ML20134G618

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Insp Rept 50-395/96-14 on 961201-28.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support
ML20134G618
Person / Time
Site: Summer 
Issue date: 01/27/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20134G593 List:
References
50-395-96-14, NUDOCS 9702100472
Download: ML20134G618 (18)


See also: IR 05000395/1996014

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U. S. NUCLEAR REGULATORY COMMISSION

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REGION II

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Docket No.:

50-395

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License No.:

NPF-12

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Report No.:

50-395/96 14

Licensee:

South Carolina Electric & Gas (SCE&G)

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Facility:

V. C. Summer Nuclear Station

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Location:

P. O. Box 88

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Jenkinsville SC 29065

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Dates:

December 1-28, 1996

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Inspectors:

B. Bonser, Senior Resident Inspector

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T. Farnholtz, Resident Inspector

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W. Holland, Reactor Inspector, RII (Section M8.1)

Approved by:

G. Belisle, Chief, Reactor Projects Branch 5

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Division of Reactor Projects

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ENCLOSURE 2

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9702100472 970127

PDR

ADOCK 05000395

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EXECUTIVE SUMARY

V. C. Summer Nuclear Station

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NRC Inspection Report 50 395/96 14

This integrated inspection included aspects of licensee operations,

maintenance, engineering, and plant support. The report covers a 4-week

period of resident inspection: in addition, it includes the results of an

announced inspection by a regional reactor inspector.

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Operations

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In general, the conduct of operations was professional and

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safety conscious (Section 01.1).

A review of the licensee's cold weather protection program revealed no

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discrepancies or concerns. Appropriate actions were taken prior to the

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onset of sub-freezing temperatures (Section 02.2).

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A violation was identified concerning the failure to properly store

ladders in accordance with the approved engineering analysis which

represented a failure to follow Station Administrative Procedure

(SAP) 142. Station Housekeeping Program. This violation was a repeat of

a similar violation issued in August 1996 (Section 02.3).

An Unresolved Item (URI) was identified concerning the status and the

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proposed disposition of three different components that had been in the

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Removal and Restoration (R&R) log book for several years (Section 02.4).

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The inspectors concluded that the Plant Safety Review Committee (PSRC)

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was satisfying the Technical Specification (TS) required function of

reviewing matters related to nuclear safety (Section 07.1).

Maintenance

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Maintenance activities were generally completed thoroughly and

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professionally (Section M1.1).

Personnel conducting observed surveillance tests were knowledgeable and

performed the testing as required (Section M2.1).

An URI uas identified concerning a missed surveillance test on the

Turbine Driven Emergency Feedwater (TDEFW) pump and the licensee's

review for other missed surveillance tests on the Emergency Feedwater

(EFW) pumps (Section M2.2).

The licensee's root cause analysis of the scaffolding erection problems

that occurred in the A diesel generator room was thorough and accurately

determined the root causes of the problems (Section M7.1).

Maintenance and surveillance activities relating to remote shutdown

equipment (control room evacuation panel) were being performed in a good

manner. This conclusion was based on both inspection and review of the

licensee's Quality Assurance surveillances of this area. A weak Fire

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Emergency Procedure was identified. Additionally, a weakness was

identified for lack of routine monitoring of the Refueling Water Storage

Tank level indication in the Auxiliary Building and the source range

nuclear instrumentation in the Intermediate Building (Section H8.1).

Enoineerina

A review of engineering action on Reactor Building Cooling Unit motor

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failure, a review of Engineering and Operations interfaces and the

Temporary Accept As Is program was conducted. No concerns or

discrepancies were identified (Section E1.1).

Plant Support

Radiological controls observed during the conduct of tours and

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observation of plant activities were acceptable (Section R1.1).

Security and safeguards activities observed during the conduct of tours

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and observation of plant activities were good (Section S1.1).

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Report Details

Summary of Plant Status

Unit 1 maintained full power throughout the inspection period.

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Operations

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Conduct of Operations

01.1 General Comments (71707)

Using Inspection Procedure 71707, the inspectors conducted frequent

reviews of ongoing plant operations.

