ML20217G465

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Insp Rept 50-395/98-01 on 980111-0221.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support
ML20217G465
Person / Time
Site: Summer South Carolina Electric & Gas Company icon.png
Issue date: 03/20/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20217G436 List:
References
50-395-98-01, 50-395-98-1, NUDOCS 9804020359
Download: ML20217G465 (27)


See also: IR 05000395/1998001

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U. S. NUCLEAR REGULATORY COMMISSION

REGION II

. Docket No.: 50-395

License No.: NPF-12

Report No.: 50-395/98-01

Licensee': South Carolina Electric & Gas (SCE&G)

Facility: V. C. Sumer Nuclear Station

Location: P. O. Box 88

Jenkinsville. SC 29065

Dates: January 11 - February 21, 1998

Inspectors: B. Bonser. Senior Resident Inspector

T. Farnholtz. Resident Inspector

R. Gibbs. Reactor Inspector. RII-(Sections M8.1, and M8.2)

P. Kellogg. Reactor Inspector. RII (Section E8.1)

W. Miller Reactor Inspector. RII (Sections F2.1.-F2.2. F2.3

F5.1. F8.1, and F8.2)

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Approved by: R. C. Haag. Chief. Reactor Projects Branch 5

Division of Reactor Projects

Enclosure 2

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9804020359 980320

PDR

0 ADOCK 05000395

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EXECUTIVE SUMMARY

V. C. Summer Nuclear Station

NRC Inspection Report No. 50-395/98-01

This integrated inspection included aspects of licensee operations

maintenance, engineering, and plant support. The report covers a 6-week-

period of resident ins)ection: in addition, it includes the results of

announced inspections ]y three regional inspectors.

Doerations

able to perform its design functions for normal-and accident conditions

(Section 02.1).

  • During an emergency drill operators exhibited good control and

communications while implementing emergency operating procedures

(Section 05.1).

Maintenance

e Maintenance activities associated with the B diesel generator, the A

charging pump. the turbine driven emergency feedwater pump, and the

train A sequencer were performed in accordance with applicable

procedures. Good maintenance practices and coordination of work

activities were noted (Section M1.1).

system flow rate was adequate. The test was performed in accordance

with the approved procedure and the results were within the acceptance

criteria (Section M1.2).

  • Portions of the feedwater isolation logic circuit that had not been

)reviously tested were adequately incorporated into Solid State

)rotection System (SSPS) testing 3rocedures. An unresolved item was

identified pending a review of SS)S Technical Specification operability

and testing requirements (Section M1.3).

Enaineerina-

  • - An unresolved item was identified concerning inconsistencies between

relief valve testing requirements in the valve inservice test program

controlling procedure and the referenced implementing test procedures.

The licensee is reviewing the actual testing that was performed on

relief valves to determine if the applicable ASME Section XI testing

requirements were satisfied (Section E1.1).

.- Licensee's actions concerning a broken fuel injection pump tappet

assembly hold down stud on the B diesel generator were considered

adequate. The engineering evaluation was sufficiently detailed to

L support.the corrective actions (Section E1.2).

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  • ' A non-cited violation was identified concerning a failure to correctly

translate condensate storage tank design basis information into-

specifications, procedures, and instructions (Section E1.3).

Plant Sucoort

e A violation was identified involving a lack of adecuate )rogrammatic

controls for temporary shielding. Temporary shielcing tlat remained in

place for longer than six months was not evaluated in accordance with

engineering requirements (Section R1.2).

  • An emergency drill met its objectives and provided beneficial training

to the site emergency organization (Section P5.1).

.- The licensee's actions following an inadvertent attempted introduction

of a handgun into the protected area were appropriate. Security

personnel demonstrated good knowledge and performance during this event

(Section S4.1).

  • The low number of inoperable or degraded fire protection components, in

conjunction with the good material condition of the fire protection

.com)onents and fire brigade equipment, indicated that appro)riate

emplasis was placed on the maintenance and operability of tie fire

protection equipment and components (Section F2.1).

  • Ekcellent surveillance inspection and test procedures were provided for

fire barriers and the fire protection water distribution system (Section

F2.2),

e Evaluations to justify the differences between as-built fire barrier

penetration seals and corresponding test reports were not readily

available. Based on the inspector's reviews, no immediate concerns

exist. The licensee has initiated a project to resolve these

differences (Section F2.3).

  • The fire brigade organization and training were up-to-date and met the

requirements of the site procedure. The fire brigade demonstrated good

response and fire fighting performance during a simulated fire brigade

drill (Section FS.1).

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Reoort Details

Summary of Plant Status

The unit began this inspecticn period at approximately 100 percent power and

remained at that level for the entire inspection period.

I. Doerations

01 Conduct of Operations

01.1 General Comments (71707)

The inspectors conducted frequent reviews of ongoing plant operations.

In general, the conduct of operations was professional and

safety-conscious: specific events and noteworthy observations are

detailed in the sections below.

02 Operational Status of Facilities and Equipment

02.1 Enaineered Safety Feature System Walkdown (71707)

a. Insoection Scoce (71707)

The inspectors conducted a detailed system walkdown of the Emergency

Feedwater (EFW) System.

b. Observations and Findinas

The inspectors conducted a detailed system walkdown of the EFW system to

assess the general condition of system com)onents including labeling, to

verify that system valve positions match tie system drawings and station

operating procedures, and to assess plant housekeeping around system

components. The inspectors considered that the EFW system was able to

perform its design function for both normal and accident conditions. No

misaligned valves were identified and component labeling was adequate.

Several minor discrepancies and questions identified were resolved

promptly by the licensee. The inspectors also reviewed the applicable

sections of the Final Safety Analysis Report (FSAR) and identified no

discrepancies,

c. Conclusions

A detailed system walkdown found that the Emergency Feedwater System was

able to perform its design functions for normal-and accident conditions.

05.1 Doerator Trainina and Qualification

a. Insoection Scone-(71707)

The inspectors observed a training drill in the simulator in which

operators responded to and recovered from a loss of all Alternating

Current (AC) power.

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b. 0bservations and Findinas

On February 18. during an emergency drill, the~ inspectors observed-

operators in the control room simulator respond to and recover from a

loss of all AC power. The use of several Emergency 0perating Procedures

(EOP)_was observed. The inspectors observed good control and

communication by the control room staff in response to the simulated.

emergency.

^c. Conclusions

During an emergency drill operators exhibited good control and

communications while implementing emergency operating procedures.

II. Maintenance

M1 Conduct of Maintenance

M1.1 -General Comments

a. Insoection Scoce (62707)

The inspectors observed or reviewed all or portions of the following

work activities:

  • Preventive Maintenance Task Sheet (PMTS) 9720546. Diesel Generator

(DG) Area B Ventilation . Air Supply Fan B Motor.

  • PMTS 9720906, Operational Check of the B DG 7.2 kV Breaker.

