ML20128K010

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Insp Rept 50-395/96-09 on 960721-0907.Violation Noted.Major Areas Inspected:Operations,Maint,Engineering,Plant Support
ML20128K010
Person / Time
Site: Summer South Carolina Electric & Gas Company icon.png
Issue date: 10/04/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20128J985 List:
References
50-395-96-09, 50-395-96-9, NUDOCS 9610100262
Download: ML20128K010 (23)


See also: IR 05000395/1996009

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U. S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket No.-

50-395

License No..

NPF-12

Report No.

50-395/96-09

Licensee:

South Carolina Electric & Gas (SCE&G) Company

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Facility:

V. C. Summer Nuclear Station

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Location:

P. O. Box 88

Jenkinsville. SC 29065

Dates:

July 21 - September 7, 1996

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Inspectors:

B. Bonser. Senior Resident Inspector

T. Farnholtz. Resident Inspector

R. Gibbs. Reactor Inspector RII (Section M1.1)

C. Ogle. Senior Resident Inspector. Vogtle (Section E8.1)

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Approved by:

G. Belisle. Chief. Reactor Projects Branch 5

Division of Reactor Projects

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ENCLOSURE 2

9610100262 961004

PDR

ADOcK 05000395

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PDR

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EXECUTIVE SUMMARY

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V. C. Summer Nuclear Station

NRC Inspection Report 50-395/96-09

This integrated inspection included aspects of licensee operations.

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maintenance, engineering, and plant support.

The report covers a 7 week

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period of resident insaection: in addition. it includes the results of

announced inspections ]y a regional reactor inspector and a senior resident

inspector from Vogtle.

Ooerations

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The inspectors identified a Non-Cited Violation for failure to establish

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an approved procedure for determining the source of leakage on a power

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operated relief valve tailpipe high temperature alarm (Section 02.2).

The inspectors' review of the operator work around 3rogram concluded

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that appropriate compensatory actions had been esta31ished for each of

the safety significant deficient conditions and that in the aggregate.

they did not pose a significant challenge to operator performance. The

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inspectors considered this program to be useful and effective in

identifying and acting upon deficient conditions (Section 04.1).

A review of two plant transients during the inspection period concluded

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that control room operators had demonstrated good piant awareness and

knowledge.

During normal operations, two examples of poor operator

awareness were identified. A component cooling water pump switch on the

main control board was slightly out of position and not showing the

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proper flag and six status lights on the main control board were not

functioning properly (Section 04.2).

A Non-Cited Violation was identified concerning an operator starting a

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centrifugal charging pump without first establishing the required

component cooling water flow (Section 04.2).

Based on attending two Plant Safety Review Committee (PSRC) meetings

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during the inspection period, the inspectors concluded that the

requirements of the applicable sections of the Technical Specifications

and the station administrative procedure were met.

The inspectors noted

that the PSRC review of a Licensee Event Report (LER) was done after the

LER had already been issued (Section 07.1).

Maintenance

An overview inspection of the maintenance area provided a favorable

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impression of the overall maintenance program at V. C. Summer.

Personnel appeared to be well qualified for their positions. work areas

were orderly and well maintained. the plant material condition was

excellent. and procedures were clear and concise.

The existence of a

number of health pnysics drip funnels in tne plant indicated a lack of

maintenance action to correct system leakage problems (Section M1.1).

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All observed surveillance activities were conducted in a arofessional

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manner and resulted in a high degree of confidence that t1e tested

components would perform as designed (Section M2.1).

A weakness in the revision process for safety related Instrument &

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Calibration procedures was identified and illustrated by two examples.

Both examples involved a change in the plant that was not correctly

implemented in the appropriate procedure.

The inspectors also concluded

that the licensee was appropriately identifying and documenting problems

in this area (Section M3.1).

The inspectors identified a violation of Technical Specification

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Sutveillance Requirement 4.8.2.1.a. Weekly Battery Surveillance. The

surveillance was performed while the B battery was on an equalize charge

and not on a float charge as specified in the Technical Specification

Surveillance Requirement (Section M3.2).

Enaineerina

The inspectors observed and reviewed the work done on the turbine driven

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emergency feedwater pump to correct a low speed oscillation and

determined that it was adequate.

Post-maintenance testing and

surveillance testing were satisfactory (Section E2.1).

The inspectors did not identify any concerns regarding the calibration

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or operation the post-accident hydrogen analyzers (Section E2.2).

Plant Suocort

The inspectors observed radiological controls during the conduct of

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tours and observation of maintenance activities and found them to be

acceptable (Section R1.1).

The licensee continued to maintain the reauired radiation monitors in an

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operable condition (Section R2.1).

The licensee prepared the emergency response team adequately and readied

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the plant to minimize the risk and potential damage to plant facilities

from potential high winds and rain expected from hurricane Fran. The

inspectors also observed that plant management had fully supported all

emergency preparations (Section Pl.1).

The inspectors observed security and safeguards activities during the

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conduct of tours and observation of maintenance activities and found

them to be good.

