Performance

211.161-997-179 Glow Plug Equivalency Evaluation for Hydrogen Igniter

Assembly #6043 Autolite Model 1106 vs. Autolite

Model 1109 AC DELCO 7G, and 12G

EC-34819

Issue Calculation G13.18.14.1-037 R0, Residual Heat

Removal System Heat Exchanger Performance

Guidance

Procedures

Number

Title

Revision

EN-OP-104

Operability Determination Process

SOP-0040

Hydrogen Mixing, Purge, Recombiners, and Igniters

306

SOP-0059

Containment HVAC System

STP-000-0001

Daily Operating Logs

STP-000-0001

Daily Operating Logs

STP-208-4208

Containment System/MSIV Positive Leakage Control-

Reactor-Steam Line Differential Pressure Channel

Calibration Test (E33-N623, E33-R623, E33-N629,

E33-N630, E33-K623)

STP-254-1402

Div II Hydrogen Igniter Train Current and Voltage Check 24

STP-254-1402

Div II Hydrogen Igniter Train Current and Voltage Check 26

STP-403-0301

Containment Unit Cooler HVR-UC1A Flow Rate

Verification

Work Orders

00478283

00513411

00514664

00514722

00514723

00520091

00520586

00769860

2624439

2687133

2751160

2753000

2843654

71111.19 - Post Maintenance Testing

Condition Reports (CR-RBS-)

2001-01031

2008-05122

2016-01725

2019-01362

2019-01386

Miscellaneous

Document

Number

Title

Revision

CEP-IST-4

Standard on Inservice Testing

309

Procedures

Number

Title

Revision

EN-MA-118

Foreign Material Exclusion

EN-MA-141

Limitorque Valve Operator Model SMB/SB/SBD-000

Through 5 MOV and HBC Periodic Inspection

SOP-0037

Fire Protection Water System Operating Procedure

(Sys #251)

SOP-0059

Containment HVAC System

STP-251-3205

Diesel Fire Pump Operational Test

STP-251-7608

FPW-P1B Fire Pump Engine Maintenance and

Inspection

STP-403-0301

Containment Unit Cooler HVR-UC1A Flow Rate

Verification

Work Orders

00514461

00514462

00520586

2760448

2816820

2820964

2829384

71111.20 - Refueling and Other Outage Activities

Condition Reports (CR-RBS-)

2019-01756

2019-01792

2019-01806

Miscellaneous

Document

Number

Title

Date

Outage Risk Assessment Team RF-20 Outage Report

03/18/2019

Procedures

Number

Title

Revision

CMP-0102

Reactor Vessel Disassembly

EN-OU-108

Shutdown Safety Management Program (SSMP)

GOP-0002

Power Decrease/Plant Shutdown

2

OSP-0034

Control of Obstructions for Primary Containment/Fuel

Building Operability

OSP-0037

Shutdown Operations Protection Plan (SOPP)

STP-050-0700

RCS Pressure Temperature Limits Verification

309

STP-057-3804

Containment Breach Monitoring

Work Order 2825116

71111.22 - Surveillance Testing

Condition Reports (CR-RBS-)

2018-02035

2018-03079

2018-03958

2018-04679

2018-05556

2018-05909

2018-06433

2018-06522

2019-00144

2019-00198

2019-00347

Procedures

Number

Title

Revision

PEP-0026

Diesel Generator Operating Logs

015

SEP-RBS-IST-1

RBS Inservice Testing Bases Document

SEP-RBS-IST-2

RBS Fourth Ten-Year Interval Inservice Testing

Program Plan

SEP-RBS-IST-3

RBS Inservice Testing Cross Reference Document

SOP-0053

Standby Diesel Generator and Auxiliaries (SYS 309)

339

Procedures

Number

Title

Revision

STP-051-4504

NSSSS-Reactor Vessel Water Level-Low Low, Level 2;

Low Low Low, Level 1, Channel Functional Test (B21-

N682D, B21-N681D)

301

STP-201-6310

SLC Pump and Valve Operability Test

311

STP-203-0201

HPCS Piping Water Fill and Valve Position Verification

308

STP-205-6301

LPCS Pump and Valve Operability Test

STP-256-0201

Division I SWP Valve Lineup Verification

304

STP-309-0201

Division I Diesel Generator Operability Test

2

Work Orders

2609386

2626891

2641960

2660045

2680119

2691959

2709560

2726046

2741308

2756900

2763675

2772829

2788501

2805284

2820064

2834274

2843518

2846504

2849069

2849071

2849859

2850921

2854285

2856057

2856492

2859581

71114.06 - Drill Evaluation

Condition Reports (CR-RBS-)

2019-01520

2019-01583

Miscellaneous

Document

Number

Title

Date

River Bend Station ERO Team C Site Drill Report

March 12, 2019

04/10/2019

Procedures

Number

Title

Revision

AOP-0001

Reactor Scram

AOP-0052

Fire Outside the Main Control Room in Areas Containing

Safety Related Equipment

EIP-2-001

Classification of Emergencies

EN-OP-115

Conduct of Operations

EN-OP-200

Plant Transient Response Rules

EOP-0001

Emergency Operating Procedure - RPV Control

EOP-0002

Emergency Operating Procedure - Primary

Containment Control

EOP-0003

Emergency Operating Procedure - Secondary

Containment and Radioactive Release Control

EOP-0004

Emergency Operating Procedure - Contingencies

EOP-0005

Emergency Operating and Severe Accident Procedures

Enclosures

2

71151 - Performance Indicator Verification

Miscellaneous

Documents

Number

Title

Date

Main Control Room Shift Logs

01/01/2018 -

2/31/2018

Procedure

Number

Title

Revision

EN-LI-114

Regulatory Performance Indicator Process

71152 - Problem Identification and Resolution

Condition Reports (CR-RBS-)

2018-06363

2018-06375

Procedures

Number

Title

Revision

CMP-1026

MCC Circuit Breakers, Starters, and Thermal Overloads 21

EN-MA-157

Configuration Control

EN-WM-107

Post Maintenance Testing

Work Orders

00513628

00513629

71153 - Follow-up of Events and Notices of Enforcement Discretion

Condition Report (CR-RBS-)

2018-05854

Procedure

Number

Title

Revision

STP-051-4524

ECCS/RCIC-Reactor Vessel Water Level-Low Low,

Level 2; Low Low Low, Level 1; Channel Functional Test

(B21-N692E, B21-N691E)

AP-0034

Inadvertent Initiation of an ECCS System or RCIC

ML19130A200

SUNSI Review Complete

By: DLP

ADAMS:

Yes No

Publicly Available

Non-Publicly Available

Non-Sensitive

Sensitive

Keyword:

NRC-002

OFFICE

ASRI:DRP/C

ASRI/RI:DRP/C

ARI:DRP/C

BC:DRS/EB1

ABC:DRS/EB2

BC:DRS/OB

NAME

LMerker

BParks

TDeBey

VGaddy

GPick

GWerner

SIGNATURE

lnm

bdp

tmd

vgg

gap

gew

DATE

5/02/2019

5/3/2019

4/30/19

4/24/19

4/27/19

04/25/2019

OFFICE

BC:DNMS/RIB

TL:DRS/IPAT

BC:DRS/RCB

SPE:DRP/C

BC:DRP/C

NAME

GWarnick

RKellar

NMakris

DProulx

JKozal

SIGNATURE

jfk for

rlk

nfm

dlp

/RA/

DATE

4/25/2019

4/24/2019

4/27/19

4/30/19

5/10/2019