ML20210N940

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Insp Rept 50-395/97-07 on 970615-0726.Violations Noted.Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support
ML20210N940
Person / Time
Site: Summer South Carolina Electric & Gas Company icon.png
Issue date: 08/21/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20210N930 List:
References
50-395-97-07, 50-395-97-7, NUDOCS 9708260196
Download: ML20210N940 (26)


See also: IR 05000395/1997007

Text

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U.-S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket No.: 50 395

-License No.: NPF 12

--Report No.;- 50 395/97 07

Licensee: South Carolina Electric & Gas (SCE&G)

Facility: V. C. Summer Nuclear Station ,

Location: P. O. Box 88

Jenkinsville, SC 29065

Dates: June 15 July 26,1997

Inspectors: B. Bonser Senior Resident Inspector

T. Farnholtz, Resident Inspector

H. Whitener. Reactor Inspector, RII (Sections Hl.2 and H2.1).

Approved by: - G. Belisle, Chief, Reactor Projects Branch 5

Division of Reactor Projects

Enclosure 2

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EXECtRIVE SUltiARY

V. C. Summer Nuclear Station

NRC Integrated Inspection Report No. 50 395/97 07

This integrated inspection included aspects of licensee operations.

maintenance, engineering, and plant support. The report covers a 6 week

period of resident inspection; in addition, it includes the results of an

announced inspection by a regional inspector.

4 Operations

.

A violation was identified for a failure to comply with Technical

Specification (TS) 3.6.4, " Containment Isolation Systems."

Administrative controls were not established prior to opening the A

train hydrogen monitor containment isolation valves to conduct a

calibration (Section 01.2). s

. The bypass authorization program was being conducted in accordance with

the station administrative procedure. The number of bypass

authorizations approved was small (Section 01.3).

.

The tag out of a boron injection flow path was adequately prepared and

implemented and the TS re

available (Section 01.4). quired number of boron in;ection flow paths was

. A walkdown of accessible portions of the A train and B train Diesel

Generator Air Start Systems and the Yard Fire Main System identified no

concerns (Section 02.1).

. Overall material and housekeeping conditions in locked areas of the

Auxiliary Building were good with one exception noted in the letdown

heat exchanger room. Health physics was adequately monitoring

radiological conditions in these arebs (Section 02.2).

.

Lower Auxiliary Building Operator rounds were completed in accordance

with operations guidelines. The operator was knowledgeable of his

, duties and plant conditions (Section 04.1).

.

Establishing a screening committee to review Condition Event Reports

(CER) has given more consistency to the disposition of CERs and benefits

the licensee's self assessment process (Section 07.1).

Maintenance

.

Observed maintenance activities were conducted in accordance with

approved procedures. Properly calibrated equipment, as well as correct

) arts and supplies were used. The technicians performing the work were

(nowledgeable (Section H!.'.).

  • Intermediate Building Sump C, Pump Motor B preventive maintenance

activities were well performed by competent technicians who were

knowledgeable of the assigned tasks (Section Hl.2).

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e Procedures specified valves required to demonstrate boron injection flow

paths, and recently completed valve lineups demonstrated system

operability (Section M2.2),

e During observations of surveillance tests of sev6:al smoke detectors, a

motor driven emergency feedwater pump end valves and a sump pump molded

case circuit breaker, the inspectors observed detailed, concise

procedures, procedural adherence, good planning and good communications

(Section M241).

. The licensee's TS required circuit breaker testing program ensures that

selected groups of breakers will be tested and additional samples will

be taken when a bret.ker in a group fails a tcat (Section M2.3).

EnaineeriD9

e A review of the snubber replacement project identified a violation for a

failure to establish an adequate )rocedure for the installation of

Grinnel type restraints. Althoug1 this issue was licensee identified,-

the licensee missed several opportunities to identify and correct these

procedural deficiencies. Missed op>ortunities included procedure

reviews prior to performing the snu)ber replacement and during the field

installation (Section El.1).

. The licensee's evaluation to allow continued full power operation

following the failure of both reactor compartment cooling fans was >

adequate. The evaluation aas thorough and considered all relevant

aspects of the loss of fx .ed ventilation. Plant response upon

establishing natural circulation ventilatien through the reactor

compartment was as expected (Section E2.U .

. The licensee's modification design package to change the P0 fueling Water

, Storage Tank low level alarm setpoint, associated documents and

indicators was well written and complete. Engineering insttuctions and

supporting documentation were adequate to

complete the modification ($ection E2.2). provide sufficient detail to

A Non cited Violation (NCV) was identified concerning seven inadequate

maintenance and test procedures used to set up the Emergency Feedwater

System flow control valves. Improper set up of these valves resulted in

unbalanced flow to the steam generators following a reactor trip. The

licensee's root cause analysis was adequate (Section E8.1).

Plant Suooort

. A tour of locked high radiation areas ar.d locked rooms in'the Auxiliary

Buildin found that contaminated areas wire kept to a minimum and

Radiolo ical controls were well maintaind (Section R1.1).

  • The results of a monthiy pager drill conducted during the inspection

period were satisfactory. The current call back system provided

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adequate assurance that the required minimum staffing positions would be i

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filled in the event of an actual emergency (Section Pl.1). l

  • The licensee's administrative controls for the use of the biometric hand

readers were effective to prevent unauthorized use (Section S1.1).

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. * The licensee's actions concerning an overpressure condition in multiple ,

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wet pipe sprinkler systems were appropriate. The causes were identified

j and effective interim corrective actions were instituted (Section F2.1).

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Beport Details

Summary of Plant Status

At the beginning of the inspec.:1on period, the plant was operating at or near

full power until July 5 when power was reduced to 97 percent to perform main

turbine valve testing. Later that same day, power was returned to 100

and remained at that level for the remainder of the inspection period. percent

I. Operations

01 Conduct of Operations

01.1 General Comments (71707)

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Using Inspection Procedure 71707, the inspectors condu:ted frequent

reviews of ongoing plant operations. In general, the conduct of

operations was profeuional and safety conscious; specific events and

noteworthy observations are detailed in the sections below.

