IR 05000458/2021001
| ML21124A276 | |
| Person / Time | |
|---|---|
| Site: | River Bend |
| Issue date: | 05/05/2021 |
| From: | Jason Kozal NRC/RGN-IV/DRP |
| To: | Vercelli S Entergy Operations |
| References | |
| IR 2021001 | |
| Download: ML21124A276 (29) | |
Text
May 5, 2021
SUBJECT:
RIVER BEND STATION - INTEGRATED INSPECTION REPORT 05000458/2021001
Dear Mr. Vercelli:
On March 31, 2021, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at River Bend Station. On April 8, 2021, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.
Two findings of very low safety significance (Green) are documented in this report. One of these findings involved a violation of NRC requirements. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.
If you contest the violation or the significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:
Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the NRC Resident Inspector at River Bend Station.
If you disagree with a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the NRC Resident Inspector at River Bend Station. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA/
Jason W. Kozal, Chief Reactor Projects Branch C Division of Reactor Projects
Docket No. 05000458 License No. NPF-47
Enclosure:
As stated
Inspection Report
Docket Number:
05000458
License Number:
Report Number:
Enterprise Identifier: I-2021-001-0088
Licensee:
Entergy Operations, Inc.
Facility:
River Bend Station
Location:
St. Francisville, Louisiana
Inspection Dates:
January 1, 2021 to March 31, 2021
Inspectors:
B. Baca, Health Physicist
W. Cullum, Reactor Inspector
J. Drake, Senior Reactor Inspector
R. Kumana, Senior Resident Inspector
J. O'Donnell, Senior Health Physicist
B. Parks, Emergency Response Specialist
D. Reinert, Reactor Inspector
E. Simpson, Health Physicist
C. Smith, Senior Reactor Inspector
C. Wynar, Resident Inspector
Approved By:
Jason W. Kozal, Chief
Reactor Projects Branch C
Division of Reactor Projects
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at River Bend Station, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
List of Findings and Violations
Failure to Scope a Flood Control Structure in the Maintenance Rule Program Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000458/2021001-01 Open/Closed None (NPP)71111.12 The inspectors identified a Green non-cited violation of Title 10 of the Code of Federal Regulations (10 CFR) 50.65, Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, for the licensees failure to include a non-safety-related structure in the scope of their maintenance rule monitoring program. Specifically, the licensee failed to include the Unit 2 excavation flood control berm, which met the requirements of 10 CFR 50.65(b)(2) as a structure whose failure could prevent safety-related structures, systems, and components from fulfilling their safety-related function. The failure of the berm during a design basis precipitation event could prevent the standby service water system from fulfilling its safety-related function.
Manual Reactor Trip Due to Reactor Recirculation Pump Trip Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events Green FIN 05000458/2021001-02 Open/Closed None (NPP)71153 The inspectors reviewed a Green self-revealed finding for the licensees failure to follow Procedure EN-LI-102, Corrective Action Process, Revisions 16 and 20. Specifically, after suffering unexpected heater drain pump trips that occurred in the aftermath of recirculation pump trips at the plant, the licensee failed to properly investigate the causes of the trips in accordance with the procedure. Consequently, the condition that resulted in the trips was left uncorrected. This condition directly contributed to thermal hydraulic instabilities and resulted in a manual scram in August 2020.
Additional Tracking Items
Type Issue Number Title Report Section Status LER 05000458/2020-02-00 Manual Reactor Trip Due to Reactor Recirculation Pump Trip 71153 Closed
PLANT STATUS
The inspection quarter began on January 1, 2021, with the reactor operating at 100 percent power. Power was reduced to approximately 67 percent on January 8, 2021, for a control rod pattern adjustment and returned to 100 percent power on January 9, 2021. Power was reduced to 69 percent on January 22, 2021, for a control rod pattern adjustment and returned to 100 percent power on January 25, 2021.
River Bend Station shut down the unit on February 21, 2021, and entered Mode 5 on February 22, 2021, to begin Refueling Outage 21. The station performed a reactor startup on March 19, 2021, ending the outage. The unit subsequently reached approximately 100 percent power.
On March 25, 2021, operators scrammed the plant in response to a lowering main condenser vacuum due to the A air ejector inlet valve going shut. The station corrected the issue and performed a reactor startup on March 26, 2021. The unit reached 100 percent power on March 29, 2021. That same day, operators lowered power to approximately 60 percent power for a control rod pattern adjustment. Operators raised power back to 100 percent on March 30, 2021, and maintained it there for the remainder of the quarter.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
Starting on March 20, 2020, in response to the National Emergency declared by the President of the United States on the public health risks of the Coronavirus Disease 2019 (COVID-19),resident inspectors were directed to begin telework and to remotely access licensee information using available technology. During this time, the resident inspectors performed periodic site visits each week; conducted plant status activities as described in IMC 2515, Appendix D, Plant Status; observed risk-significant activities; and completed on-site portions of IPs. In addition, resident and regional baseline inspections were evaluated to determine if all or portions of the objectives and requirements stated in the IP could be performed remotely. If the inspections could be performed remotely, they were conducted per the applicable IP. In some cases, portions of an IP were completed remotely and on-site. The inspections documented below met the objectives and requirements for completion of the IP.
REACTOR SAFETY
71111.01 - Adverse Weather Protection
Seasonal Extreme Weather Sample (IP Section 03.01) (1 Sample)
- (1) The inspectors evaluated readiness for seasonal extreme weather conditions prior to the onset of seasonal cold temperatures for the following systems:
- Instrument air and station blackout diesel generator on March 15, 2021
Impending Severe Weather Sample (IP Section 03.02) (1 Sample)
- (1) The inspectors evaluated the adequacy of the overall preparations to protect risk-significant systems from impending severe weather on March 17, 2021.
