Similar Documents at Zion |
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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217H4661999-10-18018 October 1999 Forwards Changes to EPIPs IAW 10CFR50.54(q) & 10CFR50,App E, Section V.Details of Changes Encl ML20217J4411999-10-18018 October 1999 Forwards Exemption from Certain Requirements of 10CFR73.55 for Zion Nuclear Power Station,Units 1 & 2 in Response to Application Dtd 990730,to Allow Util to Discontinue Specific Aspects of Security Plan & SER ML20216J8241999-09-30030 September 1999 Notifies of Removal of NRC Headquarters & Region III Offices from Controlled Copy Distribution of Certain CE Documents. Specific Documents,Associated Controlled Copy Numbers & NRC Location Affected Are Shown on Attachment to Ltr ML20216G9541999-09-27027 September 1999 Forwards Environ Assessment & Finding of No Significant Impact Re 990730 Application for Exemption.Exemption Would Allow Zion Nuclear Power Station to Discontinue Specific Aspects of Security Plan A99025, Forwards Response to NRC 990820 RAI Re Proposed Defueled TS for Zion Station1999-09-15015 September 1999 Forwards Response to NRC 990820 RAI Re Proposed Defueled TS for Zion Station ML20211L1551999-09-0101 September 1999 Forwards Insp Repts 50-295/99-03 & 50-304/99-03 on 990608-0812 at Zion 1 & 2 Reactor Facilities.No Violations Noted.Activities in Areas of Facility Mgt & Control, Decommissioning Support,Sf & Radiological Safety Examined ML20211J9701999-08-31031 August 1999 Discusses Request for Approval of Defueled Station Emergency Plan & Exemption from Certain Requirements of 10CFR50.47, Emergency Plans, for Plant,Units 1 & 2.Exemption & Safety Evaluation Encl ML20211J0311999-08-30030 August 1999 Agrees with Content in NRC 990810 Memo Re Plant Spent Fuel Pool.Memo Contains Accurate Summation of Info That Util Communicated to NRC During 990713 Telcon ML20211G1221999-08-27027 August 1999 Forwards fitness-for-duty Program Performance Data for Each of Comm Ed Nuclear Power Stations & Corporate Support Employees within Scope of Rule for six-month Period Ending 990630,IAW 10CFR26.71(d) ML20211G8191999-08-26026 August 1999 Forwards Amend 6 to Fire Protection Rept for Zion Nuclear Power Station,Units 1 & 2, IAW 10CFR50.71(e).Attachment 1 Contains Summary of Changes ML20211F5971999-08-20020 August 1999 Submits Request for Addl Info Re Proposed Defueled TSs for Plant,Per NRC Bulletin 94-001, Potential Fuel Pool Draindown Caused by Inadequate Maint Practices at Dresden Unit 1 ML20211C7401999-08-19019 August 1999 Informs That NRC Plans to Stop Using Office Complex at Zion Nuclear Generating Station Which Commonwealth Edison Provided for NRC Resident Inspectors Under 10CFR50.70(b)(1). NRC-owned Equipment to Be Moved on or About 991001 ML20211J4421999-08-13013 August 1999 Forwards, EA & Finding of No Significant Impact Re Application for Exemption ,as Suppl by 990708 & 19 Ltrs.Proposed Exemption Would Modify Emergency Response Plan Requirements as Listed ML20210N5651999-08-0606 August 1999 Forwards Rev 8 to Nuclear Generating Stations Emergency Plan, for Plants.With Summary of Changes ML20210M9131999-08-0202 August 1999 Forwards Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for Fys 2000 & 2001 for Comed ML20210J0861999-07-30030 July 1999 Requests NRC Approval of Exemption from Certain Requirements of 10CFR73, Physical Protection of Plants & Matls, by 990921.Exemption Is Needed to Support Scheduled 991001 Implementation of Plant Sf Ni.Encl Withheld,Per 10CFR73.21 ML20210C3641999-07-20020 July 1999 Discusses OI Rept 3-98-017 Completed on 980224 Re Contract Security Officer That Inadvertently Brought Personal Handgun Into Search Area at Plant & Forward NOV ML20210C4201999-07-20020 July 1999 Discusses Investigation Rept 3-98-017 Into Info Reported to Comed on 980224,informing NRC That N Everson Brought Personal Handgun Into Personnel Search Area at Plant.Nrc Determined That Violation Occurred.Nov Encl ML20210C2561999-07-19019 July 1999 Forwards Rev 1 to Calculation 22S-B-110X-0068, Determination of Heat Load for Assemblies F50D & Z33A, as Replacement Pages to Rev 0.Calculation Submitted Re Request for Approval of Proposed Plant Defueled Station EP ML20210B7071999-07-16016 July 1999 Responds to Requesting Review & Approval of Three Proposed Changes to Ceco QA TR,CE-1A Per 10CFR50.54(a)(3) & 10CFR50.4(b)(7) ML20209E7391999-07-0808 July 1999 Forwards Proposed Revised Znps Defueled Station Emergency Plan & Supporting Calculations.Revs to Proposed Defueled Station Emergency Plan Have Been Reviewed & Approved IAW Comed QA Program ML20196J9131999-07-0101 July 1999 Submits Status of Nuclear Property Insurance Currently Maintained for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR50.54(w)(3) ML20196J9061999-07-0101 July 1999 Provides Evidence That Util Maintains Guarantee of Payment of Deferred Premiums in Amount of $10 Million for Each of Thirteen Reactors,Per 10CFR140.21 ML20209B8241999-06-30030 June 1999 Forwards Five 3.5 Inch Computer Diskettes Containing Revised Annual Dose Repts for 1994 Through 1998 for Individuals Receiving Neutron Dose Not Previously Included in Reported Total Effective Dose Equivalent Values.Without Diskettes ML20196D3301999-06-18018 June 1999 Forwards Insp Repts 50-295/99-02 & 50-304/99-02 on 990121-0608.No Violations or Deviations Were Identified. Weakness Noted in Self Assessment/Corrective Action Program in Which Series of Personnel Errors Not Recorded in PIF Sys ML20195H9391999-06-15015 June 1999 Forwards Revised Monthly Operating Rept for Apr 1999 for Zion Nuclear Power Station,Units 1 & 2.Data Was Revised to Reflect Change in Daylight Savings Time ML20207H6121999-06-10010 June 1999 Provides Synopsis of OI Rept 3-1998-012 & Summary of Relevant Facts Re Violation Involving Employment Discrimination Against SRO at Zion Station.Enforcement Conference Scheduled for 990707 ML20195E3451999-06-0707 June 1999 Forwards 3.5 Inch Computer Diskette Containing Revised File Format for Annual Dose Rept for 1998,per 990520 Telcon Request from Nrc.Each Station Data Is Preceded by Header Record,Which Provides Info Necessary to Identify Data ML20195D6351999-06-0404 June 1999 Notifies NRC of Actions That Has Been Taken in Accordance with 10CFR26, Fitness for Duty Programs A99018, Responds to NRC Re Violations Noted in IR 3-98- 017.Corrective Actions:Three Security Guards Unescorted Access to All Comm Ed Nuclear Stations Put on Temporary