01.2 Hydroaen Analyzer Containment Isolation Valyas

a. Incoection ScoDe (71707)

The inspectors reviewed the licensee's practice of openir.g the

containment hydrogen monitor Containment Isolation Valves (CIV) during

the conduct of a hydrogen monitor calibration,

b. Observations and Findinas

On June 20 during a routine control board walkdown, the inspectors

identified that the train A containment hydrogen monitor intake and

exhaust line CIVs. SVX 6050A SVX 6051A, SVX 605?.A, and SVX 6053A, were

open. These valves had been opened for a calibration of the hydrogen

monitor. The inspectors questioned whether containment integrity was

adequately maintained with these valves open. The 3/8 inch hydrogen

monitor process lines are opened to the containment atmosphere in order

to sample the post accident environment for hydrogen. During post-

accident operation, the hydrogen monitor atmospheric samples are passed

through the two hydrogen analyzers located in the Auxiliary and Fuel

Handling Buildings and returned to containment.

Valve SVX 6050A receives an automatic containment isolation signal. The

other three CIVs on the A train hydrogen monitor receive no automatic

isolation signal. The automatic isolation feature on SVX 6050A was

added to isolate a containment pressure transmitter sensing line

branching off the hydrogen monitor return line outside containment. All

these valves are operated by hand switches from the main control board.

These remotely operated manual valves are designated as CIVs in the

Final Safety Analysis Report (FSAR).

The hydrogen monitor CIVs were opened as part of a once every refueling

Surveillance Test Procedure (STP). STP 301.004, " Train A Containment

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Hydrogen Monitor Calibration," Revision 2. The licensee told the

inspectors that the valves were normally opened during this surveillance

test and this was a normal practice to conduct this test and open these

CIVs while operating, The licentee completed the surveillance and

closed the hydrogen monitor CIVs. Several days later when the

inspectors questioned the licensee again on this issue, the licensee

issued an internal Operation's memorandum directing operators to ensure

the hydrogen monitor CIVs remain closed pending a review.

The inspectors found that the control room operators were aware of the

testing and had adequately documented that testing was in progress. The

inspectors found that the testing was documented in shift turnover

checklists and the A train hydrogen monitor had been declared inoperable

in an Action Removal and Restoration (R&R) Checklist (R&R #970279)

effective on June 19, at 5:00 a.m.

The inspectors concluded that the licensee had failed to comply with the

action requirements of Technical Specification (TS) 3.6.4 " Containment

Isolation Valves," by failing to implement administrative controls while

the hydrogen monitor CIVs were open during

3.6.4, requires, when in Modes 1 through that 4. plant

each operation

containment (Mode 1).- TS

isolation valve shall be operable. The TS states that locked or sealed

closed valves may be opened on an intermittent basis under

administrative control. The hydrogen monitor CIVs are remotely operated

valves that are not locked closed during normal operation These valves

are provided for containment penetrations and do not com)ly with the

normal isolation provisions of General Design Criteria (GDC) 56,

"Primar

valves,yandContainment

hence fallIsolation," 1.e., automatic

into the category or locked

of a specific classclosed

of lines,

such as instrument lines, that have containment isolation provisions

that are acceptable on some other defined basis. The inspectors

considered that the intent of " sealed closed valves" could be applied to

the-remotely operated hydrogen monitor CIVs.

The bases for TS 3.6.4 states that the administrative controls include

the following considerations: (1) stationing an o mrator, who is in

constant communication with the control room, at tie valve controls. (2)

instructing this o

situation, and (3)rerator to close

assuring these valves in

that environmental an accident

conditions will not

preclude access to close the valves. In this case, the licensee had not

-implemented these or any similar administrative controls.

The inspectors concluded that the licensee failed to comply with TS 3.6.4 by not establishing administrative controls prior to opening the

hydrogen monitor CIVs. The inspectors, therefore, considered the

hydrogen monitor CIVs to be inoperable during the conduct of STP 301.004

on June 20. The inspectors found that these CIVs were open over two

shifts on June 20. The licensee had not documented the exact times

these CIVs were manipulated and could not accurately determine the times

these valves were opened. This surveillance, however, typically takes

eleven to twelve hours to complete. The CIVs were opened early in the

test and closed late in the test.-

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In an accident situation the hydrogen monitor CIV status would be

indicated on the main control board containment isolation light panel.

Early in the response to an event, a control board operator would be

expected to review the status of this panel and close these valves if

they were open.

This failure to comply with the requirements of TS 3.6.4, is identified

as Violation (VIO) 50 395/97007 01.

The inspectors also reviewed the FSAR descri) tion of the hydrogen

monitor and the hydrogen monitor CIVs. The :SAR states that these

valves will be normally closed during plant operation. The design of

the reactor building penetration lines containing the hydrogen monitor

CIVs for both trains was approved in the FSAR under GDC 56. The

hydrogen monitor lines do not meet the specific criteria specified in

GDC 56. GDC 56 states that exceptions to the isolation reauirements are

allowed provided that "it can be demonstrated that the cont'ainment

isolation provisions for a specific class of lines, s'ich as instrument

lines, are acceptable on some other defined basis." The Summer FSAR

provided no basis on which these lines were accepted and no basis for

opening these lines during plant operation.

The inspectors also reviewed the design of the Hydrogen Monitoring

System. Based on a vendor letter dated October 30, 1990, the pressure

boundary for the Hydrogen Monitoring System was defined to end at the

CIVs. The system was designed as a >ost accident system, which would

normally be in a standby mode with tle CIVs closed. Although the system

was built to withstand post Loss of Coolant Accident-(LOCA) temperatures

and pressures the hydrogen monitor can not be considered part of the

primary containment boundary,

c. ConclusiQD1

- A VIO was identified for a failure to comply with TS 3.6.4.

Administrative controls were not established prior to opening the A

train hydrogen monitor CIVs to conduct a calibration.