In general, the conduct of

operations was professional and safety conscious.

Specific events and

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noteworthy observations are detailed in the sections below.

02

Operational Status of Facilities and Equipment

02.1 Enaineered Safety Feature System Walkdown (71707)

The inspectors performed a walkdown of the reactor building instrument

air system.

No discrepancies were identified.

02.2 Cold Weather Preparations

a.

Insoection Scope (71714)

The inspectors conducted an independent review of the licensee's

preparation for the onset of cold (sub freezing) weather. This

inspection was conducted in accordance with Inspection Procedure 71714.

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b.

Observations and Findinas

The inspectors reviewed the requirements of Operations Administrative

Procedure (0AP) 109.1, Guidelines for Extreme Temperature Conditions.

Revision 0.

This procedure describes the necessary actions to prevent

damage to components from extreme hot or cold temperatures. Prior to

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the onset of sub freezing weather, the licensee performed the

appropriate section of this procedure (Section 6.1).

This included

preparing the Service Water System. Industrial Cooling Water System,

Condensate System, auxiliary boiler, and the various onsite buildings

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for prolonged exposure to sub-freezing ambient temperatures. The

inspectors independently examined the level sensing lines for the

Condensate Storage Tank and the Refueling Water Storage Tank to ensure

that tne heat tracing and insulation were in good condition.

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addition, the inspectors verified that power was available to the heat

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tracing panels and that they were operating properly.

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The inspectors reviewed all open Maintenance Work Requests (MWRs) having

to do with freeze protection. There were a total of four open MWRs.

Three were either working or in planning. The fourth MWR (91I3015) was

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written on a heat trace panel for the waste evaporator which is no

longer in use. The licensee indicated that they were evaluating options

to retire this equipment and clear the open MWR.

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c.

Concbsions

A review of the licensee's cold weather protection program revealed no

discrepancies or concerns. Appropriate actions were taken prior to the

onset of sub-freezing temperatures.

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02.3 P1 ant Tour

a.

Insoection Scope (71707)

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The inspectors performed plant tours of accessible portions of the

plant. During the plant tours the inspectors visually inspected major

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components to identify any general conditions that might degrade system

operation.

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b.

Observations and Findinos

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On December 11, during a tour of the 436 foot level of the Auxiliary

Building, inside the Radiologically Controlled Area (RCA), the

inspectors observed a ladder storage area in an area designated room

36 17(SE). A posted sign adjacent to the ladders read as follows:

" ladder storage area, maximum number of ladders to be stored in this

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area: 3."

The inspectors observed four ladders lying on their sides.

Three of the ladders were secured by a chain to a nearby handrail while

the fourth ladder was not secured in any way. The inspectors informed

the Shift Engineer of this situation and the fourth ladder was removed.

The inspectors reviewed Designated Storage Area Change Request Number

129 and the associated engineering analysis for this storage area. lhe

analysis indicated that the primary concern for this storage area was to

ensure that the maximum floor load limit was not exceeded.

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case, the area was only analyzed for three ladders. The analysis also

specified that the ladders should be chained to eliminate fall down

concerns.

Station Administrative Procedure (SAP) 142. Station Housekeeping

Program, Revision 11. Section 6.11, provides the requirements for the

designation of storage areas in the plant. As required by the

procedure, an engineering analysis had been performed, attached to the

storage request, and had ap3ropriately identified limitations due to

floor loading concerns.

SA) 142 also requires that the storage area

request originator ensure that all provisions, recommendations, or

limitations identified in the engineering review are complied with.