Compensatory measures were posted when necessary and

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properly conducted (Section 51.1).

a Non-Cited V olation '..as "dert m d ' r ? e '311ure to ccg ensate for

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inoperable fire barriers in the Intermediate Building (Section F4.1).

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Report Details

Summarv of Plant Status

Unit 1 began this inspection period at 100 percent power.

On August 4. power

was reduced to 70 percent due to the loss of a circulating water pump. The

plant returned to full power on August 11 after repair of the circulating

water pump motor and remained at that level for the remainder of the

inspection period.

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Doerations

01

Conduct of Operations

01.1 General Comments (71707)

Using Inspection Procedure 71707 the inspectors conducted frequent

reviews of ongoing plant operations.

In general, the conduct of

operations was professional and safety-conscious; specific events and

noteworthy observations are detailed in the sections below.

02

Operational Status of Facilities and Equipment

02.1 Plant Walkdowns

The inspectors toured accessible plant areas.

Major components were

visually inspected to identify any general conditions that might degrade

system operation.

During plant tours the inspectors checked the

containment isolation lineup by verifying that all penetrations not

capable of being closed by automatic isolation valves and required to be

closed during accident conditions were closed by either valves or blind

flanges.

02.2 Station Orders

a.

Insoection Scope (71707)

The ins)ectors reviewed the Special Instruction and Station Order (50)

Log Boot maintained in the control room to determine if the intent and

purpose of these dcauments, as stated in the Station Administrative

Procedure (SAP). were being met.

b.

Observations and Findinas

The inspectors reviewed 50 95-05. Pressurizer Power Operated Relief

Valve (PORV) Tailpipe High Temperature, dated April 1995.

This provided

instructions to operators for responding to a computer generated high

pressurizer PORV tailpipe temperature alarm resulting from PORV seat

leakage.

The alarm provides a warning when pressurizer PORV tailpipe

temperature 's several Me"ree "* *m

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pressurizer safety valve talipipe temperatures.

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The inspectors noted that the S0 provided specific instructions on valve

manipulations to determine the source of potential leakage.

A review of

SAP-204. Operating Logs and Records, revision 6 indicated that the

intent of S0s is to provide a means of disseminating short duration

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information and instructions of a general nature to shift personnel.

This 50 was neither of a short duration (since April 1995) or of a

general nature (contained specific operator actions).

Based on the

review of SAP-204, the inspectors concluded that the 50 represented a

procedere.

As such it required the review and controls specified by

Technical Specification (TS) 6.8. Procedures and Programs.

The inspectors concluded that the safety significance of this failure to

establish approved procedures for these activities was minimal.

Based

on discussions with operations personnel it had not been necessary to

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use the 50 since it was issued.

This failure constitutes a violation of

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minor significance and is being treated as a Non-Cited Violation (NCV).

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consistent with Section IV of the NRC Enforcement Policy (50-395/96009-

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c.

Conclusions

The inspectors identified an NCV for failure to establish an approved

procedure for determining the source of leakage on a PORV tailpipe high

temperature alarm.

04

Operator Knowledge and Performance

04.1 -Review of Coerator Work Arounds

a.

Insoection Scooe (71707. 40500)

The inspectors reviewed operator work arounds to assess their overall

safety significance and the potential impact of the collective work

arounds on plant performance.

The inspectors also reviewed the level of

licensee support for resolving the work arounds.

b.

Observations and Findinas

The licensee has established an informal operator work around program in

which operator work amunds are identified, documented, periodically

reviewed by plant management and given priority for resolution. The

licensee has defired an operator 30rk around as an equipment, program.

or procedure deficiency that could adversely affect normal, abnormal, or

emergency plant operations and/or could result in an inappropriate

response due to the required compensatory actions being performed.

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The inspectors noted several safety significant operator work arounds in

this review.

The inspectors res iened each of the safety significant

work arounds in more detail and found that appropriate compensatory

actions had been established for each of these conditions.

Corrective

action due dates had been established and appeared reasonable based on

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the deficieny.

The inspectors concluded that in the aggregate, these

work arounds did not pose a significant challenge to operator

performance.

The inspectors concluded that this was a useful and effective program to

identify and act upon those deficiencies that were considered operator

work arounds..

c.

Conclusions

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The inspectors * review of the licensee's operator work around program

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concluded that appropriate compensatory actions had been established for

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each of the safety significant deficiencies and that, in the aggregate,

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they did not pose a significant challenge to operator performance. The

inspectors considered this program to be useful and effective in

identifying and acting upon work arounds.

04.2 Ooerator Performance

a.

Insoection Scooe (71707. 40500)

The inspectors reviewed two unplanned operational transients that

occurred during the inspection period.

Observations were also made

during routine control room tours.

Condition Evaluation Reports (CERs)

were reviewed.

b.

Observations and Findinos

On August 4, with the plant operating at full power. an apparent

lightning strike caused a loss of the B circulating water pump. As

required by procedure, power was reduced to 70 percent at 5 percent a

minute.

