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Category:INSPECTION REPORT
MONTHYEARIR 05000395/19990061999-10-0808 October 1999 Insp Rept 50-395/99-06 on 990801-0911.One Violation Identified & Being Treated as Ncv.Major Areas Inspected: Operations,Maint,Engineering & Plant Support IR 05000395/19990051999-08-30030 August 1999 Insp Rept 50-395/99-05 on 990620-0731.Non-cited Violation Noted.Major Areas Inspected:Operations,Maintenance, Engineering & Plant Support IR 05000395/19990041999-07-16016 July 1999 Insp Rept 50-395/99-04 on 990509-0619.Noncited Violation Identified.Major Areas Inspected:Aspects of Licensee Operation,Maint,Engineering & Plant Support ML20207H5331999-06-0707 June 1999 Insp Rept 50-395/99-03 on 990328-0508.Six Violations of NRC Requirements Occurred & Being Treated as non-cited Violations.Major Areas Inspected:Aspects of Licensee Operations,Maint,Engineering & Plant Support IR 05000395/19990031999-06-0707 June 1999 Insp Rept 50-395/99-03 on 990328-0508.Six Violations of NRC Requirements Occurred & Being Treated as non-cited Violations.Major Areas Inspected:Aspects of Licensee Operations,Maint,Engineering & Plant Support IR 05000395/19990021999-04-26026 April 1999 Insp Rept 50-395/99-02 on 990214-0327.Non-cited Violation Noted.Major Areas Inspected:Operations,Maintenance, Engineering & Plant Support IR 05000395/19990011999-03-15015 March 1999 Insp Rept 50-395/99-01 on 990103-0213.No Violations Noted. Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000395/19980101999-02-0101 February 1999 Insp Rept 50-395/98-10 on 981122-990122.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000395/19980091998-12-21021 December 1998 Insp Rept 50-395/98-09 on 981011-1121.Violation Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000395/19980081998-11-0909 November 1998 Insp Rept 50-395/98-08 on 980906-1010.No Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000395/19980071998-10-0505 October 1998 Insp Rept 50-395/98-07 on 980726-0905.No Violations Noted. Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000395/19980061998-09-24024 September 1998 Insp Rept 50-395/98-06 on 980628-0725.No Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000395/19980051998-07-27027 July 1998 Insp Rept 50-395/98-05 on 980517-0627.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000395/19980041998-06-15015 June 1998 Insp Rept 50-395/98-04 on 980405-0516.Violation Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000395/19980031998-05-29029 May 1998 Insp Rept 50-395/98-03 on 980330-0417.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20216C6681998-05-0404 May 1998 Insp Rept 50-395/98-02 on 980222-0404.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20217G4651998-03-20020 March 1998 Insp Rept 50-395/98-01 on 980111-0221.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20203J7531998-02-0909 February 1998 Insp Rept 50-395/97-14 on 971130-980110.Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000395/19970131997-12-23023 December 1997 Insp Rept 50-395/97-13 on 971019-1129.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000395/19970121997-11-17017 November 1997 Insp Rept 50-395/97-12 on 970907-1018.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000395/19970111997-10-0202 October 1997 Insp Rept 50-395/97-11 on 970727-0906.Violations Noted.Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support ML20203L2831997-09-24024 September 1997 Insp Rept for VC Summer Nuclear Station on 970227.No Conditions Observed at Time of Insp That Could Be Considered Immediate Threat to Safety of Dams or Nuclear Facility.Major Areas Inspected:Service Water Pond Dams IR 05000395/19970101997-08-22022 August 1997 Insp Rept 50-395/97-10 on 970714-18.No Violations Noted. Major Areas Inspected:Observation & Evaluation of Biennial EP Exercise ML20210N9401997-08-21021 August 1997 Insp Rept 50-395/97-07 on 970615-0726.Violations Noted.Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000395/19970091997-08-11011 August 1997 Insp Rept 50-395/97-09 on 970707-11.No Violations Noted. Major Areas Inspected:Area of Plant Support by Two Regional Safeguards Inspectors IR 05000395/19970081997-08-0808 August 1997 Insp Rept 50-395/97-08 on 970707-11.No Violations Noted. Major Areas Inspected:Plant Support ML20149G7411997-07-11011 July 1997 Insp Rept 50-395/97-05 on 970504-0614.Violations Noted.Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000395/19970061997-06-27027 June 1997 Insp Rept 50-395/97-06 on 970527-30.No Violations Noted. Major Areas Inspected:Physical Security Program for Power Reactors ML20140D4521997-06-0202 June 1997 Insp Rept 50-395/97-03 on 970323-0503.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000395/19970011997-04-17017 April 1997 Insp Rept 50-395/97-01 on 970209-0322.No Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000395/19960151997-03-10010 March 1997 Insp Rept 50-395/96-15 on 961229-970208.Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support ML20134G6181997-01-27027 January 1997 Insp Rept 50-395/96-14 on 961201-28.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000395/19960131996-12-30030 December 1996 Insp Rept 50-395/96-13 on 961027-1130.Noncited Violations Identified.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 05000395/19960111996-11-25025 November 1996 Insp Rept 50-395/96-11 on 960908-1026.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000395/19960121996-10-11011 October 1996 Insp Rept 50-395/96-12 on 960916-19.No Violations Noted. Major Areas Inspected:Physical Security Program for Power Reactors ML20128K0101996-10-0404 October 1996 Insp Rept 50-395/96-09 on 960721-0907.Violation Noted.Major Areas Inspected:Operations,Maint,Engineering,Plant Support IR 05000395/19960101996-09-20020 September 1996 Insp Rept 50-395/96-10 on 960819-23.No Violations Noted. Major Areas Inspected:Protected Area Detection Equipment, Alarm Stations & Communications,Testing,Maint,Compensatory Measures,Security Training & Qualifications & Followup Insp IR 05000395/19930281994-01-11011 January 1994 Insp Rept 50-395/93-28 on 931213-17.No Violations Noted. Major Areas Inspected:Organization & Staffing,Audits & Appraisals,Training & Qualifications & External & Internal Exposure Controls IR 05000395/19930251993-12-0202 December 1993 Insp Rept 50-395/93-25 on 931014-1120.No Violations Noted. Major Areas Inspected:Monthly Surveillance & Maint Observations,Operational Safety Verification,Esf Sys Walkdown & Review of Licensee self-assessment Capability IR 05000395/19930241993-10-27027 October 1993 Insp Rept 50-395/93-24 on 930904-1013.No Violations or Deviations Noted.Major Areas Inspected:Monthly Surveillance Observations,Monthly Maint Observations,Operational Safety Verification & Installation & Testing of Mods IR 05000395/19930231993-09-28028 September 1993 Insp Rept 50-395/93-23 on 930830-0903.No Violations or Deviations Noted.Major Areas Inspected:Mgt Support,Security Program Plans,Protected & Vital Area Barriers,Detection & Assessment Aids & Vital Area Access.Partially Withheld IR 05000395/19930221993-09-21021 September 1993 Insp Rept 50-395/93-22 on 930801-0903.Violations Noted But Not Cited.Major Areas Inspected:Monthly Surveillance Observations,Monthly Maint Observations,Operational Safety Verification,Esfs Sys Walkdown & Fire Protection IR 05000395/19930211993-08-12012 August 1993 Insp Rept 50-395/93-21 on 930719-23.No Violations Noted. Major Areas Inspected:Audits Performed by Licensee,Ts Chemistry Parameters,Dose Calculations,Semiannual Radioactive Effluents Rept & Organizational Changes ML20056E9721993-08-11011 August 1993 Insp Rept 50-395/93-20 on 930712-16.Weaknesses Noted.Major Areas Inspected:Annual Emergency Preparedness Exercise ML20056F6031993-08-10010 August 1993 Insp Rept 50-395/93-19 on 930716-31.Violations Noted.Major Areas Inspected:Monthly Surveillance Observations,Monthly Maint Observations,Operational Safety Verification & Review of Licensee self-assessment Capabilities IR 05000395/19930171993-07-0202 July 1993 Insp Rept 50-395/93-17 on 930511-0615.Violations Noted.Major Areas Inspected:Monthly Surveillance Observations,Monthly Maint Observations,Operational Safety Verification,Review of Noncomformance Conditions & Info Meetings W/Local Officials IR 05000395/19930021993-02-0505 February 1993 Insp Rept 50-395/93-02 on 930111-15.No Violations or Deviations Noted.Major Areas Inspected:Emergency Preparedness IR 05000395/19920231993-01-21021 January 1993 Insp Rept 50-395/92-23 on 921201-930108.No Violations or Deviations Noted.Concern Noted.Major Areas Inspected: Monthly Surveillance & Maint Observations,Operational Safety Verification,Esf Sys Walkdown & Installation & Testing Mods IR 05000395/19920221992-12-30030 December 1992 Insp Rept 50-395/92-22 on 921130-1204.Violation Noted,But Not Cited.Major Areas Inspected:Occupational Radiation Safety,Including Exam of Organization & Staffing,Audits, Appraisals & Training & Qualifications IR 05000395/19920211992-12-11011 December 1992 Insp Rept 50-395/92-21 on 921101-30.Violation Noted But Not Cited.Major Areas Inspected:Monthly Maint/Surveillance Observations,Operational Safety Verification,Cold Weather Preparations & Installation & Testing of Mods 1999-08-30