Hold1999-05-27027 May 1999 Responds to NRC Re Violations Noted in IR 3-98- 017.Corrective Actions:Three Security Guards Unescorted Access to All Comm Ed Nuclear Stations Put on Temporary Hold ML20195B2301999-05-19019 May 1999 Requests Approval of Proposed Changes to QA Topical Rept CE-1-A,rev 66a.Attachment a Describes Changes,Reason for Change & Basis for Concluding That Revised QAP Incorporating Proposed Changes Continues to Satisfy 10CFR50AppB ML20207B5991999-05-14014 May 1999 Informs That NRC Ofc of NRR Reorganized,Effective 990328.As Part of Reorganization,Div of Licensing Project Mgt Was Created.Reorganization Chart Encl ML20206F5381999-04-30030 April 1999 Forwards Magnetic Tape Containing Annual Dose Repts for 1998 for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR20.2206(c).Without Magnetic Tape ML20206D8041999-04-30030 April 1999 Forwards Zion Nuclear Power Station Annual Radiological Environ Operating Rept & Listing of Commitments ML20206B9371999-04-27027 April 1999 Discusses Investigation Rept 3-98-17 Re Info Reported by Licensee on 980224 That Firearm Detected During Routine Search of Contractor Employee & Failure to Rept Incident to Supervisor.Oi Rept Synopsis Encl ML20206B4051999-04-23023 April 1999 Ack Receipt of Encl FEMA Ltr,Transmitting FEMA Evaluation Rept for 980819 Annual Medical Drill for Zion Nuclear Power Station.No Deficiencies Noted.Two Areas Requiring Corrective Action Noted During Drill ML20206B2471999-04-20020 April 1999 Informs That SE Kuczynski Has Been Transferred to Position No Longer Requiring SRO License.Cancel License SOP-31030-1, Effective 990412 ML20205S5811999-04-16016 April 1999 Responds to Which Urged Full Public Hearing to Held on Concerns Raised by R Robarge & E Dienethal Re Zion Npp.Commission Issued 990302 Memo & Order Affirming ASLB Decision to Deny Petition to Intervene A99014, Provides Description of Actions Comed Has Taken to Reinforce Safety Conscious Work Environ at Zion Nuclear Power Station1999-04-15015 April 1999 Provides Description of Actions Comed Has Taken to Reinforce Safety Conscious Work Environ at Zion Nuclear Power Station ML20205Q9971999-04-13013 April 1999 Requests NRC Approval of Plant Defueled Station Emergency Plan in Accordance with 10CFR50.54(q).Ltrs of Agreement Between Util & Offsite Agencies Who Have Agreed to Provide Assistance to Plant Encl.Calculations Also Encl ML20205P2071999-04-0909 April 1999 Discusses Insp Repts 50-295/98-02,50-304/98-02 & OI Rept 3-98-015 Completed on 981112 & Forwards Nov.Violation Involves Zion Supervisor Who Willingly Failed to Protect Unattended SGI from Unauthorized Disclosure ML20205K5841999-03-31031 March 1999 Submits Rept on Status of Decommissioning Funding for Reactors Owned by Comm Ed.Attachment 1 Contains Amount of Decommissioning Funds Estimated to Be Required Pursuant to 10CFR50.75(b) & (C) ML20206B4331999-03-26026 March 1999 Forwards Rept for Annual Medical Drill Conducted for Zion Nuclear Power Station on 980819.Two Areas Requiring Corrective Action Identified During Drill ML20205B4241999-03-23023 March 1999 Provides Results of drive-in Drill Conducted on 990208,as Well as Augmentation Phone Drills Conducted Since 981015,as Committed to in Util A99011, Responds to NRC Re Violations Noted Insp Repts 50-295/98-02 & 50-304/98-02.Corrective Actions:Uncontrolled Safeguards Documents Were Immediately Taken Into Possession & Controlled by Plant Security Supervisor1999-03-18018 March 1999 Responds to NRC Re Violations Noted Insp Repts 50-295/98-02 & 50-304/98-02.Corrective Actions:Uncontrolled Safeguards Documents Were Immediately Taken Into Possession & Controlled by Plant Security Supervisor ML20207D6831999-03-0101 March 1999 Forwards fitness-for-duty Program Performance Data for Each Comed Nuclear Power Station & Corporate Support Employees for Six Month Period Ending 981231,per 10CFR26.71(d) A99009, Forwards Znps Annual Occupational Exposure Rept, for Exposures Occurring in 1998.Listing of Commitments Contained in Ltr Provided as Attachment B1999-03-0101 March 1999 Forwards Znps Annual Occupational Exposure Rept, for Exposures Occurring in 1998.Listing of Commitments Contained in Ltr Provided as Attachment B ML20202J4381999-02-0303 February 1999 Forwards Zion Fuel Evaluation Info,Per Discussion ML20203C7001999-02-0202 February 1999 Informs That Mhb Technical Associates No Longer Wishes to Receive Us Region III Docket Info Re Comed Nuclear Facilities.Please Remove Following Listing from Service List A99001, Forwards Zion 1998 Annual Rept of Revised Regulatory Commitments1999-01-19019 January 1999 Forwards Zion 1998 Annual Rept of Revised Regulatory Commitments 1999-09-30
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217H4661999-10-18018 October 1999 Forwards Changes to EPIPs IAW 10CFR50.54(q) & 10CFR50,App E, Section V.Details of Changes Encl ML20216J8241999-09-30030 September 1999 Notifies of Removal of NRC Headquarters & Region III Offices from Controlled Copy Distribution of Certain CE Documents. Specific Documents,Associated Controlled Copy Numbers & NRC Location Affected Are Shown on Attachment to Ltr A99025, Forwards Response to NRC 990820 RAI Re Proposed Defueled TS for Zion Station1999-09-15015 September 1999 Forwards Response to NRC 990820 RAI Re Proposed Defueled TS for Zion Station ML20211J0311999-08-30030 August 1999 Agrees with Content in NRC 990810 Memo Re Plant Spent Fuel Pool.Memo Contains Accurate Summation of Info That Util Communicated to NRC During 990713 Telcon ML20211G1221999-08-27027 August 1999 Forwards fitness-for-duty Program Performance Data for Each of Comm Ed Nuclear Power Stations & Corporate Support Employees within Scope of Rule for six-month Period Ending 990630,IAW 10CFR26.71(d) ML20211G8191999-08-26026 August 1999 Forwards Amend 6 to Fire Protection Rept for Zion Nuclear Power Station,Units 1 & 2, IAW 10CFR50.71(e).Attachment 1 Contains Summary of Changes ML20210N5651999-08-0606 August 1999 Forwards Rev 8 to Nuclear Generating Stations Emergency Plan, for Plants.With Summary of Changes ML20210M9131999-08-0202 August 1999 Forwards Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for Fys 2000 & 2001 for Comed ML20210J0861999-07-30030 July 1999 Requests NRC Approval of Exemption from Certain Requirements of 10CFR73, Physical Protection of Plants & Matls, by 990921.Exemption Is Needed to Support Scheduled 991001 Implementation of Plant Sf Ni.Encl Withheld,Per 10CFR73.21 ML20210C2561999-07-19019 