IR 05000482/2016002: Difference between revisions

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| number = ML16218A501
| number = ML16218A501
| issue date = 08/03/2016
| issue date = 08/03/2016
| title = Wolf Creek Generating Station - NRC Integrated Inspection Report 05000482/2016002
| title = NRC Integrated Inspection Report 05000482/2016002
| author name = Taylor N H
| author name = Taylor N
| author affiliation = NRC/RGN-IV
| author affiliation = NRC/RGN-IV
| addressee name = Heflin A C
| addressee name = Heflin A
| addressee affiliation = Wolf Creek Nuclear Operating Corp
| addressee affiliation = Wolf Creek Nuclear Operating Corp
| docket = 05000482
| docket = 05000482
Line 18: Line 18:


=Text=
=Text=
{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION REGION IV 1600 E. LAMAR BLVD.
{{#Wiki_filter:UNITED STATES ust 3, 2016


ARLINGTON, TX 76011-4511 August 3, 2016 Adam C. Heflin, President and Chief Executive Officer Wolf Creek Nuclear Operating Corporation P.O. Box 411
==SUBJECT:==
WOLF CREEK GENERATING STATION - NRC INTEGRATED INSPECTION REPORT 05000482/2016002


Burlington, KS 66839
==Dear Mr. Heflin:==
On June 30, 2016, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Wolf Creek Generating Station. On July 27, 2016, the NRC inspectors discussed the results of this inspection with Cleveland Reasoner, Site Vice President, and other members of your staff. Inspectors documented the results of this inspection in the enclosed inspection report.


SUBJECT: WOLF CREEK GENERATING STATION - NRC INTEGRATED INSPECTION REPORT 05000482/2016002
NRC inspectors documented one finding of very low safety significance (Green) in this report.


==Dear Mr. Heflin:==
This finding involved a violation of NRC requirements. Further, inspectors documented five licensee identified violations, which were determined to be of very low safety significance in this report. The NRC is treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2.a of the NRC Enforcement Policy.
On June 30, 2016, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Wolf Creek Generating Station. On July 27, 2016, the NRC inspectors discussed the results of this inspection with Cleveland Reasoner, Site Vice President, and other members of your staff. Inspectors documented the results of this inspection in the enclosed inspection report. NRC inspectors documented one finding of very low safety significance (Green) in this report. This finding involved a violation of NRC requirements. Further, inspectors documented five licensee identified violations, which were determined to be of very low safety significance in this report. The NRC is treating these violations as non
-cited violations (NCVs) consistent with Section 2.3.2
.a of the NRC Enforcement Policy.


If you contest the violations or significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S.
If you contest the violations or significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC resident inspector at the Wolf Creek Generating Station.


Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555
If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region IV and the NRC resident inspector at the Wolf Creek Generating Station.
-0001; and the NRC resident inspector at the Wolf Creek Generating Station. If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region IV and the NRC resident inspector at the Wolf Creek Generating Station. In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, "Public Inspections, Exemptions, Requests for Withholding,"
a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC
's Public Document Room or from the Publicly Available Records (PARS) component of the NRC's Agencywide Document s Access and Management System (ADAMS).


ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading
In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public Inspections, Exemptions, Requests for Withholding, a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRCs Public Document Room or from the Publicly Available Records (PARS) component of the NRC's Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
-rm/adams.html (the Public Electronic Reading Room).


Sincerely,/RA/ Nicholas H. Taylor, Branch Chief Project Branch B Division of Reactor Projects Docket No.: 50-482 License No.: NPF
Sincerely,
-42  
/RA/
Nicholas H. Taylor, Branch Chief Project Branch B Division of Reactor Projects Docket No.: 50-482 License No.: NPF-42


===Enclosure:===
===Enclosure:===
Inspection Report 05000482/2016002 w/ Attachment s: 1.Supplemental Information2.Request for Information for the OccupationalRadiation Safety Inspection
Inspection Report 05000482/2016002 w/ Attachments:
 
1. Supplemental Information 2. Request for Information for the O
SUNSI Review By: NTaylor ADAMS Yes No Non-Sensitive Sensitive Publicly Available Non-Publicly Available OFFICE SRI/DRP/B RI/DRP/B C:DRS/PSB2 C:DRS/EB1 C: DRS/EB2 TL/DRS/IPAT NAME DDodson FThomas RDeese TFarnholtz GWerner THipschman SIGNATURE /RA/ /RA/ /RA/ /RA/ /RA/ /RA/ DATE 8/2/16 8/2/16 8/1/16 8/1/2016 7/29/16 7/29/16 OFFICE C:DRS/OB C:DRP/B NAME JKirkland NTaylor SIGNATURE /RA/ /RA/ DATE 8/1/16 8/3/16 Letter to Adam from Nicholas H. Taylor dated August 3, 2016


SUBJECT: WOLF CREEK GENERATING STATION
REGION IV==
- NRC INTEGRATED INSPECTION REPORT 05000482/2016002 DISTRIBUTION
Docket: 05000482 License: NPF-42 Report: 05000482/2016002 Licensee: Wolf Creek Nuclear Operating Corporation Facility: Wolf Creek Generating Station Location: 1550 Oxen Lane NE Burlington, KS 66839 Dates: April 1 through June 30, 2016 Inspectors: D. Dodson, Senior Resident Inspector F. Thomas, Resident Inspector L. Carson II, Senior Health Physicist J. Drake, Senior Reactor Inspector N. Greene, PhD, Health Physicist P. Hernandez, Health Physicist M. Phalen, Senior Health Physicist D. Proulx, Senior Project Engineer W. Sifre, Senior Reactor Inspector C. Stott, Reactor Inspector Approved Nicholas H. Taylor By: Chief, Project Branch B Division of Reactor Projects-1- Enclosure 1
: Regional Administrator (Kriss.Kennedy@nrc.gov)
Deputy Regional Administrator (Scott.Morris@nrc.gov) DRP Director (Troy.Pruett@nrc.gov)
DRP Deputy Director (Ryan.Lantz@nrc.gov)
DRS Director (Anton.Vegel@nrc.gov)
DRS Deputy Director (Jeff.Clark@nrc.gov)
Senior Resident Inspector (Douglas.Dodson@nrc.gov)
Resident Inspector (Fabian.Thomas@nrc.gov)
Administrative Assistant (Susan.Galemore@nrc.gov)
Branch Chief, DRP/B (Nick.Taylor@nrc.gov)
Senior Project Engineer, DRP/B (David.Proulx@nrc.gov)
Project Engineer, DRP/B (Shawn.Money@nrc.gov)
Project Engineer, DRP/B (Steven.Janicki@nrc.gov)
Public Affairs Officer (Victor.Dricks@nrc.gov
) Project Manager (Fred.Lyon@nrc.gov)
Team Leader, DRS/TSS (Thomas.Hipschman@nrc.gov)
RITS Coordinator (Marisa.Herrera@nrc.gov)
ACES (R4Enforcement.Resource@nrc.gov)
Regional Counsel (Karla.Fuller@nrc.gov)
Technical Support Assistant (Loretta.Williams@nrc.gov)
Congressional Affairs Officer (Jenny.Weil@nrc.gov)
RIV Congressional Affairs Officer (Angel.Moreno@nrc.gov)
RIV/ETA: OEDO (Jeremy.Bowen@nrc.gov)
RIV RSLO (Bill.Maier@nrc.gov)
ACES (R4Enforcement.Resource@nrc.gov)
ROPreports.Resource@nrc.gov ROPassessment.Resource@nrc.gov
 
-1- Enclosure 1 U.S. NUCLEAR REGULATORY COMMISSION REGION IV Docket: 05000 482 License: NPF-42 Report: 05000 482/20 16 0 02 Licensee: Wolf Creek Nuclear Operating Corporation Facility: Wolf Creek Generating Station Location: 1550 Oxen Lane NE Burlington, KS 66839 Dates: April 1 through June 30, 2016 Inspectors:
D. Dodson, Senior Resident Inspector F. Thomas, Resident Inspector L. Carson II, Senior Health Physicist J. Drake, Senior Reactor Inspector N. Greene, PhD, Health Physicist P. Hernandez, Health Physicist M. Phalen, Senior Health Physicist D. Proulx, Senior Project Engineer W. Sifre, Senior Reactor Inspector C. Stott, Reactor Inspector Approved By: Nicholas H. Taylor Chief, Project Branch B Division of Reactor Projects  


=SUMMARY=
=SUMMARY=
IR 05000 482/2016002; 04/01/2016
IR 05000482/2016002; 04/01/2016 - 06/30/2016; Wolf Creek Generating Station; Follow-up of


- 06/30/2016
Events and Notices of Enforcement The inspection activities described in this report were performed between April 1 and June 30, 2016, by the resident inspectors at Wolf Creek Generating Station and inspectors from the NRCs Region IV office. One finding of very low safety significance (Green) is documented in this report. This finding involved a violation of NRC requirements. Additionally, NRC inspectors documented in this report five licensee-identified violations of very low safety significance. The significance of inspection findings is indicated by their color (Green, White, Yellow, or Red),
; Wolf Creek Generating Station
which is determined using Inspection Manual Chapter 0609, Significance Determination Process. Their cross-cutting aspects are determined using Inspection Manual Chapter 0310,
; Follow-up of Events and Notices of Enforcement The inspection activities described in this report were performed between April 1 and June 30, 2016 , by the resident inspectors at Wolf Creek Generating Station and inspectors from the NRC's Region IV office. One finding of very low safety significance (Green) is documented in this report.
Aspects within the Cross-Cutting Areas. Violations of NRC requirements are dispositioned in accordance with the NRC Enforcement Policy. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process.
 
This finding involved a violation of NRC requirements. Additionally, NRC inspectors documented in this report five license e-identified violations of very low safety significance. The significance of inspection findings is indicated by their color (Green, White, Yellow, or Red),
which is determined using Inspection Manual Chapter 0609, "Significance Determination Process.Their cross-cutting aspects are determined using Inspection Manual Chapter 0310, "Aspects within the Cross-Cutting Areas.Violations of NRC requirements are dispositioned in accordance with the NRC Enforcement Policy.
 
The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG
-1649, "Reactor Oversight Process."


===Cornerstone: Mitigating Systems===
===Cornerstone: Mitigating Systems===
: '''Green.'''
: '''Green.'''
The inspectors identified a Green non-cited violation of Technical Specification Limiting Condition for Operation 3.7.11 and 3.0.3 for the licensee's failure to place the unit in mode 3 within 7 hours, mode 4 within 13 hours, and mode 5 within 37 hours with two trains (SGK04A and SGK04B) of the control room air conditioning system (CRACS) inoperable. Specifically, the licensee failed to adequately establish CRACS testing flow rate acceptance criteria, which resulted in train A of the safety-related CRACS being inoperable from October 11, 2005, to August 13, 2013; and train B being inoperable from October 3, 2002, to July 18, 2013.
The inspectors identified a Green non-cited violation of Technical Specification Limiting Condition for Operation 3.7.11 and 3.0.3 for the licensees failure to place the unit in mode 3 within 7 hours, mode 4 within 13 hours, and mode 5 within 37 hours with two trains (SGK04A and SGK04B) of the control room air conditioning system (CRACS)inoperable. Specifically, the licensee failed to adequately establish CRACS testing flow rate acceptance criteria, which resulted in train A of the safety-related CRACS being inoperable from October 11, 2005, to August 13, 2013; and train B being inoperable from October 3, 2002, to July 18, 2013. The licensees immediate corrective actions included corrective maintenance on the CRACS to increase the airflow to meet acceptance criteria limits. Condition Report 105208 was initiated by the licensee for any necessary process changes and extent of condition actions.


The licensee's immediate corrective actions included corrective maintenance on the CRACS to increase the airflow to meet acceptance criteria limits. Condition Report 105208 was initiated by the licensee for any necessary process changes and extent of condition actions.
This finding is more than minor because it is associated with the equipment performance attribute of the Mitigating Systems Cornerstone, and affected the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). The inspectors utilized Inspection Manual Chapter 0609.04, Initial Characterization of Findings, and Exhibit 2 of Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, and determined this finding was not a deficiency affecting the design or qualification of a mitigating SSC that maintained its operability or functionality, the finding did not represent a loss of system and/or function, the finding did not represent an actual loss of function of at least a single train for greater than its Technical Specification allowed outage time, and the finding did not represent an actual loss of function of one or more non-Technical Specification trains of equipment designated as high safety-significant. Therefore, the inspectors determined the finding was of very low safety significance (Green). The finding has a cross-cutting aspect in the area of human performance, change management, because leaders did not use a systematic process for evaluating and implementing change so that nuclear safety remains the overriding priority. Specifically, there is not currently a formal process for procedure writers to consider measurement uncertainty when establishing and changing testing acceptance criteria, which resulted in extended inoperability of both the SGK04A and SGK04B units following significant changes to Technical Specifications that included adding surveillance requirements for the SGK04A and SGK04B units in 1999. This issue is indicative of current performance because the same issue would be expected to occur today [H.3]. (Section 4OA3)


This finding is more than minor because it is associated with the equipment performance attribute of the Mitigating Systems Cornerstone, and affected the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage).
===Licensee-Identified Violations===


The inspectors utilized Inspection Manual Chapter 0609.04, "Initial Characterization of Findings," and Exhibit of Inspection Manual Chapter 0609, Appendix A, "The Significance Determination Process (SDP) for Findings At-Power," and determined this finding was not a deficiency affecting the design or qualification of a mitigating SSC that maintained its operability or functionality, the finding did not represent a loss of system and/or function, the finding did not represent an actual loss of function of at least a single train for greater than its Technical Specification allowed outage time, and the finding did not represent an actual loss of function of one or more non-Technical Specification trains of equipment designated as high safety-significant. Therefore, the inspectors determined the finding was of very low safety significance (Green). The finding has a cross-cutting aspect in the area of human performance, change management, because leaders did not use a systematic process for evaluating and implementing change so that nuclear safety remains the overriding priority. Specifically, there is not currently a formal process for procedure writers to consider measurement uncertainty when establishing and changing testing acceptance criteria, which resulted in extended inoperability of both the SGK04A and SGK04B units following significant changes to Technical Specifications that included adding surveillance requirements for the SGK04A and SGK04B units in 1999.
Five violations of very low safety significance that were identified by the licensee have been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. These violations and associated corrective action tracking numbers are listed in Section 4OA7 of this report.


This issue is indicative of current performance because the same issue would be expected to occur today
=PLANT STATUS=
[H.3].  (Section 4OA3)


===  Licensee-Identified Violations===
Wolf Creek Generating Station operated at or near full power for the entire inspection period.


Five violations of very low safety significance that were identified by the licensee ha ve been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensee's corrective action program.
REPORT DETAILS
 
These violation s and associated corrective action tracking numbers are listed in Section 4OA7 of this report.
 
=PLANT STATUS=
 
Wolf Creek Generating Station operated at or near full power for the entire inspection period. REPORT DETAILS


==REACTOR SAFETY==
==REACTOR SAFETY==
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity 1 R 01 Adverse Weather Protection (71111.01)
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity {{a|1R01}}
==1R01 Adverse Weather Protection==
{{IP sample|IP=IP 71111.01}}
Readiness for Impending Adverse Weather Conditions
Readiness for Impending Adverse Weather Conditions


====a. Inspection Scope====
====a. Inspection Scope====
On April 26, 2016, the inspectors completed an inspection of the station's readiness for impending adverse weather conditions. The inspectors reviewed plant design features, the licensee's procedures to respond to severe thunderstorms and tornado watch es, and the licensee's planned implementation of these procedures. The inspectors evaluated operator staffing and accessibility of controls and indications for those systems required to control the plant.
On April 26, 2016, the inspectors completed an inspection of the stations readiness for impending adverse weather conditions. The inspectors reviewed plant design features, the licensees procedures to respond to severe thunderstorms and tornado watches, and the licensees planned implementation of these procedures. The inspectors evaluated operator staffing and accessibility of controls and indications for those systems required to control the plant.


These activities constituted one sample of readiness for impending adverse weather conditions, as defined in Inspection Procedure 71111.01.
These activities constituted one sample of readiness for impending adverse weather conditions, as defined in Inspection Procedure 71111.01.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R04}}
 
==1R04 Equipment Alignment==
1 R 04 Equipment Alignment (71111.04)
{{IP sample|IP=IP 71111.04}}
Partial Walk
Partial Walk-Down
-Down


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors performed partial system walk
The inspectors performed partial system walk-downs of the following risk-significant systems:
-downs of the following risk
* April 28, 2016, control room air conditioning unit B
-significant systems:   April 28, 2016, control room air conditioning unit B May 18, 2016, component cooling water pump B May 25, 2016, emergency diesel generator B June 7, 2016, component cooling water pump D The inspectors reviewed the licensee's procedures and system design information to determine the correct lineup for the systems. They visually verified that critical portions of the systems were correctly aligned for the existing plant configuration.
* May 18, 2016, component cooling water pump B
* May 25, 2016, emergency diesel generator B
* June 7, 2016, component cooling water pump D The inspectors reviewed the licensees procedures and system design information to determine the correct lineup for the systems. They visually verified that critical portions of the systems were correctly aligned for the existing plant configuration.


These activities constituted four partial system walk
These activities constituted four partial system walk-down samples as defined in Inspection Procedure 71111.04.
-down sample s as defined in Inspection Procedure 71111.04.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R05}}
 
==1R05 Fire Protection==
1 R 05 Fire Protection (71111.05)
{{IP sample|IP=IP 71111.05}}
 
===.1 Quarterly Inspection===
===.1 Quarterly Inspection===


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors evaluated the licensee's fire protection program for operational status and material condition. The inspectors focused their inspection on four plant areas important to safety:
The inspectors evaluated the licensees fire protection program for operational status and material condition. The inspectors focused their inspection on four plant areas important to safety:
May 25, 2016 , fire area F-1 , general floor area, elevation 2047 feet   May 31, 2016 , fire area A-15, auxiliary feedwater pump room C, elevation 2000 feet   June 17, 2016 , fire area A-27 , motor generator set room, elevation 2026 feet   June 29, 2016, fire area ESW
* May 25, 2016, fire area F-1, general floor area, elevation 2047 feet
-1, essential service water pump house A train , elevation 2000 feet For each area, the inspectors evaluated the fire plan against defined hazards and defense-in-depth features in the licensee's fire protection program. The inspectors evaluated control of transient combustibles and ignition sources, fire detection and suppression systems, manual firefighting equipment and capability, passive fire protection features, and compensatory measures for degraded conditions.
* May 31, 2016, fire area A-15, auxiliary feedwater pump room C, elevation 2000 feet
* June 17, 2016, fire area A-27, motor generator set room, elevation 2026 feet
* June 29, 2016, fire area ESW-1, essential service water pump house A train, elevation 2000 feet For each area, the inspectors evaluated the fire plan against defined hazards and defense-in-depth features in the licensees fire protection program. The inspectors evaluated control of transient combustibles and ignition sources, fire detection and suppression systems, manual firefighting equipment and capability, passive fire protection features, and compensatory measures for degraded conditions.


These activities constituted four quarterly inspection samples, as defined in Inspection Procedure 71111.05.
These activities constituted four quarterly inspection samples, as defined in Inspection Procedure 71111.05.
Line 160: Line 117:


====a. Inspection Scope====
====a. Inspection Scope====
On June 24, 2015, the inspectors completed their annual evaluation of the licensee's fire brigade performance. This evaluation included observation of an unannounced fire drill for a fire in the north end of the auxiliary building, elevation 1974 feet (A
On June 24, 2015, the inspectors completed their annual evaluation of the licensees fire brigade performance. This evaluation included observation of an unannounced fire drill for a fire in the north end of the auxiliary building, elevation 1974 feet (A-1), on June 24, 2016.
-1), on June 24, 2016. During this drill, the inspectors evaluated the capability of the fire brigade members, the leadership ability of the brigade leader, the brigade's use of turnout gear and fire
 
-fighting equipment, and the effectiveness of the fire brigade's team operation. The inspectors also reviewed whether the licensee's fire brigade met NRC requirements for training, dedicated size and membership, and equipment.
During this drill, the inspectors evaluated the capability of the fire brigade members, the leadership ability of the brigade leader, the brigades use of turnout gear and fire-fighting equipment, and the effectiveness of the fire brigades team operation. The inspectors also reviewed whether the licensees fire brigade met NRC requirements for training, dedicated size and membership, and equipment.


These activities constituted one annual inspection sample, as defined in Inspection Procedure 71111.05.
These activities constituted one annual inspection sample, as defined in Inspection Procedure 71111.05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R07}}
 
==1R07 Heat Sink Performance==
1 R 07 Heat Sink Performance (71111.07)
{{IP sample|IP=IP 71111.07}}
 
===.1 Annual Review===
===.1 Annual Review===


====a. Inspection Scope====
====a. Inspection Scope====
On April 5, 2016, the inspectors completed an inspection of the readiness and availability of risk-significant heat exchangers. The inspectors observed the licensee's inspection of the SGK04B control room air
On April 5, 2016, the inspectors completed an inspection of the readiness and availability of risk-significant heat exchangers. The inspectors observed the licensees inspection of the SGK04B control room air-conditioning unit heat exchanger and the material condition of the heat exchanger internals. Additionally, the inspectors walked down the SGK04B heat exchanger to observe its performance and material condition and verified that the SGK04B heat exchanger was correctly categorized under the Maintenance Rule and was receiving the required maintenance.
-conditioning unit heat exchanger and the material condition of the heat exchanger internals.
 
Additionally, the inspectors walked down the SGK04B heat exchanger to observe its performance and material condition and verified that the SGK04B heat exchanger was correctly categorized under the Maintenance Rule and was receiving the required maintenance.


These activities constituted completion of one heat sink performance annual review sample, as defined in Inspection Procedure 71111.07.
These activities constituted completion of one heat sink performance annual review sample, as defined in Inspection Procedure 71111.07.
Line 187: Line 140:


====a. Inspection Scope====
====a. Inspection Scope====
On May 23, 2016 , through May 26, 2016, the inspectors completed an inspection of the readiness and availability of risk
On May 23, 2016, through May 26, 2016, the inspectors completed an inspection of the readiness and availability of risk-significant heat exchangers. The inspectors reviewed licensee programs to verify heat exchanger performance and operability for the following heat exchangers:
-significant heat exchangers. The inspectors reviewed licensee programs to verify heat exchanger performance and operability for the following heat exchangers:
* Component cooling water heat exchanger A
Component cooling water heat exchanger A Containment air cooler A Air compressor and aftercooler B Fuel pool cooling pump room cooler B Class 1E switchgear cooler A The inspectors verified whether testing, inspection, maintenance, and chemistry control programs are adequate to ensure proper heat transfer. The inspectors verified that the periodic testing and monitoring methods, as outlined in commitments to NRC Generic Letter 89-13, utilized proper industry heat exchanger guidance. Additionally, the inspectors verified that the licensee's chemistry program ensured that biological fouling was properly controlled between tests. The inspectors reviewed previous maintenance records of the heat exchangers to verify that the licensee's heat exchanger inspections adequately addressed structural integrity and cleanliness of their tubes.
* Containment air cooler A
* Air compressor and aftercooler B
* Fuel pool cooling pump room cooler B
* Class 1E switchgear cooler A The inspectors verified whether testing, inspection, maintenance, and chemistry control programs are adequate to ensure proper heat transfer. The inspectors verified that the periodic testing and monitoring methods, as outlined in commitments to NRC Generic Letter 89-13, utilized proper industry heat exchanger guidance. Additionally, the inspectors verified that the licensees chemistry program ensured that biological fouling was properly controlled between tests. The inspectors reviewed previous maintenance records of the heat exchangers to verify that the licensees heat exchanger inspections adequately addressed structural integrity and cleanliness of their tubes.


These activities constitute completion of five triennial heat sink inspection samples as defined in Inspection Procedure 71111.07-05.
These activities constitute completion of five triennial heat sink inspection samples as defined in Inspection Procedure 71111.07-05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R08}}
{{a|1R08}}
==1R08 Inservice Inspection Activities==
==1R08 Inservice Inspection Activities==
{{IP sample|IP=IP 71111.08}}
{{IP sample|IP=IP 71111.08}}


====a. Inspection Scope====
====a. Inspection Scope====
This inspection was focused on closing an Unresolved Item (URI) opened during the performance of Inspection Procedure 71111.08, "Inservice Inspection Activities," documented in NRC Inspection Report 05000482/
This inspection was focused on closing an Unresolved Item (URI) opened during the performance of Inspection Procedure 71111.08, Inservice Inspection Activities, documented in NRC Inspection Report 05000482/2015001. The inspectors reviewed additional licensing basis information provided by the licensee, as well as industry standards and regulatory guidance. Information in Section 4OA5 of this report documents the resolution of this URI.
2015001. The inspectors reviewed additional licensing basis information provided by the licensee, as well as industry standards and regulatory guidance.
 
Information in Section
{{a|4OA5}}
==4OA5 of this report documents the resolution of this URI.==


====b. Findings====
====b. Findings====
No findings were identified. 1 R 11 Licensed Operator Requalification Program and Licensed Operator Performance (71111.11)
No findings were identified. {{a|1R11}}
 
==1R11 Licensed Operator Requalification Program and Licensed Operator Performance==
{{IP sample|IP=IP 71111.11}}
===.1 Review of Licensed Operator Requalification===
===.1 Review of Licensed Operator Requalification===


====a. Inspection Scope====
====a. Inspection Scope====
On May 16, 2014, the inspectors observed an evaluated simulator scenario performed by an operating crew. The inspectors assessed the performance of the operators and the evaluators' critique of their performance. The inspectors also assessed the modeling and performance of the simulator during the requalification activities
On May 16, 2014, the inspectors observed an evaluated simulator scenario performed by an operating crew. The inspectors assessed the performance of the operators and the evaluators critique of their performance. The inspectors also assessed the modeling and performance of the simulator during the requalification activities.
.
 
These activities constituted completion of one quarterly licensed operator requalification program sample, as defined in Inspection Procedure 71111.11.
These activities constituted completion of one quarterly licensed operator requalification program sample, as defined in Inspection Procedure 71111.11.


Line 223: Line 174:


====a. Inspection Scope====
====a. Inspection Scope====
On June 1, 2016, the inspectors observed the performance of on
On June 1, 2016, the inspectors observed the performance of on-shift licensed operators in the plants main control room. At the time of the observations, the plant was in a period of heightened risk due to the ongoing performance of STS IC-508A, Refueling Water Storage Tank Level Transmitter Calibration, Revision 6; during two previous performances of the same procedure on May 19 and 26, 2016, the station received a reactor partial trip alarm concurrent with a low steam line pressure bistable trip.
-shift licensed operators in the plant's main control room. At the time of the observations, the plant was in a period of heightened risk due to the ongoing performance of STS IC
-508A, "Refueling Water Storage Tank Level Transmitter Calibration," Revision 6; during two previous performances of the same procedure on May 19 and 26, 2016, the station received a reactor partial trip alarm concurrent with a low steam line pressure bistable trip.


In addition, the inspectors assessed the operators' adherence to plant procedures, including the conduct of operations procedure and other operations department policies.
In addition, the inspectors assessed the operators adherence to plant procedures, including the conduct of operations procedure and other operations department policies.


These activities constitute d completion of one quarterly licensed operator performance sample, as defined in Inspection Procedure 71111.11.
These activities constituted completion of one quarterly licensed operator performance sample, as defined in Inspection Procedure 71111.11.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R12}}
 
==1R12 Maintenance Effectiveness==
1 R 12 Maintenance Effectiveness (71111.12)
{{IP sample|IP=IP 71111.12}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed one instance of degraded performance or condition of safety
The inspectors reviewed one instance of degraded performance or condition of safety-related structures, systems, and components (SSCs):
-related structures, systems, and components (SSCs):
* March 10, 2016, SKG04A and SGK04B control room air conditioning units, refrigerant leaks The inspectors reviewed the extent of condition of possible common cause SSC failures and evaluated the adequacy of the licensees corrective actions. The inspectors reviewed the licensees work practices to evaluate whether these may have played a role in the degradation of the SSCs. The inspectors assessed the licensees characterization of the degradation in accordance with 10 CFR 50.65 (the Maintenance Rule), and verified that the licensee was appropriately tracking degraded performance and conditions in accordance with the Maintenance Rule.
March 1 0, 2016, SKG04A and SGK04B control room air conditioning units, refrigerant leaks The inspectors reviewed the extent of condition of possible common cause SSC failures and evaluated the adequacy of the licensee's corrective actions. The inspectors reviewed the licensee's work practices to evaluate whether these may have played a role in the degradation of the SSCs. The inspectors assessed the licensee's characterization of the degradation in accordance with 10 CFR 50.65 (the Maintenance Rule), and verified that the licensee was appropriately tracking degraded performance and conditions in accordance with the Maintenance Rule.


These activities constituted completion of one maintenance effectiveness sample, as defined in Inspection Procedure 71111.12.
These activities constituted completion of one maintenance effectiveness sample, as defined in Inspection Procedure 71111.12.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R13}}
 
==1R13 Maintenance Risk Assessments and Emergent Work Control==
1 R 13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
{{IP sample|IP=IP 71111.13}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed two risk assessments performed by the licensee prior to changes in plant configuration and the risk management actions taken by the licensee in response to elevated risk:
The inspectors reviewed two risk assessments performed by the licensee prior to changes in plant configuration and the risk management actions taken by the licensee in response to elevated risk:
April 28, 2106, planned maintenance on control room air conditioning unit A   May 25, 2016, planned maintenance outage s for emergency diesel generator A and essential service water system A
* April 28, 2106, planned maintenance on control room air conditioning unit A
The inspectors verified that these risk assessment s were performed timely and in accordance with the requirements of 10 CFR 50.65 (the Maintenance Rule) and plant procedures. The inspectors reviewed the accuracy and completeness of the licensee's risk assessment s and verified that the licensee implemented appropriate risk management actions based on the result s of the assessment s.
* May 25, 2016, planned maintenance outages for emergency diesel generator A and essential service water system A The inspectors verified that these risk assessments were performed timely and in accordance with the requirements of 10 CFR 50.65 (the Maintenance Rule) and plant procedures. The inspectors reviewed the accuracy and completeness of the licensees risk assessments and verified that the licensee implemented appropriate risk management actions based on the results of the assessments.