[Table view] Category:NRC-GENERATED
MONTHYEARIR 05000395/19990061999-10-0808 October 1999 Insp Rept 50-395/99-06 on 990801-0911.One Violation Identified & Being Treated as Ncv.Major Areas Inspected: Operations,Maint,Engineering & Plant Support IR 05000395/19990051999-08-30030 August 1999 Insp Rept 50-395/99-05 on 990620-0731.Non-cited Violation Noted.Major Areas Inspected:Operations,Maintenance, Engineering & Plant Support IR 05000395/19990041999-07-16016 July 1999 Insp Rept 50-395/99-04 on 990509-0619.Noncited Violation Identified.Major Areas Inspected:Aspects of Licensee Operation,Maint,Engineering & Plant Support ML20207H5331999-06-0707 June 1999 Insp Rept 50-395/99-03 on 990328-0508.Six Violations of NRC Requirements Occurred & Being Treated as non-cited Violations.Major Areas Inspected:Aspects of Licensee Operations,Maint,Engineering & Plant Support IR 05000395/19990031999-06-0707 June 1999 Insp Rept 50-395/99-03 on 990328-0508.Six Violations of NRC Requirements Occurred & Being Treated as non-cited Violations.Major Areas Inspected:Aspects of Licensee Operations,Maint,Engineering & Plant Support IR 05000395/19990021999-04-26026 April 1999 Insp Rept 50-395/99-02 on 990214-0327.Non-cited Violation Noted.Major Areas Inspected:Operations,Maintenance, Engineering & Plant Support IR 05000395/19990011999-03-15015 March 1999 Insp Rept 50-395/99-01 on 990103-0213.No Violations Noted. Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000395/19980101999-02-0101 February 1999 Insp Rept 50-395/98-10 on 981122-990122.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000395/19980091998-12-21021 December 1998 Insp Rept 50-395/98-09 on 981011-1121.Violation Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000395/19980081998-11-0909 November 1998 Insp Rept 50-395/98-08 on 980906-1010.No Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000395/19980071998-10-0505 October 1998 Insp Rept 50-395/98-07 on 980726-0905.No Violations Noted. Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000395/19980061998-09-24024 September 1998 Insp Rept 50-395/98-06 on 980628-0725.No Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000395/19980051998-07-27027 July 1998 Insp Rept 50-395/98-05 on 980517-0627.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000395/19980041998-06-15015 June 1998 Insp Rept 50-395/98-04 on 980405-0516.Violation Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000395/19980031998-05-29029 May 1998 Insp Rept 50-395/98-03 on 980330-0417.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20216C6681998-05-0404 May 1998 Insp Rept 50-395/98-02 on 980222-0404.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20217G4651998-03-20020 March 1998 Insp Rept 50-395/98-01 on 980111-0221.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20203J7531998-02-0909 February 1998 Insp Rept 50-395/97-14 on 971130-980110.Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000395/19970131997-12-23023 December 1997 Insp Rept 50-395/97-13 on 971019-1129.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000395/19970121997-11-17017 November 1997 Insp Rept 50-395/97-12 on 970907-1018.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000395/19970111997-10-0202 October 1997 Insp Rept 50-395/97-11 on 970727-0906.Violations Noted.Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support ML20203L2831997-09-24024 September 1997 Insp Rept for VC Summer Nuclear Station on 970227.No Conditions Observed at Time of Insp That Could Be Considered Immediate Threat to Safety of Dams or Nuclear Facility.Major Areas Inspected:Service Water Pond Dams IR 05000395/19970101997-08-22022 August 1997 Insp Rept 50-395/97-10 on 970714-18.No Violations Noted. Major Areas Inspected:Observation & Evaluation of Biennial EP Exercise ML20210N9401997-08-21021 August 1997 Insp Rept 50-395/97-07 on 970615-0726.Violations Noted.Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000395/19970091997-08-11011 August 1997 Insp Rept 50-395/97-09 on 970707-11.No Violations Noted. Major Areas Inspected:Area of Plant Support by Two Regional Safeguards Inspectors IR 05000395/19970081997-08-0808 August 1997 Insp Rept 50-395/97-08 on 970707-11.No Violations Noted. Major Areas Inspected:Plant Support ML20149G7411997-07-11011 July 1997 Insp Rept 50-395/97-05 on 970504-0614.Violations Noted.Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000395/19970061997-06-27027 June 1997 Insp Rept 50-395/97-06 on 970527-30.No Violations Noted. Major Areas Inspected:Physical Security Program for Power Reactors ML20140D4521997-06-0202 June 1997 Insp Rept 50-395/97-03 on 970323-0503.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000395/19970011997-04-17017 April 1997 Insp Rept 50-395/97-01 on 970209-0322.No Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000395/19960151997-03-10010 March 1997 Insp Rept 50-395/96-15 on 961229-970208.Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support ML20134G6181997-01-27027 January 1997 Insp Rept 50-395/96-14 on 961201-28.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000395/19960131996-12-30030 December 1996 Insp Rept 50-395/96-13 on 961027-1130.Noncited Violations Identified.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 05000395/19960111996-11-25025 November 1996 Insp Rept 50-395/96-11 on 960908-1026.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000395/19960121996-10-11011 October 1996 Insp Rept 50-395/96-12 on 960916-19.No Violations Noted. Major Areas Inspected:Physical Security Program for Power Reactors ML20128K0101996-10-0404 October 1996 Insp Rept 50-395/96-09 on 960721-0907.Violation Noted.Major Areas Inspected:Operations,Maint,Engineering,Plant Support IR 05000395/19960101996-09-20020 September 1996 Insp Rept 50-395/96-10 on 960819-23.No Violations Noted. Major Areas Inspected:Protected Area Detection Equipment, Alarm Stations & Communications,Testing,Maint,Compensatory Measures,Security Training & Qualifications & Followup Insp IR 05000395/19930281994-01-11011 January 1994 Insp Rept 50-395/93-28 on 931213-17.No Violations Noted. Major Areas Inspected:Organization & Staffing,Audits & Appraisals,Training & Qualifications & External & Internal Exposure Controls IR 05000395/19930251993-12-0202 December 1993 Insp Rept 50-395/93-25 on 931014-1120.No Violations Noted. Major Areas Inspected:Monthly Surveillance & Maint Observations,Operational Safety Verification,Esf Sys Walkdown & Review of Licensee self-assessment Capability IR 05000395/19930241993-10-27027 October 1993 Insp Rept 50-395/93-24 on 930904-1013.No Violations or Deviations Noted.Major Areas Inspected:Monthly Surveillance Observations,Monthly Maint Observations,Operational Safety Verification & Installation & Testing of Mods IR 05000395/19930231993-09-28028 September 1993 Insp Rept 50-395/93-23 on 930830-0903.No Violations or Deviations Noted.Major Areas Inspected:Mgt Support,Security Program Plans,Protected & Vital Area Barriers,Detection & Assessment Aids & Vital Area Access.Partially Withheld IR 05000395/19930221993-09-21021 September 1993 Insp Rept 50-395/93-22 on 930801-0903.Violations Noted But Not Cited.Major Areas Inspected:Monthly Surveillance Observations,Monthly Maint Observations,Operational Safety Verification,Esfs Sys Walkdown & Fire Protection IR 05000395/19930211993-08-12012 August 1993 Insp Rept 50-395/93-21 on 930719-23.No Violations Noted. Major Areas Inspected:Audits Performed by Licensee,Ts Chemistry Parameters,Dose Calculations,Semiannual Radioactive Effluents Rept & Organizational Changes ML20056E9721993-08-11011 August 1993 Insp Rept 50-395/93-20 on 930712-16.Weaknesses Noted.Major Areas Inspected:Annual Emergency Preparedness Exercise ML20056F6031993-08-10010 August 1993 Insp Rept 50-395/93-19 on 930716-31.Violations Noted.Major Areas Inspected:Monthly Surveillance Observations,Monthly Maint Observations,Operational Safety Verification & Review of Licensee self-assessment Capabilities IR 05000395/19930171993-07-0202 July 1993 Insp Rept 50-395/93-17 on 930511-0615.Violations Noted.Major Areas Inspected:Monthly Surveillance Observations,Monthly Maint Observations,Operational Safety Verification,Review of Noncomformance Conditions & Info Meetings W/Local Officials IR 05000395/19930021993-02-0505 February 1993 Insp Rept 50-395/93-02 on 930111-15.No Violations or Deviations Noted.Major Areas Inspected:Emergency Preparedness IR 05000395/19920231993-01-21021 January 1993 Insp Rept 50-395/92-23 on 921201-930108.No Violations or Deviations Noted.Concern Noted.Major Areas Inspected: Monthly Surveillance & Maint Observations,Operational Safety Verification,Esf Sys Walkdown & Installation & Testing Mods IR 05000395/19920221992-12-30030 December 1992 Insp Rept 50-395/92-22 on 921130-1204.Violation Noted,But Not Cited.Major Areas Inspected:Occupational Radiation Safety,Including Exam of Organization & Staffing,Audits, Appraisals & Training & Qualifications IR 05000395/19920211992-12-11011 December 1992 Insp Rept 50-395/92-21 on 921101-30.Violation Noted But Not Cited.Major Areas Inspected:Monthly Maint/Surveillance Observations,Operational Safety Verification,Cold Weather Preparations & Installation & Testing of Mods 1999-08-30