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this case, the procedure was not followed because the maximum number of

ladders allowed to be stored in this area was exceeded and all the

ladders were not chained as required. This failure to follow SAP 142 is

a violation of TS 6.8.1.a and is identified as Violation 50 395/96014-

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This NRC identified violation is a repeat of a previously issued

violation which was documented in NRC Inspection Report 50 395/96008

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dated August 16, 1996 (Violation 50 395/96008 01, failure to follow

station housekeeping program procedure). The licensee responded to this

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Notice of Violation in a letter dated August 29, 1996. The corrective

actions taken to avoid further violations described in this letter

indicated that management reviewed the incident with the civil

maintenance supervisors to heighten their awareness of compliance with

engineering designated requirements. The violation on December 11,

1996, could have reasonably been prevented by corrective actions for the

violation issued on August 16, 1996, and the corrective actions for

similar examples of storage problems identified after August 16, 1996,

by the licensee's Quality Assurance group.

c.

Conclusions

A violation was identified concerning the failure to properly store

ladders in accordance with the approved engineering analysis which

represented a failure to follow SAP-142 Station Housekeeping Program.

This violation was a repeat of a similar violation issued in

August 1996.

02.4 Review of System Status and Removal and Restoration (R&R) Loo Book

a.

Inspection Scope (71707)

The inspectors conducted a review of the daily system status controls

audit and the R&R Log Book.

b.

Observations and Findinas

On December 24, the inspectors reviewed the daily system status controls

audit required by Station Administrative Procedure. SAP 205, Status

Control And Removal And Restoration, Revision 8.

The audit verifies

that the R&R log book, the computer status of all systems required to

function during accident conditions Bypassed Inoperable Status

Indication, and main control board orange tags are in agreement as to

system status. The audit also verifies that the R&R check sheets are

accurate. The inspectors found that the audit was complete and

accurately verified system status.

During this review the inspectors also identified three R&Rs in the R&R

log book that had existed for several years. These included Action R&R

  1. 910742 dated July 30, 1991, for the B Train Waste Gas Recombiner:

Tracking R&R #880794 dated November 13, 1988, for Pressurizer Group 1

Backup Heaters; and Tracking R&R #930013 dated January 7, 1993, for the

Waste Evaporator, Evaporator Level Control.

Procedure SAP 205 defines

Action R&Rs as normally R&R entries for which TS Limiting Conditions for

Operations (LCO) requirements are met only by reliance on the action

requirements and that action must be completed to restore the equipment

to full LC0 requirements within a specified time period or additional

actions must be initiated. A Tracking R&R is normally an R&R entry

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which is prepared at the Shift Supervisor's discretion to track systems

or components to ensure timely and proper restoration.

Station Administrative Procedure, SAP-205, requires an evaluation of

non outage R&Rs in effect for greater than 30 days. The procedure

states that the evaluation should document the reason why the equipment

has not been restored to operable status and what the final disposition

is to be. The inspectors reviewed the current evaluations attached to

these R&Rs and found they were not clear as to why these R&Rs had

existed for so long, what was necessary to restore this equipment, and

what the final disposition was expected to be. The inspectors were

concerned that the appropriate controls had not been applied to track

and disposition this equipment.

Pending further review of this issue with the licensee to determine

equipment status and the 3roposed disposition of each R&R. this issue

will be identified as an Jnresolved Item, URI 50 395/96014 02.

c.

Conclusions

An URI was identified concerning the status and the proposed disposition

of three different components that had been in the R&R log book for

several years.

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Quality Assurance in Operations

07.1 Licensee Self-Assessment Activities

a.

Insoection Scope (40500)

The inspectors observed the monthly Plant Safety Review Committee (PSRC)

meeting to verify that it met the TS requirements.

b.

Observations and Findinas

The inspectors attended the monthly PSRC meeting on December 17. The

meeting was called to order by the Operations Manager with the required

quorum present. An agenda was distributed to all PSRC members or

alternates aresent to define the subject matter to be discussed at the

meeting. T1e PSRC reviewed Condition Evaluation and Reporting reports,

procedure revisions, a Radiation Emergency Plan change, safety

evaluations, Final Safety Analysis Report (FSAR) changes, and Non

Conformance Notices (NCN). Personnel from specific areas were present

at the meeting to provide more information and explain particular

issues.

The discussions were open and members participated by asking

questions or voicing concerns. The inspectors concluded that the PSRC

meeting satisfied the TS required function of reviewing matters related

to nuclear safety.