July 1999 Forwards Rev 1 to Calculation 22S-B-110X-0068, Determination of Heat Load for Assemblies F50D & Z33A, as Replacement Pages to Rev 0.Calculation Submitted Re Request for Approval of Proposed Plant Defueled Station EP ML20209E7391999-07-0808 July 1999 Forwards Proposed Revised Znps Defueled Station Emergency Plan & Supporting Calculations.Revs to Proposed Defueled Station Emergency Plan Have Been Reviewed & Approved IAW Comed QA Program ML20196J9061999-07-0101 July 1999 Provides Evidence That Util Maintains Guarantee of Payment of Deferred Premiums in Amount of $10 Million for Each of Thirteen Reactors,Per 10CFR140.21 ML20196J9131999-07-0101 July 1999 Submits Status of Nuclear Property Insurance Currently Maintained for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR50.54(w)(3) ML20209B8241999-06-30030 June 1999 Forwards Five 3.5 Inch Computer Diskettes Containing Revised Annual Dose Repts for 1994 Through 1998 for Individuals Receiving Neutron Dose Not Previously Included in Reported Total Effective Dose Equivalent Values.Without Diskettes ML20195H9391999-06-15015 June 1999 Forwards Revised Monthly Operating Rept for Apr 1999 for Zion Nuclear Power Station,Units 1 & 2.Data Was Revised to Reflect Change in Daylight Savings Time ML20195E3451999-06-0707 June 1999 Forwards 3.5 Inch Computer Diskette Containing Revised File Format for Annual Dose Rept for 1998,per 990520 Telcon Request from Nrc.Each Station Data Is Preceded by Header Record,Which Provides Info Necessary to Identify Data ML20195D6351999-06-0404 June 1999 Notifies NRC of Actions That Has Been Taken in Accordance with 10CFR26, Fitness for Duty Programs A99018, Responds to NRC Re Violations Noted in IR 3-98- 017.Corrective Actions:Three Security Guards Unescorted Access to All Comm Ed Nuclear Stations Put on Temporary Hold1999-05-27027 May 1999 Responds to NRC Re Violations Noted in IR 3-98- 017.Corrective Actions:Three Security Guards Unescorted Access to All Comm Ed Nuclear Stations Put on Temporary Hold ML20195B2301999-05-19019 May 1999 Requests Approval of Proposed Changes to QA Topical Rept CE-1-A,rev 66a.Attachment a Describes Changes,Reason for Change & Basis for Concluding That Revised QAP Incorporating Proposed Changes Continues to Satisfy 10CFR50AppB ML20206D8041999-04-30030 April 1999 Forwards Zion Nuclear Power Station Annual Radiological Environ Operating Rept & Listing of Commitments ML20206F5381999-04-30030 April 1999 Forwards Magnetic Tape Containing Annual Dose Repts for 1998 for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR20.2206(c).Without Magnetic Tape ML20206B2471999-04-20020 April 1999 Informs That SE Kuczynski Has Been Transferred to Position No Longer Requiring SRO License.Cancel License SOP-31030-1, Effective 990412 A99014, Provides Description of Actions Comed Has Taken to Reinforce Safety Conscious Work Environ at Zion Nuclear Power Station1999-04-15015 April 1999 Provides Description of Actions Comed Has Taken to Reinforce Safety Conscious Work Environ at Zion Nuclear Power Station ML20205Q9971999-04-13013 April 1999 Requests NRC Approval of Plant Defueled Station Emergency Plan in Accordance with 10CFR50.54(q).Ltrs of Agreement Between Util & Offsite Agencies Who Have Agreed to Provide Assistance to Plant Encl.Calculations Also Encl ML20205K5841999-03-31031 March 1999 Submits Rept on Status of Decommissioning Funding for Reactors Owned by Comm Ed.Attachment 1 Contains Amount of Decommissioning Funds Estimated to Be Required Pursuant to 10CFR50.75(b) & (C) ML20206B4331999-03-26026 March 1999 Forwards Rept for Annual Medical Drill Conducted for Zion Nuclear Power Station on 980819.Two Areas Requiring Corrective Action Identified During Drill ML20205B4241999-03-23023 March 1999 Provides Results of drive-in Drill Conducted on 990208,as Well as Augmentation Phone Drills Conducted Since 981015,as Committed to in Util A99011, Responds to NRC Re Violations Noted Insp Repts 50-295/98-02 & 50-304/98-02.Corrective Actions:Uncontrolled Safeguards Documents Were Immediately Taken Into Possession & Controlled by Plant Security Supervisor1999-03-18018 March 1999 Responds to NRC Re Violations Noted Insp Repts 50-295/98-02 & 50-304/98-02.Corrective Actions:Uncontrolled Safeguards Documents Were Immediately Taken Into Possession & Controlled by Plant Security Supervisor A99009, Forwards Znps Annual Occupational Exposure Rept, for Exposures Occurring in 1998.Listing of Commitments Contained in Ltr Provided as Attachment B1999-03-0101 March 1999 Forwards Znps Annual Occupational Exposure Rept, for Exposures Occurring in 1998.Listing of Commitments Contained in Ltr Provided as Attachment B ML20207D6831999-03-0101 March 1999 Forwards fitness-for-duty Program Performance Data for Each Comed Nuclear Power Station & Corporate Support Employees for Six Month Period Ending 981231,per 10CFR26.71(d) ML20202J4381999-02-0303 February 1999 Forwards Zion Fuel Evaluation Info,Per Discussion ML20203C7001999-02-0202 February 1999 Informs That Mhb Technical Associates No Longer Wishes to Receive Us Region III Docket Info Re Comed Nuclear Facilities.Please Remove Following Listing from Service List A99001, Forwards Zion 1998 Annual Rept of Revised Regulatory Commitments1999-01-19019 January 1999 Forwards Zion 1998 Annual Rept of Revised Regulatory Commitments A98056, Forwards List of Revised Various Commitments Originally Contained in Util to Nrc.Changes in Commitments Were Satisfactorily Evaluated Using NEI Commitment Change Methodology1998-12-11011 December 1998 Forwards List of Revised Various Commitments Originally Contained in Util to Nrc.Changes in Commitments Were Satisfactorily Evaluated Using NEI Commitment Change Methodology ML20198C2501998-12-11011 December 1998 Forwards Rev 45 to Zion Nuclear Power Station Security Plan, Per Requirements of 10CFR50.4(b)(4).Rev Includes Listed Changes.Licensee Has Concluded That Changes Do Not Decrease Safeguards Effectiveness of Plan.Encl Withheld ML20196B5871998-11-20020 November 1998 Requests That Svc List for All NRC Correspondence Re Any of Six Comed Nuclear Stations Be Modified Per Attached List.All Other Names Previously Listed Should Be Removed A98051, Forwards List of Revised Regulatory Commitments Which Were Evaluated as Satisfactory Using NEI Commitment Change Methodology1998-11-20020 November 1998 Forwards List of Revised Regulatory Commitments Which Were Evaluated as Satisfactory Using NEI Commitment Change