ML20216C668

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Insp Rept 50-395/98-02 on 980222-0404.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support
ML20216C668
Person / Time
Site: Summer South Carolina Electric & Gas Company icon.png
Issue date: 05/04/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20216C650 List:
References
50-395-98-02, 50-395-98-2, NUDOCS 9805190380
Download: ML20216C668 (25)


See also: IR 05000395/1998002

Text

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U. S. NUCLEAR REGULATORY COMMISSION

REGION II

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. Report No.: 50-395/98-02

Licensee: South Carolina Electric & Gas (SCE&G)-

Facility: V. C. Summer Nuclear Station

Location: P. O. Box 88 I

Jenkinsville. SC 29065

Dates: February 22 - April 4,1998

Inspectors: B Bonser Senior Resident Inspector

T. Farnholtz, Resident Inspector

W. Stansberry, Reactor Inspector RII (Sections S2.1, S4.1.

S4.2 S6.1, S6.2. S6.3 and S7.1)

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Approved by: R. C. Haag, Chief Reactor Projects Branch 5

Division of Reactor Projects

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9805190380 980504

PDR ADOCK 05000395

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EXECUTIVE SUMMARY

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V. C. Summer Nuclear Station 1

NRC Inspection Report No. 50-395/98-02

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This integrated inspection included aspects of licensee operations.

j maintenance, engineering, and plant support. The report covers a six-week

t period of resident inspection: in addition, it includes the results of an

j announced inspection by a regional inspector.

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l Ooerations

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. Operators acted promptly in response to a deaerator relief valve lifting

l and prevented a more significant challenge to plant operation (Section )

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01.2). j

e A review of four admistrative control programs implemented by Operations

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identified inattention to or lack of awareness of administrative control l

details in three of the programs. The specific examples were
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recognizing an engineering evaluation should have been updated when the

work scope changed: not caution tagging three non-safety related valves;

and. not revising an operating administrative procedure when painting

criteria were revised (Section 01.3).

. Compensatory actions for an emergency feedwater isolation issue were

satisfactorily implemented (Section 01.4).

l . The knowledge level and performance of the intermediate building

i operator during routine rounds were good. The observed diesel generator

l compensatory actions were effective to ensure diesel operability. The

( observed scope of the o)erator rounds was effective to ensure that

l potential equipment pro)lems were identified (Section 04.1).

e A review of the V. C. Summer Institute For Nuclear Power Operations

! report concluded that the content of tne report was consistent with

recent NRC assessments of licensee performance (Section 08.3).

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Maintenance

e ' Observed maintenance on a component cooling water pump. a molded case

circuit breaker. and a diesel generator identified no concerns. Good

work practices and techniques were noted (Section M1.1).

! . Surveillance activities were conducted satisfactorily and in accordance

with applicable procedures. Good planning for the tests was evident and

communications during the tests were effective (Section M1.2).

. A pre-job briefing for a moisture se)arator reheater performance test

I was thorough, clear. and detailed. Expected plant response was

discussed (Section M1.3).

maintenance was performed adequately. A review of maintenance

procedures for similar RCP seal water flow transmitters identified

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procedures of significantly different ages. Although the older revision

was performed adequately the inspectors considered it a poor practice to

not revise all applicable procedures together (Section M3.1).

  • A licensee assessment and failure cause determination reports of four

previous diesel generator failures adequately identified the root causes

and corrective action (Section M8.2).

Enaineerina

e An engineering evaluation to allow gagging a secondary plant deaerator

relief valve in the closed position and to allow raising the setpoint of

a second deaerator relief valve was technically adequate

(Section E1.1).

  • An unresolved item was identified to assess the safety significance of

raising turbine first stage pressure during moisture seaarator reheater

testing on steam line isolation actuation setpoints. T11s was not

addressed in the se"ety evaluation for the test (Section E1.2).

Plant Sucoort

e A violation was identified for the failure of a security officer to

prevent access to a vehicle until the vehicle search was completed.

(Section S2.1).

  • Security personnel possessed appropriate knowledge to carry out their

assigned duties and responsibilities, including response procedures, use

of deadly force, and armed response tactics (Section S4.1).

  • The security organization's response capability to security threats,

contingencies, and routine response situations including drills, were

consistent with the security procedures and the approved Physical

Security Plan and the Safeguards Contingency Plan (Section S4.2).

  • Management support for the security program was generally strong. A

notable exception to this support was compensatory measures remaining in

place for two years (Section S6.1).

  • Management's administration of the security program was proactive and

effective (Section S6.2).

. The total number of trained security officers and armed personnel

immediately available to fulfill response requirements met Physical

Security Plan requirements. One full-time member of the security

organization who had the authority to direct security activities did not

have duties that conflicted with the assignment to direct all activities

during an incident (Section S6.3).

.- Overall the licensee was effective in identifying analyzing, and

resolving security related problems. The adequacy of corrective actions

to prevent recurring problems was found to be excellent. There were

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strengths in the maintenance program of the security equipment and

system that supported plant operations and safety. The licensee was

aware of the weakness in the security system due to aging equipment that

could eventually lead to system degradation (Section S7.1). j

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Reoort Details

Summary of Plant Status

Unit 1 began this inspectir,n period at 100 percent power. On March 8 power

was reduced to 94 percent to reseat a deaerator relief valve. On March 14,

power was returned to 100 percent following completion of maintenance on the

deaerator relief valves. On April 4. power was reduced to 87 percent for main

steam safety valve (MSSV) testing. Power was returned to 100 percent l

following completion of MSSV testing on April 4. l

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I. Operations j

01 Conduct of Operations

01.1 General Comments (71707)

Using Inspection Procedure 71707, the inspectors conducted frequent

reviews of ongoing plant operations. In general, the conduct of

operations was professional and safety-conscious; specific events and

noteworthy observations are detailed in the sections below. l

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01.2 Resoonse To Deaerator Relief Valve Liftina