71111.04 - Equipment Alignment
Partial Walkdown Sample (IP Section 03.01) (3 Samples)
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
- (1) Division I emergency diesel generator on January 16, 2021
- (2) Division II standby service water on January 25, 2021
- (3) Division I decay heat removal on March 5, 2021
71111.05 - Fire Protection
Fire Area Walkdown and Inspection Sample (IP Section 03.01) (6 Samples)
The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:
- (1) Diesel generator A room, fire area DG-6/Z-1, on January 16, 2021
- (2) Standby cooling tower pump B room, fire area PH-2/Z-1, on January 25, 2021
- (3) Standby switchgear 1B room, fire area C-14, on March 2, 2021
- (4) Low pressure core spray pump room, fire area AB-6/Z-1, on March 18, 2021
- (5) Cable chase I, fire area C-1, on March 23, 2021
- (6) Cable chase II, fire area C-2, on March 23, 2021
71111.08G - Inservice Inspection Activities (BWR)
BWR Inservice Inspection Activities Sample - Nondestructive Examination and Welding
Activities (IP Section 03.01)
- (1) The inspectors verified that the reactor coolant system boundary, reactor vessel internals, risk-significant piping system boundaries, and containment boundary are appropriately monitored for degradation and that repairs and replacements were appropriately fabricated, examined, and accepted by reviewing the following activities from February 15, 2021 to March 10, 2021:
03.01.a - Nondestructive Examination and Welding Activities.
- Nondestructive Examinations a. Ultrasonic i. Reactor Coolant System, RCS-900CX-SW023A, Elbow to Pipe ii. Reactor Coolant System, RCS-900CX-SW014CA, Tee to Reducer iii. Reactor Pressure Vessel, B13-D001-AE, BW-Vessel to Flange iv. Standby Liquid Control, SLS-150-037-1 Weld XI-FW001 v. Standby Liquid Control, SLS-150-037-1 Weld XI-FW002 b. Radiographic i. Standby Liquid Control, SLS-150-037-1 Weld XI-FW001 ii. Standby Liquid Control, SLS-150-037-1 Weld XI-FW002 c. Dye Penetrant i. Standby Liquid Control, SLS-150-037-1 Weld XI-FW001 ii. Standby Liquid Control, SLS-150-037-1 Weld XI-FW002 iii. Residual Heat Removal, E12-AOVF041A, Check valve Bearing Cover before weld and machine repair iv. Residual Heat Removal, E12-AOVF041A, Check valve Bearing Cover after weld and machine repair d. Magnetic Particle i. Feedwater System FWS 107 FWS-063A-FW013, PIPE SECTION - SADDLE e. Visual i. Standby Liquid Control, SLS-150-037-1 Weld XI-FW001 ii. Standby Liquid Control, SLS-150-037-1 Weld XI-FW002
- Welding a. Gas Tungsten Arc Welding i. Standby Liquid Control System, SLS-150-037-1, XI-FW001 ii. Standby Liquid Control System, SLS-150-037-1, XI-FW002
Problem Identification and Resolution Review of Inservice Items
The inspector evaluated a sample of 68 condition reports associated with inservice inspection activities. No findings or violations of more than minor significance were identified.
71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (2 Samples)
- (1) The inspectors observed and evaluated licensed operator performance in the Control Room during a reactor shutdown in preparation for a refueling outage on February 21, 2020.
- (2) The inspectors observed and evaluated licensed operator performance in the Control Room during plant startup on March 19, 2021.
71111.12 - Maintenance Effectiveness
Maintenance Effectiveness (IP Section 03.01) (1 Sample)
The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:
- (1) Flood control structures for standby service water on March 1, 2021
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Risk Assessment and Management Sample (IP Section 03.01) (4 Samples)
The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:
- (1) Yellow risk during surveillance testing on Division I low pressure core spray and Division I emergency diesel generator, and planned inspections on Division I standby service water on February 2, 2021
- (2) Yellow risk with Division I electrical power out of service during refueling operations on March 3, 2021
- (3) Yellow risk with residual heat removal unavailable for inventory control on March 8, 2021
- (4) Yellow risk with containment unit cooler 1B out of service on March 31, 2021
71111.15 - Operability Determinations and Functionality Assessments
Operability Determination or Functionality Assessment (IP Section 03.01) (4 Samples)
The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:
- (1) Operability of Division I main steam positive leakage control system with drain valve E33-MOVF006 closed in response to leakage across E33-MOVF007 and E33-MOV5008 on January 11, 2021 (CR-RBS-2021-00058)
- (2) Operability of Division II battery with heater out of service on March 5, 2021 (CR-RBS-2021-00123)
- (3) Operability of primary containment with valve E12-FV0044B failure on March 22, 2021 (CR-RBS-2021-02384)
- (4) Operability of standby service water with non-conservative flooding analysis on March 23, 2021 (CR-RBS-2020-04429)
71111.17T - Evaluations of Changes, Tests, and Experiments Sample Selection (IP Section 02.01)
The inspectors reviewed the following evaluations, screenings, and/or applicability determinations for 10 CFR 50.59 from March 1-5, 2021:
- (1) Engineering Change EC-3950, Installation of RF14 C11-AOVF010 O-rings, Revision 2 (Screening)
- (2) Engineering Change EC-3955, Installation of RF15 DFR-AOV102 O-rings, Revision 2 (Screening)
- (3) Engineering Change EC-30980, Revision to the SLC Orifice C41-ROD001 Bore Size, Revision 2 (Screening)
- (4) Engineering Change EC-39182, ERIS Upgrade for Rod Scram Timing and Feedwater Valve Position Indication Software, Revision 1 (Screening)
- (5) Engineering Change EC-72271, Install Key-Lock Switches on Main Control Room Panels H13-P691 and H13-P692, Revision 0 (Screening)
- (6) Engineering Change EC-72716, Replacement of Obsolete Recirculation Pump Seal Purge Supply Flow Control Valve, Revision 0 (Screening)
- (7) Engineering Change, EC-87166, Plug Weep Holes in Concrete Duct to G Tunnel, Revision 0 (Screening)
- (8) Engineering Change EC-5000070744, Change Elastomer Materials for Fisher AOV O-rings to Viton, Revision 2 (Screening)
- (9) Engineering Change EC-70846, EDG Lube Oil Header Alternate Seal Assembly, Revision 0 (Screening)
- (10) Engineering Change EC-71797, Auxiliary Building Steam Tunnel Floor Plugs Sealant Alternative, Revision 0 (Screening)
- (11) Engineering Change EC-23335, Residual Heat Removal (RHR) High Level Output Optical Isolator Card Sneak Power Path, Revision 0 (Screening)
- (12) Engineering Change EC-31934, Determine Potential Cold Spring Load at the Intercooler Support Brackets (ISB) on Division II Standby Diesel Generator, Revision 0 (Screening)
