IR 05000482/2023004
ML24004A058 | |
Person / Time | |
---|---|
Site: | Wolf Creek ![]() |
Issue date: | 01/11/2024 |
From: | Greg Werner NRC/RGN-IV/DORS/PBB |
To: | Reasoner C Wolf Creek |
References | |
IR 2023004 | |
Download: ML24004A058 (18) | |
Text
January 11, 2024
SUBJECT:
WOLF CREEK GENERATING STATION - INTEGRATED INSPECTION REPORT 05000482/2023004
Dear Cleve Reasoner:
On December 31, 2023, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Wolf Creek Generating Station. On January 11, 2024, the NRC inspectors discussed the results of this inspection with J. McCoy, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.
No findings or violations of more than minor significance were identified during this inspection.
This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely, Gregory E. Werner, Chief Reactor Projects Branch B Division of Operating Reactor Safety Docket No. 05000482 License No. NPF-42
Enclosure:
As stated
Inspection Report
Docket Number:
05000482
License Number:
Report Number:
Enterprise Identifier:
I-2023-004-0002
Licensee:
Wolf Creek Nuclear Operating Corp.
Facility:
Wolf Creek Generating Station
Location:
Burlington, KS
Inspection Dates:
October 1 to December 31, 2023
Inspectors:
K. Chambliss, Senior Resident Inspector
S. Hedger, Senior Emergency Preparedness Inspector
C. Henderson, Senior Resident Inspector
H. Strittmatter, Emergency Preparedness Inspector
W. Tejada, Senior Physical Security Inspector
J. Vera, Resident Inspector
Approved By:
Gregory E. Werner, Chief
Reactor Projects Branch B
Division of Operating Reactor Safety
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Wolf Creek Generating Station, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
List of Findings and Violations
No findings or violations of more than minor significance were identified.
Additional Tracking Items
None.
PLANT STATUS
Wolf Creek Generating Station began the inspection period at full power. On October 23, 2023, the licensee reduced power to 70 percent for flexible power operations (based on daily market demand) and commenced power accession to 100 percent on October 24, 2023, when a tube leak was identified in low pressure feedwater heater 2B. The licensee, in accordance with off-normal procedure associated low pressure heater tube leaks, lowered power to 47 percent to commence repairs of low-pressure feedwater heater 2B. On October 29, 2023, the licensee raised power to 67 percent for conducting repairs of the low-pressure feedwater heater 2B and returned to full power on October 31, 2023. The unit remained at full power for the remainder of the inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, Appendix D, Plant Status, observed risk significant activities, and completed onsite portions of IPs. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.01 - Adverse Weather Protection
Seasonal Extreme Weather Sample (IP Section 03.01) (1 Sample)
- (1) The inspectors evaluated readiness for seasonal extreme weather conditions prior to the onset of seasonal cold temperatures for the following systems:
- station blackout diesel generator diesel fuel oil cloud point and refuel water storage tank loss of insulation on December 8, 2023
71111.04 - Equipment Alignment
Partial Walkdown Sample (IP Section 03.01) (2 Samples)
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
(1)train A essential service water system on October 24, 2023 (2)control room envelope and emergency core cooling system leakage paths to the refueling water storage tank on November 6, 2023
71111.05 - Fire Protection
Fire Area Walkdown and Inspection Sample (IP Section 03.01) (2 Samples)
The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:
(1)volume control tank room (room 1318) transient combustible loading, fire area A-8, on October 3, 2023 (2)train B component cooling water pump room, fire area A-16, on October 16, 2023
71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)
- (1) The inspectors observed and evaluated licensed operator performance in the control room during flexible power operations (based on daily market demand) on October 23, 2023.
Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)
- (1) The inspectors observed and evaluated the licensed operator evaluation and training scenarios on October 31, 2023.