[Table view] Category:INSPECTION REPORT
MONTHYEARIR 05000395/19990061999-10-0808 October 1999 Insp Rept 50-395/99-06 on 990801-0911.One Violation Identified & Being Treated as Ncv.Major Areas Inspected: Operations,Maint,Engineering & Plant Support IR 05000395/19990051999-08-30030 August 1999 Insp Rept 50-395/99-05 on 990620-0731.Non-cited Violation Noted.Major Areas Inspected:Operations,Maintenance, Engineering & Plant Support IR 05000395/19990041999-07-16016 July 1999 Insp Rept 50-395/99-04 on 990509-0619.Noncited Violation Identified.Major Areas Inspected:Aspects of Licensee Operation,Maint,Engineering & Plant Support ML20207H5331999-06-0707 June 1999 Insp Rept 50-395/99-03 on 990328-0508.Six Violations of NRC Requirements Occurred & Being Treated as non-cited Violations.Major Areas Inspected:Aspects of Licensee Operations,Maint,Engineering & Plant Support IR 05000395/19990031999-06-0707 June 1999 Insp Rept 50-395/99-03 on 990328-0508.Six Violations of NRC Requirements Occurred & Being Treated as non-cited Violations.Major Areas Inspected:Aspects of Licensee Operations,Maint,Engineering & Plant Support IR 05000395/19990021999-04-26026 April 1999 Insp Rept 50-395/99-02 on 990214-0327.Non-cited Violation Noted.Major Areas Inspected:Operations,Maintenance, Engineering & Plant Support IR 05000395/19990011999-03-15015 March 1999 Insp Rept 50-395/99-01 on 990103-0213.No Violations Noted. Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000395/19980101999-02-0101 February 1999 Insp Rept 50-395/98-10 on 981122-990122.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000395/19980091998-12-21021 December 1998 Insp Rept 50-395/98-09 on 981011-1121.Violation Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000395/19980081998-11-0909 November 1998 Insp Rept 50-395/98-08 on 980906-1010.No Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000395/19980071998-10-0505 October 1998 Insp Rept 50-395/98-07 on 980726-0905.No Violations Noted. Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000395/19980061998-09-24024 September 1998 Insp Rept 50-395/98-06 on 980628-0725.No Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000395/19980051998-07-27027 July 1998 Insp Rept 50-395/98-05 on 980517-0627.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000395/19980041998-06-15015 June 1998 Insp Rept 50-395/98-04 on 980405-0516.Violation Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000395/19980031998-05-29029 May 1998 Insp Rept 50-395/98-03 on 980330-0417.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20216C6681998-05-0404 May 1998 Insp Rept 50-395/98-02 on 980222-0404.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20217G4651998-03-20020 March 1998 Insp Rept 50-395/98-01 on 980111-0221.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20203J7531998-02-0909 February 1998 Insp Rept 50-395/97-14 on 971130-980110.Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000395/19970131997-12-23023 December 1997 Insp Rept 50-395/97-13 on 971019-1129.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000395/19970121997-11-17017 November 1997 Insp Rept 50-395/97-12 on 970907-1018.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000395/19970111997-10-0202 October 1997 Insp Rept 50-395/97-11 on 970727-0906.Violations Noted.Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support ML20203L2831997-09-24024 September 1997 Insp Rept for VC Summer Nuclear Station on 970227.No Conditions Observed at Time of Insp That Could Be Considered Immediate Threat to Safety of Dams or Nuclear Facility.Major Areas Inspected:Service Water Pond Dams IR 05000395/19970101997-08-22022 August 1997 Insp Rept 50-395/97-10 on 970714-18.No Violations Noted. Major Areas Inspected:Observation & Evaluation of Biennial EP Exercise ML20210N9401997-08-21021 August 1997 Insp Rept 50-395/97-07 on 970615-0726.Violations Noted.Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000395/19970091997-08-11011 August 1997 Insp Rept 50-395/97-09 on 970707-11.No Violations Noted. Major Areas Inspected:Area of Plant Support by Two Regional Safeguards Inspectors IR 05000395/19970081997-08-0808 August 1997 Insp Rept 50-395/97-08 on 970707-11.No Violations Noted. Major Areas Inspected:Plant Support ML20149G7411997-07-11011 July 1997 Insp Rept 50-395/97-05 on 970504-0614.Violations Noted.Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000395/19970061997-06-27027 June 1997 Insp Rept 50-395/97-06 on 970527-30.No Violations Noted. Major Areas Inspected:Physical Security Program for Power Reactors ML20140D4521997-06-0202 June 1997 Insp Rept 50-395/97-03 on 970323-0503.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000395/19970011997-04-17017 April 1997 Insp Rept 50-395/97-01 on 970209-0322.No Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000395/19960151997-03-10010 March 1997 Insp Rept 50-395/96-15 on 961229-970208.Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support ML20134G6181997-01-27027 January 1997 Insp Rept 50-395/96-14 on 961201-28.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000395/19960131996-12-30030 December 1996 Insp Rept 50-395/96-13 on 961027-1130.Noncited Violations Identified.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 05000395/19960111996-11-25025 November 1996 Insp Rept 50-395/96-11 on 960908-1026.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000395/19960121996-10-11011 October 1996 Insp Rept 50-395/96-12 on 960916-19.No Violations Noted. Major Areas Inspected:Physical Security Program for Power Reactors ML20128K0101996-10-0404 October 1996 Insp Rept 50-395/96-09 on 960721-0907.Violation Noted.Major Areas Inspected:Operations,Maint,Engineering,Plant Support IR 05000395/19960101996-09-20020 September 1996 Insp Rept 50-395/96-10 on 960819-23.No Violations Noted. Major Areas Inspected:Protected Area Detection Equipment, Alarm Stations & Communications,Testing,Maint,Compensatory Measures,Security Training & Qualifications & Followup Insp IR 05000395/19930281994-01-11011 January 1994 Insp Rept 50-395/93-28 on 931213-17.No Violations Noted. Major Areas Inspected:Organization & Staffing,Audits & Appraisals,Training & Qualifications & External & Internal Exposure Controls IR 05000395/19930251993-12-0202 December 1993 Insp Rept 50-395/93-25 on 931014-1120.No Violations Noted. Major Areas Inspected:Monthly Surveillance & Maint Observations,Operational Safety Verification,Esf Sys Walkdown & Review of Licensee self-assessment Capability IR 05000395/19930241993-10-27027 October 1993 Insp Rept 50-395/93-24 on 930904-1013.No Violations or Deviations Noted.Major Areas Inspected:Monthly Surveillance Observations,Monthly Maint Observations,Operational Safety Verification & Installation & Testing of Mods IR 05000395/19930231993-09-28028 September 1993 Insp Rept 50-395/93-23 on 930830-0903.No Violations or Deviations Noted.Major Areas Inspected:Mgt Support,Security Program Plans,Protected & Vital Area Barriers,Detection & Assessment Aids & Vital Area Access.Partially Withheld IR 05000395/19930221993-09-21021 September 1993 Insp Rept 50-395/93-22 on 930801-0903.Violations Noted But Not Cited.Major Areas Inspected:Monthly Surveillance Observations,Monthly Maint Observations,Operational Safety Verification,Esfs Sys Walkdown & Fire Protection IR 05000395/19930211993-08-12012 August 1993 Insp Rept 50-395/93-21 on 930719-23.No Violations Noted. Major Areas Inspected:Audits Performed by Licensee,Ts Chemistry Parameters,Dose Calculations,Semiannual Radioactive Effluents Rept & Organizational Changes ML20056E9721993-08-11011 August 1993 Insp Rept 50-395/93-20 on 930712-16.Weaknesses Noted.Major Areas