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a. Jnsgection Scooe (71707)

The inspectors reviewed the response by operators to a deaerator relief j

valve lifting on March 8. j

b. Observations and Findinas

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At about 8:58 a.m. on March 8. the intermediate building auxiliary {

operator, while on rounds, notified the control room that it appeared a l

deaerator (DA) alief valve was lifting. It was confirmed that DA i

relief valve XVa-2252A-HV was lifting. Control room operators also i

observed a corresponding decrease in DA level. In order to reduce i

pressure in the DA and reseat the relief valve the shift supervisor  !

directed a power reduction. During the aower reduction. DA relief valve

XVR-22528-HV also started to lift. At a]out 9:20 a.m.. both relief

valves reseated. At 9:35 a.m. the power reduction was stopped and  ;

power was stabilized at 94 percent. i

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The DA system is pressurized by the condensate pumps and provides i

sufficient head to meet the net positive suction head requirements for )

the feedwater booster pumps during steady-state operation. The prompt '

action by operators to reduce pressure in the DA prevented a loss of DA j

level control and a potential challenge to plant operation.

l c. Conclusions  !

Operators acted promptly in response to a deaerator relief valve lifting

and prevented a more significant challenge to plant operation. l

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01.3-Review of Ooerations Administrative Controls

! a. Insoection Scooe (71707)

The inspectors reviewed several operations administrative control

programs, i

b. Observations and Findinas

Control of Temocrary Eauioment

On March 10. 1998, the licensee generated Work Request (WR) 9805330 to

install temporary demineralizers on the 412 foot level of the

intermediate building to facilitate draining chromated water from the B

Component Cooling Water (CCW) pump to re) lace the outboard seal. An

engineering evaluation was attached to t1e Removal and Restoration (R&R)

form to support the installation of the demineralizers. The evaluation

was written for work on the B CCW pump and included considerations such

as floor loading, impact on essential equipment, fire concerns, and

flooding concerns. The B CCW pump work was completed, and the p_ ump was )

tested and declared operable on March 11.

The licensee determined that similar seal replacement work would be

3erformed on another CCW pump within a short time frame and elected to

cee) the demineralizers in place beyond the completion of the B CCW aump

wort. A revision to WR 9805330 was made to take out references to t1e

B CCW pump and to make it generic to include all CCW pumps. The

associated R&R remained in effect but personnel failed to identify that

the supporting engineering evaluation should be updated to consider the

increased time that the demineralizers would be in place. This

oversight was discussed with cognizant ]ersonnel. An updated

engineering evaluation was prepared. T1e results of the evaluation were 1

the same. The requirement in Operations Administrative Procedure (OAP)-

111.1 to have a R&R to track the demineralizer installation and removal

was satisfied. However, operations demonstrated an inattention to

administrative controls in not recognizing that the supporting

engineering evaluation did not address the most current demineralizer 1

application.

Eauioment Misalianment Control

On March 18, the inspectors reviewed the equipment misalignment status

and monthly misalignment audits. Equipment is allowed to be misaligned

under specific guidelines given in OAP-105.2 " Equipment Misalignment

Procedure." Revision 1. The purpose of the procedure is to allow short

term misalignment of equipment and ensure proper configuration control.

A review of the status log found that there was no listed misaligned

i equipment on the day of the review. The procedure requires that

equipment exceeding 30 days of misalignment shall be evaluated for

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continued misalignment. If continued misalignment is required, a '

i Caution Tagout shall be issued and the item (s) removed from the

l Equipment Misalignment Status Log. The inspectors review of 30 day

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-evaluations for January, February, and March of 1998 identified that

three valves. XVT00127A-AR. XVT001278-AR and XVT00127C-AR. had been

l misaligned since December 16. 1997. These three non-safety related

valves were on the Condenser Air Removal system. The three misalignment

! evaluations the inspectors reviewed identified the misaligned valves but

did not caution tag the valves. On March 16 the licensee identified the

oversight and caution tagged the three valves. Since regulatory

requirements were not applicable to configuration control of these three

l valves, no violation occurred. However, since the same equipment

misalignment controls were used for both safety and non-safety related

ecuipment, the inspectors were concerned that future similar

acministrative oversights, if not corrected, could result in problems

controlling safety-related equipment. When the inspectors identified

this concern to the licensee, a Condition Evaluation Report (CER) 98-

0256 was prepared documenting the oversight. This was the second

example of operation's inattention to administrative controls.

Control Room Paintina

On March 24. the inspectors ooserved painting in the control room. A

review by the inspectors of the controlling maintenance procedure and

the operations procedure for )ainting identified that guidelines in the

two procedures conflicted. T1e inspectors were concerned with the

controls govorning painting in the control room and the potential for

degradation d ventilation system efficiency. The inspectors brought

this issue to the attention of the shift supervisor. The shift

supervisor reviewed the conflict and found that the requirements in

Operations Administrative Procedure (0AP)-111.1, " Guidelines For

Operations Department Special Instructions." Revision 1 were outdated.

Procedure OAP-111.1 limited touch up painting in the control room to 200

square feet per day or a total of 1000 square feet. Any painting in

excess of the limits required an erigineering evaluation. The procedure

in use by the pair.ters was Civil Maintenance Procedure (CMP)-500.003,

" Application of Paint To Surfaces Outside The Reactor Building."