71111.12 - Maintenance Effectiveness
Maintenance Effectiveness (IP Section 03.01) (1 Sample)
The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components remain capable of performing their intended function:
(1)control room and building envelope maintenance effectiveness on November 6, 2023
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Risk Assessment and Management Sample (IP Section 03.01) (1 Sample)
The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:
(1)low pressure feedwater heater 2B tube leak emergent work activities on October 30, 2023
71111.15 - Operability Determinations and Functionality Assessments
Operability Determination or Functionality Assessment (IP Section 03.01) (4 Samples)
The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:
(1)emergency diesel generator B east bank air distributor leak operability determination on October 4, 2023 (2)emergency diesel generator B silencer degraded weld past operability determination on October 11, 2023 (3)essential service water SMB-000 motor-operated valves nonconforming condition operability determination on October 18, 2023 (4)train B component cooling water room cooler calculation failure to include all required heat inputs operability determination on October 26, 2023
71111.24 - Testing and Maintenance of Equipment Important to Risk
The inspectors evaluated the following testing and maintenance activities to verify system operability and/or functionality:
Post-Maintenance Testing (PMT) (IP Section 03.01) (4 Samples)
(1)control room ventilation isolation system card replacement post-maintenance testing on October 10, 2023 (2)emergency diesel generator B silencer weld repair post-maintenance testing on October 27, 2023 (3)emergency diesel generator B engine driven jacket water pump discharge check valve removal and inspection post-maintenance testing on October 27, 2023 (4)emergency diesel generator B starting air system leak repair post-maintenance testing on October 27, 2023
Surveillance Testing (IP Section 03.01) (2 Samples)
(1)train B essential service water discharge check valve surveillance testing on November 8, 2023 (2)control room ventilation system flow rate and combined pressure drop test on November 29, 2023
71114.01 - Exercise Evaluation
Inspection Review (IP Section 02.01-02.11) (1 Sample)
- (1) The inspectors evaluated the biennial emergency plan exercise conducted on November 14, 2023. The exercise scenario simulated damage to the containment emergency personnel hatches; an emergency diesel generator control failure, tornado damage onsite to safety system equipment; loss of offsite electrical sources; a turbine driven auxiliary feedwater pump trip, a loss of reactor coolant system coolant; and degradation of core cooling that results in fuel cladding damage.
71114.04 - Emergency Action Level and Emergency Plan Changes
Inspection Review (IP Section 02.01-02.03) (1 Sample)
- (1) The inspectors evaluated the following submitted Emergency Action Level and Emergency Plan changes.
"On Shift Staffing Analysis," revision 2, submitted February 13, 2023
- EP 06-012, "Dose Assessment," revisions 18 and 18A, submitted on May 16, 2023
- APF 06-002-02, "Emergency Action Levels Technical Bases," revision 2, submitted November 1, 2023 Several screenings and evaluations associated with the 10 CFR 50.54(q) emergency plan change process were reviewed as well. These evaluations do not constitute NRC approval.
71114.08 - Exercise Evaluation - Scenario Review
Inspection Review (IP Section 02.01 - 02.04) (1 Sample)
- (1) The inspectors reviewed the licensee's preliminary exercise scenario that was submitted to the NRC on September 12, 2023 (ML23255A284 and ML23255A285),for the exercise scheduled on November 14, 2023. The inspectors discussed the preliminary scenario comments with J. Bousum, Manager, Emergency Planning, and other members of the emergency planning staff on October 12, 2023. The inspectors' review does not constitute NRC approval of the scenario.
OTHER ACTIVITIES - BASELINE
===71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:
MS08: Heat Removal Systems (IP Section 02.07)===
- (1) October 1, 2022, through September 30, 2023
MS09: Residual Heat Removal Systems (IP Section 02.08) (1 Sample)
- (1) October 1, 2022, through September 30, 2023
EP01: Drill/Exercise Performance (DEP) Sample (IP Section 02.12) (1 Sample)
- (1) July 1, 2022, through September 30, 2023 EP02: Emergency Response Organization (ERO) Drill Participation (IP Section 02.13) (1 Sample)
- (1) July 1, 2022, through September 30, 2023 EP03: Alert And Notification System (ANS) Reliability Sample (IP Section 02.14)
In that the licensee transitioned its alert and notification system (ANS) to a purely non-siren based system in April 2020, the ANS PI and associated data is no longer required to be reported by the licensee. Thus, it is not subject to further inspection/verification per IP 71151. Evaluation of the licensee's non-siren based ANS is completed separately per IP 71114.02, Alert and Notification System Evaluation.
71152A - Annual Follow-up Problem Identification and Resolution Annual Follow-up of Selected Issues (Section 03.03)
The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:
(1)missed fire watch corrective actions effectiveness review on November 6, 2023 (2)essential service water motor-operated valve lock rotor condition and 480 volt breaker not automatically tripping open on November 27, 2023
71152S - Semiannual Trend Problem Identification and Resolution Semiannual Trend Review (Section 03.02)
- (1) The inspectors reviewed the licensees corrective action program for potential adverse trends in age-related equipment degradation and impacts on equipment reliability that might be indicative of a more significant safety issue on December 14,
INSPECTION RESULTS
No findings were identified.