Methodology A98055, Forwards List of Revised Regulatory Commitments Which Were Evaluated as Satisfactory Using NEC Commitment Change Methodology1998-11-20020 November 1998 Forwards List of Revised Regulatory Commitments Which Were Evaluated as Satisfactory Using NEC Commitment Change Methodology ML20195E6451998-11-12012 November 1998 Provides Results of drive-in Drill Conducted on 981007,as Well as Augmentation Phone Drill Conducted on 980917 A98059, Forwards Page Change Instruction for Aug 1998 DSAR for Zion Nuclear Power Station,Units 1 & 2.Instruction Was Omitted from 981110 DSAR Due to Administrative Error1998-11-11011 November 1998 Forwards Page Change Instruction for Aug 1998 DSAR for Zion Nuclear Power Station,Units 1 & 2.Instruction Was Omitted from 981110 DSAR Due to Administrative Error A98053, Forwards Change Instructions for Update to Zion UFSAR, Rewritten to Reflect Permanent Defueled Condition of Plant. & DSAR,1998-11-10010 November 1998 Forwards Change Instructions for Update to Zion UFSAR, Rewritten to Reflect Permanent Defueled Condition of Plant. & DSAR, ML20155D2701998-10-27027 October 1998 Forwards Changed Pages from 980423 Submittal Providing Addl Info Marked with Revision Bars & Revised Pages to QA Topical Rept Section 18,for Review ML20198C7401998-10-21021 October 1998 Informs That Encl Correspondence Was Received from Constituent,C Paxton Re Request for Investigation as to Documentation Also Encl.Without Encl ML20154J4951998-10-0707 October 1998 Forwards Revised Security Plans for CE Listed Nuclear Power Stations,Per 10CFR50.4(b)(4).Changes Do Not Decrease Effectiveness of Station Security Plans.Encl Withheld A98050, Forwards Zion Station Special Rept Number 30412398002SR.Rept for Reporting Period of Jan 1996-Dec 1997.Attachment B Provides Listing of Commitments Contained in Submittal1998-10-0505 October 1998 Forwards Zion Station Special Rept Number 30412398002SR.Rept for Reporting Period of Jan 1996-Dec 1997.Attachment B Provides Listing of Commitments Contained in Submittal ML20151Y5101998-09-11011 September 1998 Provides Results of drive-in-drill Conducted on 980804 & Augmentation Phone Drills Conducted Between 980601 & 0831 ML20238F7571998-08-28028 August 1998 Forwards fitness-for-duty Program Performance Data for Each of Util Nuclear Power Stations for Six Month Period Ending 980630 A98047, Forwards Revised Scope of One Commitment Contained in Response to NOV1998-08-28028 August 1998 Forwards Revised Scope of One Commitment Contained in Response to NOV ML20153F6811998-08-26026 August 1998 Informs of E Dienethal & R Robarge Concerns Re Safety of Areas in & Around City of Zion ML20237D9281998-08-24024 August 1998 Provides Description of Approach Being Taken by Comed to Develop Dsar.New Safety Classification Will Be Developed for Equipment Determined to Be Important to Defueled Condition 1999-09-30
[Table view] Category:UTILITY TO NRC
MONTHYEARML20059L0341990-09-20020 September 1990 Forwards Addl Station Blackout Info Re Diesel Loading & Alternate Ac Analysis,Per 900404 Meeting.Info Will Be Helpful When Evaluating Unit O Diesel Generator cross-tie Mod ML20059G1611990-09-0606 September 1990 Submits Supplemental Response to Generic Ltr 89-06, Certifying That SPDS Satisfies or Will Be Modified to Satisfy Requirements of Suppl 1 to NUREG-0737.Classroom Instruction on SPDS Incorporated Into Program ML20059G1751990-08-31031 August 1990 Provides Results of Util Reevaluation of Response to NRC Bulletin 85-003.Util Believes That Previous Testing Results & Subsequent Submittals Provide Assurance of Continued Operability of Sys motor-operated Valves ML20059D8271990-08-23023 August 1990 Provides Written Communication Re Util Intentions & Commitments,Per 900808 Telcon W/M Wallace.Standing Order 90-24 Issued to Provide Administrative Controls Beyond Tech Spec Requirements to Assure Svc Water Pump Availability ML20059C0781990-08-22022 August 1990 Submits Supplemental Info to Util 900412 Response to Notice of Violation in Insp Repts 50-295/89-40 & 50-304/89-36.Info Regards Requalification program,180 H of Required Training Through SAT Process & Policy for Remediation of Individual ML20056B4331990-08-20020 August 1990 Forwards Errata,To Radioactive Effluent Rept for Jan-June 1990 & Gaseous Effluent Errata Sheet ML20058P7791990-08-13013 August 1990 Provides Supplemental Response to NRC Bulletin 89-001 Re Mechanical Plugs Supplied by Westinghouse,Per .All Mechanical Plugs from Heats NX-3513 & NX-4523 Removed from Hot Legs of Plant Steam Generators ML20058N0651990-08-0707 August 1990 Responds to NRC Bulletin 88-009 Re Incore Neutron Monitoring Sys Thimble Tube Integrity.Thimble Tube Insps Will Be Performed at Every Refueling Outage Until Sufficient Data Accumulated on Thimble Tube Wear ML20056A0271990-07-30030 July 1990 Provides Addl Info Re Resolution of Number of Older Licensing Issues,Including Containment Isolation Valve Position Indication,Per NRC ML20056A0741990-07-27027 July 1990 Forwards Justification for Rev to Installation Schedules for Two Commitments Re Safeguards Inadequacies & Program Concerns.Encl Withheld ML20055J1191990-07-26026 July 1990 Responds to Generic Ltr 90-04, Request for Info Re Status of Implementation of Generic Safety Issues Resolved W/ Imposition of Requirements or Corrective Actions. Current Status of Issues Encl ML20055J2231990-07-26026 July 1990 Requests Withdrawal of Proposed Amend Re Deletion of Confirmatory Order ML20055H7631990-07-25025 July 1990 Forwards Financial Info Re Decommissioning of Plants ML20055H0871990-07-20020 July 1990 Provides Status Rept on Molded Case Circuit Breakers Replacement,Per NRC Bulletin 88-010.Traceable Replacement Breakers for Units 1 & 2 Being Procured safety-related & Meet Criteria of Bulletin Action 7 ML20058N6821990-07-0606 July 1990 Suppls 900626 Response to CAL-RIII-90-011 Re Torque Switch Settings,Per NRC Bulletin 85-003.Program to Address Generic Ltr 89-10 Which Expands Scope of Bulletin 85-003 Testing to safety-related motor-operated Valves,Being Developed ML20055D5291990-06-27027 June 1990 Forwards Table Outlining Status of Significant Events Re PWR Reload Safety Analysis Methods for Plant Cycle 13.Requests That Transient Analysis Topical Rept Be Reviewed & SERs Issued Prior to 910830 ML20055D5231990-06-26026 June 1990 Responds to Confirmatory Action Ltr CAL-RIII-90-11 Re Actions Required to Confirm Valve Operability for Unit 1,per IE Bulletin 85-003 ML20055D8461990-06-24024 