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c.

Conclusions

The inspectors concluded that the PSRC was satisfying the TS required

-function of reviewing matters related to nuclear safety.

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Miscellaneous Operations Issues (92901)

08.1 (0 pen) Unresolved . Item 50-395/96007-05, conducting core alteration

without containment integrity. On April 18, 1996, with the plant.

shutdown for a refueling outage the licensee aerformed FHP 604,

Functional Testing of Fuel Handling Systems.. Revision 10, Change A, in

preparation for fuel movement. As part of this procedure the

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containment refueling bridge was indexed over the reactor vessel and the

gripper was lowered within the pressure vessel. A question was raised

as to whether this should be considered a Core Alteration. The Summer

TS define a Core Alteration as the movement or mani >ulation of any

component within the reactor pressure vessel with t1e vessel head

. removed and fuel in the vessel. The Summer TS definition contains the

language " movement or manipulation of any component" a literal

interpretation would include lowering the fuel handling bridge gr!pper

into the pressure vessel and therefore should be considered a Core

Alteration. The licensee may not have established containment integrity

when this evolution was performed. This URI will remain open pending_

completion of an NRC evaluation of this issue.

08.2 (0 pen) Unresolved Item 50 395/96007 03, paint coat in containment does-

not meet application specification. On May 7, 1996, the licensee

identified (NCN 5452), during an inspection of the floors outside the

RCS loops in containment, that qualified coatings had not been applied

as described in safety related Civil Maintenance Procedure CMP 500.001,

Application of Protective Coating To Concrete Surfaces Inside The

Reactor Building, Revision 4.

The licensee identified that Keeler &

Long paint H1 had not been applied as described in CMP 500.001. Only

one coat of the H1 paint was applied when two coats were specified. The

paint vendor reviewed the single coat of H1 paint concern for the

licensee and determined that although a single coat of H1 paint had not

been tested in this application on the containment floor a single coat

was tested on containment walls and passed the ANSI N101.2 criteria.

The vendor concluded that it was not critical to apply a second coat of

paint and recommended that the licensee plan to apply another coat of

paint during the next refueling outage. The inspector concluded that

there was a high probability that a single coat of paint would probably

pass the testing criteria and did not constitute a significant safety

concern.

As part of the NCN review the licensee performed a 10 CFR Part 50.59

screening. The licensee concluded that this NCN did not represent a

change to the procedures or facility as described in the FSAR. The FSAR

Section 6.2.1.6, Materials, states that safety related coating systems

are used in containment for concrete and carbon steel surfaces. These

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coating systems satisfy the quality assurance requirements of ANSI

N101.4Property "ANSI code" (as page type) with input value "ANSI</br></br>N101.4" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., 1972, " Quality Assurance for Protective Coatings Applied to

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Nuclear Facilities." The FSAR also states that selected coating

manufacturers have documented test results certifying compliance with

ANSI N5.12,1974, " Protective Coatings (Paints) for the Nuclear

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Industry", and ANSI N101.2, 1972, " Protective Coatings (Paints) for

Light Water Nuclear Reactor Containment Facilities." From the review of

the 10 CFR Part 50.59 screening document and the wording in the FSAR it

was not clear to the inspectors how the licensee reached their

conclusion that this issue did not represent a change to the facility.

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This URI will remain open pending a more thorough review of the 10 CFR Part 50.59 screening.

II.

Maintenance

M1

Conduct of Maintenance

M1.1 General Comments

a.

Inspection Scope (62707)

The inspectors observed all or portions of the following work

activities:

PMTS P0205663, calibration of suction pressure indicator gauge on

the A Motor Driven Emergency Feedwater (MDEFW) pump.

PMTS P0205576, perform semi annual lubrication check on the A

MDEFW pump.

PMTS P0201261, perform 2 year operational check of the A MDEFW

pump 7.2 KV breaker.

PMTS P0202876, perform 2 year molded case circuit breaker testing

on the 480 volt EFW pump area cooling fan breaker.

b.