Revision 4. The maintenance procedure allowed up to 1000 square feet of

painting a day in the control room envelope. An engineering evaluation

is necessary when painting a total of 4000 square feet. The inspectors

observed that the painters were following the guidelines contained in-

the maintenance procedure. The maintenance procedure was based on an

engineering review of painting in the control room. The inspectors

reviewed the engineering analysis and it appeared satisfactory. The

inspectors concluded that the painting in t1e control room was being

performed in accordance with established procedures. The inspectors

considered the outdated 0AP as a third example of operation's

inattention to administrative controls.

Eauioment Bvoass Authorization

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On March 18. the inspectors reviewed the licensee's Bypass Authorization

! log bcok and the licensee's administrative controls for authorizing

bypass installation (Station Administrative Procedure (SAP)-148). At

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the time the inspectors reviewed the log there were three active bypass

authorizations. The oldest bypass had been installed in November 1997.

Each of the bypasses was installed in accordance with the administrative

controls and had received the appropriate 10 CFR 50.59 screening and had

be3n approved by the Plant Safety Review Committee.

c. Conclusions

A review of four admistrative control programs implemented by Operations l

' identified inattention to or lack of awareness of administrative control !

details in three of the programs. The specific examples were: not i

recognizing an engineering evaluation should have been updated when the

work scope changed: not caution tagging three non-safety related valves:

and, not revising an operating administrative procedure when painting j

criteria were revised

01.4 Emeraency Feedwater (EFW) Isolation

a. Insoection Scooe (71707)

The inspectors verified the licensee's compensatory actions in response

to an issue concerning isolation of EFW.

b. Observations and Findinas

On March 20. the licensee identified an issue concerning the ability to

isolate EFW to a faulted steam generator for a secondary system pipe

break outside containment. This issue was reviewed and is documented in

NRC Inspection Report No. 50-395/98003.

The inspectors verified the implementation of the licensee's interim

compensatory actions. They included a revision to the Emergency

0)erating Procedure (EOP) Users guide to describe operator actions for

t11s event and stationing an o)erator at the control room evacuation

panels where EFW isolation can se performed. On several occasions ,

during the ins)ection period the inspectors verified the operatar 1

stationed at tie control room evacuation Janels was attentive and

knowledgeable of the required actions to ]e taken in response to a

faulted steam generator. The inspectors identified no concerns,

c. Conclusions <

Compensatory actions for an emergency feedwater isolation issue were

satisfactorily implemented.

04 Operator Knowledge and Performance

04.1 Intermediate Buildina 00erator Rounds

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a. Insoection-Scoce (71707)

The inspectors accompanied the Intermediate Building (IB) operator

during the performance of a routine tour and TS required log taking.

b. Observations anj Findinas

On March 29. the inspectors observed the routine activities of the IB

operator which included a complete tour of the assigned spaces and the

recording of logs. Areas toured in the IB included vital switchgear

rooms, the reactor control rod equipment room, the control room

evacuation panels, the Diesel Generator (DG) rooms, the main steam

isolation valve area, and ventilation' equipment areas. Also included

were the Service Water (SW) building, and the fire pump and circulating

water pump areas. The operator toured these areas in a systematic

manner and inspected all areas. During the tour the_ IB operator also

verified DG operability due to a failure of the A DG local annunciator

panel. The annunciator failure had caused DG annunciators to alarm in

the control room. As a compensatory action the IB operator verified

locally that the DG was operable. Logs were recorded on a handheld

electronic device which was later downloaded into a computer for data

storage and reviewing. The o)erator demonstrated a good level of

knowledge and familiarity wit 1 his duties and responsibilities.

c. Conclusions

The knowledge level and performance of the intermediate building

-operator during routine rounds'was good. The observed diesel generator

compensatory actions were effective to ensure diesel operability. The

observed scope of tne operator rounds was effective to ensure that

potential equipment proalems were identified.

08 Miscellaneous Operations Issues (92901)

08.1 (Closed) Violation (VIO) 50-395/97003-01: Failure to establish

procedures appropriate to the circumstances. On April 26, 1997, the

licensee failed to establish operating procedures that would enable

operators to maintain adequate control of Steam Generator (SG) water

levels and failed to provide adequate operating instructions for

response to a turbine trip.

Corrective actions taken by the licensee included revising General

Operai.ing Procedure (GOP)-4 " Power Operation (Mode 1)." The inspectors

verified that the revisions provided additional guidance to the

operators for maintaining the required feedwater differential pressure

during power escalation. .Also. Abnormal Operating Procedure (AOP)-

, 214.2. " Response to Load Rejection / Runback." Revision 3 was revised to

provide additional guidance for response to a potential feedwater

isolation as the result of a turbine-trip due to high-high SG water

levels. The inspectors reviewed these revisions and considered them to

be adequate. The revised procedures were validated on the simulator and

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lessons learned from this event were-incorporated into operator training

scenarlos.

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08.2 (Closed) VIO 50-395/97003-03: Failure to follow procedure to raise

l Reactor Building (RB) pressure. On April 13. 1997, the licensee failed

l to implement the requirements of System Operating Procedure (SOP)-114, 1

, " Reactor Building. Ventilation System." when an operator opened the l

l containment purge exhaust isolation valves instead of the reactor i

building alternate purge supply isolation valves as required by the

procedure.