The inspectors also observed portions of two emergent work activities that had the potential to cause an initiating event and to affect the functional capability of mitigating systems:   April 12, 2016, repair of Benton 345 kilovolt offsite power line support structure May 23, 2016, maintenance on emergency diesel generator A channel 1 undervoltage bistable power supply The inspectors verified that the licensee appropriately developed and followed a work plan for these activities. The inspectors verified that the licensee took precautions to minimize the impact of the work activities on unaffected SSCs.
The inspectors also observed portions of two emergent work activities that had the potential to cause an initiating event and to affect the functional capability of mitigating systems:
* April 12, 2016, repair of Benton 345 kilovolt offsite power line support structure
* May 23, 2016, maintenance on emergency diesel generator A channel 1 undervoltage bistable power supply The inspectors verified that the licensee appropriately developed and followed a work plan for these activities. The inspectors verified that the licensee took precautions to minimize the impact of the work activities on unaffected SSCs.


These activities constitute d completion of four maintenance risk assessments and emergent work control inspection sample s, as defined in Inspection Procedure 71111.13.
These activities constituted completion of four maintenance risk assessments and emergent work control inspection samples, as defined in Inspection Procedure 71111.13.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R15}}
 
==1R15 Operability Determinations and Functionality Assessments==
1 R 15 Operability Determinations and Functionality Assessments (71111.15)
{{IP sample|IP=IP 71111.15}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed three operability determinations and functionality assessments that the licensee performed for degraded or nonconforming SSCs:
The inspectors reviewed three operability determinations and functionality assessments that the licensee performed for degraded or nonconforming SSCs:
April 25, 2016, operability determination of essential service water pump discharge check valves and cross
* April 25, 2016, operability determination of essential service water pump discharge check valves and cross-connect check valves
-connect check valves May 5, 2016, operability determination of essential service water pump B discharge check valve June 7, 2016, functionality determination of diesel fire pump The inspectors reviewed the timeliness and technical adequacy of the licensee's evaluations. Where the licensee determined the degraded SSC to be operable or functional, the inspectors verified that the licensee's compensatory measures were appropriate to provide reasonable assurance of operability or functionality. The inspectors verified that the licensee had considered the effect of other degraded conditions on the operability or functionality of the degraded SSC.
* May 5, 2016, operability determination of essential service water pump B discharge check valve
* June 7, 2016, functionality determination of diesel fire pump The inspectors reviewed the timeliness and technical adequacy of the licensees evaluations. Where the licensee determined the degraded SSC to be operable or functional, the inspectors verified that the licensees compensatory measures were appropriate to provide reasonable assurance of operability or functionality. The inspectors verified that the licensee had considered the effect of other degraded conditions on the operability or functionality of the degraded SSC.


These activities constitute d completion of three operability and functionality review sample s as defined in Inspection Procedure 71111.15.
These activities constituted completion of three operability and functionality review samples as defined in Inspection Procedure 71111.15.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R19}}
 
==1R19 Post-Maintenance Testing==
1 R 19 Post-Maintenance Testing (71111.19)
{{IP sample|IP=IP 71111.19}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed five post-maintenance testing activities that affected risk
The inspectors reviewed five post-maintenance testing activities that affected risk-significant SSCs:
-significant SSCs:
* April 6, 2016, SGK04B control room air conditioning unit
April 6, 2016 , SGK04B control room a ir conditioning unit   April 21, 2016, shutdown rod bank E demand counter May 3, 2016, emergency diesel generator B emergency fuel oil storage tank level indicator replacement May 19, 2016, steam line low pressure bistable card replacement May 31, 2016, turbine driven auxiliary feedwater pump test The inspectors reviewed licensing- and design
* April 21, 2016, shutdown rod bank E demand counter
-basis documents for the SSCs and the maintenance and post
* May 3, 2016, emergency diesel generator B emergency fuel oil storage tank level indicator replacement
-maintenance test procedures. The inspectors observed the performance of the post
* May 19, 2016, steam line low pressure bistable card replacement
-maintenance tests to verify that the licensee performed the tests in accordance with approved procedures, satisfied the established acceptance criteria, and restored the operability of the affected SSCs.
* May 31, 2016, turbine driven auxiliary feedwater pump test The inspectors reviewed licensing- and design-basis documents for the SSCs and the maintenance and post-maintenance test procedures. The inspectors observed the performance of the post-maintenance tests to verify that the licensee performed the tests in accordance with approved procedures, satisfied the established acceptance criteria, and restored the operability of the affected SSCs.


These activities constitute d completion of five post-maintenance testing inspection sample s, as defined in Inspection Procedure 71111.19.
These activities constituted completion of five post-maintenance testing inspection samples, as defined in Inspection Procedure 71111.19.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R22}}
 
==1R22 Surveillance Testing==
1 R 22 Surveillance Testing (71111.22)
{{IP sample|IP=IP 71111.22}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors observed six risk-significant surveillance tests and reviewed test results to verify that these tests adequately demonstrated that the SSCs were capable of performing their safety functions:
The inspectors observed six risk-significant surveillance tests and reviewed test results to verify that these tests adequately demonstrated that the SSCs were capable of performing their safety functions:
In-service tests:
In-service tests:
May 5, 2016, STS EF
* May 5, 2016, STS EF-100B, [Essential Service Water] System Inservice Pump B
-100B, "[Essential Service Water] System Inservice Pump B & [Essential Service Water] B Check Valve Test," Revision 47 June 1, 2016
              & [Essential Service Water] B Check Valve Test, Revision 47
, STS AL-201C, "Turbine Driven Auxiliary Feedwater System Inservice Valve Test," Revision 9 Containment isolation valve surveillance tests:
* June 1, 2016, STS AL-201C, Turbine Driven Auxiliary Feedwater System Inservice Valve Test, Revision 9 Containment isolation valve surveillance tests:
April 11, 2016 , STS BM-205, "[Steam Generator Blowdown]
* April 11, 2016, STS BM-205, "[Steam Generator Blowdown] System Inservice Valve Test, Revision 13 Reactor coolant system leak detection tests:
System Inservice Valve Test," Revision 13 Reactor coolant system leak detection tests:
* May 4, 2016, STS BB-006, [Reactor Coolant System] Water Inventory Balance Using the NPIS Computer, Revision 14 Other surveillance tests:
May 4, 2016 , STS BB-006, "[Reactor Coolant System]
* April 7, 2016, STS GG-001B, Emergency Exhaust Filtration System Train B Operability Test, Revision 23
Water Inventory Balance Using the NPIS Computer," Revision 14 Other surveillance tests:
* May 12, 2016, STS IC-255B, Channel Operational Test Control Room Air Intake Radiation Monitor, Revision 16A The inspectors verified that these tests met technical specification requirements, that the licensee performed the tests in accordance with their procedures, and that the results of the test satisfied appropriate acceptance criteria. The inspectors verified that the licensee restored the operability of the affected SSCs following testing.
April 7, 2016 , STS GG-001B, "Emergency Exhaust Filtration System Train B Operability Test," Revision 23 May 12, 20 16 , STS IC-255B, "Channel Operational Test Control Room Air Intake Radiation Monitor," Revision 16A The inspectors verified that these tests met technical specification requirements, that the licensee performed the tests in accordance with their procedures, and that the results of the test satisfied appropriate acceptance criteria. The inspectors verified that the licensee restored the operability of the affected SSCs following testing.


These activities constitute d completion of six surveillance testing inspection sample s, as defined in Inspection Procedure 71111.22.
These activities constituted completion of six surveillance testing inspection samples, as defined in Inspection Procedure 71111.22.


====b. Findings====
====b. Findings====
Line 307: Line 257:


==RADIATION SAFETY==
==RADIATION SAFETY==
Cornerstones: Public Radiation Safety and Occupational Radiation Safety
Cornerstones: Public Radiation Safety and Occupational Radiation Safety {{a|2RS5}}
{{a|2RS5}}
==2RS5 Radiation Monitoring Instrumentation==
==2RS5 Radiation Monitoring Instrumentation==
{{IP sample|IP=IP 71124.05}}
{{IP sample|IP=IP 71124.05}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors evaluated the accuracy and operability of the radiation monitoring equipment used by the licensee to monitor areas, materials, and workers to ensure a radiologically safe work environment. This evaluation included equipment used to monitor radiological conditions related to normal plant operations, anticipated operational occurrences, and conditions resulting from postulated accidents. The inspectors interviewed licensee personnel, walked down various portions of the plant, and reviewed licensee performance associated with radiation monitoring instrumentation, as described below:   The inspectors performed walk downs and observations of selected plant radiation monitoring equipment and instrumentation, including portable survey instruments, area radiation monitors, continuous air monitors, personnel contamination monitors, portal monitors, and small article monitors. The inspectors assessed material condition and operability, evaluated positioning of instruments relative to the radiation sources or areas they were intended to monitor, and verified performance of source checks and calibrations
The inspectors evaluated the accuracy and operability of the radiation monitoring equipment used by the licensee to monitor areas, materials, and workers to ensure a radiologically safe work environment. This evaluation included equipment used to monitor radiological conditions related to normal plant operations, anticipated operational occurrences, and conditions resulting from postulated accidents. The inspectors interviewed licensee personnel, walked down various portions of the plant, and reviewed licensee performance associated with radiation monitoring instrumentation, as described below:
.
* The inspectors performed walk downs and observations of selected plant radiation monitoring equipment and instrumentation, including portable survey instruments, area radiation monitors, continuous air monitors, personnel contamination monitors, portal monitors, and small article monitors. The inspectors assessed material condition and operability, evaluated positioning of instruments relative to the radiation sources or areas they were intended to monitor, and verified performance of source checks and calibrations.
 
* The inspectors evaluated the calibration and testing program, including laboratory instrumentation, whole body counters, post-accident monitoring instrumentation, portal monitors, personnel contamination monitors, small article monitors, portable survey instruments, area radiation monitors, electronic dosimetry, air samplers, and continuous air monitors.
The inspectors evaluated the calibration and testing program, including laboratory instrumentation , whole body counters , post-accident monitoring instrumentation, portal monitors, personnel contamination monitors, small article monitors , portable survey instruments, area radiation monitors , electronic dosimetry , air samplers, and continuous air monitors
* The inspectors assessed problem identification and resolution for radiation monitoring instrumentation. The inspectors reviewed audits, self-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution.
.
 
The inspectors assessed problem identification and resolution for radiation monitoring instrumentation. The inspectors reviewed audits, self
-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution.


These activities constituted completion of the three required samples of radiation monitoring instrumentation, as defined in Inspection Procedure 71124.05.
These activities constituted completion of the three required samples of radiation monitoring instrumentation, as defined in Inspection Procedure 71124.05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|2RS6}}
{{a|2RS6}}
==2RS6 Radioactive Gaseous and Liquid Effluent Treatment==
==2RS6 Radioactive Gaseous and Liquid Effluent Treatment==
{{IP sample|IP=IP 71124.06}}
{{IP sample|IP=IP 71124.06}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors evaluated whether the licensee maintained gaseous and liquid effluent processing systems and properly mitigated, monitored, and evaluated radiological discharges with respect to public exposure. The inspectors verified that abnormal radioactive gaseous or liquid discharges and conditions, when effluent radiation monitors are out-of-service, were controlled in accordance with the applicable regulatory requirements and licensee procedures. The inspectors verified that the licensee's quality control program ensured radioactive effluent sampling and analysis adequately quantified and evaluated discharges of radioactive materials. The inspectors verified the adequacy of public dose projections resulting from radioactive effluent discharges. The inspectors interviewed licensee personnel and reviewed licensee performance in the following areas:
The inspectors evaluated whether the licensee maintained gaseous and liquid effluent processing systems and properly mitigated, monitored, and evaluated radiological discharges with respect to public exposure. The inspectors verified that abnormal radioactive gaseous or liquid discharges and conditions, when effluent radiation monitors are out-of-service, were controlled in accordance with the applicable regulatory requirements and licensee procedures. The inspectors verified that the licensees quality control program ensured radioactive effluent sampling and analysis adequately quantified and evaluated discharges of radioactive materials. The inspectors verified the adequacy of public dose projections resulting from radioactive effluent discharges. The inspectors interviewed licensee personnel and reviewed licensee performance in the following areas:
During walk downs and observations of selected portions of the radioactive gaseous and liquid effluent equipment, the inspectors evaluated routine processing and discharge of effluents, including sample collection and analysis. The inspectors observed equipment configuration and flow paths of selected gaseous and liquid discharge system components , effluent monitoring systems, filtered ventilation system material condition, and significant changes to effluent release points.
* During walk downs and observations of selected portions of the radioactive gaseous and liquid effluent equipment, the inspectors evaluated routine processing and discharge of effluents, including sample collection and analysis.
 
Calibration and testing program for process and effluent monitors, including National Institute of Standards and Technology (NIST) traceability of sources , primary and secondary calibration data, channel calibrations, set-point determination bases, and surveillance test results.
 
Sampling and analysis controls used to ensure representative sampling and appropriate compensatory sampling. Reviews included results of the inter
-laboratory comparison program
.
 
Instrumentation and equipment, including effluent flow measuring instruments, air cleaning systems, and post
-accident effluent monitoring instruments.


Dose calculations for effluent releases. The inspectors reviewed a selection of radioactive liquid and gaseous waste discharge permits and abnormal gaseous or liquid tank discharges, and verified the projected doses were accurate. The inspectors also reviewed 10 CFR Part 61 analyses and methods used to determine which isotopes were included in the source term. The inspectors reviewed land use census results, offsite dose calculation manual changes, and significant changes in reported dose values from previous years.
The inspectors observed equipment configuration and flow paths of selected gaseous and liquid discharge system components, effluent monitoring systems, filtered ventilation system material condition, and significant changes to effluent release points.
* Calibration and testing program for process and effluent monitors, including National Institute of Standards and Technology (NIST) traceability of sources, primary and secondary calibration data, channel calibrations, set-point determination bases, and surveillance test results.
* Sampling and analysis controls used to ensure representative sampling and appropriate compensatory sampling. Reviews included results of the inter-laboratory comparison program.
* Instrumentation and equipment, including effluent flow measuring instruments, air cleaning systems, and post-accident effluent monitoring instruments.
* Dose calculations for effluent releases. The inspectors reviewed a selection of radioactive liquid and gaseous waste discharge permits and abnormal gaseous or liquid tank discharges, and verified the projected doses were accurate. The inspectors also reviewed 10 CFR Part 61 analyses and methods used to determine which isotopes were included in the source term. The inspectors reviewed land use census results, offsite dose calculation manual changes, and significant changes in reported dose values from previous years.
* Problem identification and resolution for radioactive gaseous and liquid effluent treatment. The inspectors reviewed audits, self-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution.


Problem identification and resolution for radioactive gaseous and liquid effluent treatment. The inspectors reviewed audits, self
These activities constituted completion of the six required samples of radioactive gaseous and liquid effluent treatment program, as defined in Inspection Procedure 71124.06.
-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution.
 
These activities constitute d completion of the six required samples of radioactive gaseous and liquid effluent treatment program, as defined in Inspection Procedure 7112 4.0 6.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|2RS7}}
{{a|2RS7}}
==2RS7 Radiological Environmental Monitoring Program==
==2RS7 Radiological Environmental Monitoring Program==
{{IP sample|IP=IP 71124.07}}
{{IP sample|IP=IP 71124.07}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors evaluated whether the licensee's radiological environmental monitoring program quantified the impact of radioactive effluent releases to the environment and sufficiently validate d the integrity of the radioactive gaseous and liquid effluent release program. The inspectors also verified that the licensee continued to implement the voluntary Nuclear Energy Institute/Industry Ground Water Protection Initiative. The inspectors reviewed or observed the following items:
The inspectors evaluated whether the licensees radiological environmental monitoring program quantified the impact of radioactive effluent releases to the environment and sufficiently validated the integrity of the radioactive gaseous and liquid effluent release program. The inspectors also verified that the licensee continued to implement the voluntary Nuclear Energy Institute/Industry Ground Water Protection Initiative. The inspectors reviewed or observed the following items:
The inspectors observed selected air sampling and dosimeter monitoring stations , sampler station modifications, and the collection and preparation of environmental samples. The inspectors reviewed calibration and maintenance records for selected air samplers , composite water samplers, and environmental sample radiation measurement instrumentation, and inter-laboratory comparison program results. The inspectors reviewed selected events documented in the annual environmental monitoring report and significant changes made by the licensee to the offsite dose calculation manual as the result of changes to the land census. The inspectors evaluated the operability, calibration, and maintenance of meteorological instruments and assessed the meteorological dispersion and deposition factors. The inspectors verified the licensee had implemented a sampling and monitoring program sufficient to detect leakage from SSCs with credible mechanism for licensed material to reach ground water and reviewed changes to the licensee's written program for identifying and controlling contaminated spills/leaks to groundwater
* The inspectors observed selected air sampling and dosimeter monitoring stations, sampler station modifications, and the collection and preparation of environmental samples. The inspectors reviewed calibration and maintenance records for selected air samplers, composite water samplers, and environmental sample radiation measurement instrumentation, and inter-laboratory comparison program results. The inspectors reviewed selected events documented in the annual environmental monitoring report and significant changes made by the licensee to the offsite dose calculation manual as the result of changes to the land census. The inspectors evaluated the operability, calibration, and maintenance of meteorological instruments and assessed the meteorological dispersion and deposition factors. The inspectors verified the licensee had implemented a sampling and monitoring program sufficient to detect leakage from SSCs with credible mechanism for licensed material to reach ground water and reviewed changes to the licensees written program for identifying and controlling contaminated spills/leaks to groundwater.
.
* Groundwater protection initiative implementation, including assessment of groundwater monitoring results, identified leakage or spill events and entries made into 10 CFR 50.75(g) records, licensee evaluations of the extent of the contamination and the radiological source term, and reports of events associated with spills, leaks, and groundwater monitoring results.
* Problem identification and resolution for the radiological environmental monitoring program. The inspectors reviewed audits, self-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution.


Groundwater protection initiative implementation, including assessment of groundwater monitoring results
These activities constituted completion of the three required samples of radiological environmental monitoring program, as defined in Inspection Procedure 71124.07.
, identified leakage or spill events and entries made into 10 CFR 50.75(g) records , licensee evaluations of the extent of the contamination and the radiological source term
, and reports of events associated with spills, leaks, and groundwater monitoring results.
 
Problem identification and resolution for the radiological environmental monitoring program. The inspectors reviewed audits, self
-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution. These activities constitute d completion of the three required sample s of radiological environmental monitoring program
, as defined in Inspection Procedure 71124.0 7.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.
{{a|2RS8}}
{{a|2RS8}}
==2RS8 Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and Transportation==
==2RS8 Radioactive Solid Waste Processing and Radioactive Material Handling, Storage,==
{{IP sample|IP=IP 71124.08}}
 
and Transportation (71124.08)


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors evaluated the effectiveness of the licensee
The inspectors evaluated the effectiveness of the licensees programs for processing, handling, storage, and transportation of radioactive material. The inspectors interviewed licensee personnel and reviewed the following items:
's programs for processing, handling, storage, and transportation of radioactive material.
* Radioactive material storage waste storage areas including container labeling/marking and monitoring containers for deformation or signs of waste decomposition.
* Radioactive waste system walk-down including radioactive waste processing and handling equipment. Review of waste processing equipment that is not operational or abandoned in place equipment consistent with system descriptions and the process control program.
* Waste characterization and classification including radio-chemical sample analysis results for radioactive waste streams and use of scaling factors and calculations to account for difficult-to-measure radionuclides, processes for waste classification including use of scaling factors and 10 CFR Part 61 analysis.
* Shipment preparation packaging, surveying, labeling, marking, placarding, vehicle checking, driver instructing, and preparation of the disposal manifests.
* Shipping records including for LSAI, II, III; SCOI, II: Type A or Type B records.
* Problem identification and resolution for radioactive solid waste processing and radioactive material handling, storage, and transportation. The inspectors reviewed audits, self-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution.


The inspectors interviewed licensee personnel and reviewed the following items:
These activities constituted completion of the six required samples of radioactive solid waste processing and radioactive material handling, storage, and transportation program, as defined in Inspection Procedure 71124.08.
Radioactive material storage waste storage areas including container labeling/marking and monitoring containers for deformation or signs of waste decomposition
.
 
Radioactive waste system walk-down including radioactive waste processing and handling equipment. Review of waste processing equipment that is not operational or abandoned in place equipment consistent with system descriptions and the process control program
.
 
Waste characterization and classification including radio-chemical sample analysis results for radioactive waste streams and use of scaling factors and calculations to account for difficult
-to-measure radionuclides, processes for waste classification including use of scaling factors and 10 CFR Part 61 analysis
.
 
Shipment preparation packaging, surveying, labeling, marking, placarding, vehicle checking, driver instructing, and preparation of the disposal manifest s.
 
Shipping records including for LSAI, II, III; SCOI, II: Type A or Type B records.
 
Problem identification and resolution for radioactive solid waste processing and radioactive material handling, storage, and transportation. The inspectors reviewed audits, self
-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution.
 
These activities constitute d completion of the six required samples of radioactive solid waste processing and radioactive material handling, storage, and transportation program, as defined in Inspection Procedure 71124.08.


====b. Findings====
====b. Findings====
Line 403: Line 322:


==OTHER ACTIVITIES==
==OTHER ACTIVITIES==
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Security 4OA 1 Performance Indicator Verification (71151)
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Security
 
{{a|4OA1}}
==4OA1 Performance Indicator Verification==
{{IP sample|IP=IP 71151}}
===.1 Reactor Coolant System Specific Activity (BI01)===
===.1 Reactor Coolant System Specific Activity (BI01)===


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the licensee's reactor coolant system chemistry sample analyses for the period of April 1, 2015, through March 31, 2016, to verify the accuracy and completeness of the reported data. The inspectors observed a chemistry technician obtain and analyze a reactor coolant system sample on June 1 3, 2016. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, to determine the accuracy of the reported data.
The inspectors reviewed the licensees reactor coolant system chemistry sample analyses for the period of April 1, 2015, through March 31, 2016, to verify the accuracy and completeness of the reported data. The inspectors observed a chemistry technician obtain and analyze a reactor coolant system sample on June 13, 2016. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported data.


These activities constituted verification of the reactor coolant system specific activity performance indicator, as defined in Inspection Procedure 71151.
These activities constituted verification of the reactor coolant system specific activity performance indicator, as defined in Inspection Procedure 71151.
Line 418: Line 339:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the licensee's records of reactor coolant system identified leakage for the period of April 1, 2015, through March 31, 2016, to verify the accuracy and completeness of the reported data. The inspectors observed the performance of STS BB-006, "RCS Water Inventory Balance Using t he NPSI Computer," Revision 14, on June 24, 2016.
The inspectors reviewed the licensees records of reactor coolant system identified leakage for the period of April 1, 2015, through March 31, 2016, to verify the accuracy and completeness of the reported data. The inspectors observed the performance of STS BB-006, RCS Water Inventory Balance Using the NPSI Computer, Revision 14, on June 24, 2016. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported data.


The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, to determine the accuracy of the reported data. These activities constituted verification of the reactor coolant system leakage performance indicator, as defined in Inspection Procedure 71151.
These activities constituted verification of the reactor coolant system leakage performance indicator, as defined in Inspection Procedure 71151.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|4OA2}}
 
==4OA2 Problem Identification and Resolution==
4OA 2 Problem Identification and Resolution (71152)
{{IP sample|IP=IP 71152}}
 
===.1 Routine Review===
===.1 Routine Review===


====a. Inspection Scope====
====a. Inspection Scope====
Throughout the inspection period, the inspectors performed daily reviews of items entered into the licensee's corrective action program and periodically attended the licensee's condition report screening meetings. The inspectors verified that licensee personnel were identifying problems at an appropriate threshold and entering these problems into the corrective action program for resolution. The inspectors verified that the licensee developed and implemented corrective actions commensurate with the significance of the problems identified. The inspectors also reviewed the licensee's problem identification and resolution activities during the performance of the other inspection activities documented in this report.
Throughout the inspection period, the inspectors performed daily reviews of items entered into the licensees corrective action program and periodically attended the licensees condition report screening meetings. The inspectors verified that licensee personnel were identifying problems at an appropriate threshold and entering these problems into the corrective action program for resolution. The inspectors verified that the licensee developed and implemented corrective actions commensurate with the significance of the problems identified. The inspectors also reviewed the licensees problem identification and resolution activities during the performance of the other inspection activities documented in this report.


====b. Findings====
====b. Findings====
Line 438: Line 358:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the licensee's corrective action program, performance indicators, station performance reports, and other documentation to identify trends that might indicate the existence of a more significant safety issue. The inspectors verified that the licensee was taking corrective actions to address the following identified adverse trends:   Procedure use and adherence Operability evaluations These activities constitute d completion of one semiannual trend review sample, as defined in Inspection Procedure 71152.
The inspectors reviewed the licensees corrective action program, performance indicators, station performance reports, and other documentation to identify trends that might indicate the existence of a more significant safety issue. The inspectors verified that the licensee was taking corrective actions to address the following identified adverse trends:
* Procedure use and adherence
* Operability evaluations These activities constituted completion of one semiannual trend review sample, as defined in Inspection Procedure 71152.


b. Observations and Assessments The inspectors evaluated a sample of issues and events that occurred over the course of the past two quarters to determine whether issues were appropriately considered as emerging or adverse trends. The inspectors verified that these issues were addressed within the scope of the corrective action program or through department review and documentation in the quarterly trend presentation for overall assessment.
b. Observations and Assessments The inspectors evaluated a sample of issues and events that occurred over the course of the past two quarters to determine whether issues were appropriately considered as emerging or adverse trends. The inspectors verified that these issues were addressed within the scope of the corrective action program or through department review and documentation in the quarterly trend presentation for overall assessment.


The inspectors identified issues associated with implementation of Procedure AP 15C
The inspectors identified issues associated with implementation of Procedure AP 15C-002, Procedure Use and Adherence:
-002, "Procedure Use and Adherence:"
* The inspectors identified six separate issues associated with implementation of Procedure AP 15C-002, Procedure Use and Adherence, Revision 41, during one test. Section 6.1.2, for continuous use procedures, states, Review and placekeep each step after completion to ensure the step was performed correctly, and Each step of a continuous use procedure shall be completed or properly N/Ad before proceeding to the next step. On May 5, 2016, the inspectors observed activities associated with completion of Procedure STS EF-100B, [Essential Service Water] System Inservice Pump B & [Essential Service Water] B Check Valve Test, Revision 47, and noted six separate issues associated with the licensee reviewing and placekeeping each step after completion to ensure the step was performed correctly, and the licensee ensuring each step of the continuous use procedure was completed or properly N/Ad before proceeding to the next step. Specifically, Step 8.2.3.3 was inappropriately marked as N/A; Steps 8.2.23.3 and 8.2.23.4 were not performed correctly due to transposition and recording errors; Step 8.2.24.1 utilized an incorrect pressure value; and Step 8.1.17 data was recorded with a unit error. None of these six separate issues were identified by the implementing operations crew or during the operations crew review of the procedure. These issues were entered into the corrective action program as Condition Report 104532.
The inspectors identified six separate issues associated with implementation of Procedure AP 15C
* The inspectors identified that Procedure AP 15C-002, Procedure Use and Adherence, Revision 41, Section 6.1.2, for continuous use procedures, states, Perform the step as written in the sequence specified, except when the procedure or approved process specifically allows deviation. On June 1, 2016, the inspectors observed activities associated with completion of Procedure STS IC-508A, Refueling Water Storage Tank Level Transmitter Calibration, Revision 6, and noted that steps were not performed as written in the sequence specified, and the approved process did not specifically allow deviation.
-002, "Procedure Use and Adherence," Revision 41, during one test. Section 6.1.2, for continuous use procedures, states, "Review and placekeep each step after completion to ensure the step was performed correctly," and "Each step of a continuous use procedure shall be completed or properly N/A'd before proceeding to the next step.On May 5, 2016, the inspectors observed activities associated with completion of Procedure STS EF-100B, "[Essential Service Water] System Inservice Pump B & [Essential Service Water] B Check Valve Test," Revision 47, and noted six separate issues associated with the licensee reviewing and placekeeping each step after completion to ensure the step was performed correctly, and the licensee ensuring each step of the continuous use procedure was completed or properly "N/A'd" before proceeding to the next step. Specifically, Step 8.2.3.3 was inappropriately marked as "N/A;"
Steps 8.2.23.3 and 8.2.23.4 were not performed correctly due to transposition and recording errors; Step 8.2.24.1 utilized an incorrect pressure value; and Step 8.1.17 data was recorded with a unit error. None of these s ix separate issues were identified by the implementing operations crew or during the operations crew review of the procedure. These issues were entered into the corrective action program as Condition Report 104532.


The inspectors identified that Procedure AP 15C
Specifically, personnel did not recognize the need to document supervisor approval to re-perform an as-found data collection step. This issue was entered into the corrective action program as Condition Report 105566.
-002, "Procedure Use and Adherence," Revision 41, Section 6.1.2, for continuous use procedures, states, "Perform the step as written in the sequence specified, except when the procedure or approved process specifically allows deviation."  On June 1, 2016, the inspectors observed activities associated with completion of Procedure STS IC-508A, "Refueling Water Storage Tank Level Transmitter Calibration," Revision 6, and noted that steps were not performed as written in the sequence specified, and the approved process did not specifically allow deviation. Specifically, personnel did not recognize the need to document supervisor approval to re
-perform an as
-found data collection step. This issue was entered into the corrective action program as Condition Report 105566.


The inspectors discussed the issues associated with following Procedure AP 15C
The inspectors discussed the issues associated with following Procedure AP 15C-002, Procedure Use and Adherence, at the exit meeting on July 27, 2016. The licensee documented Condition Report 106079 in response to the inspectors observations.
-002, "Procedure Use and Adherence," at the exit meeting on July 27, 2016. The licensee documented Condition Report 106079 in response to the inspectors' observations.