- (13) Engineering Change EC-71135, Base Engineering Change for Replacement of Parson Peebles Voltage Regulator, Revision 0 (Screening)
- (14) Engineering Change EC-72271, Install Key-Lock Switches on Main Control Room Panels H13-P691 and H13-P692 to Bypass RHR Loop A and B 135 PSIG Isolations, Revision 0 (Screening)
- (15) Engineering Change EC-73013, Install Backdraft Dampers to Control Building HVAC System, Revision 0 (Screening)
- (16) Engineering Change EC-73497, Install Boron Carbide Aluminum Metal Matrix Composite Inserts into the Spent Fuel Pool Fuel Storage Racks to Address Boraflex Degradation, Revision 0 (Screening)
- (17) Engineering Change EC-76014, Feedwater Debris Strainer Evaluation and Installation, Revision 0 (Screening)
- (19) Engineering Change EC-86067, Temporary Modification to Install an External Oil Reservoir near B33-PC001A to Increase Margin to a Low Oil Level Alarm, Revision 0 (Screening)
- (20) Engineering Change ER-RB-2004-0307-001, Change Elastomer Materials for Fisher AOV O-rings to Viton, Revision 0 (Screening)
- (21) Engineering Change EC-76380, Open Phase Detection, Revision 0 (Evaluation)
- (22) Engineering Change EC-80989, Harris Panel Upgrade, Revision 0 (Evaluation)
- (23) Engineering Change EC-86722, Tornado Missile Risk Evaluator, Revision 0 (Evaluation)
- (24) Engineering Change EC-31805, Control Building Chiller Controls Upgrade, Revision 0 (Evaluation)
- (25) Engineering Change EC-72704, Steam Jet Air Ejector Single Point Vulnerability, Revision 0 (Evaluation)
- (26) Engineering Change EC-79427, TRACG Anticipated Operational Occurrences Updates, Revision 0 (Evaluation)
71111.19 - Post-Maintenance Testing
Post-Maintenance Test Sample (IP Section 03.01) (2 Samples)
The inspectors evaluated the following post-maintenance test activities to verify system operability and functionality:
- (1) Work Order 52869970, testing of valve SSV-MOV1A following preventive maintenance, on March 5, 2021
- (2) Work Order 00549941, testing of valve E12-F041A following flange repair, on March 26, 2021
71111.22 - Surveillance Testing
The inspectors evaluated the following surveillance tests:
Surveillance Tests (other) (IP Section 03.01)
- (1) STP-309-0201, Revision 63, Division I Diesel Generator Operability Test on February 3, 2021
- (2) STP-309-0202, Revision 332, Division II Diesel Generator Operability Test on February 17, 2021
Inservice Testing (IP Section 03.01) (1 Sample)
- (1) STP-256-6302, Revision 28, Div II Standby Service Water Quarterly Valve Operability Test on January 22, 2021
Containment Isolation Valve Testing (IP Section 03.01) (1 Sample)
- (1) STP-208-3601, Revision 13, 'A' Steam Line MSIVs and Outboard Drain Valve Leak Rate Test and Inboard MSIV Inleakage Test on March 12,
RADIATION SAFETY
71124.01 - Radiological Hazard Assessment and Exposure Controls
Radiological Hazard Assessment (IP Section 03.01) (1 Sample)
- (1) The inspectors evaluated how the licensee identified the magnitude and extent of radiation levels and the concentrations and quantities of radioactive materials and how the licensee assessed radiological hazards.
Instructions to Workers (IP Section 03.02) (1 Sample)
The inspectors evaluated instructions to workers including radiation work permits used to access high radiation areas for the following:
- (1) Radiation Work Packages (RWP)
- RWP 2021-1800, Refuel Floor Reactor Vessel Disassembly & Reassembly Activities, Revision 0
- RWP 2021-1901, Radiation Protection Activities in the Drywell, Revision 0
- RWP 2021-1606, Radwaste, Shipping, and Decontamination Activities in LHRA/HRA, Except Drywell, Revision 0
- (2) Electronic Alarming Dosimeter Alarms
- One dose rate alarm after exiting the area from Turbine Building Waterbox activities (CR-RBS-2019-02335)
- Two dose rate alarms during smoke alarm testing in the Spent Fuel Pool Heat Exchanger 1A room (CR-RBS-2020-01845)
- Two dose rate alarms during maintenance work on the Radwaste Oil Plate Separator (CR-RBS-2020-03041)
- (3) Labeling of Containers
- On RadWaste 106' elevation, two Low Specific Activity boxes individually tagged yellow bags of Dry Active Waste (DAW)
- On RadWaste 106' elevation, 55-gallon drums of contaminated water and oil
- On Turbine Building 95' elevation, 20' Sea/Land container (#148216)
- On Turbine Building 95' elevation, Chem Nuclear Shipping Cask (CNSI-14-195L No. 3) - Empty
Contamination and Radioactive Material Control (IP Section 03.03) (2 Samples)
The inspectors evaluated licensee processes for monitoring and controlling contamination and radioactive material.
- (1) Observed licensee conduct surveys of potentially contaminated material leaving the radiologically controlled area.
- (2) Observed workers exiting the drywell during a refueling outage.
Radiological Hazards Control and Work Coverage (IP Section 03.04) (4 Samples)
The inspectors evaluated in-plant radiological conditions during facility walkdowns and observed radiological work activities, to include those with airborne radioactivity or the potential for airborne radioactivity, for the following:
- (1) Survey and retrieval of highly radioactive item from refueling cavity under RWP 2021-1800, Refuel Floor Reactor Vessel Disassembly & Reassembly Activities, Revision 0
- (2) Transfer of highly radioactive item from Reactor Building to RadWaste Building under RWP 2021-1606, Radwaste, Shipping, and Decontamination Activities in LHRA/HRA, Except Drywell, Revision 0
- (3) Removal and control of reactor vessel head (RVH) on the Refuel Floor under RWP 2021-1800, Refuel Floor Reactor Vessel Disassembly & Reassembly Activities, Revision 0
- (4) Drywell down-posting survey after shielding of RHR valve under RWP 2021-1901, Radiation Protection Drywell Activities, Revision 0
High Radiation Area and Very High Radiation Area Controls (IP Section 03.05) (4 Samples)
The inspectors evaluated licensee controls of the following High Radiation Areas and Very High Radiation Areas:
- (1) RadWaste Building 106' elevation, Liner Bay - High Radiation Area (>1 R/hr)
- (2) RadWaste Building 65' elevation, Reactor Water Cleanup Phase Separator - High Radiation Area (>1 R/hr)
- (3) Fuel Building 98' elevation, Spent Fuel Pool Demineralizer - High Radiation Area
(>1 R/hr)
- (4) Reactor Building 131' elevation, Inclined Fuel Transfer System Blind Flange Area - Very High Radiation Area
Radiation Worker Performance and Radiation Protection Technician Proficiency (IP Section 03.06) (1 Sample)
- (1) The inspectors evaluated radiation worker and radiation protection technician performance as it pertains to radiation protection requirements.
