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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217M6631999-10-19019 October 1999 Forwards Insp Rept 50-277/99-07 & 50-278/99-07 on 990920.No Violations Noted ML20217K9241999-10-14014 October 1999 Forwards Amend 234 to License DPR-56 & Se.Amend Consists of Changes to TS in Response to Application & Suppls ,1001 & 06,which Will Support PBAPS Mod P00507,which Will Install Digital Pr Neutron Mining Sys ML20217F7391999-10-14014 October 1999 Requests Addl Info Re Peach Bottom Atomic Power Station Units 2 & 3 Appendix R Exemption Requests ML20217F6841999-10-13013 October 1999 Forwards Senior Reactor Operator Initial Exam Repts 50-277/99-302(OL) & 50-278/99-302(OL) Conducted on 990913- 16.All Applicants Passed All Portions of Exam ML20217F3021999-10-12012 October 1999 Provides Written Confirmation That Thermo-Lag 330-1 Fire Barrier Corrective Actions at PBAPS Have Been Completed.Ltr Also Confirms Completion of Actions Required by Confirmatory Order Modifying Licenses, ML20217E7451999-10-0808 October 1999 Forwards Response to NRC 990820 RAI Concerning Proposed Alternatives Associated with Third ten-yr Interval ISI Program for Pbaps,Units 2 & 3 ML20217B7701999-10-0606 October 1999 Submits Corrected Info to NRC 980528 RAI Re Util Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design-Basis Accident Conditions ML20217B9151999-10-0606 October 1999 Provides Clarifying Info to Enable NRC to Complete Review of License Change Request ECR 98-01802,re Changes Necessary to Support Installation of Digital Pr Neutron Monitoring & Incorporate long-term T/H Stability Solution Hardware ML20217C4141999-10-0606 October 1999 Forwards Response to NRC 981109 RAI Re Resolution of USI A-46 for Pbaps.Proprietary Excerpts from GIP-2,Ref 25 Results of BWR Trial Plant Review Section 8 Also Encl. Proprietary Excerpts Withheld ML20217B3181999-10-0505 October 1999 Advises That Info Submitted in 990712 Application,Which Contained Attachment Entitled, Addl Info Re Cycle Spec SLMCPR for Peach Bottom 3 Cycle 13,dtd 990609, with Affidavit,Will Be Withheld from Public Disclosure ML20217B4051999-10-0505 October 1999 Forwards Amend 233 to License DPR-56 & Safety Evaluation. Amend Changes Minimum Critical Power Ratio Safety Limit & Approved Methodologies Referenced in Core Operating Limits Report 05000278/LER-1999-004, Forwards LER 99-004-00 Re Multiple Unplanned ESF Actuations During Planned Mod Activities in Main Cr,Per Requirements 10CFR50.73(a)(2)(iv)1999-10-0101 October 1999 Forwards LER 99-004-00 Re Multiple Unplanned ESF Actuations During Planned Mod Activities in Main Cr,Per Requirements 10CFR50.73(a)(2)(iv) ML20217B8891999-10-0101 October 1999 Forwards Response to RAI Re Request to Install Digital Power Range Neutron Monitoring Sys & Incorporate long-term,thermal-hydraulic Stability Solution Hardware. Revised TS Table 3.3.2.1-1 Encl ML20217D5211999-09-30030 September 1999 Informs That Remediating 3D Monicore Sys at Pbaps,Units 2 & 3 & 3D Monicore/Plant Monitoring Sys at Lgs,Unit 2 Has Been Completed Ahead of Schedule ML20212J6851999-09-29029 September 1999 Informs of Completion of mid-cycle PPR of Peach Bottom Atomic Power Station on 990913.No Areas Identified in Which Licensee Performance Warranted Addl New Insps Beyond Core Insp Program.Historical Listing of Plant Issues Encl ML20216J3981999-09-29029 September 1999 Submits Comments for Lgs,Unit 1 & Pbaps,Units 2 & 3 Rvid,Rev 2,based on Review as Requested in GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity ML20212J5751999-09-28028 September 1999 Informs of Individual Exam Results for Applicants on Initial Exam Conducted on 990913-16 at Licensee Facility.Without Encls ML20216J0191999-09-27027 September 1999 Forwards Request for Addl Info Re Util 990301 Request to Support Installation of Digital Power Range Neutron Monitoring Sys & Incorporation of long-term thermal- Hydraulic Stability Solution Hardware,For Plant ML20212H6171999-09-24024 September 1999 Forwards Rev 2 to COLR for Pbaps,Unit 2,Reload 12,Cycle 13, IAW TS Section 5.6.5.d.Rept Incorporates Revised Single Loop Operation MAPLHGR Flow Multiplier ML20216H6451999-09-24024 September 1999 Forwards Notice of Withdrawal of Util 990806 Application for Amends to Fols DPR-44 & DPR-56.Proposed Change Would Have Involved Temporary Change to Increase Limit for Average Water Temp of Normal Heat Sink ML20212H5431999-09-24024 September 1999 Informs of Decision to Inspect H-3 & H-4 Shroud Welds During Upcoming 3R12 Outage Scheduled to Begin Late Sept 1999 ML20216H6751999-09-24024 September 1999 Forwards Amends 229 & 232 to Licenses DPR-44 & DPR-56, Respectively & Ser.Amends Will Delete SR Associated Only with Refueling Platform Fuel Grapple Fully Retracted Position Interlock Input,Currently Required by SR 3.9.1.1 ML20216F8811999-09-23023 September 1999 Withdraws 990806 Exigent License Change Application.Tech Spec Change to Allow Continued Power Operation with Elevated Cooling Water Temps During Potentially Extreme Weather Conditions No Longer Needed Due to Favorable Weather ML20212E8661999-09-22022 September 1999 Discusses GL 98-01 Y2K Readiness of Computer Sys at NPPs & Supplement 1 & PECO Response for PBAPS Dtd 990630. Understands That at Least One Sys or Component Listed May Have Potential to Cause Transient During Y2K Transition ML20212F5481999-09-20020 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing, for Pbaps,Units 2 & 3 & Lgs,Units 1 & 2 ML20212D1191999-09-17017 September 1999 Forwards SE Re Proposed Alternatives to ASME Section XI Requirements for Containment Inservice Insp Program at Plant,Units 2 & 3 ML20212A0091999-09-0909 September 1999 Provides Notification That Licenses SOP-11172 & SOP-11321, for SO Muntzenberger & Rh Wright,Respectively,Are No Longer Necessary as Result of Permanent Reassignment ML20211P2961999-09-0707 September 1999 Provides Authorization to Administer NRC Approved Initial Written Exams to Listed Applicants on 990913 at Peach Bottom Npp,Delta,Pennsylvania ML20211K7031999-08-30030 August 1999 Forwards Response to NRC 990826 RAI Re License Change Application ECR 99-01255,revising TSs 2.1.1.2 & 5.6.5 ML20211E6941999-08-26026 August 1999 Forwards Request for Addl Info Re Min Critical Power Ratio. Response Should Be Submitted within 30 Days of Ltr Receipt ML20211Q4491999-08-25025 August 1999 