Inspected:Annual Emergency Preparedness Exercise ML20056F6031993-08-10010 August 1993 Insp Rept 50-395/93-19 on 930716-31.Violations Noted.Major Areas Inspected:Monthly Surveillance Observations,Monthly Maint Observations,Operational Safety Verification & Review of Licensee self-assessment Capabilities IR 05000395/19930171993-07-0202 July 1993 Insp Rept 50-395/93-17 on 930511-0615.Violations Noted.Major Areas Inspected:Monthly Surveillance Observations,Monthly Maint Observations,Operational Safety Verification,Review of Noncomformance Conditions & Info Meetings W/Local Officials IR 05000395/19930021993-02-0505 February 1993 Insp Rept 50-395/93-02 on 930111-15.No Violations or Deviations Noted.Major Areas Inspected:Emergency Preparedness IR 05000395/19920231993-01-21021 January 1993 Insp Rept 50-395/92-23 on 921201-930108.No Violations or Deviations Noted.Concern Noted.Major Areas Inspected: Monthly Surveillance & Maint Observations,Operational Safety Verification,Esf Sys Walkdown & Installation & Testing Mods IR 05000395/19920221992-12-30030 December 1992 Insp Rept 50-395/92-22 on 921130-1204.Violation Noted,But Not Cited.Major Areas Inspected:Occupational Radiation Safety,Including Exam of Organization & Staffing,Audits, Appraisals & Training & Qualifications IR 05000395/19920211992-12-11011 December 1992 Insp Rept 50-395/92-21 on 921101-30.Violation Noted But Not Cited.Major Areas Inspected:Monthly Maint/Surveillance Observations,Operational Safety Verification,Cold Weather Preparations & Installation & Testing of Mods 1999-08-30
[Table view] Category:UTILITY
MONTHYEARIR 05000395/19900271990-11-16016 November 1990 Insp Rept 50-395/90-27 on 901001-31.No Violations Noted. Major Areas Inspected:Surveillance Observations,Monthly Maintenance Observation,Operational Safety verification,on- Site follow-up of Written Repts of Nonroutine Events ML20058A6011990-10-19019 October 1990 Partially Withheld Insp Rept 50-395/90-26 on 900918-19 (Ref 10CFR73.21).Violations Noted But Not Cited.Major Areas Inspected:Access Control Packages,In Response to Reported Introduction of Firearm in Protected Area on 900813 IR 05000395/19900241990-10-12012 October 1990 Insp Rept 50-395/90-24 on 900901-30.No Violations or Deviations Noted.Major Areas Inspected:Monthly Surveillance & Maint Observations,Operational Safety Verification,Onsite Followup of Written Repts & Followup of Events IR 05000395/19900211990-08-0909 August 1990 Insp Rept 50-395/90-21 on 900701-31.Violation Noted.Major Areas Inspected:Monthly Surveillance Observations,Monthly Maint Observation,Operational Safety Verification & Onsite Followup Written Repts of Nonroutine Events at Facilities IR 05000395/19900181990-07-12012 July 1990 Insp Rept 50-395/90-18 on 900601-30.Violation Noted.Major Areas Inspected:Monthly Surveillance & Maint Observations, Operational Safety Verification,Onsite Followup of Written Repts of Nonroutine Events at Power Reactor Facilities IR 05000395/19900191990-07-0303 July 1990 Insp Rept 50-395/90-19 on 900611-15.Noncited Violation Noted.Major Areas Inspected:Emergency Preparedness to Determine If Licensee Program Being Maintained in State of Operational Readiness for Responding to Emergencies IR 05000395/19890171989-09-12012 September 1989 Insp Rept 50-395/89-17 on 890801-31.Violations Noted.Major Areas Inspected:Monthly Surveillance Operations,Monthly Maint Operation,Operational Safety Verification,Esf Sys Walkdown & Onsite Followup of Events & Written Repts IR 05000395/19890151989-08-16016 August 1989 Insp Rept 50-395/89-15 on 890724-28.Violations Noted.Major Areas Inspected:Inservice Testing & Followup on Previous Insp Findings IR 05000395/19890161989-08-0404 August 1989 Partially Withheld Insp Rept 50-395/89-16 on 890710-14 (Ref 10CFR2.790).No Violations or Deviations Noted.Major Areas Inspected:Security Plan & Implementing Procedures,Mgt Effectiveness & Security Program & Organization ML20246A5341989-08-0404 August 1989 Insp Rept 50-395/89-13 on 890701-31.Violation Noted.Major Areas Inspected:Monthly Surveillance Observations,Monthly Maint Observation,Operational Safety Verification,Action on Previous Insp Findings & Other Areas IR 05000395/19890121989-07-28028 July 1989 Insp Rept 50-395/89-12 on 890626-30.No Violations or Deviations Noted.Major Areas Inspected:Followup of Osti Insp Completed in Dec 1988 IR 05000395/19890111989-07-12012 July 1989 Insp Rept 50-395/89-11 on 890601-30.No Violations Noted. Major Areas Inspected:Monthly Maint Observations,Operational Safety Verification,Esf Sys Walkdown & Onsite Followup of Events IR 05000395/19890101989-07-0707 July 1989 Insp Rept 50-395/89-10 on 890605-08.No Violations or Deviations Noted.Major Areas Inspected:Observation & Evaluation of Annual Radiological Emergency Response Exercise IR 05000395/19890091989-06-0909 June 1989 Insp Rept 50-395/89-09 on 890501-31.No Violations Noted. Major Areas Inspected:Monthly Surveillance,Maint & Surveillance Observations,Operational Safety Verification, ESF Sys Walkdown,Onsite Followup of Events & Written Repts IR 05000395/19890081989-05-11011 May 1989 Partially Withheld Insp Rept 50-395/89-08 on 890417-21 (Ref 10CFR2.790(d) & 73.21).No Violations or Deviations Noted. Major Areas Inspected:Vital & Protected Area Barriers, Detection & Assessment Aids & Access Control of Personnel IR 05000395/19890051989-04-18018 April 1989 Insp Rept 50-395/89-05 on 890227-0303.No Violations Noted. Major Areas Inspected:Licensee Program to Maintain Occupational Radiation Exposures ALARA IR 05000395/19890061989-04-12012 April 1989 Insp Rept 50-395/89-06 on 890301-31.No Violations or Deviations Noted.Major Areas Inspected:Monthly Surveillance Observations,Monthly Maint Observation,Operational Safety Verification & ESF Sys Walkdown IR 05000395/19890041989-03-15015 March 1989 Insp Rept 50-395/89-04 on 890213-17.One licensee-identified Violation Noted.Major Areas Inspected:Design Control,Changes & Mods IR 05000395/19880031989-03-0909 March 1989 Insp Rept 50-395/88-03 on 890206-28.Violation Noted.Major Areas Inspected:Monthly Surveillance & Maint Observations, Operational Safety Verification,Esf Sys Walkdown & Action on Previous Insp Findings ML20246L2641989-02-23023 February 1989 Insp Rept 50-395/89-02 on 890123-27.Violations Noted.Major Areas Inspected:Review of Training,Changes to Emergency Organization,Distribution of Changes to Emergency Plan & Emergency Plan Procedures & Audits Repts ML20235Y5671989-02-17017 February 1989 Insp Rept 50-395/88-26 on 881114-18,1205-09 & 20-23. Violations Noted.Major Areas Inspected:Current Level of Performance in Area of Plant Operations W/Evaluation of Effectiveness of Various Plant Groups,Including Operations IR 05000395/19890011989-02-0909 February 1989 Insp Rept 50-395/89-01 on 890101-0205.No Violations or Deviations Noted.Major Areas Inspected:Monthly Surveillance & Maint Observations,Operational Safety Verification & ESF Sys Walkdown IR 05000395/19880231988-12-0101 December 1988 Insp Rept 50-395/88-23 on 881017-21.Violation Noted.Major Areas Inspected:Environ Qualification of Electrical Equipment,Including Review of Util Implementation of Program to Meet 10CFR50.49 Requirements & Followup on Previous Insp IR 05000395/19880251988-11-22022 November 1988 Insp Rept 50-395/88-25 on 881001-31.No Violations or Deviations Noted.Major Areas Inspected:Monthly Surveillance Observations,Monthly Maint Observation,Operational Safety Verification & Onsite Followup of Events IR 05000395/19880271988-11-18018 November 1988 Insp Rept 50-395/88-27 on 881031-1104.No Violations or Deviations Noted.Major Areas Inspected:Refueling Activities, Routine Surveillance of Core Power Distribution Limits & Shutdown Margin & Reactivity Anomaly IR 05000395/19880221988-10-25025 October 1988 Insp Rept 50-395/88-22 on 880926-30.No Violations or Deviations Noted.Major Areas Inspected:Inservice Insp,Review of Program,Review of Procedure & Observation of Work & Work Activities & NRC Bulletin 87-001 IR 05000395/19880241988-10-24024 October 1988 Insp Rept 50-395/88-24 on 880926-30.No Violations or Deviations Noted.Major Areas Inspected:Witnessing Primary Containment Integrated Leak Rate Test & Review of Containment Integrated Leak Rate Test Procedure IR 05000395/19880201988-10-24024 October 1988 Insp Rept 50-395/88-20 on 880912-17.No Violations or Deviations Noted.Major Areas Inspected:Complex Surveillance Testing,Ie Bulletin & IE Notice Followup IR 05000395/19880211988-10-24024 October 1988 Insp Rept 50-395/88-21 on 880919-22.No Violations or Deviations Noted.Major Areas Inspected:Licensee Conformance to Reg Guide 1.97, Instrumentation for Light-Water-Cooled Nuclear Power Plants to Assess Plant & Environs.. IR 05000395/19880191988-10-11011 October 1988 Insp Rept 50-395/88-19 on 880901-30.Violation Noted.Major Areas Inspected:Monthly Surveillance Observations,Monthly Maint Observation,Operational Safety Verification, ESF Sys Walkdown & Other Areas IR 05000395/19880181988-09-23023 September 1988 Insp Rept 50-395/88-18 on 880829-0902.No Violations or Deviations Noted.Major Areas Inspected:Nrc Bulletins & Matl Identification.Investment in Mobile Spectographic Equipment Is Positive Example of Mgt Involvement in QA ML20155A8751988-09-15015 September 1988 Insp Rept 50-395/88-17 on 880801-31.Violations Noted.Major Areas Inspected:Unresolved Items,Monthly Surveillance & Maint Observations,Operational Safety Verification,Esf Sys Walkdown & Onsite Followup of Events IR 05000395/19880141988-08-0808 August 1988 Insp Rept 50-395/88-14 on 880601-0731.No Violations or Deviations Noted.Major Areas Inspected:Monthly Surveillance & Maint Observations,Operational Safety Verification,Esf Sys Walkdown & Generic Ltr 83-28 Followup ML20151R9961988-07-26026 July 1988 Insp Rept 50-395/88-15 on 880613-17.Violations & Deviations Noted.Major Areas Inspected:Review of Current Svc Water Sys & Design Bases & Plant Actions Taken to Respond to Current NRC Svc Water Concerns ML20195K2551988-06-14014 June 1988 Insp Rept 50-395/88-13 on 880501-31.Violation Noted.Major Areas Inspected:Monthly Surveillance Observations,Monthly Maint Observation,Operational Safety Verification,Esf Walkdown,Design & Design Changes & Mod IR 05000395/19880121988-05-19019 May 1988 Insp Rept 50-395/88-12 on 880502-05.No Violations Noted. Major Areas Inspected:Reportability Determination,Qa Reviews & Security IR 05000395/19880101988-05-13013 May 1988 Insp Rept 50-395/88-10 in Apr 1988.No Violations Noted. Major Areas Inspected:Previous Insp Findings,Monthly Surveillance Observations,Monthly Maint Observations & Operational Safety Verification IR 05000395/19880061988-05-0303 May 1988 Insp Rept 50-395/88-06 on 880315-18.No Violations or Deviations Noted.Major Areas Inspected:Selected Procedures & Representative Records,Emergency Response Facilities & Related Equipment & Interviews W/Licensee Personnel ML20153E7631988-04-22022 April 1988 Insp Rept 50-395/88-01 on 880111-15.Violations Noted.Major Areas Inspected:Environ Qualification of Electrical Equipment IR 05000395/19880091988-04-13013 April 1988 Partially Withheld Physical Security Insp Rept 50-395/88-09 on 880314-18 (Ref 10CFR2.790(d) & 73.21).No Violations Noted.Major Areas Inspected:Security Program Audit,Records & Repts,Testing & Maint & Security Sys Power Supply IR 05000395/19880081988-04-0606 April 1988 Insp Rept 50-395/88-08 on 880301-31.No Violations or Deviations Noted.Major Areas Inspected:Licensee Action on Previous Insp Findings,Monthly Surveillance Observations, Radiological Protection,Physcial Security & Written Repts ML20148K8391988-03-21021 March 1988 Insp Rept 50-395/88-07 on 880229-0304.Violations Noted.Major Areas inspected:post-refueling Startup Tests & Local Leak Rate Testing IR 05000395/19880051988-03-14014 March 1988 Insp Rept 50-395/88-05 on 880201-29.No Violations or Deviations Noted.Major Areas Inspected:Monthly Surveillance Observations,Monthly Maint Observation,Operational Safety Verification,Esf Sys Walkdown & Physical Security IR 05000395/19880041988-02-29029 February 1988 Insp Rept 50-395/88-04 on 880201-05.No Violations Noted. Major Areas Inspected:Seismic Monitoring Program & Fire Protection/Prevention Program IR 05000395/19870361988-01-20020 January 1988 Insp Rept 50-395/87-36 on 871201-880104.No Violations or Deviations Noted.Major Areas Inspected:Licensee Action on Previous Insp Findings,Monthly Surveillance Observation, Operational Safety Verification & IE Bulletin Followup IR 05000395/19870351988-01-0606 January 1988 Insp Rept 50-395/87-35 on 871207-11.No Violations or Deviations Noted.Major Areas Inspected:Liquid & Gaseous Effluents & Gathering of Data on Collocated Licensee & NRC Environ TLDs IR 05000395/19870321987-12-31031 December 1987 Insp Rept 50-395/87-32 on 871116-20.No Violations or Deviations Noted.Major Areas Inspected:Licensed & Nonlicensed Staff Training IR 05000395/19870331987-12-0808 December 1987 Insp Rept 50-395/87-33 on 871101-30.No Violations or Deviations Noted.Major Areas Inspected:Licensee Action on Previous Insp Findings,Onsite Followup of Events,Subsequent Written Rept & ESF Sys Walkdown IR 05000395/19870311987-11-27027 November 1987 Partially Withheld Insp Rept 50-395/87-31 on 871102-06. Violation Noted.Major Areas Inspected:Physical Security Plan & Implementing Procedures,Mgt Effectiveness - Security Program,Security Organization,Locks Keys & Combinations IR 05000395/19870301987-11-12012 November 1987 Insp Rept 50-395/87-30 on 871020-30.Violations Noted.Major Areas Inspected:Followup on Environ Qualification Deficiencies Involving V-stub Taped Splices Used for Various Components 1990-08-09
[Table view] Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS
MONTHYEARIR 05000395/19990061999-10-0808 October 1999 Insp Rept 50-395/99-06 on 990801-0911.One Violation Identified & Being Treated as Ncv.Major Areas Inspected: Operations,Maint,Engineering & Plant Support IR 05000395/19990051999-08-30030 August 1999 Insp Rept 50-395/99-05 on 990620-0731.Non-cited Violation Noted.Major Areas Inspected:Operations,Maintenance, Engineering & Plant Support IR 05000395/19990041999-07-16016 July 1999 Insp Rept 50-395/99-04 on 990509-0619.Noncited Violation Identified.Major Areas Inspected:Aspects of Licensee Operation,Maint,Engineering & Plant Support ML20207H5331999-06-0707 June 1999 Insp Rept 50-395/99-03 on 990328-0508.Six Violations of NRC Requirements Occurred & Being Treated as non-cited Violations.Major Areas Inspected:Aspects of Licensee Operations,Maint,Engineering & Plant Support IR 05000395/19990031999-06-0707 June 1999 Insp Rept 50-395/99-03 on 990328-0508.Six Violations of NRC Requirements Occurred & Being Treated as non-cited Violations.Major Areas Inspected:Aspects of Licensee Operations,Maint,Engineering & Plant Support IR 05000395/19990021999-04-26026 April 1999 Insp Rept 50-395/99-02 on 990214-0327.Non-cited Violation Noted.Major Areas Inspected:Operations,Maintenance, Engineering & Plant Support IR 05000395/19990011999-03-15015 March 1999 Insp Rept 50-395/99-01 on 990103-0213.No Violations Noted. Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000395/19980101999-02-0101 February 1999 Insp Rept 50-395/98-10 on 981122-990122.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000395/19980091998-12-21021 December 1998 Insp Rept 50-395/98-09 on 981011-1121.Violation Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20198N8491998-12-21021 December 1998 Notice of Violation from Insp on 981011-1121.Violation Noted:On 980715,operations Personnel Authorized Maint Activities on ECCS Accumulators a & C Outlet Isolation Valve Breakers Without Recognizing Sys Would Become Inoperable IR 05000395/19980081998-11-0909 November 1998 Insp Rept 50-395/98-08 on 980906-1010.No Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000395/19980071998-10-0505 October 1998 Insp Rept 50-395/98-07 on 980726-0905.No Violations Noted. Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000395/19980061998-09-24024 September 1998 Insp Rept 50-395/98-06 on 980628-0725.No Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000395/19980991998-08-26026 August 1998 SALP Rept 50-395/98-99 for Period of 961027-980725 IR 05000395/19980051998-07-27027 July 1998 Insp Rept 50-395/98-05 on 980517-0627.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000395/19980041998-06-15015 June 1998 Insp Rept 50-395/98-04 on 980405-0516.Violation Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20236H0021998-06-15015 June 1998 Notice of Violation from Insp on 980405-0516.Violation Noted:On 980123 Condition Adverse to Quality Was Not Promptly Identified & Corrected IR 05000395/19980031998-05-29029 May 1998 Insp Rept 50-395/98-03 on 980330-0417.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20248J3281998-05-29029 May 1998 Notice of Violation from Insp on 980330-0417.Violation Noted:Instructions or Procedures Not Followed for Performance of Listed Activities ML20216C6681998-05-0404 May 1998 Insp Rept 50-395/98-02 on 980222-0404.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20216C6581998-05-0404 May 1998 Notice of Violation from Insp on 980222-0404.Violation Noted:On 980319,security Officer Failed to Ensure That Neither Operator Nor Accompanying Personnel Were Provided Access to Any Portion of Vehicle Until Search Completed ML20217G4431998-03-20020 March 1998 Notice of Violation from Insp on 980111-0221.Violation Noted:Licensee Failed to Establish Adequate Requirements to Insure That Temporary Shielding Properly Controlled ML20217G4651998-03-20020 March 1998 Insp Rept 50-395/98-01 on 980111-0221.