The licensee revised SOP-114 to show a clear difference between the

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purge supply and exhaust sections to clarify the different recuirements

for the operators. The inspectors reviewed the revision and cetermined

that the revised procedure was improved in that the two operations

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(raising and lowering RB 3ressure) were each contained in separate

sections. In addition, t1e licensee installed operator aids in the form

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of red plastic labels on the Heating. Ventilation, and Air Conditioning

(HVAC) panel. The purpose of these tags was to help prevent inadvertent

operation of the containment purge exhaust isolation valves. The

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inspectors considered these actions adequate to prevent recurrence of

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08.3 Review of Institute For Nuclear Power Ooerations (INPO) Reoort

a. Insoection Scooe-(71707)

The inspectors reviewed the final INP0 evaluation report for

V. C. Summer.

b. Observations and Findinas-

The INPO onsite assessment was conducted during the weeks of June 23 and

June 30, 1997. The inspectors reviewed the INP0 report to identify any

issues that were not consistent with NRC findings and assessments. The

issues identified in the INP0 report were found to be consistent with

recent NRC assessments of licensee performance.

c. -Conclusions

A review of the V. C. Summer INP0 report concluded that the content of

the report was consistent with recent NRC assessments of licensee

performance.

II. Maintenance

M1 Conduct of Maintenance

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M1.1 fagneral Comments

a. Insoection Scoce (62707)

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The inspectors observed all or portions of the following work

activities:

. WR 9800102. B Component Cooling Water (CCW) Pump Outboard Seal

Replacement

. Preventive Maintenance Task Sheet (PMTS) 9801120. Inspect Fuel

Injection Pump Studs on the A Diesel Generator (DG).

  • PMTS P0211043. Inspection (Partial Teardown) of the A DG Main Air

Start Valve B.

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. PMTS P0211042. Inspection (Partial Teardown) of the A DG Main Air

l Start Valve A.

. PMTS 9801547. A DG Engine Quarterly Maintenance.

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. WR 9718157. Repair A DG Number 11 Cylinder Lube Oil Leak Where Oil

is Fed to Rocker Arm.

. WR 9717799. Realace Tubing from Gage Panel to Valve Before Failure

-Starting Air pressure Number 1.

. WR 9717800. Re) lace Tubing from Gage Panel to Valve Before Failure

-Starting Air 3ressure Number 2.

. WR 9800091. Replace Bound Up Stator Temperature Selector Switch.

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. PMTS 9722364. Molded Case Circuit Breaker Testing XMC1DB24-12GH.

b. Observations and Findinas

The observed maintenance activities were conducted using the appropriate

)rocedures, tools, and technicues. The maintenance technicians were

(nowledgeable and demonstratec good work practices. No concerns were

identified.

c. Conclusions

Observed maintenance on a component cooling water pump, a molded case ,

circuit breaker, and a diesel generator identified no concerns. Good l

work practices and techniques were noted. l

M1.2 Surveillance Observation

a. Insoection Scooe (61726)

The inspectors observed or reviewed the following surveillance testing

activities:

, STP-123.003B Train B Service Water System Valve Operability Test.

! Revision 3.

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l -STP-116.001. Reactor Building Cooling Unit Functional Test. Revision 5.

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l. STP-117.001. Iodine Removal System' Test. ?,evision 3.

STP-125.002. Diesel Generator Operability Test. Revision 18

b. Observations and Findinas

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Observation and review of surveillance testing found good planning. '

communications and procedural adherence. Test acceptance criteria were

met.

c. Conclusions j

Surveillance activities were conducted satisfactorily and in accordance

with applicable procedures. Good planning for the tests was evident and !

communications during the tests were effective.

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M1.3 Moisture Seoarator Reheater (MSR) Testina

a. Insoection Scooe (62707)

The inspectors attended a pre-job briefing for aerforming an MSR test.

The attendees included on shift operators and t1e engineer in charge of

the test,

b. Observations ~and Findinas

On March 16, 1998, the inspectors attended a pre-job briefing for the

3erformance of Preventative Test Procedure (PTP)-230.001. "MSR Steam

low Setup and Verification." Revision 3. The purpose of the test was

to verify the optimal operation of the MSRs

The pre-job briefing was conducted by the engineer in charge. The  !

inspectors considered the briefing to be thorough, clear, and detailed. 1

The details of the test and the expected plant response was discussed.

All questions were addressed.

c. Conclusions

A pre-job briefing for a MSR performance test was thorough, clear, and .

detailed. Expected plant response was discussed.  !

M3 Maintenance Procedures and Documentation

M3.1 Observation and Review of Flow Transmitter Calibration Procedures

a. Insoection Scooe (61726)

The inspectors observed 3erformance of preventive maintenance on a

Reactor Coolant Pump (RC)) seal water flow transmitter and reviewed the

procedures.

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b. Observations and Findinos

On March 13. the inspectors observed Instrument and Control (I&C)

technicians perform Instrument Control Procedure (ICP)-340.022. "RCP 3

Seai Water Flow JFT00124." Revision 3 to complete PMTS 9717006. The

inspectors observed testing of the transmitter and reviewed the

procedure. The testing was performed satisfactorily and no concerns

were identified.

The inspectors reviewed the procedures for the similar flow transmitters

in the other two RCP seal water loops. The procedure the inspectors

observed the I&C technicians utilizing was dated March 14. 1986. The

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inspectors identified that the similar procedure for RCP 1 seal water

loop. ICP-340.024, "RCP 1 Seal Water Flow IFT00130," Revision 4, was

dated July 7, 1994. The inspectors were concerned that procedures of

significantly different ages were being used on similar transmitters and

that all the procedures for the similar flow instruments had not been

updated since 1986.

The inspectors review of both procedures identified several differences.

