ML20235Y567

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Insp Rept 50-395/88-26 on 881114-18,1205-09 & 20-23. Violations Noted.Major Areas Inspected:Current Level of Performance in Area of Plant Operations W/Evaluation of Effectiveness of Various Plant Groups,Including Operations
ML20235Y567
Person / Time
Site: Summer South Carolina Electric & Gas Company icon.png
Issue date: 02/17/1989
From: Lawyer L, Peebles T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20235Y562 List:
References
50-395-88-26, GL-82-33, IEC-80-02, IEC-80-2, IEIN-88-086, IEIN-88-86, NUDOCS 8903140335
Download: ML20235Y567 (51)


See also: IR 05000395/1988026

Text

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NUCLEAR REGULATORY COMMISSION

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LReport No:- 50-395/88-26

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Licensee: South' Carolina' Electric &' Gas Company

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Columbia,'SC 29218

' Docket-No:

50-395-

-License No. NPF-12

Facility Name:

Virgil

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Summer

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Inspection Conduct

ov ber 14-18

ecember 5-9, and.' December 20-23, 1988-

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Inspectors:<

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Dite Signed

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L. L.

_awyer, . TeampcTer1

Team Members:

K.'Brockman

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P. Kellogg

W. Miller

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T. O'Connor

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R..Schin

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D. Starkey

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Approved by:

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T., A. Peebles, Chief

Date Signed

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Operations Branch

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Division of Reactor Saftey

SUMMARY"

Scope:

This was a special announced , Operational Safety Team Inspection -

(OSTI). The OSTI evaluated the11icensee's current. level of perform >

ance in the area of plant. operations'. - The inspection included an

evaluation of the effectiveness of- various iplant groups including -

Operations, Maintenance, Quality Assurance, Engineering,.and Training.

in the support of safe plant ~ operations. Plant-management awareness

of,-involvement in, and support of safe plant operation.were also

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evaluated.

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The inspection' was divided into four major areas' including . Opera-

tions, Maintenance _ Support .of Operations, Management. Controls,

and Emergency Operating. Procedures.

The team' placed emphasis on

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numerous interviews of personnel-at all levels, observations:of plant.

activities and meetings, extended control room observations, - and

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system . wal kdowns.

The ? inspectorsi also reviewed' plant - deviation

reports and LERs for the current Systematic Assessment of. Licensee-

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Performance (SALP) evaluation period, and evaluated the effectiveness

of the licensee's root cause identification; short term and progra-

matic corrective actions; and repetitive failure trending and related

corrective actions.

Results:

The licensee's management organization exhibited a high degree of

professionalism and control and was well directed to support effec-

tive and efficient operations.

The team performed this inspection

during a four week period in which the licensee was conducting a

refueling outage and entering into Mode 4.

This afforded the team

the opportunity to observe the operations, maintenance and engineer-

ing departments performing activities that required a great deal

of coordination and organization during a period of potentially

,

high stress.

The . departments exhibited a calm demeanor and were

apparently in good control of the many diverse activities that were

being accomplished during this period of recovery from the refueling

outage.

Emergency Operating Procedures were found to be adequate to place

the plant in a safe, stable condition.

The team observed a number of noteworthy items which were considered

as contributors to the exhibition of proper command and control.

Among these were shift turnover forms which provided a vehicle

for continuity of plant status during shift changes, operations

department logs that were all legible and complete with off-normal

conditions clearly indicated, large status boards containing the

names and stations of watchstanders as well as the boron injection

flow path, the required reading was up-to-date providing the

operators with new information on plant safety, operator response

to abnormal conditions was prompt and thorough, control room access

was well controlled, operator access to locked spaces was well

organized,

and engineering department evaluation of potential

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problems was aggressive. (Paragraph 2.a.)

Another noted strength was the use of a shift engineer throughout

the outage to coordinate with and resolve problems involving other

departments.

(Paragraph 2..c.)

The addition of licensed individuals to the maintenance scheduling

and planning section has provided operational expertise to the

process. The team considered this to be a strength in the scheduling

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process.

(Paragraph 3.b.)

The NRC saw the scheduling section's preparation of a daily '" trip

package" which contained planned maintenance for unscheduled shut-

downs of short duration and the "sho.t duration outage package"

for an outage of less than 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> as a strength. '(Paragraph 3.b.)

In addition, they considered the low backlog of maintenance work

requests that were older than three months to be a strength.

(Paragraph 3.f.)

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They also saw as a strength the engineering department's preparation

of design basis documents for the plant systems.' These provide a

living history of the systems from design through construction and to

present configuration.

(Paragraph 4.)

The team considered the independent safety engineering group's self

initiative of ' performing safety system functional inspections as a

strength.

(Paragraph 5.)

The team identified several areas which were considered to be weak-

nesses. Of these, inadequate procedures and inattention to procedure

adherence seemed to the team to be the most serious and resulted

in a violation.

(Paragraphs 3.c. and 3.1.1.)

The team considered the failure of the licensee to completely and

effectively respond to grounds on the dc bus and to previously detect

and correct a design problem in the ground detection circuit to be

problems of nearly equal seriousness.

(Paragraph 2.b.)

The licensee's lack of review thoroughness led to problems in the

areas of configuration control, drawing control, and procedural

control.

(Paragraph 2.d.,

e., and g.)

Inadequacies in 50.59 evaluations, which led to erroneous conclu-

sions were another weakness which resulted in a violation.

(Paragraph 2.j.)

The deficiency identification and correction process was considered

to be a weakness due to the fact that tagging is optional which

could result in not identifying known deficiencies.

(Paragraph 2.k.)

Lack of a formalized training program for maintenance planners was

a weakness.

(Paragraph 3.d.)

Blanket overtime authorization during outages was identified as

another area of weakness.

(Paragraph 3.f.)

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REPORT DETAILS

1.

Persons Contacted

Licensee Employees

    1. 0. Bradham, Vice President Nuclear Operations
  • W. Baehr, Manager Chemistry & Health Physics
  • M. Browne, Manager, Systems & Performance Engineering
  • C. Bowman, Manager, Scheduling & Modifications
  • R. Campbell, Senior Engineer, ISEG
    1. R. Clary, Manager, Design Engineering
  • H. Donnely, Senior Licensing Engineer
    1. W. Higgins, Supervisor, Regulatory Compliance
  • S. Hunt, Manager, Quality Systems
  1. M. Garrett, Associate Manager, Quality Control

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  • A. Koon, Manager, Nuclear Licensing
  • P. LaCoe, Assistant Manager, Facilities
  • G. Moffatt, Manager, Maintenance Services

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    1. D. Moore, General Manager, Engineering Services

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    1. K. Nettles, General Manager, Nuclear Safety
  • M. Quinton, General Manager, Station Support
  • L. Shealy, Senior Engineer, Operating Experience
  • J. Shepp, Associate Manager, Operations
    1. J. Skolds, General Manager, Nuclear Plant Operations
  1. A. Smith, Manager, Facilities & Administration

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    1. G. Soult, General Manager, Operations & Maintenance
  • G. Taylor, Manager, Operations
  • G. Walker, Coordinator, Maintenance Services
    1. D. Warner, Manager, Core Engineering & Nuclear Computer Services

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    1. M. Williams, General Manager, Nuclear Services
  • W. Williams, Santee Cooper, Special Assistant, Nuclear Operations
    1. K. Woodward, Manager, Nuclear Operator Training

Other licensee employees contacted included Technicians, Operations

Personnel, Maintenance and Instrumentation personnel, Engineering person-

nel, and Office personnel.

NRC Representatives

    1. P. Hopkins, Resident Inspector
  1. E. Merschoff, Deputy Director, Division of Reactor Safety

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  • R. Prevatte, Senior Resident Inspector

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  • Attended Pre-exit interview on 12/09/88
  1. Attended exit interview

Acronyms used throughout this report are listed in Attachment 8.

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2.

Operations (41400,41707,42700,61700,71707,93802)

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Many of the positive attributes of operational safety can be directly

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observed in the Control Room. These attributes include such things as

adequate shift manning, delegation of Shift Supervisor (SS) non safety

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related duties, Reactor Operator (RO) and Senior Reactor Operator (SRO)

system knowledge, relief turnover procedures, ' etc.

Adequate shift

manning assures that qualified plant personnel to man the operational

shifts are readily available . and that - excessive overtime need not be

. utilized;

delegation of nonsafety-related duties assures the SS

attention to the command function will not be diverted to nonsafety-

related duties;

accurate diagnosis and response. to plant transients,

minor and major, require detailed operator systems knowledge, etc.

Other operational safety attributes can be better assessed through

plant tours and system walkdowns. . These include material condition;

conformance to approved procedures; attentiveness to duties;

and return

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to service of equipment important to safety, including correct system

alignments.

Finally, interviews with personnel holding a variety of positions on the

plant staff together with some review of= records is necessary to provide

indirect indicators of operational safety and to corroborate preliminary

assessments.

To assess the operational safety of the facility, the Nuclear Regulatory

Conaission (NRC) team performed extended observations of control room

activities, including back shifts, with the plant in mode 5.

Also, the

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team conducted system walkdowns and plant tours.

In addition, they

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interviewed operators during these observations, walkdowns, and tours,

observed shift turnovers, and reviewed operator logs.

The team also

reviewed records used for indication or control of plant status for

adequacy and vF:d operator awareness of their contents.

These

included the Ra n

and Restoration (R&R) Log, configuration control

records, Danger Tag Log, Caution Tag Log, and plant drawings.

The NRC monitored operator performance, control room decorum, awareness

of plant status, response to alarms, and use of procedures. The team

conducted interviews or plant tours with the General Manager 'of Nuclear

Plant Operations, General Manager of Operations and Maintenance, Manag-

of Operations, and Associate Manager of- Operations. 'The NRC team also

reviewed engineering evaluations, training, and maintenance as related to

questions that arose from observations in the plant.

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3

a.

Summary of Observations

The NRC team made a number of observations of good operating

practices, which are summarized below:

All operators used shift turnover forms.

The forms included a

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thorough checklist, and required operators to sign for reviewing

logs and plant status indicators. These forms helped to ensure

that oncoming watchstanders were knowledgeable of the safety

status of the plant.

Operator logs were all legible and complete. Off-normal condi-

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tions were clearly indicated and explained. The team noted no-

recordkeeping errors.

These logs helped to provide auditable

records of plant conditions and to ensure operator awareness' of

the important ones.

The names of watchstanders and duty technicians were all clearly

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visible on a large status board in the control room.

These

included fire brigade, duty chemist, duty H.P. specialist, and

shift engineer.

This board enhanced control room operator

awareness of who to contact for various operational needs. The

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licensee's use of one watch position' on the board, the ~ shift

engineer, is considered a strength and is discussed later in

this report.

The boron injection flowpath that was to be maintained in an

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operable condition by the operators was clen jy posted on

another large status board in the control room.

This board

enhanced operator awareness of equipment that was in standby

for emergency use.

The required reading book contained signatures of operators

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which were up-to-date as required.

It included many types of

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information, such as design changes, NRC Information Notices

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(IEN), Licensee Event Reports (LERs), and Institute. Of Nuclear

Power Operations (INPO) Significant Operating Event Reports

(SOERs). The operators were keeping informed of new information

important to plant safety.

Operator response to an abnormal condition was prompt and

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thorough.

The abnormal condition was that both source range

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Nuclear Instruments (NIs) were inoperable at the same time.

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This is discussed later in the report.

Prompt and thorough

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operator response to abnormal conditions is important to plant

safety.

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Control room access was well controlled, and watchstanders

maintained an appearance of proper decorum and professionalism.

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A professional approach to plant operation enhances plant safety

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by providing operators who are alert to off-normal conditions

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and by providing a model for similar vigilance on the part of

plant workers coming into contact with them.

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Key control for operator access to spaces and equipment was

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provided -through a well organized key system and is discussed

later in this report.

Operator access to plant equipment in

emergencies is important to enable the accomplishment of

emergency actions.

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The aggressive and thorough engineering evaluation of NRC

questions.during the inspection relating to direct current (de)

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grounds was noteworthy,

prompt evaluation and correction of

potential safety problems is important in minimizing the risks

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of plant operation.

The team also observed a number of areas in need of improvement:

The areas of Limiting Condition for Operation (LCO) control,

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configuration control, drawing control, and procedure control

were in need of improvement and are each discussed later in

this report. Accurate control of safety-related plant systems

is important to overall plant safety.

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The team considered the . failure to completely and effectively

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respond to grounds on the dc bus and to previously detect and

correct a design problem with the ground detection circuit

as problems of nearly equal importance.

These problems are

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discussed later in this report.

Inadequacies existed in a safety evaluation of a modification

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to the fire protection system ' alignment, and are discussed -

later in this report. Complete and timely safety evaluation of

plant modifications is important, to minimize the potential of

introducing new conditions that may in some way reduce plant

safety.