June 1990 Forwards WCAP-10962,Rev 1, Zion Units 1 & 2 Reactor Vessel Fluence & Ref Temp for PTS Evaluations ML20055D8391990-06-18018 June 1990 Provides Supplemental Info in Response to Generic Ltr 88-17, Loss of Dhr. Permanently Installed Level Transmitter, Independent from Refueling Vessel Level Recorder & Led Readout Will Be Utilized ML20055J4471990-04-26026 April 1990 Responds to NRC Re Violations Noted in Insp Repts 50-295/90-03 & 50-304/90-03.Corrective Actions:Training Rev Request Initiated & Personnel Counseled ML20055C2921990-02-21021 February 1990 Forwards Errata Data for Radioactive Effluent Rept for Jan- June 1989 & Solid Radwaste Rept for Jul-Dec 1988 ML20248G1171989-09-29029 September 1989 Forwards Revised Tech Spec Section 3/4.9,Page 210 to 890925 Application for Amends to Licenses DPR-39 & DPR-48 Re Containment Isolation,Per 890927 Request for Clarification ML20248D0881989-09-21021 September 1989 Forwards Rev 56 to QA Program Topical Rept CE-1-A ML20247N9031989-09-18018 September 1989 Forwards Revised Zion Station,Fire Hazard Analysis,App a of Branch Technical Position Apcsb 9.5-1 ML20247H5171989-09-15015 September 1989 Submits Supplemental Info Re Generic Ltr 88-17, Loss of Dhr. Evaluation of Rh Pump Motor Alarm Recommended That Inputs from Parameters Should Be Processed Through Computer W/Graphic Configuration Similar to SPDS Iconic ML20247F9641989-09-11011 September 1989 Documents 890711 Telcon Between CP Patel, J Bongarra & Author Re Deferral of Certain Dcrdr Commitments.Conversation Directed to Three Specific Issues & Related Human Engineering Deficiencies ML20247C4061989-09-0808 September 1989 Initiates Discussion Over Need to Reconsider Installation Date for Unit 1 Re Atws.Due to New Design,Implementation for Unit 1 Scheduled for Spring 1991 & Unit 2 for Spring 1990 ML20247M3201989-09-0101 September 1989 Forwards Corrected Operating Status Rept Re Unit Shutdowns & Power Reductions for Jul 1989 ML20246F5021989-08-24024 August 1989 Suggests Performance of Study to Determine Alternate Methods to Perform Preventative Maint of Diesel Generator O, Including Mod of Existing Plant Design or Operational Changes to Plant Evolutions ML20246Q1661989-08-23023 August 1989 Responds to NRC Re Violations Noted in Insp Repts 50-295/89-15 & 50-304/89-15.Corrective actions:nonsafety- Related Instrument Maint Procedures Reviewed & Error Evaluation Committee Meeting Held on 890517 ML20246E4761989-08-21021 August 1989 Forwards Errata Data to Effluent & Waste Disposal Semiannual Rept,1988, for Jul-Dec 1988 ML20245J2601989-08-10010 August 1989 Provides Addl Info Re Proposed Amend to Tech Specs Section 3.15, Auxiliary Electric Power Sys. Info Answers & Resolves Questions Raised by NRC Re Tech Spec Amend Request ML20245H3771989-08-0909 August 1989 Forwards Listed Policies,Including Endorsements 24 & 25 to Nelia Policy NF-294,Endorsements 19 & 20 to Maelu Policy MF-128,Endorsements 36 & 37 to Nelia Policy NF-277 & Endorsements 29 & 30 to Maelu Policy MF-114 ML20245J2501989-08-0404 August 1989 Provides Clarification Re Proposed Amend to Tech Specs Section 3.15, Auxiliary Electric Power Sys. Areas That Warrant Clarification Can Be Grouped Into Impact or Risk Assessment of Diesel Generator & Use of LOCA Events ML20247M5181989-07-28028 July 1989 Forwards Response to Safeguards Inadequacies Noted in Regulatory Effectiveness Review Insp on 890515-19.Encl Withheld (Ref 10CFR73.71) ML20247P4991989-07-27027 July 1989 Confirms 890725 Telcon Re Util Intention to Withdraw Pages 199a & 199b of 890613 Application for Amend to Tech Specs, Revising Guidance on RCS & Containment Isolation Valves Per Generic Ltr 87-09 ML20245F1701989-07-21021 July 1989 Responds to NRC 890526 & 0619 Ltrs Re Violations Noted in Insp Rept 50-295/89-19.Corrective Actions:Standing Order Issued on 890601 to Administratively Control Future Failures of 1(2)MOV-CS0049 or 1(2)MOV-CS00050 05000295/LER-1989-008, Forwards LER 89-008-00 Re Room Cooler Svc Water Supply Discrepancy Discovered on 8906091989-07-10010 July 1989 Forwards LER 89-008-00 Re Room Cooler Svc Water Supply Discrepancy Discovered on 890609 ML20247J0481989-07-0505 July 1989 Responds to 890622 Request for Addl Info Re Allegation RIII-88-A-0032,providing Info to Substantiate Allegations 1-4 & Corrective Actions Taken Re Allegation 5.Allegations Regard Unsatisfactory Performed Work ML20245K9321989-06-30030 June 1989 Suppls Util 880711 Response to NRC Bulletin 88-004.Util Confirmed That RHR Sys Could Experience pump-to-pump Interaction.Min Flow Rate of 50 Gpm for RHR Pump Would Prevent Cavitation & Pump Failure within 30 Minutes ML20245H1391989-06-20020 June 1989 Responds to NRC 890405 Request for Addl Info Re Design of Component Cooling Water Sys ML20245G2411989-06-19019 June 1989 Forwards Endorsements 55,28,205,179,55,37,117,100,108 & 97 to Nelia & Maelu Policies NF-227,MF-114,NF-43,MF-22,NF-253, MF-104,NF-187,MF-54,NF-201 & MF-64.respectively ML20244E5951989-06-16016 June 1989 Responds to NRC Bulletin 89-001, Failure of Westinghouse Steam Generator Tube Mechanical Plugs. No Westinghouse Plugs Were Installed at Byron & Braidwood Stations.Remedial Actions Will Be Taken for Zion for Suspect Heats ML20247Q9321989-05-31031 May 1989 Provides Evaluation of Operation for NRC Bulletin 88-011, Pressurizer Surge Line Thermal Stratification. Util Participating in Program for Partial Resolution of Issue Through Westinghouse Owners Group ML20245G9631989-05-26026 May 1989 Provides Response to Allegation RIII-88-A-0140 Forwarded to Licensee by for Investigation ML20244E2861989-05-25025 May 1989 Forwards Response to Allegation RIII-88-A-0176.Response Withheld (Ref 10CFR2.790) ML20247J7101989-05-18018 May 1989 Forwards Response to Allegation RIII-88-A-162.Encl Withheld (Ref 10CFR2.790(a)) ML20247C1451989-05-10010 May 1989 Forwards Appropriate Revs to Proposed Amends to Licenses DPR-39 & DPR-48 Re Reactor Protection Sys ML20247B4751989-05-0808 May 1989 Responds to NRC Re Violations Noted in Insp Repts 50-295/89-08 & 50-304/89-08.Corrective Actions:Change Made to Weld Map,Revising Weld Numbers to Agree W/Data Sheet & Discrepancy Rept Initiated to Document Error ML20246B2431989-05-0101 May 1989 Forwards Ltr Inadvertently Omitted from 1988 Radwaste & Environ Monitoring Annual Rept 1990-09-06
[Table view] |
Text
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Commonw 11th Edison One First National Plaza Chicago, liknois
( y{C__,/ '7 Chicago.