These included a different procedure format different references to

test equipment and the plant computer, and the inclusion of ste)s for

lifted leads and fitting replacement in the newer procedure. T1e older

procedure required going to other procedures to document lifted leads or

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fitting replacements. The inspectors found that licensee guidelines for

procedure revisions contained in Station Administrative Procedure (SAP)-

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139 " Procedure Development, Review. Approval and Control." Revision 18.

did not "pecifically require a timeframe for. updating procedures. The

inspectors concluded that the older revision was adequate to perform the

maintenance. However, the inspectors considered not revising all

applicable procedures for other similar instrument loops when a revision

was made to an instrument loop procedure was a poor practice.

c. Conclusions

Reactor Coolant Pump (RCP) seal water flow transmitter preventive

maintenance was performed adequately. A review of maintenance

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procedures for similar RCP seal water flow transmitters identified

procedures with revisions that were eight years apart. Although the

older revision was performed adequately, the inspectors considered not

revising all applicable procedures together was a poor practice.

M8 Miscellaneous Maintenance Issues (92902, 92903)

M8.1 (00en) Unresolved Item (URI) 50-395/98001-01: Review solid state

protection system TS operability and testing requirements. The

inspectors verified that procedures STP-345.037, " Solid State-Protection

System Actuation Logic and Master Relay Test Train A." Revision 14. and

STP-345.074, " Solid State Protection System Actuation Logic and Master

Relay Test Train B," Revision 9, were revised. Procedure STP-345.037

was revised on January 29 and performed on January 30, 1998. Procedure

STP-345.074 was revised on February 17 and performed on February 20.

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1998. The rocedures were revised to verify that the parallel inputs

for high-high SG level and SI were tested in the feedwater isolation fj

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circuitry.

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The licensee documented this issue on January 23.1998, in CER 98-0087.

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This was based on a Westinghouse Technical Bulletin dated December 20.

l 1997. The licensee considered these procedural changes as an (

i enhancement to their Solid State Protection System (SSPS) testing and i

L considered the surveillance tests to be adequate prior to making the l

changes in the surveillance test procedure. The inspectors questioned '

the licensee's position on this issue based on the definition of

Actuation Logic Test in the TS. The TS definition states that an

Actuation Logic Test shall be the ap)lication of various simulated input

combinations in conjunction with eac1 possible interlock logic state and

verification of the required logic output. On March 19. the licensee 1

reevaluated their position on this issue and concluded that the SSPS

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, surveillance testing was not adequately testing these circuits and the

inadequate surveillance testing was re)ortable. On March 23. during a

telephone conference with NRC staff, tie licensee stated that they had

l reevaluated their position on this issue. The NRC staff is continuing

l to review the licensee's resolution to the inadequate TS surveillance

testing and how these actions compare to TS required actions for

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inadequate surveillance testing.

M8.2 (Closed) Insoection Followuo Item (IFI) 50-395/97013-01: Licensee's

effort to identify the root cause and corrective action for the A diesel

generator problems. In response to the four failures of the A DG the

licensee performed an independent assessment of the failures and ,

performed Failure Cause Determinations for each of the failures. The i

inspectors reviewed each of the licensee's assessments.

The inde)endent assessment of the licensee's actions in response to the

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A DG aro31 ems concluded that the A DG was operable and recurrence of the

insta)ility would not be expeci.ed. This conclusion was based on the

corrective actions taken by the licensee, analysis results by Woodward,

the governor vendor, bench testing of components on site, and completion

of comprehensive post-maintenance testing. Failure analysis results

performed on the suspect. components verified that the abnormal

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conditions observed on the A DG were attributable to the component

l failures. It was concluded that no common component failure linked the

four failures on the A DG. The inspectors concluded that the licensee

had adequately reviewed and identified the root cause of each A DG

problem.

l The independent assessment also made several recommendations. These l

recommendations included suggested improvements in the process for l

controlling troubleshooting activities and governor set-up procedures:

improvements in training of operations and maintenance personnel and

adjustment of the governor system; and the documentation of all

unexpected events during maintenance and troubleshooting. Several other '

testing and maintenance recommendations were made by the assessment

team. The assessment team also concluded that the licensee's actions

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L -taken and responses provided to industry information documents were

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inadequate with regards to the information directly applicable to the

recent events at Summer. The licensee prepared a summary of corrective

actions and proposed completion dates. The inspectors concluded that

the independent assessment of the A DG events had provided the licensee

with . ,eful feedback and proposed enhancements to licensee programs,

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The inspectors also reviewed the Failure Cause Determination reports  !

prepared by engineering for each of the four A DG problems. The

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inspectors were satisfied that the licensee had adequately reviewed each

A DG issue and proposed corrective actions. The failure reports

concluded the following: 1) the A DG load swings experienced on November

11, 1997, and December 2,1997, were attributed to failure of the

governor electronic control (EGA) unit: 2) the A DG load swings on

November 21. 1997, were attributed to a failure of the relay which

caused droop to not be inserted properly and resulted in improper load

l sharing between the A DG and the grid: and 3) the A DG problem on

December 30, 1997, that resulted in a plant shutdown, was attributed to

a failure of the governor hydraulic actuator (EGB) unit. The inspectors

concluded that the licensee had identified the root cause of the A DG

problems and proposed adequate corrective action. Based on this review

and earlier reviews of the A DG failures the inspectors did not identify

any violations of regulatory requirements. Closeout of this IFI also

closes all required followup reviews for Notice of Enforcement

Discretion (NOED) 97-2-003 which was granted on November 13. 1997, for a

twelve hour extension of the TS Action Statement involving the first A ,

DG failure. '

III. Enaineerina

El Conduct of Engineering

El.1 Review of Enaineerina Evaluation for Deaerator Relief Valve liftina

a. Insoection Scooe (37551)

The ins)ectors reviewed an engineering evaluation concerning a DA relief i

valve w11ch lifted on March 8, 1998.