Observations and Findinas

The inspectors found the work performed under these activities to be

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professional and thorough. All work observed was performed with the

work package present and in active use. Technicians were experienced

and knowledgeable of their assigned tasks. The inspectors frequently

observed supervisors and system engineers monitoring job 3rogress, and

cuality control personnel were present whenever required )y procedure.

khen applicable, appropriate radiation control measures were in place.

c.

Conclusions

The inspectors found the work performed under these activities to be

professional and thorough.

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H2

Maintenance and Material Condition of Facilities and Equipment

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M2.1 Surveillance ObservatioD

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a.

Insoection Scope (61726)

The inspectors observed all or portions of the following surveillance

tests:

STP 105.014, Train A Slave Relay Go Circuit Testing, Revision 14.

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STP 503.003, Functional Test of SW TO EF Cross Connect Circuits,

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Revision 5.

b.

Observations and Findinos

The inspectors found that the tests were conducted using correct

procedures and test equi > ment.

For STP 503.003 the inspectors observed

the pre job briefing wit 1 the electricians, the interfacing between the

groups required to conduct the test, and the control of the test

activity. The inspectors concluded that personnel conducting the

observed surveillance tests were knowledgeable and performed the testing

as required.

c.

Conclusions

The inspectors concluded that personnel conducting the observed

surveillance tests were knowledgeable and performed the testing as

required.

M2.2 Hissed TS Surveillance Test On The Turbine Driven Emeraency Feedwater

(TDEFW) Pump

a.

Inspection Scope (61726)

The inspectors reviewed the circumstances surrounding a missed TS

surveillance test on the TDEFW pump.

b.

Observations and Findinas

On December 2, the licensee identified that a TS required quarterly

slave relay test for the TDEFW pump, due no later than November 30, had

not been performed within the TS required time interval. The TS

Surveillance Requirement 4.3.2.1, Table 4.3 2, Functional Unit 6.b,

Emergency Feedwater, requires that a slave relay test for Automatic

Actuation Logic and Actuation Relays be performed quarterly. The test

of the A train slave relay (K634) had last been performed on August 7,

1996.

The surveillance requirement is documented in procedure, STP 220.002,

Turbine Driven Emergency Feedwater Pump Test, Revision 1.

The

inspectors reviewed this issue with the licensee and found that the

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licensee was reviewing the surveillance history for all threa EFW pumps

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to determine if other surveillances had been missed. Pending completion

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of the licensee's surveillance history review, this issue is identified

as an Unresolved Item and is identified as URI 50-395/96014 03.

c.

Conclusions

An URI was identified concerning a missed surveillance test on the TDEFW

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pump and the licensee's review for other missed surveillance tests on

the EFW pumps.

M7

Quality Assurance in Maintenance Activities

M7.1 Review of Scaffolding Problems Root Cause Analysis

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a.

Inspection Scope (62707. 40500)

As a result of scaffolding erection problems in the A diesel generator

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room, the licensee initiated a root cause analysis which included a

review of the scaffolding erection program. The inspectors reviewed

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this root cause analysis.

b.

Observations and Findinas

The inspectors concluded from their review of the root cause analysis

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that it was thorough and accurately determined the root causes of the

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scaffolding erection problems that occurred in the A diesel generator

room (see NRC Inspection Report 50-395/96013). The root causes included

a failure to identify to the crew erecting the scaffolding the

safety related equipment in the Diesel Generator (DG) room, a failure to

use self checking to ensure intended actions were correct before they

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were performed, a failure to identify in documentation that the Heating,

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Ventilation and Air Conditioning (HVAC) duct was safety related, and a

failure to ensure in verbal communications that all safety related

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equipment in and around the job location was properly understood.

c.

Conclusions

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The licensee's root cause analysis of the scaffolding erection problems

that occurred in the A diesel generator room was thorough and accurately

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determined the root causes of the problems.

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M8

Miscellaneous Maintenance Issues

M8.1 Remote Shutdown System

a.