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20203J7471998-02-0909 February 1998 Notice of Violation from Insp on 971130-980110.Violation Noted:On 971209,licensee Failed to Sign Off Applicable Steps to Mechanical Maintenance Procedure 300.033,rev 2,at Completion of Each Step ML20203J7531998-02-0909 February 1998 Insp Rept 50-395/97-14 on 971130-980110.Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support IR 05000395/19973001998-01-14014 January 1998 NRC Operator Licensing Exam Rept 50-395/97-300 (Including Completed & Graded Tests) for Tests Administered on 971201- 05 & 1212 IR 05000395/19970131997-12-23023 December 1997 Insp Rept 50-395/97-13 on 971019-1129.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20198N6871997-12-23023 December 1997 Notice of Violation from Insp on 971019-1129.Violation Noted:On 971019,licensee Employee Failed to Adhere to Posted HP Instructions in That Individual Observed Using Chewing Tobacco Product in B Chiller Unit Room IR 05000395/19970121997-11-17017 November 1997 Insp Rept 50-395/97-12 on 970907-1018.No Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000395/19970111997-10-0202 October 1997 Insp Rept 50-395/97-11 on 970727-0906.Violations Noted.Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support ML20211K5271997-10-0202 October 1997 Notice of Violation from Insp on 970727-0906.Violation Noted:On 970817,licensee Identified That Procedures STP-345.001,STP-345.002 & STP-345.003 Had Not Been Maintained to Ensure Correct Setting of OT Delta T ML20203L2831997-09-24024 September 1997 Insp Rept for VC Summer Nuclear Station on 970227.No Conditions Observed at Time of Insp That Could Be Considered Immediate Threat to Safety of Dams or Nuclear Facility.Major Areas Inspected:Service Water Pond Dams IR 05000395/19970101997-08-22022 August 1997 Insp Rept 50-395/97-10 on 970714-18.No Violations Noted. Major Areas Inspected:Observation & Evaluation of Biennial EP Exercise ML20210N9401997-08-21021 August 1997 Insp Rept 50-395/97-07 on 970615-0726.Violations Noted.Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support ML20210N9331997-08-21021 August 1997 Notice of Violation from Insp on 970615-0726.Violation Noted:Train a Hydrogen Monitor Containment Isolation Valves, SVX-6051A,SVX-6052A & SVX-6053A,were Open on an Intermittent Basis to Perform Hydrogen Monitor Calibration IR 05000395/19970091997-08-11011 August 1997 Insp Rept 50-395/97-09 on 970707-11.No Violations Noted. Major Areas Inspected:Area of Plant Support by Two Regional Safeguards Inspectors IR 05000395/19970081997-08-0808 August 1997 Insp Rept 50-395/97-08 on 970707-11.No Violations Noted. Major Areas Inspected:Plant Support ML20149G7371997-07-11011 July 1997 Notice of Violation from Insp on 970504-0614.Violation Noted:Licensee Did Not Preclude Repetition of Failure to Implement Storage Requirements ML20149G7411997-07-11011 July 1997 Insp Rept 50-395/97-05 on 970504-0614.Violations Noted.Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support IR 05000395/19970061997-06-27027 June 1997 Insp Rept 50-395/97-06 on 970527-30.No Violations Noted. Major Areas Inspected:Physical Security Program for Power Reactors ML20140D4351997-06-0202 June 1997 Notice of Violation from Insp on 970323-0503.Violation Noted:On 970413,SOP-114 Not Implemented to Increase RB Pressure ML20140D4521997-06-0202 June 1997 Insp Rept 50-395/97-03 on 970323-0503.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support IR 05000395/19970011997-04-17017 April 1997 Insp Rept 50-395/97-01 on 970209-0322.No Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support ML20147G2981997-03-10010 March 1997 Notice of Violation from Insp on 961229-970208.Violation Noted:Between 940628-961202,EFW Pump Quarterly SG low-low Actuation Slave Relay Test Was Not Performed within Required Frequency Specified in TS Surveillance Requirement 4.3.2.1 IR 05000395/19960151997-03-10010 March 1997 Insp Rept 50-395/96-15 on 961229-970208.Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support ML20134G6181997-01-27027 January 1997 Insp Rept 50-395/96-14 on 961201-28.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support ML20134G6061997-01-27027 January 1997 Notice of Violation from Insp on 961201-28.Violation Noted: SAP-142 Was Not Implemented & Provisions of Designated Storage Area Change Request 129 Were Not Complied with IR 05000395/19960131996-12-30030 December 1996 Insp Rept 50-395/96-13 on 961027-1130.Noncited Violations Identified.Major Areas Inspected:Operations,Maint, Engineering & Plant Support ML20149M5921996-12-0606 December 1996 SALP Rept 50-395/96-99 for Period of 950129 Through 961026 IR 05000395/19960111996-11-25025 November 1996 Insp Rept 50-395/96-11 on 960908-1026.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support 1999-08-30
[Table view] |
Inspection Report - Summer - 1986012 |
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Report No.: 50-395/86-12 Licensee: South Carolina Electric and Gas Company Columbia, SC 29218 Docket No.: 50-395 License No.: NPF-12 Facility Name: V. C. Summer Inspection Conduc ed: June 1 - July 3, 1986 Inspector : ao @ -J'
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Leo P. Modenos b '
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Date Sfgned Approved by : 'bY T _ Ow" I2 Hugh C./j0ance, Section Chief Dite Signed Division of Reactor Projects SUMMARY Scope: This routine, announced inspection was conducted by the resident _ and regional inspectors onsite in the areas of licensee action on previous enforce-ment matters, monthly surveillance observation, monthly maintenance observation, operational safety verification, ESF system walkdown, onsite followup of events and subsequent written reports and onsite followup of events at operating reactor Results: Three violations were identified: 1) With one of two diesel generators inoperable, the license did not properly verify the operability of all required systems; 2) the B train charging pumps were inoperable and unable to be automatically started as intended; and 3) procedure did not provide adequate instructions for the startup and shut down of the chemical and volume control syste An enforcement conference was held on July 3,1986, in the Region II office to discuss the violations disclosed in this inspectio PDR ADOCK 05000395 G PDR
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REPORT DETAILS Licensee Employees Contacted
+*D. Nauman, Vice President, Nuclear Operations
+*0. Bradham, Director, Nuclear Plant Operations
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- J. Skolds, Deputy Director, Operations and Maintenance
- K. Woodward, Manager, Operations
- M. Browne, Group Manager, Technical and Support Services
- M. Quinton, Manager, Maintenance Services
- A. Koon, Manager, Technical Support
- G. Putt, Manager, Scheduling and Materials Management
+* Williams, Manager, Nuclear Education and Training
- L. Blue, Manager, Support Services
- S. Hunt, Manager, Quality Assurance Surveillance Systems
+*W. Higgins, Associate Manager, Regulatory Compliance
- J. Sefick, Manager, Nuclear Security
+*B. Williams, Supervisor, Operations
+ R. Waselus, Supervisor, Electrical Engineering
+ K. Nettles, Group ~ Manager, Technical Services
+ S. Furstenberg, Control Room Supervisor ;
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+ S. Lathren, Reactor Operator
+ W. Williams, Jr., Santee Cooper, Special Assistant, Nuclear Operations Nuclear Regulatory Commission - Region II
+ L. Reyes, Acting Director, Division of Reactor Projects
+ A. Gibson, Director, Division of Reactor Safety
+ G. Jenkins, Director, Enforcement and Investigations Coordination Staff
+ 0. Verrelli, Branch Chief, Division of Reactor Projects
+ H. Dance, Section Chief, Division of Reactor Projects
+ H. Wong, Senior Enforcement Specialist, I&E Headquarters
+*R. Prevatte, Senior Resident Inspector
+ L. Modenos, Project Engineer, Division of Reactor Projects
+ J. Hopkins, Project Manager, Nuclear Reactor Regulations
+ Attended Enforcement Conference on July 3,1986
- Attended Exit Interview on June 30, 1986 Other licensee employees contacted included engineers, technicians, operators, mechanics, security force members, and office personne . Exit Interview (30702,30703)
The inspection scope and findings were summarized on June 30, 1986, with those persons indicated in paragraph 1 above. The inspectors described the areas inspected and discussed the inspection finding ,. - - - - - .- -. .-- - . ..