. Work Request (WR) 9800106. Rework Welds on A Charging Pump.

  • PMTS 9721556. A Charging Pump Motor Preventative Maintenance.
  • PMTS 9720077. Lubrication Check on Turbine Driven Emergency

Feedwater (TDEFW) Pump.

  • PMTS 9714612. Lubrication Check on TDEFW Pump Turbine.

- .. WR 9719148. Add, Adjust, or Repack TDEFW Pump Turbine Steam Supply

Valve.

.- PMTS 9712339. Disassemble. Clean, and Reset TDEFW Pump Turbine

Lube.011. System-Relief Valve,

e WR 9719205, Repair or Replace TDEFW Pump Local Discharge Pressure

Indicator.

= WR 9801886, Troubleshoot. Train A Sequencer

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b. Observations and Findinas

The observed maintenance activities were performed as required by the

applicable. procedures. Proper tools and equipment were at the job site

and used in an appropriate manner. ~The maintenance technicians were

knowledgeable and demonstrated good maintenance practices. Good

coordination of work activities for different tasks on the same

equipment was noted.

c. Conclusions

Maintenance activities associated with the B diesel generator. the A

and the

charging pump, thewere

train A sequencer turbine driven emergency

performed feedwater

in accordance pump,ble

with applica

procedures. Good maintenance practices and coordination of work

activities ~were noted.

M1.2 Reactor Coolant System (RCS) Flow Rate Measurement

a. Insoection Scoce (61726)

The inspectors reviewed and observed the performance of Surveillance

Test Procedure (STP)-205.002, "RCS Flow Rate Measurement." Revision 7.

.The purpose of this test was to determine the total RCS flow rate to

ensure compliance with Technical Specification (TS) surveillance

requirement'4.2.3.5. This test is performed at least once per 18

months.

b. Observations and Findinas

The inspectors reviewed the methodology and data gathering performed

during the RCS flow rate measurement test to determine the adequacy of

this effort. The plant was maintained in a steady state condition and

precision data was obtained for feedwater venturi differential pressure,

feedwater temperature, steam pressure. RCS temperature. RCS pressure.

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and other required parameters. This data was then used to calculate

feedwater flow rate, steam enthalay. Steam Generator (SG) heat rate. RCS

inlet and outlet enthalpy, and otler necessary values for each of the

three loops. Finally, the RCS flow rate in each loop was calculated and

a total RCS flow rate of 303.590 gallons per minute (gpm) was obtained.

The acceptance criteria, specified in Section 9.0 of STP-205.002, was a

minimum of 283.600 gpm and a maximum of 321.300 gpm. The calculated

flow rate was well within the acceptance criteria. The inspectors

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reviewed the data sheets and the calculations and identified no concerns

with the performance _of this surveillance test.

c. Conclusions

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The surveillance test performed to obtain the total reactor coolant

system flow rate was adequate. The test was performed in accordance

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with the approved procedure and the results were within the acceptance

criteria.

M1.3 Solid State Protection System (SSPS) Actuation Test

a. Insoection Scooe (61726)

The inspectors observed the >erformance of STP-345.037 " Solid State

Protection System Actuation _ogic and Master Relay Test. Train A."

Revision 14. This procedure was revised on January 23, 1998.-to include

information supplied by Westinghouse in a Technical Bulletin (ESBU-TB-

97-09) dated December 30. 1997.

b. Observations and Findinas

The licensee performed STP-345.037 to functionally verify that the Train

A SSPS and the automatic actuation logic and relays were operable, and

to verify the response time of A reactor trip breaker. The inspectors

observed this test to assess the effectiveness of additional steps

placed in the procedure to test a portion of an SSPS circuit that had

not been previously tested. Westinghouse notified the licensee that the

feedwater isolation memory circuit and the P-10 (Low Setpoint Power

Range Neutron Flux Interlock) source range block memory circuit may not

have been fully tested during previous semi-automatic testing of the

system. The concerns described in the technical bulletin were not plant

specific since there are significant differences in SSPS logic between

Westinghouse plants. This required a detailed review of the V. C.

Summer Nuclear Station (VCSNS) SSPS drawings. The P-10 circuit problem

did not apply to VCSNS because the source range nuclear instruments

remain energized throughout power operation of the reactor.

The feedwater isolation circuit at VCSNS did require additional testing

to fully verify its proper operation. The feedwater isolation circuit

consists of three inputs: Safety Injection (SI). SG Hi-Hi water level,

and reactor trip (P-4). Of.these inputs. the SI and SG Hi-Hi water

level inputs are further divided on the logic card so as to provide two

identical signals for each input. This results in five input circuits

on the logic card, each being passed through an isolation diode. This

. logic card provides a feedwater isolation signal when two input signals

are present. Previous testing techniques tested only the following

combinations of inputs:

  • SI with SG Hi-Hi water level

Using this testing arrangement, a failed isolation diode in either the

SI or SG Hi-Hi water level. inputs would not be identified. The test

procedure was revised to reset the reactor trip input and to test the SI

input by itself and the SG Hi-Hi water level. input by itself in addition

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to the three combinations described above. Each of these inputs would

sup)ly two input signals and should result in a feedwater isolation if

bot 1 circuits were functioning properly. This revised testing technique

effectively tested all five isolation diodes and circuits using existing

test equipment.

The inspectors reviewed the revised test procedure and observed the

performance of the test using the revised procedure on January 30, 1998.

The technicians performing the test were knowledgeable and successfully

completed each ste) as required. No concerns were identified with the

revision or with t1e performance of the test.

This testing issue was originally identified by another utility on

November 11, 1997, and reported to the industry on November 14. 1997.

The Engineered Safety Feature ActLation System (ESFAS) automatic

actuation logic and relays are required to be operable in accordance

with TS 3.3.2 and are required to be demonstrated operable in accordance

with TS 4.3.2.1. The NRC is reviewing this issue to determine if

previous testing satisfied the TS requirements, if the licensee complied

with TS once initially notified of this potential testing inadequacy,

and if 10 CFR 50.73 reporting requirements were followed. The

licensee's position on this issue was that 3revious TS surveillance

testing had satisfied TS requirements and tie SSPS testing changes they

implemented were enhancements to the testing methodology. Pending

completion of this review, this issue is identified as an Unresolved

Item (URI) 50-395/98001-01.

c. Conclusions

Portions of the feedwater isolation logic circuit that had not been

areviously tested were adequately incorporated into Solid State

protection System testing procedures. An unresolved item was identified

pending a review of SSPS Technical Specifications operability and

testing requirements.

M8 Miscellaneous Maintenance Issues (62706)

M8.1 (Closed) IFI 50-395/97002-01: Maintenance Rule scoping of Systems.