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The deficiency identification and correction process needs

improvement, and is discussed later in this report.

Timely

and thorough identification and correction of deficiencies -is

important, even though each individual deficiency may have

only minor safety significance.

Deficiencies can range from

the very serious, where safety significance is apparent, to

seemingly minor deficiencies.

Timely and thorough identifica-

tion and correction of even those which seem to have only minor

significance is important since two or more may, in combination,

be very significant.

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b.

Electrical Grounds on 125 Volt DC Systems

On entering the control room on the first day of the inspection

(during an outage), the NRC noticed that all three of the electrical

ground indicating systems indicated grounds.

Electrical grounds

existed on both of the vital 125 volt de busses and on the nonvital

125 volt de bus.

The team then inquired about:

Promptness and methods used in clearing grounds on vital 125

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volt de systems.

Policy on magnitude of ground acceptable for plant operation.

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Whether any safety evaluations had been done for the plant that

were dependent on an ungrounded de power supply.

Whether the licensee had reviewed NRC Information Notice 88-66,

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issued October 21, 1988, on Operating with Multiple Grounds in

Direct Current Distribution Systems.

This notice identified

the potential for spurious actuation of equipment,

in response to these questions, the licensee's Operations Department

forwarded questions to the Engineering Department for evaluation and

response.

Included with 'the questions was the fact that existing

policy on operating with dc grounds required the maintenance -depart-

ment to locate and clear grounds of 5 volts or worse (positive or

negative leg to ground).

The 5 volt value represents a hard ground, on the order of 100 ohms

to ground.

With an existing ground of 100 ohms, the risk exists

that the occurrence of a second ground, of 0 ohms, could generate a

ground fault current of over 1 ampere. That amount of current could

cause a small 1-ampere fuse to blow and thus disable a piece of

safety equipment.

The plant manager stated that when grounds had. occurred while the

plant was operating, the operators. and Maintenance Department had

not always promptly cleared them. This was because the opening of

certain dc breakers with the plant operating would cause 'a reactor

trip or create unnecessary safety hazards.

The Engineering Department obtained a copy of IEN 88-66, then

responded aggressively to the questions. The IEN was already in the

licensee's system, having been received approximately one month

prior to this inspection.

Engineering determined that two safety

evaluations had been done based on an ungrounded vital 125-volt-dc

system.

The engineers also determined _ that one of the safety

evaluations, which involved -the effects of a steam break / Loss of

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Coolant Accident (LOCA) event on solenoid actuated valves, was

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adversely affected by the possibility of a ground on the de system.

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With a ground on the positive leg of a vital 125-volt-dc bus, the

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risk existed that a second ground, between the positive side of a

solenoid and its activation contact, could cause that solenoid ~ to

energize or remain energized inappropriately. This would occur since

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the two grounds would be on opposite sides of the solenoid actuation

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initiation contact, because there is no contact on the negative side

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of the solenoid. A very small existing ground (approximately 4000

ohms) on the positive leg of the de bus, coupled with a hard ground

fault on the solenoid could thus prevent the solenoid from dropping

out or even pick it up, and cause a valve to spuriously operate. For

Automatic Switch Company (ASCO) solenoids, the dropout voltage was

about 20 volts and the pickup voltage was estimated to be about 40

volts, with required current in the range of milliamps.

Shown in Attachment 1 is a typical ASCO solenoid circuit, with a

ground fault on the positive side. Also shown is this licensee's

ground detection system, which includes 1000 ohm light bulbs in

series with 2000 ohm resistors, located in both the control room and

at the battery chargers.

A complete circuit through the solenoid

and the ground detector is shown.

The ground detector is discussed

later in this section.

This failure mode adversely affected the operation of approximately

90 solenoids. They in turn operated approximately 30 valves of

concern. The safety evaluation had assumed that these valves would

fail safe in the deenergized condition, and the valves had been

exempted from Environmental Qualification (EQ) sealing requirements.

The affected valve's included all pressurizer power operated relief

valves, main steam isolation valves, feedwater isolation valves,

reactor building cooling unit bypass dampers, reactor building purge

valves, and other containment isolation valves.

Based on this analysis, the licensee promptly modified the affected

solenoid circuits to provide environmental qualification by either:

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Sealing the power supply conduit to the solenoid, or

Installing a contact on the negative side of the solenoid.

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The licensee accomplished the modifications during an outage exten-

sion of approximately seven days.

The plant manager and engineers stated that the probability of- a

steam leak /LOCA event causing the dc busses to become grounded was

high, due to the many non-EQ loads on these busses. The probability

of a ground occurring on the positive side of a . solenoid, and not

simultaneously on the negative side, was not readily estimable. The

licensee believed that the potential for a solenoid to fail energized

in a harsh environment, with a grounded dc power supply, had never

been tested.

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The Engineering Department determined that the installed ground

detectors caused permanent grounds, of approximately 1500 ohms, on

both the positive and negative legs of the vital 125-volt-dc busses.

This magnitude of existing ground was sufficient to make the ASCO

solenoids susceptible to failing energized.

Based on this analysis, the licensee promptly disconnected the ground

detection circuits on both vital 125-volt-dc 'ousses by removing the

light bulbs.

In addition, the licensee wrote and implemented a

maintenance procedure for taking daily ground readings with portable

equipment.

This procedure required locating and removing grounds

(based on voltage and current readings) that were about 5000 ohms or

less.

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The NRC asked if any other equipment, besides ASCO solenoids, existed

with circuitry and components such that it could similarly fail in an

energized condition. The licensee identified the Electro Hydraulic

Control (EHC) main turbine control as potentially susceptible to this

failure mode. The licensee plans to conduct further evaluations, and

to consider further modifications.

The licensee is pursuing the installation of a new ground detection

system that will not create a permanent ground of safety signifi-

cance.

Also, the licensee plans to purchase " state-of-the-art"

portable ground locating equipment.

The licensee stated that this

new equipment shculd enable locating dc grounds in the range of

1500 to 2000 ohms, without having to open breakers.

Better ground

locating equipment may well be a key to maintaining the de systems

ungrounded, since many dc breakers cannot be opened with the plant

at power without risking a trip of the plant.

The licensee's aggressive responsiveness to this issue was note-

worthy.

However, the team considered the past failures of the

licensee to always promptly clear de grounds while the plant

operated and to detect and correct a design problem in the ground

detection circuit as weaknesses.

c.

Shift Engineer

The licensee stated that the addition of a shift engineer during the

outage added to the effectiveness and safety of controlling outage

activities. The shift engineer is assigned to perform the required

Shif t Technical Advisor (STA) functions in modes 1-4, in addition to

many others. Qualification requirements for this position include

being a qualified STA, and in addition being a qualified SRO. A

shift engineer maintains an inactive SRO license. The shift engineer

duties are described in procedure SAP-421, Shift Engineer Conduct of

Operations, Rev. 3.

The position is filled during an outage in modes

5 and 6, as well as in modes 1-4.

A major function of the shift

engineer is to coordinate with and resolve problems involving the

engineering and maintenance departments.

The shift engineer also

performs engineering inspection and review functions, such as

conducting plant tours, investigating abnormal events, reviewing

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jumper and lif ted lead requests, and monitoring cyclic and transient

events.

The shift engineer ' qualification requirements and use

during an outage are beyond minimum regulatory requirements and are

considered to be an area of strength.

d.

Configuration Control and Procedure Control

Gooo configuration control of safety systems can _ reduce the risk of

occurrence of situations that could result in or contribute to an

accident.

To assess the effectiveness of the licensee's procedures

for configuration control of safety related systems prior to' plant

startup, the team reviewed procedures, interviewed operators, and

walked down systems.

In this area of inspection, the team noted

several procedural points that needed improvement. These improve-

ments would increase the assurance of having safety systems aligned

and operable. For each point, the licensee had already initiated

changes or subsequently committed to make changes to the configura-

tion control program, as follows:

(1) The licensee revised all System Operating Procedure (50P)

alignment checklists for safety related systems during this

outage to include independent verification.

The licensee then

performed the independent verification on these systems prior

to plant start up.

The NRC verified this completion of inde-

pendent verification on a sample of 12 of the 45 systems.

(2) The licensee committed to write a procedure on independent

verification, describing how operators are to perform this

function.

(3) The licensee committed to revise procedure SAP-201, Danger

Tagging, Rev. 3 to require that when a tagout- is cleared,

independent verification on valves inside the tagout boundary

will be accomplished and recorded.

After the licensee had completed system SDP alignments, the team

walked down several systems with A0s.

During these walkdowns, the

team compared actual valve alignments with the SOP valve alignment

checklists and plant drawings. They also questioned operators about

the independent verification process. The NRC noted no deficiencies

with the knowledge n'

operators on how to perform independent

verification. The te m walked down all or portions of the following

systems:

Service Water

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Station and Backup Instrument Air

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Process and Area Rad'ation Monitoring

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Boron Thermal Regeneration

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HVAC Chilled Water

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During the walkdowns, the NRC observed a number of equipment,

procedure, and drawing deficiencies.

The team identified these

deficiencies

to the licensee

for corrective

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The

deficiencies

are

summarized and discussed in the following

paragraphs.

In the Service Water system, one valve was open while it was required

to be closed by SOP-117, Service Water System, Rev. 13 and system

drawing D-302-222, Service Water, Rev. 24. This valve, XVG-3178-SW,

DG Air Start Aftercooler SW XConn Viv, was in a one-and-one-half-inch

pipe that cross connected the A and B diesel air start compressor

aftercoolers.

The open valve thus cross connected the two much

larger trains of service water.

The valve had become open when,

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after completing the 50P valve lineup, the licensee performed

STP-123.001, Service Water System Valve Lineup Verification, Rev. 4.

This STP, which has been done monthly in Modes 1-4, has required

this valve to be open since January 3, 1984.

The licensee closed

the valve and changed the Surveillance Test Procedure (STP) to agree

with the SOP and the system drawing.

The team assessed the safety significance of operating . the -plant

with this cross connect valve open.

The valve was in nonsafety

piping, and was downstream of.a flow limiting orifice and check

valve in each of the A and B . train Service Water (SW) supply lines

to the respective' air compressors.

Also, the SW discharge side of

each air compressor aftercooler contained a check valve. With valve

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XVG-3178-SW open and a . loss of one train of SW, the potential loss

of SW flow to the operating train would be negligible in comparison

to the design surplus in SW system flow. The error in valve position-

could not have caused a single failure (loss of one train or pipe -

break) to result in inoperability of both trains of SW.

Two Heating Ventilation & Air Conditioning (HVAC) chilled water

sample isolation valves, XVT-16364-VU and XVT-16373-VU were open

instead of closed as required by the SOP.

The licensee judged tnat

they were probably left open by Chemistry personnel .

The safety

significance of these valves being open was minimal.

The valves

were closed and the licensee stated that the following procedures

would be revised:

(1) SAP-105, Statement of Responsibilities, Chemistry and Health

Physics, Rev.

4, to include authorization for Chemistry to

operate sample valves.

i

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(2) SAP-400, Chemistry Operations Manual, Rev.

5,

to include

I

authorization for chemists to operate sample valves.

l

(3) CP-902, Chemistry Sampling Point List, Rev. 5, to require that

3

after a sample is obtained, the sample valves be returned to

<

their normal position, per the SOP.

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The NRC team also observed a number of other discrepancies, which

!

are summarized below:

-

One Instrument Air System header isolation valve (XVA-72618)

3

was missing from the SOP and plant drawings.

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1

Five Instrument Air System valves had incorrect positions

.

--

listed in the 50P.

Four Radiation Monitoring system valves were missing from the

-

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50P.

These valves were in the correct position.

Identification numbers of several valves and flow instruments

-

were missing from system drawings.

A number of valves needed maintenance, including:

handwheels

-

broken or stripped, caps missing or loose, and packing leaks.

None of these deficiencies caused a system to be inoperable.

There were many errors in SOPS that did not affect valve

-

position,

such as " vent" vs. " drain" and " closed" vs.

" closed / capped."

-

There were a number of label plates with nomenclature or number

different from the SOP.

-

Many label plates were missing from valves.

Prior to plant start up, the NRC reviewed the completed SDP system

alignment records, to verify that the ' licensee had _ completed

independent verification on safety systems. The team verified that

the independent verification had been accomplished.

The team

observed that the licensee had made a number of temporary procedure

changes to the S0P valve lineup forms during the time that they were

,

performing the valve lineups.

Many of these temporary changes

J

involved changes in the required positions of valves.

For example,

1

in the completed SOP-101, Reactor Coolant System Valve Lineup, Rev.

l

17, the required position for three valves had temporary changes,

'

from open to closed or from closed to open, that the licensee had

inserted by pen and ink and the SS had approved. Operations started

this valve lineup on Nov. 11, made the temporary changes on Dec. 10,

and completed the lineup on Dec. 15, 1988.

The licensee had issued

and used the S0P with incorrect valve positions in it.