71124.02 - Occupational ALARA Planning and Controls
Implementation of ALARA and Radiological Work Controls (IP Section 03.03) (3 Samples)
The inspectors reviewed as low as reasonably achievable practices and radiological work controls. The inspectors reviewed the following activities:
- (1) Removal of a highly radioactive item from the cavity under RWP 2021-1800, Refuel Floor Reactor Vessel Disassembly & Reassembly Activities, Revision 0
- (2) RVH movement under RWP 2021-1800, Refuel Floor Reactor Vessel Disassembly &
Reassembly Activities, Revision 0
- (3) Drywell surveys for down-posting of the drywell from locked high radiation area to high radiation area under RWP 2021-1901, Radiation Protection Drywell Activities, Revision 0
Radiation Worker Performance (IP Section 03.04) (1 Sample)
The inspectors evaluated radiation worker and radiation protection technician performance during the following Refueling Outage 21 activities:
- Cavity decontamination and removal of a highly radioactive item from the drywell head flange area
- Movement and control of the RVH (Alpha II controls)
- Down-posting radiation survey of RHR valve in the Drywell (>1 R/hr)
71124.03 - In-Plant Airborne Radioactivity Control and Mitigation
Permanent Ventilation Systems (IP Section 03.01) (1 Sample)
The inspectors evaluated the configuration of the following permanently installed ventilation system:
- (1) Control room fresh air system, subsystems A and B
Temporary Ventilation Systems (IP Section 03.02) (1 Sample)
The inspectors evaluated the configuration of the following temporary ventilation system:
- (1) HEPA ventilation system, H-20, to provide negative pressure and filtered ventilation inside the reactor pressure vessel head on refuel floor
Use of Respiratory Protection Devices (IP Section 03.03) (1 Sample)
The inspectors evaluated that the licensees use of respiratory protection devices to limit the intake of radioactive material meets the requirements of a respiratory protection program.
- (1) The inspectors observed the licensee's use of powered air purifying respirators on the refuel floor during the RVH lift.
Self-Contained Breathing Apparatus for Emergency Use (IP Section 03.04) (1 Sample)
- (1) The inspectors evaluated the licensees use and maintenance of self--contained breathing apparatuses.
OTHER ACTIVITIES - BASELINE
===71151 - Performance Indicator Verification
The inspectors verified licensee performance indicators submittals listed below:
IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 03.01)===
- (1) January 1, 2020 - December 31, 2020
IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 03.02) (1 Sample)
- (1) January 1, 2020 - December 31, 2020
IE04: Unplanned Scrams with Complications (USwC) Sample (IP Section 03.03) (1 Sample)
- (1) January 1, 2020 - December 31, 2020
OR01: Occupational Exposure Control Effectiveness Sample (IP Section 03.15) (1 Sample)
- (1) October 1, 2020 - December 31, 2020 PR01: Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual Radiological Effluent Occurrences (RETS/ODCM) Radiological Effluent Occurrences Sample (IP Section 03.16) (1 Sample)
- (1) October 1, 2020 - December 31, 2020
71152 - Problem Identification and Resolution
Annual Follow-up of Selected Issues (IP Section 02.03) (1 Sample)
The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:
- (1) Extent of condition inspection results for the failure to develop an adequate operational decision-making issue for compensatory measures related to a degraded condition of the feedwater system sparger nozzles documented in NCV 05000458/2018012-05 on March 1, 2021
71153 - Follow-up of Events and Notices of Enforcement Discretion Event Report (IP Section 03.02)
The inspectors evaluated the following licensee event reports (LERs):
- (1) LER 05000458/2020-002-00, Manual Reactor Scram Due to Reactor Recirculation Pump Trip (ADAMS Accession No. ML20293A475)
The inspection conclusions associated with this LER and an associated finding are documented in this report under the Inspection Results section.
Personnel Performance (IP Section 03.03) (1 Sample)
- (1) The inspectors evaluated the licensees performance during a reactor scram due to a loss of condenser vacuum on March 25,
INSPECTION RESULTS
Failure to Scope a Flood Control Structure in the Maintenance Rule Program Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000458/2021001-01 Open/Closed None (NPP)71111.12 The inspectors identified a Green non-cited violation of 10 CFR 50.65, Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, for the licensees failure to include a non-safety-related structure in the scope of their maintenance rule monitoring program. Specifically, the licensee failed to include the Unit 2 excavation flood control berm, which met the requirements of 10 CFR 50.65(b)(2) as a structure whose failure could prevent safety-related SSCs from fulfilling their safety-related function. The failure of the berm during a design basis precipitation event could prevent the standby service water system from fulfilling its safety-related function.
Description:
During a review of external flood protection at River Bend Station, the inspectors identified evidence of degradation of soil slopes in the Unit 2 excavation, an unfilled pit for the canceled unit. In particular, the inspectors noted an area of soil collapse in the vicinity of the Unit 2 excavation berm, a flood control berm designed to divert runoff away from the pit to prevent water accumulation from affecting the standby service water system components located in an adjacent tunnel.
The inspectors questioned whether the area of slope degradation affected the function of the berm and whether there was any monitoring conducted in accordance with the maintenance rule. The licensee determined that, during initial implementation of the maintenance rule program at River Bend Station, the station had failed to include the function of the Unit 2 excavation berm in the program scope.
The berm is not safety-related, but its failure could prevent safety-related SSCs from fulfilling their safety-related function during a design basis flood at River Bend Station. If the berm were to fail to divert runoff from a design basis precipitation event, the Unit 2 excavation could fill up to a level above the ventilation shaft opening of the G Tunnel, allowing water to enter and submerge the safety-related standby service water cooling tower return valves. This structure meets the criteria of 10 CFR 50.65(b)(2). The maintenance rule program at River Bend Station requires the station to monitor structures that meet the criteria of 10 CFR 50.65(b) in accordance with Procedure EN-DC-150, Condition Monitoring of Maintenance Rule Structures. Specifically, the licensees procedure requires them to inspect structures every 5 or 10 years based on the risk significance, and after external events that may have impacted their function. This monitoring did not take place.