Structures and Components (SSCs) used in E0Ps. During the Maintenance

Rule baseline inspection, the inspectors identified several SSCs in the

E0Ps that were not included in the scope of the licensee's Maintenance

Rule arogram. At the time of the Maintenance Rule baseline inspection.

the NRC had recently issued new guidance. Regulatory Guide 1.160.

Revision 2. concerning incorporation of equipment used in E0Ps into

Maintenance Rule programs. Thus at that time, the licensee was in the

process of reviewing this new guidance and incorporating it into their

)rogram. The licensee has now re-scoped the SSCs in their Maintenance

tule program by completing a line-by-line review of the E0PS. Results

of this re-scoping were inspected by reviewing a list of SSCs that were

added to the Maintenance Rule program and reviewing a listing of

. specific SSCs which were not added as a result of the licensee's

. classification of these as "non-significant" during re-scoping. No

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deficiencies were noted while reviewing the re-scoping effort. The

inspectors also verified that the specific SSCs discussed in the

baseline ins)ection report had been included in the scope of the

Maintenance Rule program. Additionally, the inspectors verified that

the historical review had been com)leted for these SSCs, that

performance criteria had been estaalished, and that monitoring of the

SSCs was being accomplished. Based on this inspection, the licensee's

corrective actions for re-scoping of E0P SSCs in the Maintenance Rule

program were determined to be adequate.

M8.2 (Closed) VIO 50-395/97002-03: failure to take appropriate corrective

action for an (a)(1) Structure, System, or Component (SSC). During the

Maintenance Rule baseline inspection, the inspectors identified that the

licensee had not taken appropriate corrective action for repetitive

failures of several leak detection switches which had been classified as

(a)(1) under the Maintenance Rule. The licensee's response to the

violation attributed the problem to noncompliance with Station

Administrative Procedure (SAP)-1141. "Nonconformance Control Program,"

and action taken for Nonconformance Control Notice (NCN)-5304. This

procedure required that NCNs be implemented or routed to System and

Component Engineering for re-evaluation within 90 days of issuance.

Corrective action for this deficiency was taken by CER 97-0476 which was

issued during the baseline inspection. Corrective actions included

review and correction of all open NCNs having similar conditions,

revision of SAP-1141 to assign s

compliance with the 90-day rule,pecific responsibility for trackingand replacem

an improved model.

In order to evaluate the corrective actions for this violation, the

inspectors reviewed the actions taken from the licensee's responses,

dated July 17 and December 19. 1997 Additionally the NCN and CER were

reviewed for proper corrective action and closure. The inspectors noted

that the CER provided objective evidence of the licensee's review for

other similar existing conditions. The inspectors verified that the

revision to SAP-1141 assigned tracking responsibility for the 90-day

rule as committed to in the violation response. The inspectors also

reviewed the design change for re)lacement of the level switches. The

inspectors compared the old switc1 design to the new design, and

concluded that the new switches should prove to be more reliable. The

design change addressed a population of 40 switches. Thirty-two of the

switches had already been replaced. Three switches were scheduled to be

deleted due to no emergency core cooling Jiping running through those I

s ) aces. Five switches were scheduled to 3e replaced by June 30, 1998. 1

T1e inspectors reviewed the failure history of these five switches and

determined that they had ex)erienced only one failure since 1993. The

inspectors reviewed the'worc orders that replaced the switches addressed

in the violation, verified they had been replaced with the new switches. 4

and reviewed the plans to replace the remaining switches. Based on this

. inspection, the licensee's corrective actions for the level switches

were determined to be adequate,

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III. Enaineerina

El Conduct of Engineering-

El.1 Relief Valve Inservice Testina (IST) Proaram

a. Insoection Scooe'(37551)

The inspectors reviewed the licensee's Inservice Test (IST) program for

valves as described in General Test Procedure (GTP)-302. " Inservice

Testing of Valves., Second Ten Year Interval." Revision 9. The licensee

-identified an apparent difference between the relief valve testing

program and the applicable American Society of Mechanical Engineers

(ASME)Section XI Code requirements. This finding was documented on

Condition Evaluation Report (CER) 98-0075 dated January 22. 1998,

b. Observations and Findinas

- On January 1.1994, the licensee began the second ten year interval for

inservice testing. At that time, the licensee committed to the

requirements contained in the 1989 Edition of the ASME Section XI Code,

no addenda. This edition refers to Operations and Maintenance (0M)-1.

" Requirements for Inservice Performance Testing of Nuclear Power Plant i

Pressure Relief Devices," for the testing of applicable safety and

relief valves. When the second ten year interval began, the licensee

revised GTP-302 to reflect the new requirements contained in the later

edition of the ASME Section XI Code.

The IST requirements for relief valve testing were detailed in GTP-302.

These requirements were consistent with the re

the applicable ASME Section XI Code and OM-1. quirements

In addition. GTP-302 contained in

contained a table listing all valves which were required to be tested in

accordance with this procedure. A total of 86 valves were classified as

safety / relief valves. For each valve included in the IST program an

STP was referenced as the procedure to be used to implement the testing

requirements.

The licensee identified an apparent inconsistency between the

requirements for relief valve testing contained in GTP-302 and the

testing performed in accordance with the applicable STP. As an example,

GTP-302. Section 5.4.4 " Pressure Relief Device Testing." Paragraph D.

" Periodic Testing," Subparagra)h 4.b. states. in part. that the

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following_ requirements are to 3e met during-testing of Class 2 and 3

pressure relief devices: visual examination. seat tightness testing,

set pressure determination and determination of compliance with seat

tightness criteria. However, the implementing test procedure listed for

many of the relief valves was STP-401.003. " Code Relief Valves ASME XI

Test." Revision 4 which did not address visual inspection, seat

tightness testing, or determination of compliance with seat tightness

criteria. In' addition. Section 1.0 of STP 401.003, states that this

procedure is specific for the letdown flow control header relief valve

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(XVR08117-CS): but as stated earlier. this STP is referenced for many of

the relief valves in the IST program.

Another concern documented in CER 98-0075 was that the procedures used

to conduct relief valve testing were not the procedures referenced in

GTP-302. Many relief valves were tested using Mechanical Maintenance

Procedure (MMP)-445.005. " Maintenance. Repair and Testing of Relief

Valves." Revision 13. This procedure contains steps to disassemble.

. rework reassemble, and test relief valves. However, this was not the

procedure that was specified to be used to perform the ASME required IST

testing. Work that was accomplished under MMP-445.005 may satisfy the

ASME test requirements that were not performed by the specific

referenced procedures, however, at the end of the inspection period the

licensee had not completed their review and were not able to make this

determination.

In response to the concerns documented on CER 98-0075. the licensee

initiated a root cause analysis to determine why the ASME Section XI

Code requirements for the second ten year interval were not effectively

translated into implementing procedures. In addition the licensee

initiated a complete valve IST program review to determine if all ASME

. requirements are included in the IST program and that the valves listed

as subject to IST testing is complete and accurate. Pending completion

of these efforts, this issue is identified as URI 50-395/98001-02.

c. Conclusions

An unresolved item was identified concerning inconsistencies between

relief valve testing requirements in the valve inservice test program

controlling procedure and the referenced implementing test procedures.