In SOP-112,

Safety Injection System, Rev.12, the required positions for four

valves contained similar pen and ink temporary changes.

The team

compared the previous revisions of these procedures to the revisions

j

in use, and confirmed that the temporary changes had been to correct

'

typographical errors that had been made in typing new procedure

revisions. The licensee had completely retyped the recent revisions

to S0P system lineup forms for all 45 systems important to safety,

due to a switch from one word processing system to .another ' This

retyping had introduced many errors that had not been corrected prior

_ _ _ - _ _ _ _ _ _ _ _ _ _ - _ _

_.

_

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11

to issuing and using the revised procedures. The Auxiliary Operators

(A0s) and SSs were improperly depended upon to find and correct the

errors while using the procedures.

The use of incorrect procedures

could increase the risk of situations that could contribute to

accidents.

The issuance of these procedures without sufficient

review to insure adequacy is identified as an example of violation

295/88-26-03.

Overall, the areas of configuration control and procedure control

i

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were considered to be weaknesses.

e.

Surveillance Test Procedure Errors

While conducting control room observations, the NRC witnessed the

performance of a part of STP-310.004, NIS Intermediate Range (N36)

Calibration, Rev. 6.

The TS require satisfactory completion of this

calibration procedure.

The team noted that the Instrumentation &

Control (I&C) technician performing this calibration made pen and

ink changes to Data Sheet 4 of the STP, changing acceptance

tolerances as follows:

-

plus or minus 0.010 milliamp dc was changed to 0.100

-

plus or minus 0.050 volts dc was changed to 0.150

The recorded data was acceptable using the new tolerances, but not

with the previous ones.

The NRC team inquired about the basis for making these changes, and

the technician informed them that the changes were made by verbal

authorization of the foreman, to correct typographical errors. The

pen and ink numbers were from the previous revision of the STP. The

inspector was told that the foreman had initiated a temporary change

form for the STP, which would be attached to the completed STP prior

to its approval. The licensee should not have to rely on technicians

to correct procedures while using them.

This increases the risk of

occurrences that could result in or contribute to accidents.

The issuance of this procedure revision with significant errors in

it is another example of violation 395/88-26-03.

f.

LCO Control

During the review of records used for indication and control of

plant status, the team identified a need for improvement in the

Removal and Restoration Log.

Procedure SAP-205, Status Control and

Removal and Restoration, Rev.

6,

describes the R&R Log.

The

licensee uses the R&R Log for tracking safety system status, and

uses three types of entries:

-

Action R&R:

The system is in a Technical Specification (TS)

LCO action statement.

The TS specifies time limits for

restoration of equipment or initiation of additional action.

_

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12

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Tracking R&R:

The _ TS allows the LC0 action statament -to be

-

satisfied by compensatory action indefinitely, or LC0 require-

ments can be met by C train equipment.

Non-TS R&R: Used to limit and track the amount of time certain

-

non-TS items are restricted or removed from service.

In reviewing the index in th_e R&R Log on the af ternoon of Nov,15,

1988, the team noted that Action R&R 880788, on the Chemical and

Volume Control (CS) System, had an LC0 expiration time of.1800 on

Nov. 14, 1988 (the previous day). The TS required a portion of the

CS System to be operational at the time, to provide a boration flow

path with the plant in mode 5.

The LCO expiration information was

also on the log sheet for R&R 880788, with the reason given being an

inoperable snubber.

The . inspector showed this log entry- to the SS.

The SS confirmed that,-based solely upon the log entries, the entire

CS system was inoperable 'due to exceeding a TS LCO action statement

the previous day.

He had not been aware of this problem, and

promptly began to look into the matter.

After further investigation with engineering personnel, the Associate

Manager of Operations determined that the inoperable snubber was

located on the CS letdown line' and did not _ affect the required

boration flow path.

There had actually been no violation of TS

i

requirements.

By reviewing shift schedules and watch station shift turnover sheets,

l

the team determined that a total of 12 different operators, on 3

1

different shifts, had signed for reviewing the R&R Log and had stood

l

watch during the time the log indicated that the CS system was

inoperable.

The licensee confirmed that all 12 had failed to detect

the indicated LCO expiration. The team felt that the SS, the STA,

and on watch operators should have been able to explain why the

required boration flow path was not adversely impacted by the

inoperable snubber.

To prevent future operator failure to detect important. safety

information in the R&R Log, the licensee took the following actions:

i

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Retrained operators in the importance of accurately reviewing

the R&R Log.

Made a commitment to revise procedure SAP-205, to provide a

-

better method of indexing the R&R Log so that Action R&Rs stand

out from all the less important entries. This is identified as

inspector followup item 395/88-26-04.

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g.

Control Room Drawings

Plant drawings are in the Control Room for operators to use in safely

controlling maintenance and abnormal conditions. During control room

observations and interviews, a licensed operator stated that improvement'.

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in the legibility of control room drawings was needed. The team looked

at a sample of about 20 control room drawings, and observed that about

30% of one drawing was totally illegible, and portions of some others

l

were very difficult to read.

The grossly illegible drawing was safety

related drawing 0-302-222, Service Water Cooling, Rev. 24.

This drawing

was date stamped in red:

Copy #9, issued by Document Ccntrol Section,

Aug. 5, 1988.

,

'

Aside from the legibility problem, the NRC team observed that the

drawings were very accessible and easy to use.

)

l

In response to inquiry by the NRC, the licensee stated that the

j

l

Operations Department had identified the problem of illegible

!

drawings.

The Associate Manager of Operations gave the team a

!

copy of a - November 11, 1988 memo from the Operations Manager to

Engineering requesting enhancement or redrawing of 'a list of 10

'

illegible drawings, to ensure adequate quality for use by plant

operators.

The team observed that the problem of illegible drawings also

extended to reduced size drawings in use at the Auxiliary Building

Operator station.

Other than the legibility problem, the drawings

were a very useful aid to the A0s.

The licensee took the following corrective actions:

Conducted an audit of all drawings in the control room.

This

-

audit identified a total of 29 illegible safety-related

drawings.

All of these were reissued, in a legible condition,

prior to the end of this inspection.

The team verified the

legibility of these reissued drawings in the control room.

-

Committed to revise Document Control procedures to provide

better quality control of drawings that are issued.

-

Determined that the cause of most of the legibility problems

was multiple generation and reduction of drawings affected by

plant modifications.

Long term corrective actions will include

reviewing and modifying this process to minimize the degradation

in drawing quality.

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The NRC team's assessment was that Document Control should not

!

issue illegible safety related material without specific management

approval, and the SS should have known of and rejected the illegible

l

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_ _ _ _ _ _ _ __

..

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_ _ _ _ _ _ _

14

drawings.

The licensee's issuance of a grossly . illegible Service

Water Cooling drawing and 28 other safety related illegible drawings

to the control room is identified as another example of' violation

395/88-26-03.

h,

Operator Response to Inoperability of Both Source Range NIs

While the NRC team was observing control room activities with the.

plant in mode 5 and the ~ Reactor Coolant System (RCS) partially

drained, a containment. evacuation alarm sounded.

This alarm was

caused by spiking of source range NI channel N31. At the time, the

second source range NI, channel N32, was labelled inoperable and so

recorded in the R&R Log due to previous spiking with undetermined

cause.

Immediately after the alarm, the operators confirmed both.

source ranges to be indicating steadily at about 10 counts per-

second, the same as they had previously indicated.

Also, reactor

vessel' water level indication remained steady.

The operators

energized spare. source range channel N33 and determined that it

was reading steady at ab'out 10 counts per-second.

There was. no

uncontrolled increase in ' reactor power.

The operators terminated

evacuation of the containment and were perusing the TSs as operations

department management personnel arrived in the control' room.

The operators stated that source range NI spiking had occurred many

times before due to welding activities. They initiated a search for

welding in the area or other cause of the N31 spiking. The operators

declared channel N31 inoperable, until it could subsequently be

proven operable, and initiated TS required action (calculation of

shutdown margin). In addition, they ordered an RCS sample for boron

to be taken. Shutdown margin, based on boron concentration, was well

above the minimum TS requirement.

The operators made an R&R log

entry on channel N31, which included contin 'ng TS required actions

and applicable mode restraints.

Subsequent (y,

operators declared

both channels N31 and N32 operable after the following were satis-

factorily performed:

physical walkdowns, . statistical reliability

checks, and source range analog operational tests.

Overall, the

operators' response to this abnormal condition was timely and

thorough.

i.

Key Control

A0s each carry a key ring containing keys for routine access to

administratively controlled areas. For emergency access to sensitive

!

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radiological or security areas, secure key lockers are located in the

control room and out in the plant.

t

The security door system is supplied .with vital uninterruptible

electrical power.

Should the computerized system fail, security

doors would fail shut.

They could be manually opened to4 exit an

area. However, to enter vital security areas under these conditions,

)

.

use of a security door key would be required.

Through use of the

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_ _ _ , - _ _

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. _ - _ _

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15

secure key lockers, A0s him the ability to gain emergency access to

operationally important arris of the plant. Overall, the key control

system was well organized to provide plant access to operators, and

operaturs were knowledge >Ns of the system.

J.

Fire Protection System Vaives

While accompanying an Auxiliary Building Operator on rounds, the

NRC observed caution tags on closed fire protection system manual

isolation valves for deluge valves. The instructions on each tag

were to open only in the event of fire and at the direction of the

SS. The deluge valves were designed to be remotely. operated from the

,

control room.

The closing of these manual isolation valves thus

removed the control room operator's ability to initiate fire

protection water flow to the affected areas from the control room.

As listed in the Caution Tag Log, a total of 10 deluge sprinkler

i

systems were manually isolated.

The manual valves had been closed

for 15 to 24 months. A list of the valves, and the dates they were

closed, is in Attachment 2.

Six of the valves supply water to

ventilation charcoal filter units in the Control and Fuel Buildings.

These six are shown as normally open -in the Final Safety Analysis

Report (FSAR) and are in systems covered by TS.

.The other four

valves supply water to the charcoal filter units in the Auxiliary

~

and Reactor Buildings.

These four are also shown as normally open

in the FSAR and are in systems not covered by TS. The licensee had

closed the 10 fire. protection system deluge isolation valves to

prevent damage to the charcoal filters in the event of an unplanned

actuation of the deluge valves,

i

The team reviewed the affected control room annunciator response

i

procedure, and noted that procedure ARP-016-XCP-6210, Annunciator

Response Procedure (ARP) for the HVAC Board, Rev 0, did not indicate

the additional immediate action required in the event of a "Hi/Hi-Hi

Bed Temperature" alarm in the charcoal filter units. The procedure

requires activation from the control room of the deluge spray system

in each filter unit in the event of an actual Hi-Hi temperature. The

need to open the nanual isolation valve is not mentioned in the pro-

cedure.

Also, the procedure provided no such instructions for the

operator at the deluge valve control switches in the Control Room.

Further, the licensee had no record of having conducted formal

operator training on this subject.

The incomplete ARP could have

contributed to an inadequate operator response to an emergency

situation.

_ _ _ _ - - - _

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The NRC team reviewed the licensee's safety evaluation for closure

of these valves. That safety evaluation covered only the T$ systems

and was dated July 15, 1987. The safety evaluation addressed only TS

operability concerns, and was incomplete in that it failed to specify

that closure of the valves-(in 1986 and 1987) would require changes

,

to- the control room alarm response procedures, plant drawings, and

i

the FSAR, and would require an associated 10CFR50.59 report to the

NRC. The failure to report this change to the NRC precluded an NRC

safety review of the change. The licensee had a second 10CFR50.59

safety evaluation on this change.

It was-dated November 18, 1988,

and properly required a revision to the FSAR. This latter evaluation

was dated almost two years after the first valve was closed and still

failed to require' changes to the control room alarm response proce-

dures and plant drawings.

The failure to perform adequate safety evaluations for the closure

of these fire protection system valves is identified as violation

395/88-26-02.

In reviewing this deficiency, the Control Room operators could not -

locate their assigned control copy of the Fire Protection Evaluation

Report (FPER).

The FPER is part of- the FSAR, and is .important

reference information for the operators, in that it describes the

approved design of plant systems.

The licensee determined that the

control room controlled copy had been lost for many months. The

clerk in an adjacent office was accumulating changes to be put in

that copy. The licensee pointed out that the fire protection office

located in the control room complex also has .a controlled copy of'

the FPER.

However, that copy was not in the fire protection office

on the date of this inspection, so was not readily available for use

by the control room. The licensee stated that a replacement copy of

i

the FPER would be issued to the control room.

k.

Deficiency Identification and Correction

]

During this inspection, the NRC team observed many minor equipment

deficiencies that had not been entered into the Maintenance Work

Request (MWR) system.

These included such items as broken valve

handwheels, leaking valves, and missing name tags.

Many system

]

leaks existed in the plant which had not been repaired during the

'

outage.