On August 16, with the plant operating at full power, a steam

flow instrument failed high causing increased feedwater flow and a Steam

Generator (SG) level deviation.

Both of these transients required operator action to restore the plant

to a_ stable condition.

The inspectors found that during these plant

transients, operators identified the abnormal conditions promptly and

acted correctly to stabilize the plant.

- The inspectors concluded that control room operators demonstrated good

plant awareness and knowledge in responding to these minor plant

transients..

However, during normal operations the inspectors observed two instances

of poor operator awareness. On July 24. during a main control board

wal(down the inspectors observed the A Component Cooling Water (CCW)

pump switch cocked slightly towards the STOP position.

Also, the flag

in the swit-h was ont showing 9'ther 3 3reer yF) gr c9d 'O'j)

indication.

At the time of this observation the A CCW pump was in a

standby condition.

The pump was not running but would automatically

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start if required.

The normal after stop position of this switch is

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vertical with a green flag showing in the window. When questioned by

the inspectors, the operator corrected the switch position with a green

flag visible.

The inspectors did not identify any concerns as to the

ability of the A CCW pump to start if required.

On August Q the inspectors pointed out to the Shift Supervisor that

six status

.ghts on the phase A isolation and the safety injection

status panei., did not appear to be functioning properly. These status

lights consisted of two lamps for each component w11ch are either dim or

bright depending on the current condition of the component.

In these

six cases, one of the two lamps did not appear to be lit.

The control

room operators corrected the status lights when it was brought to their

attention.

The inspectors concluded that the control room operators were not always

aware of the status of partially degraded indications on the main

control board.

On August 25. the licensee started the C Centrifugal Charging Pump (CCP)

without first establishing CCW flow to support pump operation. The

operators were using SOP-102, Chemical and Volume Control System,

revision 15. The initial conditions of the section used for placing an

idle charging pump in service specify that the CCW system is to be in

service.

CCW flow provides cooling for the lube oil coolers associated

with the CCP.

The operator immediately realized the mistake and shut

off the pump.

Computer records indicated that the pump ran a total of

13 seconds without CCW flow.

B train CCW flow was established and the C

CCP was run to inspect for any possible damage

No damage was

identi fied.

The licensee indicated that SOP-102 would be revised to

make establishing CCW flow a procedural step rather than an initial

condition to increase operator awareness of this requirement.

This

failure constitutes a violation of minor significance and is being

treated as an NCV. consistent with Section IV of the NRC Enforcement

Policy (50-395/96009-02).

c.

Conclusions

A review of two plant transients during the inspection period concluded

that control room operators had demonstrated good plant awareness and

knowledge.

During normal operations two examples of poor operator

awareness were identified.

A CCW pump switch on the main control board

was slightly out of position and not showing the proper flag and six

status lights on the main control board were not functioning properly.

An NCV was identified concerning an operator starting a CCP without

first establishing the required CCW flow.

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07

Quality Assurance in Operations

07.1 Licensee Self-Assessment Activities

a.

Insoection Scone (40500)

The inspectors attended two Plant Safety Review Committee (PSRC)

meetings to verify that they met the requirements of TS 6.5.1 and SAP-

120. Plant Safety Review Committee, revision 7.

b.

Observations and Findinas

The inspectors attended two PSRC meetings on August 13 and August 30.

Each meeting was called to order with the required quorum present.

TS 6.5.1.5 specifies the required quorum as the Chairman or his designated

alternate and a majority of the PSRC appointed members including their

alternates. An agenda was distributed to all PSRC members or their

alternates to define the subject matter to be discussed at the meeting.

Off-normal occurrence reports, procedure revisions, safety evaluations.

and non-conformance notices were an.ong the subjects reviewed during the

meetings.

The discussions were open and all members were allowed to

voice questions or concerns.

The August 30 meeting included a review of a Licensee Event Report

(LER).

TS 6.5.1.6.h and SAP-120 specify that the PSRC must review all

reportable events.

The ins)ectors noted that the PSRC review of this

LER was done after the LER 1ad already been issued.

c.

Conclusions

Based on attending two PSRC meetings during the inspection period, the

inspectors concluded that the requirements of the applicable sections of

the TS and the SAP were met.

08

Miscellaneous Operations Issues (92901)

08.1

(Closed) Insoection Follow-UD Item 50-395/94028-02:

scaling of steam

flow transmitters.

This item was opened pending review of data taken

during the first operating cycle following the steam generator

replacement.

On January 11, 1995, the licensee performed Surveillance

Test Procedure (STP)-205.002. Reactor Coolant System Flow Rate

Measurement, revision 7

Data taken during this test was used to

determine the actual steam flow from each of the three SGs at 100

percent rated thermal power.

In addition. rack voltage measurements

were taken at the output of each installed steam flow transmitter to

determine the differential pressure across each SG flow restrictor and a

restriction flow constant was calcu 3ted.