Responds to Re Changes to PBAPS Physical Security Plan,Safeguards Contingency Plan & Guard Training & Qualification Plan Identified as Revs 13,11 & 9, Respectively.No NRC Approval Is Required,Per 10CFR50.54(p) ML20211E9191999-08-24024 August 1999 Forwards fitness-for-duty Program Performance Data for Jan-June 1999 for PBAPS & LGS IAW 10CFR26.71(d).Data Includes Listed Info ML20211D5421999-08-23023 August 1999 Forwards Amends 228 & 231 to Licenses DPR-44 & DPR-56, Respectively & Se.Amends Revise TSs to Correct Typographical & Editorial Errors Introduced in TSs by Previous Amends ML20211A9721999-08-20020 August 1999 Forwards Request for Addl Info Re Third 10-year Interval Inservice (ISI) Insp Program Plan for Plant,Units 2 & 3 ML20210T5451999-08-12012 August 1999 Forwards Copy of Environ Assessment & Findings of No Significant Impact Re Licensee Request for Amends to Plant. Amends Consist of Changes to TS to Correct Typos & Editorial Errors Introduced in TS by Previous Amends ML20210P8321999-08-11011 August 1999 Responds to NRC 990715 Telcon Re Util 990217 Submittal of Proposed Alternatives to Requirements of 10CFR50.55a(g)(6)(ii)(B)(1) Re Containment Inservice Insp Program ML20210P8151999-08-11011 August 1999 Forwards Final Pages for Pbaps,Unit 2 & 3 OLs Re License Change Application ECR 99-01497,which Reflects Change in Corporate Structure at Pse&G ML20211B6521999-08-10010 August 1999 Informs That Dp Lewis,License SOP-11247,has Been Permanently Reassigned & No Longer Requires License,Per 10CFR50.74.Util Requests That Subject Individual Be Removed from List of License Holders ML20210P1561999-08-10010 August 1999 Submits Response to Requests for Addl Info Re GL 92-01,rev 1,Suppl 1, Rv Structural Integrity, for Pbap,Units 1 & 2. NRC Will Assume That Data Entered Into Rvid Are Acceptable for Plants,If Staff Does Not Receive Comments by 990901 ML20211B7881999-08-10010 August 1999 Transmits Summary of Two Meetings with Risk-Informed TS Task Force in Rockville,Md on 990514 & 0714 ML20210N7831999-08-0909 August 1999 Forwards Copy of Notice of Consideration of Issuance of Amends to Fols,Proposed NSHC Determination & Opportunity for Hearing, Re 990806 Request for License Amends.Amends Incorporate Note Into PBAPS TS to Permit One Time Exemption ML20210P0801999-08-0404 August 1999 Forwards Initial Exam Repts 50-277/99-301 & 50-278/99-301 on 990702-14 (Administration) & 990715-22 (Grading).Six of Limited SRO Applicants Passed All Portion of Exam ML20210M7571999-08-0404 August 1999 Forwards Response to Requesting Addl Info Re Status of Decommissioning Funding for Lgs,Pbaps & Sngs. Attachment Provides Restatement of Questions Followed by Response NUREG-1092, Informs J Armstrong of Individual Exam Results for Applicants on Initial Exam Conducted on 990702 & 990712-14 at Facility.All Six Individuals Who Were Administered Exam, Passed Exam.Without Encls1999-08-0303 August 1999 Informs J Armstrong of Individual Exam Results for Applicants on Initial Exam Conducted on 990702 & 990712-14 at Facility.All Six Individuals Who Were Administered Exam, Passed Exam.Without Encls ML20210J0161999-07-30030 July 1999 Forwards Copy of Notice of Consideration of Approval of Transfer of FOL & Issuance of Conforming Amends Re 990723 Application ML20210H5341999-07-27027 July 1999 Forwards Insp Repts 50-277/99-05 & 50-278/99-05 on 990518- 0628.NRC Determined That Two Severity Level IV Violations of NRC Requirements Occurred & Being Treated as non-cited Violations Consistent with App C of Enforcement Policy ML20210F3731999-07-23023 July 1999 Submits Confirmation That,Iaw 10CFR50.80,PSE&G Is Requesting NRC Approval of Transfer of Ownership Interests in PBAPS, Units to New Affiliated Nuclear Generating Company,Pseg Nuclear LLC ML20210E6211999-07-22022 July 1999 Submits Rev to non-limiting Licensing Basis LOCA Peak Clad Temps (Pcts) for Limerick Generating Station (Lgs),Units 1 & 2 & Pbaps,Units 2 & 3 ML20210E5811999-07-21021 July 1999 Forwards Final Tech Specs Pages for License Change Application.Proposed Change Will Revise Tech Specs to Delete Requirement for Refuel Platform Fuel Grapple Fully Retracted Position Interlock Currently Required by TS ML20216D8041999-07-19019 July 1999 Submits Summary of Final PECO Nuclear Actions Taken to Resolve Scram Solenoid Pilot Valve Issues Identified in Info Notice 96-007 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217F3021999-10-12012 October 1999 Provides Written Confirmation That Thermo-Lag 330-1 Fire Barrier Corrective Actions at PBAPS Have Been Completed.Ltr Also Confirms Completion of Actions Required by Confirmatory Order Modifying Licenses, ML20217E7451999-10-0808 October 1999 Forwards Response to NRC 990820 RAI Concerning Proposed Alternatives Associated with Third ten-yr Interval ISI Program for Pbaps,Units 2 & 3 ML20217C4141999-10-0606 October 1999 Forwards Response to NRC 981109 RAI Re Resolution of USI A-46 for Pbaps.Proprietary Excerpts from GIP-2,Ref 25 Results of BWR Trial Plant Review Section 8 Also Encl. Proprietary Excerpts Withheld ML20217B9151999-10-0606 October 1999 Provides Clarifying Info to Enable NRC to Complete Review of License Change Request ECR 98-01802,re Changes Necessary to Support Installation of Digital Pr Neutron Monitoring & Incorporate long-term T/H Stability Solution Hardware ML20217B7701999-10-0606 October 1999 Submits Corrected Info to NRC 980528 RAI Re Util Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design-Basis Accident Conditions ML20217B8891999-10-0101 October 1999 Forwards Response to RAI Re Request to Install Digital Power Range Neutron Monitoring Sys & Incorporate long-term,thermal-hydraulic Stability Solution Hardware. Revised TS Table 3.3.2.1-1 Encl 05000278/LER-1999-004, Forwards LER 99-004-00 Re Multiple Unplanned ESF Actuations During Planned Mod Activities in Main Cr,Per Requirements 10CFR50.73(a)(2)(iv)1999-10-0101 October 1999 Forwards LER 99-004-00 Re Multiple Unplanned ESF Actuations During Planned Mod Activities in Main Cr,Per Requirements 10CFR50.73(a)(2)(iv) ML20217D5211999-09-30030 September 1999 Informs That Remediating 3D Monicore Sys at Pbaps,Units 2 & 3 & 3D Monicore/Plant Monitoring Sys at Lgs,Unit 2 Has Been Completed Ahead of Schedule ML20216J3981999-09-29029 September 1999 Submits Comments for Lgs,Unit 1 & Pbaps,Units 2 & 3 Rvid,Rev 2,based on Review as Requested in GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity ML20212H6171999-09-24024 September 1999 Forwards Rev 2 to COLR for Pbaps,Unit 2,Reload 12,Cycle 13, IAW TS Section 5.6.5.d.Rept Incorporates Revised Single Loop Operation MAPLHGR Flow Multiplier ML20212H5431999-09-24024 September 1999 Informs of Decision to Inspect H-3 & H-4 Shroud Welds During Upcoming 3R12 Outage Scheduled to Begin Late Sept 1999 ML20216F8811999-09-23023 September 1999 Withdraws 990806 Exigent License Change Application.Tech Spec Change to Allow Continued Power Operation with Elevated Cooling Water Temps During Potentially Extreme Weather Conditions No Longer Needed Due to Favorable Weather ML20212F5481999-09-20020 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing, for Pbaps,Units 2 & 3 & Lgs,Units 1 & 2 ML20212A0091999-09-0909 September 1999 Provides Notification That Licenses SOP-11172 & SOP-11321, for SO Muntzenberger & Rh Wright,Respectively,Are No Longer Necessary as Result of Permanent Reassignment ML20211K7031999-08-30030 August 1999 Forwards Response to NRC 990826 RAI Re License Change Application ECR 99-01255,revising TSs 2.1.1.2 & 5.6.5 ML20211E9191999-08-24024 August 1999 Forwards fitness-for-duty Program Performance Data for Jan-June 1999 for PBAPS & LGS IAW 10CFR26.71(d).Data Includes Listed Info ML20210P8321999-08-11011 August 1999 Responds to NRC 990715 Telcon Re Util 990217 Submittal of Proposed Alternatives to Requirements of 10CFR50.55a(g)(6)(ii)(B)(1) Re Containment Inservice Insp Program ML20210P8151999-08-11011 August 1999 Forwards Final Pages for Pbaps,Unit 2 & 3 OLs Re License Change Application ECR 99-01497,which Reflects Change in Corporate Structure at Pse&G ML20211B6521999-08-10010 August 1999 Informs That Dp Lewis,License SOP-11247,has Been Permanently Reassigned & No Longer Requires License,Per 10CFR50.74.Util Requests That Subject Individual Be Removed from List of License Holders ML20210M7571999-08-0404 August 1999 Forwards Response to Requesting Addl Info Re Status of Decommissioning Funding for Lgs,Pbaps & Sngs. Attachment Provides Restatement of Questions Followed by Response ML20210F3731999-07-23023 July 1999 Submits Confirmation That,Iaw 10CFR50.80,PSE&G Is Requesting NRC Approval of Transfer of Ownership Interests in PBAPS, Units to New Affiliated Nuclear Generating Company,Pseg Nuclear LLC ML20210E6211999-07-22022 July 1999 Submits Rev to non-limiting Licensing Basis LOCA Peak Clad Temps (Pcts) for Limerick Generating Station (Lgs),Units 1 & 2 & Pbaps,Units 2 & 3 ML20210E5811999-07-21021 July 1999 Forwards Final Tech Specs Pages for License Change Application.Proposed Change Will Revise Tech Specs to Delete Requirement for Refuel Platform Fuel Grapple Fully Retracted Position Interlock Currently Required by TS ML20216D8041999-07-19019 July 1999 Submits Summary of Final PECO Nuclear Actions Taken to Resolve Scram Solenoid Pilot Valve Issues Identified in Info Notice 96-007 05000278/LER-1999-002, Forwards LER 99-002-01 to Correct Title Contained in Box (4) of LER Coversheet Form.Rev Does Not Change Reportability Requirements or Any Other Info Contained in Original Submittal of LER1999-07-12012 July 1999 Forwards LER 99-002-01 to Correct Title Contained in Box (4) of LER Coversheet Form.Rev Does Not Change Reportability Requirements or Any Other Info Contained in Original Submittal of LER ML20209G9121999-07-0909 July 1999 Informs That Ja Hutton Has Been Appointed Director,Licensing for PECO Nuclear,Effective 990715.Previous Correspondence Addressed to Gd Edwards Should Now Be Sent to Ja Hutton ML20209D9781999-07-0808 July 1999 Forwards Addl Info to Support EA of Proposed 990212 License Application ECR 98-01675,correcting Minor Administrative Errors in TS Figure Showing Site & Exclusion Areas Boundaries & Two TS SRs ML20209D8821999-07-0707 July 1999 Submits Estimate of Number of Licensing Actions Expected to Be Submitted in Years 2000 & 2001,as Requested by Administrative Ltr 99-02.Renewal Applications for PBAPS, Units 2 & 3,will Be Submitted in Second Half of 2001 ML20209D2671999-07-0202 July 1999 Responds to NRC 990322 & 0420 RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20209E1131999-06-30030 June 1999 Forwards Proprietary NRC Form 398, Personal Qualification Statement-Licensee, for Renewal of RO Licenses for EP Angle,Md Lebrun,Jh Seitz & Zi Varga,Licenses OP-10646-1, OP-11081,OP-11082 & OP-11085,respectively.Encls Withheld ML20209B7001999-06-30030 June 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20209C1201999-06-30030 June 1999 Informs of Util Intent to Request Renewed License for PBAPS, Units 2 & 3,IAW 10CFR54.Licensee Anticipates That License Renewal Application Will Be Submitted in Second Half of 2001 05000277/LER-1999-004, Forwards LER 99-004-00 Re Unplanned ESF Actuations During Planned Electrical Bus Restoration Following Maint Activities1999-06-20020 June 1999 Forwards LER 99-004-00 Re Unplanned ESF Actuations During Planned Electrical Bus Restoration Following Maint Activities ML20196A5291999-06-14014 June 1999 Forwards Final Pbaps,Unit 3 TS Pages for License Change Request ECR 98-01802 Re Installation of Digital Power Range Neutron Monitoring (Prnm) Sys & Incorporation of long-term thermal-hydraulic Stability Solution Hardware ML20195E6051999-05-27027 May 1999 Requests Exemption from Requirements of 10CFR72.44(d)(3) Re Submittal Date for Annual Rept of Principal Radionuclides Released to Environ.Exemption from 10CFR72.72(d) Re Storage of Spent Fuel Records,Additionally Requested ML20195B8171999-05-25025 May 1999 Forwards Final TS Pages for License Change Application ECR 96-01511 Re Rev to Loss of Power Setpoints for 4 Kv Emergency Buses ML20195B6191999-05-19019 May 1999 Forwards PBAPS Units 2 & 3 Annual Radiological Environ Operating Rept 56 for 980101-1231, Per Section 6.9.2 of Ol. Trace Concentrations of Cs-137 Were Found in Sediment Consistent with Levels Observed in Previous Years ML20206P9171999-05-10010 May 1999 Updates Some of Transmitted Data Points Provided in Data Point Library ERDS for Pbaps,Units 2 & 3.Data Point Info Format Consistent with Guidance Specified in NUREG-1394 ML20206K6581999-05-0404 May 1999 Forwards PBAPS Bases Changes Through Unit 2 Bases Rev 25 & Units 3 Bases Rev 25.Bases Reflect Change Through Apr 1999, Thereby Satisfying Frequency Requirements of 10CFR50.71 ML20206D4651999-04-29029 April 1999 