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
- On October 12, 2023, the inspectors presented the emergency preparedness exercise scenario inspection results to J. Bousum, Manager, Emergency Planning, and other members of the licensee staff.
- On December 20, 2023, the inspectors presented the emergency preparedness exercise inspection results to J. McCoy, Site Vice President, and other members of the licensee staff.
- On January 11, 2024, the inspectors presented the integrated inspection results to J. McCoy, Site Vice President, and other members of the licensee staff.
DOCUMENTS REVIEWED
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Corrective Action
Documents
Condition Reports
10027755, 10028182, 10028233, 10028306
Drawings
M-12BN01
Piping and Instrumentation Diagram Borated Refueling
Water Storage Tank
Drawings
M-12EC01
Piping and Instrumentation Diagram Fuel Pool Cooling and
Clean-up System
Drawings
M-12EC02
Piping and Instrumentation Diagram Fuel Pool Cooling and
Clean-up System
Miscellaneous
WCRE-34
Fourth 10-Year Interval Inservice Testing Basis Document
Procedures
Operability Determination and Functionality Assessments
Procedures
CKL ZL-009
Site Reading Sheets
29
Procedures
SYS EC-121
Recirc of the RWST Through the Fuel Pool Cleanup System
Procedures
SYS OPS-008
Cold Weather Operation
Work Orders
Calculations
AN-99-020
Control Room Habitability of a Postulated LOCA, based on a
Control Room Unfiltered Inleakage of 20.0 cfm
Corrective Action
Documents
Condition Reports
25216, 137179, 10025355
Corrective Action
Documents
Resulting from
Inspection
Condition Report
10028359
Drawings
M-12BG03
Piping and Instrumentation Diagram Chemical & Volume
Drawings
M-12BN01
Piping and Instrumentation Diagram Borated Refueling
Water Storage System
Drawings
M-12EJ01
Piping and Instrumentation Diagram Residual Heat Removal
System
Drawings
M-12EM01
Piping and Instrumentation Diagram High Pressure Coolant
Injection System
Drawings
M-12EN01
Piping and Instrumentation Diagram Containment Spray
System
Drawings
M-K2EF01
Piping and Instrumentation Diagram Essential Service Water
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
System
Engineering
Changes
SA-17-001
Control Room A/C and SAS Door Maximum Breach Time to
Support Control Room Dose Limits
Miscellaneous
WCRE-34
Fourth 10-Year Interval Inservice Testing Basis Document
Miscellaneous
WCRE-35
Boundary Matrix
Procedures
AP 23-009
Control Room Envelope Habitability Program
3A
Procedures
CKL EF-120
Essential Service Water Valve, Breaker and Switch Lineup
Procedures
EMG ES-12
Transfer to Cold Leg Recirculation
Procedures
STS BN-206
Borated Refueling Water Storage System Inservice Valve
Test
Procedures
STS CV-210A
ECCS SI Comprehensive Pump and Inservice Check Valve
Test
Procedures
STS PE-061
Control Room/Control Building Habitability Test
Work Orders
21-473908-000, 21-474136-000, 22-477646-00
Calculations
XX-X-004
Combustible Fire Loading for Each Room in the Various Fire
Areas at WCNOC
Corrective Action
Documents
Resulting from
Inspection
Condition Reports
10027534, 10027679
Miscellaneous
Transient Combustible Permit - PT17458
Miscellaneous
E-1F9905
Fire Hazard Analysis
Procedures
AP 10-102
Control of Combustible Materials
Procedures
AP 10-106
Fire Preplans
Procedures
AI 21-300
Flexible Power Operations
Procedures
AP 21-001
Conduct of Operations
Procedures
GEN 00-004
Power Operation
101A
Calculations
AN-99-020
Control Room Habitability of a Postulated LOCA, based on a
Control Room Unfiltered Inleakage of 20.0 cfm
Calculations
GK-M-001
Cooling and Heating Load Calculation for Control Room
HVAC System Capabilities during Normal Plant Operation
and Accident Conditions - (SGK04A/B)