Using this data. the steam

flow transmitters were calibratea.

During part of operating cycle nine. one high steam flow protection

system bistable was in a tripped condition at full power.

The licensee

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developed and implemented a process to renormalize the steam flow

bistables to the feedwater flow indication.

No further bistable trip

problems were experienced. The inspectors reviewed the correspondence,

methodology, and data associated with this issue and concluded that the

steam flow transmitters were calibrated using good engineering

judgement.

II.

Maintenance

M1

Conduct of Maintenance

M1.1 General Comments

a.

Insoection Scooe (62703. 61726)

The inspectors observed the performance of routine maintenance to verify

that applicable aspects of the licensee's maintenance program were being

complied with.

In addition, an overview inspection of the maintenance

area was performed to provide the necessary background to support

future, more detailed inspections in this area.

The inspection included

attendance at the plan of the day meeting. interviews with maintenance

management personnel, tours of work areas and facilities, review of

maintenance performance indicators, review of the maintenance

organization and staffing, and a review of several key maintenance

administrative procedures which define the licensee's maintenance

program.

In addition the inspectors observed preventive maintenance on

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a Motor Control Center (MCC) in accordance with Maintenance Work Order

(MWO) P0199971 and Electrical Maintenance Procedure (EMP) 280.006.

Molded Case Circuit Breaker and Controller Inspection and Preventive

Maintenance, revision 4. change C. vibration analysis on the bearing oil

pump for the A CCP in accordance with procedure EMP 295.005. Vibration

Analysis, revision 6. and surveillance of a pressurizer pressure

instrument in accordance with Surveillance Test Task Sheet (STTS)

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0061661 and STP 302.005. Pressurizer Pressure Instrument IPT 00456

Operational Test. revision 4.

The inspectors also conducted an

extensive plant tour to assess overall plant material conditions.

Review of the following maintenance related documents and activities

were included in this inspection:

SAP 103. Statement of Responsibilities Maintenance Services,

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revision 5. change A

SAP 123. Procedure Use and Adherence. revision 1. change B

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SAP 134. Control of Station Surveillance Activities. revision 8.

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change B

SAP 300. Conduct of Maintenance, revision 7 change E

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SAP 601. Application. Scheduling and Handling of Maintenance

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Activities, revision 9, change B

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SAP 1286. Material System User Procedure. revision 0

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MWR 96E3197 Place A Train Battery on Equalize Charge

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Preventive Maintenance Task Sheet (PMTS) P0200421. RHR Spray Pump

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Roughing Filter Differential Pressure Indicator

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PMTS P0200967. RHR Pump B Flow Switch

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MWR 9603910. Turbine Driven Emergency Feedwater (TDEFW) Pump -

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Investigate and Repair as Necessary

MWR 96M3147. Correct Loose Linkage on the TDEFW Pump

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PMTS P0201407. ATWS Mitigation System Actuation Circuitry

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b.

Observations and Findinas

The inspectors observed that all of the work areas were clean and

orderly.

All calibrated equipment observed by the inspectors in the

work areas was noted to be within the required calibration due date, and

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material stored in maintenance storage areas was properly identified and

protected.

Maintenance personnel performing work were knowledgeable of

plant procedures and equipment, and conducted the work in a professional

manner.

Work was conducted in accordance with plant procedures. and no

deficiencies in the work or documentation of the work were observed.

Plant material condition was excellent.

The inspectors observed a

number of Health Physics (HP) drip funnels under equipment in the plant

indicating lack of maintenance action to correct system leakage

problems.

c.

Conclusions

An overview inspection of the maintenance area during this inspection

provided a favorable impression of the overall maintenance program at

V. C. Summer.

Personnel appeared to be well qualified for their

positions, work areas were orderly and well maintained. the plant

material condition was excellent, and procedures were clear and concise.

The existence of a number of HP drip funnels in the plant indicated a

lack of maintenance action to correct system leakage problems.

M2

Maintenance and Material Condition of Facilities and Equipment

M2.1 Surveillance Observation

a.

Insoection Scooe (61726)

The inspectors observed surveillance activities to verify that they were

planned and conducted as required by applicable procedures and

satisfactorily demonstrated equipment operability.

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b.

Observations & Findinas

The inspectors observed all or part of the following surveillance tests:

STP 206.003. Charging / Safety Injection Pump and Valve Test.

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revision 4.

STP 123.003B. Train B Service Water System Valve Operability Test,

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revision 2.

STP 220.002. Turbine Driven Emergoncy Feedwater Pump Test.

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revision 1.

STP 209.002. Incore vs. Excore Axial Offset. revision 8.

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STP 212.001. Reactor Core Flux Mapping, revision 6.

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STP 125.002. DG A Operability Test. revision 17.

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c.

Conclusions

All observed surveillance activities were conducted in a professional

manner and resulted in a high degree of confidence that the tested

components would perform as designed.

M3

Maintenance Procedures and Documenta

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M3.1 Procedural Discreoancies

a.