The licensee is reviewing the actual testing that was performed on

relief valves to determine if the applicable ASME Section XI testing

requirements were satisfied.

El.2 Diesel Fuel In.iection Pumo Stud Insoection

a. Insoection Scooe (37551)

The inspectors reviewed the licensee's engineering efforts concerning a

broken B Diesel Generator (DG) fuel injection pump tappet assembly hold

down stud. The broken stud was identified during a routine preventive

maintenance task.

b. Observations'and Findinas

On January 12. 1998. the licensee performed Preventive Maintenance Task

Sheet (PMTS) 9720700 to inspect the fuel injection pump tappet assembly

hold down studs on the B DG. This task is performed every six months on

each DG and consists of inspecting a total of 24 studs per DG (two per

fuel injection Jump). During this inspection, a broken stud was

identified on tie number 2 fuel injection pump. The broken portion of

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the stud along with'the attached nut was recovered.

A review of historical records revealed that a broken stud was

identified on the number 1 fuel injection pump on the B DG in January

1986. A second stud broke while adjusting the number 3 fuel injection

pump on the same DG at that same time. As a result of these two events.

the licensee instituted a PMTS to periodically inspect these studs. No

other broken studs were identified until the recent observation in

January 1998. The purpose of the studs was to secure the fuel injection

pump linkage adjustment to prevent movement.

When the broken stud was identified the licensee wrote NCN 98-0043 to

document the event and the corrective actions. The broken stud and nut

were replaced along with the associated intact stud and nut on the

number 2 fuel injection pump. This NCN disposition was discussed with

the DG vendor who concurred with the proposed course of action. The

engineering evaluation was sufficiently detailed to support the

corrective actions. The DG was successfully run following this work.

The inspectors considered the actions taken to be adequate and no

operability concerns were identified,

c. Conclusions

A review of the licensee's actions concerning a broken fuel injection

pump tappet assembly hold down stud on the B DG was considered adequate.

The engineering evaluation was sufficiently detailed to support the

corrective actions.

E1.3 Condensate Storaae Tank Volume

a. Insoection Scooe (37551)

The inspectors reviewed a discrepancy between the TS required Condensate

Storage Tank (CST) volume and the actual volume requirements,

b. Observations and Findinas

On February 12. the licensee identified a discrepancy between the actual

CST inventory requirements and the required TS volume of 172.700 gallons

stated in TS 3.7.1.3 " Condensate Storage Tank." The existing TS value

was based on a sum of the Emergency Feedwater (EFW) required volume of

150.000 gallons arid the unusable volume of the tank calculated to be

approximately 22.700 gallons.

The required CST volume is based on sufficient water to cool the plant

to the point where the residual heat removal system can complete the

cooldown. The TS required inventory of 172.700 gallons, however, was

incorrect. Prior to the plant uprate in May 1996 the licensee

identified that the actual EFW required volume in the CST was 155,000

gallons. For the plant uprate, that raised maximum plant authorized

core power level from 2775 Megawatts thermal (Mwt) to 2900 Mwt. a new

CST volume of 158.570 gallons was identified to be. required for EFW.

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This raised the total CST inventory that should have been specified in

the TS for EFW requirements to approximately 181.270 gallons. The

licensee failed to recognize the impact of the plant uprate and

corresponding increase in CST inventory on the fS and therefore did not

amend the TS or revise the appropriate plant procedures for the correct

required inventory in the CST.

During this review the inspectors identified that a note was incorrect

on the CST figure (Figure VI-12. dated 2/6/87) maintained in the curve

book in the control room. The note stated that volume below the EFW

pump suction is 12.302 gallons. This unusable volume has been

calculated by the licensee to be approximately 22.700 gallons. The

inspectors informed the licensee of this observation.

When this issue was identified the licensee prepared a Station Order

alerting plant operators to the actual required volume in the CST and

set an administrative low limit of 14 feet which corresponds to greater

than 181.270 gallons as measured by the CST level instrumentation. This

low limit ensures that the maximum CST volume for EFW would be

available. The licensee also recognized that the CST low level alarm

setpoint was incorrect and was preparing further action to revise this

setpoint. The licensee also performed a data review and determined that

level in the CST had not been below 19.5 feet since June 1. 1996. The

licensee stated that a TS amendment request would be submitted to

reflect the correct CST volume requirement. The licensee does not

believe the failure to properly translate CST volume requirements into

applicable plant documents is indicative of a problem with their

engineering processes or programs.

This failure to implement adequate design controls for the CST is a

violation. The licensee failed to correctly translate design basis

information into specifications procedures, and instructions. This

non-repetitive, licensee identified and corrected violation is being

treated as a Non-Cited Violation (NCV) consistent with Section VII.B.1

of the NRC Enforcement Policy. This is identified as NCV 50-395/98001-

03.

c. Conclusions

A non-cited violation was identified concerning failures to correctly

translate condensate storage tank design basis information into

specifications, procedures, and instructions.

E8 Miscellaneous Engineering Issues (92903)

E8.1 (Ocen) Insoection Follow uo Item 50-395/97013-01: failure of the A DG

during a surveillance test. The A DG failed the monthly surveillance

test on November 11, 1997, due to load instability. The licensee began

troubleshooting the DG to determine if the )roblem was related to the

governor electronic control unit (EGA) or t1e hydraulic actuator (EGB).

Following some indeterminate testing, the licensee replaced both the EGA

and EGB. The licensee made several maintenance starts of the A DG and

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made adjustments to the governor. The A DG was declared operable on

November 14 following a successful retest. The A DG failed the weekly

surveillance test on November 21 due to load instabilities that

prevented the diesel from being fully loaded. Trcubleshooting

identified high resistance across contacts of the Isochronous/ Droop

relay. Additionally, two contacts of the relay did not change state

when the relay was energized. The relay was replaced and the A DG was

declared operable on November 22. following a successful retest.

The A DG failed the weekly surveillance on December 2 due to load

instability. The load swings observed on this occasion were comparable

to those observed on November 11. During troubleshooting, the output of

the EGA was noted to be spiking. The EGA was replaced with a unit from

the warehouse. The licensee performed a maintenance run during which

the governor worked satisfactorily during the initial no load, loading,

and unloading conditions. However, when the output breaker was opened a

frequency swing was observed. Additional adjustments were performed to

attempt to obtain stable operations from the EGA and EGB. Stable

operation could not be achieved. Management decided to replace the

installed EGA with the previously removed EGA which had been refurbished

by the vendor. The A DG was declared operable on December 5. following

successful testing.

On December 30. a weekly surveillance of the A DG was conducted. The

diesel started and loaded properly. However, when the output breaker

was opened, significant frequency (speed) oscillations were observed.