Corrective Action
Documents
Condition Reports
106725, 10007817, 10007842, 10011825, 10016478,
10024531, 10025355, 10026107, 10027306, 10027564
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Miscellaneous
BAP-23-0136
Breach Authorization Permit
05/18/2023
Miscellaneous
WCRE-35
Boundary Matrix
4, 5, 6, 7, 10
Procedures
AP 10-104
Breach Authorization
Procedures
AP 23-009
Control Room Envelope Habitability Program
3A
Procedures
EMG E-0
Reactor Trip or Safety Injection
Procedures
MPE VD-001
M627A Ventilation Damper Maintenance
Procedures
STS PE-004
Aux Building and Control Room Pressure Test
Procedures
STS PE-009
Control Room Ventilation System Flow Rate and Combined
Pressure Drop Test
8B
Procedures
STS PE-010A
Control Room A/C System Flow Rate Verification A Train
4B
Procedures
STS PE-061
Control Room/Control Building Habitability Test
Work Orders
WO 299, 16-411502-000, 16-411901-000, 16-417067-009,
16-417067-010, 18-441895-000, 19-447730-000,
19-447821-000, 20-46179-000, 20-466517-000,
21-469039-000, 21-469040-000, 21-472265-000,
2-477646-000, 22-478271-000, 23-488124-000,
23-488125-000
Calculations
AN-07-009
GOTHIC Model for CCW Pump Room Temperature
Calculations
GL-03-W
Auxiliary Building HVAC
W-1
Calculations
GL-M-007
Calculate Cooling Load in SR Pump Rooms Post LOCA:
1107, 1108, 1109, 1111, 1112, 1113, 1114, 1401 and 1406
Calculations
KJ-M-003
Operability of the Diesel Generators Due to an Exhaust Leak
Corrective Action
Documents
Condition Reports
25196, 127280, 130629, 134350, 69495, 73421, 75236,
75795, 75821, 81790, 81818, 10023559, 10024686,
10024802, 10027276, 10027368, 10027468, 10027496
Corrective Action
Documents
Resulting from
Inspection
Condition Report
10027517
Drawings
E-025-00007
Sheet 20
ESW Screen A Spray
W14
Drawings
M-12KJ05
Piping and Instrumentation Diagram Standby Diesel
Generator B Intake Exhaust, F.O. and Start Air System
Drawings
M-1G023
Equipment Location Reactor and Auxiliary BLDG Plan EL
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
26
Drawings
M-K2EF01
Piping and Instrumentation Diagram Essential Service Water
System
Miscellaneous
E-025-00003
Limitorque Design Information
W31
Miscellaneous
M-018-00309
Instruction Manual for Emergency Diesel Generator System
W141
Miscellaneous
WCRE-34
Fourth 10-Year Interval Inservice Testing Basis Document
Procedures
Operability Determinations and Functionality Assessments
Procedures
AP 28-011
Resolving Degraded or Nonconforming Conditions Impacting
SSCS
Procedures
Corrective Action Program
Procedures
CKL KJ-121
Diesel Generator NE01 and NE02 Valve Checklist
43A
Procedures
EDI 23M-050
Engineering Desktop Instruction Equipment Evaluation for
Maintenance Rule
Procedures
MGE LT-008
Routine Electrical Limitorque Operator Maintenance
8B
Procedures
MGE LT-099
MOV Diagnostic Testing
14A
Procedures
STS KJ-005B
Manual/Auto Start, Sync and Loading of EDG NE02
Work Orders
WO 21423, 13-326807-001, 13-326807-014, 14-385283-000,
14-385283-001, 19-449557-000, 20-460889-000,
23-489131-000, 23-489131-024
Calculations
EF-M-077
Estimated Allowed Leakage to Preclude Column Separation
in the Essential Service Water System
Calculations
EF-M-078
Evaluation of Wolf Creek Essential Service Water System
(ESW) Modifications during LOOP/LOCA Conditions
Corrective Action
Documents
Condition Reports
10027368, 10027468, 10027492, 10027496, 10027493,
10027564, 10027593, 10028049
Corrective Action
Documents
Resulting from
Inspection
Condition Reports
10027391, 10028094, 10028283
Drawings
E-025-00007
Sheet 177
B ESW/SW Cross Connect EFHV0024
W13
Drawings
E-025-00007
Sheet 201
ESW Screen B Spray EFHV0092
W14
Drawings
E-025-00007
ESW Pump B Discharge Air Release EFHV0098