Address Reply lllinois to Post Office Box 767 60690 ,
May 14, 1986 ,
I l
I l
Mr. James M. Taylor Office of Inspection and Enforcement U.S. Nuclear Regulatory Commission Washington, D.C. 20555
Subject:
Zion Nuclear Power Station Units 1 and 2
{' Response to I&E Inspection Report Nos.
50-295/86-002 and 50-304/86-002 NRC Docket Nos. 50-295 and 50-304 References (a): March 17, 1986 letter from C. E. Norelius to Cordell Reed.
(b): April 15, 1986 letter from J. G. Keppler to J. J. O'Connor.
Dear Mr. Taylor:
This letter concerns the routine safety inspection of activities at Zion Station conducted on January 4 through February 14, 1986 by M. M. Holzmer, L. E. Kanter, and J. N. Kish. Reference (a) indicated that the isolation of service water to the IB auxiliary pump oil cooler for 22 days appeared to be in noncompliance with NRC requirements. This issue was discussed on March 31, 1986 during an Enforcement Conference held in the NRC Region III office.
Reference (b) provided Commonwealth Edison with a Notice of Violation and proposed imposition of Civil Penalty for this event. This event was characterized as a Severity Level III violation and a $25,000.00 Civil Penalty was proposed. Commonwealth Edison Company's response to the Notice of Violation is provided in Attachment 1 to this letter.
Reference (b) also expressed the NRC's concern regarding Zion Station's control of non-routine valve manipulations. The current system has been examined and found to be adequate for most situations. However, the system was being inconsistently applied and lacked an effective mechanism for identifying the alignment in the field. Thus, non-routine valve alignments at Zion Station will now be controlled by the positive methods contained in Commonwealth Edison's Out-of-Service Procedure.
Commonwealth Edison Company has carefully reviewed this event and is concerned about the overall availability of Zion's auxiliary feedwater system.
I This concern is reflected in the extensive and comprehensive corrective action described in Attachment 1. However, Conunonwealth Edison Company believes that this event has been improperly classified as a Severity Level III violation.
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+
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Mr. J. M. Taylor May 14, 1986 i A review has been performed of the auxiliary feedwater system's normal operating configuration at a number of the industry's PWRs utilizing information from NURBGs 0611 and 0560. This review has demonstrated that the configuration of the Zion auxiliary feedwater system during the 22 day event provided either equivalent or superior flow capacity and/or redundancy than is provided by the norwal auxiliary feedwater configurations at a number of operating nuclear power plants across the nation. This fact is inconsistent with the characterization of this event as being a significant safety violation.
By virtue of these plant's continued operation, their auxiliary
, feedw<.ter systems must provide a sufficient level of redundancy, reliability,
! and capacity to satisfy the statutory requirement of adequate protection of the public health and safety. Thus, although a number of these plants are being reviewed by the NRC for the adequacy of their auxiliary feedwater systers, the fact of their current operation renders it inconsistent to fine Zion Station for operation for 22 days in a condition equivalent or superior i to these operating plants. The imposition of a civil penalty in this instance effectively penalizes Commonwealth Edison for constructing Zion Station with an auxiliary feedwater system design that exceeds the minimum requirements.
In addition to the review discussed above, a study was made of past enforcement actions taken in response to violations concerning auxiliary feedwater systems. This study demonstrated clearly that the proposed enforcement action for Zion is more severe than for comparable incidents across the nation. Thus, Commonwealth Edison believes that the enforcement
- policy delineated in 10 CPR 2, Appendix C, has not been consistently applied e
in this instance.
The details of these two studies, and their relationship to the enforcement policy, are contained in Attachment 2. The conclusion of these assessments is that the isolation of service water to the IB auxiliary feedwater pump at Zion Station for a period of 22 days is more properly characterized as a Severity Level IV violation.
j Reference (b) also expressed the NRC's concern regarding the timeliness of Zion Station's actions following the discovery of this event.
Commonwealth Edison Company believes that Zion Station personnel pursued the
- investigation of this event diligently. This was a complicated event, whose details required considerable effort to unravel. While it is recognized that the Resident Inspector could have been kept more informed as this investigation progressed, any such delay in communication does not have any bearing on the timeliness of Zion's corrective actions nor on the realization of the safety significance of this event.
a I
. - _ _ _ _ _ - ~ _ _ . _ __ _ . _ . _ . _ , _ _ _ _ .__ _ _ _-___
Mr. J. M. Taylor May 14, 1986 The enforcement policy allows for mitigation of a proposed civil penalty for both prompt identification and for extensive corrective action.
Reference (b) states that further mitigation of this penalty was not applied due to Zion Station's lack of timeliness in dealing with this issue.
Attachment 3 discusses these issues in detail and demonstrates that the event was promptly identified and that the corrective actions taken were both timely and extensive. Commonwealth Edison's conclusion regarding this matter is that the enforcement policy allows for more extensive mitigation than was exercised on this issue.
For the reasons discussed above, Commonwealth Edison Company believes that this event has been improperly categorized as a Severity Level III violation. In addition, notwithstanding our assertion that this event is a Severity Level IV violation, Commonwealth Edison Company also believes that the proposed civil penalty should be completely mitigated. Thus, in accord-ance with 10 CFR 2.205.b, we are protesting both the classification of the violation as Severity Level III and the limited mitigation of the proposed civil penalty.