The A DG was declared inoperable and a troubleshooting )lan was

initiated to address the aroblem. Troubleshooting of t1e EGA did not

identify any spiking of tie output. Following several EGB oil changes

oscillations were not observed. The A DG was started for additional

testing on January 1. 1998. After the output breaker was opened large

frequency swings were observed. The vendor service representative

believed that the cause of the problem was binding in the fuel racks or

the yield link. The yield link was replaced and the fuel rack linkages

at each injector pump and the cross connect members were inspected. No

binding was identified. Following a one hour run the diesel again

started to oscillate when its output breaker was opened. After this

occurrence, management decided to replace the EGB. Testing of the

diesel following the EGB replacement was performed and the governor was

adjusted. Three confidence runs were )erformed to assure the

oscillation problems were resolved. T1e data collected during these

runs indicated the A DG was ready for surveillance testing. All testing

was completed satisfactorily on January 5 and the A DG was declared

operable.

The ins)ectors reviewed the history of the EGAs and EGB: installed on A

DG and 1 eld discussions with the licensee's staff. The following issues

had been identified and were being addressed by the licensee.

Refurbishment by the vendor of the EGA units consisted of the

replacement of several Mylar and electrolytic ca)acitors. Three

potentiometers on the EGA were also replaced. W111e the aging of

capacitors was well known, problems with aging of the potentiometers was

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not. The vendor had indicated that while the capacitors were replaced

due to an aging concern, there had been only one failure of an EGA unit

due to capacitor failure. The more frequent failure cause was that of

the potentiometers. One of the EGAs which had been refurbished failed

the licensee's bench test. The licensee returned the unit to the vendor

who then conducted a test similar to the licensee *s. The EGA failed

again. This test failure identified that the vendor did not test as

long as the licensee and that the failure.. spiking of te out

time to develop. The licensee also identified potential she'put.

f life took

concerns with the EGA and EGB units.

The inspectors concluded that the licensee had conducted a thorough

review of the EGA and EGB failures. Several issues were still being

evaluated by the licensee, these included aging of components, failure

of an EGB unit, vendor testing methodolcgy, and governor upgrades. This

item remains open pending the completion of the licensee's review of

these. issues.

IV. Plant Suooort

R1 Radiological Protection and Chemistry (RP&C) Controls

RI.1 General Comments

The inspectors observed radiological controls during the conduct of

tours and observation of maintenance activities and found them to be

-acceptable.

R1.2 Temocrary Shieldina Procram

a. Insoection Scooe (71750)

The inspectors reviewed the licensee's temporary shielding program. The i

licensee identified temporary shielding packages installed in the plant

for extended periods without the appropriate engineering evaluations.

b. Observations and Findinas

On February 5 the licensee identified in CER 98-129 that Health Physics

-(HP) procedural guidance on temporary shielding did not contain adequate

controls to ensure shielding was removed or received an engineering

review when it was installed longer than six months. Seven Temporary

Shielding Requests (TSRs) were identified that had been installed in the

plant longer than six months and had not received appropriate

' engineering evaluations.

The temporary shielding program is administered by HP through Health

Physics Procedure, (HPP)-819, " Temporary Shielding Evaluation.

Installation, and Removal," Revision 9. As part of the approval process

for temporary shielding. engineering performs a technical evaluation to

identify any special restrictions that may apply. Engineering

evaluations for TSRs are performed in accordance with Engineering

e

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13

Services Procedure '(ES)-409, " Engineering Evaluation of Scaffolding.

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Temporary Shielding and Designated Storage Area Change Requests."

Revision 3. The evaluations are performed on the basis that the

temporary shielding.will not be installed longer than the job duration

listed on the TSR cover sheet requesting the engineering evaluation.

Procedure ES-409 states, "If.the scaffolding or shielding is to remain

in place for longer than the lesser of the duration of the project or

six months it should be addressed as a ' Change to the facility'

requiring a 10 CFR 50.59 evaluation to be completed conforming to the

requirements of our license and design basis." Procedure ES-409 states

that this can be accomplished through a permanent )lant modification.or

dispositioning a shielding evaluation with a 10 CFR 50.59 evaluation.

Two shielding packages installed on September 30, 1994 and October 1,

1994 were originally planned to be in place for one month during an

outage. Both TSRs were installed on safety related or quality related

pi)ing. The other five TSRs were installed in 1996 and early 1997 on

otler equipment in the plant including high dose radioactive waste

storage areas, temporary demineralizers, a waste processing high

integrity container, and the boron concentration measurement system.

The duration of the shielding requests varied from one month to six

months and two listed an " unknown" duration. Engineering evaluations

were performed for each of the TSRs. The engineering evaluations for

the two TSRs of unknown duration had no indication from engineering that

further review would be necessary after six months.

The inspectors concluded that this was a programmatic failure of the

temporary shielding program in that HPP-819 had not adequately

controlled or limited the time temporary shielding was installed or

referenced the engineering requirements that would address the shielding

as a change to the facility after it had remained in place for more than

six months. The inspectors also concluded that the interface between HP

and engineering was weak in that the engineering reviews for the TSRs

had not documented a time limitation on the TSRs although two of the

shielding requests reviewed by engineering had indicated they would be

installed for an unlimited duration. Procedure HPP-819 also requires a

tracking log. The status of temporary shielding was logged, however,

the log was not effective in maintaining the status of installed

shielding, and did not ensure shielding was removed once the job

duration on the TSR was exceeded. The inspectors also observed that

there were no periodic audit requirements of the installed temporary

shielding.

At the close of the inspection period, engineering was reviewing the

seven TSRs that had been installed greater than six months. A

preliminary review identified no concerns. The failure to establish

adequate controls for temporary shielding installed in the plant is

identified as a Violation (VIO) 50-395/98001-04.

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14

c. Conclusions

A violation was identified involving a lack of adequate )rogrammatic

controls for temporary shielding.

place for longer than six monthsaswnotTemporary

evaluatedshielding tlat remained

in accordance with in

engineering requirements.

P5 ' Staff Training and Qualification in EP

P5,1 Observation of Emeroency Drill

, 'a. Insoection Scooe (71750)

The ins)ectors observed a training drill conducted in the simulator and

the Tec1nical Support Center (TSC).

b. . Observations and Findinas

The inspectors observed a training emergency drill on February 18 from

the simulator control room and the TSC. The inspectors concluded that

the drill met its objectives and provided beneficial training to the

site emergency organization. The inspectors had one significant

observation. The Shift Supervisor (SS), acting as the interim Emergency

Director (ED), and the ED did not ap) ear to be familiar with the

guidelines for turning over responsi)ilities from the interim ED to the

ED. This turnover normally occurs when the TSC is activated and

staffed. The ED position was turned over before it should have

occurred. This led to confusion as to whom was responsible for

declaration of an emergency classification. The licensee also

recognized this drill discrepancy and is reviewing additional training.

c. Conclusions

An emergency drill met its objectives and provided beneficial training

to the site emergency organization.