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Three violations related to system electrical alignment errors and inade-t quate procedures that rendered the "B" train charging pumps inoperable for an automatic start on a loss of offsite power and subsequent safety injection were identified (paragraph 10). The licensee offered no objections to the above violations but stated that their corrective action 1 should prevent recurrence. The licensee did not identify as proprietary any -
of the materials provided to or reviewed by the inspectors during this
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i n spc.cti o An enforcement conference was conducted in Region II office on July 3, 1986,
- to discuss these violations (paragraph 11). Licensee Action on Previous Enforcement Matters (92702)
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(Closed) Inspector Followup Item 85-15-01, " Issue Essential Drawings for RHR COPS Modifications". This item addressed an inspector concern with the issuing of the as-built essential drawings for the cold overpressure protection syste These drawings were issued under Gilbert / Commonwealth letter CGGS 34767 on May 14, 1986. This item is close (Closed) Inspector Followup Item 82-41-09, " Alternate Shutdown System License Condition First Refueling (SEC 9.5.1 SSER4)". This item involved the installation of source range monitor NI-33 at the alternate shutdown
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system control station. This item was addressed in SSER4 section 9. The installation activities were completed in December, 1984. The appli-cable surveillance procedure was implemented in January,1985 and the system operating procedure was implemented in February, 1985. This item is closed.
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(Closed) Inspector Followup Item TI 2515/77, " Survey of Licensee's Response to Selected Safety Issues". The inspector reviewed the licensee's responses and actions taken on biofouling of cooling water heat exchanges. A written report on this issue was provided to Region II under separate correspon-dence on June 20, 1986. This item is close (Closed) Unresolved Item 86-09-02, " Procedure For Drain Valves". The inspectors reviewed the actions taken by the licensee to preclude recurr-ence. A .special program for misaligned valves has been implemented under Special Instructions 86.14. It appears that the actions taken are adequat This item is closed.
(Closed) Violation 85-22-01, " Inadequate Review of Surveillance Test Procedures". The inspectors reviewed the procedural changes that have been
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implemented. It appears that the licensee has taken appropriate steps to
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correct deficiencies in procedural reviews of surveillance test procedure This item is considered close (Closed) Violation 85-21-01, " Failure To Apply Electrolyte Level Correction Factor During Battery Inspection". The licensee provided a written response to this violation in a letter to Region II, dated July 12, 198 The
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inspector reviewed the licensee's response and corrective actions taken to
preclude recurrenc Followup inspections in this area indicate that this .
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item has been adequately resolved. This item is close '
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(Closed) Inspector Followup Item, 79-29-01, " Inadequate Preoperational Test Procedures". The inspector reviewed a memo from J. P. O'Reilly to D. G. Eisenhut dated July 9,1982 (under module 94300) on the " Status of Facility Completion", and confirmed that construction and pre-operational testing of the Summer facility had been completed in substantial agreement with docketed commitments and regulatory requirements. This item is close (Closed) Inspector Followup Item, 82-41-16, " Inadequate Core Cooling Instru-ments (NUREG-0737, Item II.F.2)". The inspector reviewed the .11censee's response and the SER submitted by NRR dated August 3, 1984. Based on NRR's review and acceptance of the actions taken by the licensee, this item is close . Monthly Surveillance Observation (61726)
The inspectors observed surveillance activities of safety-related systems and components to ascertain that these activities were conducted in accor-dance with license requirements. The inspectors observed . portions of selected surveillance tests including all aspects of one major surveillance tes The inspectors also verified that the required administrative approvals were obtained prior to initiating the test, that the testing was accomplished by qualified personnel, that required test instrumentation was l properly calibrated, that data met TS requirements, that test discrepancies were rectified, and that the systems were properly returned to service. The following specific surveillance activities were observed:
STP 150.001 Reactor Coolant Leak Test STP 209.002 Surveillance Test Procedure for Incore/Excore Axial Offset STP 209.001 Incore/Excore Axial Offset Mapping STP 360.034 Reactor Building Sample Line Atmospheric Monitor (RMA2) Operational Testing STP 121.002 Main Steam Valve Operability Testing STP 102.002 NIS Power Range Heat Balance STP 114.002 Operational Leakage Test STP 120.002 Emergency Feedwater Turbine Pump Test STP 115.002 Reactor Building Door Leak Test and Interlock Operability STP 142.004 Manual Reactor Trip Cperational Test STP 130-003 Valve Operability Testing Modes 1,2 and 3
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STP 102-002 NIS Power Range Heat Balance I REP 109-001 Calculation of Estimated Critical Conditions STP 115-032 Reactor Building Air Lock Door Seal Leak Test STP 310.006 NIS Power Range (N42) Calibration STP 125.001 Electric Power Systems Weekly Test STP 102.002 Nuclear Power Range Heat Balance STP 114.002 Operational Leakage Test STP 133.001 Axial Flux Difference Calculation STP 126.002 Spent Fuel Ventilation Operability Test STP 134.001 Shutdown Margin Calculation STP 102.001 Analog Channel Operational Test (N-31, N-32)
STP 102.003 Analog Channel Operational Test (N-35, N-36)
Within the areas inspected, no violations or deviations were identifie . Monthly Maintenance Observation (62703)
The inspectors observed maintenance activities of safety-related systems and components to ascertain that these activities were conducted in accordance with approved procedures, Technical Specifications (TS) and appropriate industry codes and standards. The inspectors also determined that the ;
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procedures used were adequate to control the activity, and that these activities were accomplished by quali fied personne The inspectors independently verified that equipment was properly tested before being returned to service. Additionally, the inspectors reviewed several out-standing job orders to determine that the licensee was giving priority to safety-related maintenance and a backlog which might affect its performance was not developing on a given system. The following specific maintenance activities were observed:
ICP 400.018 Service Water Pump "C" Discharge Pressure Transmitter (IPT 4443) Calibration Test MWR 8600433 Replacement of Exhaust Boot on Emergency Feedwater Pump Turbine MWR 8503031 Repair Valve XVT0010-CU on the Downstream Test Vent for XVT08152CS, Containment Spray MWR 8600302 Repair Leak on High Pressure Turbine
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MWR 8503043 Replace Mechanical Seal on Waste Gas Compressor MWR 86W0026 Installation of Spare Power Range Drawer MWR 8610254 Inspect, Replace Relay LSXAMD on XCP6112 MWR 8610253 Inspect Contacts, Measure Resistance, and Replace Relay FW61BX on XCP6101 Within the areas inspected, no violations or deviations were identifie . Operational Safety Verification (71707)
The inspectors toured the control room, reviewed plant logs, records and held discussions with plant staff personnel to verify that the plant was being operated safely and in conformance with applicable requirement Specific items inspected in the control room included: adequacy of staffing and attentiveness of control room personnel; TS and procedural adherence; operability of equipment and indicated control room status; control room logs, tagout books, operating orders, jumper / bypass controls; computer printouts and annunciator Tours of other plant areas were conducted to verify equipment operability; control of ignition sources and combustible materials; the condition of fire detection and extinguishing equipment; the control of maintenance and surveillance activities in progress; the imple-mentation of radiation protective controls and the physical security pla Tours were conducted during normal and random off-hour period On May 5, 1986 during a review, the licensee identified that the set points for ITE 9880A and ITE 98808, for battery rooms A & B high temperature alarm set points, were set at 99 degrees F in accordance with instrument and control procedures, ICP 100.021 and ICP 100.02 l Technical Specification 3.7.11 established in Table 3.7-7, a temperature limit of 88 degrees F. Engineering change notice (ECN) 2424 dated August 4, 1982 established the set points to be 85 degrees F. However, in March of 1983 a personnel error was made while transposing set points from ECN 2424 to the procedure. This resulted in a 99 degrees F rather than an 85 degrees F set point being incorporated into the procedure. The error in transposing correct set points resulted in the irsuance of an inadaquate procedur Unresolved item 86-09-01, which originally identified this item, is close In accordance with the NRC enforcement policy in 10 CFR 2, Appendix C, a violation will not be issued for this licensee identified ite The licensee took immediate steps to evaluate and correct the procedures and to establish the correct set points on the affected ur its and to verify the battery room temperatures were within the allowable limit The licensee reviewed recorded daily electrolyte temperature for each battery pilot cells for May, June, July, August and September of years 1983, 1984, and 1985, and
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random reviews of other recorded readings. The highest temperature found in this review revealed that the highest known reading was 79 degrees F, with the majority being in a range of approximately 74 F - 75 degrees Other than the above, no other violations or deviations were identifie . ESF System Walkdown (71710)