01.3 Bgylew of Jumoer and lifted Leads Proaram

a. Insoection Scope (71707)

The inspectors reviewed the licensee's bypass authorization controls

established by Station Administrative Procedure (SAP), SAP 148,

" Temporary Bypass, Jumper, and Lifted Lead Control," Revision 8.

b, ObservationsandFindiD91

Procedure SAP 148 ensures that the installation of electrical jumpers

and lifted leads for in service plant equipment will be properly

identified, reviewed, and approved prior to implementation. The

inspectors found that the licensee maintains a small number (three) of

bypass authorizations. The Bypass Authorization Requests reviewed

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complied with the program requirements in SAP 148. The inspectors also

reviewed the initiation, approval. and review by the Plant Safety Review

Committee (PSRC), of a request to juniper out the EHC Electrical

Malfunction annunciator on the main control board. The inspectors were

satisfied that the Bypass Authorization Request was adequately reviewed

and appropriate compensatory actions were taken. The inspectors

concluded that by) ass authorizations were being implemented in

accordance with tle procedure.

c. Conclusions

The bypass authorization program was being conducted in accordance with

the station administrative procedure. The number of bypass

authorizations approved was small.

01.4. Observation of Taa 0ut On Boric Acid Transf2 (BAT) System

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a. Inspection Scope (71707)

The inspectors reviewed and observed a tag.out of the B train BAT system

and verified that there were adequate baron injection flow paths

availabic with this train of boron injection removed from service,

b. Observations and Findinas

On July 2. the inspectors observed an operator hang red tags on several

B train BAT system valves to isolate the B train BXT pump discharge

valve for maintenance. The inspectors also compared the tag out with

the system drawing and concluded that the valve to be repaired was

adequately isolated. The inspectors observed the control roram shift

supervisor brief the control room statf on the remaining boron injection

flow paths. The inspectors reviewed the most recent test

STP 104.003. "Boration System Valve Lineup Verification." procedure.

Revision 5. to

verify the remaining boron injection flow paths had been verified

operable. The inspectors identified no concerns.

c. Conclusions

The inspectors concluded that the tag out of a boron injection flow aath

was adequately prepared and implemented and that the TS required num)er

of boron injection flow paths was available.

02 Operational Status of Facilities and Equipment

02.1 Enaineered Safety Feature System Walkdown (71707)

The inspectors performed a walkdown of accessible portions of the A

train and B train Diesel Generator Air Start Systems and the Yard Fire

Main System. No discrepancies or concerns were identified.

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02.2 Plant Walkdown of Locked Rooms In The Auxiliary Buildina

a. Jnsoection Scope (71707)

The inspectors walked down locked high radiation rooms and locked rooms

in the Auxiliary Building to review material, housekeeping, and

radiological conditions,

b. Observation and Findinas

On July 2, the inspectors, accompanied by a Health Physics (HP)

technician, walked down locked high radiation rooms and other normally

locked areas in the Auxiliary Building. Most of these rooms are not

frequently entered and many contained areas of high radiation or the

potential for high radiation. The HP technician accompanying the

inspectors was familiar with these locked areas and identified to the

inspectors how these areas are routinely monitored. The inspectors

found that contaminated areas were kept to a minimum and overall

equipment material condition and housekeeping were good. The inspectors

identified one exception in the letdown heat exchanger room. In this

room, a high radiation area, there was boron buildu) on the head flange

area of the heat exchanger and on the floor under tw flange.

The inspectors questioned the licensee's monitoring of this leakage

since it had the potential to corrode the flange mating surface and

flange studs and result in greater Reactor Coolant System (RCS) leakage

into the Auxiliary Building. The licensee has delayed repairs to the

heat exchanger since it involves the potential for high radiation

expcsure. The inspectors reviewed a licensee inspection of the heat

exchanger performed in May 1996. The boron was cleaned off the heat

exchanger, a stud was replaced, and a visual inspection identified

noticeable corrosion on the head of the tube sheet. This leakage,

however, has not significantly increased and has not resulted in greater

RCS leakage. The licensee plans to repair the letdown heat exchanger

during the upcoming refueling outage in October.

The inspectors concluded that overall material and housekeeping

conditions in locked areas of the Auxiliary Building were good with one

exception noted in the letdown heat exchanger room. The inspectors also

concluded that HP was adequately monitoring radiological conditions in

these areas.

c. Conclusions

Overall material and housekeeping conditions in locked areas of the

Auxiliary Building were good with one exception noted in the letdown

heat exchanger room. HP was adequately monitoring radiological

conditions in these areas.

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04 Operator Knowledge and Performance

04.1 Lower Auxiliary Buildina Giserator Rounds

a. Insoection Scope (71707)

The inspectors observed the licensee performing Lower Auxiliary Building

Operator rounds,

b. Observations and Findinas

On June 29, the inspectors observed the night shift Lower Auxiliary

Building 0)eratcr recording his TS logs. The log readings were recorded

on a hand leld data entry device. The ins >ectors reviewed the log

readings with the operator as they were tacen. All data taken met

acceptance criteria and channel checks were performed as required by TS.

The inspectors observed that the operator made an effort to observe and

understand all plant conditions going beyond normal log keeping. The

operator also investigated an oil and water leak in the B chiller room.

In addition to the TS rounds, the inspectors observed the operator

>erform System Operating Procedure (SOP), S0P 119, " Waste Gas

)rocessing," Section C. Revision 14. The operator switched gas decay

tanks from Bank A to Bank B.

c. Conclusions

Lower Auxiliary Building Operator rounds were completed in accordance

with Operation's guidelines. The operator was knowledgeable of his

duties and plant conditions.

07 Quality Assurance in Operations

07.1 Condition Event Report (CER) Screenina Meetina

a. JESDection Scone (71707)

The licensee formed a CER screening committee in order to bring more

consistency to the CER review process. The inspectors attended a CER

screening meeting to review the screening process,

b. Observations and Findinas

Due to inconsistencies identified in the CER dis)osition process, the

licensee established a screening committee, whic1 meets several times a

week, to review CERs and to ensure that they receive an appropriate

review and dis)osition. These screening meetings also ensure that CERs

are assigned tie correct cause codes to aid in trending. The inspectors

observed a screening committee meeting and concluded that establishing

this review process has brought more consistency to the disposition of

CERs.