S1 Conduct of Security and Safeguards Activities

S1.1 General Comments (71750)

The inspectors observed security activities including compensatory

measures during the conduct of plant tours and plant activities and

.found them to be acceptable.

S4 ' Security and Safeguards Staff Knowledge and Performance

S4,l'. Attemoted Introduction of a Handoun into the Protected Area (PA)

P

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a. Insoection Scoce (71750)

-

The inspectors reviewed the licensee's response to an event'where an

individual attem)ted to introduce a handgun into the PA. This event was-

documented on CER 98-0078 and Security Incident Report (SIR) 980030.

b. Observations and Findinas

On January 24, a licensee employee attempting to enter the PA through

the access portal search area was found in possession of a handgun.

Requirements when entering the PA include placing all hand carried

articles on an X-Ray machine conveyor belt to allow a security officer

to ins)ect their contents. At 7:03 p.m. the security officer operating

the X-Ray equipment observed the image of a handgun on the monitor. The

officer took control of the bag containing the gun and conducted a

search of its contents. A handgun with ammunition was confiscated at

that time. The individual attempting to enter the PA was detained and

denied access. Central security was notified and the individual's badge

was deactivated to prevent access until an investigation could be

conducted.

An interview was conducted with the individual, the on-duty Shift

Supervisor, and security personnel. The individual stated that he had

inadvertently left the handgun in the bag and that he intended to leave

the gun in his personal vehicle. The gun was placed in the arms room

pending completion of the investigation. At 8:03 3.m. on January 24.

the licensee made a one hour notification to the NRC to describe this

event.

The licensee conducted an investigation to determine the facts

surrounding this event. The individual's work performance was reviewed

and a check with local law enforcement agencies was made to verify that

no recent law enforcement problems had occurred. No evidence of any

problems was discovered that would indicate anything other than an

inadvertent action as stated by the individual. The individuals access

was reinstated following the conclusion.of the investigation. On

January 26 at 11:46 a.m.. the licensee retracted the NRC notification

and classified the event as a security logable event. The inspectors

reviewed this event and did not identify any concerns. The licensee's

actions to identify the handgun, deny access to the individual. and

conduct a thorough investigation was appropriate. Security personnel

demonstrated good knowledge of the requirements for such an event and

performed in accordance with established procedures.

c. Conclusions

'The licensee's actions following an inadvertent attempted introduction

of.a handgun into the protected area were appropriate. Security

personnel demonstrated good knowledge and performance during this event.

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F2 Status of Fire Protection Facilities and Equipment

- F2.1 Doerability of Fire Protection Facilities and Eouioment (64704)

a. Insoection Scooe

The-inspectors reviewed the fire protection impairment log for fire

protection components and the o)en ~ maintenance work requests on fire

protection features to assess t1e licensee's performance for maintaining

fire protection components in service. In addition, walkdown

inspections were made to assess the material condition of fire

protection systems, equipment. features and fire brigade equipment.

b. Observations and Findinos

(1) Ooerability of Fire Protection Eauioment and Comoonents

As of February 13, there were no fire protection components listed

in the impairment log as degraded. There were 19 open maintenance

work requests of which 11 involved components designed to provide

protection for safety-related components. These work requests

were less than one year old, did not result in any component being

inoperable and were to correct minor problems, such as leaking

valves.

The inspectors reviewed the system engineer's monthly assessment

of the fire protection systems. Prior to March 1997, the system

engineer's assessments of the fire protection systems were graded

" Yellow" or considered to be in need of increased management and

maintenance attention due to the number and type of identified

problems. In March 1997, the system engineer's assessment of the

fire protection systems was changed from " Yellow" to " Green"

(good) due to performance improvements. This change was due to

completion of the modifications to the fire detection system,

resolution of corrective maintenance problems affecting several

fire protection components and the lack of any new identified

inoperable or significant maintenance issues on the fire

protection systems. The system engineer's assessment of the fire

protection system's performance has remained good since March

1997.

During tours of the plant, the inspectors noted that the material

condition of the fire protection features was good and the systems

,

were well maintained.

(2) Fire Briaade Eauioment

The turnout gear for the fire brigade members was stored in

lockers on elevation 412 of the control building and on elevation

436 of the turbine building. A sufficient number of turnout gear,

'"

consisting of helmets, coats, pants, boots, gloves, etc.. was

<

provided to equip fire brigade members expected to respond in the

m

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_ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . . . . _ _

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cvent of a fire or other emergency. . The equipment was properly

stored and well maintained.  ;

c. Conclusions

The low number of inoperable or degraded fire protection components, in

conjunction with the good material condition of the fire protection ,

com)onents and fire brigade equipment, indicated that appro)riate  ;

emplasis was placed on the maintenance and operability of t1e fire i

protection equipment and components.

F2.2 Surveillance of Fire Protection Features and Eouioment .

I

a. Insoection Scooe (64704)

The inspectors reviewed STP-728.049, " Intermediate Building Elevations

426'-422' Fire Barrier Inspection." Revision 3, and the following i

'

completed surveillance and test procedures for compliance to the

requirements of the NRC approved commitments in the " Summer Fire ,

Protection Evaluation Report":

-

STP-128.021. " Fire w rvice Three Year Flow Test." Revision 10.

Completed September 26, 1997,

1

- STP-728.038, " Auxiliary Building Elevation 426*-451' Fire Barrier

Inspections." Revision 2. Completed November 6. 1996. l

l

- STP-728.043. " Control Building Elevation 448' Fire Barrier l

Inspection.~ Revision 2. Completed August 27, 1996. I

- STP-728.048. " Intermediate Building Elevation 436' Fire Barrier I

Inspection." Revision 3. Completed November 18, 1997. l

b. Observations and Findinas l

Twenty procedures were developed for the surveillance inspection of fire

barriers. The inspection ~ procedures, acceptance criteria, and data

documentation requirements for these procedures were essentially the

same. The ins for the fire barriers on

elevation 422'pectors

-426' of reviewed STP-728.049

the intermediate building. The procedure I

included a sketch of the walls to be inspected, penetration location,

and data sheets identifying each element to be inspected. The

inspectors considered these surveillance inspection procedures to be of

excellent quality.

The completed fire barrier surveillance procedures reviewed by the

inspectors had been com)leted appropriately and met the acceptance

criteria. Work orders lad been properly submitted for identified

. discrepancies.and the discrepancies had been reinspected following

' completion of the required repairs. The licensee was performing an

-inspection every 18 months of all fire barriers and fire barrier

penetrations. The " Summer Fire Protection Evaluation Report" only

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required an inspection of 10 percent of the fire barrier penetrations

every 18 months. The inspection of all penetrations each 18 months was

considered a positive feature in the implementation of the fire

protection program to assure operability.of the fire barriers.