The team observed that many equipment deficiencies in the

plant did not have MWR tags attached and many did. The MWR procedure

implied that hanging a tag when initiating an MWR was optional. The

lack of MWR tags on equipment that has already had an MWR initiated

could be a deterrent to efficient operator initiation of needed MWRs.

i

The licensee stated that the MWR procedure would be revised to ,,

j

require that MWR tags be hung, with limited exceptions,

-

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_

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The team also observed many deficiencies in written procedures and

drawings. Most of the procedures with deficiencies had been in use

!

for years.

The accumulation of large numbers of deficiencies that

i

go uncorrected for months or years could have a resultant negative

I

safety impact on the operation of the facility. The' licensee needs

to improve the overall effectiveness of deficiency identification

q

and correction.

1

3.

Maintenance (62700, 62702, 92700, 92703,-71710)

a.

Licensee's Event Reports and Potential Reportable Events

The NRC Team observed the functioning of the licensee's program

for the evaluation of abnormal maintenance events to assess it's

efficiency in increasing equipment availability through correct

identification of root cause and by initiating the appropriate

corrective action.

The program was being applied to a number of

events (listed in Attachment 3) which were the scope of the team's

evaluation.

These events occurred between July 1987 and November

1988.

The licensee documents the evaluation of abnormal events in

off-normal occurrence (ONO) reports.

In addition, LERs report, to-

the NRC, events which meet the deportability criteria of 10 CFR 50.73.

Except for ONO Reports 870093 and 880004, the licensee had

determined the root cause of each event and had accomplished the-

1

appropriate corrective actions.

In the case of these latter two

ON0s, the licensee had taken the required corrective actions but had

not documented their completion.

The licensee promptly obtained

this information and made the necessary documentation changes.

b. Maintenance Scheduling and Planning

l

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The MWR scheduling and planning ' process, when appropriately and

i

effectively applied, maximizes equipment availability by minimizing

'

its out-of-service time and optimizes plant safety by giving prefer-

,

ential treatment to those components most important to safety.

~l

The inspector observed the MWR scheduling and' planning process by

i

walking an active MWR through each step of the review process. An

j

operations scheduler, maintenance planner, maintenance engineer,

j

health physics scheduler, and quality control inspector reviews each

l

MWR, except emergency maintenance. A maintenance scheduler, during

this particular scenario, hand carried the MWR to each person noted

above. That permitted the inspector to briefly interview each person

!

in the review chain.

The assignment of a " Status Code", which

permits ready location of the document in the review cycle, normally

tracks each MWR through the review process. The licensee also enters

the MWR data into . Computerized History And Maintenance Planning

System (CHAMPS).

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18

The team observed two strengths'in the maintenance. scheduling area.

Fi rst , three SR0s and one A0 staffed the Operations' Scheduling

.

Section.

Personnel fill these assignments on a temporary one year

i

rotating basis.

The. expertise of licensed personnel was a strong

1

d

point of the scheduling process.

Second, each day the Scheduling Section prepared a " Trip Package"

which contained planned maintenance activities requiring a duration

of less than 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> to perform.

The Scheduling Section delivered

the " Trip Package" to the Shift supervisor at the end of each normal

werk day and picked it up the following morning. The " Trip Package"-

included only items that could be accomplished in Mode 3. - Addition-

ally, the scheduling section planned a "Short Duration Outage

Package" for those activities which could be completed in the event

,

plant trip recovery took longer than 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> but less than 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.

]

'{

The team noted one weakness in the scheduling area. Although each

1

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maintenance planner had plant work experience ranging from apptentice

to foreman in his respective work speciality, there was no formal

qualification or training program for maintenance planners.

Some

planners had attended systems training and supervisory training but

i

this training was not routinely offered to all planners.

c.

Work Orders in Process

The maintenance planning and scheduling process above had priori-

tized, planned, and scheduled for implementation during the NRC

]

team's on-site assessment period those MWRs listed in Attachment 4.

4

Each MWR contained adequate procedures and instructions to ensure

that the maintenance craft personnel could accomplish the specified

1

work.

These procedures and instructions contained appropriate

~

Quality Control (QC) hold points.

The MWRs provided good interface

between the maintenance and operations staffs.

They also contained

appropriate radiation controls, spqcial housekeeping, scaffolding

controls, and burning and transient permits, except for MWR 8801131

which is discussed in the next paragraph.

During a plant tour the NRC inspection. team identified a total of 45

drums of charcoal, 200 pounds each, stored on the 463' level of the

auxiliary building.

Maintenance personnel performing the work

directed by MWR 8801131 had temporarily stored this charcoal in this

,

area preparatory to replacing the auxiliary building ventilation

1

system (XAA0040A) charcoal.

This charcoal storage resulted in an

increased fire load for which appropriate compensatory fire protec-

tion considerations had not been established.

Procedure SAP-601,

Application, Scheduling and Handling of Maintenance Activities

(Rev. 4) Section 7.2.15 requires transient combustible requirements

i

to be determined by the discipline planner.

Procedure FPP-003,

Control of Transient Combustibles, Sect-ion 3.1, 4.3 and 5.1, requires

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19

4

maintenance planners and job supervisors to generate a transient

1

combustible permit and specify the applicable fire protection

i

requirements for jobs which result in an increased fire. loading

within the plant. The NRC has identified this failure to perform an

appropriate transient combustible evaluation for MWR 8801131 as

another example of violation 395/88-26-01.

d.

Completed Maintenance Work Requests

The NRC team evaluated the recently completed maintenance work

requests listed in Attachment 4 for maintenance work in the mechan-

ical, electrical and I&C areas. The team concluded that completion

of 'these work requests contributed to better equipment availability.

'

This conclusion was based upon the team's consideration of several

l

licensee actions on ' each MWR:

adequate review and processing; post

l

maintenance testing; special housekeeping (as specified); independent

l

verification of lifted lead restoration and similar items; QC

l

inspector review of QC hold points; and technical evaluations of

.

i

inoperative systems or systems in need of repair to determine root

p

cause.

e.

Maintenance Overtime

The NRC has concluded that an individual's' detection of visual

signals deteriorates markedly with fatigue. Additionally the time

it takes for a person to make a decision increases and'more errors

are made.

For these reasons, the licensee should have a sound

policy covering working hours for the plant staff, such as' key

l

maintenance personnel, who perform safety related functions.

(IE

!

Circular 80-02)

The team reviewed the licensee's policy for control of outage

overtime.

The review included inspection of time and attendance

sheets for hourly paid maintenance personnel, interviews with

]

personnel from each maintenance discipline, and review of TS and

1

procedural guidelines concerning overtime.

The responsible department manager granted authorization to deviate

j

from established overtime guidelines prior to the outage and docu-

)

i

mented it on a properly executed " Authorization to Deviate From

I

Overtime Guidelines".

This authorization was for the entire depart-

'

ment for a 31/2 month time period encompassing the outage and post

outage start up.

Work hours during the current refueling outage

generally consisted of 6 consecutive 12-hour days followed by 1 day

off.

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20

Interviews with maintenance technicians, particularly in the I&C and

electrical groups, indicated - that personnel were discouraged from-

working more than 6 consecutive 12-hour. days without a day off.

However, in the mechanical maintenance area, the ' team noted several

instances of personnel working 12-hour days continuously, for 3 to 6

weeks, without a day off. While the team recognized that TS and

procedures may permit such extended work hours during a' refueling

. outage, they regarded this to be excessive use of overtime and

therefore not a good personnel managemant practice.

If not care-

fully monitored, blanket overtime authorization can lead to increased

error rate among key maintenance personnel while performing safety

related functions.

f.

Backlog Status of Maintenance Work Requests

It is'self evident that returning equipment to service in the order

of importance leads to optimization of availability of safety related

equipment.

Management controls on MWR backlog such as backlog

trending are necessary in order to ensure that the backlog of

important equipment requiring repair does not exceed the capability

of the maintenance group while working' within a sound overtime

policy. To measure these present and future equipment availability

indicators, the NRC' team reviewed the MWR backlog trend and manage-

ment controls on the MWR backlog.

They also covered the method of

work prioritization to ensure that equipment was returned to service

in order of importance.

Work priority was based on the importance that the work activity had

i

to the centrol of the plant. While "importance to control of the

plant" is not synonymous with "importance to safety", the team felt

they are so close that the difference will have a negligible effect

on safety.

The Summer staff assigns to all maintenance one of the

I

following priorities: emergency maintenance, priority 1,1S, 2, 25,

3, 4, or 5.

The SS determines those MWRs that require emergency

maintenance.

The SS also has the sole responsibility of assigning

Priority 1.

The Security Maintenance Supervisor may . assign priority

IS.

Af ter Maintenance has addressed all priority 1 work 'they can

then work Priority 2 and 2S MWRs.

The Operations Schedulers assign

the remaining classifications of priority. The licensee managed well

!

the prioritization of maintenance activities.

Scheduling generated a monthly report which listed all MWRs greater

than 3 months old. The Manager, Maintenance Services, then reviewed

the report and presented his findings to plant management.

For the

seven months preceding the current refueling outage, the percentage

of total corrective MWRs greater than 3 months old (MWRs greaters

than 3 months old/ total open MWRs) was approximately 47 percent which

is below the industry average of 52 percent.

The team considered

timely review of MWR oacklog and the relatively small number of MWRs

older than 3 months to be a strength.

'

l

__

-

.

21

g.

Calibration of Instrumentation

A good instrument calibration program ensures that those instruments

required by TS or associated with routine operator duties are

maintained within the required operating bands of the instrument.

The NRC Team reviewed the implementation of the calibration program

for permanently installed

instrumentation.

Procedure SAF-141,

Control and Calibration of Measuring and Test Equipment, Rev. 2,

establishes the calibration ' requirements.

The team verified that a

sample of-12 installed instruments used by the plant operators during

routine shift rounds to record plant data and 8 installed instruments

used by the plant staff to record data during surveillance testing

were included in the instrument calibration program and that they

had not exceeded their calibration due date. These instruments are

listed in Attachment 5.

The licensee's program for maintaining the

calibration of permanently installed instrumentation devices appeared

to be effective.

h.

Status of Maintenance Work Requests Older Than 6 Months

At the time of this inspection approximately 525 MWRs had been written

and approved for work.

Of this total approximately 110 work requests

were more than 6 months old.

The NRC Team reviewed these MWRs and-

.

found that the work had not been accomplished due to: maintenance work

assigned a low priority; repair parts had been ordered but had not been

received; or, the work had been scheduled to be accomplished at the

next available system / component shutdown.

This review indicated that

maintenance work which must be performed to preclude a possible major

load reduction, unit shutdown or meet an NRC requirement received a

'

high priority and appears to be accomplished.in a timely manner.

Based

upon this information, the .tean concluded that equipment availability

was enhanced by the timely review and small number of those MWRs greater

than 6 months old.

4

1

1.

Plant Observations

Plant housekeeping is indicative of plant management attention to

plant cleanliness, maintenance of equipment and structures, and

I

controlling the spread of contaminated material. There is a definite

i

relationship between plant material condition and proper' housekeeping'

l

practices.

'

1.

General Plant Housekeeping

The team conducted a housekeeping tour of the auxiliary, fuel

handling, and diesel generator buildings. Even though the unit

was in a refueling outage, the licensee was maintaining good

housekeeping practices. The licensee promptly corrected several

minor discrepancies which the team had pointed out.

The.

following two paragraphs discuss two of the more significant -

observations.

_ _ - _ _ _ _ _ _

_

._.

22'

The licensee needs to improve the labeling of components and

component room doors.

Room doors were identified only with an

alpha-numeric identification and did not- have a word description-

of the contents of the. room. Similarly, major componentsLlacked

prominent labeling with a word description of . the component.

The licensee is considering a label enhancement program that

would improve component tags and component room door'identifica-

tion.

This label enhancement program would result. in more

easily identified plant equipment which would be especially

beneficial ' during' emergency situations when time is of the

essence.

The team noted, during a walkdown of Diesel Generator Room "A",

that the local control panel ARP was missing from the panel.

The licensee stated that they had removed ARP-004-XCX-5201,

l

Annunciator Response Procedure .for "A" Diesel. Generator, Rev. 2 '

as required in SAP-139, Procedure Development,. Review, Approval'

and Control, Rev. 11, because it exceeded its 2 year review -

date on November 4, 1988.

SAP-139 requires that "No safety-

l

related/ quality related proceedure shall.be used beyond its-

'

two year review date".. However, SAP-139 also states that a

l

monthly print out shall be issued identifying procedures that-

l-

are due for a 2 year review in the next 3 months. Therefore,

i

the licensee should have'been cognizant of the expiration date

at least 3 months prior to reaching that date.

The licensee

placed the ARP on hold and removed.it from the panel on November.3,

1988, then subsequently reviewed and reissued-.it on' November 18,

1988.