Insoection Scoce (62703. 62707. 40500)

The insportors routinely reviewed CERs related to maintenance during the

inspection period to determine if the licensee was identifying and

correcting maintenance problems.

b.

Observations and Findinas

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The inspectors reviewed two safety related procedural problems

identified by the licensee in the Instrumentation & Controls (I&C) area.

The first problem occurred on August 16 when a circuit card failed in

the B SG steam flow instrument loop.1FT00484.

While attempting to

return the loop to service. the licensee identified that a gain setting

for a multiplier / divider card identified in calibration procedure. STP-

395.005. Steam Generator B Steam /Feedwater Flow Instrument

1FT00484/1FT00487 Calibration, revision 8. had not been revised as

expected following the recent refueling outage.

The incorrect gain

setting made the circuit card calibration less accurate.

The gain had

changed en W e o rd due to the nlant ucrate and tho ,rrroasod steam

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flow.

Four other similar procedures had also not been revised. The

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other flow instrument loops were checked and founa to be fully operable.

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The gain settings in the other loops had been set at the new value.

Subsequently, the affected procedures were revised.

A second procedural problem was identified on August 20 when Volume

Control Tank (VCT) purge isolation valve. PCV-1092. closed during the

conduct of VCT pressure transmitter 1PT00117 loop calibration procedure

ICP-130.008. Volume Control Tank Pressure 1PT00117, revision 4.

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valve trip)ed closed on a low VCT pressure signal from 1PT00117. The

procedure lad been revised to remove the auto closure feature of PCV-

1092.

The licensee had intended to implement a modification to remove

the auto closure of the VCT valve. The modification was not completed

but ICP-130.008 was revised and approved for use.

After this was

identified, the licensee installed the modification.

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Both of these procedure problems were identified and documented by the

licensee in their internal problem reporting program.

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c.

Conclusions

A weakness in the revision 3rocess for safety related I&C procedures was

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identified and illustrated )y two examples.

Both examples involved a

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change in the plant that was not correctly implemented in the

appropriate procedure.

The inspectors also concluded that the licensee

was appropriately identifying and documenting problems in this area.

M3.2 Missed Batterv Surveillance

a.

Insoection Scooe (61726)

The inspectors reviewed activities associated with the safety related

batteries and completion of the weekly battery surveillance test.

b.

Observations and Findings

During plant tours on the week of August 4. the inspectors observed that

the A train battery charger equalize / float switch was in the equalize

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position.

The inspectors questioned the position of the equalize / float

switch when the battery should have been on float charge.

The

inspectors also questioned how the weekly battery surveillance was being

accomplished on the B battery when the B battery was on equalize charge

and the surveillance initial requirements required a battery on float

charge.

The inspectors found that the licensee had identified a problem with the

float / equalize switch on the A train charger.

The inspectors reviewed

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the licensee's evaluation of the problem.

The evaluation provided

justification for leavina the switch in the enualize oosition and

adjusting the equalize potentiometer on the cnarger to the float

voltage. The inspectors had no further questions.

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The inspectors also reviewed performanc

of the weekly battery

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surveillance test. STP-501.001. Batter.) .eekly Test. revision 7.

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inspectors found that the B train batte y weekly surveillance test was

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3erformed incorrectly on August 5.

Th( licensee performs the weekly

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)attery surveillance requirement each handay. The surveillance data

recorded on August 5 was taken at an equalize voltage of 138.1 volts

direct current (VDC) instead of a float voltage of 133-135 VDC. The TS

surveillance requirement. 4.8.2.1.a. specifically requires that the

battery be on a float charge when the surveillance test is performed.

Conducting the surveillance at this higher voltage had the Jotential to

mask a degraded DC source.

This failure to perform the weecly battery

surveillance correctly is a violation of TS surveillance requirement 4.8.2.1.a (50-395/96009-03).

When the error was identified the licensee re-performed the weekly

surveillance on the B train battery.

The tests results indicated the

battery was operable.

The inspectors concluded from a review of weekly

surveillance test data taken before and after this problem was

identified that the B train battery had remained operable.

The inspectors reviewed surveillance procedure. STP-501.001. and found

that the initial conditions did not state a requirement for the battery

to be on a float charge before conducting the surveillance procedure.

This surveillance had been performed correctly several times before with

one of the batteries on an equalize charge.

The licensee indicated that

the technicians knew of the float charge requirement before performing

the previous tests and had adjusted the battery voltage.

The inspectors

concluded that an inadequate surveillance procedure was a significant

contributor to this error.

c.

Conclusions

The inspectors identified a violation of TS Surveillance Requirement 4.8.2.1.a. Weekly Battery Surveillance.

The surveillance was performed

while the B battery was on an eaualize charge and not on a float charge

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as specifieo in the TS surveillance requirement.

III.

Enaineerina

E2

Engineering Support of Facilities and Equipment

Turbine Dr ;cn Emergency Feedwater fTCEF'.0 Pumo Low Sceed Oscillations

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a.