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c. Conclusions

Establishing a screening comittee to review CERs has brought more

consistency to the disposition of CERs and benefits the licensee's

self assessment process.

08- Miscellaneous Operations Issues (92901)

08.1 (Closed) Unresolved Item (URI) 50 395/96007 04: control room meters

reading outside green indication zone. The licensee committed to

completing a modification to instrument meter green bands by

Maren 31, 1997. The purpose of the modification was to change the

placement of the bands such that the metors would read within the green

zone when the parameters were in a normal at power condition. The

modification was performed under Modification Review Forms (MRFs) 90102C

and G.- The inspectors reviewed the MRFs and observed the completed

meter changes in the control room and concluded that the modification

was completed satisfactorily. The modification was completed on

March 26, 1997.

II. Maintenance

M1 Conduct of Maintenance

M1.1 General Comments

a. InSDection Scooe (62707)

The inspectors observed or reviewed all or portions of the following

work activities:

  • Maintenance Work Request (MWR) 9711331. Remove A Diesel Generator

(DG) Heat Exchanger End Covers and Perform Visual Inspection of

Selected Tubes.

  • MWR 9710720, Clean or Replace A DG Lube Oil Strainer.
  • Preventive Maintenance Task Sheet (PMTS) P0211153, A DG Engine

Quarterly Maintenance.

Check.

-- * MWR 9603078, Perform VT Examination on A Component Cooling Water

Pump Support,

b. Observations and Findinas

The inspectors observed the licensee's use of approved procedures,

calibrated equipment, and parts and supplies during the performance of

plant maintenance activities.

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The observed work was conducted in an appropriate manner and the

technicians exhibited a good level of knowledge and expertise regarding

the erk they were performing. No concerns were identified.

c. (20clusions

Observed maintenance activities were conducted in accordance with

approved procedures. Properly calibrated equipment, as well as correct

> arts and supplies were used. The technicians performing the work were

(nowledgeable.

Hl.2 Intermediate Buildina Sumo Puma Motor Preventive Maintenance

a. J.ntoection Scope (62700)

The inspectors reviewed and observed the electrical portions of

Haintenance Work Request / Task Sheet (HWR/TS) 9705447, Preventive

Haintenance Task Sheet (PHTS) P0211021, Perform PH on Sump C, Sump

Pump B Hotor,

b. Observations and Findinas

The insmetors observed portions of the Intermediate Building Sump C,

Pump B iotor preventive maintenance which involved and was performed in

conjunction with the molded case circuit breaker testing in accordance

with procedure EMP 295.004, " Inspection and PM of Electric Hotors."

Revision 9. Activities witnessed included visual inspection of the

breaker, overload reset (three times minimum), gasket material

inspection, and cycling of the breaker (five times minimum). These

activities were adequately performed.

c. Conclusions

Intermediate Building sump motor preventive maintenance activities were

well performed by competent technicians who were knowledgeable of the

assigned tasks.

H2 Maintenance e.nd Haterial Condition of Facilities and Equipment

H2.1 Surveillance Observations

a. Insoection Scone (62700)

The inspectors reviewed or observed all or portions of the following

surveillance tests:

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STP 128.302, " Intermediate Building Pre Action Sprinkler

Operational Test," Revision 11.

  • STP 220.001A. "Hotor Driven En:ergency Feedwater Pump and Valve

Test," Revision 5.

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STP 508.003, "Holded Case Circuit Breaker Testing," Revision 8.

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b. Observations and Findinas

The inspectors observed the actuation of smoke detectors in the field.

The licensee used a test gas to simulate smoke at the detectors.

Observations were made in the field to verify that the detectors

actuated and then reset when the gas dissipated. The inspectors also

verified that the Simplex Graphics Monitor in the control room

identificd the detector and its location and status. Communication

between the control room and the fiele, was maintained, test personnel

were knowledgeable of the system. and test procedure STP 128.302 was

followed in performance of the test.

The inspectors observed the pre job briefing and test performance of-

Motor Driven Emergency Feedwater Pump A in accordance with procedure

STP 220.001A. The following activities were observed and determined to

be satisfactory:

. Recording as found conditions.

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Installation of calibrated test instrumentation.

.- Valve alignment to recirculation flow path.

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. Pump start and operation from the control room.

. Adjustment of flow to the reference value.

. Recording measured pump parameters and vibrations.

. Verification of check valve operability.

Test group personnel were knowledgeable of the procedure and the system.

The test was performed in a competent and professional manner.

The inspectors observed the testing of the molded case circuit breaker

for Intermediate Building Sump C, Puap B. This testing was performed in

the electt ical shop by procedure STP 508.003. The breaker was

disassembled, inspected, cleaned and meggered. In addition, the breaker

contacts were replaced and the trip setpoints were adjusted und tested.

The procedure specified acceptable ranges, torque values, and lifted

wire data sheets. The technicians were knowledgeable of the assigned

task and used appropriate safety precautions,

c. Conclusions

During observations of surveillance. tests of several smoke detectors, a

motor driven emergency feedwater pump and valves and a sump pump molded

case circuit breaker, the inspectors observed detailed, concise

procedures, procedural adherence, good planning and good communications.

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H2.2 Boration System Valve lineuo Verification

a. Inspection Scooe (61726)

The inspectors reviewed surveillance procedure STP 104.003, "Boration

System Valve Lineup Verification," Revision 5 to verify that it included

all the required valves to demonstrate operability of the boron

injection flow paths required in Mode 1.

b. Observations and Findinas

The inspectors reviewed STP 104.003 with the system drawings and found

that the surveillance procedure included all the valves required to

demonstrate operability of the boron in,1ection flow paths. The

inspectors also reviewed recent boration system valve lineups to verify

that they were completed satisfactorily,

c. Conclusioni

The inspectors verified that-procedures specified valves required to

demonstrate boron injection flow paths, and recently completed valve

lineups demonstrated system operability.