After review by the licensees maintenance rule review panel, the licensee added the berm to the maintenance rule program scope on January 10, 2021. The licensee determined that the identified degradation of the slope did not prevent the berm from performing its function but placed the system in (a)(1) status because additional monitoring would need to be implemented to provide reasonable assurance of the berms continued functionality.
Corrective Actions: The licensee convened the maintenance rule expert panel and entered the berm into their maintenance rule program in (a)(1) status.
Corrective Action References: CR-RBS-2020-02275
Performance Assessment:
Performance Deficiency: The failure to monitor the condition of a non-safety-related structure whose failure could prevent a safety-related system from fulfilling its safety function was a performance deficiency.
Screening: The inspectors determined the performance deficiency was more than minor because if left uncorrected, it would have the potential to lead to a more significant safety concern. Specifically, by failing to monitor or conduct appropriate preventive maintenance on the Unit 2 excavation berm, the licensee failed to identify slope degradation that could have affected the berms function, and reasonable assurance of the ability of the standby service water system to function during a design basis flood could not be maintained.
Significance: The inspectors assessed the significance of the finding using NRC Inspection Manual Chapter 0609 Appendix A, The Significance Determination Process (SDP) for Findings At-Power. Using Exhibit 2, Mitigating Systems Screening Questions, the inspectors determined that the finding was of very low safety significance (Green) because it did not involve the loss or degradation of equipment or function specifically designed to mitigate a seismic, flooding, or severe weather initiating event (e.g., seismic snubbers, flooding barriers, tornado doors) for greater than 14 days.
Cross-Cutting Aspect: Not Present Performance. No cross-cutting aspect was assigned to this finding because the inspectors determined the finding did not reflect present licensee performance.
Enforcement:
Violation: Title 10 CFR 50.65(b)(2) requires, in part, that the scope of the monitoring program specified in paragraph (a)(1) include non-safety-related SSCs whose failure could prevent safety-related SSCs from fulfilling their safety-related function.
Contrary to the above, from July 10, 1996, to January 10, 2021, the scope of the licensees monitoring program specified in paragraph (a)(1) did not include the Unit 2 excavation flood control berm, a non-safety-related SSC whose failure could prevent safety-related SSCs from fulfilling their safety-related function. The inclusion of the berm in the scope of the monitoring program was necessary because the failure of that structure could prevent the standby service water system, a safety-related system, from fulfilling its safety-related function.
Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.
Manual Reactor Trip Due to Reactor Recirculation Pump Trip Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events
Green FIN 05000458/2021001-02 Open/Closed None (NPP)71153 The inspectors reviewed a Green self-revealed finding for the licensees failure to follow Procedure EN-LI-102, Corrective Action Process, Revisions 16 and 20. Specifically, after suffering unexpected heater drain pump trips that occurred in the aftermath of recirculation pump trips at the plant, the licensee failed to properly investigate the causes of the trips in accordance with the procedure. Consequently, the condition that resulted in the trips was left uncorrected. This condition directly contributed to thermal hydraulic instabilities and resulted in a manual scram in August 2020.
Description:
On August 21, 2020, reactor recirculation pump B tripped. Reactor power level fell to approximately 66 percent, and operators entered Procedures GOP-0004, Single Loop Operations, Revision 28, and AOP-0024, Thermal Hydraulic Stability Controls, Revision 34. Following that event, the extraction steam supply was isolated, leading to a reduction in the water level in the B third point feedwater heater. The level eventually fell below the low level setpoint, causing the C heater drain pump (HDL-P1C) to trip. The licensee then entered AOP-0006, Condensate/Feedwater Failures, Revision 26.
Plant operators lowered recirculation flow to maintain A recirculation loop flow within allowable limits. An unexpected entry into the restricted region of the power-to-flow map specified in AOP-0024 led them to begin inserting control rods. The operators then received multiple alarms for the period-based detection system. Reactor power was observed to be fluctuating between 62 percent and 68 percent. To address the potential thermal hydraulic instabilities signified by these alarms, the operator at the controls inserted a reactor scram by placing the mode switch in shutdown.
Upon subsequent review, the licensee concluded that the alarms were associated with actual thermal hydraulic instabilities in the plant. The licensee was able to demonstrate that these instabilities began almost immediately after the C heater drain pump tripped off, indicating that the trip of the heater drain pump, and the temperature transient that it brought about, was the cause.
The licensee determined that the trip of the heater drain pump was caused by a buildup of debris in the air relays of the positioner that controls the high-level dump valve for the B third point heater (HDL-LV24B). The debris originated in the instrument air system, and there is no filter between that system and the positioner. Additional licensee review revealed that the station had experienced unexplained heater drain pump trips in the aftermath of recirculation pump trips on at least two prior occasions. Specifically, after a trip of recirculation pump B in November 2010, a low-level condition occurred in the A third point heater, leading to a trip of the D heater drain pump. After a trip of recirculation pump A in December 2012, a low-level condition occurred in the B heater, causing a trip of the C heater drain pump.
Section 5.2.1.a and Attachment 9.2 of EN-LI-102, the station's corrective action process procedure, require that condition reports be written for events or conditions that could negatively impact reliability or availability and for unplanned conditions or events that affect reactivity. The unexpected low-level condition in the heater that occurred after the 2012 recirculation pump trip met both criteria, but the licensee failed to write a condition report for the issue. No corrective actions were taken for the issue, which allowed the vulnerability to persist until it was triggered again in the 2020 event.
Following the 2010 recirculation pump trip event, the licensee did write a condition report documenting the heater drain pump trip; however, the responsible manager that was assigned to address the condition failed to take appropriate corrective actions in accordance with EN-LI-102. Because the event was classified as a category C condition, the procedure required the responsible manager to ensure that actions were appropriately assigned to correct the problem and appropriately completed within the prescribed time frame. The action of investigating and correcting the cause of the low-level condition in the heater was never appropriately completed, as the individual to whom the action was assigned determined that the heater drain pump trip was expected due to the low-level condition. The responsible manager closed the condition report without requiring that the reasons why the low-level condition had occurred were identified and corrected.
This finding closes licensee event report LER 2020-002-00 dated October 19, 2020.