Please direct any further questions to Commonwealth Edison's Department of Nuclear Licensing.
Very truly yours, on -
Cordell Reed Vice-president la Attachments cc: Zion Resident Inspector J. A. Norris - NRR J. G. Keppler - Region III SUBSCRIBED AND y N to befor Joe this / - day of' ' Idn. -
, 1986 i Yi (b1R
" Notary public 1641K
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ATTACHMENT 1 ZION NUCLEAR POWER STATION UNIT 1 RESPONSE TO NOTICE OF VIOLATION l
4 4
ITEM OF NONCOMPLIANCE
! As a result of the inspection conducted on January 4 through February 14, 1986, and in accordance with the " General Policy and Procedures for NRC Enforcement Actions, "10 CFR Part 2, Appendix C (1985), the following violation was identified:
Technical Specification 3.7.2.A.(1) and (2) requires that during plant operation in Modes 1, 2, and 3, three Independent steam generator auxiliary feedwater pumps shall be operable with two motor driven and c
! one steam turbine-driven auxiliary feedwater pump. With one motor-driven auxiliary feedwater pump inoperable, the pump must be 1 restored to operable status within seven days, or the plant must be in Mode 4 within the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.
Contrary to the above, from December 21, 1985 until January 12, 1986 with the plant operating in Mode 1, one motor-driven auxiliary feedwater pump was inoperable with the applicable action statement not satisfied, in that the pump was not restored to operable status within seven days and the plant was not in Mode 4 within the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.
Corrective Action Taken and Results Achieved l
The immediate corrective action was to open 1SWO656 to provide a source of cooling water for the IB auxiliary feedwater pump oil cooler. In addition, the remainder of the service water supplies to the Unit 1 auxiliary feedwater pumps were verified to be lined up correctly.
3 Corrective Action Taken to Avoid Further Violation i
- 1. Changes to the Unit 1 and 2 SW hydro procedure valve lineups have been instituted to make permanent the valving alignment which ensures SW is provided for both AFW pumps on the opposite unit.
- 2. Personnel involved in hydro package review have been made aware of this event and cautioned to ensure attention to detail is given to the review
- of these packages. However, it should be noted that of the 58 hydro packages reviewed and performed during this and the preceding refueling outage, there were literally thousands of valva positions examined by i these reviewers with only this one problem identified. All hydro i
packages have been re-reviewed since'the identification of this problem and no other problem has been found. In addition, these hydro tests are '
only performed once during each unit's ten-year inspection interval.
Therefore, this is considered an isolated event.
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- 3. A Zion Administrative procedure change has been initiated and training to reviewers has been provided to ensure procedure changes clearly state the reason for each change.
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} 4. The existing non-routine valve lineup procedure is being abolished. All
}
valve manipulations will be controlled by the Out of Service procedure.
- This procedure will provide more positive control over the plant's configuration.
- 5. A review of valve lineup procedures is being conducted to ensure that any l components normally supplied with Service Water from the opposite unit are 1
4 i never inadvertently isolated. Procedure changes will be made to correct j any deficiencies.
) 6. A memo has been provided to all shift supervisors alerting them to the cross connected condition which exists presently in the SW system and which may potentially exist in other " service systems" or common systems.
- 7. The fact that some components receive their cooling from the opposite unit presents a potentially confusing condition that could_ lend itself to 3
future errors. Thus, a review of the benefits obtained by allowing one
) unit's SW system to supply cooling to components on the opposite unit will j be conducted.
- 8. TraininghasbeenprovidedtoallRadWasteForemanonZionAbsinistrative
! procedures pertaining to operation. Adherence to procedures was emphasized j during this training.
}
Date When Full Compliance Will Be Achieved Actions #4, 5, and 7 will be completed by June 30, 1986.
! All other actions have been completed.
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I ATTAQWENT 2
SUMMARY
i Commonwealth Edison Company has reviewed the auxiliary feedwater systems at many of the nation's operating PWR's and the nation's recent enforcement history concerning auxiliary feedwater. These reviews have concluded that the NRC's Enforcement Policy has not been properly applied in 2
this instance.
The NRC's Enforcement Policy authorizes the Region to issue a Severity Level III violation where a licensee's failure to satisfy an Action Statement in the time allotted by the Technical Specification results in a
- significant violation of a limiting condition for operation (Lco) (10 CPR Part 50, App. C. Supplement I.C.1). However, the Enforcement Policy also l
- distinguishes between Lco violations of varying significance. A less l significant violation of an Lco is characterized as a Severity Level IV i (Supplement I.D.1). Thus, the proper classification of a Technical Specification Lco violation depends heavily on the safety significance of ;
the event.
f Edison has reviewed auxiliary feedwater operations at other plants 1 and civil penalties for similar incidents to establish a framework for evaluating the significance of this event. As summarized above, these comparisons show that:
1- operation of the Zion plant with one pump inoperable still left >
Zion with capacity and/or redundancy that was either equivalent or superior to the capacity and/or redundancy available during the ;
] normal operation of several other plants; and l
! 2- the escalated civil penalty is significantly more severe than any j other penalty levied in comparable situations.
I i i Thus, the circumstances of this event and previous evaluations of the significance of similar events show that this event did not have a ,
safety significance warranting a Severity Level III violation. The ;
appropriate classification for this violation is Severity Level IV. ;
i i
DISCUSSION l
! The number of auxiliary feed water pumps at other Westinghouse !
i plants and system capacities at those plants are enumerated in Table I. j i That Table shows that Zion's normal operating configuration, 3 auxiliary [
i feed water pumps having a total capacity of 400% of required flow, joins ,
several other Westinghouse plants at the high end of the spectrum of .
- capabilities at all operating Westinghouse plants. More importantly, that !
I Table also shows that the normal operating conditions for four Westinghouse plants provide less flow capacity or redundancy than was available at Zion during this incident. Five additional' plants have normal operating :
i configurations that provide equivalent flow capacity and/or' redundancy. l
)
t I
t i
During the Zion incident, 2 pumps capable of providing 300% of required auxiliary feedwater were available. By contrast, under normal operation, San Onofre-1, and Prairie Island have 2 pumps available, and are capable of providing only 200% of required flow. Turkey Point has available only 1 1/2 pumps capable of providing 300% of flow. Yankee Rowe has 1 pump with 100% capacity as its normal auxiliary feedwater system lineup. The continued operation of these four plants implies that the temporary operation of Zion with 2 pumps available and capable of providing 300% of flow was consistent with the adequate protection of public health and safety.
A review of Combustion-Engineering plants reinforces this conclusion. Table II enumerates the number and capacities of the auxiliary feed water pumps at those plants. Four of those plants operate with only two pumps with a range of pump capacities from 200% to 400%. Thus, the pump configuration at Zion during the incident was right in the middle of the operation of pump capacities for these Combustion-Engineering plants. Again, it follows that operation of Zion in this configuration was consistent with the adequate protection of public health and safety.