Inspection Scope (62700. 71707)

The inspectors reviewed the licensee's maintenance and testing program

for the Control Room Evacuation Panel (CREP) and associated circuitry

for plant shutdown control in the event control room habitability is

lost at the Summer Nuclear Station.

Specific areas of review included

the FSAR, TS, the Fire Protection Evaluation Report (FPER), selected

work order packages, selected surveillance packages, selected

preventative maintenance activities, and procedures directly related to

operation of the CREP and associated equipment. The inspectors also

reviewed recent quality assurance surveillance observations relating to

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maintenance calibration activities.

b.

Observations and Findinas

During inspection preparation, the inspectors reviewed the FSAR, Section

9.5.1 and noted that it referenced the FPER as the design basis document

for the evaluation of the potential effects of a fire on any location in

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the plant. The FPER also was used to demonstrate that a fire would not

adversely affect safe shutdown. During the review of the FPER, the

inspectors noted that significant reliance was placed on manual operator

action for system alignments to support safe shutdown operations during

fire scenarios.

The inspectors reviewed the Fire Emergency Procedures

(FEP) associated with control room evacuation due to a fire.

Procedures

reviewed were:

Procedure No.

Title

FEP-1.0, Revision 9

FIRE EMERGENCY PROCEDURE SELECTION

FEP 4.0, Revision 2

CONTROL ROOM EVACUATION DUE TO FIRE

FEP 4.1, Revision 1

PLANT SHUTDOWN FROM HOT STANDBY TO

COLD SHUTDOWN DUE TO FIRE IN CONTROL

BUILDING

During review of FEP-4.1, the inspectors noted that step 3.4 required

operators to " Borate the Reactor Coolant System per Attachment II."

Attachment II of FEP 4.1 provided instructions to borate the reactor

coolant system (RCS) using the normal boration equipment (boric acid

tank, flowpath, valves, and piping). The inspectors reviewed section

3.4.2.2 of the FPER which listed equipment deleted as safe shutdown

equipment in fire scenarios.

Section 3.4.2.2 stated, in part, "Boration

was previously to have been accomplished using boric acid tanks, pumps,

and associated valves. Equipment formerly listed for boration has been

either be(sic) deleted (boric acid tanks and pumps) or secured to

prevent spurious operation....

Boration required for safe shutdown will

now be accomplished by taking makeup water from the refueling water

storage tank (RWST), which provides a source of makeup water with 2000

ppm concentration of boric acid to the suction side of the charging

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pumps." The licensee informed the inspectors that initial conditions

for FEP 4.1 had been established during performance of FEP 4.0.

Ste)

3.3 of FEP 4.0 required, in part, that operators establish a flowpati

from the RWST to the suction side of the charging aumps which the

licensee considered met the intent of the FPER. T1e inspectors agreed

that the above flowpath was established as stated: however, step 3.4 of

FEP 4.1 recuired operators to establish a boration flowpath using

equipment celeted as safe shutdown equipment by the FPER.

Based on the

above. FEP 4.1 could be )otentially confusing to the o)erators, in that

the operators could get aogged down trying to align a ) oration flow path

that may not function correctly. The inspectors considered the

procedure weak, in that, it relies on operator knowledge to understand

that step 3.4 of FEP 4.1 is an additional means of boration and is not

needed if the boration path (step 3.4) can not be established.

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The Summer Nuclear Station CREP included two cabinets located in the

intermediate building (XPN7200A and XPN7200B) and various local

component controls and instrumentation. The CREP was installed and

modified to current configuration arior to 1987. The inspectors

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reviewed the licensee's component listory records and selected three

modification packages for review. The documentation reviewed was:

Work Reauest No.

Component

Work Performed

208010013

XPN7200A

Equipment and wiring

modifications to

XPN7200A

208000017

XPN7200A

Install auxiliary panel

and pull cable

208010014

XPN7200B

Delete indicator

No discrepancies were noted.

The inspectors also reviewed four completed work request packages and

the most recent preventative maintenance packages for XPN7200A and

XPN7200B. The documentation reviewed was:

Work Reauest No.