Corrective Actions: Following the 2020 event, the licensee took actions to remove the debris buildup in the positioner and developed a plan to install an air filter upstream of the regulator that feeds the positioner to prevent buildups from recurring.
Corrective Action References: CR-RBS-2020-03497
Performance Assessment:
Performance Deficiency: The station's failure to take appropriate corrective actions in accordance with Procedure EN-LI-102 was a performance deficiency.
Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Equipment Performance attribute of the Initiating Events cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, the station's failure to take appropriate corrective actions for the heater drain pump trips that occurred in the aftermath of recirculation pump trips in 2010 and 2012 allowed a vulnerability to persist in the heater drain system that led to thermal hydraulic instabilities and a manual scram when a heater drain pump tripped in response to a recirculation pump trip in 2020.
Significance: The inspectors assessed the significance of the finding using NRC Inspection Manual Chapter 0609 Appendix A, The Significance Determination Process (SDP) for Findings At-Power. Using Exhibit 1, Initiating Events Screening Questions, the inspectors determined that the finding was of very low safety significance (Green) because the loss of injection did not cause both a reactor trip and the loss of mitigation equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition.
Cross-Cutting Aspect: Not Present Performance. No cross-cutting aspect was assigned to this finding because the inspectors determined the finding did not reflect present licensee performance.
Enforcement:
Inspectors did not identify a violation of regulatory requirements associated with this finding.
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
- On February 26, 2021, the inspectors presented the occupational radiation safety inspection results to Mr. S. Vercelli, Site Vice President, and other members of the licensee staff.
- On March 5, 2021, the inspectors presented the evaluation of changes, tests, and experiments inspection results to Mr. P. Penny, Manager, Design and Program Engineering, and other members of the licensee staff.
- On March 15, 2021, the inspectors presented the inservice inspection results to Mr. B. Chenard, Director, Engineering, and other members of the licensee staff.
- On April 8, 2021, the inspectors presented the integrated inspection results to Mr. S. Vercelli, Site Vice President, and other members of the licensee staff.
- On April 22, 2021, the inspectors presented the inservice inspection re-exit results to Mr. S. Vercelli, Site Vice President, and other members of the licensee staff.
DOCUMENTS REVIEWED
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
71111.08G Corrective Action
Documents
CR-2020-02095, CR-HQN-2020-00198,
CR-HQN-2020-00205, CR-HQN-2020-00208,
CR-HQN-2020-00214, CR-RBS-2019-03211,
CR-RBS-2019-04720, CR-RBS-2021-00099,
CR-RBS-2011-00443, CR-RBS-2018-06601,
CR-RBS-2019-02540, CR-RBS-2019-02545,
CR-RBS-2019-02565, CR-RBS-2019-02606,
CR-RBS-2019-02646, CR-RBS-2019-02725,
CR-RBS-2019-02762, CR-RBS-2019-02841,
CR-RBS-2019-02851, CR-RBS-2019-02883,
CR-RBS-2019-02922, CR-RBS-2019-02982,
CR-RBS-2019-03004, CR-RBS-2019-03020,
CR-RBS-2019-03025, CR-RBS-2019-03050,
CR-RBS-2019-03106, CR-RBS-2019-03137,
CR-RBS-2019-03173, CR-RBS-2019-03275,
CR-RBS-2019-03305, CR-RBS-2019-03309,
CR-RBS-2019-03329, CR-RBS-2019-03373,
CR-RBS-2019-03404, CR-RBS-2019-03459,
CR-RBS-2019-03484, CR-RBS-2019-03839,
CR-RBS-2019-03862, CR-RBS-2019-04192,
CR-RBS-2019-04720, CR-RBS-2019-04889,
CR-RBS-2019-05308, CR-RBS-2019-05367,
CR-RBS-2019-05420, CR-RBS-2019-05830,
CR-RBS-2019-06067, CR-RBS-2019-06946,
CR-RBS-2019-06954, CR-RBS-2019-07497,
CR-RBS-2019-08037, CR-RBS-2020-00384,
CR-RBS-2020-00386, CR-RBS-2020-00594,
CR-RBS-2020-01193, CR-RBS-2020-02738,
CR-RBS-2020-03077, CR-RBS-2020-03619,
CR-RBS-2020-03885, CR-RBS-2020-04083,
CR-RBS-2020-04119, CR-RBS-2020-04162,
CR-RBS-2020-04483, CR-RBS-2020-04570,
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
CR-RBS-2020-04729, CR-RBS-2020-05045,
CR-RBS-2020-05064, CR-RBS-2020-05142,
CR-RBS-2020-05407, CR-RBS-2015-05149,
CR-RBS-2018-01037, CR-RBS-2018-06188,
CR-RBS-2018-06601, CR-RBS-2019-01805,
Corrective Action
Documents
Resulting from
Inspection
CR-RBS-
21-01204, 2021-02263, 2021-02264, 2021-02265,
21-02266, 2021-02267, 2021-02268
Procedures
CEP-IST-4
Standard On Inservice Testing
309
CEP-NDE-0255
Radiographic Examination ASME, ANSI, AWS, API, AWWA
Welds and Components
010
CEP-NDE-0400
Ultrasonic Examination
008
CEP-NDE-0641
Liquid Penetrant Examination (PT) for ASME Section XI
009
CEP-NDE-0901
VT-1 Examination
006
CEP-NDE-0902
VT-2 Examination
009
CEP-NDE-0903
VT-3 Examination
006
CEP-NDE-0955
Visual Examination (VE) of Bare-Metal Surfaces
307-1
CEP-WP-002
Qualification, Development, and Control of Welding
Procedure Specifications
CEP-WP-003
Qualification and Control of Welders
CEP-WP-004
Control and Documentation of Welding Activities
CEP-WP-005
Control and Issuance of Welding Material
CEP-WP-005
Control and Issuance of Welding Material
004
CEP-WP-GWS-1
General Welding Standard ASME/ANSI
005-1
CEP-WP-GWS-5
General Welding Standard Stud Welding
CEP-WP-PHT-1
Preheat and Postweld Heat Treatment Requirements
CEP-WP-RBMD-
Repair Of Base Material Defects
CEP-WP-TCG-1
Thermal Cutting And Gouging
CEP-WP-WIIR-1
Weld Inprocess Inspection Requirements
DR-ECH-
CEP_WP_IGP
Internal Gas Purging