Forwards Rev 16 to UFSAR & Rev 11 to Fire Protection Program (Fpp), for Pbaps,Units 2 & 3.Page Replacement Instructions for Incorporating Rev 16 to UFSAR & Rev 11 to Fpp,Encl ML20207B8431999-04-23023 April 1999 Forwards Final Rept for 981117,plume Exposure Pathway Exercise of Offsite Radiological Emergency Response Plans site-specific for Peach Bottom Atomic Power Station.One Deficiency & 27 Areas Requiring C/A Identified ML20206C5461999-04-20020 April 1999 Forwards Radioactive Effluent Release Rept 41 for Jan-Dec 1998 for Pbaps,Units 1 & 2. Revs Made to ODCM & Station Process Control Program (PCP) During Rept Period,Encl 05000277/LER-1999-003, Forwards LER 99-003-00 Re 990318 Failure to Maintain Provisions of Fire Protection Program to Properly Address Effects of Flooding1999-04-16016 April 1999 Forwards LER 99-003-00 Re 990318 Failure to Maintain Provisions of Fire Protection Program to Properly Address Effects of Flooding ML20205K4541999-04-0808 April 1999 Forwards Revised Info Re 990330 NRC Nuclear Power Reactor Licensee Financial Qualifications & Decommissioning Funding Assurance Status Rept 05000278/LER-1999-001, Forwards LER 99-001-00 Re 990312 ESF Actuation of Rcics Due to High Steam Flow Signal During Sys Restoration.Rept Submitted Per 10CFR50.73(a)(2)(iv)1999-04-0808 April 1999 Forwards LER 99-001-00 Re 990312 ESF Actuation of Rcics Due to High Steam Flow Signal During Sys Restoration.Rept Submitted Per 10CFR50.73(a)(2)(iv) ML18106B1431999-03-31031 March 1999 Forwards Pse&G Rept on Financial Min Assurance for Period Ending 981231 for Hope Creek,Salem,Units 1 & 2 & Pbaps,Units 2 & 3,IAW 10CFR50.75 ML20205F8981999-03-31031 March 1999 Provides Info Re Status of Decommissioning Funding for LGS, Units 1 & 2,PBAPS,Units 1,2 & 3 & Sgs,Units 1 & 2,per Requirements of 10CFR50.75(f)(1) ML18106B1411999-03-30030 March 1999 Forwards Decommissioning Info on Behalf of Conectiv Nuclear Facility License Subsidiaries,Atlantic City Electric Co & Delmarva Power & Light Co,For Listed Nuclear Facilities ML20205J0831999-03-26026 March 1999 Requests Enforcement Discretion from Requirements of PBAPS, Units 2 & 3 Ts.Enforcement Discretion Pursued to Avoid Unneccessary Plant Transient Which Would Result from Compliance with TS ML20205B6421999-03-24024 March 1999 Submits 1998 Annual Decommission Rept for Pbaps,Unit 1. There Were No Reportable Events Involving Unit 1 for 1998 1999-09-09
[Table view] Category:UTILITY TO NRC
MONTHYEARML20064A7171990-09-18018 September 1990 Comments on SALP Board Repts 50-277/89-99 & 50-278/89-99. Author Pledges Continued Mgt Support of & Attention to Rate of Improvement,Achievement of Goals & Performance of Routine Activities ML20065D4421990-09-14014 September 1990 Responds to Generic Ltr 90-07, Operator Licensing Natl Exam Schedule. Proposed Schedules for Operator Licensing Exams, Requalification Exams & Generic Fundamental Exams Encl ML20064A7751990-09-13013 September 1990 Advises That Ba Stambauth No Longer Maintains Need to Hold Senior Operator License ML20065D3741990-09-11011 September 1990 Forwards Rev to Relief Request 10-VRR-2 Re RHR stay-fill Supply Check Valves,Per ML20059F0541990-08-31031 August 1990 Responds to NRC Re Violations Noted in Safety Insp Repts 50-277/90-13 & 50-278/90-13.Corrective Actions: Training Will Be Provided for Personnel Re Requirements of Drawing E1317 & Administrative Procedures A-2 & A-6 ML20028G8181990-08-27027 August 1990 Forwards Peach Bottom Atomic Power Station Semiannual Effluent Release Rept,Jan-June 1990. No Revs Made to ODCM During Rept Period ML20059A6461990-08-15015 August 1990 Responds to Violation Noted in Insp Repts 50-277/90-200, 50-278/90-200,50-277/90-06 & 50-278/90-06 & Payment of Civil Penalty in Amount of $75,000.Corrective Actions:Emergency Svc Water Sys Restored to Operable Status ML20058N1991990-08-0909 August 1990 Advises of Change of Address for Correspondence Re Util Operations.All Incoming Correspondence Must Be Directed to One of Listed Addresses ML20058Q4051990-08-0606 August 1990 Forwards Public Version of Revised Emergency Response Procedures,Including Rev 12 to ERP-140,App 2,Rev 13 to ERP-140,App 3,Rev 4 to ERP-230,Rev 3 to ERP-305 & Rev 3 to ERP-660 ML20058M6631990-08-0303 August 1990 Responds to NRC 890406 Integrated Assessment Team Insp Repts 50-277/89-81 & 50-278/89-81.Based on Encl Schedule,Overall Projected Implementation Date Will Be 901119 ML20056A9611990-08-0303 August 1990 Notifies That Be Saxman Terminated Employment & Operating Responsibilities W/Util on 900706 ML20081E1581990-07-30030 July 1990 Forwards List of 1990 QA Program Changes for Plant.List Identifies Page & Paragraph Number,Brief Description & Type of Change ML20056A0421990-07-27027 July 1990 Forwards Updated Human Resource Status Rept for Jan-Jul 1990 for Areas Identified in Integrated Assessment Team Insp Repts 50-277/89-81 & 50-278/89-81 ML18095A3761990-07-26026 July 1990 Forwards Decommissioning Repts & Certification of Financial Assurance for Plants ML18095A3661990-07-26026 July 1990 Forwards Decommissioning Repts for Hope Creek,Peach Bottom & Salem Nuclear Generating Stations ML18095A3721990-07-24024 July 1990 Forwards Rept & Certification of Financial Assurance for Decommissioning for Plants,Per 10CFR50.75 ML20055H8331990-07-20020 July 1990 Submits Change of Addresses for Correspondence Re Util Nuclear Operations ML20044B2621990-07-12012 July 1990 Forwards Annual Progress Rept on Implementation of Control Room Enhancements,Per NUREG-0737.Corrective Actions for All Priority 1 Human Engineering Discrepancies Completed for Unit.Remaining Priority 2 Discrepancies Under Reevaluation ML20055G5481990-07-11011 July 1990 Forwards Public Version of Revised Epips,Including Rev 12 to ERP-140,App 3 & Revs 3 to ERP-310 & ERP-317 ML20043H7041990-06-21021 June 1990 Forwards Endorsements 143-146 to Nelia Policy NF-140 & Endorsements 93-96 to Maelu Policy MF-67 ML20044A2961990-06-21021 June 1990 Submits Revised Response to NRC Bulletin 89-002 Re safety- Related Swing Check Valves to Be Installed on Emergency Diesel Generator.Bolts Will Not Be Replaced Because Valves W/Original Internal Bolts Meet Requirements of Bulletin ML20043H6081990-06-19019 June 1990 Corrects 900427 Response to Generic Ltr 87-07, Info Transmittal of Final Rulemaking for Revs to Operator Licensing - 10CFR55 & Conforming Amends. ML20055C7621990-06-18018 