Component

Work Performed

94T3276

XPN7200B

Investigate for possible

problem with circuit for

XVT08152

9304214

XPN7200A

Repair as necessary

(temperature indicator

pegged low)

93I3338

XPN7200A

Replace fuse for power

to ITY00430C

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Work Reauest No.

Comoonent

Work Performed

(cont'd)

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9303524

XPN7200B

Repair as necessary

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(wiring problem)

PM Task No.

ComDonent

Work Performed

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P0199833

XPN7200A

Inspect, clean, & check

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termination integrity

(annual)

P0199834

XPN7200B

Inspect, clean, & check

electrical termination

integrity (annual)

The inspectors verified that work activities were approved, controlled.

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and completed in accordance with procedural requirements. The

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documentation clearly discussed work request problems discovered and

maintenance corrective actions implemented. Also, adequate )ost

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maintenance testing was documented for maintenance accomplis 1ed.

The inspectors reviewed TS surveillance requirements (SR) 4.3.3.5 and

verified that instrumentation listed in Table 4.3 6 of the TS were

installed at the locations described.

In addition, field observations

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verified that required instrumentation on the CREPs was in operation and

the interiors of the panels were in good condition.

In addition,

walkdowns were accomplished to verify that remote switches were

installed at selected locations as required by the FPER. The inspectors

also reviewed surveillar.ce test documentation to verify that TS SR were

being accomplished as required. The documentation reviewed was:

Procedure No.

Title

1

STP 113.001, Revision 4

REMOTE SHUTDOWN INSTRUMENTS CHANNEL

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CHECK (performed in October and

November 1996)

STP-345.058, Revision 3

CONDENSATE STORAGE TANK LEVEL

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(ILT03631A) CALIBRATION (performed

'

February 12, 1996)

STP 345.064. Revision 4

RCS LOOP "C" COLD LEG TEMPERATURE

INSTRUMENT (ITE00430A) CALIBRATION

(performed February 20, 1996)

No discrepancies were noted.

The insaectors also reviewed the safety evaluation reports referenced in

the FPER and noted that two remote shutdown monitoring instrumentation

components not referenced in TS 3.3.3.5 were used to monitor important

safe shutdown aarameters during fire scenarios requiring control room

evacuation. Tlese components were source range nuclear instrument

.

12

indication and Auxiliary Building (AB) RWST level indication. The

inspectors reviewed the licensee's surveillance requirements for these

components and noted that calibrations were being accomplished on the

l

same frequency as instrumentation listed in TS SR 4.3.3.5.

However, no

channel checks were being documented as accomplished on the AB RWST

level indicator.

In addition, no documentation was available which

indicated that the source range nuclear instrumentation, located

adjacent to XPN7200B was being periodically monitored.

The apparent

lack of routine monitoring of RWST level indication in the AB and the

source range nuclear instrumentation in the Intermediate Building was

identified as a weakness.

The inspectors reviewed three Quality Assurance Technical Service's

I

surveillances of maintenance calibration or preventative maintenance

activities which had been accomplished during 1996. No deficiencies

were identified by Quality Assurance in these areas. The inspectors

considered the licensee's performance in the calibration area was good

based on both inspection results and QA surveillances.

c.

Conclusions

Maintenance and surveillance activities relating to remote shutdown

equipment (control room evacuation panel) were being performed in a good

manner. This conclusion was based on both inspection and review of the

licensee's Quality Assurance surveillances of this area. A weak fire

emergency procedure was identified. Additionally, a weakness was

identified for lack of routine monitoring of the RWST level indication

in the Auxiliary Building and the source range nuclear instrumentation

in the Intermediate Building.

III. Enaineerina

El

Conduct of Engineering

E1.1 General Comments (37551)

General engineering activities were reviewed to determine their

effectiveness in preventing, identifying, and resolving safety issues,

events, and problems. These included a review of engineering action on

Reactor Building Cooling Unit motor failure, a review of Engineering and

Operations interfaces and the Temporary Accept As Is program.