'

b. Observations and Findinas

On March 8,1998 a DA relief valve (XVR-2252A-HV) lifted at a system

operating pressure of approximately 107 psig (See Section 01.2). Plant

power was reduced until the valve reseated at a pressure of

approximately 99 psig. In addition, a second DA relief valve

(XVR-2252B-HR) showed evidence that it had lifted and reseated during

the same event.

The setpoint for these two valves (A and B) was 116 +/- 3 asig to

correspond to the maximum allowable working pressure for t1e DA. When

the A valve lifted and reseated, it was observed that there could be a

mechanical problem with the valve internals which could potentially

.

,

12

prevent the valve from reseating if it lifted again, The licensee

. performed an engineering evaluation to allow the A valve to be gagged in

'

the closed position. To do this, the licensee calculated the DA relief

valve flow ca)acity to ensure that sufficient capacity would be

available wit 1 the A valve gagged closed. In addition to the A and B j

valves, the DA has two other relief valves installed to prevent over

pressurization (XVR-1304-EX and XVR-1306-EX). The total flow capacity

was calculated through the three operable valves and it was determined

'

that a sufficient design margin existed to allow the A valve to be

gagged closed.

In addition to gagging the A valve closed, the licensee performed an l

engineering evaluation to raise the setpoint pressure of the B valve to i

12] +0/-8 psig. This would continue to meet the American Society of l

Mechanical Engineers (ASME) Code allowance for the DA. The maximum

working pressure for the DA is 116 psig. The ASME Code specifies that

no pressure relieving devices can be set higher than 105 percent of the

maximum working pressure (121 psig for the DA).

The inspectors reviewed the engineering evaluation and calculations and

determined that they were adequate to provide reasonable assurance that

the DA would continue to be overpressure protected with the new

configuration until such time that the permanent repairs could be i

performed. The method used represented good engineering practice and

contained all necessary data. No concerns were identified.

Also contained in the engineering evaluation were three 10 CFR 50.59

screenings to allow gagging closed the A relief valve, to allow

in-place testing of the A and B valves, and to raise the setpoint of the

B valve. These screenings were sufficiently detailed to support that no

10 CFR 50.59 evaluations were required.

c. Conclusions

An engineering evaluation to allow gagging a secondary plant deaerator

relief valve in the closed position and to allow raising the setpoint of

a second deaerator relief valve was technically adequate.

E1.2 Turbine First Staae Steam Pressure Chanaes

a. Insoection Scooe (37551)

The inspectors reviewed the effect of changing main turbine first stage

pressure during MSR testing.

b. Observations and Findinas

On March 16 the licensee began MSR steam flow testing (see Section

' M1.3) to establish the optimal amount of high pressure steam flow to the

High Pressure (HP) turbine and the MSRs. The licensee believed by

rebalancing steam flow between the MSRs and the HP turbine. greater

j secondary plant efficiency could be obtained. The actual test was well

1

. =

13 j

controlled and involved decreasing steam flow to the MSRs and increasing l

steam flow to the HP turbine incrementally. The test was performed

slowly over severai days to allow the plant to reach equilibrium after

each incremental change.  ;

1

The steam flow rebalancing had the effect of increasing HP turbine first i

stage steam pressure as indicated on pressure transmitters IPT-446 and

IPT-447. These steam pressure transmitters provide input into the rod

control and steam dump control systems, and provide inputs into the

protection channels used to calculate the high steam flow coincident

with Lo-Lo Tave main steam line isolation setpoint. On March 23. ],

'

during the conduct of the test, the operations shift engineer questioned

the effect of the change on first stage pressure on the protection

channels. The test had raised first stage c

pressure of about 676 psi to a peak of 711.)ressure from

psi on March 23.a normal

The test

was terminated and the MSRs were placed back in service in accordance

with the system operating procedure.

The steam line isolation engineered safeguards feature system actuation

instrumentation requirements are given in TS 3.3.2. Table 3.3-3. 4.d and

Table 3.3-4. 4.d. The high steam line flow setpoint is described in TS

as a function of load corresponding to 40 percent of full power steam

flow between zero and 20 percent load followed by a linear ramp to 110 1

percent of full power steam flow at 100 percent load. Turbine first

stage pressure is used as a measure of percent load. At the end of the

inspection period the licensee was continuing to evaluate the potential

effects of increasing first stage turbine pressure prior to resuming the

test.

The ins)ectors reviewed the safety evaluation for increasing steam flow

to the iP turbine. A discussion of the effects on the high steam line

flow accident and the main steam isolation setpoint had not been

included in the safety evaluation. Pending completion of the licensee's

evaluation to assess the safety significance of raising turbine first

stage pressure, this issue is identified as URI 50-395/98002-01.

c. Conclusions

An unresolved item was identified to assess the safety significance of

raising turbine first stage pressure during moisture se]arator reheater

testing on steam 1ine isolation actuation setpoints. T1is was not

addressed in the safety evaluation for the test.

IV. Plant Support

R1 Radiological-Protection and Chemistry (RP&C) Controls

R1.1 General Comments (71750)

The inspectors observed radiological controls during the conduct of

tours and observation of maintenance activities and found them to be

acceptable.

]

. .

14

S2- -Status of Security Facilities and Equipment

$2.1 Protected Area Access Control-Vehicles

,

a. Insoection Scooe (81700)

1

I The ins)ectors evaluated the licensee's vehicle access control program

l for. paccages, personnel and vehicles entering the protected area. This

l was to ensure compliance with criteria in Sections 1 and 3 of the

Physical Security Plan (PSP) and Security Plan Procedures (SPPs) 202 and

203.

b. Observation and Findinas

l

The inspectors reviewed applicable access control procedures to ensure

that the licensee provided appropriate access controls for the protected

areas.

!