No ARP was available for operator _use'in Diesel Generator

3

Room "A" during the 15-day interval .between removal and reissuance

'

of the ARP.

During that' time, the diesel.was in.an operable-

status. Absence of the ARP could have resulted in an untimely

or inappropriate response to a diesel alarm with'resulting damage

to safety-related equipment.

The failure.t'o follow procedure

concerning the required review of a safety-related procedure within

!

the 2 year time restraint and resultant failure to provide an.

]

approved procedure for operable safety related equipment during

1

l

a 15-day interval is identified as another. example of violation

,

395/88-26-01.

'

Overall plant housekeeping was very good.

l

2.

Scaffolding Controls

I

Procedure GMP-100.009, Scaffolding,-provides for the control of

erecting scaffolding within the plant.

It provides sufficient

controls to prevent damage to safety related components - from

>

scaffolding related accidents such as scaffolding collapse or

dropped equipment, and to provide for personnel safety.

The

L

procedure requires approval by the SS prior to scaffolding

'

being erected over or in~ the vicinity of safety-related equip -

ment.

However, at the beginning of the inspection, the . NRC

l

Inspection Team noted that scaffolding erected to work on

1

-

_ ___ _____-______--___- - - _ _--___ __ .________-- _-___ __

,

.__ ._ . _ _ _ _ _ - _ _ _ _ _ _

__

23

equipment and components installed above floor level did not

contain toeboards as required by the procedure.

The licensee

promptly initiated appropriate corrective action.

By the

conclusion of this inspection licensee personnel were providing

toeboards for all scaffolding, where required.

\\

3.

Radiation Controls

Each of the MWRs reviewed by the Team indicated the assigned

radiation work permit, if the work was to be accomplished within

the radiation controlled areas of the plant. The NRC Team did

not identify any noncompliance with the radiation protection

procedures during observation of personnel performing work in

radiation areas.

j.

Preventive and Predictive Maintenance Programs

The CHAMPS tracked all routinely performed preventive maintenance

tasks.

Three months prior to a Preventive Maintenance Task Sheet

(PMTS) due date, CHAMPS generated a PMTS which was routed through a

maintenance scheduler who forwarded it to the appropriate maintenance

discipline for review.

When feasible,

maintenance personnel

performed PMTS in conjunction with other scheduled maintenance

activities. When repetitive equipment failures occurred, the program

allowed increasing the frequency of the associated PMTS.

The

licensee performed PMTSs or lubrication tasks, unless specifically

identified to the contrary, within their scheduled due date +25% of

the PMTS interval.

For mandatory PMTS activities, i.e. , those required by regulatory or

engineering commitment, that could not be performed within their

required periodicity, Systems Engineering performed an evaluation of

the effect of the delay on the equipment.

Review of SAP-143 and

interviews with personnel indicated that the definition of " mandatory

activities"

was not clearly defined in SAP-143 nor adequately

understood by the Systems Engineers who have the responsibility of

determining whether a specific

PMTS i s mandatory.

The team was

informed by the Coordinator of Maintenance that the definition of

" mandatory activities" would be inserted into SAP-143.

l

In May 1988, Summer Nuclear Station Quality Assurance (QA) issued

I

finding #09-RMB-88-0-02 concerning an overdue PMTS on Service Water

Booster Pump

"A".

A recommendation of that finding was that

appropriate personnel perform a review of the PMTS program and

identify all overdue PMTSs.

On June 27, 1938, the Manager,

Scheduling and Modifications, in response to that finding, stated

that a large number of PMTSs were lost and/or overdue and that the

_

_

_

____. .__

.

. - . . _ _ _ _ _ _

_

__

_. _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ - _ _ _ _

_

24

initial corrective action would be to distribute to the responsible

supervisors monthly reports showing overdue or near overdue PMTSs.

QA stated in subsequent reviews that although the manager of

scheduling and modifications was generating monthly overdue reports,

that action was generating no progress in the reduction of the total

number of overdue PMTSs (Inter-Of fice Correspondence, CGSS-494-QA,

dated August 22, 1988).

Also, QA would continue the review of the

effectiveness of the program until it had established an ac eptable

trend.

Additionally, QA stated that the Manager, Scheduling and

Modifications failed to identify any safety-related PMTSs in the

monthly overdue report.

QA stated in Inter-Of fice Correspondence

CGSS-591-QA, dated September 20, 1988, that limited data received to

that date indicated a possible adverse trend in the area of overdue

PMTSs.

QA had scheduled for April 7,1989 a verification of the

implementation of the corrective action measures to reduce the

number of PMTSs.

The Manager Scheduling and Modifications did not issue overdue PMTS

monthly reports during the current refueling outage.

Due to the

lack of overdue PMTS data, the team could not determine the trend of

overdue PMTSs.

This item will be reviewed in a future NRC

inspection and is identified as IFI 395/88-26-05.

The team discussed with maintenance management the predictive

maintenance proomm.

They specifically discussed the chemistry

ferrography laooratory and the electrical maintenance vibration

trending programs. The team also toured the ferrography lab with a

chemistry supervisor.

The ferrography lab had been in existence for approximately 2 years,

l

while the vibration trending program was begun about 6 years ago.

'

Each program had regularly scheduled sampling and data collection

i

intervals for each major piece of equipment.

The lab was to trend

'

data using a computer program.

They closely monitored any unusual

trends and initiated corrective maintenance prior to predicted

equipment failure.

The ferrography and vibration trending programs

are functioning well and the licensee is considering expanding their

predictive maintenance efforts.

The team concluded that such

preventive and predictive maintenance programs have the capability

of identifying equipment problems prior to actual equipment failure.

Early identification of equipment deficiencies permits timely

maintenance response and the possible prevention of loss of safety-

related components.

t

.

_ . .

m

-

_

-- _

_ - - . - - - , - - - _ _ _ - - - - _ - - - -

!

25

i

4.

Engineering (37700,37828,42700,37702)

The safe operation of a nuclear power plant.is predicated on an adequate

design

This design incorporates various codes and standards governing

the construction and operations of the facility to ensure the. safe

.

operation. The design engineering function at the plant is carried on to

ensure this. design basis is maintained ' throughout- the -lifetime of the

facility and is not ~ abrogated by changes to- the structures, systems and

components or the manner in which they are operated.

.

The team reviewed the procedures used by the Design Engineering Department

to ensure that .the functions of the department would, if accurately

carried out, maintain the design basis. -The team also reviewed the

Modification Request Form (MRF) packages being installed during the

current outage and those previously installed as ~ noted in Attachment 4.

The team conducted this review to ensure that the packages contained

adequate procedures and instructions for installation, protective tagging,

housekeeping, QA/QC controls, and material procurement control. The team

walked through the MRF process noting especially .the initiation of the

,

MRFs by operations, the screening . process by which MRFs are prioritized

l

and scheduled.

The team reviewed completed MRF packages to verify

they contained the results of post maintenance testing; QA/QC review,

engineering technical review,and close-out procedures.

The team interviewed engineers, mechanics, and' electricians to ascertain

the procedural adequacy lof .the MRF packages received for installation,

the operations / maintenance interface on MRF installation, and ' problems /

concerns that should be addressed.

The team held discussions with members of the engineering services

department and the scheduling personnel to verify that MRFs are screened

for priority

and scheduling is done on the bases of importance to

s a fe ty .

I

The Engineering Services Department has started a program to establish a

l

design bases document (DBD) for plant systems. This document contains an

introductory section that describes the purpose and organization and

scope of the document.

It also contains a system description, a system

design basis, a component design basis, an accident analysis, a margin

summary, and a listing of reference documents.

DBDs have been prepared

for 14 plant systems and several more are in the process of being

,

prepared.

The team considered the preparation of these DBDs to be a

l

strength of the facility.

These DBDs will be a living document which

l

will enable the plant staff to maintain. a safe margin in plant operations

l

as well as document the design bases of the system and components.

l

No violations or deviations were identified.

l

I

1

l

E ----------------- ---

- - - - - - - - -

- - - - - - - -

-

b

_-_ _ ____--

26

5.

Independent Safety Engineering Group (ISEG)

'The ISEG functions to provide an independent review of plant operations,

operating experience feedback and operating characteristics of the plant

with a responsibility to ensure the plant activities are conducted.

correctly and that human errors'are reduced as much as practical.

The team reviewed the ISEG reports for safety system functional inspec-

tions (SSFI) the licensee had performed on the ac & dc distribution system

and the. service water system.

The ISEG has utilized contractors to

supplement their own expertise in performing these inspections.

The

inspection results reviewed by the team _ appeared to be of sufficient

depth and scope to provide the licensee with a valuable tool for evalu-

ating system performance.

The ISEG current goal is to perform two of

-

these SSFI inspections each year. The team considered the performance

of these inspections to be a strength.

No violations or deviations were identified.

6.

Quality Assurance

The Quality Assurance (QA) function is important to operations in that it

verifies that those activities affecting the quality of safety-related

components, systems, and structures are carried out' in accordance with

approved procedures and that the quality of those items affected is

maintained.

The QA Department accomplishes this function by. conducting

audits and surveillance

of safety-related functions accomplished by the

other departments of the plant organization.

The team reviewed the requirements of TS 6.5.2.8 on the scope and

frequency of audits in conjunction with the audit planning matrix and

schedule.

The team confirmed that the planning matrix and schedule

addressed all TS requirements.

The personnel of the QA department also

perform a number of surveillance type activities which encompass various

aspects of plant operation.

In discussions held with the team, the QA manager outlined the facility's

plans to correct what the manager perceived to be a a lack of commercial

nuclear power plant operational experience in the QA department.

Pending

completion of the present outage, a licensed operator will be transferred

into the QA department.

The QA manager also noted that individuals

with strong engineering, I&C, and maintenance backgrounds are also being

requested.

The acquisition of these individuals will greatly assist in

the completion of performance based audits with operationally constructive

findings. As a result of efforts thus far, personnel of other departments

perceive the QA department as becoming more creditable and constructive.1

'

,

_ _ _ _ _ _ _ _ _ _

,

_

_

_ _ . - . - _

_

. _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ - _ - _ _ -

27

QA conducted an audit, Audit Report II-12-88-E, Control Room and Station

Operations, between July 6 and July 21, 1988, not only to meet the commit-

ments of TS and the operational quality assurance plan, but also to

assess performance in the area of operations. The. results of the audit

documented a large' number of compliance items with summations on 'the

thoroughness of processes and personnel activities. The team considers

incorporation of performance based audits into the realm of QA activities

as being extremely beneficial to the . facility's safe operation. As noted

by the QA manager, Audit Report II-12-88-E was the facility's first

performance oriented audit. The lessons learned from identified findings

and audit methodology, coupled with the incorporation of engineering,

maintenance and operational experience,

will serve to develop the QA

department into a significant tool in the safe operation of the facility.

,

No violations or deviationswere identified.

7.

Plant Status Meetings

Communications or the exchange of information among members of the plant

staff is important to safety.

Changes in plant status affect every

department of the staff and accurate information is vital to -the proper

i

functioning of the departments and thereby, to the safe operation of

the plant.

It is therefore important that communications be effective, .

efficient, and accurate.

Important information must be thoroughly

disseminated through the plant organization in a timely manner.

The team attended various plant status meetings to determine whether the

licensee adequately disseminated day-to-day plant activities and planned'

future activities to the applicable staff. Status meetings are conducted

by the General Manager of Operations and Maintenance.

Discussions of

particular ongoing' activities are provided by. the various department

I

managers. They also identify support that is needed from other depart-

ments. Overall, while members of the plant management staff are cognizant

of plant status, ongoing activities, and general problem areas, a sense

'

of heightened importance was lacking during the course of these meetings,

i

especially when viewed in light of the ongoing outage.

In particular,

)

discussions pertaining to the outage's critical path were absent from the

status meetings.

I

No' violations or deviations were identified.

8.

Plant Safety Review Committee (PSRC)

The PSRC is responsible to advise the Plant Manager on all matters

related to nuclear safety.

This group is the last collective body where

various interfaces are brought together below the Plant Manager level to

i

ensure that all disciplines are considered in the operation of the

facility and changes to that operation.

i

_ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ . _ . _ _ _ _ . _ _ _

__

_

._.

_

__

_

.___-____ __ _ _ _ _ __ - _-_ _

28

The team examined the activities of the PSRC to assess whether it was

functioning in a manner that optimizes safe plant operation by providing

adequate interface with various plant disciplines, and by performing

adequate safety reviews. This assessment encompassed an interview with

l

the PSRC chairman, a review of TS Section 6.5.1, a review of the governing

station administrative procedure sap-120, Plant Safety Review Committee,

.Rev. 4, observation of PSRC meetings and review of selected minutes of

PSRC meetings. The PSRC met regularly on Wednesdays and as required to

l

address urgent matters.

Prior to PSRC meetings, members were provided

I

with the meeting's agenda.

