IR 05000395/1986007

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Insp Rept 50-395/86-07 on 860301-31.Violation Noted: Inadequate Cable Tray thermo-lag Installation
ML20205M264
Person / Time
Site: Summer South Carolina Electric & Gas Company icon.png
Issue date: 04/07/1986
From: Dance H, Hopkins P, Prevatte R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20205M250 List:
References
50-395-86-07, 50-395-86-7, NUDOCS 8604150145
Download: ML20205M264 (6)


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Report No. : 50-395/86-07

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Licensee : South Carolina Electric and Gas Company Columbia, SC 29218 Docket No. : 50-395 License No. : NPF-12

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Facility Name : V. C. Summer Inspection Conduc d: March 1-31, 1986

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.7 un en_ b Richard Prevatte f // Date Signed i d(7/ L Perry- . Hoph ns s/,/frG Date igned Approved by: d*W Hdgh C. Dancb, Section Chief h7 [

Date Signed Division of Reactor Projects

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SUMMARY Scope: This routine, announced inspection involved 234 resident inspector-hours on site in the areas of Licensee action on previous enforcement matters, onsite followup of events and subsequent written reports, monthly surveillance observa-tions, offsite review committee, Engineered Safety Features system walkdown, monthly maintenance observation, operational safety verification, fire protec-tion / prevention and other area Results: One violation was identified: Inadequate Cable Tray Thermo-lag Installatio .

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y l REPORT DETAILS 1. Persons Contacted Licensee Employees D. Nauman, Vice President, Nuclear Operations 0. Bradham, Director, Nuclear Plant Operations J. Skolds, Deputy Director, Operations and Maintenance K. Woodward, Manager, Operations M. Browne, Group Manager, Technical and Support Services M. Quinton, Manager, Maintenance Services A. Koon, Manager, Technical Support G. Putt, Manager, Scheduling and Materials Manageme M. Williams, Manager, Nuclear Education and Training L. Blue, Manager, Support Services S. Hunt, Manager, Quality Assurance Surveillance Systems W. Higgins, Associate Manager, Regulatory Compliance J. Sefick, Manager, Nuclear Security B. Williams, Supervisor, Operations Other licensee employees contacted included engineers, technicians, operators, mechanics, security force members, and office personne . Exit Interview (30702,30703)

The inspection scope and findings were summarized on March 31, 1986, with those persons indicated in paragraph 1 above. The inspectors described the areas inspected and discussed the inspection findings. The licensee did not identify as proprietary any of the materials provided to or reviewed by the inspectors during the inspection. One violation was identified:

Violation 86-07-01: Inadequate procedures resulted in work and inspection deficiencies during the installation of a fire barrier for electrical cable tray 308 This is a violation of 10CFR50 Appendix B Criteria The licensee offered no objection to the violation and stated that all deficiencies were in the process of being correcte .

Licensee Action on Previous Enforcement Matters (92702)

(Closed) Violation (85-28-01), Failure to Adequately Evaluate Existing Plant Conditions Prior to Performance of Surveillance Resulted in Both ECCS Trains Being Inoperable. The licensee provided a written response to this violation in a letter to Region II dated August 20, 1985. The inspectors reviewed the licensee's response and corrective action taken to prevent recurrenc The licensee has implemented a new program that provides for testing and maintenance on safety trains A & B on alternating weeks. This corrective action and added training to personnel appear adequate to prevent recurrenc s ;

(Closed) Inspector Followup Item (83-27-07), Technical Specifications are in Error. This item was the result of an error in the number used for system flow rate for surveillance testing of the control room normal and emergency air handling system. This item was corrected in Amendment Number 24 to the Technical Specifications issued on April 25, 198 (Closed) Inspector Followup Item (84-27-05), Auxiliary Building Charcoal Filter Testing. This item identified that the charcoal filters were tested but were not included in the surveillance test program. A surveillance test procedure (STP) 554.004 was issued and implemented on September 13, 1985 to correct this ite The testing under this procedure was satisfactorily l completed on March 18, 198 No violations or deviat'ons were identifie . Onsite Followup of Events and Subsequent Written Reports (92700, 93702)