H2.3 Circuit Breaker Surveillance Testina

a. Insoection Scope (61726)

The inspectors reviewed the licensee's program for TS required circuit

breaker surveillance testing.

b. Observations and Findinas

On June 26, breaker XHCIC3X 51JL failed to meet the acceptance criteria

for instantaneous overcurrent trip on surveillance test STP 508.003,

"Holded Case Circuit Breaker Testing," Revision 8. The breaker was

replaced and returned to service. The inspectors reviewed the

licensee's program for compliance with TS 4.8.4.3, " Circuit Protection

Devices." The TS requires that for each circuit breaker found

inoperable, an addition'1 representative sample of at least ten percent

of all the circuit breakers of the inoperable type shall also be

functionally tested until no more failures are found or all circuit

breakers of that type have been functionally tested.

The inspectors found that the licensee had separated the breakers to be

tested into groups and monitored the testing of breakers in each group

to ensure each breaker was tested on a rotating basis. The inspectors

also found that when a breaker test failure occurred, an additional

sample was taken as required.

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c. Cenclusions

The inspectors concluded that the licensee's breaker testing program

ensured that selected groups of breakers would be tested and additional

samples would be taken when a breaker in a group fails a test.

III. Enaineerina

El Conduct of Engineering

E1.1 Snubber Removal /Reclacement Pro.iect

a. Inspection Scoce (37551)

ectors reviewed the licensee's on line snubber

The insp/ replacement project.

removal The inspectors observed a snubber removal

and replacement with a strut, reviewed the modification )ackage, and the

licensee's guidance and controls fer implementation of tie project,

b. Observations and Findinos

During the inspection period, the licensee im)lemented the on line phase

of their snubber reduction project. The snub >er reductions occurred in

two manners, either specified snubbers were removed or specified

snubbers were removed and were replaced with struts.

The inspectors reviewed the licensee's evaluation of system operability

during the transition between the-two piping analyses that applied while

the project was in progress. There was an original analysis for the

snubbers in place before the snubber reduction project began and an

analysis for the completed project that included the snubbers that were

replaced with struts and/or removed. There was no specific analysis for

the transition between the two analysis. The licensee's review

concluded that the seismic qualification of the systems being modified

would not be degraded below what was minimally acceptable to maintain

compliance with American Society of Hechanical Engineers Code criteria

during the temporary configurations created by the snubber removal

project. The inspectors reviewed the licensee's evaluation and

concluded that the licensee had adequately estat,lished that system

operability during these system transitions would be maintained.

The inspectors found that the licensee had established clear operational

guidelines for the snubber reduction project through a Station Order.

The first items worked on a specific system were snubber removals.

During this phase the system was considered operable. When a snubber

was re) laced with a strut. Operations declared the system inoperable

until Engineering provided Operations with evidence that the work was

complete and that the system configuration was in accordance with the

modifict. tion specifications.

_ _ _ _ _ _ _ _ .

'

.

1

12

On June 26, the inspectors observed a snLbber to strut replacement on

safety related su) port MK CSH 1494 on the Chemical and Volume Control

System (CVCS). T11s was the first snubber to strut replacement

performed. The inspectors observed the conduct of the work and

discussed the modification with the design engineer during the snubber

replacement. The work was completed under MWR 9707569 and performed

using Mechanical Maintenance Procedure. MMP 305.004, " Installation,

Removal, Rework and Reinstallation of Pipe Supports," Revision 5, and

MRF 223528 " Snubber Reduction for CVCS System." The inspectors had no

questions and concluded that the strut was installed correctly.

On July 10, during a review of MWR 9707569 the licensee identified an

inconsistency between the steps in the body of

the sign off steps in the proceduce data sheet.The procedure procedureMMP

data 305.004 and

sheet did not require that the strut movement tolerance measurements

specified in step 7.12.8.C be documented. The licensee's investigation

found that the step had been completed but not specifically documented.

An engineering review of the step determined that documentation was not

necessary based on other verifications performed in the procedure.

A further review of the procedure and other completed work documentation

by the licensee identified that MMP 305.004 had not been adequately

revised to reflect specific installation requirements for Grinnel type

restraints. The original modification package had been prepared using

Bergen Paterson restraints. The MRF was later revised to use Grinnel

restraints. A review of the procedure had not been performed to ensure

that the different installation requirements were included in the

procedure. The procedural discrepancies identified included: Step

7.12.9 of INP 305.004 required verification of less than a four degree

angular tolerance between the structural attachment and the pipe

attachment. The MRF for the Grinnel restraints required a maximum three

degree-angalar tolerance. Step 7.12.11 re

to-torque values given in Enclosure 10.4. quired torquing

The torque the locknuts

schedule given in

Enclosure 10.4 was for Bergen Paterson type restraints. The Grinnel

restraints required hand tightening plus 1/8 of a turn.

When these )rocedural issues were identified, the licensee immediately

stopped wor ( on the snubber replacement project until the hardware and

procedural issues were resolved. 1he licensee verified in the field

-

that the two Grinnel restraints installed were installed correctly. The

licensee also revised HMP 305.004 to reflect-the MRF requirements for

the Grinnel type restraints. A root cause evaluation team was also

established to determine the causes of this problem.

The ins >ectors' review of this issue with the licensee concluded that

althoug1 a deficient procedure had been used, the restraints were

installed correctly. The technicians performing the snubber

re)lacements were aware of the correct installation requirements in the

MR: and had noted the specific Grinnel restraint installation

requirements on the procedure data sheet. The technicians, however, had

not followed procedure adherence requirements by failing to revise the

procedure before proceeding with restraint installation.

._ _ _. _

I .

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13

The inspectors concluded that procedure HMP 305.004 was inadequate in

that it did not include all the specific requirements for installation

of the Grinnel type restraints. The procedure had not received the

appropriate interface review prior to implementing the snubber

replacement. The inspectors also concluded that the technicians

prforming the restraint installation had not followed SAP 139.

Procedure Development, Review, Approval and Control," Revision 17, in

that they had not corrected the discrepan ios in procedure MMP 305.004

prior to performing the Grinnel restraint installation. A quality

control ins)ector raised a question on HMP 305.004 which resulted in the

review of t1e snubber replacement project.