The inspectors noted that NRC Inspection Report 05000482/2015004 documented an apparent increase in the number of operability evaluation issues. The inspectors observed apparent station improvement in this area as a result of actions associated with Condition Report 96033, increased control room oversight, and periodic operability determination training. Although operability process implementation improvement was recognized by the inspectors, the inspectors noted some continuing NRC
The inspectors noted that NRC Inspection Report 05000482/2015004 documented an apparent increase in the number of operability evaluation issues. The inspectors observed apparent station improvement in this area as a result of actions associated with Condition Report 96033, increased control room oversight, and periodic operability determination training. Although operability process implementation improvement was recognized by the inspectors, the inspectors noted some continuing NRC-identified issues. Specifically, these included:
-identified issues. Specifically, these included:
* The inspectors identified that Procedure AP 26C-004, Determination and Functionality Assessment, Revision 32, states that operability determinations should include whether there is a reasonable expectation of operability, including the basis for the determination and any compensatory measures put in place to establish or restore operability. This procedure was not adequately implemented on two occasions in response to Condition Reports 104268 and 104066. Neither Condition Report 104268 nor Condition Report 104066 adequately addressed operability concerns associated with the emergency diesel generator fuel oil transfer pump control circuitrys potential to activate the thermal overloads that would stop the pump and render the emergency diesel generator inoperable; NCV 05000482/2016007-02, Failure to Verify the Adequacy of Design of the Control Circuitry of the Fuel Oil Transfer Pumps, documents additional details concerning the technical issue. Specifically, the immediate operability screening for both conditions reports was determined to be, N/A, and failed to evaluate the issue for immediate operability. Although an immediate operability determination was not immediately completed, the licensee revised its operability screening, completed an immediate operability determination, and adequately justified operability. This issue was entered into the corrective action program as Condition Report 104322.
The inspectors identified that Procedure AP 26C
* The licensee identified that the operability determination associated with Condition Report 104910 was inadequately completed. Specifically, a negative trend in B component cooling water pump outboard bearing oil leakage rate was identified, and the operability determination did not quantify the leakage rate and compare that to the mission time specified in AP 26C-004, Operability Screening, Revision 32. After additional information from engineering was received and quantification of the oil leakage rate was completed, the operability determination was changed to Inoperable. A licensee identified violation documented in Section 4OA7 of this report discusses this issue.
-004, "Determination and Functionality Assessment," Revision 32, states that operability determinations should include "whether there is a reasonable expectation of operability , including the basis for the determination and any compensatory measures put in place to establish or restore operability.This procedure was not adequately implemented on two occasions in response to Condition Reports 104268 and 104066. Neither Condition Report 104268 nor Condition Report 104066 adequately addressed operability concerns associated with the emergency diesel generator fuel oil transfer pump control circuitry's potential to activate the thermal overloads that would stop the pump and render the emergency diesel generator inoperable; NCV 05000482/20 16007-02, "Failure to Verify the Adequacy of Design of the Control Circuitry of the Fuel Oil Transfer Pumps," documents additional details concerning the technical issue. Specifically, the immediate operability screening for both conditions reports was determined to be, "N/A," and failed to evaluate the issue for immediate operability. Although an immediate operability determination was not immediately completed, the licensee revised its operability screening, completed an immediate operability determination , and adequately justified operability. This issue was entered into the corrective action program as Condition Report 104322.
* The inspectors identified that operability evaluations were not always completed in a timely manner while additional information was being gathered to justify operability. Specifically, completion of operability evaluations associated with the 2016 Component Design Basis team inspection and issues associated with resident inspector activities were sometimes delayed to prevent burdening Operations with unanswered questions during operability screenings. Also, operability determinations for issues associated with resident inspector activities and questions were apparently delayed while additional analyses were performed to justify operability. Specifically, following inspector questions that identified issues associated with a penetration into a safety related area, an operability determination and condition report appeared to be delayed to facilitate completion of analysis that could be used to justify operability. Condition Report 105307 documented the inspectors concerns.


The licensee identified that the operability determination associated with Condition Report 104910 was inadequately completed. Specifically, a negative trend in B component cooling water pump outboard bearing oil leakage rate was identified, and the operability determination did not quantify the leakage rate and compare that to the mission time specified in AP 26C
The inspectors discussed the continuing operability process issues at the exit meeting on July 27, 2016. The licensee documented Condition Report 106062 to address continuing operability process issues.
-004, "Operability Screening," Revision 32. After additional information from engineering was received and quantification of the oil leakage rate was completed, the operability determination was changed to "Inoperable."  A licensee identified violation documented in Section
{{a|4OA7}}
==4OA7 of this report discusses this issue.==
 
The inspectors identified that operability evaluations were not always completed in a timely manner while additional information was being gathered to justify operability. Specifically, completion of operability evaluations associated with the 2016 Component Design Basis team inspection and issues associated with resident inspector activities were sometimes delayed to prevent burdening Operations with unanswered questions during operability screenings. Also, operability determinations for issues associated with resident inspector activities and questions were apparently delayed while additional analyses were performed to justify operability. Specifically, following inspector questions that identified issues associated with a penetration into a safety related area, an operability determination and condition report appeared to be delayed to facilitate completion of analysis that could be used to justify operability.
 
Condition Report 105307 documented the inspectors' concerns.
 
The inspectors discussed the continuing operability process issues at the exit meeting on July 27, 2016. The licensee documented Condition Report 106062 to address continuing operability process issues
.


====c. Findings====
====c. Findings====
No findings were identified.
No findings were identified. {{a|4OA3}}
 
==4OA3 Follow-up of Events and Notices of Enforcement Discretion==
4OA 3 Follow-up of Events and Notices of Enforcement Discretion (71153)
{{IP sample|IP=IP 71153}}
 
===.1 (Closed) Licensee Event Report (LER) 05000482/2014-001-00: Failure to Comply with===
===.1 (Closed) Licensee Event Report (LER) 05000482/2014===


00:  Failure to Comply with Required Action of Technical Spec ification 3.4.3 while Performing a Vacuum Fill of the Reactor Coolant System During a review of outside operating experience on January 6, 2014, the licensee determined that the reactor coolant system pressure was placed in a vacuum cond ition, in violation of Technical Specification 3.4.3
Required Action of Technical Specification 3.4.3 while Performing a Vacuum Fill of the Reactor Coolant System During a review of outside operating experience on January 6, 2014, the licensee determined that the reactor coolant system pressure was placed in a vacuum condition, in violation of Technical Specification 3.4.3, which specifies a minimum operating pressure of 0 psig. Wolf Creek operators drew a vacuum on the reactor coolant system to support reactor coolant system filling operations on May 8, 2011, and March 30, 2013, using Procedure SYS BB-112, Vacuum Fill of the RCS (to approximately 20 inches of Hg, absolute pressure). Technical Specification 3.4.3, [Reactor Coolant System]
, which specifies a minimum operating pressure of 0 psig. Wolf Creek operators drew a vacuum on the reactor coolant system to support reactor coolant system filling operations on May 8, 2011
Pressure and Temperature Limits, requires, in part, that the licensee maintain the reactor coolant system pressure, temperature, and heatup and cooldown rates to the limits specified in the Pressure and Temperature Limits Report (PTLR) at all times. The limits of the curves in the PTLR specify a minimum pressure of 0 psig. Required Action C.1 of Technical Specification 3.4.3 specifies that with the reactor coolant system parameters outside of the limits of the PTLR, restore the parameters to within the limits immediately. Because the plant was outside of the PTLR limits with respect to pressure and not restored immediately, the plant was in a condition prohibited by the Technical Specifications, which is reportable pursuant to 10 CFR 50.73(a)(2)(i)(B).
, and March 30, 2013
, using Procedure SYS BB-112, "Vacuum Fill of the RCS" (to approximately 20 inches of Hg, absolute pressure)
. Technical Specification 3.4.3, "[Reactor Coolant System]
Pressure and Temperature Limits," requires, in part, that the licensee maintain the reactor coolant system pressure, temperature, and heatup and cooldown rates to t he limits specified in the Pressure and Temperature Limits Report (PTLR) at a ll times. The limits of the curves in the PTLR specify a minimum pressure of 0 psig. Required Action C.1 of Technical Specification 3.4.3 specifies that with the reactor coolant system parameters outside of the limits of the PTLR, restore the parameters to within the limits immediately.


Because the plant was outside of the PTLR limits with respect to pressure and not restored immediately, the plant was in a condition prohibited by the Technical Specifications , which is reportable pursuant to 10 CFR 50.73(a)(2)(i)(B).
The licensee placed this issue in the corrective action program as Condition Report 78920. For immediate corrective actions, the licensee cancelled the procedure that implemented vacuum fill of the reactor coolant system. The inspectors determined that this constituted a licensee-identified violation, and the enforcement aspects of this violation are discussed in Section 4OA7 of this inspection report.
 
The licensee placed this issue in the corrective action program as Condition Report 78920. For immediate corrective actions, the licensee cancelled the procedure that implemented vacuum fill of the reactor coolant system. The inspectors determined that this constituted a licensee
-identified violation, and the enforcement aspects of this violation are discussed in Section
{{a|4OA7}}
==4OA7 of this inspection report.==


This licensee event report is closed.
This licensee event report is closed.


===.2 (Closed) LER 05000482/2014===
===.2 (Closed) LER 05000482/2014-004-00: Condition Prohibited by Technical Specifications===


00:  Condition Prohibited by Technical Specifications    due to an Instrument Tunnel Sump Level Indication Transmitter Incompatible with the Containment Environment On June 2, 2014, the licensee determined that the instrument tunnel sump level indication was inoperable from the period of July 13, 2013, to November 20, 2013, due to erratic and unreliable indication. Therefore, the required actions of Technical Specification 3.4.15 "[Reactor Coolant System]
due to an Instrument Tunnel Sump Level Indication Transmitter Incompatible with the Containment Environment On June 2, 2014, the licensee determined that the instrument tunnel sump level indication was inoperable from the period of July 13, 2013, to November 20, 2013, due to erratic and unreliable indication. Therefore, the required actions of Technical Specification 3.4.15 [Reactor Coolant System] Leakage Detection Instrumentation,"
Leakage Detection Instrumentation
were not met. Because the licensee did not take the required actions of Technical Specification 3.4.15, the plant was in a condition prohibited by the Technical Specifications, which is reportable pursuant to 10 CFR 50.73(a)(2)(i)(B). The licensees root cause analysis determined that the local transmitter was not qualified for the long term exposure of the radiation levels encountered in containment, resulting in the erratic indication.
," were not met. Because the licensee did not take the required actions of Technical Specification 3.4.15, the plant was in a condition prohibited by the Technical Specifications , which is reportable pursuant to 10 CFR 50.73(a)(2)(i)(B). The licensee's root cause analysis determined that the local transmitter was not qualified for the long term exposure of the radiation levels encountered in containment, resulting in the erratic indication.


The licensee placed this issue in the corrective action program as Condition Report 84690. For immediate corrective actions, the licensee instituted compensatory measures for alternate means of identifying reactor coolant system leakage. In April 2015 , the licensee replaced the instrument tunnel sump transmitter with two newly designed and fully qualified transmitters, and tested them satisfactorily. The inspectors reviewed the licensee
The licensee placed this issue in the corrective action program as Condition Report 84690. For immediate corrective actions, the licensee instituted compensatory measures for alternate means of identifying reactor coolant system leakage. In April 2015, the licensee replaced the instrument tunnel sump transmitter with two newly designed and fully qualified transmitters, and tested them satisfactorily. The inspectors reviewed the licensees corrective action documents and determined the actions had been completed. The inspectors determined that this constituted a licensee-identified violation, and the enforcement aspects of this violation are discussed in Section 4OA7 of this inspection report.
's corrective action documents and determined the actions had been complete d. The inspectors determined that this constituted a licensee
-identified violation, and the enforcement aspects of this violation are discussed in Section
{{a|4OA7}}
==4OA7 of this inspection report.==


This licensee event report is closed.
This licensee event report is closed.


===.3 (Closed) LER 05000482/2015===
===.3 (Closed) LER 05000482/2015-002-00: Two Control Room Air Conditioning Trains===


0 0:  Two Control Room Air Conditioning Trains Inoperable Due to Failure to Meet Surveillance Requirement, and LER 05000482/2015 01: Two Control Room Air Conditioning Trains Inoperable Due to Failure to Meet Surveillance Requirement
Inoperable Due to Failure to Meet Surveillance Requirement, and LER 05000482/2015-002-01: Two Control Room Air Conditioning Trains Inoperable Due to Failure to Meet Surveillance Requirement


====a. Inspection Scope====
====a. Inspection Scope====
On April 16, 2015, an apparent cause evaluation associated with Condition Report 92274, "Application of SR 3.0.1," identified the potential that the acceptance criteria in Procedures STS PE
On April 16, 2015, an apparent cause evaluation associated with Condition Report 92274, Application of SR 3.0.1, identified the potential that the acceptance criteria in Procedures STS PE-010A, Control Room A/C System Flow Rate Verification A Train, and STS PE-010B, Control Room A/C System Flow Rate Verification B Train, may not have been met when the acceptance criteria was revised on January 3, 2013. The acceptance criteria was revised from greater than 18,360 cubic feet per minute (CFM)and less than 22,440 CFM to a new value of greater than 21,012 CFM, which incorporated instrument uncertainty based on vendor information. The licensee determined that the prior performances of STS PE-010A and STS PE-010B did not meet the new acceptance criteria. Additionally, Procedure STS PE-010B was not performed successfully until July 18, 2013, and Procedure STS PE-010A was not performed successfully until August 13, 2013.
-010A, "Control Room A/C System Flow Rate Verification A Train," and STS PE
 
-010B, "Control Room A/C System Flow Rate Verification B Train," may not have been met when the acceptance criteria was revised on January 3, 2013. The acceptance criteria was revised from greater than 18,360 cubic feet per minute (CFM) and less than 22,440 CFM to a new value of greater than 21,012 CFM, which incorporated instrument uncertainty based on vendor information. The licensee determined that the prior performances of STS PE
The licensee determined that the apparent cause of this event was information in operability evaluation OE-GK-017 that addressed a separate issue on the same equipment, and enabled control room operators and engineering personnel to rationalize the assumption that the change to the acceptance criteria was bounded and did not impact the ability to meet surveillance requirement SR 3.7.11.1.
-010A and STS PE
-010B did not meet the new acceptance criteria. Additionally, Procedure STS PE
-010B was not performed successfully until July 18, 2013, and Procedure STS PE
-010A was not performed successfully until August 13, 2013.


The licensee determined that the apparent cause of this event was information in operability evaluation OE
The licensees immediate corrective actions included performing corrective maintenance on both control room air conditioning system (CRACS) trains to increase the airflow to meet the procedure acceptance criteria, and subsequent performances of Procedures STS PE-010A and STS PE-010B were successful. An adjustable sheave was installed in the B CRACS train in July 2013 and in the A CRACS train in March 2015.
-GK-017 that addressed a separate issue on the same equipment, and enabled control room operators and engineering personnel to rationalize the assumption that the change to the acceptance criteria was bounded and did not impact the ability to meet surveillance requirement SR 3.7.11.1.


The licensee's immediate corrective actions included performing corrective maintenance on both control room air conditioning system (CRACS) trains to increase the airflow to meet the procedure acceptance criteria, and subsequent performances of Procedures STS PE-010A and STS PE
Furthermore, procedure AP 15C-004, Preparation, Review and Approval of Procedures, Instructions and Forms, is being revised to require operations surveillance coordinator review of technical specification surveillance requirement procedures that result in a change in acceptance criteria.
-010B were successful. An adjustable sheave was installed in the B CRACS train in July 2013 and in the A CRACS train in March 2015. Furthermore, procedure AP 15C
-004, "Preparation, Review and Approval of Procedures, Instructions and Forms," is being revised to require operations surveillance coordinator review of technical specification surveillance requirement procedures that result in a change in acceptance criteria.


The licensee event report is closed.
The licensee event report is closed.


====b. Findings====
====b. Findings====
Failure to Adequately Establish Control Room Air Conditioning System Testing Flow Rate Acceptance Criteria
Failure to Adequately Establish Control Room Air Conditioning System Testing Flow   Rate Acceptance Criteria


=====Introduction.=====
=====Introduction.=====
The inspectors identified a Green non-cited violation (NCV) of Technical Specification Limiting Condition for Operation (LCO) 3.7.11 and 3.0.3 for the licensee's failure to place the unit in mode 3 within 7 hours, mode 4 within 13 hours, and mode 5 within 37 hours with two trains (SGK04A and SGK04B) of the CRACS inoperable. Specifically, the licensee failed to adequately establish CRACS testing flow rate acceptance criteria, which resulted in train A of the safety
The inspectors identified a Green non-cited violation (NCV) of Technical Specification Limiting Condition for Operation (LCO) 3.7.11 and 3.0.3 for the licensees failure to place the unit in mode 3 within 7 hours, mode 4 within 13 hours, and mode 5 within 37 hours with two trains (SGK04A and SGK04B) of the CRACS inoperable.
-related CRACS being inoperable from October 11, 2005, to August 13, 2013; and train B being inoperable from October 3, 2002, to July 18, 2013.
 
Specifically, the licensee failed to adequately establish CRACS testing flow rate acceptance criteria, which resulted in train A of the safety-related CRACS being inoperable from October 11, 2005, to August 13, 2013; and train B being inoperable from October 3, 2002, to July 18, 2013.


=====Description.=====
=====Description.=====
Technical Specification LCO 3.7.11, "Control Room Air Conditioning System (CRACS)", states, "Two CRACS trains shall be operable," in modes 1, 2, 3, 4, 5, and 6, and during movement of irradiated fuel assemblies. Technical Specification 3.7.11, Condition B, requires the reactor to be in mode 3 within 6 hours if one train of the CRACS has been inoperable for 30 days. Condition E, requires immediate entry into Technical Specification 3.0.3, if two CRACS trains are inoperable in modes 1, 2, 3, or 4. Technical Specification 3.0.3, requires, in part, that when an LCO is not met and the associated actions are not met, the unit shall be placed in a mode or other specified condition in which the LCO is not applicable. Action shall be initiated within 1 hour to place the unit, as applicable, in mode 3 within 7 hours, mode 4 within 13 hours, and mode 5 within 37 hours.
Technical Specification LCO 3.7.11, Control Room Air Conditioning System (CRACS), states, Two CRACS trains shall be operable, in modes 1, 2, 3, 4, 5, and 6, and during movement of irradiated fuel assemblies. Technical Specification 3.7.11, Condition B, requires the reactor to be in mode 3 within 6 hours if one train of the CRACS has been inoperable for 30 days. Condition E, requires immediate entry into Technical Specification 3.0.3, if two CRACS trains are inoperable in modes 1, 2, 3, or 4.


On December 18, 1999, Wolf Creek Nuclear Operating Corporation implemented license amendment number 123 that converted the Technical Specifications to the improved Technical Specifications. The amendment included new specification 3.7.11, "Control Room Air Conditioning System (CRACS)," and the new surveillance requirement SR 3.7.11.1. SR 3.7.11.1 verifies that the heat removal capabilities of CRACS units SGK04A and SGK04B are adequate to remove the heat load assumed in the control room during design basis accidents. This surveillance requirement consists of verifying the heat removal capability of the condenser heat exchanger, ensuring the proper operation of major components in the refrigeration cycle, verification of unit air flow capacity, and water flow measurement. Station Procedures STS PE
Technical Specification 3.0.3, requires, in part, that when an LCO is not met and the associated actions are not met, the unit shall be placed in a mode or other specified condition in which the LCO is not applicable. Action shall be initiated within 1 hour to place the unit, as applicable, in mode 3 within 7 hours, mode 4 within 13 hours, and mode 5 within 37 hours.
-010A, "Control Room A/C System Flow Rate Verification A Train," and STS PE
 
-010B, "Control Room A/C System Flow Rate Verification B Train," were initially issued on December 18, 1999.
On December 18, 1999, Wolf Creek Nuclear Operating Corporation implemented license amendment number 123 that converted the Technical Specifications to the improved Technical Specifications. The amendment included new specification 3.7.11, Control Room Air Conditioning System (CRACS), and the new surveillance requirement SR 3.7.11.1. SR 3.7.11.1 verifies that the heat removal capabilities of CRACS units SGK04A and SGK04B are adequate to remove the heat load assumed in the control room during design basis accidents. This surveillance requirement consists of verifying the heat removal capability of the condenser heat exchanger, ensuring the proper operation of major components in the refrigeration cycle, verification of unit air flow capacity, and water flow measurement. Station Procedures STS PE-010A, Control Room A/C System Flow Rate Verification A Train, and STS PE-010B, Control Room A/C System Flow Rate Verification B Train, were initially issued on December 18, 1999.


For verification of unit air flow capacity, acceptance criteria of greater than 20,400 CFM were specified.
For verification of unit air flow capacity, acceptance criteria of greater than 20,400 CFM were specified.


On March 11, 2002, the acceptance criteria associated with unit air flow capacity were inappropriately revised to greater than 18,360 CFM and less than 22,440 CFM based on information in ASME/ANSI N510
On March 11, 2002, the acceptance criteria associated with unit air flow capacity were inappropriately revised to greater than 18,360 CFM and less than 22,440 CFM based on information in ASME/ANSI N510-1980, Testing of Nuclear Air-Cleaning Systems. NRC finding 05000482/2012004-03, Safety-Related Fan Flow Rate Acceptance Criteria Reduced Below Design Basis Limit, which was documented in Inspection Report 05000482/2012004 (ADAMS Accession #: ML12314A296), discusses how ASME/ANSI N510-1980 was incorrectly applied to the testing of the Class IE electrical equipment air-conditioning system.
-1980, "Testing of Nuclear Air
-Cleaning Systems.NRC finding 05000482/2012004
-03, "Safety
-Related Fan Flow Rate Acceptance Criteria Reduced Below Design Basis Limit," which was documented in Inspection Report 05000482/2012004 (ADAMS Accession #: ML12314A296), discusses how ASME/ANSI N510-1980 was incorrectly applied to the testing of the Class IE electrical equipment air
-conditioning system.


The acceptance criteria of Procedures STS PE
The acceptance criteria of Procedures STS PE-010A and STS PE-010B remained the same until January 3, 2013, when the acceptance criteria were revised to greater than 21,012 CFM to correct the previously inadequate acceptance criteria of greater than 18,360 CFM and less than 22,440 CFM. Subsequently, on November 6, 2013, Calculation GK-M-001, Cooling and Heating Load Calculation for Control Room
-010A and STS PE
[Heating Ventilation and Air Conditioning] System Capabilities During Normal Plant Operation and Accident Conditions - (SGK04A/B), Revision 3, was issued and revised the minimum required accident air flow to 20,480 CFM. Accounting for 3 percent instrument uncertainty in accordance with vendor documentation, the minimum required accident air flow during testing would have been 21,094 CFM following the November 6, 2013, calculation revision. On April 14, 2015, Calculation WCN-15-CA-CBV-001, Impact of ESW Pipe Chase on Control Building [Heating, Ventilation, and Air Conditioning], Revision 2, was completed and required the design flow be revised to greater than 20,520 CFM. The testing acceptance criteria of STS PE-010A and STS PE-010B were revised to account for 3 percent instrument uncertainty and to add margin, and were revised to 21,250 CFM (without the additional margin, the minimum required accident air flow plus 3 percent for instrument uncertainty is 21,136 CFM).
-010B remained the same until January 3, 2013, when the acceptance criteria were revised to greater than 21,012 CFM to correct the previously inadequate acceptance criteria of greater than 18,360 CFM and less than 22,440 CFM. Subsequently, on November 6, 2013, Calculation GK
-M-001, "Cooling and Heating Load Calculation for Control Room [Heating Ventilation and Air Conditioning] System Capabilities During Normal Plant Operation and Accident Conditions  
- (SGK04A/B)," Revision 3, was issued and revised the minimum required accident air flow to 20,480 CFM. Accounting for 3 percent instrument uncertainty in accordance with vendor documentation, the minimum required accident air flow during testing would have been 21,094 CFM following the November 6, 2013, calculation revision. On April 14, 2015, Calculation WCN CA-CBV-001, "Impact of ESW Pipe Chase on Control Building [Heating, Ventilation, and Air Conditioning]," Revision 2, was completed and required the design flow be revised to greater than 20,520 CFM. The testing acceptance criteria of STS PE
-010A and STS PE-010B were revised to account for 3 percent instrument uncertainty and to add margin, and were revised to 21,250 CFM (without the additional margin, the minimum required accident air flow plus 3 percent for instrument uncertainty is 21,136 CFM). 21,250 CFM is the current STS PE
-010A and STS PE
-010B unit air flow acceptance criteria for the SGK04A and SGK0 4 B units.


On April 16, 2015, a Wolf Creek apparent cause evaluation associated with Condition Report 92274, "Application of SR 3.0.1," identified the potential that the acceptance criteria in Procedures STS PE
21,250 CFM is the current STS PE-010A and STS PE-010B unit air flow acceptance criteria for the SGK04A and SGK04B units.
-010A and STS PE
-010B may not have been met when the acceptance criteria were revised on January 3, 2013. The acceptance criteria had been revised from greater than 18,360 CFM and less than 22,440 CFM to a new value of greater than 21,012 CFM. Licensee Event Report 2015 01 was submitted to the NRC on August 26, 2015, and stated, "From January 3, 2013, through August 13, 2013, the Conditions and Required Actions of LCO 3.7.11, LCO 3.0.3 and LCO 3.0.4 were not met."    Based on questions by the inspectors the licensee initiated Condition Report 105208 to document that from December 18, 1999, until January 3, 2013, instrument uncertainty was not included in the acceptance criteria of STS PE
-010A and STS PE
-010B. The inspectors noted that LER 2015-002-01 documented that instrument uncertainty was not included in the acceptance criteria of STS PE
-010A and STS PE
-010B from March 11, 2002, until January 3, 2013. However, the licensee's cause evaluation and Licensee Event Report failed to identify that instrument uncertainty had never been included in the STS PE-010A and STS PE
-010B acceptance criteria from December 18, 1999, until March 11, 2002.


Also as a result of questions by the inspectors Condition Report 105208 documented that there was no formal process for procedure writers to consider measurement uncertainty when changing acceptance criteria and that a check for measurement uncertainty in the procedure change process was needed. The inspectors concluded that the licensee's cause evaluation and LER failed to identify this concern, which appeared to be the original cause of the licensee's failure to establish adequate acceptance criteria and failure to recognize the inoperability of trains A and B of the CRACS.
On April 16, 2015, a Wolf Creek apparent cause evaluation associated with Condition Report 92274, Application of SR 3.0.1, identified the potential that the acceptance criteria in Procedures STS PE-010A and STS PE-010B may not have been met when the acceptance criteria were revised on January 3, 2013. The acceptance criteria had been revised from greater than 18,360 CFM and less than 22,440 CFM to a new value of greater than 21,012 CFM. Licensee Event Report 2015-002-01 was submitted to the NRC on August 26, 2015, and stated, From January 3, 2013, through August 13, 2013, the Conditions and Required Actions of LCO 3.7.11, LCO 3.0.3 and LCO 3.0.4 were not met.


Based on previous performances of STS PE
Based on questions by the inspectors the licensee initiated Condition Report 105208 to document that from December 18, 1999, until January 3, 2013, instrument uncertainty was not included in the acceptance criteria of STS PE-010A and STS PE-010B. The inspectors noted that LER 2015-002-01 documented that instrument uncertainty was not included in the acceptance criteria of STS PE-010A and STS PE-010B from March 11, 2002, until January 3, 2013. However, the licensees cause evaluation and Licensee Event Report failed to identify that instrument uncertainty had never been included in the STS PE-010A and STS PE-010B acceptance criteria from December 18, 1999, until March 11, 2002.
-010A and STS PE
-010B and considering the design basis required flow with instrument uncertainty included, SGK04A was inoperable from October 11, 2005, to August 13, 2013; and SGK04B was inoperable from October 3, 2002, to July 18, 2013. Thus, in accordance with Technical Specification 3.7.11, the station should have entered mode 3 on November 3, 2002, with the SGK04B unit inoperable for greater than 30 days. The station did not meet Technical Specification 3.7.11 until August 13, 2013. The SGK04A and SGK04B units were simultaneously inoperable from October 11, 2005, through July 18, 2013. Although the SGK04A and SGK04B units were simultaneously inoperable for an extended period of time, the inspectors noted that the SGK04 units functioned and provided control room cooling throughout the inoperability period, the inspectors noted that licensee air flow calculations contained additional margin, and the inspectors noted that measured air flow rate testing results were never less than required design basis flow rates by more than 1.8 percent, which is less than the 3 percent instrument uncertainty.


The licensee's immediate corrective actions included corrective maintenance on the CRACS trains to increase the airflow to meet acceptance criteria limits, Procedures STS PE-010A and STS PE
Also as a result of questions by the inspectors Condition Report 105208 documented that there was no formal process for procedure writers to consider measurement uncertainty when changing acceptance criteria and that a check for measurement uncertainty in the procedure change process was needed. The inspectors concluded that the licensees cause evaluation and LER failed to identify this concern, which appeared to be the original cause of the licensees failure to establish adequate acceptance criteria and failure to recognize the inoperability of trains A and B of the CRACS.
-010B were performed successfully on March 6, 2015, and January 13, 2015, for A and B trains, respectively. Condition Report 105208 was initiated by the licensee for evaluation of any necessary process changes and extent of condition. Furthermore, procedure AP 15C
 
-004, "Preparation, Review and Approval of Procedures, Instructions and Forms," is being revised to require operations surveillance coordinator review of technical specification surveillance procedures that result in a change in acceptance criteria.
Based on previous performances of STS PE-010A and STS PE-010B and considering the design basis required flow with instrument uncertainty included, SGK04A was inoperable from October 11, 2005, to August 13, 2013; and SGK04B was inoperable from October 3, 2002, to July 18, 2013. Thus, in accordance with Technical Specification 3.7.11, the station should have entered mode 3 on November 3, 2002, with the SGK04B unit inoperable for greater than 30 days. The station did not meet Technical Specification 3.7.11 until August 13, 2013. The SGK04A and SGK04B units were simultaneously inoperable from October 11, 2005, through July 18, 2013. Although the SGK04A and SGK04B units were simultaneously inoperable for an extended period of time, the inspectors noted that the SGK04 units functioned and provided control room cooling throughout the inoperability period, the inspectors noted that licensee air flow calculations contained additional margin, and the inspectors noted that measured air flow rate testing results were never less than required design basis flow rates by more than 1.8 percent, which is less than the 3 percent instrument uncertainty.
 