Insoection Scoce (37551)

During the performance of the monthly surveillance test of the TDEFW

pump on July 9. a speed oscillation of approximately 300-400 Revolutions

Per Minute OPM) was evoerlenced while the cumo nas coeratina at low

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speed. On August 7. during the performance of the same monthly

surveillance test, a similar low speed oscillation was experienced.

The

inspectors reviewed actions taken by plant engineering personnel to

resolve this problem.

b.

Observations and Findinas

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On July 9. the TDEFW pump speed was reduced from the normal operating

speed of 4150 RPM following the completion of the data taking portion of

STP 220.002. Turbine Driven Emergency Feedwater Pump Test, revision 1.

When the pump speed was reduced to approximately 3000 RPM, a speed

oscillation of about 300-400 RPM was experienced.

The licensee was

unable to reproduce the oscillations during subsequent pump runs.

The

governor was replaced and the pump was run successfully.

A detailed

examination of the governor by the vendor did not reveal the cause of

the oscillations.

On August 7. a similar low speed oscillation occurred after the pump

speed was reduced following surveillance testing.

At that time the

licensee was able to reproduce the oscillations.

The linkage between

the governor and the governor valve appeared to have noticeable

freeplay.

This linkage consists of two arms extending from a pivot pin

with the governor connected at one end and the governor valve connected

at the other end.

The freeplay in the linkage appeared to be

concentrated in the arm to pivot pin connections.

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The licensee documented this condition on CER 96-0056 and generated MWR

96M3147 to correct the loose linkage.

Tapered boles were fashioned

through each of the arms and the pivot pin and two properly sized

tapered pins were installed.

In addition. Non-Conformance Notice (NCN)

960052 was written to fabricate and install a new carbon steel bonnet

spacer in the governor valve. to install a new buf fer spring with a

higher spring constant in the governor, and to grind a bevel in the

governor lever fork to relieve some slight binding.

Post-maintenance

testing of the TDEFW pump was cerformed following this work with no

furtner low speed oscillations.

STP 220.002 was performed

satisfactorily.

c.

Conclusions

The inspectors observed and reviewed the work done on the TOEFW pump to

correct a low speed oscillation and determined that it was adequate.

Post-maintenance testing and Lrveillance testing were satisfactory.

E2.2 Post-Accident Hydroaen AnalvZer Status

a.

Insoection Scooe (37551)

The insoectors reviewed the ctatus of the cost-accident hydroaen

analyzers.

The review incluaea tne iatest surveliiance testing data.

the STP. and the 50P.

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b.

Observations and Findinas

The purpose of the post-accident hydrogen analyzers is to sample the

atmosphere in the reactor building following an accident to determine

the hydrogen concentration.

This is accomplished using two separate

hydrogen analyzers. train A and train B.

Each of these analyzers is

calibrated every 18 months.

The latest calibration test was performed

on the A train analyzer on November 8. 1995 (STP-301.004 Train A

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Containment Hydrogen Monitor Calibration. revision 2) and on the B train

analyzer on February 12. 1996 (STP-301.005. Train B Containment Hydrogen

Monitor Calibration, revision 2).

The inspectors reviewed the

1

procedures and data sheets for these two tests and verified that all

data points were within the required setpoint band for both the as-found

and the as-left conditions.

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Operation of the post-accidert hydrogen analyzers is done using SOP-122.

Post Accident Hydrogen Removal System revision 7.

This procedure

covers both the startup and shutdown of the A train and B train

analyzers.

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c.

. Conclusions

The inspectors did not identify any concerns regarding the calibration

or operation of the post-accident hydrogen 6nalyzers.

E7

Quality Assurance in Engineering Activities (37551)

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E7.1 Review of Uodated Final Safety Analvsis Reoort (UFSAR) Commitments

A recent discovery of a licensee operating their facility in a manner

contrary to the UFSAR description highlighted the need for a special

focused review that compared plant practices. procedures and/or

parameters to the UFSAR description.

While performing the inspections

discussed in this report. the inspectors reviewed the applicable

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portions of the UFSAR that related to the areas insoected.

No

discrepancies were laentified.

E8

Miscellaneous Engineering Issues (92903)

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E8.1

(Closed) Insoection Follow-uo Item 50-395/94019-03:

verification of

service water pond temperature and level.

This item was opened pending

further review of potential instrument inaccuracies associated with

measurement ;f service .sater pond temperature and level.

On July 24. 1996. the licensee initiated CER 96-10 in response to

concerns identified during a recent licensee service water self-

assessment.

Specifically at issue was that the TS limit of 95 F for

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service water pond temperature did not take into account the expected

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temperature rise during a postulated Loss Of Coolant Accident (LOCA) nor

account for instrument error when measuring pond temperature.

This

could potentially conflict with the post-accident design basis service

water pond temperature specified in the UFSAR of 95 F.

In response the

licensee developed calculation DC 00020-196.