June 1990 Informs NRC of Plans Re Licensing of Senior Reactor Operators (Sros) Limited to Fuel Handling at Plants.Util in Process of Implementing New Program for Establishment & Maint of Licensed SROs Limited to Fuel Handling at Plants ML20043G8131990-06-13013 June 1990 Responds to NRC 900515 Ltr Re Violations Noted in Insp Repts 50-277/90-06 & 50-278/90-06.Corrective Actions:Surveillance Test 6.16, Motor Driven Fire Pump Operability Test, Will Be Revised ML20043H0111990-06-12012 June 1990 Advises That AR Wargo Reassigned from Operating Shift Responsibilities & Will Be Resigning License,Effective on 900514 ML20055D1141990-06-0808 June 1990 Forwards Public Version of Revs to Emergency Response Procedures,Including Rev 9 to ERP-140 & Rev 3 to ERP-315 ML20043D7351990-06-0404 June 1990 Responds to NRC 900504 Ltr Re Violations Noted in Insp Repts 50-277/90-04 & 50-278/90-04.Corrective Actions:Procedural Controls Strengthened to Preclude Licensed Operators from Performing Licensed Duties W/O Successfully Passing Exams ML20043E9261990-06-0404 June 1990 Forwards Response to 900327 Request for Addl Info Re Generic Ltr 88-01, NRC Position on IGSCC in BWR Austenitic Stainless Steel Piping. ML20043D2681990-05-31031 May 1990 Forwards Response to NRC Requests Re PECo-FMS-0006, Methods for Performing BWR Reload Safety Evaluations. Util Core Monitoring Activities Routinely Access Accuracy of steady-state Physics Models Used in Evaluation of Parameter ML20043D6451990-05-30030 May 1990 Responds to NRC 900503 Ltr Re Violations Noted in Insp Repts 50-277/90-08 & 50-278/90-08.Corrective Actions:Glaucoma Testing Program Initiated for Security Personnel & Necessary Equipment to Perform Glaucoma Testing Onsite Obtained ML20055C5491990-05-18018 May 1990 Forwards Response to Request for Addl Info on 900412 Tech Spec Change Request 89-20 Re Postponement of Next Snubber Visual Insp,Due 900526,until Scheduled mid-cycle Outage in Fourth Quarter 1990 ML20055C5121990-05-18018 May 1990 Provides Info Inadvertently Omitted in Re Property Insurance Coverage for Plants.Limerick Generating Station Unit 2 Should Have Been Ref as Being Included Under Insurance Coverage ML20055C4851990-05-15015 May 1990 Forwards Annual Financial Repts for 1989 for Philadelphia Electric Co,Pse&G,Atlantic Energy,Inc & Delmarva Power & Light Co ML20043A3341990-05-14014 May 1990 Advises of Util Proposal to Provide Response to NRC Request for Schedule for Compliance W/Reg Guide 1.97 Re Neutron Monitoring Instrumentation 3 Months After NRC Concurrence W/Bwr Owners Group Design Criteria ML20042E7651990-04-27027 April 1990 Informs That Mod 2285 Completed on Unit 3,but That Mod 2285 Will Not Be Completed on Unit 2 During 8th Refueling Outage ML20042E8931990-04-27027 April 1990 Responds to Violation Noted in Insp Rept 50-278/90-01. Corrective Actions:Automatic Depressurization Sys Logic Sys Functional Tests Will Be Revised to Include Guidance in Unique Application of Test Lights ML20042F3241990-04-27027 April 1990 Advises That Organizational Changes Made in Advance of Approval of Tech Spec Change Request 88-06.Changes Do Not Present Unreviewed Safety Question ML20042E8741990-04-27027 April 1990 Responds to Generic Ltr 87-07, Info Transmittal of Final Rulemaking for Revs to Operator Licensing. Certifies That Limerick Operator Requalification Training Program Renewed on 900125 & Peach Bottom Subj Program Renewed on 890622 ML20012F4801990-04-0202 April 1990 Forwards Errata to Unit Shutdowns and Power Reductions Monthly Operating Rept for Feb 1990 ML20012F0971990-03-22022 March 1990 Forwards Summary of ASME Repairs & Replacement Completed, Per Facility Second 10-yr Interval Inservice Insps Completed During 900331-891111 Extended Refueling Outage ML20012E2151990-03-20020 March 1990 Responds to Generic Ltr 89-19, Request for Action Re Resolution of USI A-47, 'Safety Implication of Control Sys in LWR Nuclear Power Plants,' for Peach Bottom.Response for Limerick Generating Station Will Be Provided by 900504 ML20012C2931990-03-12012 March 1990 Responds to Generic Ltr 90-01, Request for Voluntary Participation in NRC Regulatory Impact Survey, Per 900118 Request ML20012B6211990-03-0808 March 1990 Provides Actions Taken to Ensure & Verify Sys Design Basis Performance,Per 900205 SSFI at Facility ML20012B9011990-03-0606 March 1990 Forwards 870331-891111 Inservice Insp Program Final Rept for Peach Bottom Atomic Power Station Unit 3 1987-1989 Extended Refuel Outage. Several Indications Identified ML20012A2661990-02-26026 February 1990 Forwards Application for Amends to Licenses DPR-44 & DPR-56, Consisting of Tech Spec Change Requests 89-13 & 89-14, Revising Nuclear Review Board Membership & Meeting Frequency & Adding Independent Safety Engineering Group Requirements ML20011F2541990-02-23023 February 1990 Forwards Revs to Physical Security Plan.Encls Withheld (Ref 10CFR73.21 & 2.790) ML20011F3791990-02-21021 February 1990 Provides Revised Schedule for Installation of Hardened Wetwell Vent,Per Generic Ltr 89-16 & Explanation Why Jan 1993 Completion Date Cannot Be Met Due to Unavailability of Matls.Intallation Scheduled for Cycle 9 Outage ML20006F5491990-02-16016 February 1990 Certifies That 891122 Tech Spec Change Request (Tscr) 89-15, 891228 Tscr 88-18 & 900214 Tscr 90-04 Mailed to Commonwealth of Pa,Dept of Environ Resources ML20006F1621990-02-15015 February 1990 Forwards Progress Rept Re Implementation of Control Room Enhancements as of End of Seventh Refueling Outage,Per NUREG-0737.Rept Delayed to Allow for Independent Verification of Control Room Enhancement Status ML20012B1731990-02-15015 February 1990 Forwards Public Version of Revs to Epips,Including Rev 5 to ERP-101,App 1 to Rev 13 to ERP-110,App 2 to Rev 10 to ERP-110,App 1 to Rev 7 to ERP-140,App 2 to Rev 10 to ERP-140,App 3 to Rev 11 to ERP-140 1990-09-18
[Table view] |
Text
e PHILADELPHIA ELECTRIC COMPANY 23O1 M ARKET STREET P.O. BOX 8699 PHILADELPHI A. PA.19101 SHIE LDS L. DALTROFF stscraicraoo csom March 3, 1983 Docket Nos. 50-277 50-278 r
Mr. J. F. Stolz, Chief Operating Reactors Branch #4 Division of Licensing U. S. Nuclear Regulatory Commission Washington, D. C. 20555
SUBJECT:
NUREG-0737, Item II.D.1, Safety-Relief Valve Operability Test
Dear Mr. Stolz:
The attachment to this letter provides the information requested in your letter of January 5, 1993 (J. F. Stolz to E. G.