The inspectors reviewed the following Licensee Event Reports (LER's) to ascertain whether the licensee's review, corrective action and report of the identified event were in conformance with regulatory requirements, technical specifications, license conditions, and licensee procedures and control Based upon this review the following items are closed:

(Closed) LER 84-045, Residual Heat Removal Suction Isolation (Closed) LER 84-051, Reactor Protection System Actuation, The Licensee is presently Repairing XIT-5902 and Investigating The Cause of Transformer Failur (Closed) LER 85-015, Inoperability of Residual Heat Removal Syste No violations or deviations were identifie . Monthly Surveillance Observation (61726)

The inspectors obsyved surveillance activities of safety-related systems and components to ascertain that these activities were conducted in accor-dance with license requirements. The inspectors observed portions of selected surveillance tests including all aspects of one major surveillance test involving safety-related systems. The inspectors also verified that the required administrative approvals were obtained prior to initiating the test, that the testing was accomplished by qualified personnel, that test instrumentation was properly calibrated, that data met TS requirements, that test discrepancies were rectified, and that the systems were properly returned to service. The following specific surveillance activities were observed:

STP 120.001 Motor Driven Emergency Feedwater Pump STP 125.002 Diesel Generator Weekly Operability Test STP 345.040 ESFA Slave Relay Test l

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STP 133.001 Axial Flux Difference Calculation STP 108.001 Quaarant Power Tilt Ratio STP 212.001 Reactor Core Flux Mapping STP 506.009 Reactor Trip Breaker Shtnt and Undervoltage Trip Verification STP 120.002 Turbine Driven Emergency Feedwater Pump No violations or deviations were identifie . Offsite Review Committee (40701)

The inspectors conducted a review of the offsite nuclear safety review cmmittee (NSRC) to ascertain whether the offsite review functions were conducted in accordance with TS and other regulatory requirements. It was determined that review group membership and qualifications were as required; that meetings were convened when required; and the meeting frequency and quorum met applicable requirement The inspectors attended the NSRC nieeting at corporate headquarters on March 11, 198 No violations or deviations were identifie . ESF System Walkdown (71710)

The inspectors verified the operability of two engineered safety features (ESF), system by performing a walkdown of the accessible portions of the Residual Heat Removal and Reactor Building Spray Systems. The inspectors confirmed that the licensee's system lineup procedures matched plant drawings and the as-built configuration. The inspectors looked for equipment conditions and items that might degrade performance (hangers and supports were operable, housekeeping, etc.) and inspected the interiors of electrical and instrumentation cabinets for debris, loose material, jumpers, evidence of rodents, etc. The inspectors verified that valves, including instru-mentation isolation valves, were in proper position, power was available, and valves were locked as appropriate. The inspectors compared both local and remote position indication No violations or deviations were identifie . Monthly Maintenance Observation (62703)

The inspectors observed maintenance activities of safety-related systems and components to ascertain that these activities were conducted in accordance with approved procedures, Technical Specifications (TS) and appropriate industry codes and standards. The inspectors also determined that the procedures used were adequate to control the activity, and that these activities were accomplished by qualified personnel. The inspectors independently verified that equipment was properly tested before being returned to service. Additionally, the inspectors reviewed several out-standing job orders to determine that the licensee was giving priority to

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safety-related maintenance and a backlog which might affect its performance was not developing on a given system. The following specific maintenance activities were observed:

MWR8600439 Maintenance on turbine driven emergency feedwater pump GMP100.002 turbine throttle valve overspeed tri MWR8501571 Replace gasket on the service water syste MWR8501570 MWR8501572 GMP100.002 MWR8503042 Repaired level control valve LCU01328WG on the waste gas syste MMP445.006 Maintenance of diaphragm valve MWR80M0026 Repair of damage to emergency diesel generator valve train assembly valve XE0001B MMP180.033 Emergency diesel generator 18 months maintenanc GMP100.002 MWRS50-2041 Replaced seals on the liquid waste system valves XEV0029-PP MMP320 104 Certified pump general maintenance procedur No violations or deviations were identifie . Operational Safety Verification (71707)

The inspectors toured the control room, reviewed plant logs, records and held discussions with plant staff personnel to verify that the plant was being operated safely and in conformance with applicable requirement Specific items inspected in the control room included: adequacy of staffing and attentiveness of control room personnel; TS and procedural adherence; operability of equipment and indicated control room status; control room logs, tagout books, operating orders, jumper / bypass controls; computer printouts and annunciators. Tours of other plant areas were conducted to verify equipment operability; control of ignition sources and combustible materials; the condition of fire detection and extinguishing equipment; the control of maintenance and surveillance activities in progress; the imple-mentation of radiation protective controls and the physical security pla Tours were conducted during normal and random off-hour period No violations or deviations were identifie . Fire Protection / Prevention (64704)

The inspectors conducted an inspection in the above area to determine the status and actions taken by the licensee on open items that had been identified.in Region II inspections report 395/85-2 One of the areas inspected covered the installation of thermo-lag 330 fire barrier material on cable tray 3088. This work -was accomplished under Modification Request Form (MRF) 31971 and Maintenance Work Request (MWR)

3197 This work was completed, inspected and the MWR was closed on u

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March 7, 198 A review of the MRF and MWR package against the actual installation by the inspector revealed that the final installation did not meet all requirements that were recommended and analyzed for by the vendo After noting concerns in this area the inspector requested that the licensee provide the seismic analysis that had been accomplished for the added weight on the cable trays. While awaiting this information, the licensee dis-covered that the weight of material installed on the cable tray did not match the weights used in the analysis. The analysis used a weight of 3.25 lbs/ft2 and information obtained from the manufacturer of the thermo-lag barrier material was that weight of the material provided to the licensee could be as high as 4.75 lbs/ft This deficiency led to a detailed inspection of the installation by the inspector and the licensee. Addi-tional deficiencies identified included: incorrect spacing of steel bands used to secure thermo-lag panels to the cable tray, all metal in contact with tray not insulated for 18 inches away from tray, use of wire in lieu of banding material and cracks in trowelable material. The above deficiencies were the result of the use of vendor technical notes and instructions provided with the MWR to perform the work and inspection activities asso-ciated with installation instead of developing specific work and inspection procedures to cover those activitie The above deficiencies are contrary to the requirements of 10CFR50 Appendix "B" Criteria V and the Operational Quality Assurance Plan Section 4.0 (Status Procedures) and 11.0 (Inspection)

which require that activities affecting quality shall be accomplished in accordance with procedures which contain adequate instruction to accomplish the task and provide for quantitative and qualitative acceptance criteria to determine acceptability of the completed work. This is a violation, Inade-quate Cable Tray Thermo-lag Installation, (86-07-01).

The licensee had documented the above deficiencies on nonconformance notices (NCN) Nos. 2214 and 2151. An evaluation was completed on the seismic loading of the cable trays to allow continued operation. Work is in progress to clear the above deficiencies. Other than the above, no addi-tional violations or deviations were identifie . Other Areas:

The inspectors observed the practice Emergency Plan exercise conducted on March 26, 1986. This exercise was in preparation for an evaluated exercise that will be conducted on April 9, 198 The inspectors attended the Systematic Assessment of License Performance (SALP) presentation at Corporate Offices on March 18, 1986. R. Walker, Director, Reactor Projects, Region II and H. Dance, Reactor Projects Secticn Chief made a presentation on the current SALP to licensee management. The SALP report is found in Inspection Report No. 50-395/85-47.

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