The inspectors reviewed

the calculation and noted that it determined a 1.7 F rise in service

water pond temperature may occur after a LOCA.

The same calculation

also analyzed the associated instrument error.s and recommended a reduced

maximum service water pond temperature below 95 F. (The exact

temperature varies with the measurement method).

This recommendation

has been adcated as an administrative limit.

Further. the inspectors

were informed that a historical review of plant logs revealed no cases

where this reduced temperature has been exceeded.

The inspectors

concluded that this calculation and reduced administrative limit

adequately addressed the inspectors' concerns on temperature

measurement.

This Jortion of the Inspection Followup Item (IFI) is

closed.

However tie current design basis and TS limit may be

inconsistent.

This is the subject of an ongoing licensee review.

Pending further NRC review of the resolution of this issue, this is

identified as IFI 50-395/96009-04: Inconsistent TS and Design Basis

Limits For Service Water Pond Temperature.

The inspectors reviewed the UFSAR description of the service water pond

and Monticello reservoir inter-connecting pipe, the service water pond

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low level annunciator procedure. and a surveyor's mark located in the

service water bay. The inspectors concluded that these provided

reasonable assurarice that a pond level below the TS minimum will not

occur.

E8.2 (Closed) Violation 50-395/94027-02:

failure to provide correct work

instructions for the secondary hydrostatic test.

STP-249.052. Main

Steam / Steam Generators Hydrostatic Testing. contained errors in required

test pressures and in the designation of a spring can to be pinned for

the hydrostatic test.

The inspectors reviewed changes made to this

orocedure and other hydrostatic test procedures and concluded they were

adequate.

The licensee's response dated February 9, 1995 was reviewed

and found to be acceptable.

IV.

Plant Supoort

R1

Radiological Protection and Chemistry (RP&C) Controls

R1.1 General Comments

The inspectors observed radiological controls during the conduct of

tours and observation of maintenance activities and found them to be

acceptable.

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R2

Status of RP&C Facilities and Equipment

R2.1 Plant Area and Process Radiation Monitors

a.

Insoection Scoce (71750)

The inspectors reviewed the status of the radiation monitoring equipment

which measures radiation levels in specific areas and processes

throughout the plant.

b.

Observations and Findings

The inspectors reviewed the status of the plants radiation monitoring

system and made the following observations:

RM-G6 (reactor building refueling bridge) was inoperable.

This

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radiation monitor is only required during refueling operations and

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will require a reactor building entry to repair prior to the start

of any refueling operations.

RM-L5 (monitor tank discharge) and RM-L9 (licuid waste discharge)

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were in alarm due to a low flow condition. These monitors are in

operation only when a release from the monitor tanks is in

progress.

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RM-L3 (liquid steam generator blowdown) and RM-L10 (steam

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generator blowdown effluent) were in alarm due to a low flow

condition.

The SG blowdown flow was being directed to the main

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condenser.

These radiation monitors are not in service when in

this conditton.

All other radiation monitors were in service and functioning properly.

c.

Conclusion

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The licensee continued to maintain the required radiation monitors in an

operable condition.

P1

Conduct of EP Activities

Pl.1 General Comments (71750)

The inspectors observed the licensee's preparations on September 4 and 5

for the potential high winds and rain expected from hurricane Fran.

The

inspectors concluded that the licensee had prepared the emergency

response team adequately and had readied the olant to minimize risk and

potential damage to plant facilities.

The inspectors also observed that

olant manaaement had fully succorted all emercency creoarations.

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S1

Conduct of Security and Safeguards Activities

S1.1 General Comments (71750)

The inspectors observed security and safeguards activities during the

conduct of tours and observation of maintenance activities and found

them to be good.

Compensatory measures were posted when necessary and

properly conducted

F4

Fire Protection Staff Knowledge and Performance

F4.1

Incoerable Fire Detection Eauioment

a.

Insoection Scooe (71750)

On August 24. the licensee identified an area of the plant with

inadequate compensation for inoperable fire barriers.

This condition

was documented on CER 96-0112.

b.

Observations and Findinas

During the inspection period, fire detection system panel XPN-100 was

taken out of service to perform a modification to this system. A roving

fire watch to monitor two areas of the Intermediate Building (IB) 412

foot level (IB 12-02W and IB 12-02E) at least once per hour was

established to compensate for the affected inoperable fire detection

devices.

Also located on the IB 412 level (IB 12-02) were fire barriers

containing Thermo-Lag which had been monitored by an hourly roving fire

watch for several years pending a resolution of issues surrounding the

use of this material.

When XPN-100 was taken out of service. Fire

Protection Procedure (FPP)-025. Fire Containment, revision 0. required

that this area be monitored by a continuous roving fire watch at least

every 20 minutes.

This action was separate from tne roving fire watch

established for IB 12-02W and IB 12-02E.

During a paperwork review on August 24. the licensee identified that IB

12-02 had not been monitored as required following removal of XPN-100

from service.

The continuous roving fire watch log indicated that area

IB 12-02W was monitored every 20 minutes instead of area IB 12-02.