No

concerns or discrepancies were identified.

E7

Quality Assurance in Engineering Activities (37551)

E7.1 Review of Vodated Final Safety Analysis Report (UFSAR) Commitments

A recent discovery of a licensee operating their facility in a manner

contrary to the FSAR description highlighted the need for a special

focused review that compared plant practices, procedures and/or

parameters to the FSAR description. While performing the inspections

1

.

13

discussed in this report, the inspectors reviewed the applicable

portions of the FSAR that related to the areas inspected.

No

discrepancies were identified.

j

JV.

Plant Support

R1

Radiological Protection and Chemistry (RP&C) Controls

R1.1 General Comnents (71750)

The inspectors observed radiological controls during the conduct of

tours and observation of plant activities and found them to be

i

acceptable.

S1

Conduct of Security and Safeguards Activities

S1.1 General Comments (71750)

The inspectors observed security and safeguards activities during the

conduct of tours and observation of plant activities and found them to

be good.

V.

Manaoement Meetinas

X1

Exit Meeting Summary

The inspectors ) resented the inspection results to members of licensee

management at t1e conclusion of the inspection on January 7 and 15,

1997. On January 9,1997, a teleconference between licensee management

and Region II management concerning a proposed violation involving an

inadecuate fire emergency procedure. After additional reviews, the

procecura was determined to be adequate but a weakness in procedure

content was identified.

The inspectors asked the licensee whether any materials examined during

the inspection should be considered proprietary.

No proprietary

information was identified.

3

X2

Management Meeting Sunmary

4

On December 16 NRC management presented the Systematic Assessment of

Licensee Performance (SALP) results to the licensee at a meeting on

site. Following the SALP presentation the NRC held a meeting with state

and local government officials.

. . - . .

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. . . . . _ _ . .

_ . . - -

- - . - . .

.

_ - - - -

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. -

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>

14

PARTIAL LIST OF PERSONS CONTACTED

Licensee

'

F. Bacon, Manager, Chemistry Services

L. Blue, Manager, Health Physics

M. Browne, Manager, Planning and Scheduling

'

S. Byrne, General Manager, Nuclear Plant Operations

l

R. Clary, Manager, Quality Systems

H. Fowlkes, Manager, Operations

S. Furstenberg, Manager, Maintenance Services

D. Lavigne, General Manager, Nuclear Support Services

G. Moffatt, Manager, Design Engineering

K. Nettles, General Manager, Strategic Planning and Development

H. O'Quinn, Manager, Nuclear Protection Services

A. Rice, Manager, Nuclear Licensing and Operating Experience

l

G. Taylor, Vice President, Nuclear Operations

i

T. Taylor, General Manager, Engineering Services

R. Waselus, Manager, Systems and Component Engineering

R. White, Nuclear Coordinator, South Carolina Public Service Authority

G. Williams, Associate Manager, Operations

1

l

l

l

.

_ _ _

_

. . _ _ _

_

-

.

15

INSPECTION PROCEDURES USED

IP 37551: Onsite Engineering

IP 40500: Effectiveness of Licensee Controls in Identifying, Resolving, and

Preventing Problems

IP 61726: Surveillance Observations

IP 62700: Maintenance Implementation

IP 62707: Maintenance Observations

IP 71707: Plant Oprations

IP 71714: Cold Weather Preparations

IP 71750: Plant Support

IP 92901: Followup - Plant Operations

ITEMS OPENED, CLOSED AND DISCUSSED

Opened

50 395/96014 01

VIO failure to follow station housekeeping program

procedure (Section 02.3).

50 395/96014 02

URI status and proposed disposition of three different

components in the R&R log book for several years

(Section 02.4).

50 395/96014 03

URI missed surveillance test on TDEFW pump and review of

other missed surveillance tests on EFW pumps (Section

M2.2).

Closed

None.

Discussed

50-395/96007 05

URI conducting core alteration without containment

integrity (Section 08.1).

50 395/96007 03

URI paint coat in containment does not meet application

specification (Section 08.2).

.

.