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Preventive Maintenance Component Classification
EN-FAP-LI-001
Performance Improvement Review Group (PRG) Process
Corrective Action Program
Causal Analysis Process
Operability Determination Process
Work Orders
WO- 00485441, 00485667, 00523358
Corrective Action
Documents
CR-RBS-
20-04343
Procedures
EDP-CS-15
River Bend Station Maintenance Rule Structural Monitoring
Procedure
Condition Monitoring of Maintenance Rule Structures
Maintenance Rule Scope and Basis
Calculations
E-192
Standby Diesel Generator Loading
G13.18.12.3*161
Standby switchgear room heat up
G13.18.2.1*059
Control Building Heat Load Evaluation during LOCA with
Offsite Power Available and Normal Operating Conditions
Engineering
Changes
This documents the installation of RF14 C11-AOVF010 O-
rings
This documents the installation of RF15 DFR-AOV102 O-
rings
RHR High Level Output Optical Isolator Card Sneak Power
Path
Revise the SLC orifice C41-ROD001 bore size to reflect GE
SC-10-13 information and update design documents
accordingly
Operation and Maintenance Manual for Adaptiview Chiller
Control Upgrade
Determine Potential Cold Spring Load at the Intercooler
Support Brackets (ISB) on DIV II Standby Diesel Generator
ERIS upgrade migrates rod scram timing and feedwater
valve position indicator software to new ERIS platform
Use as needed - Change elastomer materials for Fisher
AOV O-rings to Viton
EDG Lube Oil Header Alternate Seal Assembly
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Base EC for Replacement of Parson Peebles Voltage
Regulator
Auxiliary Building Steam Tunnel Floor Plugs Sealant
Alternative
Install Key-Lock Switches on Main Control Room Panels
H13-P691 and H13-P692 to Bypass RHR Loop A and B 135
PSIG Isolations
EC-72704, 2018-
Eliminate Secondary Steam Jet Air Ejector Single Point
Vulnerability by disabling auto-close function or primary
Steam Jet Air Ejector offgas suction valves ARC-AOV1A/B
Parent EC Replacement of obsolete recirculation pump seal
purge supply flow control valve C11-FCVD012A and C11-
FCVD012B
Install Backdraft Dampers to Control Building HVAC System
Install Boron Carbide Aluminum Metal Matrix Composite
Inserts into the Spent Fuel Pool Fuel Storage Racks to
Address Boraflex Degradation
Feedwater Debris Strainer Evaluation and Installation
Feedwater Sparger Nozzle Repairs
EC-79427, 2018-
TRACG Anticipated Operational Occurrences Updates
Temporary Modification to Install an External Oil Reservoir
Near B33-PC001A to Increase Margin to a Low Oil Level
Alarm
Plug Weep Holes in Concrete Duct to G Tunnel
ER-RB-2004-
0307-001
Change elastomer materials for Fisher AOV O-rings to Viton
Engineering
Evaluations
RBS-ME-18-
00001
RBS Air Ejector Isolation Valve Study
Miscellaneous
216.210-085-
010 A
Qualification Report for Trane AdaptiView Chiller Controls
216.210-085-
015 A
Factory Acceptance Test Report for HVK-CHL1D
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
N996-0108
Failure Modes and Effects Analysis (FMEA) for Trane
Adaptiview Chiller Controls
GEH Licensing Topical Report, TRACG Model Description
GEH Licensing Topical Report, TRACG Qualification
GEH Licensing Topical Report, TRACG Application for
Anticipated Operational Occurrences Transient Analyses
OMM-05215515-1 Operation and Maintenance Manual for Adaptiview Chiller
Control Upgrade
RBG-47962
River Bend Station USAR Revision 26, TRM Revision 150,
TS Bases Amendment 196, 10 CFR 50.59 Report, 10 CFR 2.48 Report, and Commitment Change Summary Report
07/26/2019
Procedures
ARP-863-74
P863-74 ALARM RESPONSE
Engineering Change Process
Process Applicability Determination
CFR 50.59 Evaluations
SOP-0031
2
Work Orders
304024
HVK-CHL1A Controls Upgrade
08/22/2019
480654
Install Key-Switch B21H-S79B
04/27/2019
Corrective Action
Documents
CR-RBS-
2019-02335, 2019-02341, 2019-02732, 2019-03058,
2019-03631, 2019-03836, 2019-03836, 2019-04614,
2019-05614, 2019-05635, 2019-05635, 2019-06210,
2019-06260, 2019-06494, 2020-00022, 2020-01845,
20-03041, 2020-03070, 2020-03165, 2020-03714,
20-04931, 2020-05346, 2020-05360, 2020-05484,
21-00198, 2021-00970
Miscellaneous
RF-21 Refuel Floor Work Plan
2/08/2021
CZT Isotope Analysis of highly radioactive item from Cavity
2/23/2021
Procedures
Radiation Worker Expectations
Access Control for Radiologically Controlled Areas
Radiological Control
Radiological Work Permits
Radiation Protection Posting
Air Sampling
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Job Coverage
Radiation Protection Fundamentals Program
Operation and Maintenance of HEPA Vacuum Cleaners and
HEPA Ventilation Units
Radiation
Surveys
Fuel Building 113' Quarterly Survey
01/19/2021
Refuel Floor Survey Reactor Building 186'
01/21/2021
Residual Heat Removal "A" Quarterly Survey
01/22/2021
Routine Quarterly Survey
01/22/2021
Refuel Cavity Post-Decontamination Survey Reactor
Building 186'
2/21/2021
Drywell 125/141 Post-Shielding survey of E21-VF007
2/22/2021
Dose Rate Investigation
2/25/2021
Survey of Piping below E12-AOVF041A
2/25/2021
RBS-AS-011321-
0053
Auxiliary Building 95' RWCU Vacuum Plate cut out and
removal
01/13/2021
RBS-AS-012921-
0159
Reactor Building 186' Inside tend during Strongback
decontamination
01/28/2021
RBS-AS-062519-
26
Fuel Building 113' Decontamination of Channel Grapple tool
06/25/2019
RBS-AS-100919-
22
Fuel Building 70' Work Area Air Sample
10/08/2019
RBS-AS-121420-
219
Reactor Building 162' Control Room Validation
2/14/2020
Radiation Work
Permits (RWPs)
21-1606
Radwaste, Shipping, and Decontamination Activities in
LHRA/HRA. Except Drywell.