The failure to establish an adequate procedure for the installation

of the Grinnel type restraints is identified as a VIO. The inspectors

concluded that although this issue was licensee identified, the licensee

had missed several opportunities during the process to implement this

modification to identify and correct the procedural deficiencies.

These included procedure reviews prior to performing the snubber

replacement and during installation in the field. This is identified

as VIO 50 395/97007 02.

c. Cpnclusions

A review of the snubber replacement project identified a VIO for a

failure to establir.h an adequate procedure for the installation of

Grinnel type restraints. Although this issue was licensee identified,

the licensee had missed several o)portunities to identify and correct

these procedural deficiencies. T1e missed op)ortunities included

procedure reviews prior to >erforming the snu)ber replacement and during

the field-installation by tie technicians.

E2 Engineering Support of Facilities and Equipment

E2.1 Evaluation oi' the Failure of Reactor comoartment Coolino Fans

a. Insoection Scooe (37551)

The inspectors reviewed an engineering evaluation performed to allow

continued operation of the 31 ant following the failure of both reactor

compartment cooling fans, X N00009A and B.

b. Observations and Findinas

Early into the present operating cycle (May 1996), the motor on reactor

compartment cooling fan XFN00009A failed. The two reactor compartment

cooling fans XFN00009A and B are each 100 percent capacity cooling fans

which provide forced ventilation to the compartments surrounding the

reactor vessel. Witt, the A fan failed, the 8 fan was able to provide

the required forced cooling with the plant operating at 100 )ercent

power. On July 11, high vibration alarms were received on tle B fan and

the fan was shut down.

_ _ _ _ _ _ _ _ _ _ _ _

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

.

14

In July 1996, the licentee evaluated the consequences of a loss of

forced ventilation to the reactor compartment during full power

,

operation. The evaluation considered the design basis functional areas

of average Reactor Building temperature, concrete temperature, and

environmental qualification of nuclear instrumentation. In addition,

the evaluation addressed flooding, fire, hot gaps, and the accuracy of

the power range nuclear detectors.

The licensee's evaluation concluded that the design basis functions of

the Reactor Building Cooling and Filtering System would continue to be

met following the loss of both reactor compartment cooling fans provided

that natural circulation ventilation was established through the reactor

compartment. The average Reactor Building temperature wou~.1 remain

below the maximum of 120*F since the cooling fans only circulate reactor

compartment air and do not provide any cooling ef fect. The calculated

temperature of the concrete inside the reactor cavity would exceed the

150'F design limit in the area of the reactor support steel. However,

an associated calculation assumed a 200"F temperature in this area. The

nuclear instrumentation was evaluated to remain operable if natural

circulation ventilation was established within 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br />. This would

ensure that the instruments would not be exposed to temperatures greater

than 200'F. The inspectors reviewed the details of the analysis and

concluded that the supporting arguments were reasonable and addressed

the concerns adequately.

As described above, the design basis functions would continue to be met

provided that natural circulation ventilation was established through

the reactor compartment. This would be achieved by opening the door to

the incore instrument chase within 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br /> of the loss of forced

cooling. The licensee's evaluation considered the consequences of 4

Vlooding and fire with this door open.

On July 11, the licensee made a Reactor Building entry to establish

natural circulation ventilation in the reactor vessel comaartments. The

inspectors reviewed computer generated plots for incore clase area

temperatures, nuclear detector instrument response, and quadrant power

tilt ratios. These plots spanned a time frame from the day before fan

XFN00009B was shut down to several days after the fan was shut down and

the incore instrument chase door was opened. The incore chase area

temperature response was as expected with the equilibrium temperature on

natural circulation reactor building cooling actually slightly lower

than with forced cooling. The plots showed a slight decrease in the

power range detector response with the N42 instrument showing the

largest change. The N42 instrument, located closest to the incore

instrument ch8se door, realized the largest temperature change upon

establishing natural circulation ventilation. The change in detector

output was less than one percent and was relatively stable as predicted.

Using a heat balance, nuclear instrumentation was adjusted to compensate

for this effect. The inspectors had no concerns with the plant

response.

.

, .

,

15  ;

c. Conclusions

The licensee's evaluation to allow continued full power operation

'

l following the failure of both reactor compartment cooling fans was

adequate. The evaluation was thorough and considered all relevant

aspects of the loss of forced cooling. Plant response upon e tab 11shing

, natural circulation ventilatio'1 through the reactor compartment was as

. expected.

l E2.2 Refuelina Water Storaoe Tank (RWST) Level Setooint Change

a. Insoection Scooe (3755D

The inspectors reviewed a plant modification design package to change

,

the RWST low level alarm setpoint from 90 percent to 93 percent,

b. Observations and Findinas

To account for measure n nt error, the licensee changed the TS

surveillance log limit for RWST minimum icvel from 88 percent to 91

percent. The previous setting for the RWST low level alarm was 90

percent which was below the new TS log minimum level. To maintain the

function of this alarm, the alarm setpoint was increased to 93 percent

'

using Engineering Change Request (ECR) 50033. This would provide an

anticipatory alarm (two percent above the TS log minimum) to allow time

for plant operators to correct the condition before entering a TS

required action. In addition. ECR 50033 changed the color labeling on
the main control board indicators for RWST level to provide a blue

.

indicator at 91 percent to correspond to the TS log minimum limit and  !

changed the green band to 91 to 100 percent-to reflect the new

conditions.

2

The inspectors reviewed the ECR and the associated 10 CFR 50.59

screening review form and concluded that they contained all pertinent

information to make the modification. All affected documents and

procedures were identified which would require revision including STPs.

annunciator response procedures, and integrated plant computer system

changes. The design package also included sufficiently detailed

<

engineering instructions for performing the required modifications. The

inspectors identified no concerns with the ECR.

c. Conclusions

,

i The licensee's modification design package to change the RWST low level

.

'

alarm setpoint, associated documents and indicators was well written and

complete. Engineering instructions and supporting-documentation were

adequate to provide sufficient detail to complete the modification.

.