This

left area :312-02 unmonitored on either the 20 minute or hourly

frequency.

These two areas are adjacent to each other and it is

reasonable to assume that smoke or flames in area IB 12-02 would be

noticed by the fire watch in area IB 12-02W.

The licensee promptly

established the proper continuous roving fire watch in area IB 12-02.

TS 6.8.1 f reau1res that written Drocedures be established. imolemented.

ano maintainea covering tne t1re Protection Program.

ine rallure to

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compensate for the inoperable fire barriers in area IB 12-02 was a

violation of TS 6.8.1.f. in that. FPP-025 required that this area be

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monitored at least every 20 minutes.

This licensee-identified and

corrected violation is being treated as an NCV. consistent with Section

VII.B.1 of the NRC Enforcement Policy (50-395/96009-05).

c.

Conclusion

An NCV was identified for the failure to compensate for inoperable fire

barriers in the Intermediate Building.

F8

Miscellaneous Fire Protection Issues (92904)

F8.1

(Closed) Insoection Follow-Uo Item 50-395/94007-05:

correction of fire

protection problems involving low flow to sprinklers and missing

sprinklers.

Extra sprinklers not included in the flow calculation.

Fire main flow tests performed in the Auxiliary and Intermediate

Buildings indicated a low flow condition in some parts of the system.

Several NCN dispositions were generated to clean the obstructed portions

of the system, install additional sprinklers, and to remove sprinklers

that were not required.

These changes were made in accordance with a

newly developed design guide which establishes a design basis for the

preaction sprinkler system and provides criteria for meeting certain

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performance based objectives.

The inspectors considered these changes

to be appropriate.

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V.

Manaaement Meetinas

X1

Exit Meeting Summary

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The inspectors presented the inspection results to members of licensee

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ruanagement at the conclusion of the inspection on September 11. 1996.

The licensee acknowledged the findings presented.

The inspectors asked the licensee whether any materials examined during

the inspection should be considered proprietary.

No proprietary

information was identified.

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PARTIAL LIST OF PERSONS CONTACTED

Licensee

F. Bacon, Manager. Chemistry Services

L. Blue. Manager. Health Physics

M. Browne. Manager. Design Engineering

S. Byrne General Manager. Nuclear Plant Operations

M. Fowlkes Manager. Operations

S. Furstenberg. Manager. Maintenance Services

S. Hunt. Manager. Quality Systems

D. Lavigne. General Manager. Nuclear Safety

G. Lippard. Acting Manager. Nuclear Licensing and Operating Experience

G. Moffatt. Manager. Planning and Scheduling

K. Nettles. General Manager. Strategic Planning and Development

H. O'Quinn. Manager. Nuclear Protection Services

A. Rice. Manager. Nuclear Licensing and Operating Experience

G. Taylor. Vice President. Nuclear Operations

T. Taylor. General Manager. Engineering Services

R. Waselus. Manager. Systems and Component Engineering

R. White. Nuclear Coordinator. South Carolina Public Service Authority

B. Williams. General Man;ger. Engineering Services

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INSPECTION PROCEDURES USED

IP 37551: Onsite Engineering

IP 40500: Effectiveness of Licensee Controls in Identifying, Resolving, and

Preventing Problems

IP 61726: Surveillance Observations

IP 62703: Maintenance Observations

IP 62707: Maintenance Observations

IP 71707: Plant Operations

IP 71750: Plant Support

IP 92901: Followup - Plant Operations

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IP 92903: Followup - Engineering

IP 92904: Followup - Plant Support

ITEMS OPENED. CLOSED AND DISCUSSED

Ooened

50-395/96009-01

NCV failure to establish approved procedures (Section

02.2).

50-395/96009-02

NCV failure to establish component cooling water flow

prior to starting a centrifugal charging pump

(Section 04.2).

50-395/96009-03

VIO failure to correctly perform a weekly battery

surveillance (Section M3.2).

50-395/96009-04

IFI

inconsistent TS and design basis limits for service

water pond temperature (Section E8.1).

50-395/96009-05

NCV failure to compensate for inoperable fire barriers

(Section F4.1).

Closed

50-395/96009-01

NCV failure to establish approved procedures (Section

02.2).

50-395/96009-02

NCV failure to establish component cooling water flow

prior to starting a centrifugal charging pump

(Section 04.2).

50-395/94028-02

IFI

scaling of steam flow transmitters (Section 08.1).

20-395/94019-03

IFI

verification of service water pond temperature and

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level (Section E8.1).

20-a95/ 940i7 -02

viu taliure to provice correct .sorK instructions for tne

secondary hydrostatic test (Section E8.2).

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50-395/96009-05

NCV failure to compensate for inoperable fire barriers

(Section F4.1).

50-395/94007-05

IFI correction of fire protection problems involving low

flow to sprinklers and missing sprinklers.

Extra

sprinklers not included in the flow calculation

(Section F8.1).

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Discussed

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None

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