1 If 13 plants can run normally with equivalent or less system capability and/or redundancy than was available at Zion during the incident, then this incident cannot be considered a significant safety matter for the purposes of the Enforcement Policy. Therefore, the incident at Zion was improperly classified as severity Level III.
This conclusion is supported by comparing the civil penalty proposed for Zion with civil penalties previously imposed in other incidents involving auxiliary feedwater systems. A compendum of those civil penalties is provided in Table III. That Table shows that the proposed civil penalty for Zion is more severe than any other civil penalty for a comparable incident. In no other case was 300% capacity still available during the incident. This information is pertinent because the proper classification of a Technical specification LCO violation depends heavily on the safety significance of the event.
In addition, in every other case leading to escalated enforcement no more than one pump was available. Thus, in all other cases of escalated enforcement there was no redundancy in the available pumps. This critical factor distinguishes the Zion event for which two pumps were still available.
At Zion, pump redundancy was still available throughout the incident.
Clearly, this makes the Zion event fundamentally different from previous
, Severity Level III events involving loss of auxiliary feedwater. Therefore, classification of the Zion event with these previous events resulted in an inconsistent application of the Enforcement Policy. Accordingly, the Zion event should be reclassified as Severity Level IV.
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TABLE I WESTINGHOUSE PLANTS Approx.
Capacity # of Pumps Plant (%/ Unit) (#/ Unit)
Beaver Valley 1 400 3 D.C. Cook 1/2 300 2 Farley 1 400 3 Ginna 600 5 Haddam Neck 300 2 i
H.B. Robinson 400 3 Isidian FL. 2/3 400 3 Kewaunee 300 3 North Anna 1 400 3 i
Prairie Island 1/2 200 2 Point Beach 1/2 300 2 Salcm 1 400 3 San onofre 1 200+ 2 Surry 1/2 400 3 Trojan 400 2 Turkey Point 3/4 300 1 1/2 Yankee Rowe 100 1 Zion 1/2 400 3 Sources: NURBG 0611 NURBG 0560 1641K
TABLE II
, . - j. COMBUSTION - ENGINEERING PLANTS Approx.
Capacity # of Pumps Plant (%/ Unit) (#/ Unit)
ANO 400 2 Calvert Cliffs 1/2 400 2 Fort Calhoun 1 200 2 Maine Yankee 600 3 Millstone 2 400 3 Palisades 300 2 St. Lucie 1 400 3 Sources: NUREG 0611 NUREG 0560 j 1641K
i TABLE III NONCOMPLIANCE HISTORY Approx. Fine Plant Date Capacity # of Pumps Level /Amt.
Turkey Pt. 4/83 0 0 II/100,000 Turkey Pt. 12/83 200 1 III/60,000 Trojan 3/84 200 1 III/O 1 D.C. Cook 8/84 100 1 III/50,000 Turkey Pt. 12/84 200 1 IV i-i Zion
! s*
I 1
, ATTACIBIENT 3 i
The NRC has stated in references (a) and (b) that it believes that '
i Zion station was slow to realize the full significance of this event.
. Specifically, the inspection report transmitted with reference (a) stated on page 6; The licensee was slow to realize the significance of this event, in that it was discovered on January 12, 1986, and was processed as a i routine deviation report (DVR) until approximately January 27, 1986, when the Operating Assistant Superintendent determined that this j event could have represented a significant reduction in the margin of safety, and informed the NRC resident inspector. The licensee
~
usually informs the resident office immediately when significant events occur. The fact that the licensee informed the resident
- inspector indicates that they were beginning to treat this as a more i serious matter.
In addition, reference (b) stated;
) However, NRC is concerned that af ter the valve misalignment was )
j diccovered and corrected two weeks passed before anyone realized the l full significance of this event. i 4
Reference (b) later stated; i
Further reduction was not applied because after the violation was j discovered, you failed to realize its safety significance for some i time.
The above statements indicate that the NRC is correlating the 15 day j time period between January 12 and January 27 with a perceived delay in the
- recognition of the significance of this event. On the contrary, Commonwealth Edison believes that Zion Station realized immediately the potential l significance of this event. We acknowledge that the Resident Inspector could have been kept better informed of the investigation during this 15 day time j
period. However, this delay in communication does not have any bearing on the timeliness of Zion's corrective actions nor on the realization of the safety
! significance of this event.
4 The immediate corrective action upon discovering the event was both timely and comprehensive from a safety standpoint. The service water cooling flow was immediately restored to the la auxiliary feedwater pump and the service water supplies to the other auxiliary feedwater pumps were verified to
! be correct. When these actions were completed, the event's effect on reactor safety was terminated. The Unit 1 auxiliary feedwater system had been restored to a fully operable status. This occurred on January 12, 1986.
) The only information available to plant personnel on January 12, 1986 was the closed condition of valve 1sWO656. Since this valve had not been l associated with any maintenance or hydrotest activities, there was no indication as to the initiating mechanism of this event. Thus, there was no j, indication regarding the event's duration.
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However, station personnel immediately recognized the need to determine the total duration of the service water isolation. From the time of the initial reviews of the deviation report, the potential for this event to be a technical specification violation was clearly understood by station personnel.. Efforts were immediately initiated to determine the total time of isolation, so that the classification of this event could be accurately established. It should be noted that in order for this event to be reportable under 10CFR50.73.2.i.B. the total time of isolation would have to exceed the 7 days allowed by the technical specifications, o
As discussed at the Enforcement Conference held on March 31, 1986, the time period between January 13, 1986 and January 25, 1986, was spent engaging in extensive interviews, discussions, and research with numerous plant personnel. This investigation uncovered the root causes, personnel involved, initiating dates, and durations of the closure of both ISWO656 and ISWO660. In addition, the involvement of the service water system hydrotest valve line up was uncovered and thoroughly researched during this time period.
Commonwealth Edison acknowledges that the Resident Inspector could h.ve been informed of the progress of this extensive investis=Lluu duelus thlm time period. However, the NRC has incorrectly identified this lack of involvement of the Resident Inspector as a failure to realize the safety significance of this event. The perception of a logical tie between this lack of communication and Zion Station's perceived inability to recognize the significance of this event is incorrect.
As discussed above, Zion Station personnel immediately recognized the
/ potential of this event on January 12, 1986. The intervening two weeks was spent diligently investigating the details of this complicated event.
The immediate corrective action taken in response to this event was to restore the Unit 1 auxiliary feedwater system to a fully operable status.
This was the proper action to take and terminated this event. The additional.
corrective actions taken are discussed in Attachment 1. These 8 actions arc extensive and are specifically directed at the contributing causes of this event to preclude additional similar violations in the future. .
For the reasons discussed above, Commonwealth Edison Company believes that this event was identified promptly. The required reports were submitted within the mandatory 30-day time frame. In addition, the corrective action taken in response to this incident was both prompt and extensive. Thus, there is considerable opportunity for additional mitigation of the proposed civil penalty that has not been exercised on this issue.
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