The licensees immediate corrective actions included corrective maintenance on the CRACS trains to increase the airflow to meet acceptance criteria limits, Procedures STS PE-010A and STS PE-010B were performed successfully on March 6, 2015, and January 13, 2015, for A and B trains, respectively. Condition Report 105208 was initiated by the licensee for evaluation of any necessary process changes and extent of condition. Furthermore, procedure AP 15C-004, Preparation, Review and Approval of Procedures, Instructions and Forms, is being revised to require operations surveillance coordinator review of technical specification surveillance procedures that result in a change in acceptance criteria.


=====Analysis.=====
=====Analysis.=====
The inspectors determined that Wolf Creek's failure to establish adequate CRACS testing flow rate acceptance criteria was a performance deficiency that impacted the station's ability to adequately implement Technical Specification surveillance requirement SR 3.7.11, "Control Room Air Conditioning System (CRACS)."
The inspectors determined that Wolf Creeks failure to establish adequate CRACS testing flow rate acceptance criteria was a performance deficiency that impacted the stations ability to adequately implement Technical Specification surveillance requirement SR 3.7.11, Control Room Air Conditioning System (CRACS). This finding is more than minor because it is associated with the equipment performance attribute of the Mitigating Systems Cornerstone, and affected the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). Specifically, the station operated in a condition prohibited by Technical Specifications with train A of the safety-related CRACS inoperable from October 11, 2005, to August 13, 2013, and train B inoperable from October 3, 2002, to July 18, 2013.


This finding is more than minor because it is associated with the equipment performance attribute of the Mitigating Systems Cornerstone, and affected the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). Specifically, the station operated in a condition prohibited by Technical Specifications with train A of the safety-related CRACS inoperable from October 11, 2005, to August 13, 2013, and train B inoperable from October 3, 2002, to July 18, 2013
In accordance with Inspection Manual Chapter 0609.04, Initial Characterization of Findings, and Exhibit 2 of Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, issued June 19, 2012, and April 29, 2015, respectively, the performance deficiency affects a mitigating SSC. The inspectors determined this finding was not a deficiency affecting the design or qualification of a mitigating SSC that maintained its operability or functionality, the finding did not represent a loss of system and/or function, the finding did not represent an actual loss of function of at least a single train for greater than its Technical Specification allowed outage time, and the finding did not represent an actual loss of function of one or more non-Technical Specification trains of equipment designated as high safety-significant. Therefore, the inspectors determined the finding was of very low safety significance (Green).
. In accordance with Inspection Manual Chapter 0609.04, "Initial Characterization of Findings," and Exhibit 2 of Inspection Manual Chapter 0609, Appendix A, "The Significance Determination Process (SDP) for Findings At
-Power," issued June 19, 2012, and April 29, 2015, respectively, the performance deficiency affects a mitigating SSC. The inspectors determined this finding was not a deficiency affecting the design or qualification of a mitigating SSC that maintained its operability or functionality, the finding did not represent a loss of system and/or function, the finding did not represent an actual loss of function of at least a single train for greater than its Technical Specification allowed outage time, and the finding did not represent an actual loss of function of one or more non
-Technical Specification trains of equipment designated as high safety
-significant. Therefore, the inspectors determined the finding was of very low safety significance (Green).


The inspectors determined that in accordance with Inspection Manual Chapter 0310, "Aspects Within The Cross
The inspectors determined that in accordance with Inspection Manual Chapter 0310, Aspects Within The Cross-Cutting Areas, issued December 4, 2014, the finding has a cross-cutting aspect in the area of human performance, change management, because leaders did not use a systematic process for evaluating and implementing change so that nuclear safety remains the overriding priority. Specifically, there is not currently a formal process for procedure writers to consider measurement uncertainty when establishing and changing testing acceptance criteria, which resulted in extended inoperability of both the SGK04A and SGK04B units following significant changes to Technical Specifications that included adding surveillance requirements for the SGK04A and SGK04B units in 1999. This issue is indicative of current performance because the same issue would be expected to occur today. Condition Report 105208, which was written in response to the inspectors questions, documents that a check for measurement uncertainty in the procedure change process is needed [H.3].
-Cutting Areas," issued December 4, 2014, the finding has a cross-cutting aspect in the area of human performance, change management, because leaders did not use a systematic process for evaluating and implementing change so that nuclear safety remains the overriding priority. Specifically, there is not currently a formal process for procedure writers to consider measurement uncertainty when establishing and changing testing acceptance criteria, which resulted in extended inoperability of both the SGK04A and SGK04B units following significant changes to Technical Specifications that included adding surveillance requirements for the SGK04A and SGK04B units in 1999. This issue is indicative of current performance because the same issue would be expected to occur today. Condition Report 105208, which was written in response to the inspectors' questions, documents that a check for measurement uncertainty in the procedure change process is needed [H.3].


=====Enforcement.=====
=====Enforcement.=====
Technical Specification 3.7.11, Condition B, requires the reactor to be in mode 3 within 6 hours if one train of the CRACS has been inoperable for 30 days while in mode 1, 2, 3, or 4. Contrary to the above, from November 3, 2002, until August 13, 2013, the reactor was not in mode 3 within 6 hours with one train of the CRACS inoperable for 30 days while in mode 1, 2, 3, or 4. Specifically, the B train of the CRACS was inoperable for 30 days while in mode 1, 2, 3, and 4. The licensee entered this condition into its corrective action program as Condition Report 95378. The licensee's immediate corrective actions included corrective maintenance on the CRACS to increase the airflow to meet acceptance criteria limits. Surveillance Procedures STS P E-010A and STS PE
Technical Specification 3.7.11, Condition B, requires the reactor to be in mode 3 within 6 hours if one train of the CRACS has been inoperable for 30 days while in mode 1, 2, 3, or 4. Contrary to the above, from November 3, 2002, until August 13, 2013, the reactor was not in mode 3 within 6 hours with one train of the CRACS inoperable for 30 days while in mode 1, 2, 3, or 4. Specifically, the B train of the CRACS was inoperable for 30 days while in mode 1, 2, 3, and 4. The licensee entered this condition into its corrective action program as Condition Report 95378. The licensees immediate corrective actions included corrective maintenance on the CRACS to increase the airflow to meet acceptance criteria limits. Surveillance Procedures STS PE-010A and STS PE-010B were performed successfully on March 6, 2015, and January 13, 2015, for A and B trains, respectively. Condition Report 105208 was initiated by the licensee for any necessary process changes and extent of condition actions. Furthermore, procedure AP 15C-004, Preparation, Review and Approval of Procedures, Instructions and Forms, is being revised to require Operations Surveillance Coordinator review of Technical Specification surveillance procedures that result in a change in acceptance criteria. Because this violation was of very low safety significance and this issue was entered into the licensees corrective action program, this violation is being treated as an NCV, consistent with Section 2.3.2.a of the Enforcement Policy.
-010B were performed successfully on March 6, 2015, and January 13, 2015, for A and B trains, respectively. Condition Report 105208 was initiated by the licensee for any necessary process changes and extent of condition actions. Furthermore, procedure AP 15C
-004, "Preparation, Review and Approval of Procedures, Instructions and Forms," is being revised to require Operations Surveillance Coordinator review of Technical Specification surveillance procedures that result in a change in acceptance criteria. Because this violation was of very low safety significance and this issue was entered into the licensee's corrective action program, this violation is being treated as a n NCV , consistent with Section 2.3.2.a of the Enforcement Policy.


(NCV 05000482/2016002
  (NCV 05000482/2016002-01, Failure to Adequately Establish Control Room Air Conditioning System Testing Flow Rate Acceptance Criteria)
-01 , Failure to Adequately Establish Control Room Air Conditioning System Testing Flow Rate Acceptance Criteria
)


===.4 (Closed) LER 05000482/2015===
===.4 (Closed) LER 05000482/2015-004-00: Inadequate Procedure Results in Two===


00:  Inadequate Procedure Results in Two Containment Isolation Valves being in a Condition Prohibited by Technical Specifications, and LER 05000482/2015 01: Incorrect Decision Results in Two Containment Isolation Valves being in a Condition Prohibited by Technical Specifications On May 5, 2015, it was discovered that the motive force (air supply) was not removed for two containment shutdown purge valves as required by Technical Specification 3.6.3, "Containment Isolation Valves.The motive force was restored to allow the performance of Procedure STS KJ
Containment Isolation Valves being in a Condition Prohibited by Technical Specifications, and LER 05000482/2015-004-01: Incorrect Decision Results in Two Containment Isolation Valves being in a Condition Prohibited by Technical Specifications On May 5, 2015, it was discovered that the motive force (air supply) was not removed for two containment shutdown purge valves as required by Technical Specification 3.6.3, Containment Isolation Valves. The motive force was restored to allow the performance of Procedure STS KJ-001A, Integrated Diesel Generator and Safeguards Actuation Test - Train A, on April 26, 2015. After performance of Procedure STS KJ-001A, the motive force was not removed for the two containment shutdown purge valves. The plant entered Mode 4 on April 28, 2015.
-001A, "Integrated Diesel Generator and Safeguards Actuation Test - Train A," on April 26, 2015. After performance of Procedure STS KJ
-001A, the motive force was not removed for the two containment shutdown purge valves. The plant entered Mode 4 on April 28, 2015.


Upon discovery, the air supply valves for the two containment shutdown purge valves were locked closed, removing the motive force. The cause of the event was determined to be the decision to only track components listed on a locked component log using Form APF 21G 01, "Log of Locked Component Manipulations," Revision 1, during plant start up, which allowed a mode change with components out of position. Each impacted penetration flow path had a redundant valve that was closed with the motive force removed.
Upon discovery, the air supply valves for the two containment shutdown purge valves were locked closed, removing the motive force. The cause of the event was determined to be the decision to only track components listed on a locked component log using Form APF 21G-001-01, Log of Locked Component Manipulations, Revision 1, during plant start up, which allowed a mode change with components out of position. Each impacted penetration flow path had a redundant valve that was closed with the motive force removed.


The licensee implemented the following corrective actions:
The licensee implemented the following corrective actions:
: (1) On May 5, 2015, the air supply valves for GTHZ0007 and GTHZ0009 were locked closed and verified, which removed the motive force; and
: (1) On May 5, 2015, the air supply valves for GTHZ0007 and GTHZ0009 were locked closed and verified, which removed the motive force; and
: (2) Procedure AP 21G
: (2) Procedure AP 21G-001, Control of Locked Component Status, was revised to ensure an Equipment Out of Service Log entry was made for components required to be locked by technical specifications. The inspectors determined that this constituted a licensee-identified violation, and the enforcement aspects of this violation are discussed in Section 4OA7 of this inspection report.
-001, "Control of Locked Component Status," was revised to ensure an "Equipment Out of Service Log" entry was made for components required to be locked by technical specifications.


The inspectors determined that this constituted a licensee
The licensee event reports are closed.
-identified violation, and the enforcement aspects of this violation are discussed in Section
 
{{a|4OA7}}
These activities constituted completion of four event follow-up samples, as defined in Inspection Procedure 71153.
==4OA7 of this inspection report.==


The licensee event reports are closed. These activities constituted completion of four event follow
-up sample s, as defined in Inspection Procedure 71153.
{{a|4OA5}}
{{a|4OA5}}
==4OA5 Other Activities==
==4OA5 Other Activities==


  (Closed) Unresolved Item (URI)05000482/2015001
(Closed) Unresolved Item (URI) 05000482/2015001-01, Questions Related to Ultrasonic Examination of Reactor Vessel Flange Stud Hole Threads On May 7, 2015, the NRC issued Wolf Creek Nuclear Operating Corporation a URI related to the examination technique utilized by the licensee to perform reactor vessel flange ligament inspections for ASME Code compliance. The concern was that the technique being utilized by the licensee might not provide adequate coverage of the required examination area and may not be capable of detecting indications orientated on a plane normal to the axis of the stud that were equal to or exceeded 0.2 inch, as measured radially from the root of the thread, as required by the licensee's procedure and Section XI of the ASME Code. Demonstrations of the technique were completed by the licensee and verified that the technique could detect flaws in the required examination area. The results of these demonstrations were reviewed by the NRC staff and considered acceptable. Based on these facts, the NRC considers this item to be closed and no follow-up inspection activity for this item is planned.
-01, Questions Related to Ultrasonic Examination of Reactor Vessel Flange Stud Hole Threads On May 7, 2015, the NRC issued Wolf Creek Nuclear Operating Corporation a URI related to the examination technique utilized by the licensee to perform reactor vessel flange ligament inspections for ASME Code compliance. The concern was that the technique being utilized by the licensee might not provide adequate coverage of the required examination area and may not be capable of detecting indications orientated on a plane normal to the axis of the stud that were equal to or exceed ed 0.2 inch, as measured radially from the root of the thread, as required by the licensee's procedure and Section XI of the ASME Code.


Demonstrations of the technique were completed by the licensee and verified that the technique could detect flaws in the required examination area. The results of these demonstrations were reviewed by the NRC staff and considered acceptable. Based on these facts, the NRC considers this item to be closed and no follow
No findings were identified. The unresolved item is closed.
-up inspection activity for this item is planned.


No findings were identified.
{{a|4OA6}}
==4OA6 Meetings, Including Exit==


The unresolved item is closed.
===Exit Meeting Summary===
 
4OA 6 Meetings, Including Exit


===Exit Meeting Summary===
On May 26, 2016, regional inspectors presented the final heat sink performance inspection results to Mr. J. McCoy, Vice President, Engineering, and other members of the licensee staff.


On May 26, 2016 , regional inspectors presented the final heat sink performance inspection results to Mr. J. McCoy, Vice President, Engineering, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspector asked the licensee whether any materials examined during the inspection should be considered proprietary.
The licensee acknowledged the issues presented. The inspector asked the licensee whether any materials examined during the inspection should be considered proprietary. Proprietary information was returned or destroyed.


Proprietary information was returned or destroyed
On June 10, 2016, regional inspectors presented the inservice inspection activity inspection results via telephonic exit to Mr. W. Muilenburg, Supervisor, Licensing. The licensee acknowledged the issue presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.
. On June 10, 2016, regional inspectors presented the inservice inspection activity inspection results via telephonic exit to Mr. W. Muilenburg, Supervisor, Licensing. The licensee acknowledged the issue presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.


On June 23, 2016, regional inspectors presented the radiation safety inspection results to Mr. M. Skiles, and other members of the licensee staff via teleconference. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.
On June 23, 2016, regional inspectors presented the radiation safety inspection results to Mr. M. Skiles, and other members of the licensee staff via teleconference. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.


On July 27, 2016, the resident inspectors presented the inspection results to Cleveland Reasoner, Site Vice President, and other members of the licensee staff. The licensee acknowledged the issues presented.
On July 27, 2016, the resident inspectors presented the inspection results to Cleveland Reasoner, Site Vice President, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.


The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.
{{a|4OA7}}
==4OA7 Licensee-Identified Violations==


4OA 7 Licensee-Identified Violations The following violation s of very low safety significance (Green)were identified by the licensee and are violations of NRC requirements
The following violations of very low safety significance (Green) were identified by the licensee and are violations of NRC requirements, which meet the criteria of the NRC Enforcement Policy for being dispositioned as NCVs.
, which meet the criteria of the NRC Enforcement Policy for being dispositioned as NCVs.
* Technical Specification 5.7.2 states, in part, that high radiation areas with dose rates greater than 1.0 rem per hour at 30 centimeters shall be conspicuously posted as a high radiation area and shall be provided with a locked or continuously guarded door or gate to prevent unauthorized entry. Contrary to the above, on January 27, 2016, room 7406 on the 2013 foot elevation of the radwaste building areas had dose rates greater than 1.0 rem per hour and was not conspicuously posted as a high radiation area nor provided with a locked or continuously guarded door or gate to prevent unauthorized entry. This issue was identified by radiation protection technicians performing radiological surveys in the area. The licensee documented this issue in the corrective action program as Condition Report 102344. The finding was determined to be of very low safety significance (Green) because it was not an as-low-as-reasonably-achievable planning issue, there was no overexposure or potential for overexposure, and the licensees ability to assess dose was not compromised.
* Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, requires, in part, that activities affecting quality shall be accomplished in accordance with documented instructions, procedures, or drawings of a type appropriate to the circumstances. Licensee Procedure AP 26C-004, Operability Determination and Functionality Assessment, Revision 32, an Appendix B quality related procedure, provides instructions for determining whether equipment is operable when oil leakage is identified. Procedure AP 26C-004, Step 6.2.1.1, states in part, that if operability of a system/component is being questioned due to system leakage that the leak rate has been quantified and total identified leakage for the affected system has been determined and compared to the limits of Attachment F, Allowable Oil Leakage for Successful Mission. Contrary to the above, from May 28, 2016, until May 31, 2016, operability of a system/component was being questioned due to system leakage and the leak rate had not been quantified and the total identified leakage for the affected system was not determined and compared to the limits of Attachment F, Allowable Oil Leakage for Successful Mission. Specifically, operability of the B component cooling water pump was questioned due to system leakage as documented in Condition Report 104910, and the leak rate had not been quantified and the total identified leakage for the affected system was not determined, which resulted in the immediate operability determination being incorrect and the immediate operability determination requiring revision.


Technical Specification 5.7.2 states, in part, that high radiation areas with dose rates greater than 1.0 rem per h our at 30 centimeters shall be conspicuously posted as a high radiation area and shall be provided with a locked or continuously guarded door or gate to prevent unauthorized entry.
Immediate corrective actions included revising the immediate operability determination for the B component cooling water pump from operable to inoperable, generating a required reading for senior reactor operators, and documenting Condition Report 104959. Using Exhibit 2, Mitigating Systems Screening Questions, of Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process for Finding At-Power, dated June 19, 2012, the inspectors determined this finding was not a deficiency affecting the design or qualification of a mitigating SSC that maintained its operability or functionality, the finding did not represent a loss of system and/or function, the finding did not represent an actual loss of function of at least a single train for greater than it Technical Specification allowed outage time, and the finding did not represent an actual loss of function of one or more non-Technical Specification trains of equipment designated as high safety-significant. Therefore, the inspectors determined the finding was of very low safety significance (Green).
* Technical Specification 3.4.3, [Reactor Coolant System] Pressure and Temperature Limits, states, in part, that reactor coolant system pressure, reactor coolant system temperature, and reactor coolant system heatup and cooldown rates shall be maintained within the limits specified in the Pressure and Temperature Limits Report (PTLR).


Contrary to the above, on January 27, 2016, room 7406 on the 2013 foot elevation of the radwaste building areas had dose rates greater than 1.0 rem per h our and was not conspicuously posted as a high radiation area nor provided with a locked or continuously guarded door or gate to prevent unauthorized entry. This issue was identified by radiation protection technicians performing radiological surveys in the area. The licensee documented this issue in the corrective action program as Condition Report 102344. The finding was determined to be of very low safety significance (Green) because it was not an as-low-as-reasonably
Section 2.1.2 of the PTLR specifies that the reactor coolant system shall be maintained within the parameters of Figure 2.1-1 of the PTLR, which specifies a minimum pressure of 0 psig. Required Action C.1 of Technical Specification 3.4.3 specifies that with the reactor coolant system parameters outside the limits of the PTLR, restore the parameters to within the limits immediately. Contrary to the above, on May 8, 2011, and March 30, 2013, with the reactor coolant system parameters outside the limits of the PTLR, parameters were not restored to within the limits immediately. Specifically, the licensee drew a vacuum on the reactor coolant system to less than 0 psig to support filling operations but did not take action to immediately restore the reactor coolant system pressure to greater than or equal to 0 psig, as specified in the PTLR. The licensee placed this issue in the corrective action program as Condition Report 78920.
-achievable planning issue, there was no overexposure or potential for overexposure, and the licensee's ability to assess dose was not compromised.


Title 10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," requires, in part, that activities affecting quality shall be accomplished in accordance with documented instructions, procedures, or drawings of a type appropriate to the circumstances.
The licensee performed Engineering Evaluation EER 92-BB-02 and determined that drawing a vacuum on the reactor coolant system would not result in excessive stresses for reactor coolant system structures, systems and components. Using Manual Chapter 0609, Appendix G, Shutdown Operations Significance Determination Process, dated May 9, 2014, this issue screened to Green because it did not result in a loss of reactor coolant system barrier integrity.
* Technical Specification 3.4.15, [Reactor Coolant System] Leakage Detection Instrumentation, states, in part, that reactor coolant system leakage detection instrumentation shall be operable, including the containment sump level and flow monitoring system. Required Action A of Technical Specification 3.4.15, states, in part, that with the required containment sump level and flow monitoring system inoperable, restore the required containment sump level and flow monitoring system to operable status within 30 daysif the required action and associated completion time are not met, Condition E requires the reactor to be in mode 3 within 6 hours and in mode 5 within 36 hours. Contrary to the above, from the period of July 13, 2013, to November 20, 2013, with the containment sump level and flow monitoring system inoperable for greater than 30 days, the reactor was not placed in mode 3 within 6 hours or mode 5 within 36 hours.


Licensee Procedure AP 2 6C-004, "Operability Determination and Functionality Assessment," Revision 32, an Appendix B quality related procedure, provides instructions for determining whether equipment is operable when oil leakage is identified.
Specifically, the instrument tunnel sump level indication was inoperable because of erratic indication, but the licensee did not take the required action of Technical Specification 3.4.15. The licensee placed this issue in the corrective action program as Condition Report 84690. Using Manual Chapter 0609, Appendix A, Significance Determination Process, for Findings at Power, dated June 19, 2012, this issue screened to Green because it did not result in reactor coolant system leakage or degrade the licensees ability to detect and mitigate a small break loss of coolant accident.
* Technical Specification 3.6.3, Containment Isolation Valves, requires each containment isolation valve to be operable in modes 1, 2, 3, and 4. To be operable, containment isolation valves GTHZ0007 and GTHZ0009, which are Category 3 valves, must be closed with the motive force removed. Technical Specification 3.6.3, Condition A, Required Action A.1, requires, in part, that the affected penetration flow path for any inoperable Category 3 containment isolation valve be isolated within 12 hours.


Procedure AP 26C
Additionally, Required Action A.2, requires, in part, that the licensee verify the affected penetration flow path is isolated prior to entering mode 4 from mode 5. Contrary to the above, from April 28, 2015, through May 5, 2015, the licensee failed to verify the affected penetration flow path was isolated prior to entering mode 4 from mode 5 on April 28, 2015. As a result, Technical specification 3.6.3, Condition A, was not met On May 5, 2015, the licensee discovered that the motive force for valves GTHZ0007 and GTHZ0009 was not removed and the air supply valves had not been locked closed, and the affected penetration flow paths were not isolated prior to entering mode 4 from mode 5 on April 28, 2015. The inspectors noted that although the motive force was not removed for valves GTHZ0007 and GTHZ0009, the valves were in their closed safeguards positions and redundant valves in series were closed with the motive force removed, which ensured each penetration flow path had one operable valve closed with its motive force removed. Using Exhibit 3, Barrier Integrity Screening Questions, of Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process for Finding At-Power, dated June 19, 2012, the inspectors determined the finding did not represent an actual open pathway in the physical integrity of reactor containment (valves, airlocks, etc.), containment isolation system (logic and instrumentation), or heat removal components, and the finding did not involve an actual reduction in function of hydrogen igniters in the reactor containment. Therefore, the inspectors determined that this finding is of very low safety significance (Green).
-004, Step 6.2.1.1, states in part, that if operability of a system/component is being questioned due to system leakage that the leak rate has been quantified and total identified leakage for the affected system has been determined and compared to the limits of Attachment F, "Allowable Oil Leakage for Successful Mission."  Contrary to the above, from May 28, 2016, until May 31, 2016, operability of a system/component was being questioned due to system leakage and the leak rate had not been quantified and the total identified leakage for the affected system was not determined and compared to the limits of Attachment F, "Allowable Oil Leakage for Successful Mission."
 
Specifically, operability of the B component cooling water pump was questioned due to system leakage as documented in Condition Report 104910, and the leak rate had not been quantified and the total identified leakage for the affected system was not determined, which resulted in the immediate operability determination being incorrect and the immediate operability determination requiring revision. Immediate corrective actions included revising the immediate operability determination for the B component cooling water pump from operable to inoperable, generating a required reading for senior reactor operators, and documenting Condition Report 104959. Using Exhibit 2, "Mitigating Systems Screening Questions," of Inspection Manual Chapter 0609, Appendix A, "The Significance Determination Process for Finding At-Power," dated June 19, 2012, the inspectors determined this finding was not a deficiency affecting the design or qualification of a mitigating SSC that maintained its operability or functionality, the finding did not represent a loss of system and/or function, the finding did not represent an actual loss of function of at least a single train for greater than it Technical Specification allowed outage time, and the finding did not represent an actual loss of function of one or more non
-Technical Specification trains of equipment designated as high safety
-significant.
 
Therefore, the inspectors determined the finding was of very low safety significance (Green).
 
Technical Specification 3.4.3
, "[Reactor Coolant System]
Pressure and Temperature Limits ," states, in part
, that reactor coolant system pressure, reactor coolant system temperature, and reactor coolant system heatup and cooldown rates shall be maintained within the limits specified in the "Pressure and Temperature Limits Report (PTLR)."  Section 2.1.2 of the PTLR specifies that the reactor coolant system shall be maintaine d within the parameters of Figure 2.1
-1 of the PTLR, which specifies a minimum pressure of 0 psig. Required Action C.1 of Technical Specification 3.4.3 specifies that with the reactor coolant system parameters outside the limits of the PTLR, restore the parameters to within the limits immediately. Contrary to the above, on May 8, 2011, and March 30, 2013, with the reactor coolant system parameters outside the limits of the PTLR, parameters were not restored to within the limits immediately. Specifically, the licensee drew a vacuum on the reactor coolant system to less than 0 psig to support filling operations but did not take action to immediately restore the reactor coolant system pressure to greater than or equal to 0 psig, as specified in the PTLR. The licensee placed this issue in the corrective action program as Condition Report 78920.
 
The licensee performed Engineering Evaluation EER 92
-BB-02 and determined that drawing a vacuum on the reactor coolant system would not result in excessive stresses for reactor coolant system structures, systems and components.
 
Using Manual Chapter 0609, Appendix G, "Shutdown Operations Significance Determination Process," dated May 9, 2014, this issue screened to Green because it did not result in a loss of reactor coolant system barrier integrity.
 
Technical Specification 3.4.15
, "[Reactor Coolant System]
Leakage Detection Instrumentation
," states, in part, that reactor coolant system leakage detection instrumentation shall be operable, including the containment sump level and flow monitoring system. Required Action A of Technical Specification 3.4.15, states, in part, that with the required containment sump level and flow monitoring system inoperable, restore the required containment sump level and flow monitoring system to operable status within 30 days
-if the required action and associated completion time are not met, Condition E requires the reactor to be in m ode 3 within 6 hours and in mode 5 within 36 hours. Contrary to the above, from the period of July 13, 2013, to November 20, 2013, with the containment sump level and flow monitoring system inoperable for greater than 30 days, the reactor was not placed in mode 3 within 6 hours or mode 5 within 36 hours. Specifically, the instrument tunnel sump level indication was inoperable because of erratic indication, but the licensee did not take the required action of Technical Specification 3.4.15. The licensee placed this issue in the corrective action program as Condition Report 84690. Using Manual Chapter 0609, Appendix A, "Significance Determination Process, for Findings at Power," dated June 19, 2012, this issue screened to Green because it did not result in reactor coolant system leakage or degrade the licensee's ability to detect and mitigate a small break loss of coolant accident
.
 
Technical Specification 3.6.3, "Containment Isolation Valves," requires each containment isolation valve to be operable in modes 1, 2, 3, and 4. To be operable, containment isolation valves GTHZ0007 and GTHZ0009, which are Category 3 valves, must be closed with the motive force removed. Technical Specification 3.6.3, Condition A, Required Action A.1, requires, in part, that the affected penetration flow path for any inoperable Category 3 containment isolation valve be isolated within 12 hours. Additionally, Required Action A.2, requires, in part, that the licensee verify the affected penetration flow path is isolated prior to entering m ode 4 from m ode 5. Contrary to the above, from April 28, 2015, through May 5, 2015, the licensee failed to verify the affected penetration flow path was isolated prior to entering mode 4 from m ode 5 on April 28, 2015. As a result, Technical specification 3.6.3
, Condition A
, was not met O n May 5, 2015, the licensee discovered that the motive force for valves GTHZ0007 and GTHZ0009 was not removed and the air supply valves had not been locked closed, and the affected penetration flow paths were not isolated prior to entering mode 4 from m ode 5 on April 28, 2015. The inspectors noted that although the motive force was not removed for valves GTHZ0007 and GTHZ0009, the valves were in their closed safeguards positions and redundant valves in series were closed with the motive force removed, which ensured each penetration flow path had one operable valve closed with its motive force removed.
 
Using Exhibit 3, "Barrier Integrity Screening Questions," of Inspection Manual Chapter 0609, Appendix A, "The Significance Determination Process for Finding At
-Power," dated June 19, 2012, the inspectors determined the finding d id not represent an actual open pathway in the physical integrity of reactor containment (valves, airlocks, etc.), containment isolation system (logic and instrumentation), or heat removal components, and the finding d id not involve an actual reduction in function of hydrogen igniters in the reactor containment. Therefore, the inspectors determined that this finding is of very low safety significance (Green).