21-1800
Refuel Floor Reactor Vessel Disassembly and Reassembly
Activities
21-1901
Radiation Protection Drywell Activities
Self-Assessments LO-RLO-2019-
00029
RP Pre-NRC Focused Self-Assessment Radiation Safety
Inspection: IP 71124.01 - Radiological Hazard Assessment
and Exposure Controls, IP 71124.03 - In-Plant Airborne
Radioactivity Control and Mitigation, and IP 71151-OR01 -
Occupational Exposure Control Effectiveness
01/08/2020
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
LO-RLO-2019-
00076
RP Pre-NRC Focused Self-Assessment Radiation Safety
Inspection: IP 71124.01 - Radiological Hazard Assessment
and Exposure Controls, IP 71124.02 - Occupational ALARA
Planning and Controls, and IP 71152 - Problem Identification
and Resolution
11/09/2020
QA-14/15-2019-
RBS-1
Combined Radiation Protection and Radwaste
10/28/2019
ALARA Plans
RWP 2021-1235
ALARA Plan: Replace LWS-SP3 (Oil Plate Separator)
Internal Discharge Hose
RWP 2021-1235
ALARA Plan: Replace LWS-SP3 (Oil Plate Separator)
Internal Discharge Hose
RWP 2021-1800
ALARA Plan: Medium/High Risk Radioiodine Exposure
During Reactor Vessel Disassembly
RWP 2021-
1800/2021-1801
Refuel-21 Upper Pool Activities on Reactor Building 186'
Refuel Floor
RWP 2021-1936
Shielding Activities in the Drywell
Corrective Action
Documents
CR-RBS-
2019-02450, 2019-02834, 2019-04197, 2019-04680,
2019-04825, 2019-05191, 2019-06944, 2020-00518,
20-01751, 2020-03156, 2020-03295, 2020-03300,
20-03718
Miscellaneous
Daily Radiation Protection Outage Report - Refueling
Outage 21
2/23/2021
Procedures
Radiation Work Permits
Radiological Survey Documentation
EN-RP-106-01
Radiological Survey Documentation
ALARA Program
EN-RP-110-02
Elemental Cobalt Sampling
EN-RP-110-04
Collective Radiation Exposure (CRE) Reduction Guidelines
EN-RP-110-04
Radiation Protection Risk Assessment Process
EN-RP-110-06
Outage Dose Estimating and Tracking
EN-RP-141-01
Job Coverage Using Remote Monitoring Technology
EN-RP-141-02
Discrete Radioactive Particle Control
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Self-Assessments LO-RLO-2019-
00076
RP Pre-NRC Focused Self-Assessment Radiation Safety
Inspection: IP 71124.01 - Radiological Hazard Assessment
and Exposure Controls, IP 71124.02 - Occupational ALARA
Planning and Controls, and IP 71152 - Problem Identification
and Resolution
11/09/2020
LO-RLO-2019-
00076
RP Pre-NRC Focused Self-Assessment Radiation Safety
Inspection: IP 71124.01 - Radiological Hazard Assessment
and Exposure Controls, IP 71124.02 - Occupational ALARA
Planning and Controls, and IP 71152 - Problem Identification
and Resolution
11/09/2020
Corrective Action
Documents
CR-RBS-
2019-01783, 2019-01828, 2019-02157, 2019-02427
2019-03245, 2019-03829, 2019-04386, 2019-04323
2019-05360, 2019-05379, 2019-05569, 2019-06495
2019-06508, 2019-06545, 2020-02537, 2020-02764
20-03642
Procedures
Air Sampling
Operation and Maintenance of HEPA Vacuum Cleaners and
HEPA Ventilation Units
Respiratory Protection Program
Inspection and Maintenance of Respiratory Protection
Equipment
Selection, Issue and Use of Respiratory Protection
Equipment
Breathing Air
PortaCount Respirator Fit Testing
STP-402-0201
Main Control Room A/C Train A Operability Test
STP-402-0202
Main Control Room A/C Train B Operability Test
STP-402-3601
Inservice Testing of Division 1 Control Room Fresh Air
System
307
STP-402-8604
Division 1 Main Control Room Fresh Air System Laboratory
Carbon Filter Analysis
STP-402-8605
Division 2 Main Control Room Fresh Air System Laboratory
Carbon Filter Analysis
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
STP-511-4210
RMS-Control Room Fresh Air System Radiation Monitor
Remote Intake Channel Functional Test
STP-511-4212
RMS-Control Room Fresh Air System Radiation Monitor
Remote Intake Channel Calibration
STP-511-4510
RMS-Control Room Fresh Air System Radiation Monitor
Remote Intake Channel Functional Test
STP-511-4511
RMS-Control Room Fresh Air System Radiation Monitor
Remote Intake Channel Functional Test
303
STP-511-4512
RMS-Control Room Fresh Air System Radiation Monitor
Remote Intake Channel Functional Test
305
Self-Assessments EN-LI-104
Self-Assessment and Benchmark Process
QA-14/15-2019-
RBS-1
QA Audit Report: Combined Radiation Protection and
Radwaste
10/28/2019
71151
Corrective Action
Documents
CR-RBS-
20109-02316, 2019-02322, 2019-03213, 2020-01845,
20-03041
Work Orders
WO 52948729-01 RPP-0097: Manual Method of Determining Cumulative Dose
Contributions from Liquid Effluents: October 1, 2020 -
November 1, 2020
11/19/2020
RPP-0102: Dose Calculation from Gaseous Effluents:
October 1, 2020 - November 1, 2020,
11/19/2020
RPP-0097: Manual Method of Determining Cumulative Dose
Contributions from Liquid Effluents: November 1, 2020 -
December 1, 2020
2/17/2020
RPP-0102: Dose Calculation from Gaseous Effluents:
November 1, 2020 - December 1, 2020
2/17/2020
RPP-0097: Manual Method of Determining Cumulative Dose
Contributions from Liquid Effluents: December 1, 2020 -
January 1, 2021
01/15/2021
RPP-0102: Dose Calculation from Gaseous Effluents:
December 1, 2020 - January 1, 2020
01/15/2021
Corrective Action
Documents
CR-RBS-
2018-00633, 2021-00153
Corrective Action
Documents
CR-RBS-
2010-06061, 2012-07746, 2020-03497
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Procedures
Thermal Hydraulic Stability Controls
Corrective Action Process
Corrective Action Process
GOP-0004
Single Loop Operations
28