Bauer, Jr., PECo.) regarding the Safety-Relief Valve Operability
- Test required by NUREG-0737, Item II.D.l.
Should you have any questions regarding this matter, please do not hesitate to contact us.
Sincerely, A
/f.
, ' Sill ~l } [
Attachment cc: Site Inspector Peach Bottom 8303070071 830303 PDR ADOCK 05000277 P PDR ON
- c ~
Docket Nos.- 50-277 50-278 s Attachment Peach Botton Atomic Power Station NURRG-0737, Item II.D.1 NRC OUESTION 1 l
l l
The test program utilized a " rams head" discharge pipe configuration. Peach Bottom utilizes a " tee" quencher configuration at the end of the discharge line. Describe the
' discharge pipe configuration used at Peach Bottom and compare the anticipated loads on valve internals in the Peach Bottom configuration to the measured loads in the test program. Discuss the impact of any differences in loads on valve operability.
1 RESPONSE TO OUESTION 1 i
The safety / relief valve discharge piping configuration at Peach Bottom utilizes a " tee" quencher at the discharge pipe exit. The average length of the eleven SRV discharge lines (SRV DL) is 129' and the submergence length in the suppression pool is approximately 8.58 The SRV test program utilized a ramshead at the discharge pipe exit, a pipe length of 1128 and a submergence length of approximately 138 Loads on valve internals during the test program are larger than loads on valve l internals in the Pe&ch Bottom configuration for the following reasons: '
- 1. No dynamic mechanical load originating a+ the " tee" quencher is transmitted to the valve in the Peach Bottom configuration because there is at least one anchor point
- between the valve and the tee quencher.
- 2. The first segment length of the SRV piping that would be utilized for the alternate shutdown cooling mode at Peach Bottom averages less than 4 feet whereas the test facility first segment is 12 feet long thereby resulting l in a bounding dynamic mechanical load on the valve in i
i i
4 l
l l
l
. e the test progras due to the larger moment arm between the SRV and the first elbow. 3
- 3. Dynamic hydraulic loads (backpressure) are experienced i by the valve internals in the Peach Bottom configuration. The backpressuro loads may be either (i) transient backpressures occurring during valve ,
actuation, or (ii) steady-state backpressures occurring l during steady-state flow following valve actuation.
(a) The key parameters affecting the transient backpressures are the fluid pressure upstream of the valve, the valve opening time,-the fluid inertia in the submerged SRVDL and the SRVDL air volume. Transient backpressures increase with higher upstream pressure, shorter valve opening times, greater line submergence, and smaller SRVDL air volume. The transient backpressure in the test program was mariaized by utilizing a submergence of 13', which is greater than Peach Bottom and a pipe length of 112' which is less than Peach Bottom.
The maximum transient backpressure occurs with high pressure steam flow conditions. The transient backpressure for the alternate shutdown cooling mode of operation is always much less than the design for steam flow conditions because of the lower upstream pressure and the longer valve opening time.
(b) The steady-state backpressure in the test program was maximized by utilizing an orifice plate in the SRVDL above the water level and before the ramshead. The orifice was sized to produce a backpressure greater than that calculated for any of the Peach Bottom SRVDL's.
An additional consideration in the selection of the ramshead for the test facility was to allow more direct muasurement of the thrust load in the final pipe segment. Utilization of a " tee" quencher in the test program would have required quencher supports that would unnecessarily obscure accurate measurement of the pipe thrust loads.
The differences in the line configuration between the Peach Bottom plant and the test program as discussed above result in loads on the valve internals for the test facility which bound the actual Peach Bottom loads.
. l NRC OUESTION 2 f s
The test configuration utilized no spring hangers as pipe supports . Plant specific configurations do use spring hangers in conjunction with snubber and rigid supports. Describe the safety relief valve pipe supports used at Peach Botton and compare the anticipated loads on valve internals for the Peach Bottom pipe supports to the measured loads in the test program. Describe the.
impact of any differences in loads on valve operability.
RESPONSB TO QUESTION 2 The Peach Bottom safety-relief valve discharge lines (SRV DL 's) are supported by a combination of snubbers, rigid supports, and spring hangers. These supports were designed to accommodate combinations of loads resulting from piping, dead weight, thermal conditions, seismic and suppression pool hydrodynamic events, and a high pressure steam discharge transient.The locations of snubbers and rigid supports at Peach Botton are such that the loce tion of such supports in the BWR generic test facility is prototypical, i.e., in each case (Peach Bottom and the test f acility) there are supports near each change of direction in the pipe routing. Each SRYDL at Peach Bottom has 3 or 4 spring hangers, all of which are located in the drywell.
The dynamic load effects on the piping and supports of the test facility due t'o the water discharge events (the alternate shutdown cooling mode) were found to be significantly lower than corresponding loads resulting from the high pressure steam discharge event. As stated in NEDE-24988-P, this finding is considered generic to all BWR's since the test facility was designed to be prototypical of the features pertinent to this issue. Furthermore, analysis of a typical Peach Bottom SRVDL configuration has contirmed the applicability of the generic statement to Peach Bottom.
During the water discharge transient there will be significantly lower dynamic loads acting on the snubbers and rigid supports than during the steam discharge transient. This will more than offset the small increase in the dead load on i ,
L l
L - . - - . - - . . _ _ _ _ - - - - . _ . . _ . , .. -
these supports due to the weight of the water during the alternate shutdown cooling mode of operation. Therefore, design s adequacy of the snubbers and rigid supports is assured as they are designed for the larger steam discharge transient loads.