The agenda elaborated extensively on the

l-

subjects to be discussed thereby allowing the members to be better

prepared and to allow for a smooth flow of the meeting's business. The

team attended meetings during which the following areas were addressed:

TS changes; bypass authorization requests; and safety reviews associated

with modification requests and change notices, nonconformance notices,

and procedure changes and revisions.

Where appropriate, the PSRC was

assisted in its review of items by a representative of the department

responsible for the item. That facilitated communications and provided

real-time answers to questions raised.

No violations or deviations were identified.

9.

I&E Notices

l

Evaluation of information from outside sources is a valuable input to the

I

safe operation of a facility. Various sources provide information to the

plant staff for evaluation and incorporation if applicable. This informa-

tion is useful in avoiding mistakes made by others, as well as providing

for increased equipment availability.

The team selected four IENs from the past 18 months to determine the

adequacy of the licensee's review and their response.

Additionally,

IEN 88-86, Operating with Multiple Grounds in Direct Current Distribution

Systens, was examined because of recent industry problems and indications

in the control room of the presence of de grounds.

The licensee had, in all cases, reviewed the subject IENs in a timely

manner or were taking action on them. The Technical Oversight department '

coordinates the processing of IENs with input from various plant depart-

ments including the Engineering Services Group for technical evaluations

,

and the Nuclear Operations Education and Training department for training

j

requirements.

The evaluations reviewed, by the team, considered the

1

appropriate aspects of plant design, the FSAR, maintenance practices, and

i

plant operations. The thoroughness with which the IENs are evaluated, by

1

the plant staff, ensures that the licensee avoids similar problems experi-

i

I

enced by other facilities.

~.

No violations or deviations were identified.

l

l

>

L__________-___-_______-_______--______.-__

- _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

__

- - _

- - . . .

_

. _ _ _

_ - -__

_ - _ _ _ _ _ -

_ _ _ _ _ _ _ _ _ _ _ _ _ _

_ _ _ _ _ _ _ _ _ __ _ _ _ _ _ _ _ - _ _ _ _

_

1

29

l

10.

Performance Monitoring Programs

The trending of.various performance parameters is important in order to

determine the availability of equipment in the plant and operations

expertise in operating the plant effectively. It also can be utilized to

predict, in a general way, future equipment operability status and .to

avoid unnecessary challenges to safety equipment.

The Operations Technical Assistants were compiling various monthly and

quarterly trending reports for Operations management'.

The documented

trends included Emergency Core Cooling System (ECCS) availability,

overall plant performance, fuel and gas consumptions, and administrative

errors. The trending reports were distributed to various members of the

l

'

plant management. The plant management was cognizant of the existence of

,

the various trend reports and believed that the reports were providing

I

information which assisted in safe plant operations.

No violations or deviations were' identified.

11.

Emergency Operating Procedures (25592)

a.

Background Information

V.C. Summer responded to Generic . Letter 82-33, " Supplement 1 to

NUREG-0737-Requirements for Emergency Response Capability," on

July 30, 1984 in a letter to the NRC submitting their Emergency

Operating Procedure (EOP) Generation Package. The E0Ps are based on

Westinghouse Owners Group Emergency Response Guidelines (ERGS),

Revision 1.

The licensee conducted a comparison of VC Summer to the

generic plant and submitted it to the NRC in the Procedure Generation

Package (PGP). Additionally,'the submittal included an E0P deviation

document, which outlined the specific. areas where SCE&G's E0Ps differ

from the ERGS, revision 1, and an Administrative Procedure (SAP-207)

which detailed the development of the E0Ps. 'The E0P Writers Guide

and validation program were designed using guidelines published by

,

the Institute of Nuclear Power Operations (INPO).

!

In June 1987, the NRC forwarded a Draft Safety Evaluation Report

(SER) to V.C. Summer, informing them that their PGP was not _ accept-

able as submitted.

Deficiencies of note included inadequate

documentation of deviations from and additions to the generic

guidelines, Writer's Guide deficiencies, inadequate guidance and

scope in the verification and validation process and lack of depth

and content in the operator training program.

,

I

i

V.C.

Summer had not obtained an approved PGP.

They had initiated

I

actions to resolve the discrepancies noted in the Draft SER.

Fore-

i

most'among these efforts were a new draft E0P Writer's Guide for use

j

in procedure generation, a revised SAP-207 which specified the

1

programmatic guidance and administrative requirements for the

]

development and maintenance 'of E0Ps, generation of a draft E0P

1

Setpoints Document to provide technical justification for process

j

I

i

_____

_ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ . _ . _ _ _ _ . _ _ _ .

._.

_

_

_ . _ _

v

.

30

'

-

.-

.

-variables and trigger .setpoints used in_ the E0Ps and the generation

'

of a draft E0P Plant Differences Document to identify and provide

justification for deviations and additions to the generic Westing-

house guidelines.

It 'was.. the licensee's intent ~ that. once these

~

documents are in place', an independent ;outside organization will

conduct an audit' to ensure that the intent of .the Westinghouse. ERGS

and NUREG-0899 are met.

Then a : major rewrite of all E0Ps will:

be initiated in 1989, with .all procedures in place and ' training

completed by the 4th' quarter of 1989.

b.

Review of the E0Ps by In-Plant and Control' Room Walkdowns

The team conducted in plant andi control' room ' walkdowns of the

emergency procedures listed in Attachment .6.

They . evaluated the

.

effectiveness of the E0Ps;by focusing on the current status of ..the

procedures and whether they can successfully mitigate' accidents given

the procedures as they.now exist. The team verified, that indicators,

annunciators, and controls.were accurately referenced in the EOPs,

that the steps in the E0Ps could physically be performed, considering

human factors conditions, and'that the' operators were confident in

the procedures' ability'to mitigate the consequences of an. accident.

The team has identified discrepancies in-labelling and human factors

concerns in Attachment 7.

The comments in Attachment 7 are identi-

fied as : .pector followup item 395/88-26-06.

Emergency Operating Procedures were found to be adequate to place the

plant in a safe, stable condition'.

While the procedures do ~ not

conform to the format required by the draft Writer's Guide, .the team

concluded that the procedures could ' physically.-be- performed as

q

written, with the exceptions noted .-in Attachment -7.... Generally, the

'

l

team found that setpoints are. not supported. by..a Setpoint Document.

l

The licensee has created a draft Setpoint Document 'that includes

allowances for potential cable degradation losses (I.R. ' Loss). Two

'~

licensed operators demonstrated the E0Ps during the walkdowns.

They were proficient in their use of the procedures and confident

that the procedures would mitigate the consequences of an accident.

c.

Simulator Exercise Observation-

1

The. team observed NRC-directed simulator exercises involving E0P

usage for an operating crew. The crew was briefed ahead of time on

the emergency procedures that would be utilized.

The team concen-

trated on the usability of the E0Ps, the operators' familiarity with

the E0Ps, the extent of physical interference and duplication of .

effort among the operators while performing the~ E0Ps, and the

efficiency and thoroughness of procedural transitions.

The . team,

utilized their observations - of the operators' ability to use :the

E0Ps, as well as postscenario discussions, - to determine whether-

l

procedural or training deficiencies existed.

Deficiencies or

j

observations not noted in the following paragraphs will be found in

Attachment 7.

'~

j

,

,

i

1

i

_ _ _ _ . _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _

_

_ . _ _ ~

l

..

m

31

The first simulator event consisted of a loss of'all alternating

current (AC) power, with subsequent recovery of one diesel generator,

complicated by a small break loss of coolant accident (SBLOCA).,

The simulator modeling of_ the characteristics and response of the

Seal Injection Flow Control Valve, HCV-186, were inadequate.

Its

throttling characteristics were incorrectly modeled.

This led to

negative training in that another locally operated. valve downstream

had to be operated to perform the important step of restering seal

injection flow in a controlled manner.

l

I

The second simulator event consisted of a loss of heat sink accident,

with the intent being to force the crew into a bleed' and feed

initiation until levels were recovered in the steam generators

"

( S/G s),.

at which time they would recover from the bleed and feed

situation. Again, the team noted simulator modeling problems which

provided an unrealistic plant response that would lead to negative

operator training.

The steam line power relief valves (PORVs)

provided little S/G' depressurization effect until they were almost

full open. Also, when these valves were closed, S/G pressure would

increase, even when there was very little mass in the S/Gs and the

only pressure source was a condensate booster pump with a discharge

pressure of less than 300 psig. Another modeling deficiency pre-

vented establishing a natural circulation condition once delta T

across the core had been raised above 60 degrees F by a " Loss of Heat

Sink" accident. Therefore, even with level restored in two S/Gs and

800 gpm bleed and feed flow cooling the core, cooldown could not be

established. This prevented the operators from continuing on into

the procedure to recover from bleed and feed operations.

The team

concluded that this was caused by the simulator model assuming

natural circulation flow was zero if delta T across the core was

greater than 60 degrees F.

Several procedural problems were noted. The most significant were:

1.

Step 4.h requires initiation of 100 gpm flow to the S/Gs though

the meters / recorders are calibrated in MPPH (mass pounds per

hour). The operator cannot adequately determine if 100 gpm is

I

established. The purpose of this step is to limit the potential

)

for thermal shock of the S/G tubes.

j

2.

Step 4.1 does not provide guidance with respect to the condi-

tions that must exist before the operator can start increasing

,

feed flow above the 100 gpm established in the preceding step.

l

This could either result in thermal shock of the tubes if done

i

l

too early, or delay the recovery of a S/G as a heat sink'if done

too late.

1

i

m

32

.

3.

Steps 19-25 do not have a hold point to keep the operator in the

loss of heat sink procedure (E0P-15.0), if the criteria in steps

19 a, b, and c are not met.

These criteria need to be met in

order to enter the subsequent procedure, E0P-1.2, Safety Injec-

tion (SI) Termination.

These E0P procedural problems are identified as inspector

followup item 395/88-26-07.

The third simulator event that was observed was a S/G tube rupture,

with 'a subsequen.t SBLOCA af ter the ruptured S/G was isolated.

The

team found it and the simulator response to be adequate,

d.

Independent Technical Adequacy Review of the E0Ps.

~

The team reviewed the E0P verification and validation documentation

for the procedures listed in Attachment 6.

The vendor recommended

step sequences were followed. The documentation for step deviations

were of borderline value to future E0P developers in that they

typically stated the reason for the deviation to be a " plant specific

requirement." The team found that the licensee had resolved comments

that had been made concerning procedural discrepancies and had

changed the procedure accordingly.

The validation process had

l

generated the comments.

l

The QA Department and ISEG did not actively participate in the

development and validation of the E0Ps.

The QA group conducted two

l

audits in 1986 and one audit in 1987.

Currently, QA has no open

items on the E0Ps, other than monitoring the program once per quarter

l

to ensure completion of the Procedure Generation Package. _ QA has

'

planned performance based inspections to begin with SAP-207 implemen-

tation. Through the performance of SSFIs, the ISEG has addressed the

E0P-Systems interface.

ISEG had four open items on the E0Ps.

The

team found that one of the four had been corrected, but had not been

closed out in the ISEG's records.

pparently, the procedures group

use of the informal feedback program caused this error.

The team reviewed the E0P feedback program used. This program

4

l

receives procedure change requests from users and from the design

!

control process.

The team found that changes requested from the

operators were kept informally and no tracking or tickler systems

~

existed. Numerous feedback requests lacked the name of the requestor

or the date of the request

The licensee intends to implement a

,

formal operator feedback form with the issuance of the final SAP-207.

1

To assess the adequacy of the changes to the E0Ps resulting from,

t

design changes, the team reviewed all the Modification Request Forms

associated with the procedures listed in Attachment 6.

Plant

,

modifications which could have effected the E0Ps had been reviewed

and the procedures had been revised where necessary. Where modifi-

cation.s effected plant drawings used by the operators they"were

i

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _

_ _ _ _ _ _ _ _

~

.

33

updated by the use of interim drawings. The oldest' interim drawing

was dated August 1, 1986.

More timely incorporation into a permanent

plant drawing is appropriate.

This will aid the operators by reducing

the number of references they may have to use during an emergency. - The

team noted no other discrepancies in this area.

The team did note that the ECP procedure index was out of date with

regard to the revision number and the cate for numerous E0Ps.

However, the operators used controlled copies which are verified to

be current revisions without relying on the index.

The licensee

intends to delete the revision numbers and dates from the index to

avoid duplicating information found in the Master Control Copy.

12. Action on Previous Inspection Findings (92700, 92701, 92702)

(CLOSED) Inspector Follow Item 395/88-03-03, Completion of revisions to

natural circulation cooldown procedure.

This item involved several procedural deficiencies noted during the NRC

review of the natural circulation cooldown procedure.

The team reviewed

the revised procedure against the items listed in the inspection report

and concluded that all items identified in that report had been included

in the revised procedure. The actions taken to address this issue are

therefore considered satisfactory and this item is closed.