The inspectors verified the operability of an engineered safety features (ESF) system by performing a walkdown of the accessible portions of the turbine driven emergency feedwater pump. The inspectors confirmed that the licensee's system lineup procedures matched plant drawings and the as-built configuration. The inspectors looked for equipment conditions and items that might degrade performance (hangers and supports were operable, house-keeping, etc.) and inspected the interiors of electrical and instrumentation cabinets for debris, loose material, jumpers, evidence of rodents, etc. The inspectors verified that valves, including instrumentation isolation valves, were in proper position, power was available, and valves were locked as appropriat The inspectors compared both local and remote position indication No violations or deviations were identifie . Onsite Followup of Events and Subsequent Written Reports (92700, 93702)
The inspectors reviewed the following Licensee Event Reports (LER's) and Special Reports (SPR's) to ascertain whether the licensee's review, co'rrec-tive action and report of the identified event were in conformance with regulatory requirements, technical specifications, license conditions, and licensee procedures and controls. Based upon this review the following items are close 'LER 85-26 Inoperable Turbine Driven Emergency Feedwater Pump, Repair and Retest of Valve LER 85-30 Out of Tolerance Main Steam Safety Valve Setpoints SPR 85-005 Inoperable Delta Temperature Detection System for Meteorological Data LER 84-044 Residual Heat Removal Suction Isolation, the Cause Was Determined to be Drawing Errors SPR 85-013 Inoperable Meteorological Instrumentation due to Lightning Strike LER 84-042 Reactor Building Purge Supply and Exhaust Valves LER 84-043 Inoperable Reactor Building Penetration
$PR 85-033 Diesel Generator "B" 0-Ring Failure
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No violations or deviations were identifie . Onsite Followup of Events at Operating Reactor (93702) On June 18, 1986 the licensee identified an error in the 5 Cals Calorimetric Computer Program used to control reactor thermal powe Preliminary investigation indicates that reactor thermal power may have exceeded the technical specifications limit of 2775 MWt by approxi-mately one percent when operating at 100 percent power. The licensee immediately reduced power by approximately one percent and suspended further use of this program until an evaluation could be complete The licensee is presently using feedwater temperature for a computer
' calorimetric and backing this up with manual calculations every 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> This item was documented in Off-Normal-Occurrence Report No.86-116 and the resident inspector was informed of the event and corrective action
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being taken on June 19, 1986. The licensee is currently evaluating this event to determine what additional corrective action is require This item will be tracked as an inspector followup item, Error in 5 Cals Program, 395/86-12-02, On May 31,1986, at 10:26 AM, a reactor trip from 100 percent power occurred. During' an operational test (STP 302-039) of power range channel N-42, one of the four power range channels, the bistables associated with N-42 channel was inadvertently left in the tripped
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position while:a test was being performed on channel N4 Initiation of a two.out of three protection system logic resulted in an over-
temperature delta temperature reactor tri Immediately following the reactor trip, the condensate system experi-enced severe water hamme The licensee investigated the event and determined the cause to be incomplete work and inadequate testing of modifications associated with MRF 20388-0049. Subsequent engineering evaluations and repairs were completed and the unit restarted on June 4, 1986. Additional details on this event are contained in
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Licensee Event Report 86-00 On June 29, 1985 at 2:15 AM the unit tripped from 90 percent power due to the feedwater isolation valve on steam generator "A" going shu This resulted in an automatic reactor trip from steam flow /feedwater flow mismatch and low low steam generator water level. No safety injection occurred and systems responded as required to the automatic trip. An investigation by the licensee determined the cause to be a high resistance connection in.a plug connector to the solenoid for the hydraulic valve actuator. The plug was replaced and the unit was returned to power on July 1, 198 Additional information will be provided by the licensee in an LE No violations or deviations were identified.
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1 Inoperability of Charging Pumps (93702)
While operating in Mode 1 at 100 power on June 11, 1986, the operator at the controls -questioned why B charging pump control switch was in the -
pull-to-lock position. The shift supervisor ordered that the switch be placed in the normal-after-stop position. Due to questions that arose as to the operability of the B pump and B train under the above conditions, an investigation was conducted to determine how .long the switch was in the pull-to-lock position and the applicaole statu '
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A subsequent investigation by the licensee revealed that the control switch for the B pump had been placed in the pull-to'-lock position at approximately-1:00 p. m. on June 6, 1986. The switch had been placed in this position due to questions on- pump operability while performing work activities on a solenoid valve in the cooling water supply to the lube oil coole The above investigation, after extensive research, revealed that placing B pump control switch in the pull-to-lock position prevented the B and C charging
, pumps, aligned to B train, from starting automatically during a loss of offsite power (LOOP) and subsequent safety injection (SI). TS Action Statement 3.5.2.a requires with one ECCS subsystem inoperable, the licensee must restore the inoperable subsystem to operable status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or be in at least hot standby within the next six hours and in hot standby I within the following six~ hours. The B train charging pumps were inoperable for a period of 111 hour0.00128 days <br />0.0308 hours <br />1.835317e-4 weeks <br />4.22355e-5 months <br /> Failure to restore the inoperable subsystem train B of the charging pumps or shutdown as specified is a violation (86-12-01)~of TS 3.5. A further review of events during this time period revealed that while the control switch was in pull-to-lock, A diesel generator was taken out of service on June 10, 1986, for a raintr . ce ~ period of approximately thirteen hours. During this thirteen hour period no charging pumps would have been available to . start automatically under a LOOP and subsequent SI. Charging pumps B and C were aligned to the B train and dependent upon the remaining operable diesel generator as a source of emergency power. Charging pumps B
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and C were inoperable because the control switch position for the B pump would have prevented the automatic start of the pump and electrical inter-locks would have prevented the automatic start of the C pump under the conditions of a loss of offsite power followed by a safety injection signa TS Action Statement 3.8.1.1.c requires with one diesel generator inoperable, the licensee must verify that all required systems, subsystems, trains, components, and devices that depend on the remaining operable diesel generator as a source of emergency power are operable. If these conditions are not satisfied within two hours, the unit'must be in at least hot standby within the next six hours and in cold shutdown within the next 30 hour3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br /> Failure to place the unit in hot standby within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> (2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> + 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />)
is a violation (86-12-01) of TS 3.8.1.1.c.
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Review of the system operating procedure (S0P-102) revealed that it did
- not fully address or cover this design feature of the swing pump alignmen The failure to have an adequate procedure to cover this particular
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operation is a violation (86-12-01) of TS 6.8.1 which requires that the applicable procedures recommended in Appendix A of Regulatory Guide 1.33, Revision 2, February 1978, be established, implemented, and maintaine . Enforcement Conference An enforcement conference was conducted .in the Region II Office on July 3, 1986, to discuss the violations referenced in paragraph 10. The licensee presented the sequence of events that resulted in the misalignment of the charging pumps and emphasized that although this event appears to be similar to violation 86-06-01, they believed it to be different. The i licensee has implemented both interim and long term corrective action to i preclude recurrence. Interim measures include: (1) abandonment of adminis-trative inoperability. philosophy, (2) require racking down of breakers on components that are not fully operable, (3) allow use of pull-to-lock only
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when specifically covered by procedures, and (4) issued a moratorium on implementing design changes. Long term corrective actions include: (1)
human factors evaluation of plant systems, (2) procedural ' reviews and updates, (3) stricter enforcement of procedural adherence, (4) increased preplanning for maintenance and mcdifications, (5) improvements to equipment status control program and (6) greater training emphasis on determining equipment operability and lessons learne The NRC regional representative stated that the licensee's review of this complex design appeared t.o be thorough. However, it is the licensee's responsibility to understand the design alignment features of their systems
and the recent review of the swing pump alignment on the component cooling
, water and service water event of January 30, 1986 (violation 86-06-01)
should have increased the licensee's awareness of all swing pump arrange-ments at .their plant. The meeting was beneficial in that the views of the licensee and the NRC were candidly expressed.
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