=SUPPLEMENTAL INFORMATION=
=SUPPLEMENTAL INFORMATION=
Line 705: Line 525:
: [[contact::C. Adkinson]], Environmental Biologist IV
: [[contact::C. Adkinson]], Environmental Biologist IV
: [[contact::T. Baban]], Manager, System Engineering
: [[contact::T. Baban]], Manager, System Engineering
: [[contact::W. Brown]], Superintendent, Security Operations  
: [[contact::W. Brown]], Superintendent, Security Operations
: [[contact::T. Broyles]], Manager, Information Services
: [[contact::T. Broyles]], Manager, Information Services
: [[contact::D. Campbell]], Superintendent, Maintenance
: [[contact::D. Campbell]], Superintendent, Maintenance
: [[contact::C. Carman]], Supervisor, Chemistry
: [[contact::C. Carman]], Supervisor, Chemistry
: [[contact::J. Dorsey]], Technician I, Chemistry
: [[contact::J. Dorsey]], Technician I, Chemistry
: [[contact::T. East]], Superintendent, Emergency Planning  
: [[contact::T. East]], Superintendent, Emergency Planning
: [[contact::J. Edwards]], Manager, Operations  
: [[contact::J. Edwards]], Manager, Operations
: [[contact::D. Erbe]], Manager, Security  
: [[contact::D. Erbe]], Manager, Security
: [[contact::R. Flannigan]], Manager, Nuclear Engineering
: [[contact::R. Flannigan]], Manager, Nuclear Engineering
: [[contact::K. Fredrickson]], Engineer, Licensing
: [[contact::K. Fredrickson]], Engineer, Licensing
: [[contact::J. Freeman]], Supervisor of Treatment Systems, Operations
: [[contact::J. Freeman]], Supervisor of Treatment Systems, Operations
: [[contact::J. Fritton]], Oversight  
: [[contact::J. Fritton]], Oversight
: [[contact::C. Garcia]], Supervisor Engineer
: [[contact::C. Garcia]], Supervisor Engineer
: [[contact::D. Gibson]], Master HP Technician
: [[contact::D. Gibson]], Master HP Technician
Line 732: Line 552:
: [[contact::M. Legresley]], Engineer
: [[contact::M. Legresley]], Engineer
: [[contact::K. Lemaster]], Master Technician, Chemistry
: [[contact::K. Lemaster]], Master Technician, Chemistry
: [[contact::D. Mand]], Manager, Design
: [[contact::D. Mand]], Manager, Design Engineering
Engineering
: [[contact::N. Mayhew]], Engineer III
: [[contact::N. Mayhew]], Engineer III
: [[contact::J. McCoy]], Vice President, Engineering
: [[contact::J. McCoy]], Vice President, Engineering
Line 739: Line 558:
: [[contact::C. Medenciy]], Radioactive Materials Shipper
: [[contact::C. Medenciy]], Radioactive Materials Shipper
: [[contact::C. Menke]], Supervisor Maintenance
: [[contact::C. Menke]], Supervisor Maintenance
: [[contact::K. Miller]], Master Instruments and Controls
: [[contact::K. Miller]], Master Instruments and Controls Technician
Technician
: [[contact::N. Mingle]], Engineer
: [[contact::N. Mingle]], Engineer
: [[contact::K. Mitchell]], Master Chemistry Technician
: [[contact::K. Mitchell]], Master Chemistry Technician
: [[contact::W. Muilenburg]], Supervisor, Licensing  
: [[contact::W. Muilenburg]], Supervisor, Licensing
: [[contact::L. Ratzlaff]], Manager, Maintenance
: [[contact::L. Ratzlaff]], Manager, Maintenance
: [[contact::R. Raymer]], Engineering Technologist V
: [[contact::R. Raymer]], Engineering Technologist V
Line 750: Line 568:
: [[contact::J. Rudeen]], Supervisor, Regulatory Support
: [[contact::J. Rudeen]], Supervisor, Regulatory Support
: [[contact::K. Sheridan]], Engineer III
: [[contact::K. Sheridan]], Engineer III
Attachment 1
: [[contact::M. Skiles]], Manager, Radiation Protection
: [[contact::M. Skiles]], Manager, Radiation Protection
: [[contact::T. Slenker]], Supervisor, Operations Support
: [[contact::T. Slenker]], Supervisor, Operations Support
: [[contact::S. Smith]], Plant Manager
: [[contact::S. Smith]], Plant Manager
: [[contact::M. Staiger]], Engineer II
: [[contact::M. Staiger]], Engineer II
: [[contact::L. Stevens]], Licensing
: [[contact::L. Stevens]], Licensing Engineer V
Engineer V
: [[contact::L. Stone]], Licensing Engineer V
: [[contact::L. Stone]], Licensing Engineer
V  
: [[contact::A. Stull]], Vice President and Chief Administrative Officer
: [[contact::A. Stull]], Vice President and Chief Administrative Officer
: [[contact::J. Suter]], Supervisor Engineer
: [[contact::J. Suter]], Supervisor Engineer
: [[contact::M. Tate]], Superintendent, Security
: [[contact::M. Tate]], Superintendent, Security Operations
Operations
: [[contact::J. Truelove]], Supervisor, Chemistry
: [[contact::J. Truelove]], Supervisor, Chemistry
: [[contact::J. Vopat]], Technician II, Chemistry  
: [[contact::J. Vopat]], Technician II, Chemistry
 
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==


===Opened/Closed===
===Opened/Closed===
: 05000482/2016002-01 NCV Failure to Adequately Establish Control Room Air Conditioning System Testing Flow Rate Acceptance Criteria
: 05000482/2016002-01       NCV     Failure to Adequately Establish Control Room Air Conditioning System Testing Flow Rate Acceptance Criteria (4OA3)
(4OA3)
 
===Closed===
===Closed===
: 05000482/2014
: 05000482/2014-001-00      LER     Failure to Comply with Required Action of Technical Specification 3.4.3 while Performing a Vacuum Fill of the Reactor Coolant System (4OA3)
-001-0 0 LER Failure to Comply with Required Action of Technical Spec ification 3.4.3 while Performing a Vacuum Fill of the Reactor Coolant System (4OA3)
: 05000482/2014-004-00     LER     Condition Prohibited by Technical Specifications due to an Instrument Tunnel Sump Level Indication Transmitter Incompatible with the Containment Environment (4OA3)
: 05000482/2014
: 05000482/2015-001-01     URI     Questions Related to Ultrasonic Examination of Reactor Vessel Flange Stud Hole Threads (4OA5)
-004-00 LER Condition Prohibited by Technical Specifications due to an Instrument Tunnel Sump Level Indication
: 05000482/2015-002-00     LER     Two Control Room Air Conditioning Trains Inoperable Due to Failure to Meet Surveillance Requirement (4OA3)
: Transmitter Incompatible with the Containment Environment (4
: 05000482/2015-002-01     LER     Two Control Room Air Conditioning Trains Inoperable Due to Failure to Meet Surveillance Requirement (4OA3)
: OA 3)  
: 05000482/2015-004-00     LER     Inadequate Procedure Results in Two Containment Isolation Valves being in a Condition Prohibited by Technical Specifications (4OA3)
: 05000482/2015
: 05000482/2015-004-01     LER     Incorrect Decision Results in Two Containment Isolation Valves being in a Condition Prohibited by Technical Specifications (4OA3)
-001-01 URI Questions Related to Ultrasonic Examination of Reactor Vessel Flange Stud Hole Threads
(4OA5)  
: 05000482/2015
-002-00 LER Two Control Room Air Conditioning Trains Inoperable Due to Failure to Meet Surveillance Requirement
(4OA3)  
: 05000482/2015
-002-01 LER Two Control Room Air Conditioning Trains Inoperable Due to Failure to Meet Surveillance Requirement
(4OA3)  
: 05000482/2015
-004-00 LER Inadequate Procedure Results in
: Two Containment Isolation Valves being in a Condition Prohibited by Technical Specifications (4OA3)
: 05000482/2015
-004-01 LER Incorrect Decision Results in Two Containment Isolation Valves being in a Condition Prohibited by Technical Specifications
(4OA3)    


==LIST OF DOCUMENTS REVIEWED==
==LIST OF DOCUMENTS REVIEWED==
==Section 1R01: Adverse Weather Protection==
===Procedures===
: Number Title Revision
: AP 17C-028 Emergency Response Duties and Responsibilities
: OFN
: AF-025 Unit Limitations
: SYS
: OPS-009 Hot Weather Operations Miscellaneou
s Number Title Date Wolf Creek FYI
: Wolf Creek Corporate Communications Notice
- Early Release Due to Impending Severe Weather April 26, 2016
: Section 1R04
:
: Equipment Alignment
===Procedures===
: Number Title Revision CKL
: EG-120 Component Cooling Water System Valve, Switch and Breaker Lineup
: CKL
: GK-121 Control Building HVAC Valve Checklist
: CKL
: GK-131 Control Building HVAC Electrical Checklist
: CKL
: KJ-121 Diesel Generator NE01 and NE02 Valve Checklist
: SYS
: EG-120 Component Cooling Water System Drawing s Number Title Revision
: J-12SA04
: Control Logic Diagram ESFAS Control Room Ventilation Isolation Safety Limits
: J-104-00390 Logic Block Diagram ESFAS (KP1909W), Sheet 1
: W08 M-1H1521
: Heating, Ventilating, & Air Cond. Auxiliary Building EL.
: 2047'-6" Area 2 9 M-12EB03
: Piping & Instrumentation Diagram Component Cooling Water System
: M-12EG01
: Piping & Instrumentation Diagram Component Cooling Water System
: Drawing s Number Title Revision
: M-12EG02 Piping & Instrumentation Diagram Component Cooling Water System
: M-12EG0 3 Piping & Instrumentation Diagram Component Cooling Water System
: M-12GK01 Piping & Instrumentation Diagram Control Building H.V.A.C
: M-12GK02 Piping & Instrumentation Diagram Control Building HVAC
: M-12GK03 Piping & Instrumentation Diagram Control Building HVAC
: M-12GK04 Piping & Instrumentation Diagram Control Building HVAC
: M-12KJ04 Piping & Instrumentation Diagram Standby Diesel Generator "B" Cooling Water System
: M-12KJ05 Piping & Instrumentation Diagram Standby Diesel Generator "B" Intake Exhaust, F.O. & Start Air Sys.
: M-12KJ06 Piping &Instrumentation Diagram Standby Diesel Generator "B" Lube Oil System Section 1R05
:
: Fire Protection
===Procedures===
: Number Title Revision
: AI 10-001 Fire Brigade Equipment Inventory, Maintenance and Cleaning 12
: AP 10-105 Fire Protection Training and Drills
: AP 10-106 Fire Preplans
: AP 10-106 Fire Preplans Drawing s Number Title Revision E-1F9905 Fire Hazard Analysis
: E-1F9905 Fire Hazard Analysis
: E-1F9910 Post-Fire Safe Shutdown Area Analysis
===Condition Report===
s 62669
: 105119
: 105426
: 105533
: 105534 
: Miscellaneou
s Number Title Date 062416/0900/U/D
: PC Storage Fire June 24, 2016
==Section 1R07: Heat Sink Performance==
===Procedures===
: Number Title Revision
: AI 07A-008 Lake Water Chemical Treatment Program
: AI 07D-001 Resource Management and Ecological Monitoring Programs 12
: AI 23L-005 Lake Water Piping Integrity
: ALR 00-055A Essential Service Water Pump A Pressure Low
: 11A
: ALR 00-055B Essential Service Water Pump B Pressure Low
: 2A
: ALR 00-055C Essential Service Water Pump Trouble
: AP 15C-002 Procedure Use and Adherence
: AP 21-001 Conduct of Operations
: AP 23L-001 Lake Water Systems Corrosion and Fouling Mitigation Program 7
: AP 23L-002 Heat Exchanger Program 4
: AP 23L-003 Buried Piping and Tanks Program
: MPE
: GK-004 GK Unit Preparation for Work
: OFN
: EF-033 Loss of Essential Service Water
: OFN
: SG-003 Natural Events
: QCP-20-514 Eddy Current Testing
: QCP-20-518 Visual Examination of Heat Exchangers and Piping Components
: STN
: EF-022A ESW Train A Post
-LOCA Flow Balance
: 8B STN
: EF-022B ESW Train A Post
-LOCA Flow Balance
: STN
: PE-033 CCW Heat Exchanger Performance Test
: STN
: PE-036 Safety Related Room Cooler Heat Transfer Verification and Performance Trending
: STN
: PE-037A ESW Train A Heat Exchanger Flow and DP Trending
: 18A STN
: PE-037B ESW Train A Heat Exchanger Flow and DP Trending
===Procedures===
: Number Title Revision STN
: PE-038 Containment Cooler Performance Test
: STN
: PE-040 ESW Crosstie Valve Leak Test
: STN
: PE-056 ESW Emergency Make
-Up Piping Flow Test
: STS
: MT-073 SGK04B Heat Exchanger Inspection
: 3B SYS
: CI-010A A Train ESW Chemical Addition
: SYS
: CI-010B B Train ESW Chemical Addition
: SYS
: CI-003 S/U and S/D for the Macrofoul Treatment of ESW/Service Water
: SYS
: CI-004 S/U and S/D for the Copper Corrosion Inhibitor Treatment of ESW/Service Water
: SYS
: CI-006 S/U and S/D of the Scale Inhibitor Treatment for Service Water 2 SYS
: CI-008 Operation of the Circulating and Service Water Corrosion Monitoring System
: SYS
: EF-300 ESW/Service Water Macrofouling Treatment
: SYS
: OQT-001B Operations B Train Quarterly Tasks
===Drawings===
: Number Title Revision M-1HX001 Heat Exchanger Tube Sheet Maps
===Condition Reports===
: 36334 99593
: 100883
: 100950
: 101790
: 102575
: 103515
: 104817
: Jobs 10-324747 10-328253 12-352168 12-354020 12-354021 12-358715 12-358716 12-359623 13-370650 13-370651 13-374576 13-379272 14-385020 14-390223 14-394444 15-397194 15-400748
===Calculations===
: Number Title Revision/Date 25360-000-MOC-AN-0001 Emergency Diesel Generator Frequency Variation Impact on Motor Operated Mechanical Equipment Performance
: 96227-TR-01 CN001 Containment Fan Cooler Response to a Simultaneous LOCA and LOOP Event
: AN-00-037 Containment Cooler Requirements for Loss of RHR Shutdown Cooling
: AN-05-016 Updated MSLB Containment Pressure and Temperature Response Analysis for the Limiting Cases, Accounting for the Uncertainty of the Initial Containment Temperature
: AN-97-004 Updated Containment Pressure and Temperature Response Analysis for the Limiting LOCA Scenario, Accounting for Additional Time Delay for Fan Coolers Activation
: CA-529-452 Design Report for Replacement Coil for SGG04A/B
: CA-529-1236 Design Report Addendum for Replacement Coil for SGG04A/B 0
: CA-529-1236-000-CN001 Vendor Calculation: Aerofin Design Report CA
-529-452 for SGG04A and SGG04B Spent Fuel Pool Room Coolers 3
: CA-529-1236-000-CN002 Design Report Addendum for Replacement Coil for SGG04A/B 0
: EF-10 Essential Service Water Flow Requirements
: EF-10-002-CN001 Essential Service Water (ESW) System Flow Requirements
: EF-22 Essential Service Water Power Block Piping Differential Pressure During LOCA/SIS Conditions
: EF-39 Heat Exchanger Tube Minimum Wall 0
: EF-M-076 Hydraulic Analysis for Essential Service Water (ESW) System following a Loss of Offsite Power (LOOP)
: EF-M-078 Evaluation of Wolf Creek Essential Service Water System (ESW) Modification During LOOP/LOCA Conditions
: EG-08-W Minimum Wall Thickness of Tubing in Cooling Water Heat Exchangers EEG01A and EEG01B
: EG-09-W Tube Plugging for CCW Heat Exchangers
===Calculations===
: Number Title Revision/Date
: EG-M-032 Component Cooling Water Heat Exchanger Performance During Normal Operations, Shutdown at 4 Hours (and Hours), and Post
-LOCA Recirculation
: EG-M-032 CN004 Component Cooling Water Heat Exchanger Performance During Normal Operations, Shutdown at Four Hours (and 12 hours) and Post
-LOCA Recirculation
: GG-352 Fuel building HVAC System
: GG-M-004 Cooling Load and Fuel Pool Area Temperature
- Normal Operation 0
: GG-M-005 Spent Fuel Pump (PEC01A/PEC01B) and Heat Exchanger (EEC01A/EEC01B) Rooms 6104 and 6105 Temperature and Equipment Operability
: GG-M-005-000-CN001 Spent Fuel Pump (PEC01A / PEC01B) and Heat Exchanger (EEC01A / EEC01B) Rooms 6104 and 6105 Temperatures and Equipment Operability
: GG-MH-001 Mechanical
- Calculate the Cooling Capacity of Spent Fuel Pump Room Coolers at Low Flow Conditions
: GK-06-W SGK05A/B Class 1E Electrical Equipment Rooms A/C Units, Single Unit Operation Capability
: GK-99 No Media Per PIR 98
-1545 Criteria for Minimum Wall for Room Coolers Cu
-Ni Tubes 2
: GK-361 Control Building HVAC Nodal Points for the Flow Diagram 1
: GK-372 Nozzle Movements Due to Thermal Growth of Air Handling Unit SGK05A
and B 0
: GK-C-004 Test Response Spectra for Proportional Three Mode Controllers in GK System
: GK-C-004 Test Response Spectra for Proportional Three Mode Controllers in GK System December 1991
: GK-M-009 Tube Plugging Criteria for Control Room AC Unit SGK04A/B Condensers and ESF Switchgear Rooms
: AC Unit SGK05A/B Condensers
: GK-M-010 Tube Pitting Criteria for Control Room SGK04A/B
and Electrical Switch Gear Rooms SGK05A/B Condensing Units
: GK-M-014 Cooling and Heating Load for Control Building Class 1E Electrical Equipment Areas During Accident Conditions
- Train A 0
===Calculations===
: Number Title Revision/Date
: GN-M-011 Containment Air Coolers (SGN01A, SGN01B, SGN01C, SGN01D) Tube Plugging Criteria
: GN-MW-004 Minimum Tube Wall Thickness for Containment Cooler Tubes onSGN01A/D
: GN-S-005 WCGS CuNi Replacement Containment Air Cooler Coils Evaluations for ASME Section III Subsections ND and NF
: GN-S-006 WCGS
: AL-6XN Replacement Containment Air Cooler Coils Evaluations for ASME Section III Subsection ND and NF 1
: KA-M-004 Sizing of Cooling Water Booster Pumps for the Atlas Copco Air Compressors
: KA-MH-003 Cooling Duty for the Atlas Copco Air Compressors (CKA01A and CKA01B)
: M-612C-00015 Performance Calculations and Curves
: XX-C-022-000-CN001 Seismic Qualification of Room Coolers Procured from UE
: XX-M-067 Tube Pitting Criteria for Safety
-Related Room Cooler Cooling Coils
: XX-M-068 Tube Plugging Criteria for Safety
-Related Room Cooler (Aerofin AL6XN) Cooling Coils Thermal Performance Analyses Number Title Date EEG01A-1 CCW Heat Exchanger Performance Test December 24, 2015 EEG01A-2 CCW Heat Exchanger Performance Test March 17, 2011
: SGL15B-1 Safety Related Room Cooler Heat Transfer Verification and Performance Trending October 9, 2014
: SGL15B-2 Safety Related Room Cooler Heat Transfer Verification and Performance Trending August 14, 2013
: SGN01D-1 Containment Cooler Performance Test April 6, 2016
: SGN01D-2 Containment Cooler Performance Test October 15, 2014 
: Modifications Number Title Revision
: 014003 Containment Air Cooler Coil Replacement for SGN01D
: 014732 Containment Air Cooler Coil Replacement
- SGN01A, B, & C 2
: Vendor Documents Number Title Revision/ Date M-612C-00015 Performance Calculations and Curves December 12, 2007 M-620-00154 Coil Performance Topical Report
: W02 M-622.1A-VDS-1.07 SGK05A/B Condenser Vendor Data Sheet April 11, 2005
: M-622.1A-00052 Design Report No. N251
: March 7, 2003
===Miscellaneous===
: Number Title Revision/ Date 14-0209-TR-001 Containment Cooler Tube Condition Assessment
: 755200/2 Wolf Creek Nuclear Operating Corporation Hydrographic Survey of UHS Reservoir and ESWS Intake Channel at the Wolf Creek Generating Station, Burlington, Kansas June 18, 2015
: ET 90-0023 Docket No. 50
-482, Response to Generic Letter 89
-13, "Service Water System Problems Affecting Safety
-Related Equipment" January 30, 1990
: ET 94-0012 Docket No.50
-482, Updated Response to Generic Letter 89-13 February 18, 1994
: ET 94-0075 Docket No.50
-482, Final Response to Generic Letter 89-13 November 28, 1994
: ET 99-0042 Docket No.50
-482, Updated Response to Generic Letter 89-13 November 17, 1999 OE
: EF-16-001 "Evaluation of Wolf Creek Essential Service Water System (ESW) Modifications during LOOP/LOCA Conditions
===Miscellaneous===
: Number Title Revision/ Date OE
: GK-15-012 SGK05A, Class 1E Electrical Equipment Air
-Conditioning Unit, was found in a "Lube Oil Failure" trip condition after elevated temperatures were noticed on the 2,016 feet elevation of the control building.
: SA-2013-0068 Lake Water Program Formal Self
-Assessment March 30, 2015
: SA-201 3-0073 Lake Water Self
-Assessment January 16, 2014
: WCEM-06-005 Zebra Mussel, Water Quality, and Aquatic Vegetation Monitoring
- Coffey County Lake
- 2015 Report and 2016 Plans 16 WCNOC - 22 2009 Thru 2014 Periodic Surveillance Report for Ultimate Heat Sink and Associated Safety
-Related Structures Section 1R11
:
: Licensed Operator Requalification Program
===Procedures===
: Number Title Revision
: ALR 00-083C Rx Partial Trip
: 5A
: AP 21-001 Conduct of Operations
: AP 22-001 Conduct of Pre
-Job and Post
-Job Briefs 19 OFN
: SB-008 Instrument Malfunctions
: STS
: IC-507D Steam Line Pressure Instrumentation Channel Calibration
- Protection Set 1
: STS
: IC-508A Refueling Water Storage Tank Level Transmitter Calibration
===Condition Report===
s
: 104976
: 105566
: Miscellaneou
s Number Title Revision/ Date
: EPF 06-007-01 Wolf Creek Generating Station Emergency Notification (Message #CR
-001) 12E LR4412001 Annunciator Response Practice
: Miscellaneou
s Number Title Revision/ Date
: LR4640001 Operating Crew Simulator Performance Evaluation Summary Sheet May 16, 2016 LR4640001 Simulator Evaluation
: LR5001005 E-Plan Simulator Performance Evaluation Summary Sheet May 16, 2016
: Section 1R12
:
: Maintenance Effectiveness
===Procedures===
: Number Title Revision MPE
: GK-004 GK Unit Preparation for Work
: QCP-20-518 Visual Examination of Heat Exchangers and Piping Components
: STS
: MT-073 SGK04B Heat Exchanger Inspection
: 3B
===Condition Report===
s
: 101867
: 103311
: 104838
: 104878
: Miscellaneou
s Number Title Date 2016-010 RER Reportability Determination March 14, 2016
: 51493 Functional Failure Determination Checklist May 23, 2012
: 53159 Functional Failure Determination Checklist June 15, 2012
: 299 Functional Failure Determination Checklist June 22, 2012
: 68661 Functional Failure Determination Checklist June 7, 2013
: 71634 Functional Failure Determination Checklist September 4, 2013
: 74985 Functional Failure Determination Checklist November 14, 2013 85936 Functional Failure Determination Checklist August 14, 2014
: 101867 Functional Failure Determination Checklist January 26, 2016
: 103311 Functional Failure Determination Checklist April 1, 2016
: GK System Health Report January 1, 2016, through March 31, 2016 
: Section 1R13
:
: Maintenance Risk Assessment and Emergent Work Controls
===Procedures===
: Number Title Revision
: AP 22C-003 On-Line Nuclear Safety and Generation Risk Assessment
: AP 22C-007 Risk Management and Contingency Planning
: INC
: C-1008 Calibration of Power Supplies
: 3B RNM
: C-0064 KGB1907 Power Supply Acceptance Test
: STS
: GK-001A Control Room Emergency Vent System Train A Operability Test 32 STS
: GK-002A Control Room A/C Unit Operability Test
: STS
: IC-208A 4KV Loss of Voltage & Degraded Voltage TADOT NB01 Bus
- SEP GRP 1 29A SYS
: GK-123 Control Building A/C Units Startup and Shutdown
: 29A
===Condition Report===
s
: 104760
: 104761
: 104857
: Job s 15-408144-000 15-408144-001 15-408144-002 15-408144-003
: Miscellaneou
s Number Title Date 16-203
: On-Line Nuclear Safety and Generation Risk Assessment:
: Risk Assessment Dates:
: April 11, 2016 through April 17, 2016
: April 13, 2016
: 16-203 On-Line Nuclear Safety and Generation Risk Assessment:
: Risk Assessment Dates
: April 11, 2016 through April 17, 2016 April 14, 2016
: 16-203 On-Line Nuclear Safety and Generation Risk Assessment:
: Risk Assessment Dates:
: April 11, 2016 through April 17, 2016 April 15, 2016
: 16-205 On-Line Nuclear Safety and Generation Risk Assessment:
: Risk Assessment Dates:
: April 25, 2016 through May 1, 2016 April 28, 2016
: 16-209 On-Line Nuclear Safety and Generation Risk Assessment: 
: Risk Assessment Dates:
: May 23, 2016 through May 29, 2016 May 23, 2016
: Miscellaneou
s Number Title Date 16-209 On-Line Nuclear Safety and Generation Risk Assessment:
: Risk Assessment Dates
: May 23, 2016 through May 29, 2016 May 27, 2016
: Section 1R15
:
: Operability Evaluations
===Procedures===
: Number Title Revision STN
: FP-211 Diesel Fire Pump 1FP01PB Monthly Operation and Fuel Level Check
: STS
: EF-100B ESW System Inservice Pump B & ESW B Check Valve Test
===Condition Report===
s
: 104184
: 104425
: 104427
: 104523
: 105031
: 105032
: 105033
: 105034
: 105263
: 105264
: 105347
: Drawing s Number Title Revision M-0023 P&ID Fire Protection System (FP), Sheet 1
: Miscellaneou
s Number Title Revision/ Date A-3824-06 Installation Operation and Maintenance
- Diesel Fire Pump 1FP001PB and Jockey Pump 1FP003P
: W13 P-1-W Starting of Essential Service Water Pump Against Reverse Rotation 0 STS
: EF-100B ESW System Inservice Pump B & ESW B Check Valve Test Performed May 5, 2016
: Section 1R19
:
: Post-Maintenance Testing
===Procedures===
: Number Title Revision
: AP 12-003 Foreign Material Exclusion
===Procedures===
: Number Title Revision
: AP 21F-001 Equipment Out
-of-Service Control
: GEN 00-004 Power Operation
: INC
: C-1004 Calibration of Indicators
: 6B STN
: IC-256B
: Calibration of Emergency Fuel Oil Storage Tank B Level Loop 13 STN
: SF-001 Control Rod Parking 18A STS
: AL-103 TDAFW Pump Inservice Pump Test
: 66A STS
: CH-008B Emergency Fuel Oil Storage Tank B
: STS
: EG-100A Component Cooling Water Pumps A/C Inservice Pump Test
: STS
: GK-002B Control Room A/C Unit Operability Test
: STS
: SF-001 Control and Shutdown Rod Operability Verification Drawing s Number Title Revision
: M-761-0214-01 Interconnecting Wiring Diagram Cabinet 01 Steam Pressure
- Loop 1 Protection 1 Cabinet 01 Card Fram 04
: W05 M-761-0216-01 Interconnecting Wiring Diagram Cabinet 01
===Condition Report===
s
: 104121
: 104337
: 104346
: 104727
: 104883
: 104942
: 104943
: 104957
: Jobs 15-405389-000 15-407456-000 15-407456-003 15-407456-004 15-407456-006 15-407456-007 15-407487-000 15-407487-001 15-407953-000 15-408111-000 15-408319-000 16-411548-000 16-413431-000 16-413431-001 16-414528-000
: Section 1R22
:
: Surveillance Testing
===Procedures===
: Number Title Revision
: AP 29G-001 RCS Unidentified Leak Rate Monitoring Program
: CKL
: ZL-003 Control Room Daily Readings
: 69A
===Procedures===
: Number Title Revision
: STS
: AL-201C Turbine Driven Auxiliary Feedwater System Inservice Valve Test 9 STS
: BB-006 RCS Water Inventory Balance Using the NPIS Computer
: STS
: BM-205
: SGBD System Inservice Valve Test
: STS
: CR-001 Shift Log for Modes 1, 2, & 3
: STS
: EF-100B ESW System Inservice Pump B & ESW B Check Valve Test
: STS
: GG-001B Emergency Exhaust Filtration System Train B Operability Test 23 STS
: IC-255B Channel Operational Test Control Room Air Intake Radiation Monitor GK RE
-0004 16A SYS
: GG-200 Fuel Building Emergency Exhaust Operations Drawing s Number Title Revision
: J-12SA04 Control Logic Diagram ESFAS Control Room Ventilation Isolation Safety Limits
: J-104-00390 Logic Block Diagram ESFAS (KP1909W), Sheet 1
: W08 M-12AL01 Piping and Instrumentation Diagram Auxiliary Feedwater System
: M-12GK01 Piping & Instrumentation Diagram Control Building H.V.A.C
: M-12GK02 Piping & Instrumentation Diagram Control Building H.V.A.C
: M-12GK03 Piping & Instrumentation Diagram Control Building H.V.A.C
===Condition Report===
s
: 101098 10 1865
: 103374
: 104425
: 104427
: 104532
: Job s 15-405388-000 15-409511-000
: Miscellaneou
s Number Title Date 16-207 On-Line Nuclear Safety and Generation Risk Assessment:
: Risk Assessment Dates:
: May 9, 2016 through May 16, 2016 May 12, 2016
: Miscellaneou
s Number Title Date
: NPIS-A-Active RCS Leakage Summary Report, Wolf Creek Nuclear Generating Plant
-
: NPIS-A May 5, 2016
: STS
: EF-100B ESW System Inservice Pump B & ESW B Check Valve Test Performed May 5, 2016
==Section 2RS5: Radiation Monitoring Instrumentation==
===Procedures===
: Number Title Revision
: AI 02E-009 Instructions for Intrinsic Germanium Detector Energy Calibration
: AI 02E-010 Instructions for IG Detector Efficiency Calibration
: 7A
: AI 03-008 Control Chart Development, Use and Review Using Lab Stats
: AP 02-008 Verification of Analytical Performance
: AP 02E-001 Chemistry Calibration Program
: RPP 01-405 HP Instrument Program
: RPP 03-407 Testing of Portal Monitors as Passive Whole Body Counters
: 1A
: RPP 06-103 Ludlum 9-4 Calibration
: RPP 06-113 MGP Telepole Calibration
: RPP 06-306 PM12 Calibration
: RPP 06-315 Eberline PCM
-1B Calibration
: RPP 06-317 Eberline PCM
-2 Calibration
: RPP 06-319 SAM11 Calibration
: RPP 06-825 J. L. Shephard Multi
-Source Calibration System Operation
: 8A STS
: IC-452B Channel Calibration New Fuel Storage Facility Criticality Monitor SDRE
-0035 4A STS
: IC-454B Channel Calibration Spent Fuel Pool Criticality Monitor Area Radiation Monitor SDRE
-0038 11
===Condition Reports===
: 83414 88407 93007 97554
: 100307 
: Audits, Self
-Assessments, and Surveillances Number Title Date 14-01-RP/PC Radiation Protection/Solid Radwaste Process Control Programs April 7, 2014
: 14-03-ENV Quality Assurance Audit Report Environmental Management/Effluents December 18, 2014 14-11-CHM Quality Assurance Audit Report: Chemistry December 18, 2014 16-01-RP/PC Radiation Protection/Solid Radwaste Process Control Programs February 24, 2016 16-03-ENV Quality Assurance Audit Report Environmental Management/Effluents March 31, 2016
: K03-001B Instrument Calibration Frequency Evaluation December 17, 2015 NUPIC 23677
: Thermo Fisher Scientific May 15, 2014
: Calibration Records Number Title Date 1503 Liquid Scintillator January 21, 2015 1503 Liquid Scintillator May 23, 2016
: 10066 Whole Body Counter Calibration Certificate September 8, 2015 10178 Telepole March 29, 2016
: 242
: PCM-2 January 21, 2016 10256
: ASP-1/NRD April 6, 2016
: 257
: ASP-1/NRD June 25, 2015
: 11005
: SAM 11
: January 28, 2016 11075 Shepherd Calibrator April 6, 2016
: 11377
: PCM-1B July 27, 2015
: 11451 Radeco H809V
-I May 24, 2016
: 107974
: ASP-1 June 15, 2016
: WO 12-360791 Channel Calibration High Range Area Monitor
: GTRE-0059
: March 21, 2014
: Calibration Records Number Title Date
: WO 12-360792 Channel Calibration High Range Area Radiation Monitor GTRE60 March 22, 2014
: WO 14-389735 Channel Calibration High Range Area Radiation Monitor GTRE59 March 3, 2015
: WO 14-389743 Channel Calibration High Range Area Radiation Monitor GTRE60 March 3, 2015
===Miscellaneous===
: Number Title Date
: WO 15-407110 STN
: IC-534
: WO 15-407112 STN
: IC-535
: WO 15-407152
: STN
: IC-537
: WO 15-407227 Replace GM tube in 0042
: WO 15-407228 Replace GM tube in 0040
: System Health Report: Radiation Monitoring March 31, 2016
: WC Radiation Monitors Considered for Maintenance Rule Equipment May 23, 2016
==Section 2RS6: Radioactive Gaseous and Liquid Effluent Treatment==
===Procedures===
: Number Title Revision
: AI 07B-037 Unit and Radwaste Vent Permits Using RADEAS
: AP 02E-001 Chemistry Calibration Program
: AP 07B-003 Offsite Dose Calculation Manual
: AP 20A-003 QA Audit Requirements, Frequencies, and Scheduling
: CHS
: AX-G01 Unit Vent Sampling and/or Exchange of Filters
: 9A CHS
: RW-G02 Radwaste Vent Sampling and/or Exchange of Filters
: 3D STN
: PE-004 Charcoal Adsorber In
-Place Leak Test Non
-Safety Related Units 11
===Procedures===
: Number Title Revision STN
: SP-010B Channel Operation Test Radwaste Building Vent System Radiation Monitor GH RE
-0010B 9 STS
: PE-002 Charcoal Adsorbent Sampling for Nuclear Safety Related Units 14 STS
: PE-005 HEPA Filter In
-Place Leak Test Safety Related Units
: STS
: PE-006 Charcoal Adsorber In
-Place Leak Test Safety Related Units
===Condition Reports===
: 84942 87594 92222 92921 92959 95488 98578 99405
: 102541
: 102590
: 103675
: 103811
: 103812
: 103813
: Audits, Self
-Assessments, and Surveillances Number Title Date 14-11-CHM Quality Assurance Audit Report: Chemistry December 18, 2014 16-03-ENV Quality Assurance Audit Report Environmental Management/Effluents March 31, 2016
: Gaseous and Liquid Release Permits Permit No.
: System Release Type Date U1GB2014-198 Gas Decay Tank Gas June 25, 2014
: U1GB2015-005 Containment Purge Release Gas January 12, 2015
: U1GC2014-258 Unit Vent Gas December 2, 2014 U1GC2015-039 Radwaste Vent Gas March 12, 2015
: U1LB2016-014 THF04A Liquid March 21, 2016
: U1LC2014-172 Turbine Building Sump to Oily Waste Liquid September 5, 2014 U1LC2015-083 Steam Generator Blowdown to the Lake Liquid October 5, 2015
: In-Place Filter Testing Records Work Order Test
: Date STS
: PE-002 Charcoal Adsorbent Sampling
- FGG02B February 24, 2015 STS
: PE-002 Charcoal Adsorbent Sampling
- FGG02A February 23, 2016 STS
: PE-005 HEPA Filter In
-Place Leak Test
- FGG02B January 17, 2015 STS
: PE-005 HEPA Filter In
-Place Leak Test
- FGG02A February 16, 2015 STS
: PE-005 HEPA Filter In
-Place Leak Test
- FGK01A July 22, 2015
: STS
: PE-006 Charcoal Adsorber In
-Place Leak Test
- FGG02B October 7, 2015 STS
: PE-006 Charcoal Adsorber In-Place Leak Test
- FGG02A February 16, 2015 STS
: PE-006 Charcoal Adsorber In
-Place Leak Test
- FGK01B May 4, 2015
===Miscellaneous===
: Number Title Date
: RA 15-0039 WCNOC 2014 Annual Radioactive Effluent Release Report April 27, 2015
: RA 16-0034 WCNOC 2015
: Annual Radioactive Effluent Release Report April 28, 2016
: System Health Report: Radiation Monitoring March 31, 2016
: WC Radiation Monitors Considered for Maintenance Rule Equipment May 23, 2016
==Section 2RS7: Radiological Environmental Monitoring Program Procedures==
: Number Title Revision
: AI 07B-002 Review of Radiological Environmental Laboratory Analysis Results 12
: AI 07B-004 Reporting of Requirements for the Radiological Environmental Monitoring Program
: AI 07B-005 Radiological Environmental Monitoring Program Implementation
: AI 07B-015 Land Use Census
===Procedures===
: Number Title Revision
: AI 07B-033 Annual Radiological Environmental Operating Report Generation
: AI 07B-034 Radiological Environmental Monitoring Program Air Sampling 12
: AI 07B-035 REMP Optically Stimulated Luminescence
: AP 07B-004 Offsite Dose Calculation Manual (REMP)
: AP 07E-001 Validation of Meteorological Data
===Condition Reports===
: 29337 84764 84920 85428 854 86 854 94 8 5514 8 6521 87608 88 198 88 295 97943 10177
: 103808
: Audits, Self
-Assessments, and Surveillances Number Title Date 14-03-ENV Quality Assurance Audit Report April 24, 2014
: 16-03-ENV Quality Assurance Audit Report April 14, 2016
: 23869 WCNOC Audit Report of Environmental Inc. Midwest Laboratory July 31, 2014
: Calibration and Maintenance Records Number Title Date 15-401597-000 Channel Calibration of Wind Direction Meteorological Instrumentation October 13, 2015 15-401598-000 Channel Calibration of Wind Speed Meteorological Instrumentation October 12, 2015 15-401601-000 Channel Calibration of Sonic Wind Speed Direction Deviation Meteorological Instrumentation October 15, 2015 15-408739-000 Channel Calibration of Sonic Wind Speed Direction Deviation Meteorological Instrumentation April 14, 2016
: 15-408747-000 Channel Calibration of Wind Speed Meteorological Instrumentation April 11, 2016
: 15-408753-000 Channel Calibration of 60M 10M Differential Temperature Instrumentation April 13, 2016
: Calibration and Maintenance Records Number Title Date 15-408750-000 Channel Calibration of Wind Direction Meteorological Instrumentation April 12, 2016
: Digital Venturi Calibrator Serial Number 3302
: February 3, 2016
: Digital Venturi Calibrator Serial Number 3302
: January 21, 2015
===Miscellaneous===
: Number Title Date
: QH-2014-0950 REMP Review of 2011 through 2013 Wind Direction December 11, 2014
: QH-2015-1115 REMP Review of 2012 through 2014 Wind Direction July 23, 2015
: RA-13-0099 Periodic Hydrogeological Review for Groundwater Protection Program September 11, 2013
: 2014 Annual Radiological Environmental Operating Report April 23, 2015
: 2015 Annual Radiological Environmental Operating Report April 15, 2016
==Section 2RS8: Radioactive Solid Waste Processing, and Radioactive Material Handling, Storage, and==
: Transportation
===Procedures===
: Number Title Revision
: AP-31A-100 Solid Radwaste Process Control Program
: CKL-ZL-007 RadWaste Reading Sheets
: CS-OP-PR-008 Setup and Operations of the Energy Solutions Self
-Engaging Dewatering System Fill
-head 4
: CS-OP-PR-009 Ecodex Precoat/Powdex/Solka
-Floc/Diatomaceous Earth/Zoelite Dewatering Procedure for the SEDS
: CS-OP-PR-010 Bead Resin/Activated Carbon Dewatering Procedure for SEDS 3
: HP-1406902 ZERO System Fundamentals
: HW12155801
: Regulations and Requirements Lesson Plan
: 2A HW12155802
: Regulatory Awareness for Hazardous Material Handlers Lesson Plan
: HW8115901 Wolf Creek Hazardous Material Transportation Security Plan
===Procedures===
: Number Title Revision
: LR-23-303-02 High Ammonia Chemistry Lesson Plan
: MG-8306900 DTS Zero Skid for Maintenance
: RPP-07-110 Solid Radwaste Processing
: RPP-07-112 Processing Cartridge Filters
: RPP-07-123 Preparation and Shipment of Radioactive Waste and Material 8
: RPP-07-131 Bead Resin / Activated Carbon Dewatering Procedure for CNSI 14-215 or Smaller Liners
: SYS-BG-207 Adding Chemicals to the Reactor Coolant System 30 TO1515901 Fill Head (SEDS) Installation and Operation
===Condition Reports===
: 84856 84863 86829 91086 91087 91089 91751 96453 96530 96759 97752 98340 98341 98630
: 101503
: 102344
: 102803
: 102820 1028 22
===Miscellaneous===
: Number Title Date 14-01-RP/PC Radiation Protection / Solid Radwaste Process Control Programs April 22, 2014
: 16-01-RP/PC Radiological Protection Process Control February 24, 2016
: 14R52 Radioactive Material Shipping Record December 9, 2014
: 15R45 Radioactive Waste Shipping Record November 10, 2015
: 16R09 Radioactive Waste Shipping Record December 11, 2016
: 342275001 Radioactive RCS Crud Filter Analysis February 21, 2014
: 366240001 Radioactive Sample (DHUT) Analysis February 24, 2015
===Miscellaneous===
: Number Title Date
: 39023003 Radioactive Scaling Factor (RCS Filters) Analysis January 13, 2016
: 390235001 Radioactive Sample (SFP Filter) Analysis February 25, 2016
===Miscellaneous===
: Radioactive Material Shipping Training Records, Selected Individuals May 24, 2016
==Section 4OA1: Performance Indicator Verification==
===Procedures===
: Number Title Revision
: CHA
: RC-004 Gamma Isotopic, Total Curie Content and Dose Equivalent Iodine Determination
: CHA
: RC-005 Determination of Gas Activity
: CHS
: SJ-143B RCS/CVCS/RHR Sampling At SJ
-143 Panel 2 STS
: BB-006 RCS Water Inventory Balance Using the NPIS Computer
===Condition Report===
s
: 105050
: Miscellaneou
s Number Title Revision
: NEI 99-02 Regulatory Assessment Performance Indicator Guideline
==Section 4OA2: Identification and Resolution of Problems==
===Procedures===
: Number Title Revision
: AP 15C-002 Procedure Use and Adherence
: AP 15C-002 Procedure Use and Adherence
: AP 26C-004 Operability Determination and Functionality Assessment
: STN
: MA-001 Main Generator Hydrogen Leak Rate Test
: 16A STN
: MA-001 Main Generator Hydrogen Leak Rate Test
: STS
: IC-508A Refueling Water Storage Tank Level Transmitter Calibration
===Condition Report===
s 99351
: 100589
: 101215
: 104066
: 104184
: 104266
: 104268 10432 2 10432 3
: 104389
: 104390
: 104532
: 104694
: 104703
: 104712
: 104782
: 104801
: 104848
: 104910
: 104959
: 104960
: 105050
: 105307
: 105566
: Miscellaneou
s Number Title Date 16-04-OPS Quality Assurance Audit Report (Operations)
: June 8, 2016
: STN
: MA-001 Main Generator Hydrogen Leak Rate Test Completed May 22, 2016
: STS
: EF-100B ESW System Inservice Pump B & ESW B Check Valve Test Completed May 5, 2016
: STS
: IC-508A Refueling Water Storage Tank Level Transmitter Calibration Completed May 26, 2016
: Quality Oversight Report 1
st Quarter 2016
: May 18, 2016
: Quality Oversight Report 4
th Quarter 2 015 February 17, 2016
==Section 4OA3: ==
: Event Follow
-Up Procedures Number Title Revision
: AP 21G-001 Control of Locked Component Status
: 66A
: AP 21G-001 Control of Locked Component Status
: 66B
: AP 21G-001 Control of Locked Component Status
: AP 21G-001 Control of Locked Component Status
: GEN 00-002 Cold Shutdown To Hot Standby
: 95B STS
: KJ-001 Integrated Diesel Generator and Safeguards Actuation Test - Train A 58 STS
: PE-010A Control Room A/C System Flow Rate Verification A Train
: STS
: PE-010A Control Room A/C System Flow Rate Verification A Train
: STS
: PE-010A Control Room A/C System Flow Rate Verification A Train
: STS
: PE-010A Control Room A/C System Flow Rate Verification A Train
: 2A
===Procedures===
: Number Title Revision STS
: PE-010A Control Room A/C System Flow Rate Verification A Train 3 STS
: PE-010A Control Room A/C System Flow Rate Verification A Train
: 3A STS
: PE-010A Control Room A/C System Flow Rate Verification A Train
: STS
: PE-010B Control Room A/C System Flow Rate Verification B Train
: STS
: PE-010B Control Room A/C System Flow Rate Verification B Train
: STS
: PE-010B Control Room A/C System Flow Rate Verification A Train
: STS
: PE-010B Control Room A/C System Flow Rate Verification A Train
: 2A STS
: PE-010B Control Room A/C System Flow Rate Verification B Train
: STS
: PE-010B Control Room A/C System Flow Rate Verification B Train
: SYS
: GT-121 Containment shutdown Purge System Operation
: SYS
: GT-120 Containment Mini Purge System Operations
===Drawings===
: Number Title Revision M-12GT01 Piping & Instrumentation Diagram Containment Purge Systems HVAC
===Condition Reports===
: 214 58535 60099 78920 84690 92109 92274 95378 96131
: 102455
: 105208
: 105260
: 105540
: 105543
: 105546
: Jobs 12-362198-002 13-373669-002 13-373669-006
===Miscellaneous===
: Number Title Revision/Date 2001-3149 Performance Improvement Request December 18, 2001 2015-011 RER Reportability Determination March 14, 2015
: APF 21G-001-01 Log of Locked Component Manipulations
===Miscellaneous===
: Number Title Revision/Date
: GK-M-001 Cooling and Heating Load Calculation for Control Room HVAC System Capabilities During Normal Plant Operation and Accident Condition
-(SGK04A/B)
: LER 05000482/2014
-001-00 Failure to Comply with Required Action of Technical Specification 3.4.3 while Performing a Vacuum Fill of the Reactor Coolant System March 6, 2014
: LER 05000482/2014
-004-00 Condition Prohibited by Technical Specifications due to an Instrument Tunnel Sump Level Indication Transmitter Incompatible with the Containment Environment July 31, 2014
: LER 05000482/2015
-002-01 Two Control Room Air Conditioning Trains Inoperable Due to Failure to Meet Surveillance Requirement August 26, 2015 LER 05000482/2015
-004-00 Inadequate Procedure Results in Two Containment Isolation Valves being in a Condition Prohibited by Technical Specifications July 1, 2015
: LER 05000482/2015-004-01 Incorrect Decision Results in Two Containment Isolation Valves being in a Condition Prohibited by Technical Specifications September 14, 2015 OE
: GK-12-017 Operability Evaluation
: STS
: PE-010A Control Room A/C System Flow Rate Verification A Train Completed April 18, 2001
: STS
: PE-010A Control Room A/C System Flow Rate Verification A Train Completed October 16, 2002 STS
: PE-010A Control Room A/C System Flow Rate Verification A Train Completed April 14, 2004
: STS
: PE-010A Control Room A/C System Flow Rate Verification A Train Completed October 11, 2005 STS
: PE-010A Control Room A/C System Flow Rate Verification A Train Completed April 12, 2007
: STS
: PE-010A Control Room A/C System Flow Rate Verification A Train Completed April 8, 2010
: STS
: PE-010A Control Room A/C System Flow Rate Verification A Train Completed October 04, 2011 STS
: PE-010A Control Room A/C System Flow Rate Verification A Train Completed August 13, 2013
===Miscellaneous===
: Number Title Revision/Date STS
: PE-010A Control Room A/C System Flow Rate Verification A Train Completed February 19, 2015 STS
: PE-010A Control Room A/C System Flow Rate Verification A Train Completed March 06, 2015
: STS
: PE-010B Control Room A/C System Flow Rate Verification B Train Completed April 3, 2001
: STS
: PE-010B Control Room A/C System Flow Rate Verification B Train Completed October 3, 2002 STS
: PE-010B Control Room A/C System Flow Rate Verification B Train Completed April 1, 2004
: STS
: PE-010B Control Room A/C System Flow Rate Verification B Train Completed September 28, 2005 STS
: PE-010B Control Room A/C System Flow Rate Verification B Train Completed March 28, 2007
: STS
: PE-010B Control Room A/C System Flow Rate Verification B Train Completed September 25, 2008 STS
: PE-010B Control Room A/C System Flow Rate Verification B Train Completed March 22, 2010 STS
: PE-010B Control Room A/C System Flow Rate Verification B Train Completed
: September 19, 2011 STS
: PE-010B Control Room A/C System Flow Rate Verification B Train Completed July 18, 2013 STS
: PE-010B Control Room A/C System Flow Rate Verification B Train Completed January 13, 2015 SYS
: GT-120 Containment Mini purge System Operations Completed May 2, 2015
: WC004976 Calibration Data Sheet December 7, 2015
: WCN-15-CA-CBV-001 Impact of ESW Pipe Chase on Control Building HVAC
: WCN-15-CA-CBV-001 Impact of ESW Pipe Chase on Control Building HVAC
==Section 4OA5: Other Activities==
: Miscellaneou
s Title Documentation of Technique Demonstration Results