In the early 1990's, portions of the facility's fire protection water

distribution system were found to be partially obstructed due to

interior plaing corrosion. This piping was cleaned and, subsequently.

i flow tests lad been performed annually to evaluate the performance of

the piping system. The inspectors reviewed completed STP-128.021 which

was performed on September 26, 1997. This procedure required

comprehensive flow tests of the fire protection water distribution  ;

system and evaluations of the flow test data. The 1997 test data

indicated that a sufficient quantity of water was available to meet the

fire protection demands. In addition, the data did not indicate any.

a)preciable pressure drop or flow reduction from the 1996 test data.

T1e licensee stated that they were planning to continue flow tests and

evaluations to monitor system performance. ,

!

c. Conclusions

Excellent surveillance inspection and test procedures were provided for

the fire barriers and fire protection water distribution system.

F2.3 Fire Barrier Penetration Seals (64704)

a. Insoection Scooe

The ir spectors reviewed a sample of the facility's fire barrier

penetration seal installations to determine if the installed penetration

seals met the design documents and were bound by configurations which i

had satisfactorily passed a fire test that met the requirements of NRC

Generic Letter 86-10 and NRC Information Notices 88-04, 88-56 and 95-24.

b. Observations and Findinas

' The inspectors inspected each of the following fire barrier penetration

seals and reviewed the licensee's design and referenced test report for

each seal:

PEN. LOCATION SIZE SEAL TEST REPORT COMMENTS

TRACE IN CONFIGURATION N0./ Design

NO. INCHES

AB-236 Wall between Control 43x75' 18" silicone without Carborumdum 1/ Engineering -

and Auxiliary 61dgs. damming boards. 9" silicone avaluation I

and Rooms CB 12-03 with damming required. l

and AB 12 17 boards.

_-_ ___ _ -__-_____- _____ - _- ____-__ _ - ____ -_ ____ __ - _ _ - __ - _ -

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PEN. LOCATION SIZE SEAL TEST REPORT COMMENTS

TRACE IN 'CCNFIGURATION NO./ Design

NO. INCHES

CB 1237 Wall between Rooms CB 30x72 10" Silicone without BISCO . Tested with 1"

12-03 and CB 12-04 daming boards. 1064-10 overlap on each

9 3/4" Silicone side of a wall.

without daming Installed with 2"

boards, overlap on one side

of a wall.

Evaluation

required.

18 206' Wall between Rooms IB 28x27 10" Silicone and 3" PCA-0CT 76 PCA-0CT 76 failed

36-02 and IB 36-03 B1500 elastomer 9" Silicone tha test. Requires

pressure seal without daming evaluation,

without daming boards,

boards18-335 Wall between Rooms IB 10x30 10" Silicone without BISCO Tested with 1"

36-02 and IB 36 04 daming boards. 1064-10 overlap on each

9 3/4" silicone side of a wall.

without daming installed with 2"

boards, overlap on one side

of a wall

Evaluation

required.

IB-471 Floor between Rooms 9" 10" Silicone with 3" BISCO Evaluation

IB 36-03 sleeve elastomer pressure 748-49 required,

and IB 26-02 seal. 12" Silicone.18-472 Floor between Rooms 15x48 10" Silicone with BISCO Evaluation

IB 36-03 and IB 26-02 34" elastomer 748-220 required.

pressure seal. 9" Silicone

with 1" daming

board.

In late 1997, the licensee initiated a project to evaluate all of the

facility's fire barrier penetration seals to determine if the "As Built"

configurations met the design requirements. The evaluation will

determine if the seals are either bound by a tested configuration or

justified by an engineering evaluation. Discrepancies will be corrected

or additional evaluations will be performed. Previously, in 1987.'the

licensee identified a number of fire barrier penetrations which did not

meet the design or test requi>ements. This issue was resolved by

performing engineering evalur.tinns to justify the installation of

approximately 21 seals and upgradng or modifying approximately 15

penetration seals. The current preiect will reevaluate this issue and

provide enhanced documentation on the facility's fire barrier

penetration-seals. This project was scheduled to be completed in April-

1999.

During this inspection, the inspectors reviewed a sample of the various

types of penetration seals installed at the facility. The design of

penetration seals inspected.did not fully conform to the referenced fire

test for the seals. It appeared that an evaluation was required for the

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20

seals which were different from an acceptable tested configuration to

justify that these seals would perform their design function. These

penetration seals did not meet the basis of the design due to one or

more of the following:

. Penetration size exceeded the tested penetration size.

  • Penetration seals' free space exceeded the free space of the

tested configuration.

. Seal configuration was different from tested configurations i.e.,

tested configurations extended one-inch on both sides of the

barrier whereas the installed configuration was flush on one side

of the barrier and extended two-inches on the other side of the

barrier.

. Seal penetration was of a different configuration (cable trays in

lieu of a pipe) than the tested configuration.

. Installed penetration seals utilized an elastomer pressure seal

material on one side of the seal, whereas the tested i

configuration did not utilize the elastomer material. i

The licensee stated that evaluations for configuration differences were

probably performed; however, these evaluations were difficult to locate

and retrieve. Evaluations previously performed for penetration seals

which did not meet the design and tested configurations were documented

by a number of different means such as vendor work packages,

modification packages, field change requests to installation

modification or design packages, condition reports, engineering change

requests, request for engineering evaluations, engineering information

requests, etc. The licensee's fire barrier penetration seal

revalidation project would locate each of these evaluations and

assimilate and document this information for future retrieveability.

During the plant tours and inspection of the above penetration seals,

the inspectors noted that the penetration seals appeared to be well

maintained. In addition, all penetration seals were being inspected

every 18 months by the licensee's surveillance program. Any identified

discrepancies were repaired. Based on the licensee's efforts to

maintain the as-built configuration for seal barrier seals and the

extent of differences between the test reports and the actual plant

penetrations seals, the inspectors concluded that this issue was not an

immediate concern. The licensee's completed fire barrier penetration

seal revalidation project will be reviewed during a subsequent NRC

inspection and will be tracked as an Inspecticn Followup Item (IFI)

50-395/98001-05.

c. Conclusions

Evaluations to 'iustify the differences between as-built fire barrier

penetrationsealsandcorrespondingtestreportswerenotreadily

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available. Based on the inspector's reviews, no immediate concerns

exist. The licensee has initiated a project to: 1) review all fire

barrier penetration seals for conformance to the design requirements and

referenced fire tested configurations: 2) enhance design basis

documentation for the seals; and 3) correct any identified

discrepancies.

F5 Fire Protection Staff Training and Qualification

F5.1 Fire Briaade (64704)

a. Insnection Scoce

The inspectors reviewed the fire brigade organization and training

3rogram for compliance with the NRC approved " Summer Fire Protection

Evaluation Report."

b. Observations and Findinas

The site fire brigade organization and training requirements were

implemented by Procedure FPP-026. " Fire /HAZMAT Response." Revision 2.