'

,

The inspectors verified that personnel, hand-carried packages or

l material, and delivered packages or materials were searched adequately

'

before being admitted to the )rotected area. The inspectors observed

that security personnel searcled for firearms, explosives, incendiary

devices, and other items that could be used for radiological sabotage.

These searches were either by physical search or by search equipment.

! The inspectors found the following circumstances concerning personnel

l access control at the Vehicle Access Portal (VAP). A coded, numbered.

l picture badge identification system was used for personnel who were

authorized unescorted access to the protected area through the VAP.

I Picture badges issued to nonlicensee personnel indicated authorized

access areas and showed that no escort was required. The licensee used

I

biometric hand geometry to ensure personal identification of individuals

I entering the protected area at the VAP.

The inspectors verified that access control program records were

available for review and contained sufficient information for

identification of persons and vehicles authorized access to the

protected area.

During an evaluation of vehicle access control at the VAP, the

inspectors observed two individuals, a vehicle operator and accompanying

personnel, being processed through the personnel search equipment. They

l were cleared for access to the protected area by the security biometric l

system before the vehicle was searched. The first individual cleared l

went from the VAP search building directly to the unsearched vehicle and

, began to unload material from the vehicle to be searched by the security

l

officer. SPP 202. " Vehicle Access Requirements," Revision ll, paragraph

5.3.3.A.1.2).c), states that when a security officer conducts a search

of a vehicle. the security officer is to ensure that neither the

operator nor the accompanying aersor el are provided access to any 1

portion of the vehicle until tie vehicle search is completed. The

.

15

failure to search a vehicle properly before the vehicle entered the

protected area is identified as a Violation (VIO) 50-395/98002-02.

c. Conclusions

l

l A violation was identified for the failure of a security officer to

! prevent access to a vehicle until the vehicle search was completed. ,

l l

l S4 Security and Safeguards Staff Knowledge and Performance

'S4.1 Security Force Knowledae

l a. Insoection Scooe (81700)

The inspectors interviewed and observed security personnel to determine

if they possessed adequate knowledge to carry out their assigned duties

and responsibilities, including response procedures, use of deadly

force, and armed response tactics.

,

b. Observations and Findinas

The inspectors randomly interviewed approximately 20 security personnel, .

including supervisors, and witnessed approximately 30 others in the l

3erformance of their duties during normal and security event conditions. )

iembers of the security force were knowledgeable in their duties and I

responsibilities, response commitments and procedures, and armed  !

response tactics. The inspectors found that armed response personnel  !

had been instructed in the use of deadly force as required by i

10 CFR Part 73.

c. Conclusions .

l

Security personnel possessed appropriate knowledge to carry out their

assigned duties and responsibilities, including response procedures, use

of deadly force, and armed response tactics.

S4.2 Resoonse Caoabilities

a. Insoection Scooe (81700)

The inspectors evaluated the security organization's response capability

to security threats, contingencies, and routine response situations,

including drills to ensure consistency with the security procedures, the

approved PSP. and Safeguards Contingency Plan (SCP).

b. Observations and Findinas

The inspectors reviewed the response commitments of the SCP in the

following areas: deadly force, central and secondary alarm station

operations, communications, and security system degradations. Response

personnel were required to be competent in these skills before doing

response duties. As stated in S4.1. response personnel interviewed were

. .

.

16

knowledgeable of their responsibilities and duties indicated in these

skills. The licensee conducted two table top drills and two response

exercises during the inspection. The ins)ectors observed the drills and

exercises, and reviewed the critiques. T1e critiques stated the number

of adversaries and their objectives involved in each drill. The 1

performance of each res

weaknesses were noted. ponse member was indicated and any strengths or

c. Conclusions

The security organization's response capability to security threats,

contingencies, and routine response situations including drills, were

consistent with the security procedures, the approved Physical Security

Plan, and the Safeguards Contingency Plan.

S6 Security Organization and Administration

S6.1 Manaaement Sucoort

a. Insoection Scooe (81700)

The inspectors evaluated the level of management support for the

security program.

i

b. Observations and Findinas

The ins)ectors verified that station and security management support was

'

thorougl in identifying, reviewing, and analyzing the root cause of

problems. setting priorities for corrective actions and, usually, timely

correcting identified problems. The problems of the security computer

system were reviewed and are discussed in S7.1. The inspectors reviewed

the progress to correct the protected and vital area violation stated in

the Safeguards Information Inspection Report No. 50-395/96-03 dated 4

March 22. 1996. The compensatory measures implemented to temporarily l

secure the subject areas were still in place. The inspectors indicated

that compensatory measures which are two years old were not indicative

of proactive management support for the security program. '

c. Conclusions

t

Management support for the security program was generally strong. A

notable exception to this support was compensatory measures remaining in

, place for two years.

S6.2 Manaaement Effectiveness

a. Insoection Scooe (81700)

The inspectors evaluated the effectiveness of management's

administration of the security program.

.

17

b. Observations and Findinas-

The inspectors verified station and security management had established

l organizational goals and objective measures necessary to determine

l- security effectiveness Management has ensured that responsibility for

l all necessary activities were assigned to qualified subordinates as

L evident by Security Plan revisions and organizational improvements.