==Section 4OA7: ==
: Licensee
-Identified Violations
===Condition Report===
s
: 102344       
: The following items are requested for the Occupational/Public Radiation Safety Inspection At Wolf Creek Nuclear Operating Center
(May 23 - June 23, 2016
)
: Integrated Inspection Report
: 2016002
: Inspection areas are listed in the attachments below.
: Please provide the requested information on or before May 6, 2016.
: Please submit this information using the same lettering system as below.
: For example, all contacts and phone numbers for Inspection Procedure 71124.0
should be in a file/folder titled
"5- A," applicable organization charts in file/folder "
: 5- B," etc.
: If information is placed on ims.certrec.com, please ensure the inspection exit date entered is at least 30 days later than the onsite inspection dates, so the inspectors will have access to the information while writing the report.
: In addition to the corrective action document lists provided for each inspection procedure listed below, please provide updated lists of corrective action documents at the entrance meeting.
: The dates for these lists should range from the end dates of the original lists to the day of the entrance meeting.
: If more than one inspection procedure is to be conducted and the information requests appear to be redundant, there is no need to provide duplicate copies.
: Enter a note explaining in which file the information can be found.
: If you have any questions or comments, please contact Martin Phalen at (817)
: 200-1158 or Martin.Phalen@nrc.gov.
: Alternatively, you can contact Pete Hernandez at (817) 200
-1168 or Pete.Hernandez@nrc.gov.
: PAPERWORK REDUCTION ACT STATEMENT
: This letter does not contain new or amended information collection requirements subject to the Paperwork Reduction Act of 1995 (44 U.S.C. 3501 et seq.).
: Existing information collection requirements were approved by the Office of Management and Budget, control number 3150
-0011.
: 1.
: Radiation Monitoring Instrumentation (71124.05)
: Date of Last Inspection:
: June 2, 2014
: A. List of contacts and telephone numbers for the following areas:
: 1. Effluent monitor calibration
: 2. Radiation protection instrument calibration
: 3. Installed instrument calibrations
: 4. Count room and Laboratory instrument calibrations
: B. Applicable organization charts
: C. Copies of audits, self
-assessments, vendor or NUPIC audits for contractor support and LERs, written since date of last inspection
, related to:
: 1. Area radiation monitors, continuous air monitors, criticality monitors, portable survey instruments, electronic dosimeters, teledosimetry, personnel contamination monitors, or whole body counters
: 2. Installed radiation monitors
: D. Procedure index for:
: 1. Calibration, use
, and operation of continuous air monitors, criticality monitors, portable survey instruments, temporary area radiation monitors, electronic dosimeters, teledosimetry, personnel contamination monitors, and whole body counters.
: 2. Calibration of installed radiation monitors
: E. Please provide specific procedures related to the following areas noted below.
: Additional Specific Procedures will be requested by number after the inspector reviews the procedure indexes.
: 1. Calibration of portable radiation detection instruments (for portable ion chambers) 2. Whole body counter calibration
: 3. Laboratory instrumentation quality control
: F. A summary list of corrective action documents (including corporate and sub
-tiered systems) written since date of last inspection, related to the following programs: 1. Area radiation monitors, continuous air monitors, criticality monitors, portable survey instruments, electronic dosimeters, teledosimetry, personnel contamination monitors, whole body counters,
: 2. Installed radiation monitors,
: 3. Effluent radiation monitors
: 4. Count room radiation instruments
: NOTE: The lists should indicate the significance level of each issue and the search criteria used.
: Please provide in document formats which are "searchable" so that the inspector can perform word searches.
: G. Offsite dose calculation manual, technical requirements manual, or licensee controlled specifications which lists the effluent monitors and calibration requirements.
: H. Current calibration data for the whole body counter's. I. Primary to secondary source calibration correlation for effluent monitors.
: J.
: A list of the point of discharge effluent monitors with the two most recent calibration dates and the work order numbers associated with the calibrations.
: K. Radiation Monitoring System health report for the previous 12 months
: 2. Radioactive Gaseous and Liquid Effluent Treatment (71124.06)
: Date of Last Inspection:
: June 2, 2014
: A. List of contacts and telephone numbers for the following areas:
: 1. Radiological effluent control 2. Engineered safety feature air cleaning systems
: B. Applicable organization charts
: C. Audits, self
-assessments, vendor or NUPIC audits of contractor support, and LERs written since date of last inspection, related to:
: 1.
: Radioactive effluents
: 2.
: Engineered Safety Feature Air cleaning systems
: D. Procedure indexes for the following areas
: 1.
: Radioactive effluents
: 2.
: Engineered Safety Feature Air cleaning systems
: E. Please provide specific procedures related to the following areas noted below.
: Additional Specific Procedures will be requested by number after the inspector reviews the procedure indexes.
: 1. Sampling of radioactive effluents
: 2. Sample analysis
: 3. Generating radioactive effluent release permits
: 4. Laboratory instrumentation quality control
: 5. In-place testing of HEPA filters and charcoal adsorbers
: 6. New or applicable procedures for effluent programs (e.g., including ground water monitoring programs)
: F. List of corrective action documents (including corporate and sub
-tiered systems) written since date of last inspection, associated with:
: 1.
: Radioactive effluents
: 2.
: Effluent radiation monitors
: 3.
: Engineered Safety Feature Air cleaning systems
: NOTE: The lists should indicate the significance level of each issue and the search criteria used.
: Please provide in document formats which are "searchable" so that the inspector can perform word searches.
: G. 2015 Annual Radioactive Effluent Release Report or the two most recent reports.
: H. Current Copy of the Offsite Dose Calculation Manual
: I. Copy of the
: 201 5 inter-laboratory comparison results for laboratory quality control performance of effluent sample analysis, or the two most recent results.
: J. Effluent sampling schedule for the week of the inspection
: K. New entries into 10
: CFR 50.75(g) files since date of last inspection
: L. Operations department
(or other responsible dep ar tment) log records for effluent monitors removed from service or out of service
: M. Listing or log of liquid and gaseous release permits since date of last inspection
: N. A list of the technical specification
-required air cleaning systems with the two most recent surveillance test dates of in
-place filter testing (of HEPA filters and charcoal adsorbers) and laboratory testing (of charcoal efficiency) and the work order numbers associated with the surveillances
: O. System Health Report for radiation monitoring instrumentation.
: Also, please provide a specific list of all effluent radiation monitors that were considered inoperable for 7 days or more since June 2, 2014
.
: If applicable, please provide the relative Special Report and condition report(s).
: P. A list of all radiation monitors that are considered §
: 50.65/Maintenance Rule equipment.
: Q. A list of all significant changes made to the Gaseous and Liquid Effluent Process Monitoring Syst em since the last ins
p ection.
: If applicable, please provide the corresponding UFSAR section in which this change was documented.
: R.
: A list of any occurrences in which a non
-radioactive system was contaminated by a radioactive system.
: Please include any relative condition report(s).
: 7. Radiological Environmental Monitoring Program (71124.07)
: Date of Last Inspection:
: June 2, 2014
: A. List of contacts and telephone numbers for the following areas:
: 1. Radiological environmental monitoring
: 2. Meteorological monitoring
: B. Applicable organization charts
: C. Audits, self
-assessments, vendor or NUPIC audits of contractor support, and LERs written since date of last inspection, related to:
: 1. Radiological environmental monitoring program (including contractor environmental laboratory audits, if used to perform environmental program functions)
: 2. Environmental TLD processing facility
: 3. Meteorological monitoring program
: D. Procedure index for the following areas:
: 1. Radiological environmental monitoring program
: 2. Meteorological monitoring program
: E. Please provide specific procedures related to the following areas noted below.
: Additional Specific Procedures will be requested by number after the inspector reviews the procedure indexes.
: 1. Environmental Program Description
: 2. Sampling, collection and preparation of environmental samples
: 3. Sample analysis (if applicable)
: 4. Laboratory instrumentation quality control
: 5. Procedures associated with the Offsite Dose Calculation Manual
: 6. Appropriate QA Audit and program procedures, and/or sections of the station's QA manual (which pertain to the REMP)
: F. A summary list of corrective action documents (including corporate and sub
-tiered systems) written since date of last inspection, related to the following programs: 1. Radiological environmental monitoring
: 2. Meteorological monitoring
: NOTE: The lists should indicate the significance level of each issue and the search criteria used.
: Please provide in document formats which are "searchable" so that the inspector can perform word searches.
: G. Wind Rose data and evaluations used for establishing environmental sampling locations H. Copies of the 2 most recent calibration packages for the meteorological tower instruments
: I. Copy of the
: 2015 Annual Radiological Environmental Operating Report and Land Use Census, and current revision of the Offsite Dose Calculation Manual, or the two most recent reports.
: J. Copy of the environmental laboratory's inter
-laboratory comparison program results for
: 2015, or the two most recent results, if not included in the annual radiological environmental operating report
: K. Data from the environmental laboratory documenting the analytical detection sensitivities for the various environmental sample media (i
.e., air, water, soil, vegetation, and milk)
: L. Quality Assurance audits (e.g.
, NUPIC) for contracted services
: M. Current NEI Groundwater Initiative Plan and status
: N.
: Technical requirements manual or licensee controlled specifications which lists the meteorological instruments calibration requirements
: O. A list of Regulatory Guides and/or NUREGs that you are currently committed to relative to the Radiological Environmental Monitoring Program
.
: Please include the revision and/or date for the committed item and where this can be located in your current licensing basis/UFSAR.
: P. If applicable, per NEI 07
-07, provide any reports that document any spills/leaks to groundwater since the last inspection
: 8. Radioactive Solid Waste Processing, and Radioactive Material Handling, Storage, and Transportation (71124.08)
: Date of Last Inspection:
: June 2, 2014
: A. List of contacts and telephone numbers for the following areas:
: 1. Solid Radioactive waste processing
: 2. Transportation of radioactive material/waste
: B. Applicable organization charts (and list of all personnel involved in solid radwaste processing, transferring, and transportation of radioactive waste/materials)
: C. Copies of audits, department self
-assessments, and LERs written since date of last inspection related to:
: 1. Solid radioactive waste managemen
t 2. Radioactive material/waste transportation program
: D. Procedure index for the following areas:
: 1. Solid radioactive waste management
: 2. Radioactive material/waste transportation
: E. Please provide specific procedures related to the following areas noted below.
: Additional Specific Procedures will be requested by number after the inspector reviews the procedure indexes.
: 1. Process control program
: 2. Solid and liquid radioactive waste processing 
: 3. Radioactive material/waste shipping
: 4. Methodology used for waste concentration averaging, if applicable
: 5. Waste stream sampling and analysis
: F. A summary list of corrective action documents (including corporate and sub
-tiered systems) written since date of last inspection related to:
: 1. Solid radioactive waste
: 2. Transportation of radioactive material/waste
: NOTE: The lists should indicate the significance level of each issue and the search criteria used.
: Please provide in document formats which are "searchable" so that the inspector can perform word searches.
: G. Copies of training lesson plans for 49CFR172 subpart H, for radwaste processing, packaging, shipping,
: H. A summary of radioactive material and radioactive waste shipments made from date of last inspection to present.
: I.
: Waste stream sample analyses results and resulting scaling factors for 2014 and 2015, or the two most recent results.
: J. Waste classification reports if performed by vendors (such as for irradiated hardware) K. A listing of all onsite radwaste/RAM storage facilities.
: Please include a summary or listing of the items stored in each facility, including the total amount of radioactivity and the highest general area dose rate.
: Although it is not necessary to compile the following information, the inspector will also review: L.
: Training, and qualifications records of personnel responsible for the conduct of radioactive waste processing, package preparation, shipping, and security
.
}}
}}

Latest revision as of 19:38, 19 December 2019

NRC Integrated Inspection Report 05000482/2016002
ML16218A501
Person / Time
Site: Wolf Creek Wolf Creek Nuclear Operating Corporation icon.png
Issue date: 08/03/2016
From: Nick Taylor
NRC Region 4
To: Heflin A
Wolf Creek
nick taylor
References
IR 2016002
Download: ML16218A501 (68)


Text

UNITED STATES ust 3, 2016

SUBJECT:

WOLF CREEK GENERATING STATION - NRC INTEGRATED INSPECTION REPORT 05000482/2016002

Dear Mr. Heflin:

On June 30, 2016, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Wolf Creek Generating Station. On July 27, 2016, the NRC inspectors discussed the results of this inspection with Cleveland Reasoner, Site Vice President, and other members of your staff. Inspectors documented the results of this inspection in the enclosed inspection report.