This question addresses the design adequacy of the spring hangers with respect to the increased dead load due to the weight of the water during the liquid discharge transient. As was discussed with respect to saubbers and rigid succorts, the dynamic loads resulting f rom liquid discharge during the alternate shutdown cooling mode of operation are significantly lower than those from the high pressure steam discharge. The spring hangers have been reviewed for the deflections resulting from the steam discharge dynamic event and found to be acceptable. In addition, the spring hangers have been evaluated for the increased dead load due to a water filled condition.
Both the spring hangers and piping stresses were acceptable.
Furthermore, the effect of the water dead weight load does not affect the ability of SRVs to open to establish the alternate shutdown Cooling path since the loads occur in the SRVDL only after valve opening.
9
2 l .
l NRC QUESTION 3
.s Report NEDE-24938-P did not identify any valve functional deficiencies or anomalies encountered during the test program.
Describe the impact on valve safety function of any valve functional deficiencies or anomalies encounted during the program.
RESPONSE TO OUESTION 3 No functional deficiencies or anomalies of the safety relief or relief valves were experienced during the testing at Wyle Laboratories for compliance with the alternate shutdown cooling mode requirement. All of the valves opened and closed without loss of pressure integrity or damage during all test runs, whether the run was valid or invalid. Anomalies encountered during the test program were all due to failures of test tacility instrumentation, equipment, data acquisition equipment, or deviation from the approved test procedure.
The test specification for each valve required six runs.
Under the test procedure, any anomaly caused the test run to be judged invalid. All anomalies were reported in the test report.
The Wyle Laboratories test log sheet for the Target Rock 3-Stage valve tests is attached. This valve is used in the Peach Bottom Atomic Power Statioh.
Each Wyle test report for the respective valve identifies each test run performed and documents whether or not the test run is valid or invalid and states the reason for considering the run invalid. No anomaly encountered during the required test program af fects any valve safety or ' operability function.
All valid test runs are identified in Table 2.2-1 of NEDE-24988-P. The data presented in Table 4.2-1 of NEDE-24986-P for each valve were obtained from Table 2.2-1 test runs and were based upon the selection criteria of:
I
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l . .
(a) Presenting the maximum respresentative loading I information obtained from the steam run data, - l (b) Presenting the maximum respresentative water loading information obtained from the 150F subcooled water test data, (c) Presenting the data on the only test run performed for the 500F subcooled water test condition.
6 6-
PAOE NO. 9 kh j TEST REPORT NO. 17476-03 s g Revision A N
TABLE I II TEST LOG FOR SRV TR-2 TEST TEST LOAD LINE TEST
. N0. MEDIA C0htlGURATl0N DATE REMARKS
- 201 Steam I 3/10/81 Back pressure low. Test Unacceptable.
. 202 Steam I 3/10/81 Installed 6.8" orifice.
Test Acceptable.
203 Water 1 3/10/81 Test Acceptable.
.' 204 Steam I 3/11/81 Test Acceptable.
, 205 Water i 3/11/81 Pipe loads high. See
, N0A # 5.
, 206 Steam I 3/11/81 Test Acceptable.
207 Water i 3/11/81 Not Acceptable. Low steam chest pressure.
. 208 Water i 3/11/81 Test Acceptable. Water
, temperature low.
3 209 Water i 3/30/81 Test Acceptable.
, ..)
210 Water i 3/30/81 Test Acceptable.
211 Water 1 3/30/81 Test Acceptable.
t P
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i WYLE LABORATORIES l Huntsyd6e F4C334fy
._____ . .N
i . .
- PAGE NQ. [8 h TEST REPORT NO. 17476-03 '
Revision A NOTICE OF ANOMALY NOTICE NO. 5 P. O. MUMBER: 205-XH212 WYLE JOS NO. 17476-01 c CONTR ACT NUMBER: N/A CATEGORY: O SPECIMEN O PROC 9 DURE D TEST EQUIPMENT DATE: 3/u/A1 TO: General Electric CornpanY ATTN: Mr. R. Miller c PART NAME. Target Rock 3-Stage SRV _PART NO. N/A ,,
TEST: Low Pressure Water 1. D. NO. TR-2 SPECIFICATION: WTP 17450-01 PARA.NO. N/A NOTIFICATION MADE TO: J. Mross/A. Sallman DATE: 1/14/81 NOTIFICATION MADE BY: t- Mill m < VIA: Verbal e
REQUIREMENTS:
N/A c e
DESCRIPTION OF ANOMALY: e When the water control valve was opened to initiate the test, the entire system was subjected to a shock wave similar to water hammer. As a re.sult, loads of approximately c 10,000 and 16,000 pounds were observed at Struts I and 2. Review of the recorded data showed no abnormal pressure in the discharge line, but did show sharply varying pres-sure in the steam chest' and inlet water pipe.
DISPOSITION - COMMENTS - RECOMMENDATIONS:
The recorded data shows that the anomaly occurred in the inlet piping and/or stcom chest and, therefore, was not caused by the SRV. The probable cause was the forming of vapor "
in the inlet pipe because of the higher water temperature (233'F) and the low pressure (8 to 10 psig). The vapor then compressed when subjected to the higher pressure water (300 psigJ, thus causing a shock wave in the water system. Since the discharge pipe x loads were caused by the shock wave rather than the SRV, the data must be considered invalid.
5 The test was not repeated. However, three other water tests were conducted on this SRV, ,
and all data was consistent, in addition, water tests were performed on a two-stage Target Rock SRV, and no anomalies occurred, it ic, therefore, recommended that the test not be repeated.
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NRC OUES? ION 4 i
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The purpose of the test program was to determine valve performance under conditions anticipated to be encountered in the
! plants. Describe the events and anticipated conditions at Peach Botton for which the valves are required to operate and compare these plant conditions to the conditions in the test program.
Describc the plant features assumed in the event evaluations used to scope the test program and compare them to plant features at Peach Botton. For example, describe high level trips to prevent water from entering the steam lines ander high pressure operating conditions as assumed in the test event and compare them to trips.
used at Peach Bottom.
RESPONSE TO NRC OUESTION 4 The purpose of the S/RV test program was to demonstrate that the Safety Relief Valve (S/RV) will open and reclose under all expected flow conditions. The expected valve operating conditions were determined through the use of analyses of accidents and anticipated operational occurrences referanced in Regulatory Guide 1.70, Revision 2. Single failures were applied to these analyses so that the dynamic forces on the safety and relief valves would be maximized. Test pressures were the highest predicted by conventional safety analysis procedures.
The BWR Owners Group, in their enclosure to the September 17, 1980 letter from D. B. Waters to R. H. Vollmer, identified 13 events which may result in liquid or two-phase S/RV inlet flow that would maximize the dynamic forces on the safety and relief valve. These events were identified by evaluating the initial events described in Regulatory Guide 1.70, Revision 2, with and
! without the additional conservatisa of a single active component failure or operator error postulated in the event sequence. It was concluded from this evaluation that the alternate shutdown cooling mode is the only expected event which will result in liquid at the valve inlet. Consequently, this was the event
! simulated in the S/RV test program. This conclusion and the test
[ results applicable to Peach Bottom are discussed below. The
- l.
alternate shutdown cooling mode of operation will ha described in the response to NRC Question 5. ,
s The BWR Owners Group identified 13 events by evaluating the initiating events described in Regulatory Guide 1.70, aevision 2, with the additional conservatism of a single active component failure or operator error postulated in the events sequence.