13.

Exit Interview (30703)

The inspection scope and findings were summarized on December 22,1988,

with those persons indicated in paragraph 1 above. The team described

the areas inspected and discussed in detail the inspection results listed

below.

,

Item Number

Status

Description / Reference Paragraph

j

395/88-26-01

OPEN

VIOLATION - Inadequate procedure or failure

to

follow procedures,

paragraphs

3.c.

1

and 3.1.1.

l

395/88-26-02

OPEN

VIOLATION - Inadequate 50.59 evaluation of

fire protection valves, paragraph 2.j.

395/88-26-03

OPEN

VIOLATION - Inadequate review of procedures

and drawings, paragraphs 2.d., 2.e. & 2.g.

395/88-26-04

OPEN

IFI - Revise R&R Log so Action LCOs stand

-

out, paragraph 2.f.

395/88-26-05

OPEN

IFI - The PMTS report of overdue preventive

maintenance items needs to be reviewed

following the outage, paragraph 3.J.

_ - ___ _ __ - ___

m-

34

395/88-26-06

OPEN

IFI - Correct E0P discrepancies, parag'raph

11.b.

395/88-26-07

OPEN

IFI - Correct E0P procedural problems,

paragraph 11.c.

395/88-03-03

CLOSED

IFI - Incorporation of comments into

natural

circulation

cooldown

procedure,

paragraph 12.

.

-

i

.

1

,

J

.-

r

1

- -

_ . - _ _ _ _ _ - - - _ - _ _ _ - - _ _ _ - _ - _ - _ _ _ _ - _ _ _ _ _ _ _ - _ _ _ _ _ _ _ - _ _ _ _ _ _ - -

_

_

-

- - _

,

c.

Attachment 1

.

DIAGR/N DESCRIPTION CF FAILU:E MODE

',

__

1

switch contact

l

ground indicating

for solenoid

(

C.__

light bulbs

4

i

resistors

"

'

125 v

.

1

e

ground fault

l

tfi tal

dc

-

battery

F

  • installed

y'

ground

1

ASCO

y

jE

'

'

    • """

solenoid

j

L

CR

,

i

!

)

L

Local

-

i

l

CR - Control P,oom

'

41 ASCO solenoid is shown, with a ground fault on the positive side of the

I

solenoid. TFe circuit for this solenoid contains one actuation switch

I

contact, on the positive side of the solenoid.

l

The installed ground detection system is also shown. This system consists of

two 1000 chn light bulbs plus plus 2000 ohm resistors, connecting each of the

positive and negative legs of tFe dc tx.is to ground. Net resistance to grcund

is 1500 chTrs on each of tFe positive and negative legs. Ground indication is

provided in the control room and at the battery charger.

A complete circuit through the solenoid, the ground fault, and the ground

detector is show) by dark lines.

l

l

l

l

lY

_ _ _ _ _ _ _ _ _ _ _ _ _

_

y

ATTACHMENT 2

FIRE PROTECTION VALVES CLOSED

DATE VALVE

VALVE NO.

PROTECTION AREA

CLOSED

XIG-4107

  • Control Building Emergency Plenum "B"

08-18-87

X1G-4109

  • Control Building Emergency Plenum "A"

08-18-87

XVG-4111

  • Control Building Exhaust Plenum

02-02-87

XVG-6751

Auxiliary Building Filter "A"

Plenum

02-02-87

l

XVG-6753

Auxiliary' Building Filter "B"; Plenum

02-02-87

XVG-6759

Reactor Building Purge Exhaust

02-02-87

l

XVG-6794

Reactor Building Sprinkler System

12-05-86

'

XVM-6786

  • Fuel Building Plenum "C"

08-18-87

XVM-6788

  • Fuel Building Plenum "B"

08-18-87

XVM-6790

  • Fuel Building Plenum "A"

08-18-87

  • SYSTEMS COVERE0 BY TECHNICAL SPECIFICATIONS

l

i

l

l

l

l

l

i

i

i

_

/

_ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _

- _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _

_ _ _ _ _ -

_ _ .

-

J

)

ATTACHMENT 3

~

EVENT REPORTS

l

ON0/LER

TITLE

ONO 870083

Diesel Generator Building Preaction Check Valve

Failure

i

ONO 870093 &

Negative Rate Reactor Trip During Control Rod Drive

!

1

l

LER 870024

Cabinet Maintenance

ONO 870099 &

Reactor Trip on Power Loss To Panel 7008

LER 870027

l.

ONO 870102 &

Improper Light Bulb Application Cause Reactor LER

'

LER 870028

Trip

ONO 870108

Diesel Generator "A" Air Start Filter

Installation Error

ONO 870111

Diesel Generator Building Preaction Sprinkler

System Valve Failed to Operate

ONO 880004 &

Inverter Power Failure Led to Security Equipment

LER 880001

Malfunction

1

ONO 880017

Improper Installation of Jumper To Open Valves

]

on ORPI

ONO 880045

Ruptured Lube Oil Pressure Switch in the "A"

Main Feedwater Pump

ONO 880063

Isolation of RHR Train "A" During Performance

of Safeguard Test

i

..

l

l

.

- - - - - - _ - - _ - - _

i

'

.

I

ATTACHMENT 4

l

i

MAINTENANCE WORK ORDERS IN PROCESS

]

WORK REQUEST NO.

TITLE

88E0165

Repair

Valve

XVG03107A

for

Service

Water System.

88E0220

Perform Low Voltage Field Flash Test for

Diesel Generator XEG0001B.

8801688

Repair Valve XVB00002A to Radiation

Monitor RMA-004.

88E0253

Replace Diaphram Hose to Valve XVT08871 -

0-SI to Accumulators.

88D0082

Remove Diaphram from Reactor Make-up Water

Storage Tank XTK-39-MU.

8801131

Replace

Charcoal

Filter

in

Auxiliary

Building Ventilation system XAA0040A.

COMPLETED MAINTENANCE WORK REQUESTS

WORK REQUEST NO.

TITLE

8810504

Trouble Shoot and Repair or Replace as Required

Leak Detection Transmitter IL TO 1969

88T0158

Block Open and Unblock PCV 00445B To

Support ILRT

8810446

Replace NCH Card C01-542

l

8810348

Repair NLL Card in "C" Steam Generator

Pressure Cabinet

88 WOO 49

Investigate and Repair Steam Dump System

Valve IV02026-MB

88D0064

Open Check Valve XVC03135B-SW and Remove

<

Internals for. Engineering Inspection.

Replace after inspection.

88E0169

Remove Jumpers From TB 1 TB Prior to

Placing Inverter XIT 5908 In Service

i

(

8801632

Replace Blown Fuses FV2B in Panel XPN 5253

J

,

'

-

-__

_ _ _ _ _

_

\\

_ _ _ _

Attachment 4

2

DESIGN CHANGES REVIEWED

NUMBER

NAME

20726

AMSAC

20390

REACTOR COOLANT PUMP

21262

VANTAGE V FUEL TECH SPEC CHG.

31092

H2 RECOMBINERS

10131

INSTALL REACH RODS ECCS CK VLV

-20285

RCP FLEX HOSE FOR CC PIPING

l

1

i

,

O

i

mi_________

___

_

l

,

f

ATTACHMENT 5

INSTRUMENT CALIBRATION

CALIBRATION

INSTRUMENT NO.

FUNCTION

DATE

.ITE-00604A

RHR Pump A Discharge Temperature

6-24-88

IPI-00601B

RHR Pump B Suction Pressure

6-14-88-

IPI-07377

RB Spray Pump B Discharge Pressure

9-26-88

IPI-04523

SW Booster Pump A Discharge Pressure

9-16-88

ILI-05420

D/G Fuel Oil Day Tank B Level

11-11-88

'

ITM-07052

CCW From CC Heat Exchange A Temperature

_10-06-88

-

IPI-00152A

Charging Pump B Suction Pressure

11-25-88

IPI-00152B

Charging Pump B Discharge Pressure

06-01-88-

IPI-04402

SW Pump A Discharge Pressure-

06-28-88

ILI-04418

SW Pond Level

01-30-88

ILI-01963

RW Sump Level

11-05-88

ILI-00991

RWST Level

-09-06-88

ILI-07433

Spent Fuel Pool Level

07-06-88

ILI-00926

Accumulator B Level

11-02-88

IPI-00927

Accumulator B Pressure

10-31-88

IPI-00163

Boric Acid Tank B Level

08-12-88

ILI-00461

Pressurizer Level

11-18-88

ITI-00432D

RCS Loop C Probe

10-16-88

ITI-09964

SW Building Room Temperature

07-22-88

IPI-15423B

D/G Starting Air Pressure

11-11-88

!

!

l

1

-

b

a

-

L_._______________

_

ATTACHMENT 6

E0P PROCEDURES REVIEWED

NUMBER

TITLE

E0P-2.0

Loss of Reactor or Secondary Coolant

E0P-2.1

POST-LOCA Cooldown and Depressurization

E0P-2.4

Loss of Residual Heat Removal System

E0P-2.5

LOCA Outside Containment

E0P-3.0

Faulted Steam Generator Isolation.

E0P-4.0

Steam Generator Tube Rupture

'

E0P-4.1

POST-SGTR Cooldown

E0P-4.2

SGTR with Loss of Reactor Coolant:Subcooled Recovery

E0P-6.0

Loss of all AC Power Recovery with Safety Injection

Required

E0P-6.2

Loss of all AC Power Recovery with Safety Injection

Not Required

,

l

E0P-7.0

Refueling Emergency

E0P-8.0

Control Room Evacuation

j

l

E0P-11.0

Emergency Boration

'

E0P-13.0

Response to Abnormal Nuclear Power Generation

l

E0P-15.0

Loss of Secondary Heat Sink (Feedwater)

i

E0P-15.3

Loss of Normal Steam Release Capabilities

l

E0P-18.2

Response to Voids in Reactor Vessel

!

l

l

!

l

"

l

!

ATTACHMENT 7

{

TECHNICAL REVIEW COMMENTS

The following are inspector comments as a result of reviews of the V.C. Summer

E0Ps.

1.

VCSNS E0P-2.0, Loss of Reactor or Secondary Coolant, Rev. 3; WOG E-1 Loss

of Reactor or Secondary Coolant

a.

Step 1.a does not check the alternate SI header flow as an

ALTERNATIVE ACTION.

With single failure criteria the normal SI

header may not have flow; the operator should then determine if

the alternate SI header is available or has flow established.

The team also noted this item in E0P-4.0 step 1.

b.

No criteria is provided for checking Reactor. Building Spray flow

in step AA.7.a.2 and 3.

Specific flow requirements are not provided

to the operator. The team found_ that the green' band labeled on the

Reactor Building Spray flow indicator is not based upon design basis

criteria.

The design basis flow is 2500 gpm while the indicated

green band range begins at 2000 gpm, therefore, less Qan design

basis flow could be present while the operator could have indication

that flow is adequate via the green band.

,

To preclude entering into a Critical Safety Function due to insuffi-

cient Reactor Building Spray flow, either the green band shouh. be

adjusted or a specific flow rate provided for the operator to verify

in this step.

c.

An inappropriate procedure is referenced.

In the event of a loss

of offsite power to one of the ESF buses, step 13 has the operator

attempt to restore power to the bus by using SOP-304, "7.2KV Switch-

gear." The team found that this procedure does not adequately guide

the operator in the restoration of offsite power to the ESF buses.

The step should have the operators use A0P-304.1 to restore offsite

power to a deenergized ESF bus.

Similarly, this item was noted by

the team in E0P-4.0, step 14.

2.

VCSNS E0P-2.1, POST-LOCA Cooldown and Depressurization, Rev. 2; WOG

ES-1.2, POST-LOCA Cooldown and Depressurization

a.

NOTE 15 provides the operator guidance that "The Charging Pumps

should be stopped on alternate Emergency Core Cooling System trains

when possible." This note is out of date with current plant opera-

tions and should be deleted,

b.

Step 32 provides guidance to the operator concerning ' actions to be

I

taken with the RHR System during certain RCS pressure and temperature

conditions.

The directions are not specific, in that there are

l

plausible conditions (e.g. Temperature = 300 Deg F and Pressure = 450

j

psig) when the guidance will not work.

The procedure needs to be

'

corrected to alleviate this problem.

~

-

l

L-______-_-_______.

..

Attachment 7

2

3.

VCSNS E0P-2.4, Loss of Residual Heat Removal System, Rev. 3; WOG ECA 1.1,

Loss of Emergene/ Coolant Recirculation

a.

Step A.3.b is constructed in a format inconsistent with the guidance

of the Owners' Group guidelines.

It is, in reality an ALTERNATIVE

ACTION (Response Not Obtained) action for Step 3.a, and should be

adjusted accordingly.

b.

At Step B.6, there is not a NOTE for supervisory personnel to remain

in the vicinity of the Reactor Building air locks to ensure that the

l

integrity check can be properly performed. This NOTE is included in

Part C of the procedure.