NRC inspectors documented one finding of very low safety significance (Green) in this report.

This finding involved a violation of NRC requirements. Further, inspectors documented five licensee identified violations, which were determined to be of very low safety significance in this report. The NRC is treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2.a of the NRC Enforcement Policy.

If you contest the violations or significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC resident inspector at the Wolf Creek Generating Station.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region IV and the NRC resident inspector at the Wolf Creek Generating Station.

In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public Inspections, Exemptions, Requests for Withholding, a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRCs Public Document Room or from the Publicly Available Records (PARS) component of the NRC's Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Nicholas H. Taylor, Branch Chief Project Branch B Division of Reactor Projects Docket No.: 50-482 License No.: NPF-42

Enclosure:

Inspection Report 05000482/2016002 w/ Attachments:

1. Supplemental Information 2. Request for Information for the O

REGION IV==

Docket: 05000482 License: NPF-42 Report: 05000482/2016002 Licensee: Wolf Creek Nuclear Operating Corporation Facility: Wolf Creek Generating Station Location: 1550 Oxen Lane NE Burlington, KS 66839 Dates: April 1 through June 30, 2016 Inspectors: D. Dodson, Senior Resident Inspector F. Thomas, Resident Inspector L. Carson II, Senior Health Physicist J. Drake, Senior Reactor Inspector N. Greene, PhD, Health Physicist P. Hernandez, Health Physicist M. Phalen, Senior Health Physicist D. Proulx, Senior Project Engineer W. Sifre, Senior Reactor Inspector C. Stott, Reactor Inspector Approved Nicholas H. Taylor By: Chief, Project Branch B Division of Reactor Projects-1- Enclosure 1

SUMMARY

IR 05000482/2016002; 04/01/2016 - 06/30/2016; Wolf Creek Generating Station; Follow-up of

Events and Notices of Enforcement The inspection activities described in this report were performed between April 1 and June 30, 2016, by the resident inspectors at Wolf Creek Generating Station and inspectors from the NRCs Region IV office. One finding of very low safety significance (Green) is documented in this report. This finding involved a violation of NRC requirements. Additionally, NRC inspectors documented in this report five licensee-identified violations of very low safety significance. The significance of inspection findings is indicated by their color (Green, White, Yellow, or Red),

which is determined using Inspection Manual Chapter 0609, Significance Determination Process. Their cross-cutting aspects are determined using Inspection Manual Chapter 0310,

Aspects within the Cross-Cutting Areas. Violations of NRC requirements are dispositioned in accordance with the NRC Enforcement Policy. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process.

Cornerstone: Mitigating Systems

Green.

The inspectors identified a Green non-cited violation of Technical Specification Limiting Condition for Operation 3.7.11 and 3.0.3 for the licensees failure to place the unit in mode 3 within 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br />, mode 4 within 13 hours1.50463e-4 days <br />0.00361 hours <br />2.149471e-5 weeks <br />4.9465e-6 months <br />, and mode 5 within 37 hours4.282407e-4 days <br />0.0103 hours <br />6.117725e-5 weeks <br />1.40785e-5 months <br /> with two trains (SGK04A and SGK04B) of the control room air conditioning system (CRACS)inoperable. Specifically, the licensee failed to adequately establish CRACS testing flow rate acceptance criteria, which resulted in train A of the safety-related CRACS being inoperable from October 11, 2005, to August 13, 2013; and train B being inoperable from October 3, 2002, to July 18, 2013. The licensees immediate corrective actions included corrective maintenance on the CRACS to increase the airflow to meet acceptance criteria limits. Condition Report 105208 was initiated by the licensee for any necessary process changes and extent of condition actions.

This finding is more than minor because it is associated with the equipment performance attribute of the Mitigating Systems Cornerstone, and affected the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). The inspectors utilized Inspection Manual Chapter 0609.04, Initial Characterization of Findings, and Exhibit 2 of Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, and determined this finding was not a deficiency affecting the design or qualification of a mitigating SSC that maintained its operability or functionality, the finding did not represent a loss of system and/or function, the finding did not represent an actual loss of function of at least a single train for greater than its Technical Specification allowed outage time, and the finding did not represent an actual loss of function of one or more non-Technical Specification trains of equipment designated as high safety-significant. Therefore, the inspectors determined the finding was of very low safety significance (Green). The finding has a cross-cutting aspect in the area of human performance, change management, because leaders did not use a systematic process for evaluating and implementing change so that nuclear safety remains the overriding priority. Specifically, there is not currently a formal process for procedure writers to consider measurement uncertainty when establishing and changing testing acceptance criteria, which resulted in extended inoperability of both the SGK04A and SGK04B units following significant changes to Technical Specifications that included adding surveillance requirements for the SGK04A and SGK04B units in 1999. This issue is indicative of current performance because the same issue would be expected to occur today [H.3]. (Section 4OA3)

Licensee-Identified Violations

Five violations of very low safety significance that were identified by the licensee have been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. These violations and associated corrective action tracking numbers are listed in Section 4OA7 of this report.

PLANT STATUS

Wolf Creek Generating Station operated at or near full power for the entire inspection period.

REPORT DETAILS

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

Readiness for Impending Adverse Weather Conditions

a. Inspection Scope

On April 26, 2016, the inspectors completed an inspection of the stations readiness for impending adverse weather conditions. The inspectors reviewed plant design features, the licensees procedures to respond to severe thunderstorms and tornado watches, and the licensees planned implementation of these procedures. The inspectors evaluated operator staffing and accessibility of controls and indications for those systems required to control the plant.

These activities constituted one sample of readiness for impending adverse weather conditions, as defined in Inspection Procedure 71111.01.

b. Findings

No findings were identified.

1R04 Equipment Alignment

Partial Walk-Down

a. Inspection Scope

The inspectors performed partial system walk-downs of the following risk-significant systems:

  • April 28, 2016, control room air conditioning unit B
  • May 18, 2016, component cooling water pump B
  • June 7, 2016, component cooling water pump D The inspectors reviewed the licensees procedures and system design information to determine the correct lineup for the systems. They visually verified that critical portions of the systems were correctly aligned for the existing plant configuration.

These activities constituted four partial system walk-down samples as defined in Inspection Procedure 71111.04.

b. Findings

No findings were identified.

1R05 Fire Protection

.1 Quarterly Inspection

a. Inspection Scope

The inspectors evaluated the licensees fire protection program for operational status and material condition. The inspectors focused their inspection on four plant areas important to safety:

  • May 25, 2016, fire area F-1, general floor area, elevation 2047 feet
  • June 17, 2016, fire area A-27, motor generator set room, elevation 2026 feet
  • June 29, 2016, fire area ESW-1, essential service water pump house A train, elevation 2000 feet For each area, the inspectors evaluated the fire plan against defined hazards and defense-in-depth features in the licensees fire protection program. The inspectors evaluated control of transient combustibles and ignition sources, fire detection and suppression systems, manual firefighting equipment and capability, passive fire protection features, and compensatory measures for degraded conditions.

These activities constituted four quarterly inspection samples, as defined in Inspection Procedure 71111.05.

b. Findings

No findings were identified.

.2 Annual Inspection

a. Inspection Scope

On June 24, 2015, the inspectors completed their annual evaluation of the licensees fire brigade performance. This evaluation included observation of an unannounced fire drill for a fire in the north end of the auxiliary building, elevation 1974 feet (A-1), on June 24, 2016.

During this drill, the inspectors evaluated the capability of the fire brigade members, the leadership ability of the brigade leader, the brigades use of turnout gear and fire-fighting equipment, and the effectiveness of the fire brigades team operation. The inspectors also reviewed whether the licensees fire brigade met NRC requirements for training, dedicated size and membership, and equipment.

These activities constituted one annual inspection sample, as defined in Inspection Procedure 71111.05.

b. Findings

No findings were identified.

1R07 Heat Sink Performance

.1 Annual Review

a. Inspection Scope

On April 5, 2016, the inspectors completed an inspection of the readiness and availability of risk-significant heat exchangers. The inspectors observed the licensees inspection of the SGK04B control room air-conditioning unit heat exchanger and the material condition of the heat exchanger internals. Additionally, the inspectors walked down the SGK04B heat exchanger to observe its performance and material condition and verified that the SGK04B heat exchanger was correctly categorized under the Maintenance Rule and was receiving the required maintenance.

These activities constituted completion of one heat sink performance annual review sample, as defined in Inspection Procedure 71111.07.

b. Findings

No findings were identified.

.2 Triennial Review

a. Inspection Scope

On May 23, 2016, through May 26, 2016, the inspectors completed an inspection of the readiness and availability of risk-significant heat exchangers. The inspectors reviewed licensee programs to verify heat exchanger performance and operability for the following heat exchangers:

  • Component cooling water heat exchanger A
  • Containment air cooler A
  • Air compressor and aftercooler B
  • Fuel pool cooling pump room cooler B
  • Class 1E switchgear cooler A The inspectors verified whether testing, inspection, maintenance, and chemistry control programs are adequate to ensure proper heat transfer. The inspectors verified that the periodic testing and monitoring methods, as outlined in commitments to NRC Generic Letter 89-13, utilized proper industry heat exchanger guidance. Additionally, the inspectors verified that the licensees chemistry program ensured that biological fouling was properly controlled between tests. The inspectors reviewed previous maintenance records of the heat exchangers to verify that the licensees heat exchanger inspections adequately addressed structural integrity and cleanliness of their tubes.

These activities constitute completion of five triennial heat sink inspection samples as defined in Inspection Procedure 71111.07-05.

b. Findings

No findings were identified.

1R08 Inservice Inspection Activities

a. Inspection Scope

This inspection was focused on closing an Unresolved Item (URI) opened during the performance of Inspection Procedure 71111.08, Inservice Inspection Activities, documented in NRC Inspection Report 05000482/2015001. The inspectors reviewed additional licensing basis information provided by the licensee, as well as industry standards and regulatory guidance. Information in Section 4OA5 of this report documents the resolution of this URI.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program and Licensed Operator Performance

.1 Review of Licensed Operator Requalification

a. Inspection Scope

On May 16, 2014, the inspectors observed an evaluated simulator scenario performed by an operating crew. The inspectors assessed the performance of the operators and the evaluators critique of their performance. The inspectors also assessed the modeling and performance of the simulator during the requalification activities.

These activities constituted completion of one quarterly licensed operator requalification program sample, as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

.2 Review of Licensed Operator Performance

a. Inspection Scope

On June 1, 2016, the inspectors observed the performance of on-shift licensed operators in the plants main control room. At the time of the observations, the plant was in a period of heightened risk due to the ongoing performance of STS IC-508A, Refueling Water Storage Tank Level Transmitter Calibration, Revision 6; during two previous performances of the same procedure on May 19 and 26, 2016, the station received a reactor partial trip alarm concurrent with a low steam line pressure bistable trip.

In addition, the inspectors assessed the operators adherence to plant procedures, including the conduct of operations procedure and other operations department policies.

These activities constituted completion of one quarterly licensed operator performance sample, as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors reviewed one instance of degraded performance or condition of safety-related structures, systems, and components (SSCs):

  • March 10, 2016, SKG04A and SGK04B control room air conditioning units, refrigerant leaks The inspectors reviewed the extent of condition of possible common cause SSC failures and evaluated the adequacy of the licensees corrective actions. The inspectors reviewed the licensees work practices to evaluate whether these may have played a role in the degradation of the SSCs. The inspectors assessed the licensees characterization of the degradation in accordance with 10 CFR 50.65 (the Maintenance Rule), and verified that the licensee was appropriately tracking degraded performance and conditions in accordance with the Maintenance Rule.

These activities constituted completion of one maintenance effectiveness sample, as defined in Inspection Procedure 71111.12.

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed two risk assessments performed by the licensee prior to changes in plant configuration and the risk management actions taken by the licensee in response to elevated risk:

  • April 28, 2106, planned maintenance on control room air conditioning unit A
  • May 25, 2016, planned maintenance outages for emergency diesel generator A and essential service water system A The inspectors verified that these risk assessments were performed timely and in accordance with the requirements of 10 CFR 50.65 (the Maintenance Rule) and plant procedures. The inspectors reviewed the accuracy and completeness of the licensees risk assessments and verified that the licensee implemented appropriate risk management actions based on the results of the assessments.

The inspectors also observed portions of two emergent work activities that had the potential to cause an initiating event and to affect the functional capability of mitigating systems:

  • April 12, 2016, repair of Benton 345 kilovolt offsite power line support structure
  • May 23, 2016, maintenance on emergency diesel generator A channel 1 undervoltage bistable power supply The inspectors verified that the licensee appropriately developed and followed a work plan for these activities. The inspectors verified that the licensee took precautions to minimize the impact of the work activities on unaffected SSCs.

These activities constituted completion of four maintenance risk assessments and emergent work control inspection samples, as defined in Inspection Procedure 71111.13.

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments

a. Inspection Scope

The inspectors reviewed three operability determinations and functionality assessments that the licensee performed for degraded or nonconforming SSCs:

  • June 7, 2016, functionality determination of diesel fire pump The inspectors reviewed the timeliness and technical adequacy of the licensees evaluations. Where the licensee determined the degraded SSC to be operable or functional, the inspectors verified that the licensees compensatory measures were appropriate to provide reasonable assurance of operability or functionality. The inspectors verified that the licensee had considered the effect of other degraded conditions on the operability or functionality of the degraded SSC.

These activities constituted completion of three operability and functionality review samples as defined in Inspection Procedure 71111.15.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed five post-maintenance testing activities that affected risk-significant SSCs:

  • April 6, 2016, SGK04B control room air conditioning unit
  • April 21, 2016, shutdown rod bank E demand counter
  • May 19, 2016, steam line low pressure bistable card replacement
  • May 31, 2016, turbine driven auxiliary feedwater pump test The inspectors reviewed licensing- and design-basis documents for the SSCs and the maintenance and post-maintenance test procedures. The inspectors observed the performance of the post-maintenance tests to verify that the licensee performed the tests in accordance with approved procedures, satisfied the established acceptance criteria, and restored the operability of the affected SSCs.

These activities constituted completion of five post-maintenance testing inspection samples, as defined in Inspection Procedure 71111.19.

b. Findings

No findings were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors observed six risk-significant surveillance tests and reviewed test results to verify that these tests adequately demonstrated that the SSCs were capable of performing their safety functions:

In-service tests:

  • May 5, 2016, STS EF-100B, [Essential Service Water] System Inservice Pump B

& [Essential Service Water] B Check Valve Test, Revision 47

  • June 1, 2016, STS AL-201C, Turbine Driven Auxiliary Feedwater System Inservice Valve Test, Revision 9 Containment isolation valve surveillance tests:
  • April 11, 2016, STS BM-205, "[Steam Generator Blowdown] System Inservice Valve Test, Revision 13 Reactor coolant system leak detection tests:
  • May 4, 2016, STS BB-006, [Reactor Coolant System] Water Inventory Balance Using the NPIS Computer, Revision 14 Other surveillance tests:
  • April 7, 2016, STS GG-001B, Emergency Exhaust Filtration System Train B Operability Test, Revision 23
  • May 12, 2016, STS IC-255B, Channel Operational Test Control Room Air Intake Radiation Monitor, Revision 16A The inspectors verified that these tests met technical specification requirements, that the licensee performed the tests in accordance with their procedures, and that the results of the test satisfied appropriate acceptance criteria. The inspectors verified that the licensee restored the operability of the affected SSCs following testing.

These activities constituted completion of six surveillance testing inspection samples, as defined in Inspection Procedure 71111.22.

b. Findings

No findings were identified.

RADIATION SAFETY

Cornerstones: Public Radiation Safety and Occupational Radiation Safety

2RS5 Radiation Monitoring Instrumentation

a. Inspection Scope

The inspectors evaluated the accuracy and operability of the radiation monitoring equipment used by the licensee to monitor areas, materials, and workers to ensure a radiologically safe work environment. This evaluation included equipment used to monitor radiological conditions related to normal plant operations, anticipated operational occurrences, and conditions resulting from postulated accidents. The inspectors interviewed licensee personnel, walked down various portions of the plant, and reviewed licensee performance associated with radiation monitoring instrumentation, as described below:

  • The inspectors performed walk downs and observations of selected plant radiation monitoring equipment and instrumentation, including portable survey instruments, area radiation monitors, continuous air monitors, personnel contamination monitors, portal monitors, and small article monitors. The inspectors assessed material condition and operability, evaluated positioning of instruments relative to the radiation sources or areas they were intended to monitor, and verified performance of source checks and calibrations.
  • The inspectors evaluated the calibration and testing program, including laboratory instrumentation, whole body counters, post-accident monitoring instrumentation, portal monitors, personnel contamination monitors, small article monitors, portable survey instruments, area radiation monitors, electronic dosimetry, air samplers, and continuous air monitors.
  • The inspectors assessed problem identification and resolution for radiation monitoring instrumentation. The inspectors reviewed audits, self-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution.

These activities constituted completion of the three required samples of radiation monitoring instrumentation, as defined in Inspection Procedure 71124.05.

b. Findings

No findings were identified.

2RS6 Radioactive Gaseous and Liquid Effluent Treatment

a. Inspection Scope

The inspectors evaluated whether the licensee maintained gaseous and liquid effluent processing systems and properly mitigated, monitored, and evaluated radiological discharges with respect to public exposure. The inspectors verified that abnormal radioactive gaseous or liquid discharges and conditions, when effluent radiation monitors are out-of-service, were controlled in accordance with the applicable regulatory requirements and licensee procedures. The inspectors verified that the licensees quality control program ensured radioactive effluent sampling and analysis adequately quantified and evaluated discharges of radioactive materials. The inspectors verified the adequacy of public dose projections resulting from radioactive effluent discharges. The inspectors interviewed licensee personnel and reviewed licensee performance in the following areas:

  • During walk downs and observations of selected portions of the radioactive gaseous and liquid effluent equipment, the inspectors evaluated routine processing and discharge of effluents, including sample collection and analysis.

The inspectors observed equipment configuration and flow paths of selected gaseous and liquid discharge system components, effluent monitoring systems, filtered ventilation system material condition, and significant changes to effluent release points.

  • Calibration and testing program for process and effluent monitors, including National Institute of Standards and Technology (NIST) traceability of sources, primary and secondary calibration data, channel calibrations, set-point determination bases, and surveillance test results.
  • Sampling and analysis controls used to ensure representative sampling and appropriate compensatory sampling. Reviews included results of the inter-laboratory comparison program.
  • Instrumentation and equipment, including effluent flow measuring instruments, air cleaning systems, and post-accident effluent monitoring instruments.
  • Dose calculations for effluent releases. The inspectors reviewed a selection of radioactive liquid and gaseous waste discharge permits and abnormal gaseous or liquid tank discharges, and verified the projected doses were accurate. The inspectors also reviewed 10 CFR Part 61 analyses and methods used to determine which isotopes were included in the source term. The inspectors reviewed land use census results, offsite dose calculation manual changes, and significant changes in reported dose values from previous years.
  • Problem identification and resolution for radioactive gaseous and liquid effluent treatment. The inspectors reviewed audits, self-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution.

These activities constituted completion of the six required samples of radioactive gaseous and liquid effluent treatment program, as defined in Inspection Procedure 71124.06.

b. Findings

No findings were identified.

2RS7 Radiological Environmental Monitoring Program

a. Inspection Scope

The inspectors evaluated whether the licensees radiological environmental monitoring program quantified the impact of radioactive effluent releases to the environment and sufficiently validated the integrity of the radioactive gaseous and liquid effluent release program. The inspectors also verified that the licensee continued to implement the voluntary Nuclear Energy Institute/Industry Ground Water Protection Initiative. The inspectors reviewed or observed the following items:

  • The inspectors observed selected air sampling and dosimeter monitoring stations, sampler station modifications, and the collection and preparation of environmental samples. The inspectors reviewed calibration and maintenance records for selected air samplers, composite water samplers, and environmental sample radiation measurement instrumentation, and inter-laboratory comparison program results. The inspectors reviewed selected events documented in the annual environmental monitoring report and significant changes made by the licensee to the offsite dose calculation manual as the result of changes to the land census. The inspectors evaluated the operability, calibration, and maintenance of meteorological instruments and assessed the meteorological dispersion and deposition factors. The inspectors verified the licensee had implemented a sampling and monitoring program sufficient to detect leakage from SSCs with credible mechanism for licensed material to reach ground water and reviewed changes to the licensees written program for identifying and controlling contaminated spills/leaks to groundwater.
  • Groundwater protection initiative implementation, including assessment of groundwater monitoring results, identified leakage or spill events and entries made into 10 CFR 50.75(g) records, licensee evaluations of the extent of the contamination and the radiological source term, and reports of events associated with spills, leaks, and groundwater monitoring results.
  • Problem identification and resolution for the radiological environmental monitoring program. The inspectors reviewed audits, self-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution.

These activities constituted completion of the three required samples of radiological environmental monitoring program, as defined in Inspection Procedure 71124.07.

b. Findings

No findings were identified.

2RS8 Radioactive Solid Waste Processing and Radioactive Material Handling, Storage,

and Transportation (71124.08)

a. Inspection Scope

The inspectors evaluated the effectiveness of the licensees programs for processing, handling, storage, and transportation of radioactive material. The inspectors interviewed licensee personnel and reviewed the following items:

  • Radioactive material storage waste storage areas including container labeling/marking and monitoring containers for deformation or signs of waste decomposition.
  • Radioactive waste system walk-down including radioactive waste processing and handling equipment. Review of waste processing equipment that is not operational or abandoned in place equipment consistent with system descriptions and the process control program.
  • Waste characterization and classification including radio-chemical sample analysis results for radioactive waste streams and use of scaling factors and calculations to account for difficult-to-measure radionuclides, processes for waste classification including use of scaling factors and 10 CFR Part 61 analysis.
  • Shipment preparation packaging, surveying, labeling, marking, placarding, vehicle checking, driver instructing, and preparation of the disposal manifests.
  • Shipping records including for LSAI, II, III; SCOI, II: Type A or Type B records.
  • Problem identification and resolution for radioactive solid waste processing and radioactive material handling, storage, and transportation. The inspectors reviewed audits, self-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution.

These activities constituted completion of the six required samples of radioactive solid waste processing and radioactive material handling, storage, and transportation program, as defined in Inspection Procedure 71124.08.

b. Findings

No findings were identified.

OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Security

4OA1 Performance Indicator Verification

.1 Reactor Coolant System Specific Activity (BI01)

a. Inspection Scope

The inspectors reviewed the licensees reactor coolant system chemistry sample analyses for the period of April 1, 2015, through March 31, 2016, to verify the accuracy and completeness of the reported data. The inspectors observed a chemistry technician obtain and analyze a reactor coolant system sample on June 13, 2016. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported data.

These activities constituted verification of the reactor coolant system specific activity performance indicator, as defined in Inspection Procedure 71151.

b. Findings

No findings were identified.

.2 Reactor Coolant System Identified Leakage (BI02)

a. Inspection Scope

The inspectors reviewed the licensees records of reactor coolant system identified leakage for the period of April 1, 2015, through March 31, 2016, to verify the accuracy and completeness of the reported data. The inspectors observed the performance of STS BB-006, RCS Water Inventory Balance Using the NPSI Computer, Revision 14, on June 24, 2016. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported data.

These activities constituted verification of the reactor coolant system leakage performance indicator, as defined in Inspection Procedure 71151.

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution

.1 Routine Review

a. Inspection Scope

Throughout the inspection period, the inspectors performed daily reviews of items entered into the licensees corrective action program and periodically attended the licensees condition report screening meetings. The inspectors verified that licensee personnel were identifying problems at an appropriate threshold and entering these problems into the corrective action program for resolution. The inspectors verified that the licensee developed and implemented corrective actions commensurate with the significance of the problems identified. The inspectors also reviewed the licensees problem identification and resolution activities during the performance of the other inspection activities documented in this report.

b. Findings

No findings were identified.

.2 Semiannual Trend Review

a. Inspection Scope

The inspectors reviewed the licensees corrective action program, performance indicators, station performance reports, and other documentation to identify trends that might indicate the existence of a more significant safety issue. The inspectors verified that the licensee was taking corrective actions to address the following identified adverse trends:

  • Procedure use and adherence
  • Operability evaluations These activities constituted completion of one semiannual trend review sample, as defined in Inspection Procedure 71152.

b. Observations and Assessments The inspectors evaluated a sample of issues and events that occurred over the course of the past two quarters to determine whether issues were appropriately considered as emerging or adverse trends. The inspectors verified that these issues were addressed within the scope of the corrective action program or through department review and documentation in the quarterly trend presentation for overall assessment.

The inspectors identified issues associated with implementation of Procedure AP 15C-002, Procedure Use and Adherence:

  • The inspectors identified six separate issues associated with implementation of Procedure AP 15C-002, Procedure Use and Adherence, Revision 41, during one test. Section 6.1.2, for continuous use procedures, states, Review and placekeep each step after completion to ensure the step was performed correctly, and Each step of a continuous use procedure shall be completed or properly N/Ad before proceeding to the next step. On May 5, 2016, the inspectors observed activities associated with completion of Procedure STS EF-100B, [Essential Service Water] System Inservice Pump B & [Essential Service Water] B Check Valve Test, Revision 47, and noted six separate issues associated with the licensee reviewing and placekeeping each step after completion to ensure the step was performed correctly, and the licensee ensuring each step of the continuous use procedure was completed or properly N/Ad before proceeding to the next step. Specifically, Step 8.2.3.3 was inappropriately marked as N/A; Steps 8.2.23.3 and 8.2.23.4 were not performed correctly due to transposition and recording errors; Step 8.2.24.1 utilized an incorrect pressure value; and Step 8.1.17 data was recorded with a unit error. None of these six separate issues were identified by the implementing operations crew or during the operations crew review of the procedure. These issues were entered into the corrective action program as Condition Report 104532.
  • The inspectors identified that Procedure AP 15C-002, Procedure Use and Adherence, Revision 41, Section 6.1.2, for continuous use procedures, states, Perform the step as written in the sequence specified, except when the procedure or approved process specifically allows deviation. On June 1, 2016, the inspectors observed activities associated with completion of Procedure STS IC-508A, Refueling Water Storage Tank Level Transmitter Calibration, Revision 6, and noted that steps were not performed as written in the sequence specified, and the approved process did not specifically allow deviation.

Specifically, personnel did not recognize the need to document supervisor approval to re-perform an as-found data collection step. This issue was entered into the corrective action program as Condition Report 105566.

The inspectors discussed the issues associated with following Procedure AP 15C-002, Procedure Use and Adherence, at the exit meeting on July 27, 2016. The licensee documented Condition Report 106079 in response to the inspectors observations.

The inspectors noted that NRC Inspection Report 05000482/2015004 documented an apparent increase in the number of operability evaluation issues. The inspectors observed apparent station improvement in this area as a result of actions associated with Condition Report 96033, increased control room oversight, and periodic operability determination training. Although operability process implementation improvement was recognized by the inspectors, the inspectors noted some continuing NRC-identified issues. Specifically, these included:

  • The inspectors identified that Procedure AP 26C-004, Determination and Functionality Assessment, Revision 32, states that operability determinations should include whether there is a reasonable expectation of operability, including the basis for the determination and any compensatory measures put in place to establish or restore operability. This procedure was not adequately implemented on two occasions in response to Condition Reports 104268 and 104066. Neither Condition Report 104268 nor Condition Report 104066 adequately addressed operability concerns associated with the emergency diesel generator fuel oil transfer pump control circuitrys potential to activate the thermal overloads that would stop the pump and render the emergency diesel generator inoperable; NCV 05000482/2016007-02, Failure to Verify the Adequacy of Design of the Control Circuitry of the Fuel Oil Transfer Pumps, documents additional details concerning the technical issue. Specifically, the immediate operability screening for both conditions reports was determined to be, N/A, and failed to evaluate the issue for immediate operability. Although an immediate operability determination was not immediately completed, the licensee revised its operability screening, completed an immediate operability determination, and adequately justified operability. This issue was entered into the corrective action program as Condition Report 104322.
  • The licensee identified that the operability determination associated with Condition Report 104910 was inadequately completed. Specifically, a negative trend in B component cooling water pump outboard bearing oil leakage rate was identified, and the operability determination did not quantify the leakage rate and compare that to the mission time specified in AP 26C-004, Operability Screening, Revision 32. After additional information from engineering was received and quantification of the oil leakage rate was completed, the operability determination was changed to Inoperable. A licensee identified violation documented in Section 4OA7 of this report discusses this issue.
  • The inspectors identified that operability evaluations were not always completed in a timely manner while additional information was being gathered to justify operability. Specifically, completion of operability evaluations associated with the 2016 Component Design Basis team inspection and issues associated with resident inspector activities were sometimes delayed to prevent burdening Operations with unanswered questions during operability screenings. Also, operability determinations for issues associated with resident inspector activities and questions were apparently delayed while additional analyses were performed to justify operability. Specifically, following inspector questions that identified issues associated with a penetration into a safety related area, an operability determination and condition report appeared to be delayed to facilitate completion of analysis that could be used to justify operability. Condition Report 105307 documented the inspectors concerns.

The inspectors discussed the continuing operability process issues at the exit meeting on July 27, 2016. The licensee documented Condition Report 106062 to address continuing operability process issues.

c. Findings

No findings were identified.