These events and the plant-specific features that mitigate these events, are summarized in Table 1. Of these 13 events, only nine are applicable to the Peach Bottom plant because of its design and specific plant configuration. Four events, namely 5, 6, 10 and 13 are not applicable to the Peach Bottom plant for the reasons listed below:
(a) Events 5 and 10 are not applicable because Peach Bottom does not have a High Pressure Core Spray system.
(b) Event 6 is not applicable because Peach Bottom does not have'RCIC head sprays.
(c) Event 13 is not applicable because large breaks will not be isolated at Peach Bottom.
For the nine remaining events, the Peach Bottom specific features, such as trip logic, power supplies, instrument line configuration, alarms and operator actions,' have been compared to the base case analysis presented in the BWR Owners Group submittal of September 17, 1980. The comparison has demonstrated that in each case, the base case analysis is applicable to Peach Bottom because the base case ant'.ysis does not include any plant features which are notsaiready present in the Peach Bottom t design. For these events, Table 1 demonstrates that the Peach l Bottom specific features are included in the base case analysis presented in the BWR Owners Group submittal of September 17, i 1980. It is seen from Table 1, that all plant features assumed L in the event evaluation are also existing features in the Peach j Bottom plant. All features included in this base case analysis j are similar to plant features in the Peach Bottom design.
Furthermore, the time available for operator action is expected i to be longer in the Peach Bottom plant than in the base case l analysis for each case where operator action is required due to the conservative nature of the base case analysis.
- Event 7, the alternate shutdown cooling mode of operation, is the only expected event which will result in liquid or two-phase i fluid at the S/RV inlet. Consequently, this event was simulated i in the BWR S/RV test prog ra m. In Peach Bottom, this event !
involves flow of subcooled water (approximately 35 oF subcooled)
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at a pressure of approximately 75 psig. The S/RV inlet fluid conditions tested in the BWR Owners Group S/RV test program, as s documented in NEDE-24988-P, are 150 to 500 subcooled liquid at 20 psig to 250 psig. These fluid conditions envelope the conditions expected to occur at Peach Botton in the alternate shutdown cooling mode of operation.
As discussed above, the DWR Owners Group evaluated transients including single active f ailures that would marinize the dynamic forces on the safety relief valves. As a result of this evaluation, the alternate shutdown cooling mode is the only expected event involving liquid or two-phase flow. Consequently this event was tested in the BWR S/RV test program. The fluid conditions and flow conditions tested in the BWR Owners Group test program conservatively envelope the Peach Bottom plant-specific fluid conditions expected for the alternate shutdown cooling mode of operation.
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NRC OUESTION 5 s
The valves are likely to be extensively cycled in a controlled depressurization mode in a plant-specific application.
Was this mode simulated in the test progras? What is the effect of this valve cycling on valve performance and probability of the valve to fail open or to fail closed?
RESPONSE TO NRC OUESTION 5 The BWR safety / relief valve (SRV) operability test program was designed to simulate the alternate shutdown cooling mode, which is the only expected liquid discharge event for Peach Bottoa. The sequence of events leading to the alternate shutdown cooling mode is given below.
Following normal reactor shutdown, the reactor operator depressurizes the reactor vessel by opening the turbine bypass valres and removing heat through the main condenset. If the main condenser is unavailable, the operator could depressurize the reactor vessel by using the SRV's to discharge steam to the suppression pool. If SRV operation is required, the operator cycles the valves in order to assure that the cooldown rate is maintained within the technical specification limit of 1000F per hour. When the vessel is depressurized, the operator initiates normal shutdown coo' ling by use of the RHR system. If that system i is unavailable because the valve on the RHR shutdown cooling i
suction line fails to open, the operator initiates the alternate j shutdown cooling mode.
For alternate shutdown cooling, the operator opens an SRV and initiates either an RHR or core spray pump utilizing the suppression pool as the suction source. The reactor vessel is filled such that water is allowed to flow into the main steam linos and out of the SRV and back to the suppression pool.
Cooling of the system is provided by use of an RHR heat exch a nger. As a result, an alternate cooling mode is maintained.
i I
In order to assure continuous long term heat removal, the SRV is kept open and no cycling of the valve is performed. In order ,
to control the reactor vessel cooldown rate, the operator is instructed to control the flow rate into the vessel.
Consequently, no cycling of the SRV is required for the alternate shutdown cooling mode, and no cycling of the SRV was performed
'for the generic BWR SRV operatility test program.
The ability of the Peach Dottom SRV to be extensively cycled for steam discharge conditions has been confirmed during steam ,
discharge qualification testing of the valve by the valvo vendor.
Based on the qualification testing of the SRV8s, the cycling of the valves in a controlled depressurization mode for steam discharge conditons will not adversely affect valve performance and the probability of the valve to fail open or closed is extremely low.
9 11 -
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.NRC OUESTION 6 s 3 Describe how the values of valve Cv's in report NEDE-24988-P will be used at Peach Bottoa. Show that the methodology used in the test program to determine the valve Cy will be consistent with the application at Peach Bottom.
RESPONSE TO NRC OUESTION 6 The flow coefficient, Cv, for the Target Rock 3-Stage safety relief valve (SRV) utilized in Peach Botton was determined in the generic SRV test program (NEDE-24988-P) . The average flow coefficient calculated from the test results for the Target Rock Valve is reported in Table 5.2-1 of NEDE-24988-P. This test value has been used by Philadelphia Electric Company to confirm that the liquid discharge flow capacity of the Peach Bottom SRV's will be sufficient to remove core decay heat when injecting into the reactor pressure vessel (RPV) in the alternate shutdown cooling mode. The Cy value determined in the SRV test demonstrates that the Peach Botton SRY's are capable of returning sufficient flow to the suppression pool to accomodate injection 1
by the RHR or CS pump.
If it were nece'ssary for the operator to place the Peach Botton plant in the alternate shutdown cooling mode, he would assure that adeguate core cooling was being provided by monitoring the following parameters: RHR or CS Flow rate, reactor vessel pressure and reactor vessel temperature.
The flow coefficient for the Target Rock valve reported in NEDE-24988-P was determined from the SRV flow rate when the valve inlet was pressurized to approximately 250 psig. The valve flow rate was measured with the supply line flow venturi upstream of the steam chest. The CV for the valve was calculated using the l nominal measured pressure ditferential between the valve inlet l (steam chest) and 3' downstream of the valve and the l corresponding measured flowrate. Furthermore, the test
,---1
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, l conditions and test configuration were. representative of Peach Bottom plant conditions for the alternate shutdown cooling mode, s e.g. pressure upstream of the valve, fluid temperature, f riction losses and liquid flowcate. Therefore, the reported Cy values ,
are appropriate for application to the Peach Bottom plant. {
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