L

w 4 - - .. ,, ,r , < , . , - ,3 -~m-- v---- c m---- m,- w,_,- , - - - - - - ,- <-- e e - - w,--

- _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _

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16

E7 Quality Assurance in Engineering Activities (37551)

E7.1 Review of Updated Final Safety Analysis Report (UFSAR) Commitments

A recent discovery of a licensee o>erating their facility in a manner

contrary to the UFSAR description lighlighted the need for a special

focused review that compared plant practices, procedures and/or

parameters to the UFSAR description. While performing the inspections

discussed in this resort, the inspectors reviewed the applicable

portions of the UFSAl that related to the areas inspected. No

discrepancies were identified.

E8 Hiscellaneous Engineering Issues (92903)

E8.1 1Clqted) URI 50 395/97003 05: evaluation of high Emergency Feedwater

(EFW) System differential flow rates. As described in NRC Integrated

Inspection Report (IIR) 50 395/97003, the licensee identified a larger

than expected differential in EFW flows to each Steam Generator (SG)

upon automatic actuation of EFW following a reactor trip on April 22,

1997. This condition was corrected prior to start up of the plant end

the inspectors had no concerns with the as left condition of the EFW

system. A subsequent consequence analysis was completed and reviewed in

NRC IIR 50 395/97005. This analysis concluded that the as found

condition of the EFW system would not have )roduced a condition which

was outside of the plant's design basis. T1e licensee completed a root

cause analysis on August 4 to determine how the EFW system had been left

in a condition that provided unbalanced flow to the three SGs. The

inspectors reviewed the analysis and the proposed corrective actions.

The cause of the flow imbalance was identified as incorrect stroke

length on the EFW flow control valves. These valves are three inch,

normally open, air operated globe valves. Adjustable mechanical stops

are used to limit the opening stroke length of the stem which in turn

limits the flow rate through the valve. The valves were left in the

incorrect condition following maintenance which did not include

verification of proper valvo set up. The analysis identified seven

maintenance and test procedures that were used on the EFW flow control

valves which did not adequately address the proper set up or testing

of the valves. Specifically, HMP 300.021. " Type 657 Actuators,"

Revision 6, contained instructions on replacement of the valve operator

diaphragm but did not recognize that this replacement could affect the

valve stroke length and did not verify stroke length following diaphragm

replacement. In addition, the following procedures did not recognize

that full stroke of the actuator may not include all available stroke

and did not address the need to verify full stroke in both normal and

emergency modes:

  • Instrumentation and Control Procedure (ICP) 195.010. "Emergcacy FW

to Stm Gen. A IFT03531," Revision 7.

  • ICP 195.011 " Emergency FW to Stm Gen. B Flow IFT03541

Calibration," Revision 8.

. . . . . . . . .

___ _ __

'

.

f 17

. ICP 195.012, * Emergency FW to Stm Gen. C Flow IFT03551

Calibration," Revision 6.

. STP 396.001, " Emergency FW to Steam Generator "A" Flow Instrument

(IFT03561) Calibration," Revision 4.

. STP 396.002. " Emergency FW to Steam Generator "B" Flow Instrument

(IFT03571) Calibration," Revision 4.

(IFT03581) Calibration," Revision 4.

The licensee's corrective actions as described in the root cause

analysis report included revising the design basis document and

supporting design documents to establish an EFW flow balance criteria

and performing the required analysis for the procedure revisions. The

corrective actions also included establishing allowable tolerances for

the set up of the flow control valves, and incorporating the tolerances

and the as found and as left stroke length measurements into the revised

procedures. In addition, a new procedure would be generated to perform

a flow balance test. The inspectors considered these actions adequate

to provide the necessary guidance to properly set up the EFW flow

control valves and to prevent a similar differential flow balance

condition. The inspectors considered the licensees' root cause analysis

to be adequate.

The failure to provide adequate maintenance and testing procedures to

maintain proper set up of the EFW flow control valves is identified as a

violation. This non repetitive, licensee identified and corrected

vinlation is being treated as a Non cited Violation (NCV) consistent

with Section VII.B.1 of the NRC Enforcement Policy. This is identified

as NCV 50 395/97007 03.

JL Plant Support

R1 Radiological Protection and Chemistry (RP&C) Controls

R1.1 General Comments

The inspectors observed radiological controls during the conduct of

tours and observation of maintenance activities and found them to be

acceptable. The inspectors observed during a tour of locked high

radiation areas and locked rooms in the Auxiliary Building that

' contaminated areas were kept to a minimum and radiological controls were

well maintained.

I

_ _ - _

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18

P1 Conduct of Emergency Preparedness (EP) Activities

Pl.1 Radio Paoer Drill

a, Insoection Scope (71750)

The inspectors reviewed the results of a radio pager drill conducted by

the licensee on June 10.

b. Observations and Findinas

On June 10, the licensee conducted a monthly pager drill designed to

test the ability of the pager system to reach the Emergency Response

Organization (ER0) members after hours and away from the site and to

test the ability of the ERO members to receive the page. The test

results indicated that 82 percent of the available members responded.

This constituted a satisfactory drill (greater than 80 percent response

is considered satisfactory) although a higher percentage is normally

expected. All positions required for minimum staffing were filled.

Several positions not required for minimum staffing were not filled.

Available licensee personnel who carry ERO pagers (approximately 200)

are required to respond to a page within one hour by calling a 1 800

number to connect to the Emergency Response Organization Notification

System computer. As an alternative, members may call a member of the

emergency response group and leave a voice mail message to acknowledge

the page. The resmnse is then correlated and tabulated by position and

the results publisled in a remrt. The inspectors considered these

expectations reasonable and t1at the call back system provided

acceptable assurance that the minimum required positions would be filled

in the event of a real emergency,

c. Conclusions

The results of a monthly pager drill conducted during the inspection

period were satisfactory. The current call back system prolided

adeguate assurance that the required minimum staffing positions would be

filled in the event of an actual emergency.

Pl.2 EP Drills 31750)

The inspectors observed a practice EP drill on June 18 which was

conducted in preparation for the scheduled biannual drill conducted in

July. Observations were made from the simulated control room, the

Emergency Operations Facility and the Technical Support Center. No

concerns were identified.