1

c.

There is no procedural reference provided the operator for installing

the Spent Fuel Pool Gate in Step B.11.

This activity is not fre-

quently performed and the proper procedure (FHP-611-5) should be

referenced for the operator.

d.

Insufficient guidance is provided the cperator in Step B.12.d

(ALTERNATIVE ACTION).

The "suppor ting equipment" for the " charging

train" is neither obvious, nor should it be memorized.

4.

VCSNS E0P-3.0, Faulted Steam Generator Isolation, Rev. 2; WOG E-2, Faulted

l

Steam Generator Isolation

a.

Inconsistent guidance is provided to the operator for filling the

Condensate Storage Tank with Demineralized Water in step 6.

This

evolution is performed at numerous points in the E0Ps and the guid-

,

ance is not always consistent. The licensee intends to standardize

the wording in upcoming revisions to the E0Ps.

b.

The Inspectors noted a typographical error in step 6.b for valve

XVG-668-CO.

Currently, the procedure has this valve listed as

XVG-643-CO.

5.

VCSNS E0P-4.0, Steam Generator Tube Rupture, Rev. 3; WOG E-3,

Steam

Generator Tube Rupture

a.

Contradicting information is given to the operator within one

Caution.

The operator is directed to depressurize the RCS using

normal spray at step 21. The team noted, however, that the operator

is also cautioned during the performance of step 21, that pressurizer

level may increase beyond indicator scale range (Caution 21 (2)).

Caution 21 (1) states that a steam bubble should be maintained in the

pressurizer. These two cautions provide contradicting information to

the operator. If a steam bubble is to be maintained then pressurizer

level should not increase beyond indicator scale range.

_ _ - _ _ _ _ _ _ _ _ _ - _ _ _ _ - -

.

.

Attachment 7

3

6.

VCSNS E0P-4.2, SGTR With Loss of Reactor Coolant: Subcooled Recovery,

Rev. 2; WOG ECA-3.1, SGTR With Loss of Reactor Coolant: Subcooled Recovery

a.

Incomplete guidance is provided to the operator for steam generator

sampling.

During performance of this procedure the ruptured steam

generator is isolated.

Step 8.b has the operator monitor blowdown

sample recorder for pH and conductivity.

This action cannot be

performed with the steam generator isolateo.

The operator is not

provided guidance on the proper restoration of sample flow.

7.

VCSNS E0P-6.0, Loss of All AC Power, Rev. 2; WOG ECA-0.0, Loss of All AC

Power, Rev. lA

a.

The procedure text does not reference the use of Attachment 2, "KW

l

Rating for Engineered Safeguard Features Equipment on Bus XSW1DA."

b.

The procedure does not instruct the. operator to attempt restoration

of offsite power. Step 5 directs the operator to restore ac power to

at least one ESF bus; however, the stated actions only refer to

restoration by using a Diesel Generator. The preferred source would

be offsite power using A0P-304.1, " Loss of One ESF Bus With the

Diesel Not Available." The licensee committed to changing this with

the next routine revision of E0P-6.

c.

Procedure steps used to reset ESF loading logic cannot be accom-

plished.

The operator is instructed to reset ESF loading logic in

step 27. The loading logic cannot be reset without first resetting

all Safety Injection signals.

If one ESF bus -is restored during

performance of steps 1-5, the operator is directed to step 26. At

this point the Safety Injection signal has not been reset; therefore,

step 27 can not be performed. Additionally, if the operators transi-

tion to E0P-6.2, " Loss of All AC Power Recovery With SI Required",

step 6 of that procedure cannot be accomplished either (establishing

i

'

RCP seal injection) since resetting Safety Injection i s 1al so a

prerequisite for establishing seal injection.

d.

The setpoint listed in step 35(a) for subcooling (2 degrees (22

degrees for adverse containment conditions)) is not supported by any

technical justification. The WOG recommended setpoint .is 0 degrees

subcooling.

8.

VCSNS E0P-6.2, Loss of All AC Power Recovery With SI Required, Rev. 2;

WOG ECA-0.2, Loss of All AC Power Recovery With SI Required

a.

The procedure text- does not reference the use of Attachment 1, "KW

Rating for Engineered Safeguard Features Equipment on Bus XSW1DB." ,

b.

Incorrect nomenclature is listed in step 5 (ALTERNATIVE ACTION)

a.1. for the MD EFP Reset Switch.

i

lL-.- ---

-

-

_. . - _ _ _ _

_

-

- _ _

Attachment 7

4

9.

VCSNS E0P-7.0, Refueling Emergency, Rev.2'

a.

Step A.6.f has the operator " Verify Fuel Handling Building sump

levels not increasing."

Accomplishment of this step is almost

impossible.

There are neither dip sticks, wall markings, level

.

indicators, or anything else that could assist the operator .in

trending the levels of the Fuel Handling Building sumps.

Some type

of indicating device is needed to allow accomplishment. of this

activity.

b.

Step 8.5 instructs the operator to take local actions to " Ensure

Reactor' Make-up System Valves closed." No notation is provided to

guide the operator to the location of these infrequently operated

,

valves.

10.

VCSNS E0P-13.0, Response to Abnormal Nuclear Power Generation, Rev. 2;

WOG FR-5.1, Response to Nuclear Power Generation /ATWS

a.

The SYMPTOMS for the procedure are not in compliance with the

guidance contained in the PGP.

Specifically, the only symptoms-

listed are entry form E0P-1.0 and E0P-12.0. The symptoms need to be

modified to be in compliance with the formatting defined in the

VCSNS PGP.

b.

Step 3.b (ALTERNATIVE ACTION) instructs the operator to take local

action to ". . manually open Steam Supply Valve to TD EFW Pump." No

notation is provided to guide the operator to the location of this

valve.

c.

Step 11.0 has the operator " Isolate each faulted SG."

This activity

is neither commonly performed

nor self-evident.

In E0P-3.0,

,

step-by step guidance is provided to the operator to accomplish this

task. Such guidance is needed in this procedure to ensure that the

actions are accomplished properly and expeditiously.

d.

Step 12.a.2 (ALTERNATIVE ACTION) instructs the operator to " Perform

actions of other procedures in effect which do not cooldown or other-

wise add positive reactivity to the core."

With the new fuel load

configuration in the Summer core, a positive moderator coefficient

.

is experienced during power operations.

This positive coefficient

l

is greater than any previously experienced positive coefficient and

will remain in effect for a significantly longer period of time

than any such previous occurrence. Analysis is needed to ascertain

whether this guidance is applicable with these new core conditions.

In effect, the operator is being given instructions to add rositive

reactivity to the core in an identified ATWS situation.

__-____--__ _ -

Attachment 7

5

11.

VCSNS E0P-15.0, Loss of Heat Sink; WOG FRP-H.1, Loss of Heat Sink

a.

The guidance in Step 2.e, " Verify EFW flow greater than 390 gpm to

at least one SG", is unclear to the operators.

Discussions with

four licensed operators of the plant staff resulted in two operators

stating that 390 gpm was needed to any one SG, while the other two

operators stated that a total EFW flow of 390 gpm was the requirement

and that it had to have a flow path to at least one SG.

This

inconsistency among the . operating staff concerning this procedural

step needs to be corrected.

b.

Guidance should be included prior to step 4.b, to state that pressure

must be below the P-11 setpoint in order to block the SI signals

listed,

c.

The alternative action in step 4.d.1 does not provide adequate

j

guidance on how rapidly the S/Gs should be depressurized,

d.

A caution warning operators of the potential loss of the condensate

pumps due to a high deaerating tank level should be inserted prior

to step 4.a.

This will make the operators aware of an impending

condition which could delay initiating feed water flow from the

condensate pumps in step 4.e.

e.

Step 9.b has the operator " Ensure PZR POWER RELIEF ISOL Valves

open." Power is normally available to at least one of these -valves.

However, since the plant is experiencing problems with " leakers",

power is not maintained to all of these valves.

Explicit guidance

concerning this anomoly, with the location of the breakers to be

reset is needed. The operators do not have these breaker locations

memorized and the only reference to their location is on the operator

aid on the control board, under the respective valve control

switches.

f.

The guidance in step 16(a) is unclear. Clarification should be made

so that the operators know that they are to continue in the loss of

heat sink procedure, vice transition to another procedure if auxil-

iary feed water flow is restored at this point in the procedure via

completion of step 2.

12.

VCSNS E0P-18.2, Response to Voids in Reactor Vessel, Rev. 1;

WOG

FR-I.3, Response to Voids in Reactor Vessel

a.

The SYMPTOMS for the procedure are not in compliance with the

guidance contained in the PGP.

b.

Step 7 does not have the operator check for hydrogen concentration,

as is required by the WOG.

No justification was in the technical

deviation documentation as to why this step was omitted from the

VCSNS E0P.

e

EE_____________._______

_ _ . . .

..

_ _ _ _

__ _ _ _ _ _ _ _ _ .

_

_ _ _ _ _ _ _ - _

_ _ _ - _ - _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _

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Attachment 7

6

1

c.

Step 8 directs the operator to " Verify RCS pressure is at least 100

psi less than Technical Specification Cooldown limit and less than

1850 psig."

This guidance is confusing and did not result in

consistent interpretation by the operators.

The cooldown limit is

a "Deg F/ Hour" parameter, 'while RCS pressure is a "PSIG" parameter -

they are not compatable.

Both the intent of this step and the

specific way of performing it need to be addressed by the facility.

d.

Step 21.a directs the operator to " Unlock and close motor control

center breakers for the Reactor Head Vent Valves."

The operator

walking down the procedure had to call the control room to find out

where the breakers were. This was only obtainable from the operator

l

aid under the valve control switches on the Main Control Board.

'

'

Specific location.for these MCC breakers'needs to be included in the

procedure.

l

I

l

l

.

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ATTACHMENT 8

ACRONYMS

AC

- ALTERNATING CURRENT

A0

- AUXILIARY OPERATOR

ARP

- ALARM RESPONSE PROCEDURE

ASCO

- AUTOMATIC SWITCH COMPANY

CHAMPS - COMPUTERIZED HISTORY AND MAINTENANCE SCHEDULING

CS

- CHEMICAL AND VOLUME CONTROL SYSTEM

.DBD

- DESIGN BASIS DOCUMENT

DC

- DIRECT CURRENT

ECCS

- EMERGENCY CORE COOLING SYSTEMS

EHC

- ELECTRO HYDRAULIC CONTROL

E0P

- EMERGENCY OPERATING PROCEDURE

EQ

- ENVIRONMENTAL QUALIFICATION

ERG

- EMERGENCY RESPONSE GUIDELINES

FPER

- FIRE PROTECTION EVALUATION REPORT

FSAR-

- FINAL SAFETY ANALYSIS REPORT

GPM

- GALLONS PER MINUTE

HVAC

- HEATING VENTILATION &' AIR CONDITIONING

I&C

- INSTRUMENT & CONTROL

IEN

- NRC INFORMATION NOTICE

INPO

- INSTITUTE OF NUCLEAR POWER OPERATIONS

ISEG

- INDEPENDENT SAFETY ENGINEERING GROUP

LCO

- LIMITING CONDITION FOR OPERATION

LER

- LICENSEE EVENT REPORT

j

LOCA

- LOSS OF COOLANT ACCIDENT

)

MPPH

- MILLONS POUNDS PER HOUR

1

'

MRF

- MODIFICATION REQUEST FORM

MWR

- MAINTENANCE WORK REQUEST

.

NI

- NUCLEAR INSTRUMENTATION

NRC

- NUCLEAR REGULATORY COMMISSION

ONO

- 0FF NORMAL OCCURRENCE

PGP

- PROCEDURE GENERATION PACKAGE

PMTS

- PREVENTIVE MAINTENANCE TASK SHEET

PORV

- POWER OPERATED RELIEF VALVE

PSIG

- POUNDS PER SQUARE INCH GAGE

PSRC

- PLANT SAFETY REVIEW COMMITTEE

QA

- QUALITY ASSURANCE

QC

- QUALITY CONTROL

RCS

- REACTOR COOLANT SYSTEM

RO

- REACTOR OPERATOR

R&R

- REMOVAL & RESTORATION

SBLOCA - SMALL BREAK LOSS OF COOLANT ACCIDENT

SER

- SAFETY EVALUATION REPORT

S/G

- STEAM GENERATOR

SI

- SAFETY INJECTION

SOER

- SIGNIFICANT OPERATING EVENT REPORT

SDP

- STANDARD OPERTING PROCEDURE

SRO

- SENIOR REACTOR OPERATOR

.

SS

- SHIFT SUPERVISOR

STA

- SHIFT TECHNICAL ADVISOR

STP

- SURVEILLANCE TEST PROCEDURE

-

SW

- SERVICE WATER

TS

- TECHNICAL SPECIFICATIONS

'

,

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