This effectiveness was also found in the security training improvements

l described in Section SS.1 of Safeguards Information Inspection Report

No. 50-395/96-06. Management's review and follow-up of the performance

'

i of delegated responsibilities were done by personal observations, formal

channels for opinions from subordinates, internal and external audits,

and tracking and trending of security events.

c. Conclusions

Management's administration of the security program was proactive and

-

i

effective, t

l S6.3 Staffina Level

a. Lrtsnection Scooe (81700)

The-inspectors evaluated the total number of trained security officers

and armed personnel immediately available at the facility to fulfill

response requirements specified in the PSP. The inspectors also

determined if one full-time member of the security organization, who had

the authority to direct security activities, did not have duties that

! conflicted with the assignment to direct all activities during an

incident.

b. Observations and Findinas

The inspectors verified that the licensee has an onsite physical

protection system and security organization. The security organization

and physical protection system were designed to protect against the

design basis threat of radiological sabotage as stated in ,

10 CFR 73.1(a). The inspectors verified that at least one full-time  !

manager of the security organization was always onsite and had no duties '

that conflicted with the assignment to direct all activities during an j

incident. This individual had.the authority to direct the physical '

, protection activities of the organization. The inspectors reviewed four

shift rosters and interviewed security force personnel on two shifts. '

The licensee had the number of trained security officers and armed

personnel immediately available to fulfill response requirements and

l commitments of the PSP.

l c. Conclusions  ;

The total number of trained security officers and armed personnel

immediately available to fulfill response requirements met Physical

l Security Plan requirements. One full-time member of the security

1

, .

18

l

organization who had the authority to direct security activities did'not ,

have duties that conflicted with the assignment to direct all activities

during an incident.

S7 Quality Assurance in Security and Safeguards Activities

S7.1 Effectiveness of Management Control

a. Insoection Scoce (81700)

The inspectors evaluated the overall effectiveness of the following:

licensee's controls for identifying, analyzing, and resolving problems:

determine adequacy of corrective actions to prevent recurring problems;

and determine whether there are strengths or weaknesses in the controls

for issues that could enhance or degrade plant operations or safety.

b. Observations and Findinas

The inspectors reviewed documented security issues, events, and problems

to determine the adequacy of the licensee's controls and effectiveness

in the following: initial identification of the problem: elevation of

the problems to the proper-level of management for resolution: root

cause analysis: disposition of operability problems; implementation of

corrective actions: and expansion of the scope of corrective actions to

include related systems, equipment, procedures, and personnel actions.

The inspectors also reviewed documented security issues, events. and

problems to determine the strengths or weaknesses in the. licensee *s

controls. These areas have been addressed in Sections S4.1. S4.2 and

S6.1. S6.2, and S6.3.

Discussions with maintenance personnel and reviews of the Security

Events Logs. Summaries, and Work Orders revealed that there was a

potential weakness in having sufficient spare parts on hand to maintain

the security computer system for the next five years. The system was

installed in the late 1980s. Presently, security maintenance personnel

were doing an exce)tional job in maintaining the security system. The l

prompt and thorougl sevicing of the security system was notable. Record  !

reviews indicated that the number of equipment failures was i

progressively escalating. This may result in a system degradation. The i

licensee indicated that there was approximately five years of spare

parts available onsite if the maintenance and repairs of the system

degradation do not increase substantially. The licensee was aware of

this problem and has plans to update the security computer system within

the next five years. i

i

c. Conclusions ,

!

Overall the licensee was effective in identifying, analyzing, and

resolving security related problems. The adequacy of corrective actions

to prevent recurring problems was found excellent. There were strengths

in the maintenance program of the security equipment and system that

supported plant operations and safety. The licensee was aware of the

i

.

.

19

weakness in the security system due to aging equipment that could

eventually lead to system degradation.

L Manaaement Meetinas

X1 Exit Meeting Summary

i

The inspectors ) resented the inspection results to members of licensee

management at t1e conclusion of the inspcction on April 20. 1998. The

licensee acknowledged the findings presented.

The inspectors asked the licensee whether any materials examined during

the inspection should be considered proprietary. No proprietary

information was identified.

PARTIAL LIST OF PERSONS CONTACTED )

Licensee

F. Bacon, Manager. Chemistry Services

L. Blue. Manager. Health Physics

S. Byrne. General Manager. Nuclear Plant Operations

R. Clary. Manager. Quality Systems

M. Fowlkes. Manager, Operations

S. Furstenberg. Manager. Maintenance Services

D. Lavigne. General Manager. Nuclear Support Services

G. Moffatt. Manager. Design Engineering

K. Nettles. General Manager. Strategic Planning and Development

L. Hipp. Manager. Nuclear Protection Services

A. Rice Manager Nuclear Licensing and Operating Experience

G. Taylor. Vice President. Nuclear Operations

R. Waselus. Manager. Systems and Component Engineering

R. White. Nuclear Coordinator. South Carolina Public Service Authority

B. Williams. General Manager. Engineering Services

G. Williams. Associate Manager. Operations

INSPECTION PROCEDURES USED

IP 37551: Onsite Engineering

IP 61726: Surveillance Observations

IP 62707: Maintenance Observations

IP 71707: Plant Operations

IP 71750: Plant Support Activities

IP 81700: Physical Security Program for Power Reactors

IP 92901: Followup - Plant Operations

IP 92902: Followup - Maintenance

IP 92903: Followup - Engineering

, .

20

ITEMS OPENED. CLOSED. AND DISCUSSED

Ooened

50-395/98002-01 URI assess safety significance of raising first

stage turbine pressure (Section E1.2)

50-395/98002-02 VIO failure to search vehicles according to Security

Plan Procedures (Section S2.1).

1

Closed

50-395/97003-01 VIO failure to establish procedures appropriate to

the circumstances (Section 08.1)

50-395/97003-03 VIO failure to follow procedure to raise reactor

building pressure (Section 08.2)  ;

50-395/97013-01 IFI licensee's effort to identify the root cause and

corrective action for the "A" diesel generator l

problems (Section M8.2)

Discussed

50-395/98001-01 URI review solid state protection system TS

operability and testing requirements '

(Section M8.1)

l

l

1

l