W14
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Sheet 203
Drawings
Logic Block Diagram
W08
Drawings
M-12EF01
Piping Instrumentation Diagram Essential SVC Water
System
Drawings
M-12KJ04
Piping and Instrumentation Diagram Standby Diesel
Generator B Cooling Water System
Drawings
M-12KJ05
Piping and Instrumentation Diagram Standby Diesel
Generator B Intake Exhaust, F.O. and Start Air System
Drawings
M-K2EF01
Piping and Instrumentation Diagram Essential Service Water
System
Miscellaneous
1-GK-35
Startup Field Report
Miscellaneous
1-GK-54
Startup Field Report
Miscellaneous
1-GK-55
Startup Field Report
Miscellaneous
M-018-00309
Instruction Manual for Emergency Diesel Generator System
W141
Miscellaneous
M-619.2
Technical Specification for Miscellaneous Safety Related
Fans
Miscellaneous
WCRE-34
Fourth 10-Year Interval Inservice Testing Basis Document
Procedures
STS EF-100B
ESW System Inservice Pump A/B and ESW A/B Valve Test
51A
Procedures
STS GK-003
Manual CRVIS Actuation Operability Test
Procedures
STS ML-001
Monthly Surveillance Log
50A
Procedures
STS PE-009
Control Room Ventilation System Flow Rate and Combined
Pressure Drop Test
8B
Procedures
SYS GK-121
Control Building HVAC Operation
Procedures
SYS KJ-124
Post Maintenance Run of Emergency Diesel Generator B
Work Orders
WO 19980, 21423, 21937,21938, 22299, 23-484702-000,
23-484702-001, 23-484702-002, 23-487089-000,
23-488124-000, 23-488125-000
Corrective Action
Documents
Condition Reports
10008468, 10008518, 10009708, 10012628, 10015873,
10017305, 10017321, 10018445, 10020339, 10021975,
10023888, 10024030, 10024489, 10025432, 10027272,
10027404, 10028456, 10028458; 10028460, 10028461,
10028463, 10028465, 10028466, 10028468, 10028470;
10028472, 10028473, 10028475, 10028478; 10028480,
10028481, 10028483, 10028490; 10028493, 10028495;
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
10028497, 10028500, 10028505, 10028506, 10028527,
10028529, 10028573, 10028574, 10028578, 10028579,
10028699, 10028758
Corrective Action
Documents
Resulting from
Inspection
Condition Reports
10029045, 10029049
Procedures
EPP 06-001
Control Room Operations
31A
Procedures
EPP 06-003
Emergency Operations Facility Operation
Procedures
EPP 06-004
Public Information Organization
Procedures
EPP 06-005
Emergency Classification
9A
Procedures
EPP 06-006
Protective Action Recommendations
10A
Procedures
EPP 06-011
Emergency Team Formation and Control
2, 13
Procedures
EPP 06-012
Dose Assessment
17B, 18A
Procedures
EPP 06-013
Exposure Control and Personnel Protection
6A
Corrective Action
Documents
Resulting from
Inspection
Condition Report
10028579
Miscellaneous
E-Plan Effectiveness Evaluation, Activity/Document Number:
APF 06-002-02; Revision: 2
09/26/2023
Miscellaneous
E-Plan Effectiveness Evaluation, Activity/Document Number:
EPF 06-007-02; Revision: 1
2/15/2023
Miscellaneous
E-Plan Effectiveness Evaluation, Activity/Document Number:
EPF 06-007-03; Revision: 1
2/15/2023
Miscellaneous
E-Plan Effectiveness Evaluation, Activity/Document Number:
EPP 06-017; Revision: 5
2/08/2023
Miscellaneous
E-Plan Screening, Activity/Document Number: EPF 06-007-
2; Revision 1
2/15/2023
Miscellaneous
E-Plan Screening, Activity/Document Number: EPF 06-007-
03; Revision 1
2/15/2023
Miscellaneous
E-Plan Screening, Activity/Document Number: EPP 06-017;
Revision 5
2/08/2023
Miscellaneous
E-Plan Screening, Activity/Document Number: AP 06-002;
09/21/2023
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Revision 23
Miscellaneous
E-Plan Effectiveness Evaluation, Activity/Document Number:
EPP 06-009; Revision: 13
07/19/2023
Miscellaneous
E-Plan Effectiveness Evaluation, Activity/Document Number:
EPP 06-012; Revision: 18
04/13/2023
Miscellaneous
E-Plan Screening, Activity/Document Number: EPP 06-012;
Revision 18
04/12/2023
Miscellaneous
E-Plan Screening, Activity/Document Number: EPP 06-012;
Revision 18A
05/9/2023
Miscellaneous
E-Plan Screening, Activity/Document Number: EPP 06-
0009; Revision 13
07/18/2023
Miscellaneous
Issuance of License Amendment No. 236
08/07/2023
Procedures
Wolf Creek Nuclear Operating Corporation On-Shift Staffing
Analysis
Procedures
AI 26A-003
Regulatory Evaluations (Other Than 10 CFR 50.59)
Procedures
APF 06-002-02
Emergency Action Level Technical Bases
Procedures
EPP 06-009
Drill and Exercise Requirements
2, 13
Procedures
EPP 06-012
Dose Assessment
14D, 17, 18,
18A
Procedures
EPP-06-017
Core Damage Assessment Methodology
4A, 5
Miscellaneous
000133
Docket No. 50-482 and 72-29: Submittal of the Radiological
Emergency Response Plan Drill Scenario for the 2023
Evaluated Exercise at Wolf Creek Generating Station
09/12/2023
Miscellaneous
APF 06-002-03
EAL Classification Matrix
Miscellaneous
Docket No. 50-482: Submittal of the Radiological Emergency
Response Plan Drill Scenario for the 2019 Evaluated
Exercise at Wolf Creek Generating Station
03/28/2019
Miscellaneous
Docket No. 50-482: Submittal of the Radiological Emergency
Response Plan Drill Scenario for the 2022 Evaluated
Exercise at Wolf Creek Generating Station
05/25/2022
Procedures
APF 06-002-02
Emergency Action Levels Technical Bases
Procedures
EPP 06-005
Emergency Classification
9A
Procedures
EPP 06-006
Protective Action Recommendations
10A
Procedures
EPP 06-012
Dose Assessment
17B
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
71151
Corrective Action
Documents
Condition Reports
10014872, 10015816, 10017336, 10017337, 10016954,
10016974, 10017914, 10024888, 10017861, 10020170,
10020770, 10024250, 10026327
71151
Miscellaneous
DEP Performance Indicator Data 3Q2022 - 3Q2023
71151
Miscellaneous
ERO Drill Participation Performance Indicator Data 3Q2022 -
3Q2023
71151
Procedures
AI 26A-004
Emergency Planning Performance Indicators
71152A
Calculations
XX-E-004
AC Motor Operated Valve Minimum Terminal Voltage
71152A
Calculations
XX-E-042
Class 1E 480V AC and 208/120V AC System Coordination
71152A
Corrective Action
Documents
Condition Reports
81790, 73421, 10013103, 10014319, 10025703, 10025767,
10023559
71152A
Corrective Action
Documents
Resulting from
Inspection
Condition Report
10028066
71152A
Drawings
E-025-00007
sheet 201
ESW Screen B Spray EFHV0092
W14
71152A
Drawings
E-11NG20
Low Voltage System Class 1E Motor Control Center
Summary
318
71152A
Engineering
Changes
CP 14923
Restore Regulatory Compliance for Ten 480V MOVs
71152A
Miscellaneous
2013-049
USAR Change Request
2/12/2013
71152A
Miscellaneous
E-1F9905
Fire Hazard Analysis
71152A
Miscellaneous
WCNOC-76
Medium Low Voltage AC and Low Voltage DC Overcurrent
Protection Coordination for Wolf Creek Generating Station
71152A
Procedures
AP 10-102
Control of Combustible Materials
71152A
Procedures
AP 10-103
Fire Protection Impairment Control
40A
71152A
Work Orders
14-385283-000, 14-385283-001
71152S
Corrective Action
Documents
Condition Reports
110853, 10027176, 10027226, 10027441, 10027491,
10027877, 10028240
71152S
Corrective Action
Documents
Resulting from
Inspection
Condition Report
10027518
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
71152S
Procedures
AI 05-005
Modifications to Non-Controlled SSC(S)
71152S
Procedures
Planning and Scheduling Preventive Maintenance
8B
71152S
Procedures
AP 23-006
Strategic Engineering Program
71152S
Procedures
AP 23-008
Equipment Reliability Program
6A, 7
71152S
Procedures
Obsolescence Program
5A
71152S
Procedures
Corrective Action Program
27