4OA3 Follow-up of Events and Notices of Enforcement Discretion

.1 (Closed) Licensee Event Report (LER) 05000482/2014-001-00: Failure to Comply with

Required Action of Technical Specification 3.4.3 while Performing a Vacuum Fill of the Reactor Coolant System During a review of outside operating experience on January 6, 2014, the licensee determined that the reactor coolant system pressure was placed in a vacuum condition, in violation of Technical Specification 3.4.3, which specifies a minimum operating pressure of 0 psig. Wolf Creek operators drew a vacuum on the reactor coolant system to support reactor coolant system filling operations on May 8, 2011, and March 30, 2013, using Procedure SYS BB-112, Vacuum Fill of the RCS (to approximately 20 inches of Hg, absolute pressure). Technical Specification 3.4.3, [Reactor Coolant System]

Pressure and Temperature Limits, requires, in part, that the licensee maintain the reactor coolant system pressure, temperature, and heatup and cooldown rates to the limits specified in the Pressure and Temperature Limits Report (PTLR) at all times. The limits of the curves in the PTLR specify a minimum pressure of 0 psig. Required Action C.1 of Technical Specification 3.4.3 specifies that with the reactor coolant system parameters outside of the limits of the PTLR, restore the parameters to within the limits immediately. Because the plant was outside of the PTLR limits with respect to pressure and not restored immediately, the plant was in a condition prohibited by the Technical Specifications, which is reportable pursuant to 10 CFR 50.73(a)(2)(i)(B).

The licensee placed this issue in the corrective action program as Condition Report 78920. For immediate corrective actions, the licensee cancelled the procedure that implemented vacuum fill of the reactor coolant system. The inspectors determined that this constituted a licensee-identified violation, and the enforcement aspects of this violation are discussed in Section 4OA7 of this inspection report.

This licensee event report is closed.

.2 (Closed) LER 05000482/2014-004-00: Condition Prohibited by Technical Specifications

due to an Instrument Tunnel Sump Level Indication Transmitter Incompatible with the Containment Environment On June 2, 2014, the licensee determined that the instrument tunnel sump level indication was inoperable from the period of July 13, 2013, to November 20, 2013, due to erratic and unreliable indication. Therefore, the required actions of Technical Specification 3.4.15 [Reactor Coolant System] Leakage Detection Instrumentation,"

were not met. Because the licensee did not take the required actions of Technical Specification 3.4.15, the plant was in a condition prohibited by the Technical Specifications, which is reportable pursuant to 10 CFR 50.73(a)(2)(i)(B). The licensees root cause analysis determined that the local transmitter was not qualified for the long term exposure of the radiation levels encountered in containment, resulting in the erratic indication.

The licensee placed this issue in the corrective action program as Condition Report 84690. For immediate corrective actions, the licensee instituted compensatory measures for alternate means of identifying reactor coolant system leakage. In April 2015, the licensee replaced the instrument tunnel sump transmitter with two newly designed and fully qualified transmitters, and tested them satisfactorily. The inspectors reviewed the licensees corrective action documents and determined the actions had been completed. The inspectors determined that this constituted a licensee-identified violation, and the enforcement aspects of this violation are discussed in Section 4OA7 of this inspection report.

This licensee event report is closed.

.3 (Closed) LER 05000482/2015-002-00: Two Control Room Air Conditioning Trains

Inoperable Due to Failure to Meet Surveillance Requirement, and LER 05000482/2015-002-01: Two Control Room Air Conditioning Trains Inoperable Due to Failure to Meet Surveillance Requirement

a. Inspection Scope

On April 16, 2015, an apparent cause evaluation associated with Condition Report 92274, Application of SR 3.0.1, identified the potential that the acceptance criteria in Procedures STS PE-010A, Control Room A/C System Flow Rate Verification A Train, and STS PE-010B, Control Room A/C System Flow Rate Verification B Train, may not have been met when the acceptance criteria was revised on January 3, 2013. The acceptance criteria was revised from greater than 18,360 cubic feet per minute (CFM)and less than 22,440 CFM to a new value of greater than 21,012 CFM, which incorporated instrument uncertainty based on vendor information. The licensee determined that the prior performances of STS PE-010A and STS PE-010B did not meet the new acceptance criteria. Additionally, Procedure STS PE-010B was not performed successfully until July 18, 2013, and Procedure STS PE-010A was not performed successfully until August 13, 2013.

The licensee determined that the apparent cause of this event was information in operability evaluation OE-GK-017 that addressed a separate issue on the same equipment, and enabled control room operators and engineering personnel to rationalize the assumption that the change to the acceptance criteria was bounded and did not impact the ability to meet surveillance requirement SR 3.7.11.1.

The licensees immediate corrective actions included performing corrective maintenance on both control room air conditioning system (CRACS) trains to increase the airflow to meet the procedure acceptance criteria, and subsequent performances of Procedures STS PE-010A and STS PE-010B were successful. An adjustable sheave was installed in the B CRACS train in July 2013 and in the A CRACS train in March 2015.

Furthermore, procedure AP 15C-004, Preparation, Review and Approval of Procedures, Instructions and Forms, is being revised to require operations surveillance coordinator review of technical specification surveillance requirement procedures that result in a change in acceptance criteria.

The licensee event report is closed.

b. Findings

Failure to Adequately Establish Control Room Air Conditioning System Testing Flow Rate Acceptance Criteria

Introduction.

The inspectors identified a Green non-cited violation (NCV) of Technical Specification Limiting Condition for Operation (LCO) 3.7.11 and 3.0.3 for the licensees failure to place the unit in mode 3 within 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br />, mode 4 within 13 hours1.50463e-4 days <br />0.00361 hours <br />2.149471e-5 weeks <br />4.9465e-6 months <br />, and mode 5 within 37 hours4.282407e-4 days <br />0.0103 hours <br />6.117725e-5 weeks <br />1.40785e-5 months <br /> with two trains (SGK04A and SGK04B) of the CRACS inoperable.

Specifically, the licensee failed to adequately establish CRACS testing flow rate acceptance criteria, which resulted in train A of the safety-related CRACS being inoperable from October 11, 2005, to August 13, 2013; and train B being inoperable from October 3, 2002, to July 18, 2013.

Description.

Technical Specification LCO 3.7.11, Control Room Air Conditioning System (CRACS), states, Two CRACS trains shall be operable, in modes 1, 2, 3, 4, 5, and 6, and during movement of irradiated fuel assemblies. Technical Specification 3.7.11, Condition B, requires the reactor to be in mode 3 within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> if one train of the CRACS has been inoperable for 30 days. Condition E, requires immediate entry into Technical Specification 3.0.3, if two CRACS trains are inoperable in modes 1, 2, 3, or 4.

Technical Specification 3.0.3, requires, in part, that when an LCO is not met and the associated actions are not met, the unit shall be placed in a mode or other specified condition in which the LCO is not applicable. Action shall be initiated within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> to place the unit, as applicable, in mode 3 within 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br />, mode 4 within 13 hours1.50463e-4 days <br />0.00361 hours <br />2.149471e-5 weeks <br />4.9465e-6 months <br />, and mode 5 within 37 hours4.282407e-4 days <br />0.0103 hours <br />6.117725e-5 weeks <br />1.40785e-5 months <br />.

On December 18, 1999, Wolf Creek Nuclear Operating Corporation implemented license amendment number 123 that converted the Technical Specifications to the improved Technical Specifications. The amendment included new specification 3.7.11, Control Room Air Conditioning System (CRACS), and the new surveillance requirement SR 3.7.11.1. SR 3.7.11.1 verifies that the heat removal capabilities of CRACS units SGK04A and SGK04B are adequate to remove the heat load assumed in the control room during design basis accidents. This surveillance requirement consists of verifying the heat removal capability of the condenser heat exchanger, ensuring the proper operation of major components in the refrigeration cycle, verification of unit air flow capacity, and water flow measurement. Station Procedures STS PE-010A, Control Room A/C System Flow Rate Verification A Train, and STS PE-010B, Control Room A/C System Flow Rate Verification B Train, were initially issued on December 18, 1999.

For verification of unit air flow capacity, acceptance criteria of greater than 20,400 CFM were specified.

On March 11, 2002, the acceptance criteria associated with unit air flow capacity were inappropriately revised to greater than 18,360 CFM and less than 22,440 CFM based on information in ASME/ANSI N510-1980, Testing of Nuclear Air-Cleaning Systems. NRC finding 05000482/2012004-03, Safety-Related Fan Flow Rate Acceptance Criteria Reduced Below Design Basis Limit, which was documented in Inspection Report 05000482/2012004 (ADAMS Accession #: ML12314A296), discusses how ASME/ANSI N510-1980 was incorrectly applied to the testing of the Class IE electrical equipment air-conditioning system.

The acceptance criteria of Procedures STS PE-010A and STS PE-010B remained the same until January 3, 2013, when the acceptance criteria were revised to greater than 21,012 CFM to correct the previously inadequate acceptance criteria of greater than 18,360 CFM and less than 22,440 CFM. Subsequently, on November 6, 2013, Calculation GK-M-001, Cooling and Heating Load Calculation for Control Room

[Heating Ventilation and Air Conditioning] System Capabilities During Normal Plant Operation and Accident Conditions - (SGK04A/B), Revision 3, was issued and revised the minimum required accident air flow to 20,480 CFM. Accounting for 3 percent instrument uncertainty in accordance with vendor documentation, the minimum required accident air flow during testing would have been 21,094 CFM following the November 6, 2013, calculation revision. On April 14, 2015, Calculation WCN-15-CA-CBV-001, Impact of ESW Pipe Chase on Control Building [Heating, Ventilation, and Air Conditioning], Revision 2, was completed and required the design flow be revised to greater than 20,520 CFM. The testing acceptance criteria of STS PE-010A and STS PE-010B were revised to account for 3 percent instrument uncertainty and to add margin, and were revised to 21,250 CFM (without the additional margin, the minimum required accident air flow plus 3 percent for instrument uncertainty is 21,136 CFM).

21,250 CFM is the current STS PE-010A and STS PE-010B unit air flow acceptance criteria for the SGK04A and SGK04B units.

On April 16, 2015, a Wolf Creek apparent cause evaluation associated with Condition Report 92274, Application of SR 3.0.1, identified the potential that the acceptance criteria in Procedures STS PE-010A and STS PE-010B may not have been met when the acceptance criteria were revised on January 3, 2013. The acceptance criteria had been revised from greater than 18,360 CFM and less than 22,440 CFM to a new value of greater than 21,012 CFM. Licensee Event Report 2015-002-01 was submitted to the NRC on August 26, 2015, and stated, From January 3, 2013, through August 13, 2013, the Conditions and Required Actions of LCO 3.7.11, LCO 3.0.3 and LCO 3.0.4 were not met.

Based on questions by the inspectors the licensee initiated Condition Report 105208 to document that from December 18, 1999, until January 3, 2013, instrument uncertainty was not included in the acceptance criteria of STS PE-010A and STS PE-010B. The inspectors noted that LER 2015-002-01 documented that instrument uncertainty was not included in the acceptance criteria of STS PE-010A and STS PE-010B from March 11, 2002, until January 3, 2013. However, the licensees cause evaluation and Licensee Event Report failed to identify that instrument uncertainty had never been included in the STS PE-010A and STS PE-010B acceptance criteria from December 18, 1999, until March 11, 2002.

Also as a result of questions by the inspectors Condition Report 105208 documented that there was no formal process for procedure writers to consider measurement uncertainty when changing acceptance criteria and that a check for measurement uncertainty in the procedure change process was needed. The inspectors concluded that the licensees cause evaluation and LER failed to identify this concern, which appeared to be the original cause of the licensees failure to establish adequate acceptance criteria and failure to recognize the inoperability of trains A and B of the CRACS.

Based on previous performances of STS PE-010A and STS PE-010B and considering the design basis required flow with instrument uncertainty included, SGK04A was inoperable from October 11, 2005, to August 13, 2013; and SGK04B was inoperable from October 3, 2002, to July 18, 2013. Thus, in accordance with Technical Specification 3.7.11, the station should have entered mode 3 on November 3, 2002, with the SGK04B unit inoperable for greater than 30 days. The station did not meet Technical Specification 3.7.11 until August 13, 2013. The SGK04A and SGK04B units were simultaneously inoperable from October 11, 2005, through July 18, 2013. Although the SGK04A and SGK04B units were simultaneously inoperable for an extended period of time, the inspectors noted that the SGK04 units functioned and provided control room cooling throughout the inoperability period, the inspectors noted that licensee air flow calculations contained additional margin, and the inspectors noted that measured air flow rate testing results were never less than required design basis flow rates by more than 1.8 percent, which is less than the 3 percent instrument uncertainty.

The licensees immediate corrective actions included corrective maintenance on the CRACS trains to increase the airflow to meet acceptance criteria limits, Procedures STS PE-010A and STS PE-010B were performed successfully on March 6, 2015, and January 13, 2015, for A and B trains, respectively. Condition Report 105208 was initiated by the licensee for evaluation of any necessary process changes and extent of condition. Furthermore, procedure AP 15C-004, Preparation, Review and Approval of Procedures, Instructions and Forms, is being revised to require operations surveillance coordinator review of technical specification surveillance procedures that result in a change in acceptance criteria.

Analysis.

The inspectors determined that Wolf Creeks failure to establish adequate CRACS testing flow rate acceptance criteria was a performance deficiency that impacted the stations ability to adequately implement Technical Specification surveillance requirement SR 3.7.11, Control Room Air Conditioning System (CRACS). This finding is more than minor because it is associated with the equipment performance attribute of the Mitigating Systems Cornerstone, and affected the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). Specifically, the station operated in a condition prohibited by Technical Specifications with train A of the safety-related CRACS inoperable from October 11, 2005, to August 13, 2013, and train B inoperable from October 3, 2002, to July 18, 2013.

In accordance with Inspection Manual Chapter 0609.04, Initial Characterization of Findings, and Exhibit 2 of Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, issued June 19, 2012, and April 29, 2015, respectively, the performance deficiency affects a mitigating SSC. The inspectors determined this finding was not a deficiency affecting the design or qualification of a mitigating SSC that maintained its operability or functionality, the finding did not represent a loss of system and/or function, the finding did not represent an actual loss of function of at least a single train for greater than its Technical Specification allowed outage time, and the finding did not represent an actual loss of function of one or more non-Technical Specification trains of equipment designated as high safety-significant. Therefore, the inspectors determined the finding was of very low safety significance (Green).

The inspectors determined that in accordance with Inspection Manual Chapter 0310, Aspects Within The Cross-Cutting Areas, issued December 4, 2014, the finding has a cross-cutting aspect in the area of human performance, change management, because leaders did not use a systematic process for evaluating and implementing change so that nuclear safety remains the overriding priority. Specifically, there is not currently a formal process for procedure writers to consider measurement uncertainty when establishing and changing testing acceptance criteria, which resulted in extended inoperability of both the SGK04A and SGK04B units following significant changes to Technical Specifications that included adding surveillance requirements for the SGK04A and SGK04B units in 1999. This issue is indicative of current performance because the same issue would be expected to occur today. Condition Report 105208, which was written in response to the inspectors questions, documents that a check for measurement uncertainty in the procedure change process is needed [H.3].

Enforcement.

Technical Specification 3.7.11, Condition B, requires the reactor to be in mode 3 within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> if one train of the CRACS has been inoperable for 30 days while in mode 1, 2, 3, or 4. Contrary to the above, from November 3, 2002, until August 13, 2013, the reactor was not in mode 3 within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> with one train of the CRACS inoperable for 30 days while in mode 1, 2, 3, or 4. Specifically, the B train of the CRACS was inoperable for 30 days while in mode 1, 2, 3, and 4. The licensee entered this condition into its corrective action program as Condition Report 95378. The licensees immediate corrective actions included corrective maintenance on the CRACS to increase the airflow to meet acceptance criteria limits. Surveillance Procedures STS PE-010A and STS PE-010B were performed successfully on March 6, 2015, and January 13, 2015, for A and B trains, respectively. Condition Report 105208 was initiated by the licensee for any necessary process changes and extent of condition actions. Furthermore, procedure AP 15C-004, Preparation, Review and Approval of Procedures, Instructions and Forms, is being revised to require Operations Surveillance Coordinator review of Technical Specification surveillance procedures that result in a change in acceptance criteria. Because this violation was of very low safety significance and this issue was entered into the licensees corrective action program, this violation is being treated as an NCV, consistent with Section 2.3.2.a of the Enforcement Policy.

(NCV 05000482/2016002-01, Failure to Adequately Establish Control Room Air Conditioning System Testing Flow Rate Acceptance Criteria)

.4 (Closed) LER 05000482/2015-004-00: Inadequate Procedure Results in Two

Containment Isolation Valves being in a Condition Prohibited by Technical Specifications, and LER 05000482/2015-004-01: Incorrect Decision Results in Two Containment Isolation Valves being in a Condition Prohibited by Technical Specifications On May 5, 2015, it was discovered that the motive force (air supply) was not removed for two containment shutdown purge valves as required by Technical Specification 3.6.3, Containment Isolation Valves. The motive force was restored to allow the performance of Procedure STS KJ-001A, Integrated Diesel Generator and Safeguards Actuation Test - Train A, on April 26, 2015. After performance of Procedure STS KJ-001A, the motive force was not removed for the two containment shutdown purge valves. The plant entered Mode 4 on April 28, 2015.

Upon discovery, the air supply valves for the two containment shutdown purge valves were locked closed, removing the motive force. The cause of the event was determined to be the decision to only track components listed on a locked component log using Form APF 21G-001-01, Log of Locked Component Manipulations, Revision 1, during plant start up, which allowed a mode change with components out of position. Each impacted penetration flow path had a redundant valve that was closed with the motive force removed.

The licensee implemented the following corrective actions:

(1) On May 5, 2015, the air supply valves for GTHZ0007 and GTHZ0009 were locked closed and verified, which removed the motive force; and
(2) Procedure AP 21G-001, Control of Locked Component Status, was revised to ensure an Equipment Out of Service Log entry was made for components required to be locked by technical specifications. The inspectors determined that this constituted a licensee-identified violation, and the enforcement aspects of this violation are discussed in Section 4OA7 of this inspection report.

The licensee event reports are closed.

These activities constituted completion of four event follow-up samples, as defined in Inspection Procedure 71153.

4OA5 Other Activities

(Closed) Unresolved Item (URI)05000482/2015001-01, Questions Related to Ultrasonic Examination of Reactor Vessel Flange Stud Hole Threads On May 7, 2015, the NRC issued Wolf Creek Nuclear Operating Corporation a URI related to the examination technique utilized by the licensee to perform reactor vessel flange ligament inspections for ASME Code compliance. The concern was that the technique being utilized by the licensee might not provide adequate coverage of the required examination area and may not be capable of detecting indications orientated on a plane normal to the axis of the stud that were equal to or exceeded 0.2 inch, as measured radially from the root of the thread, as required by the licensee's procedure and Section XI of the ASME Code. Demonstrations of the technique were completed by the licensee and verified that the technique could detect flaws in the required examination area. The results of these demonstrations were reviewed by the NRC staff and considered acceptable. Based on these facts, the NRC considers this item to be closed and no follow-up inspection activity for this item is planned.

No findings were identified. The unresolved item is closed.

4OA6 Meetings, Including Exit

Exit Meeting Summary

On May 26, 2016, regional inspectors presented the final heat sink performance inspection results to Mr. J. McCoy, Vice President, Engineering, and other members of the licensee staff.

The licensee acknowledged the issues presented. The inspector asked the licensee whether any materials examined during the inspection should be considered proprietary. Proprietary information was returned or destroyed.

On June 10, 2016, regional inspectors presented the inservice inspection activity inspection results via telephonic exit to Mr. W. Muilenburg, Supervisor, Licensing. The licensee acknowledged the issue presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.

On June 23, 2016, regional inspectors presented the radiation safety inspection results to Mr. M. Skiles, and other members of the licensee staff via teleconference. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.

On July 27, 2016, the resident inspectors presented the inspection results to Cleveland Reasoner, Site Vice President, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.

4OA7 Licensee-Identified Violations

The following violations of very low safety significance (Green) were identified by the licensee and are violations of NRC requirements, which meet the criteria of the NRC Enforcement Policy for being dispositioned as NCVs.

  • Technical Specification 5.7.2 states, in part, that high radiation areas with dose rates greater than 1.0 rem per hour at 30 centimeters shall be conspicuously posted as a high radiation area and shall be provided with a locked or continuously guarded door or gate to prevent unauthorized entry. Contrary to the above, on January 27, 2016, room 7406 on the 2013 foot elevation of the radwaste building areas had dose rates greater than 1.0 rem per hour and was not conspicuously posted as a high radiation area nor provided with a locked or continuously guarded door or gate to prevent unauthorized entry. This issue was identified by radiation protection technicians performing radiological surveys in the area. The licensee documented this issue in the corrective action program as Condition Report 102344. The finding was determined to be of very low safety significance (Green) because it was not an as-low-as-reasonably-achievable planning issue, there was no overexposure or potential for overexposure, and the licensees ability to assess dose was not compromised.
  • Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, requires, in part, that activities affecting quality shall be accomplished in accordance with documented instructions, procedures, or drawings of a type appropriate to the circumstances. Licensee Procedure AP 26C-004, Operability Determination and Functionality Assessment, Revision 32, an Appendix B quality related procedure, provides instructions for determining whether equipment is operable when oil leakage is identified. Procedure AP 26C-004, Step 6.2.1.1, states in part, that if operability of a system/component is being questioned due to system leakage that the leak rate has been quantified and total identified leakage for the affected system has been determined and compared to the limits of Attachment F, Allowable Oil Leakage for Successful Mission. Contrary to the above, from May 28, 2016, until May 31, 2016, operability of a system/component was being questioned due to system leakage and the leak rate had not been quantified and the total identified leakage for the affected system was not determined and compared to the limits of Attachment F, Allowable Oil Leakage for Successful Mission. Specifically, operability of the B component cooling water pump was questioned due to system leakage as documented in Condition Report 104910, and the leak rate had not been quantified and the total identified leakage for the affected system was not determined, which resulted in the immediate operability determination being incorrect and the immediate operability determination requiring revision.

Immediate corrective actions included revising the immediate operability determination for the B component cooling water pump from operable to inoperable, generating a required reading for senior reactor operators, and documenting Condition Report 104959. Using Exhibit 2, Mitigating Systems Screening Questions, of Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process for Finding At-Power, dated June 19, 2012, the inspectors determined this finding was not a deficiency affecting the design or qualification of a mitigating SSC that maintained its operability or functionality, the finding did not represent a loss of system and/or function, the finding did not represent an actual loss of function of at least a single train for greater than it Technical Specification allowed outage time, and the finding did not represent an actual loss of function of one or more non-Technical Specification trains of equipment designated as high safety-significant. Therefore, the inspectors determined the finding was of very low safety significance (Green).

Section 2.1.2 of the PTLR specifies that the reactor coolant system shall be maintained within the parameters of Figure 2.1-1 of the PTLR, which specifies a minimum pressure of 0 psig. Required Action C.1 of Technical Specification 3.4.3 specifies that with the reactor coolant system parameters outside the limits of the PTLR, restore the parameters to within the limits immediately. Contrary to the above, on May 8, 2011, and March 30, 2013, with the reactor coolant system parameters outside the limits of the PTLR, parameters were not restored to within the limits immediately. Specifically, the licensee drew a vacuum on the reactor coolant system to less than 0 psig to support filling operations but did not take action to immediately restore the reactor coolant system pressure to greater than or equal to 0 psig, as specified in the PTLR. The licensee placed this issue in the corrective action program as Condition Report 78920.

The licensee performed Engineering Evaluation EER 92-BB-02 and determined that drawing a vacuum on the reactor coolant system would not result in excessive stresses for reactor coolant system structures, systems and components. Using Manual Chapter 0609, Appendix G, Shutdown Operations Significance Determination Process, dated May 9, 2014, this issue screened to Green because it did not result in a loss of reactor coolant system barrier integrity.

  • Technical Specification 3.4.15, [Reactor Coolant System] Leakage Detection Instrumentation, states, in part, that reactor coolant system leakage detection instrumentation shall be operable, including the containment sump level and flow monitoring system. Required Action A of Technical Specification 3.4.15, states, in part, that with the required containment sump level and flow monitoring system inoperable, restore the required containment sump level and flow monitoring system to operable status within 30 daysif the required action and associated completion time are not met, Condition E requires the reactor to be in mode 3 within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in mode 5 within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />. Contrary to the above, from the period of July 13, 2013, to November 20, 2013, with the containment sump level and flow monitoring system inoperable for greater than 30 days, the reactor was not placed in mode 3 within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> or mode 5 within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />.

Specifically, the instrument tunnel sump level indication was inoperable because of erratic indication, but the licensee did not take the required action of Technical Specification 3.4.15. The licensee placed this issue in the corrective action program as Condition Report 84690. Using Manual Chapter 0609, Appendix A, Significance Determination Process, for Findings at Power, dated June 19, 2012, this issue screened to Green because it did not result in reactor coolant system leakage or degrade the licensees ability to detect and mitigate a small break loss of coolant accident.

  • Technical Specification 3.6.3, Containment Isolation Valves, requires each containment isolation valve to be operable in modes 1, 2, 3, and 4. To be operable, containment isolation valves GTHZ0007 and GTHZ0009, which are Category 3 valves, must be closed with the motive force removed. Technical Specification 3.6.3, Condition A, Required Action A.1, requires, in part, that the affected penetration flow path for any inoperable Category 3 containment isolation valve be isolated within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

Additionally, Required Action A.2, requires, in part, that the licensee verify the affected penetration flow path is isolated prior to entering mode 4 from mode 5. Contrary to the above, from April 28, 2015, through May 5, 2015, the licensee failed to verify the affected penetration flow path was isolated prior to entering mode 4 from mode 5 on April 28, 2015. As a result, Technical specification 3.6.3, Condition A, was not met On May 5, 2015, the licensee discovered that the motive force for valves GTHZ0007 and GTHZ0009 was not removed and the air supply valves had not been locked closed, and the affected penetration flow paths were not isolated prior to entering mode 4 from mode 5 on April 28, 2015. The inspectors noted that although the motive force was not removed for valves GTHZ0007 and GTHZ0009, the valves were in their closed safeguards positions and redundant valves in series were closed with the motive force removed, which ensured each penetration flow path had one operable valve closed with its motive force removed. Using Exhibit 3, Barrier Integrity Screening Questions, of Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process for Finding At-Power, dated June 19, 2012, the inspectors determined the finding did not represent an actual open pathway in the physical integrity of reactor containment (valves, airlocks, etc.), containment isolation system (logic and instrumentation), or heat removal components, and the finding did not involve an actual reduction in function of hydrogen igniters in the reactor containment. Therefore, the inspectors determined that this finding is of very low safety significance (Green).

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

C. Adkinson, Environmental Biologist IV
T. Baban, Manager, System Engineering
W. Brown, Superintendent, Security Operations
T. Broyles, Manager, Information Services
D. Campbell, Superintendent, Maintenance
C. Carman, Supervisor, Chemistry
J. Dorsey, Technician I, Chemistry
T. East, Superintendent, Emergency Planning
J. Edwards, Manager, Operations
D. Erbe, Manager, Security
R. Flannigan, Manager, Nuclear Engineering
K. Fredrickson, Engineer, Licensing
J. Freeman, Supervisor of Treatment Systems, Operations
J. Fritton, Oversight
C. Garcia, Supervisor Engineer
D. Gibson, Master HP Technician
C. Gross, Manager, Chemistry
D. Grove, Superintendent, Maintenance Support
C. Hafenstine, Manager, Regulatory Affairs
A. Heflin, President and Chief Executive Officer
S. Henry, Manager, Integrated Plant Scheduling
P. Herrman, Manager, Engineering Programs
R. Hobby, Licensing Engineer
J. Isch, Superintendent, Operations Work Controls
J. Jenek, Quality Specialist iii
B. Ketchum, Supervisor Engineer
B. Lee, Licensed Supervising Instructor
M. Legresley, Engineer
K. Lemaster, Master Technician, Chemistry
D. Mand, Manager, Design Engineering
N. Mayhew, Engineer III
J. McCoy, Vice President, Engineering
M. McMullen, Design Engineer
C. Medenciy, Radioactive Materials Shipper
C. Menke, Supervisor Maintenance
K. Miller, Master Instruments and Controls Technician
N. Mingle, Engineer
K. Mitchell, Master Chemistry Technician
W. Muilenburg, Supervisor, Licensing
L. Ratzlaff, Manager, Maintenance
R. Raymer, Engineering Technologist V
C. Reasoner, Site Vice President
T. Rice, Technician III, Safety
J. Rudeen, Supervisor, Regulatory Support
K. Sheridan, Engineer III

Attachment 1

M. Skiles, Manager, Radiation Protection
T. Slenker, Supervisor, Operations Support
S. Smith, Plant Manager
M. Staiger, Engineer II
L. Stevens, Licensing Engineer V
L. Stone, Licensing Engineer V
A. Stull, Vice President and Chief Administrative Officer
J. Suter, Supervisor Engineer
M. Tate, Superintendent, Security Operations
J. Truelove, Supervisor, Chemistry
J. Vopat, Technician II, Chemistry

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened/Closed

05000482/2016002-01 NCV Failure to Adequately Establish Control Room Air Conditioning System Testing Flow Rate Acceptance Criteria (4OA3)

Closed

05000482/2014-001-00 LER Failure to Comply with Required Action of Technical Specification 3.4.3 while Performing a Vacuum Fill of the Reactor Coolant System (4OA3)
05000482/2014-004-00 LER Condition Prohibited by Technical Specifications due to an Instrument Tunnel Sump Level Indication Transmitter Incompatible with the Containment Environment (4OA3)
05000482/2015-001-01 URI Questions Related to Ultrasonic Examination of Reactor Vessel Flange Stud Hole Threads (4OA5)
05000482/2015-002-00 LER Two Control Room Air Conditioning Trains Inoperable Due to Failure to Meet Surveillance Requirement (4OA3)
05000482/2015-002-01 LER Two Control Room Air Conditioning Trains Inoperable Due to Failure to Meet Surveillance Requirement (4OA3)
05000482/2015-004-00 LER Inadequate Procedure Results in Two Containment Isolation Valves being in a Condition Prohibited by Technical Specifications (4OA3)
05000482/2015-004-01 LER Incorrect Decision Results in Two Containment Isolation Valves being in a Condition Prohibited by Technical Specifications (4OA3)

LIST OF DOCUMENTS REVIEWED