Each fire brigade member was required to receive initial, quarterly and

annual fire fighting training and to satisfactorily complete an annual

medical evaluation and certification for partici)ation in fire brigade

fire fighting activities. In addition, each memaer was required to

participate in at least one fire brigade drill per year.

At the time of this inspection. 64 operations personnel and 31

maintenance personnel were on the plant's fire brigade. A sufficient

number of personnel was available to meet the staffing requirements for

the facility's operational requirements and the fire brigade complement

of one team leader and at least five members per shift.

The inspectors reviewed the fire brigade organization training and

medical records for the fire brigade members and verified that the

training and medical records were up-to-date. Additional information on

the review of the fire brigade program is located in Section F8.1. l

The inspectors witnessed a fire brigade drill on February 12. 1998.

involving a simulated fire in the Auxiliary Boiler Building east of the

power block com) lex. The response of the fire brigade to the simulated

fire included t1e fire brigade leader, three brigade members from

operations and five brigade members from maintenance. Two security

officers and two maintenance employees also responded to the fire scene.

The fire brigade members responded to the fire in full turnout gear and

with self contained breathing apparatus. The response was timely and

the brigade demonstrated the proper use of fire fighting equipment and

tactics. Comraunications between the brigade leader, the control room

and brigade members were good. The fire brigade leader's direction and

performance were also good. A critique to discuss the brigade

performance and recommendations for future enhancement was held

following the drill.

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c. Conclusions

'

The fire brigade organization and training were up-to-date and met the

requirements of the site procedure. The fire brigade demonstrated good

response and fire fightirg performance during a simulated fire brigade

drill.

F8 Hiscellaneous Fire Protection Issues (92904)

F8.1 (Closed) URI 50-395/96011-07: fire brigade personnel were not required

to participate in at least two fire brigade drills per year. The

licensee's commitment to comply with the fire brigade organization and

training guidelines of Appendix A to Branch Technical Position APCSB

9.5-1. " Guidelines for Fire Protection for Nuclear Power Plants Docketed

Prior to July 1. 1976. and the 1977 document entitled Nuclear Plant

Fire Protection Functional Responsibilities. Administrative Controls and

Quality Assurance" were reviewed and approved by the NRC in the NRC's

Safety Evaluation Report dated February 1981. These documents required

the fire brigade to participate in drills but did not specify the number

of drills to be performed per year. Procedure FPP-026. " Fire /HAZMAT

Res'onse."

Revision 2. requires fire brigade drills to be performed once

eac1 quarter for each operating shift and for all brigade members to

participate in at least one drill per year. The inspectors reviewed the

drills performed during 1997 and verified that each operations shift

participated in a fire brigade drill at least once per quarter.

Additional special drills were performed as needed to permit all

operations and maintenance personnel assigned to the fire brigade to

participate in at least one drill per year. The licensee was in

compliance with the fire brigade licensing requirements: therefore, this

unresolved item is closed.

F8.2 (Closed)IFI 50-395/96011-06: resolution of battery failures on 8-hour

Appendix R emergency lighting units. The licensee had enhanced the

)reventive maintenance and surveillance requirements for the 8-hour

)attery-powered emergency lighting units. Also, the Appendix R 8-hour

emergency lighting units had been added to the components covered by the

Maintenance Rule and a 95 percent operability requirement had been

established for these units. The inspectors reviewed the licensee's

reliability trending data for these lights and noted that the failure

rate for the past 18 months was 1.9 percent.

The licensee stated that the operability of the battery powered lighting

units was to continue as a part of the Maintenance Rule requirements.

This should assure a high operability level for these lighting units is

maintained and addresses the inspectors' previous concerns.

V. Manaaement Meetinas

X1 Exit Meeting Summary

The inspectors aresented the inspection results to members of licensee

management at t1e conclusion of the inspection on February 27, 1998.

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The licensee acknowledged the findines presented.

The inspectors asked the licensee whether any materials examined during

the inspection should be considered proprietary. No proprietary

information was identified.

PARTIAL LIST OF PERSONS CONTACTED

' Licensee

F. Bacon Manager. Chemistry Services

L. Blue. Manager. Health Physics

S. Byrne. General Manager. Nuclear Plant Operations

R. Clary Manager. Quality Systems

M. Fowlkes. Manager. Operations

S. Furstenberg. Manager. Maintenance Services

D. Lavigne. General Manager Nuclear. Support Services

.G. Moffatt. Manager. Design Engineering

K. Nettles. General Manager. Strategic Planning and Development

H. O'Quinn, Manager. Nuclear Protection Services

A. Rice. Manager. Nuclear Licensing and Operating Experience

G. Taylor. Vice President. Nuclear Operations

R. Waselus Manager.-Systems and Component Engineering

R. White. Nuclear Coordinator. South Carolina Public Service Authority

B. Williams General Manager. Engineering Services

G. Williams. Associate Manager. Operations

INSPECTION PROCEDURES USED

IP 37551: Onsite Engineering

IP 61726: Surveillance Observations

i? 62706: Maintenance Rule

IP 62707: Maintenance Observations

IP 64704: Fire Protection Program

IP 71707: Plant Operations

IP 71750: Plant Support Activities

IP 92903: Followup - Engineering

IP 92904: Followup - Plant Support

ITEMS OPENED CLOSED, AND DISCUSSED i

Ooened

50-395/98001-01 URI review solid state protection system TS operability

and' testing requirements (Section M1.3)

50-395/98001-02 URI relief valve testing requirement inconsistencies in

the valve inservice testing program controlling-

procedure and the referenced implementing test {

procedures (Section E1.1) j

50-395/98001-03 NCV failure to correctly translate condensate storage

tank design basis information into specifications.

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procedures, and instructions (Section E1.3)-

50-395/98001-04 VIO failure to establish adequate programmatic controls

for temporary shielding'(Section R1.2)

50-395/98001-05 IFI licensee's completed fire barrier penetration seal-

revalidation project will be reviewed (Section F2.3)

Closed

50-395/97002-01 IFI Maintenance Rule scoping of systems, structures and

components used in emergency operating procedures

(Section M8.1)

'50-395/97002-03 VIO failure to take appropriate corrective action for an

(a)(1) structure, system, or component (Section M8.2)

50-395/98001-03 NCV failure to correctly translate condensate storage

tank design basis information into specifications,

procedures, and instructions-(Section E1.3)

50-395/96011-07 URI fire brigade personnel were not required to

participate in at least two fire brigade drills per

year (Section F8.1)

'50-395/96011-06 IFI resolution of battery failures on 8-hour-Appendix R

emergency lighting units (Section F8.2)

Discussed

50-395/97013-01 IFI failure of the A diesel generator during a

surveillance test (Section E8.1)

c

L