The inspectors observed portions of the biannual EP drill conducted on

July 16. Details of this exercise along with observations and

conclusions are documented in NRC IIR 50 395/97010.

. _ . . _ _ _ _ . __ _ _ _ _ _ _ _ _ _ _ _ - _

.

19

S1 Conduct of Security and Safeguards Activities

S1.1 Access to the Protected Area Usino left Hand

a. Inspection Scooe (71750)

The inspectors reviewed the acceptability of a licensee employee gaining

access to the >rotected area using the left hand inserted palm up into

the biometric land reader.

b. Observations and Findinas

On July 1, the ins)ectors observed a licensee employee using the left

hand, palm up in t1e biometric hand reader to gain access to the

protected area. It was not obvious to the inspectors why the employee

could not use the right hand, palm down in the hand reader as would

normally be expected. The inspectors auestioned the licensee about this

)ractice and were informed that two people were authorized to use the

land reader in this fashion. One person was missing a finger on the

right hand such that the associated peg in the hand reader could not be

properly engaged and the other had been exposed to >oison ivy and was

experiencing swelling in his right hand such that t1e hand reader may .

not allow access. The ins

'

exposed to the poison ivy.pectors The licenseehad demonstrated

observed thethat

person that had been

acceptable

administrative controls were in place to prevent unauthorized use of the

hand readers but that some flexibility could be used when necessary,

c. Conclusions

The licensee's administrative controls for the use of the biometric hand

readers were effective to prevent unauthorized use but still provide

reasonable flexibility when necessary. Two plant employees were

authorized to use the hand readers in a manner other than the normally

used method.

F2 Status of Fire Protection Facilities and Equipment

F2.1 Wet Pioe Sorinkler System Pressures

a. Insoection Scope (71750)

The inspectors reviewed the licensee's actions regarding an overpressure

condition in several non safety related wet pipe sprinkler systems in

the Turbine Building and the Control Building.

b. Observations and Findinas

On July 26. the licensee identified an overpressure condition in three

wet pipe sprinkler systems servicing the Turbine Building and the

Control Building. The normal pressure in these systems was 125 psig.

The observed pressure on the installed pressure instruments for these

three systems ranged from 200 to 285 psig. The fire protection system

_ _ _ _ _ _ _ - _ _ - _

_. __ __ _.

'

.

20

engineer walked down the remainder of the wet pipe systems and

identified several others which were pressurized in excess of their

working pressure.

The cause of the overpressure condition was identified as pressure

surges and fluctuations in the supply pipe which trap water on the

downstream side of clapper valves installed in each individual system.

The system pressure increases with repeated pressure surges since there

were no provisions made to relieve the pressure. Also, high ambient

temperatures were identified as contributing to the condition which tend

f

to increase system pressure as the trapped water temperature increases.

The licensee did not identify any operability con wns with the observed

condition after walking down the entire Fire Protection System. No

I.

system leaks or other damage were noted. The overpressure condition was

corrected by relieving system pressure through manual valves. Six wet

pipe sprinkler systems were placed on a periodic monitoring schedule

with instructions to the operators to manually relieve system pressure

when it reached 175 psig. System pressure was to be lowered to 135

psig.

The inspectors did not identify any concerns regarding the licensee's

actions. The system engineer appeared to understand the causes and was

pursuing long term corrective actions.

c. Conclusions

The licensee's actions concerning an overpressure condition in multiple

wet pipe sprinkler systems were appropriate. The causes were

established and effective interim corrective actions were instituted.

V. Manaaement Meetinos

X1 Exit Meeting Summary

The inspectors ) resented the inspection results to members of licensee

management at t1e conclusion of the inspection on July 30, 1997. The

licensee acknowledged the findings presented.

The inspectors asked the licensee whether any materials examined during

the inspection should be considered proprietary. No proprietary

information was identified.

i

.

21

PARTIAL LIST OF PERSONS CONTACTED

Licensee

F. Bacon, Manager, Chemistr Services

L. Blue, Manager, Health Ph sics and Radwaste

S. Byrne, General Manager, uclear Plant Operations

R. Clary, Manager. Quality Systems

C. Fields Manager, Materials and Procurement

M. Fowlkes. Manager, Operations

S. Furstenberg, Manager. Maintenance Services

D. Lavigne, General Manager, Nuclear Support Services

G. Moffatt, Manager, Design Engineering

K. Nettles, General Manager, Strategic Planning and Development

H. O'Quinn, Manager, Nuclear Frotection Services

A. Rice, Manager Nuclear Licensing and Operating Experience

G. Taylor, V'.ce President Nuclear Operations.

R.-Waselus. Manager, Systems and Component Engineering

R. White, Nuclear Coordinator, South Carolina Public Service Authority

B. Williams, General Manager, Engineering Services

G. Williams, Associate Manager, Operations

.

... .

. . . . .

.. ..

. _ - - _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _

4

22

INSPECTION PROCEDURES USED

IP 37551: Onsite Engineering

IP 61726: Surveillance Observations

IP 62707: Maintenance Observations

IP 71707: Plant Operations

IP 71750: Plant Support Activities

IP 92901: Followup Plant Operations

IP 92903: Followup Engineering

ITEMS OPENED AND CLOSED

Opened

50 395/97007 01 VIO failure to comply with requirements of TS 3.6.4,

containment isolation valves (Section 01.2).

50 395/97007 02 VIO inadequate procedure for snubber replacement

(Section E1.1).

50 395/97007 03 NCV failure to provide adequate maintenance and

testing procedures to maintain proper set up of

the EFW flow control valves (Section E8.1).

ClQied

50 395/96007 04 URI control room meters reading outside green

indication zone (Section 08.1).

50 395/97003 05 URI evaluation of high Emergency Feedwater System

differential flow rates (Section E8.1).

'

50 395/97007 03 NCV failure to provide adequate maintenance and

testing procedures to maintain proper set u

the EFW flow control valves (Section E8.1).p of

.

.mm&